ML20245D531

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Insp Repts 50-321/89-02 & 50-366/89-02 on 890227-0317. Violations Noted.Major Areas Inspected:Maint Program & Implementation.Per NRC Temporary Instruction 2515/97
ML20245D531
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 05/22/1989
From: Blake J, Crowley B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20245D457 List:
References
50-321-89-02, 50-321-89-2, 50-366-89-02, 50-366-89-2, NUDOCS 8906270147
Download: ML20245D531 (81)


See also: IR 05000321/1989002

Text

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NUCLEAR REGULATORY COMMISSION

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f7 o 101 MARIETTA STREET, N.W.

' In f ATLANTA, GEORGIA 30323 -

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Report Nos.: 50-321/89-02 and 50-366/89-02

Licensee: Georgia Power Company '

-P. O. Box 1295

Birmingham, AL 35201

Docket Nos.: 50-321 and 50-366- License'Nos.: OPR-57 and NPF-5

Facility Name: Hatch 1 and 2

Inspection Conducted: February 27 -' March 17. 1989

Inspector: [. 5 22

B. R. Crowley (Team Lead y) Date Signed

Team Members

G. A. Hallstrem

M. D. Hunt l

P.. J. Fillion

F. N. Wright

S. S. Kir s

G. s

Approved by: .

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J. J. ake, Chief Date Signed

M ter als and Processes Section

ng eering Branch

Division of Reactor Safety

SUMMARY

Scope: This special announced inspection consisted' of an in-depth team

inspection of the Hatch maintenance program and its implementation.

NRC-Temporary Instruction 2515/97, dated November 3,1988, was used

for guidance.

Results: Overall, the maintenance program was judged to be " Good" with " Good" ,

implementation. Areas of strength and weakness are highlighted in }'

the Executive - Summary with details provided in the report. Four

violations were identified: inadequte administrative procedure - l

paragraph 3.a.; failure to complete adequate corrective action -  ;

paragraphs 3.b. and 3.c.; failure to take breathing air samples -

paragraph 3.d.; and failure to follow acceptance criteria for weld

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patch on reactor building roof drain paragraph 3.e. l

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8906270147 890615

PDR. ADOCK 05000321

0 PDC

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REPORT DETAILS

1. Persons Contacted

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Licensee Employees l

G. Brinson, Superintendent of QC

Y. Brown, Systems Engineer

H. Buchans, I&C Supe, visor

  • G. Barker, Superintendent of I&C

J. Cameron, Senior Maintenance Plant Engineer

B. Coleman, Supervisor, Document Control

A. Cowan, I&C Supervisor

G. Creighton, Senior Regulatory Specialist

  • S. Curtis, Supervisor -Shift Technical Advisor

J. Dawson, Maintenance Supervisor

D. Davis, Manager of General Support

  • W. Drinkard, Manager, Safety Analysis and Engineering Review

W. Duvall, HP Chemistry Supervisor

L. E11 gass, NPRDS Coordinator

  • P. Fornel, Manager of Maintenance
  • 0. Fraser, QA Site Manager

G. Gill, Senior Maintenance Plant Engineer

  • W. Glisson, Maintenance Engineering Supervisor
  • R. Godby, Maintenance Superintendent
  • M. Googe, Manager of Outages and Planning

F. Gorley, Operations Supervisor

R. Grover, Plant Engineer - Nuclear Safety and Compliance

  • L. Gucwa, Manager, Nuclear Engineering and Licensing

J. Hadden, Supervisor, Plant QC

  • J. Hammonds, Nuclear Safety and Compliance Supervisor

R. Hukill, Supervisor, Maintenance Support Group

B. Keck, Reactor Systems Engineering Superintendent

R. King, Discipline Engineering Supervisor

T. King, Maintenance Supervisor

W. Kirkley, Acting Manager of HP/ Chemistry

J. Lanier, Senior Systems Engineer - Reactor Control

  • J. Lewis, Acting Operations Manager

M. Link, Supervisor, HP Operations

A. Manning, QA Auditor

D. Matthews, Systems Engineer - Nuclear Boiler

W. Metts, Maintenance Supervisor

E. Metzler, Nuclear Safety and Compliance Supervisor

D. Midlik, Senior Maintenance Plant Engineer

L. Mikulecky, Senior Plant Engineer - Regulatory

  • C. Moore, Plant Support Manager
  • H. Nix, General Plant Manager

G. O'Donnell, I&C Supervisor

R. Ott, Supervisor, Training

R. Pooni, Acting Supervisor, Reactor Protection Engineering

.

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h 4 ENCLOSURE 2

EXECUTIVE SUMMARY

Background '

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The Nuclear Regulatory Commission considers effective maintenance of equipment

and components a major aspect of ensuring safe nuclear plant operation and has

made this area one of the NRC's highest priorities. In- this regard, the

Commission. issued'a. Policy Statement dated March 23, 1988, that states, "it is

the objective of the Commission that all components, systems, and structures of

1 ear power plants be maintained so that plant equipment will perform its

i

intended function when required. To accomplish this objective, . each licensee-

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should develop and implement a maintenance program which provides for the

l periodic evaluation, and prompt repair of plant components, systems, and

structures t4 ensure their availability." {

To- ensun.- effective implementation of the Commission's maintenance policy, the  !

NRC staff is undertaking a major program to inspect and evaluate the

effectiveness of licensee maintenance activities. As part of this inspection 1

activity, the current inspection was performed in; accordance with guidance

provided in NRC Temporary Instruction'2515/97, Maintenance Inspection Guidance, ,

dated November 3, 1988. The temporary instruction includes a " Maintenance  !

Inspection Tree" that identifies the major elements associated with effective 1

maintenance. . The tree was designed to ensure that all factors related to {

maintenance are evaluated. l

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Conduct of Inspection j

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The maintenance inspection at the Hatch Nuclear Station was initiated with a  !

site meeting on January 24-26, 1989, where the inspection scope, including the i

maintenance inspection tree, was discussed. At that meeting, the licensee i

presented to the inspection team leader an overview of the site maintenance  ;

program. In addition, a comprehensive package of material, as requested by NRC l

1etter dated January 10, 1989, was provided for inspection preparation. l

The inspection was conducted by a team consisting of a team leader and six .l

inspectors. Four of the inspectors were from RII and two were from NRR. The ,

team spent two weeks, February 27-March 3 and March 13-17, 1989, on site  !

conducting the inspection. .l

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The inspection was performance based, directed toward evaluation of- equipment l

conditions; observation of in process maintenance activities; review of

equipment histories and records; and evaluation of performance indicators,  :

maintenance control procedures, and the overall maintenance program. Based on i

known industry problems, plant specific problems, and discussions with the i

Hatch Resident Inspectors, the team selected five systems and directed the l

inspection toward determining whether these systems were being properly j

maintained and assessing if the current maintenance system would ensure proper j

maintenance in the future. The systems selected were: Ell (RHR), B21 (Main

Steam), N21 (Condensate and Feedwater), PS2 (Instrument Air), and E41 (HPCI).

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The team performed walkdown inspections'of portions of the selected systems to

, determine the material condition of the equipment. In addition, maintenance

history records for the last two years were obtained and reviewed for any

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adverse; trends. NPRDS data were also reviewed for the selected systems. In

review-of equipment history records, any questionable trends were examined in

detail to determine if equipment was being properly maintained. In the course

of the inspection, the team also observed general housekeeping and equipment

-condition for a large part of the plant.

Results

After completion of the inspection, the maintenance program was evaluated using

the.NRC TI and inspection tree as a tool. See paragraph 2 of the Inspection

Report for details of.the rating scheme.

The inspection results are presented pictorially in Figure 1 as the completed

inspection tree. As noted in Figure 1, overall, the Hatch program for

establishing and implementing an effective maintenance program was rated " Good"

both in program and implementation. For the three major areas: (1) Overall.

Plant Performance was rated " GOOD", (2) Management Support was rated

" SATISFACTORY" for program and implementation, (3) Maintenance implementation

was rated " Good" for program and implementation. These ratings were based on

specific strengths and weaknesses identified in the report details. The

following are the more significant strengths and weaknesses identified:

Strengths -

Overall, the training program for maintenance was very

strong. The facilities and the use of actual components as

training aids were outstanding.

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In general, plant housekeeping was good.

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The maintenance data base and equipment records (NPMIS)

were very good. The data base appeared to be user friendly

and records were readily retrievable.

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The overall maintenance staff was a strength. Staffing

levels appeared to be adequate. Team work was evident.

Management was well qualified and enthusiastic.

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The QC staff was well organized, qualified, and heavily

involved in the maintenance process.

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The licensee has a strong program for controlling the

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maintenance backlog. The backlog is low.

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The licensee makes good use of-performance indicators.

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Overall, plant equipment condition was good.

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A strong program (deficiency card system) for identifi-

cation of deficiencies and intiation of action was in place

and appeared to be working well.

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? Interfaces between maintenance organization and other-

organizations were well established and appeared' to be

working well. Daily planning meetings were well organized

, -and' appeared to be a strong point in the maintenance

process.

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Both clean and:" hot" machine shops were indicative of good

j' -maintenance facilities.

Weaknesses -

Weaknesses were identified in the PM program.for electrical

y' equipment in that vendor recommended PMs were not included'

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ini procedures' and no documented justification ' existed

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for excluding the recommendations - examples: 4160 : volt

i switchgear,.busbars and cable compartments not included in

procedures and' no requirement to check protection charac-

teristics. for molded-case circuit breakers.

-- Weaknesses . were identified in the root cause analysis

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program as follows: the procedure needs strengthening to

provide more. detail .on how to perform root cause analysis,

a' motor failure on a HPCI valve did not receive a root

cause analysis, excessive time was taken to determine cause

of Feedwater Pump-Seal leakage.

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Responsibilities for Systems Engineers were not well

' defined.

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Some procedural weaknesses were identified - examples: the

maintenance program procedure and predictive maintenance

vibration analysis procedure needs to include cross

reference to' ASME Section XI requirements for ASME

Section _XI components; the maintenance program procedure

needs to include additional detail relative to ensuring

proper functional / operability test when changes are made to

the MWO; and the procedure controlling the procedure update

program was inadequate to insure that vendor recommended

maintenance is included in maintenance procedures.

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Weaknesses in the program for personnel safety were

identified - examples: failure to have unique fittings

for connecting breathing air to instrument air and

procedure for maintenance of electrical equipment could

be strengthened by adding some safety precautions.

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The level and clarity of detail on some MW0s was poor

resulting.-in difficulty in determining details of work

performed - examples: MW0s 2-88-4862, 2-88-1906 and

2-88-3177.

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Weaknesses were identified relative to corrective action -

examples: failure te properly torque upper mounting bolts

on hydraulic control units (HCUs) and failure to ensure

that all fittings for connecting breathing air were unique

fittings.

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UNITED STATES

'* , [ Mar - o . NUCLEAR REGULATORY COMMISSION

g-

[ g

Igg

REGION ll .

.101 MARIETTA STREET, N.W.

  • ATLANTA, GEORGI A 30323 '

'

$

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Report-Nos'.: 50-321/89-02 and 50-366/89-02

. Licensee: Georgia. Power Company

'P. 0. Box 1295

.

Birmingham, AL 35201

Docket.Nos..: 50-321 and 50-366 License Nos.: DPR-57 and^NPF-5~

Facility Name: LHatch 1 and E

Inspection Conducted: February 27 - March 17, 1989

Inspector: .[. 5 22 'f '

B. R. Crowley (Team Leadg") Date Signed

. Team Members

G. A. Ha11strom

M. D. Hunt

P. J. .Fillion

F. N. Wright

S. S. Kir s-

G. s

L , -Approved by: , 'u E2 S7

J. J. ake, Chief Date Signed

M ter als and Processes Section

ng eering Branch

.

Division of Reactor Safety -

SUMMARY

Scope: This special announced inspection consisted of an in-depth team

inspection of the Hatch maintenance program and its implementation.

NRC Temporary Instruction 2515/97, dated November 3, 1988, was used

for guidance.

Results: Overall, the maintenance program was judged to be " Good" with " Good"

implementation. Areas of strength and weakness are highlighted in-

the Executive Summary with details provided in the report. Four

violations were identified: inadequte administrative procedure -

paragraph 3.a.; failure to complete adequate corrective action -

paragraphs 3.b. and 3.c,; failure to take breathing air. samples -

paragraph 3.d.; and failure to follow acceptance criteria for weld

patch on reactor building roof drain paragraph 3.e.

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REPORT DETAILS

1

.1. Persons Contacted

Licensee Employees.

G. Brinson, Superintendent of QC

Y. Brown, Systems Engineer

H. Buchans, I&C Supervisor

  • G. Barker, Superintendent of I&C

J- Cameron.. Senior Maintenance Plant Engineer

.

B. Coleman, Supervisor, Document Control

A. Cowan, I&C-Supervisor

G. Creighton, Senior Regulatory Specialist

  • S. Curtis, Supervisor..-Shift Technical Advisor

J.-Dawson,' Maintenance Supervisor

D. Davis, Manager.of General Support

  • W. Drinkard, Manager, Safety Analysis and Engineering Review

W.;Duvall, HP Chemistry Supervisor

L. E11 gass', NPRDS Coordinator.

  • P. Fornel, Manager of Maintenance
  • 0. Fraser, QA Site Manager

G. Gill, Senior Maintenance. Plant Engineer

  • W. Glisson, Maintenance Engineering Supervisor
  • R. Godby, Maintenance Superintendent
  • M. Googe, Manager of Outages and Planning

F. Gorley, Operations Supervisor

R. Grover, Plant Engineer - Nuclear Safety and Compliance

.

  • L. Gucwa, Manager, Nuclear Engineering and Licensing

'J. Hadden, Supervisor, Plant QC

  • J. Hammonds, Nuclear Safety and Compliance Supervisor

R. Hukill, Supervisor, Maintenance Support Group

B. Keck, Reactor Systems Engineering. Superintendent .

R. King, Discipline Engineering Supervisor I

T. King, Maintenance Supervisor

W. Kirkley, . Acting Manager of HP/ Chemistry

J. Lanier, Senior Systems Engineer - Reactor Control.

  • J. Lewis, Acting Operations Manager

M. Link, Supervisor, HP Operations

A._ Manning, QA Auditor

D. Matthews,- Systems Engineer - Nuclear Boiler

W. Metts, Maintenance Supervisor

E. Metzler, Nuclear Safety and Compliance Supervisor

l D. Midlik, Senior Maintenance Plant Engineer ,

l L. Mikulecky,- Senior Plant Engineer - Regulatory )

  • C. Moore, Plant' Support Manager
  • H. Nix, General Plant Manager

G. O'Donnell, I&C Supervisor j

R. Ott, Supervisor, Training '

R. Pooni, Acting Supervisor, Reactor Protection Engineering j

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-T. Powers, Engineering Support Manager

W. Porter,' Senior Maintenance Plant Engineer - Vibration

J_. Reddick, Supervisor, HP Support

P. Roberts, Plant' Project Superintendent

  • W. Rogers, Chemistry Superintendent

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H. Scarbrough, Maintenance Supervisor

V. Shaw Senior Plant Systems Engineer

J. Sherman, Reactor Control Systems Engineering Supervisor

D.' Smith, HP' Superintendent

R. Staines, Training Coordinator

M. Sutton, Training Supervisor

L. Sumner., Plant Manager

  • S.'Tipps, Nuclear Safety and Compliance Manager

J. Vaughn, Maintenance Supervisor

A. Vora, Senior Maintenance Plant Engineer

A. Wheeler, BOP Systems Engineering Supervisor

J. Wilkes, Superintendent of Planning and Control

D. Williams, Plant Systems Engineer'- ECCS

C. W111 yard, Senior Systems Engineer -ECCS

C. Wright, Shift Supervisor

R. Zorn, QC Supervisor

Other ; licensee' employees contacted during this -inspection included

craftsmen, engineers, operators, mechanics, security force members,

technicians, and administrative personnel.

NRC Personnel

  • A. Herdt, Branch Chief, DRP:PB3, RII

J. Menning, Senior Resident Inspector

  • E. Merschoff, Deputy Director, DRS, RII
  • R. Musser, Resident. Inspector
  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last' paragraph.

2. Inspection Methodology

The inspection was performance based, directed toward evaluation of plant

equipment condition and evaluation of maintenance for systems which have

had problems. The systems selected for evaluation were based on the

following:

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Known industry problems l

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Review of Hatch LERs - Site Specific Problems  !

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Review of NRC Bulletins and Notices I

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Review of Hatch Deficiency Reports 1

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Discussions with Resident Inspectors {

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PRA information provided by NRR i

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Inspector's Experience t

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Based on the above criteria, the following systems were selected for the

inspection effort:

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Ell, Residual Heat Removal (RHR)

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B21, Nuclear Boiler (Main Steam)

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N21, Condensate and Feedwater

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PS2, Instrument Air (including P51)

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E41, High Pressure Coolant Injection (HFCI)

Maintenance for the selected systems was inspected by: observation of

equipment condition (walkdown inspections), observation of in process

maintenance activities, review of equipment history records (MWO and

NPRDS), and evaluation of performance indicators and trending data.

Based on the inspections performed, the maintenance program was evaluated

using the inspection tree from NRC TI 2515/97 (see Figure 1). As

indicated in Figure 1, three major areas of the licensee's maintenance

program were evaluated: (1) Overall Plant Performance Related to

Maintenance, (2) Management Support of Maintenance, and (3) Maintenance

Implementation. Under each major area, a number of elements were  ;

evaluated, rated, and colored using the following guidelines:

" Good" Performance (Green) -

Overall, better than adequate; shows

more than minimal effort; can have a

few minor areas that need improvement

" Satisfactory" or " Adequate" -

Adequate, weaknesses may exist, could

Performance (Yellow) be strengthened

" Poor" Performance (Red) -

Inadequate or missing

(Blue) -

Not evaluated

In general, the top half of the box (element) was rated depending on

whether the element was in place and the bottom half was rated depending

on how well the element was being implemented.

3. Significant Issues Identified

a. Maintenance on the Indoor Metal-Clad Switchgear for the 4160 Volt

Distribur. ion System.

During tFe inspection detailed in paragraph 4 below, the team

identified issues regarding the recommended preventive maintenance,

the maintenance interval and the quality of the preventive

maintenance procedure for the 4160 volt metal-clad switchgear.

Procedure 52PM-R22-001-05, specifies preventive maintenance work for

the 4160 volt switchgear. The procedure covers verification of the

undervoltage trip attachments (UVTAs are incorporated into one

line-up per unit), breaker cleaning and inspecting (with breaker ,

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.. removed from the compartment), cell cleaning and inspecting, and

relay / control wiring compartment cleaning and inspecting. The

maintenance interval specified in the procedure was:

.(1) Recommended 18 months for the UVTAs

(2) ~ Required 60 months for four Unit 2 line-ups in Technical:

Specification 3/4.8.2.6.lb,.which is related to containment

penetration overcurrent protection.

(3) Recommended five years for.all other switchgear.

Observations

Procedure ~ 52PM-R22-001-05, Rev. 3, was reviewed in detail by the.

. team and all comments were discussed with Senior Plant Engineers (one

from the maintenance group and one from the systems engineering

group) and a Maintenance Foreman. One general comment made by the

- NRC, which applied to the circuit breaker portion. of the procedure

'(Step 7.5), was that the procedure lacked sufficient detail.

Relative to cleaning, inspecting and lubricating the breaker contact

assembly, procedure Steps 7.5.6.2, 7.5.6.3, 7.5.6.9, and 7.5.6.'11

apply. These steps do not adequately address'the following-PM items:

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Inspect all current carrying parts for evidence of overheating.

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Operate the breaker slowly, by using .the spring blocking device.

Check. for binding or friction and correct if necessary. The

manufacturer's instruction book gives detailed instructions on

this step.

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Inspect primary contacts for burns or pitting. Wipe contacts

with clean cloth. Replace badly burned or pitted contacts.

Rough or galled contacts should be smoothed with a crocus ~ cloth.

Resilver where necessary.

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Inspect arcing contacts for uneven wear or damage. 1

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Figure 2-C, Contact Dimensions, indicates six dimensions that

could be verified. I

Relative to Step 7.5.6, Breaker Contact Assembly, the team made the

following comments: j

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The contact resistance test criteria of 500 micro-ohms should be

50 micro-ohms. I

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In Step 7.5.6.5, the word "megger contacts to ground" should  !

read "megger contacts to frame."

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The ' reference diagrams were difficult to read because of the

small print.

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Addition of QC hold points should be considered.

Step 7.5.9.2 simply states " Clean and. inspect all _ parts [of the

L _ stored energy mechanism]." The following PM items are not adequately

addressed:

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Remove spring charging motor brushes. Measure brush length and

compare to acceptance criteria. Replace brushes if necessary.

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Inspect motor support for loose or ' missing bolts and tighten or

replace as necessary. (Refer to NRC Information Notice 88-42)

In addition to' commenting on the level of detail in the procedure,

the team also commented relative to items not identified for

inspection that should be inspected. The program does not include

. periodic inspection and insulation resistance measurement of the

switchgear bus. . The outgoing cable compartment is not inspected,

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although the licensee stated that thermographic imaging of the cable

termination was included in the predictive maintenance program.

Procedure 52-R22-001-0S did not incorporate steps for inspection

of the ; potential transformer compartment, although apparently

maintenance 1 work orders to inspect the PT compartment were carried

out using that _ procedure. Furthermore, the NRC questioned the

five year maintenance interval since it was much longer than the

one-year interval recommended by the manufacturer in his instruction

book. (Refer to W Instruction Book S.0. 25-Y-9285-1, dated June

1975, page 48, Hatih No. SX-13698 )

Discussions were also held with key personnel in the training

department relative to preventive maintenance on the 4160 volt

switchgear. At present, there is no lesson plan but the licensee is

in the process of developing a lesson plan for that topic as part of

Phase V of the INP0 training program. The licensee also stated that

outside courses were not provided in .this area. Therefore, plant

electricians have not received training at Plant Hatch that could

offset the lack of detail in the 4160 volt PM procedure.

The licensee's response to the above comments was as follows. The

maintenance engineer who was involved in the discussions agreed to

review and upgrade procedure 52PM-R22-001-0$ with the objective of

providing a detailed inspection checklist appropriate to the i

circumstances. The maintenance Engineering Supervisor stated that

only four failures of the 4160 volt switchgear were reported to NPRDS

for the two-year period from January 1,1987, to December 31, 1988.

He also stated that a survey was conducted of (five) other nuclear

plants. Each of these plants reported using a PM interval greater

than one year. ,

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Conclusion

The NRC's position on the matter is as follows. The NRC's SER for

Generic Letter 83-28, Item 3.2.2, Check of Vendor and Engineering

Recommendations for Testing and Maintenance (All Other Safety-Related

Components), transmitted July 29, 1987, is relevant to these inspec-

tion findings. Page 4 of that SER states: " Item 3.2.2 requires

licensees and applicants to submit the results of their check of

vendor and engineering recommendations. The licensee's supplemental

responses dated August 21, 1986, and July 1, 1987, to Item 3.2.2

stated that a procedure upgrade program has been developed and

designed to provide assurance that appropriate vendor and engineering

information is either included or referenced in the procedures. The

licensee indicates that Hatch Procedure DI-ADM-05-1085, Rev. 2,

included a requirement to ensure that applicable vendor manuals

and vendor and engineering recommendations are reviewed and are

included in all procedures, not just test and maintenance procedures."

Procedure 52PM-R22-001-0S, Rev. 3, had been through the procedure

upgrade program; however, all the manufacturer's recommendations were

not incorporated into procedures nor was proper documented justifica-

tion provided for any deviation from the recommendations.

Procedure DI-ADM-05-1085, Rev. 2, was inadequate because it did not

contain the instructions that would ensure that applicable vendor

recommendations were included in the plant procedures as stated in

the correspondence described above. The licensee is responsible for

the maintenance program. Therefore, the licensee may, on occasion,

deviate from vendor recommendations, but any such deviation should

be justified by auditable documented analysis. The 4160 volt AC

switchgear PM procedure is an example of the inadequacy of the

controlling administrative procedure. Therefore, this matter

represents a violation of NRC requirements, and is identified as

Violation 321, 366/89-02-01, Inadequate Administrative Procedure.

b. Lack of Corrective Action on HCU Bolting

Background

The Team had reviewed NRC IN 87-56, " Improper Hydraulic Control Unit

Installation at BWR Plants," previous to this inspection. IN 87-56

provides details of inadequate bolting on HCUs at two BWRs and notes

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that:

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The CRD system controls the position of the control rods within

the reactor core either to change reactor core power or to

rapidly shutdown the reactor (scram). The HCU is a major

monent of the CRD system that incorporates all the hydraulic,

.ctrical, and pneumatic equipment necessary to move one CRD

mechanism during normal or scram operations. This equipment,

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which includes the accumulators, CRD insert lines, CRD withdraw

lines, and scram' valves, is supported by the HCU frames.

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If a sufficiently large number of HCU frame bolts are missing or

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loose, a 3afe Shutdown Earhquake (SSE) could result in damage

affecting the_ ability of the CRD system to control .the

l_ ' positioning of the control rods.

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In addition, damage to a CRD

l- withdraw- line could result in a small-break loss-of-coolant

accident in the area of the HCUs.

The Team completed an inspection of'the bolting for a majority of the

Unit I and Unit 2 HCUs and identified one case of partial bolt

engagement for an upper frame mounting bolt (Unit 2 HCU 46-23) and

several cases (more than a dozen randomly dispersed betwen both

units) where the upper frames of back-to-back HCUs appeared to

indicate inadequate bolt torquing (upper plates exhibiting a gap

rather'than continuous contact).

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Documentation Examined-

Cognizant licensee personnel informed the Team of previous NRC

' Violation- 50-321/86-20-02, regarding inadequacies.(missing lock

washers) from the Unit 1 bottom HCU mounting bolts. Corrective

actions' were to install the missing washers and verify torque of

l

bottom bolts to 45-50 foot pounds for Unit 1 HCUs (MWO 1-86-7330) and

verify torque of bottom bolts to 45-50 foot ' pounds for Unit 2 HCUs

(MWO 2-86-3811).

The Team examined the documentation listed above and additional

supporting documentation as follows.

-

. December 17, 1987 Correspondence from S. B. Tipps to C. T. Jones

(Log: LR-REG-029-1287), regarding improper hydraulic control

unit installation at BWR Plants - This correspondence states

that in the process of resolving these NRC items, it was

determined that during the construction of both Units 1 and 2

the torque value for the HCU hold-down bolts was not specified.

The torque value information was subsequently obtained from GE

(letter G-GPC-6-266 of July 22,1986).

-

July 22, 1986 Correspondence from GE to GPC (G-GPC-6-266),

regarding Hatch I and 2 Hydraulic Control Unit Dynamic

Qualification - Regarding loose hold-down bolts and missing flat

washers, this correspondence states that, subject to the

conditions that no previous upset or faulted events have

occurred at the Hatch I and 2 site and that the six extreme

bolts in the eleven bolt hold-down pattern are in place and are

at least snug tight, the installed HCU's will remain operable

through at least one future faulted event.

_ _ _

u .

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.( T

8

The.. six extreme bolts are the four -bottom bolts and two upper -

bolts. The bolt torque values are given in.tho_ Reference 2-test..

specification. The relevant pages of that specification : are

provided as Attachment'1.

LThe team noted that Note 1 of Attachment 1 to GE Correspondence

G-GPC-6-266.provided a limiting torque value of 50 foot pounds for

the.0.50 inch bottom bolts and 15 foot pounds for.the 0.375 inch top

capscrews. The Team requested occumentation verifying the torque for

the Unit 1 and Unit 2 top bolts.(capscrews),

Cognizant licensee personnel responded that the torque levels had not

been previously checked for the top bolts but would be ' accomplished

during. this inspection.

Licensee Action

The'. licensee' completed. activities to torque the HCU.back-to-back top

plate mounting capscrews to 15-25 foot pounds for all HCUs and

confirm full thread. engagement. . (MWO No. 1-89-010977 for Unit.1 and

MWO. No. - 2-89-00727 -' for. Unit 2). Results revealed excessively loose

bolts on 18 HCUs for Unit 2 and 5 HCUs for Unit 1.

Conclusion ~

After review of the above, the Team informed cognizant licensee

personnel . that this. issue was considered a lack of conformance to

-10 CFR 50, Appendix B, Criterion XVI- and_ would be identified as

Violation'321/366-89-02-02. Failure to Complete Adequate Corrective

Action (See paragraph 3.c. for an additional example of this

violation).

c. Failure to have unique fittings on; the plant service air system

(breathing air) outlets.

Background

The licensee is required to have unique. fittings on the service air

system to prevent inadvertent use of nonrespirable air when using

supplied-air respirators. The need to have unique fittings was

documented.in a study made in 1981. The licensee also identified

failure to have unique fittings for the Service Air System in 1987

and again in 1988. However, in 1989, the team determined that the

licensee still did not have unique fittings for the service air

system.as identical fittings were found on Instrument-Air and Service

Air Systems. See paragraph 4.m. of the report for further details.

l

L____ _- . _ - . . _ - _ _ _ - _ _ _ _ _ - _ - - - _ _ _ _ _ _

- - _ ._ -- _.

- _. - _-_

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Findi igs

l

10 CFR, Appendix B, . Criterion XVI, requires that measures shall be

established.to assure that conditions adverse to quality, such as

' deviations and nonconformances are promptly. identified and corrected.

The, team determined that the licensee'in the past had identified at

least three': examples of noncompliance relative to. breathing air

L fittings. and failed .to take adequate corrective action to preclude

repetition '(see report paragraph 4.m below for details). The team

stated that . failure to take prompt and adequate ' corrective action

for not having unique breathing air fittings'.is a violation of the

Quality Assurance. Program,10 CFR 50, Appendix B, Criterion XVI and

is another example of Violation 321,366/89-02-02, identified in

paragraph 3.b. above.

d. Failure to Sample the Plant's' Breathing Air System

Background

Administrative Control Procedure, 60AC-HPX-006-0S requires that

respirable air supplied by air compressors and cylinders meet the

minimum requirements of Grade D air as prescribed by the Compressed

Gas - Association Commodity Specification G.7-1-1966. The procedure

further requires that respirable air be sampled at least quarterly.

Further details are provided in paragraph 4.m.

Finding

Contrary to the above, the licensee failed to follow procedure

60AC-HPX-006-0S during the fourth quarter of 1988, in that the

respirable air used to fill self-contained breathing apparatus was

not sample and analyzed. .This was identified as Violation

321,366/89-02-03, Failure to Take Breathing Air Samples.

e. Failure to Follow Acceptance Criteria for Weld Patch on Unit 2

Reactor Building Roof Drain

Background

During a general inspection of the 130 foot elevation of the Unit 2

Reactor Building, the Team noted a welded patch (approximately

3" x 4" x 3/8" plate) on the 20 inch schedule 10 Roof Drain (MPL

No. 2T55-RSD-5) which exhibited apparent welding discrepancies. The

1/4 inch fillet weld' attaching the patch to the drain pipe exhibited

poor weld profile and excessive grinding (more than 1/16 inch below

pipe' surface). Further, the welder's ID was not stamped on the pipe.

- - - - - - -

.

..

10

The Team noted that this section of roof drain also served to main- i

tain isolation of secondary containment and questioned the licensee

as to whether adequate minimum wall thickness had been maintained

for the excessively ground area. The Team further requested for

review a copy of documentation showing acceptance of the present

condition.

Licensee Action

Cognizant licensee representatives completed a deficiency card

(No. 2-89-0505) during this inspection to accomplish ultrasonic

thickness measurements which indicated that the ground area was ,

reduced to 0.165 inch thick; i.e. less than the manufacturer's i

tolerance of 0.219 inch. However, the gouge did not violate the

0.145 inch design minimum wall thickness.

Documentation Reviewed

The Team reviewed documentation associated with MWO 2-85-1424 and QC

acceptance of the initial weld dated March 27, 1985. Cognizant

licensee personnel agreed that the initial acceptance had been in

error since the weld inspection plan imposed at that time (A-MB-01,

Rev. 1) prohibited excessive grinding and required an acceptable weld

profile and the welder's ID stamp on the pipe.

During this inspection, cognizant licensee personnel completed an

independent review of other welds accepted by the QC inspector 1

involved and conducted additional training on weld acceptance. QC

management personnel felt that the error on MWO 2-85-1424 had been an

isolated example.

The Team completed an independent verification by examination of the

QC program, interviews wie several QC inspectors and reinspection of

several welds recently accepted by the QC inspector involved.

Further details of this review are included in paragraph 4.k. below.

Conclusion

After completion of the above, the Team concluded that the error in

initial acceptance of the welded patch had been an isolated example,

and that overall, QC at Plant Hatch was a strength in both program

and implementation.

The Team informed cognizant licensee personnel that this issue would

be identified as Violation 366-89-02-08, Failure to Follow Acceptance

Criteria for Weld Patch on Unit 2 Reactor Building Roof Drain.

However, due to the low safety significance, isolated occurrence, and

previously completed licensee corrective actions, this violation will

not be cited.

- __ _ _ -

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. - _ _ _ _ _ _

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a

r ~f. Programmatic Link Cetween Maintenance Procedures and ASME B&PV

Section XI Requirements

t-.

Background

b During the Team's examination of the Maintenance Program, a need was

identified for additional requirements to ensure proper coordination

and testing for ASME Section XI .:omponents. An equivalent need was

also identified for the predictive maintenance program, particularly

for vibration analysis. Details are listed below:

[ -

Procedure 50AC-MNT-001-0S establishes the requirements and

b responsibilities for the control of maintenance activities at

Plant. Hatch. This procedure details requirements for intiating

'

and processing MW0s. Additional details for MWO processing are

included in procedure DI-0AP-10-0588N. Neither 50AC-MNT-001-0S

nor. DI-0AP-10-0588N clearly specify that for a Section XI

component, - Section ' XI . programs are to be reffered to for

.

determining post maintenance testing requirements. This

omission is of concern due to the potential differences in. post

,

maintenance tests (functional ~ tests) . required for Section XI

components'versus other components.

-

Preventive. Maintenance Proceduro 53PM-MON-001-0S describes the

- ' method used to obtain and analyze vibration analysis data for -

the purpose of detecting. incipient failure of equipment. The

, program is intended to apply to. preventive maintenance only and

l not to interface with any Technical Specification requirements.

The procedure is applied by maintenance engineers and does not

necessarily require that an MWO be issued. Section 5.2.2

states:

"The vibration monitoring program governed by this proededure is

for preventive maintenance purpcses only. When actual vibration

levels exceed preidentified. suggested maximum recommended

levels, this does not necessarily mean that the associated

equipment is inoperabl.e, instead the information is intended for

use as a diagnostic tool to indicate the need to perform

additional testing, schedule future maintenance or do other

analysis of equipment condition."

The above is of concern since there is potential that the

referenced vibration analysis can apply to a Section XI pump.

In that case, if vibration results exceed the requirements of

ASME,Section XI, Subsection IWP, Table IWP-3100-2 of Section XI

must take precidence and proper actions taken to satisfy

Section XI requirements.

_ - _ _ _ _ _ _ . _ - _ _ _ - _ _ _ - _

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Conclusion

'

Cognizant licensee _ personnel agreed that correction to 50AC-MNT-003-0S

should be completed to require that an MWO for a Section XI component

be so identified. However, licensee personnel were concerned' that-

-a: predictive. maintenance vibration analysis not .be considered an

equivalent to the Section XI type test. The ' Team concurred with

'

this: reasoning but noted that a full spectrum vibration analysis was

. presently being taken when monthly readings indicated a potential

problem (1.e. a situation most apt to be equivalent to the Section XI

alert or action range) and that the computer comparison'to.Section XI

"

type vibrations in mils could be automatically accomplished. After

. . further. consideration the licensee agreed to the need for tying

vibration test results to Section XI requirements.

3

The . Team informed cognizant licensee personnel that NRC concern

,.

'

regarding' a programmatic link between Section XI requirements and

i

- procedures 50AC-MNT-001-0S and 53PM-MON-001-0S would be identified as

IFI 321,366/89-02-04, Programmatic Link Between Maintenance '

~ Procedures and ASME Section XI Requirements,

g. Inspection of RHR Hanger Weld Removal

'

l' Background

During a general inspection of QC activities, the Team became

involved in discussions between engineering and QC supervision.

regarding final review and close out of MWO 1-88-5022. This MWO

accomplished modifications of several RHR supports located in the

Unit 1 Reactor Building. Changes included installation of a new

,

embed support plate and adjustable rigid strut to the existing pipe

clamp.

Additional repairs to support E11-RHR-H293 were required due to slag

pockets in the existing welds which attached the pipe clamp support

lugs to the pipe. The support lugs were removed and the weld area

ground to sound metal. Field weld IE11-HFW-059 was made to repair

!: the ground area. However, there was no indication that a QC

inspection of the excavated area (fit-up inspection) was done.

Technical Requirements

The Team noted that ASME,Section XI, Subsection IWA-4130, requires

that:

Repair operations shall be performed in accordance with a program

delineating essential requirements of the complete repair cycle ...

including the flaw removal method, method of measurement of the

cavity created by removing the flaw, and dimensional requirements for

reference points during and after the repair ....

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l. The. Team also noted .that paragraph 7.1 of licensee procedure

42EN-ENG-014-0S, states'that:

~~

%' Documentation required by ASME Code is included in the scope of

Repair / Replacement Program and shall include the following as

applicable: a description of the flaw, the method which

^

... revealed the flaw and the location of the flaw; the flaw-removal-

method and the depth of excavation; and an evaluation of' the

g. flaw or failure to, ensure the selected repair or replacement is

F suitable prior to repair.

'

Documentation Review

! -

The . Team reviewed quality documentation associated with MWO

.1-88-5022 to re-verify the statements made above.

-

The Team reviewed additional quality documentation to verify

that:

-

A NDE (PT/MT) was intially required for the lug removal on

'

. Hanger- E11-RHR-H293 (Step 8A on Work Process Sheet No.

81-058-M105).

The. MWO was intially considered a Section XI replacement /

repair (R/R Applicability Checklist, dated September 8,

1988).

The repairs to 1E11-RHR-H293 received an engineering

exclusion (R/R Checklist, dated November 15, 1988) with

basis as follows:

"When original construction installed lugs, .2 slag pockets

were left in the pipe wall. This revision of the original

MWO is to base metal repair pipe wall. This part of MWO is

not in R/R program."

Licensee Response

Cognizant licensee personnel informed the Team that the engineering

decision to exclude the repair weld 'from the Section XI R/R program

also removed any requirements for NDE of the excavated area.

Cognizant licensee personnel were unable to provide any alternative

assurance that the flaw had been completely removed and were not

aware of any programmatic requirements for flaw removal evaluation

outside of those imposed for Section XI R/R components.

Conclusion

Cognizant licensee personnel informed the Team that a question

regarding omission of the fit-up inspection for weld IE11-HFW-059 had

been raised by the ANII during review of documentation for MWO {

4

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1-88-5022 and final resolution had not yet occurred.

a

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'At the end of the inspection, this_ problem was still being evaluated

by'the licensee. The Team informed cognizant licensee personnel that

NRC cencern - regarding programmatic requirements for examination /

evaluation of welding flaws would be reviewed during a future inspec--

tion andcident.ified as IFI 321,366/89-02-05, Inspection of RHR Hanger

l _.W eld Removal.

L

h. Design Verification of Containment Isolation Valves T48-F310 end F311

The Team examined licensee activities in response to NRC' Generic

- Letter _ (GL) 88-14. The purpose of GL 88-14 is to request that each

licensee review NUREG 1275, Volume 2 (Operating Experience Feedback

Report - Air System Problems) and then perform a design and operation

verification of their Instrument Air System (IAS). . Verification was

to include:

Item 1- -

Verification by test that actual instrument air

quality is consistent with the manufacturer's

recommendations for individual components served.

Item 2 -

Verification that . maintenance practices, emergency:

procedures, and training are adequate to ensure that

safety-related equipment will function as intended on-

loss of instrument air.

' Item 3 -

Verification that the design of the entire instrument

air system including air or other pneumatic accumula-

tors is in _accordance with its intended function,

including verification by test that air-operated

safety-related components will perform as expected in

accordance with all design basis events, including a

loss of the normal instrument' air system. This design

verification should include an analysis of current

air-operated component failure positions to verify

'that they are correct for assuring required safety

functions.

A final requirement, Item 4, was to provide a discussion of the

licensee's program for maintaining proper instrument air quality.

Background

The Team reviewed the licensee's initial response, dated February 10,

1989,'to GL 88-14 and noted licensee statements as follows: ,

-

The' reviews and/or investigations to date indicate that the

design, installation, testing, operation and maintenance of the

instrument- air systems at Hatch Nuclear Plant are adequate to

ensure the proper and reliable operation of pneumatically i

operated, safety-related equipment.

l

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Upon completion' of the . additional evaluations, a subsequent

report will - be - submitted. This report is scheduled to be

-provided by June 1, 1989. A final report will be issued upon

l- completion of all actions associated with GL 88-14.

Documentation Review

The . Team held discussions with cognizant licensee personnel and

reviewed additional documentation associated with GL 88-14 activities

as follows:

-~ Documentation associated with air sampling and station service-

air compressor (SSAC) maintenance and reliability.

3

--

. Documentation associated with design verification of MSIV,

'

Containment Vacuum Breakers, and Containment Isolation Dampers

(valves).

A ' complete. list of documentation reviewed is -included in

paragraph 4.1.

Conclusions

The. Team. noted that the licensee had completed comprehensive

activities. in response' to GL 88-14. However, design verification -

was not yet complete for critical . components (Valves T48-F310 and

F311). These valves are redundant to the torus vacuum breakers, and

use instrument air pressure' to maintain the valves in the closed

position. Upon loss of air pressure, these valves are designed to

open to ' allow the vacuum breakers to perform their safety function

of preventing containment implosion. When the valves fail open, the

isolation function of the valves is lost.

The Team further noted that the Unit 2-valves had failed LLRT testing

during the last refuel outage. The Team informed cognizant licensee

personnel that NRC concern regarding adequate design verification

would be identified as IF1 321,366/89-02-06, Design Verification of

Containment Isolation Valves T48-F310 and T48-F311. The resolution

of this matter by the licensee will be reviewed during a future NRC

inspection.

1. Failure to Have Adequate Procedures for Sampling Plant Breathing Air

Background

The licensee is required by 10 CFR 20 to sample respirable air to

meet Compressed Gas Association Commodity Specifications G.7-1. The

, specifications define limits for oxygen content, hydrocarbons, carbon

monoxide, and carbon dioxide. The licensee is required by licensee

Technical Specifications 6.11 to have procedures consistent with

= - _ _ _ . . - _ -

_- . . _ _ _

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.

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.

10 CFR 20. The Technical Specifications also. requires that the

procedures be approved, maintained and adhered to for all operations

involving personnel' radiation exposure.

Finding

The team determined that a licensee audit of health physics was being

made during the inspection period and that the lack of procedures for

sampling and-analyzing Grade D air had.been identified by the Quality

Assurance Auditor. The. inspectors determined that the licensee had

also . initiated some corrective action. concerning sampling

requirements. In order to review the licensee's corrective actions

forf failure : to have ' a written procedure, IFl 321,366/89-02-07,

Written Procedure for Sampling Breathing Air, was identified.

4 :

4. Inspection Details

' The Team performed walkdown inspections, observed maintenance in process,

reviewed maintenance history records and MW0s, and reviewed . maintenance-

procedures to evaluate the overall maintenance program. The following

paragraphs summarize the details of the. inspections / reviews performed.

,

a. Wal kdown . Inspections

The Team . conducted a ~ general inspection of Units 1 and 2 turbine

buildings, control buildings and reactor buildings. The inspection

included observation of general equipment condition, housekeeping

practices, deficiency condition and control, and identification

. practices for permanent plant equipment. In addition to general

<

cleanliness, mechanical equipment was observed for . water Land oil

leaks, corrosion, lubrication, proper fasteners, evidence of

vibrations,.etc. Electrical equipment was observed for cleanliness

of equipment. and general area. (floor, etc.), painting, equipment-

grounding, corrosion, control wiring terminations, broke or _nissing

relays, meters, lamps,' etc. , proper labels, conduit and tray '/111 and-

l support, floor and wall penetration seals, bushing tightness,

L lighting, missing fasteners, cable tie wraps and supports, wire and

cable'nos., namplates, etc.

Appendix C is a list (not all inclusive) of the equipment and areas

observed.

The following is a list of deficiencies identified by the team:

-

Small leaks at valves 2C11-F0468, 2011-F005, IN21-N8178 . and

IN43-F138.

-

Small steam leak at 1 inch union, E41 System, Unit 1, HPCI Room

-

Missing insulation - About 2 feet of 2 inch diameter pipe near

bottom of Unit 2 Main HPCI pump

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17

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Conduit support and tubing on floor in demineralized valve nest

(Unit 1)

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Tag for valve IN21-F447B laying on floor

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Valve 2P51-F087 handwheel tied in place with cable tie wraps

-

At Unit 1 Main Generator Exciter Housing - conduit loose,

bushing loose

-

At Unit 1 Main Generator - stator cooling piping, insulation

covers broken, and lamp covers missing at diode indicators

-

IP63-B001A Turbine Building Central Water chiller - water on

floor

-

208V MCC IG 1R24-S0-45 Frame 10 (RFPT 1A Hi Pres

Steam) -corrosion on starter pan

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Turbine building leak allows rain water to drip near or into

IR22-S003 4.16 KV IC SWGR

-

Stator Water Cooling System - turbine building ground floor

Small oil leak at pump B

  • Valve IN43 F138 Y-61 stator cooling make-up inlet - leaking

-

H2 and stator cooling panel IN43-P001 - annunciator "VAC TR OIL

LEV HIGH-LOW" flashing

-

At 1R23-S002 600V SWGR IB - Some compartments have heavy dirt

inside, example - normal feeder to turbine building chiller 208V

SWGR 1A

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4160-600V station service transformers have PCB insulation

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Transformer 1R23-S001 Small leak at fill valve

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Corrosion on diesel generator battery racks

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At batte ry 2R42-S002A, battery 2A - scrap and debris in sump

drain may plug drain

-

At cooling tower electrical house near tower No. 4 - metal

building siding stored on vent fan enclosure

-

Cooling tower No. 4 - loose grounding wire on SW corner

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At feedwater. pump N21-C003A-

208 V panel - most cover bolts missing

condulet cover loose

'

scrap sheet metal stored in area

valve IN21-N817B leaking-

-

Welding problems associated with a weld patch on the Unit 2

Reactor Building roof drain (see paragraph 3.e.)

-

Redundant conductivity recorders (CE-N424A and CE-N424B) for

recording condensate conductivity downstream of two of the

demineralizers were inoperative. This was more a loss of

convenience than a problem with system operation or safety as

the conductivity is recorded by larger more accurate recorders

in the demineralized area.

The' Team reached the following conclusions from the above

examinations:

,

-

General Equipment Condition

Most of the maintenance items noted had not been identified by

the licensee. However, all of the items were .reselved during

the inspection period . by. issuance of work. . orders or other

acceptable means. The licensee presented similar punchlists of

items. identified durf tp their walkdowns. When compared with the

overall equipment conaition and plant maintenance, the various

housekeeping and equipment condition problems listed above were

considered relatively minor.

-

Housekeeping

During the above inspection, the Team observed general

housekeeping conditions. Programmatic Control of Housekeeping

is maintained by procedure 51GM-MNT-002-0S.

The Team noted a general high level of cicanliness within all

areas of the plant. The Team conse sus was that general plant

housekeeping is a major strengto.

-

Deficiency Identification and Control

The Team noted relatively few discrepancies without MW0s issued

for correction. Further, no major discrepancies were identified

without MW0s issued.

1

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.The Team consensus was that deficiency - identification and

control was a programmatic strength'at Plant Hatch.

-

ID of Permanent Plant Equipment

During the above inspection, the Team observed that

identification of perranent plant equipment was never in

question, due to the use of equipment identification tags,

decals, etc. which were prominately located, securely att' ached,

and of a size to be clearly legible.

The Team consensus was that identification of permanent plant

equipment was a programmatic strength at Plant 1.atch.

b. Repeat Failures - LPCI Inverters

During the evaluation of the maintenance program, various instances

of ' what appeared +o be repeat troubles / failures were examined.

Discussions were held with various licensee personnel concerning

repeat problems with LPCI inverters. The following summarizes the

discussions and examinations:

During a period of 17 days, LPCI inverter 1R44-S002 was found to have

blown fuses twice and LPCI inverter IR44-S004 had a blown fuse once.

After the third failure, an Event Review Team was organized to

examine the problem.

L

Root cause' analysis revealed that the failures were due to the

installation of incorrectly rated parts which were supplied by the

vendor. This problem was unique to. this plant in that the output

voltage for these irverters is 600V AC (Rather than the more common

480V) and the parts of the Plant Hatch .LPCI inverters must be

modified by the manufacturer. The parts were identified by the same

part number as the 480V part, however, and therein was the problem.

Failure to uniquely identify the modified parts led to the use of

underrated parts. It should be noted further that there are. similar

'

inverters installed in other newly installed mystems wh'ch have 480V

AC as the required output.

-The reports reviewed were complete and indicated that good

engineering practices had been employed in solving this problem,

c. Feedwater Control System

Units 1 and 2 have experienced several feedwater control problems.

These problems were also investigated relative to repeat failures.

h Following is a summary of the licensee's approach to solving these  !

problems:

-

It was determined by analysis of failure rate and consultation

with GE that a certain manufacturer's capacitors were failing in

- _ _ _ _ _-__ : _ __ __ _

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the GEMAC compone'nts. I&C. started ~a program to change out these '

!

type capacitors with more reliable ones. 1

--

Based on a GE SIL recommendation, a DCR was initiated to remove

the density correction instrumentation in the feedwater. control

loop. This DCR removed approximately .11 modules (GEMAC) which

f

made.the control loop more reliable due to a lower probability

of a component failure. Of the GEMAC components that were left

'

in the loop, the majority were replaced with TOSMAC components,

a GEMAC eauivalent made by Toshiba. Any components not having

TOSMAC units for replacement were replaced with components

l

(GEMAC) . refurbished by GE. This DCR was completed on Unit 1

' this past outage and will be completed on ' Unit 2 during tne fall

refueling outage.

-

A. problem was found with the cascade switch on the GEMAC

controllers. The switches were found to be intermittent. A DCR

was initiated to solder a jumper across the switch facilitating

a much more reliable continuity path. This DCR has been

' implemented on Unit 1 but not on Unit 2.

-

Recorders have been connected to various_ points in the feedwater

control loop so . that if a failure does occur, data can be

collected for an accurate determination of the failure mode.

-

Feedwater control problems on both Units have been reduced from

feedwater swings occurring frequently, including Unit trips, to

a feedwater level dip of approximately 4 inches at which time

the controller .immediately catches the decrease and compensates

for it. These fluctuations happen very infrequently. The

.overall performance .of the feedwater control system has been

vastly improved.

In the above. listed instances, the licensee solved their problems

using a variety of different methods.

d. RHR System - NRC IN 87-30

During review of the RHR system, the Team examined the licensee's

responsive actions to NRC IN 87-30, Cracking of Surge Ring Brackets

in large General Electric Company Electric Motors. The RHR Pump

Motors 1E11-C002B and IE11-C002D had been modified by installing new

improved design surge ring brackets. The brackets for RHR Pump

Motors 1E11-C002A and IE11-C002C had been inspected and no problems

were found. The surge ring brackets for the A and C RHR Pump Motors

will be replaced during the next refueling outage. The work will be

performed under Design Change Request No.88-190, which covers the

four RHR pump motors and the two core spray pump motors. It was

further determined that the parts were onsite for the modifications.

_ - _ - _ _ - _ _ _ _

_ _ _ __

-

, ,

1..

,

E 4

For Unit 1, core spray pump motor IE21-C001B had been modified and- )

'

.

'

core spray pump motor 1E21-C001A is scheduled to be modified during ,

the next refueling outage. The motors for the core spray and RHR

pumps for _ Unit 2 are ' a different design and will _ not require

modification.

I

It appears that the licensee responded well to this industry / vendor j

-initiative'and the NRC Information Notice 87-30.

e. Observation of In-Process Maintenance

~(1) Repair _ of Intermittent Alarm on Station Service Battery Charger l

Observations

The team observed the performance of MWO 1-89-00722 which was

issued to repair an intermittent alarm condition on station

service. battery charger 10. The AC voltage failure relay which

was.specified as the part to be replaced was incorrect. The MWO

was revised and the under-voltage alarm relay was specified.

The steps required to revise the MWO were followed including QC

verifications.

The old under-voltage alarm relay was tested and the

l repeatability was cut of tolerance. A new relay was installed.

When the charger was re-energized, the AC voltage' failure relay

chattered. Voltage measurements taken indicated low output

voltage (84 VAC versus 125 VAC). During the troubleshooting to

determine the cause of the low AC voltage, it was discovered

that the control fuse holder cover was loose. When the cover

was fully in place, the AC voltage returned to normal. The fuse

holder was examined and all fuse clips and cover fingers were -

cleaned to ensure proper electrical contact. The charger was

returned to service. Later follow-up of the completion of this

MWO revealed that the battery charger was only tested for proper

operation. There was no evidence that the alarm function was

,

tested.

Conclusion

Additional examination of this MWO and the process by which MW0s

are revised revealed a procedural weakness associated with

proper review of nw:essary post-maintenance test changes for

revised MW0s. This is discussed in paragraph 5.c.(1).

_ _ _ _ __ _ _ _ - _ _ _ _ _ _ _ _ _ -

__ _ _ _

.

.,

, :> .

22

(2)' Cooling Tower Motor Changeout

'

Observations-

The Team. observed portions of a cooling tower motor changeout,

' protective. relay calibration, recirculation pump motor generator

set-brush surveillance and 480 Volt circuit breaker trip device

calibration.

Conclusion

In. all cases, procedures were being followed and data carefully

.

. recorded.

(3) Replacement of Programmable Controller in Demineralized Building

Observations

Thisf activity was assessed with respect to the adequacy of the

mainte' nance effort, whether applicable procedures were followed,

and whether operations personnel were aware that the subject

maintenance was being performed.

During this ~ activity, an I/C technician was observed while

replacing a backup battery for the programmable controller in-

. the demineralized building. This individual appeared to be

well qualified for the. task. He had previously worked.for the

manufacturer of -the control _ler. The technician received the 1

'

folder for MWO 1-88-8411 from the shift foreman; obtained a

sign-off from the . shift supervisor in the control room; and

thereby informed operations personnel that the maintenance

effort was to be performed; obtained the ' spare part (battery)

from the warehouse; and replaced the battery. Proper installa-

tion of the battery was shown when the annunciator light for

the controller cleared.

Conclusion

The task was well performed, applicable procedures were .

'followed, and the control room personnel were aware that the I

activity was underway.  !

(4) Operability Test for RHR Pump 2E11-C002A

Observations

This activity was assessed with respect to adequacy of the

maintenance effort, whether applicable procedures were followed,

and whether operations personnel were aware that the subject

maintenance was being performed.

i

s

._. _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ . . . _ _ _ _ _ _ _ _ _ _ _ _ _ _. _ . _ . _ _

,_ -_- - - _ _ _ - - _ _ _ - - - -- _.

_ - _ _ _ _ - - _ _

. _ - _ _ - - - - _

sv -

l 4 '.

, l

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23 l

"

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!. 1

During this activity, maintenance testing regarding RHR pump

2E11-C002A was observed. Procedure 34SV-E11-0012S was . used

to determine operability of_ the pump. The- following : actions ,

were performed during the operability test: (1) telephone -l

communication with control room personnel occurred, (2) oil i

level was checked,-(3) verification that the service water valve j

opened, (4) the pump ran for five minutes, (5) the discharge '

'

pressure of 190 PSIG was read from. the appropriate gauge, and l

(6)..the discharge pressure was conveyed by phone to the control  ;

room.

Conclusion

.

. The task was well performed, the applicable procedures were l

followed, and 'the control room personnel were aware thet the

activity was' underway.  !

(5) Preventive Maintenance on Fire Pump 1x43-C001 j

Observations .!

!

. The Team observed preventive maintenance on electric fire ,

protection pump 1x43-C001 (MWO 1-88-08388). l

l

The maintenance mechanics were working from a copy of l

Section 7.7 of procedure 52PM-X43-006-15. post-Maintenance i

testing of pump temperature and vibration as well as operability

tests were compitted.' j

In.the course of performing the above preventive maintenance,

the craftsmen noted.that the relief valve was lifting while the

pump.was running and' deficiency card 1-89-1209 was written. l

)

During this inspection, the Team also noted a small water leak i

from jockey fire pump IX43-C003. Deficiency card 1-89-1210 was i

written for correction.  !

1

Conclusion ]

The Team concluded that the fire pump preventive maintenance and

post-maintenance testing were performed in accordance with the j

appropriate plant procedures. Deficiency cards were written

for the deficiencies found in the course of the maintenance

operations. No discrepancies were identified.

(6) Motor Shaft Pinion Key Replacement j

l

l

1

_ _ - - - _ _ _ _

_ _ _ _ . ___

.

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24

E

r

<i Observations

".

The Team observed performance of MWO 1-89-308 to replace the -

pinion gear key (Part Number S/N '87160-63368) in MOV 1E41-F011

in response to-NRCLIN 88-84. Procedure 52GM-MEL-022-05~was used

and a QC inspector was present.

A' functional test on' the reassembled valve was performed and

indicated proper operating characteristics.

Conclusion

L

h The Team concluded that the above corrective maintenance was

performed in accordance with appropriate procedures. No

discrepancies were identified.

. (7) ' Overhauling of Waste Collector Pump Bearing

f

Observations

i. Following the performance of MWO 2-88-4862 to change the oil in

Waste. Collector Pump 2G11-C016,- the plant ' equipment operator

-felt'the inboard bearing and thought it was too hot.

MW0' 2-89-400 'was issued to " Rebuild" the pump using procedures -

51GM-MME-0020 and 51GM-MNT-0020. Maintenance craftsmen ignored

the " Rebuild" order and instead began " troubleshooting" the

pump. The. team observed the troubleshooting of the' pump. The

craftsmen could detect no' sticking or grinding as the pump shaft

was turned by hand. A maintenance engineer determined that the

temperature and . vibration. of the pump while operating were

normal. With a laser device, the engineer checked the alignment

of the motor shaft 'with the pump shaft and found .them properly

. aligned. Since. the pump was operating normally, the MWO was

closed out without further work.

Conclusion

The Team noted the proper activity of the craftsmen in response

to the." trouble" involved. However, the Team consensus was that

the MWO should have been more definitive regarding tasks to be

accomplished.

(8) PM on Overcurrent Rela" Calibrations

Observation

The Team observed the overcurrent relay calibration for Conden-

sate Booster Pump 2A, Phase 3, per procedure 57CP-CAL-108-2S.

_ _ _ _ _ _ _ _ _ _ _ _ _ -

~

25

Conclusion

No problems were identified.

f. Electrical Maintenance

The Team reviewed the electrical PM procedures as detailed below.

This inspection effort was directed at answering two questions:

(1) Were there procedures in existence to cover all the normal

preventive maintenance activities that should be governed by

procedures?

<

(2) Were the procedures of sufficient quality to be considered

acceptable for maintenance work at a nue'aar power plant?

Question (1) was addressed by studying the index of procedures and

discussing with the Maintenance Engir.eers any apparent gaps that

could be discerned from the index. . There were about 27 electrical

preventive maintenance procedures that applied to each unit. Motor

maintenance was included in the maintenance of the driver equipment.

Comments resulting from the procedure index review were:

-

The fact that the maintenance program does not include

protective trip testing of molded-case circuit breaku (other

than containment penetration circuits) is considered a weakness.

-

The fact that the maintenance program does not include periodic

visual inspection of the 4160 volt current limiting reactors is

considered a weakness.

To address question (2), the preventive maintenance procedure for the

4160 volt switchgear was reviewed in detail. Several comments were

generated during review of this PM procedure which represent program

weaknesses. Refer to Section 3.a. for complete details.

In order to help evaluate the effectiveness of the maintenance

organization, the team reviewed the work history for the 4160 Volt

System and the High Pressure Coolant Injection System for Unit 1.

These reports gave maintenance work order details for at least the

last two years. It was concluded from this review that repetitive

failures of these two systems had not been a problem at Plant Hatch

and that root cause analysis of problems for these two systems was

satisfactorily carried out.

Trending reports, as an indicator of maintenance work control, were

reviewed. One report, dated March 1,1989, indicated that the total

electrical corrective maintenance backlog was 52 work orders, which

is relatively very low. Another report indicated that for 1989, all

periodic / planned MW0s were completed within the allowable time.

_ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ - _-

,. -

- - . - - _ _ _- _

- - ___ --

.,

- ,:

it

't 26

Report No'. 41, " Equipment with greater than five corrective

L maintenance work orders for'1988," indicated that repetitive failures

>

of electrical components had not been a problem.

g. Machine Shop Facilities

Observations

The Team was able to observe . general conditions and specific

activities during this inspection for both the- clean and " Hot"

machine _ shops. The shops are well laid out with adequate space,.

equipment, and partitioning to accomplish a variety of tasks

associated with machining, cutting and welding, troubleshooting and

assembly / disassembly bench work. The clean machine shop also has

adequate ' space .and. bench cabinetry for tool storage by individual

mechanics.

The hot . machine shop has less space and equipment than the clean

.

machine shop, but large machine tools are installed and the space

L appears adequate .for a variety of " Hot" machining tasks due to good

organization. of the space involved. A. special " Bailey"

building / facility is included for CRD repair. The atmosphere of~the

L " Hot" . shop is controlled, and radiation monitors, decontamination

~

i equipment and health physics support appeared adequate.

.

Conclusion.

'

After review of the above, the team consensus was: the " Hot" and

~ clean machine shop facilities were a strength in the maintenance

program.

h. Craft Personnel and Training

. Observations

The Team completed an overview examination of all phases of the

licensee's training program for mechanical / electrical and I&C craft

l

personnel by review of programmatic procedures, courses involved, and

discussions with maintenance management personnel.

The Team also completed a review of the current interim

classification matrix records for all mechanical and electrical

craft.

In addition, interviews were conducted with a random sample of

i mechanical craft. Those interviewed were asked specific questions

! related to methods to minimize and control hot particles (radioactive

l' particulate) during grinding, troubleshooting and repair of

centrifugal pumps, inspection and repair of valves (including seat

L

i

___

14:

sc

27L

,

'

lapping, troubleshooting and repair of MOVs). General questions were

also asked, regarding the.following procedures:

o

l. 50AC-MNT-001-0S, Maintenance. Program

!~ t

51GM-MNT-002-05, Maintenance, Housekeeping and Tool

,

Control

52CM-MME-001-0S, Repacking Valves and the Adjustment

of '/alve Packing'-

<

52CM-MME-005-05, Limitorque-Valve Operator Models

SMB-0 through SMB-4 Mechanical

Maintenance

h All. questions were satisfactorily answered.

[ Findings

The . Licensee's maintenance t raining program received INP0 accredita-

tion in April 1987. -The training has been fully implemented and

includes full time- training coordinators. The training is completed

in phases. with . an additional monetary incentive attached to each

phase which ensures craft interest in advancement. An overview is

as follows:

--

Mechanical

. The mechanical training program' consists of six phases.

The completion of phases 1 through 5 is mandatory for all

mechanics. Phase 6, however, consists- of specialized

skills ~ training. All mechanics are not required to

complete all courses in phase 6.

,

-

Electrical

The electrical training ' program consists of 6 phases. The

completion. of phases -1 through 5 is mandatcry for all

electricians. Phase 6, however, consists of specialized

'

skills training. All electricians are not required to

complete all courses in phase 6.

. -

I&C

,

.The I&C technician training program consists of 4 phases. I

The completion of phases 1 through 3 is mandatory for all

technicians. Phase 4, however, consists of specialized

, skills training. All technicians are not required to

complete all courses in phase 4.

i

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1

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28

9

~ -

Continuing Training

Continuing training modules for mechanical, electrical and

I&C have been presented twice .a year since these. programs

were accredited in April 1987. To date, four modules have

L .been presented for each area.

'

Prior , to completion of formal craining, craft are assigned tasks

using an ' interim qualifications matrix. The matrix was assigned to

reflect evaluation of each craftsman' by' a qualification committee

based 'on .the. applicant's prior job performance, knowledge,

,

proficiency- and training. Control i s -' maintained by procedures

'

DI-MNT-10-0287N, and DI-MNT-11-0278N. Craftsmen unable to.

satisfactorily complete the. formal training -course also loose their

interim qualification and are considered not qualified for the area

of concern.

Present maintenance management goals are to have all craftsmen fully.

certified (through phase 5 for mechanical and electrical and phase 3

for.I&C) by the end of 1989.

Maintenance supervisors provide surveillance to assure that craft are

adequately trained for the job assigned. The Team reviewed an

example where supervisor surveillance during this -inspection

identified need for additional training for the craftsman involved.

The Team did identi fy a training deficiency since the training

department did not provide any training for performing preventive-

maintenance .on 4 KV switchgear. At the time of this inspection, a

lesson plan for this was being developed as part of the phase V of

INP0 training program.

Conclusion

The Team consensus was that the Plant Hatch training program is a

strength.

1. Instrument Air System (IAS)

Observations

The Team reviewed a listing of open MW0s on the P51 Service Air

and PS2 Instrument Air Systems for Unit I and Unit 2 to identify

potentially recurring problems. The Team noted repeat problems with

the station service air compressors (SSAC) and cognizant licensee

personnel provided additional documentation as listed below.

The Team also examined licensee activities in response to GL 88-14

(see -paragraph 3.h.). Documentation associated with design

verification of MSIVs, containment vacuum breakers, and containment

isolation dampers (valves) was also reviewed as listed below.

- __ _. - - - _ -

- - _ _ _ _ _ _ _

,

};y l

7, j

.

29

L

' Documentation Review i

i

The - Team held discussions with cognizant licensee personnel and

reviewed additional documentation associated with the above as

'follows:

-

Documentation associated with air sampling and station ' service

air compressor (SSAC) maintenance and reliability

Air Compressor Replacement Plan

-

System Engineering Concerns Regarding SSAC, dated

September:20, 1988 (Log: LR-BOP-016-0988)

Management Action Plan regarding SSAC, dat'ed

i September '21,1988 (Log: LR-MGR-006-0988)

Management approved reliability improvement action,

dated September 27, 1988 (Log: LR-MGR-009-0988)

-

Laboratory Analyses of eight air samples taken November 23,

1988, [(includes sample location, dew point (- c), particle

size (micron), oil content (ppm), carbon monoxides.-(ppm),

carbon dioxide (ppm)]

ANSI.. Standard ISA-S7.3,. Quality Standard for Instrument Air-

'

Unit 1 PM Procedure.52PM-PSI-001-IS

Unit 1 PM Procedure 51PM-P51-001-IS

Unit 2 PM Procedure 52PM-P51-001-2S

..

---

Documentation associated with ' Design Verification of MSIVs,

Containment Vacuum Breakers, and Containment Isolation Damper

(valves) ,

1

  • January 13, 15 t ,' Correspondence from G. A. Goode to

S. B.' Tipps (Lv _R-PES-016-0187) regarding testing for

Unit 2 - MSIV closure times .with and without air supply.-

(Note: MSIVs'B21-F022A-D and F028A-D met the 3 to 5 second

closing time.both with and without air supply)

~

  • ~ June 11, 1987 correspondence from T. Powers to J. Kane

(Log: 'LR-ENG-011-0687) regarding relief from ASME

Section XI, Subsection IWV-3415 requirements to allow

continued testing of MSIVs without isolation of the gas

supply to the accumulators during normal surveillance

testing.

Follow on correspondence'of August 3, 1987, August 18, 1987

and September 4, 1987 regarding MSIV fail-safe testing

requirements.

I * March 2, 1989 correspondence from BPC to GPC regarding

design verification of drywell/ torus vacuum breakers

(T48-F323A-L); torus / reactor building vacuum breakers

(T48-F328 A & B; and Unit 1, 18 inch purge valves

(T48-F318, F320 and F326).

- - - _ _ _ _ _ _ _ _ _

___

.

.' O

30

,

March 9, 1989 correspondence from K. W. McCracken to

L..T. Gucwa regarding design verification of containment

isolation / vacuum relief valves T48-F310 and F311 and

T48-F328'A & B.

April 19, 1988 correspondence from GPC to NRC regarding LER

88-004-01 (LLRT failure of Unit 2 valves including T48-F310

and T48-F311).

Conclusion

The Team concluded that the licensee had completed comprehensive

activites in response to GL 88-14. However, the Team noted a

continuing concern regarding design verification of valves T48-F310

and F311. Discussion provided in paragraph 3.h.

J. Preventive Maintenance (PM) Program

Observations

The Team reviewed procedures, held discussions with maintenance

engineering personnel and observed activities associated with  ;

predictive / preventive maintenance. '

The Team also- examined historic documentation demonstrating use of

predictive maintenance to prevent incipient failure on large rotating

equipment.

Findings

The licensee's predictive maintenance program includes vibration

analysis, lube oil analysis, equipment performance analysis,

infrared analysis, and analysis of maintenance history. The

program is run by maintenance engineers and controlled by procedure ,

50AC-MNT-007-05. Other procedures involved include 53PM-MON-002-0S  !

and 53PM-MON-001-05.

An NRC concern was identified regarding need for a programmatic link

between preventive maintenance and ASME,Section XI requirements.

Details are i ~luded in pargraph 3.f.

Conclusion

The Team consensus was that the Preventive Maintenance Program was a

programmatic strength.

l

l

l

l

_ . _ _ _ _ _ _ _ _ _ . _ _ _ _

_ _- - _ _ .

&

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31

.

k. Quality Control (QC) Program

Observations

The' Team completed an examination of the QC program; interviews with

-QC management and several QC inspectors; and reinspection of several

welds 'recently accepted by .the QC inspector involved with the weld

~

patch- problem .on the Unit 2 reactor building roof drain -(see -

paragraph 3.e. above). Further details on examination of the. QC

program' are listed below. (Note: The Team was aware of details

associated with previously identified NRC~ violation 321,366/88-31-01

of 'a related nature and responsive licensee. correction actions.

However,Lthose corrective actions were not examined in detail since -

' full compliance is not anticipated before September 1989).

Findings

The Plant Hatch QC Program provides-the following:

-

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> shift coverage for I&C, . Electrical, and . Mechanical

-

Maintenance

-

Inspection of safety systems and selected Balance of Plant .

'

systems

-

NDE testing and evaluation

-

Monitor of welding qualification and performance

-

Final MWO elosecut reviews

-

Material Receipt Inspection

The following controlling procedures were reviewed and found to be

'

adequate:

GEN-12750

40AC-QCX-001-0S

45QC-INS-004-0S

45QC-INS-005-0S

45QC-INS-006-05

45QC-INS-008-OS

45QC-QCX-002-0S

450C-QCX-009-05

45QC-PQL-001-05

45QC-QCX-001-OS

'

.c

The ANSI N45.2.6. and SNT-TC-1A certifications of all (24) QC

inspection personnel were reviewed and found to be current. All

inspectors are certified to visually inspect welding activities.

__ ___-_- __ - _ _ . -

_ ___ _

4 4 i

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, >

32~

a

'

Interviews were held with six QC ' personnel. Specific questions were

i posed; relative to acceptance criteria and other details of the

procedures: li sted 'above. All questions were adequately answered with

clear and. specific detail.

<  :

The following welds recently accepted by an inspector were re-

. examined and-verified as acceptable.

~

MWO No'. Weld No.

1-88-07300 FW001 4

2-89-0619- FW Nos. I through 8

Conclusion

' The Team consensus after examination of the above was that Quality

Control at Plant Hatch was a strength in both program and

implementation.

.1 . Engine'ering Support

Observations

1 The Team ' interacted with several systems engineering personnel

during . examination of potential repetitive failures- of critical

- components (see paragraphs 4.t .and 4.x below)';. IAS GL. 88-14 activi--

ties-(paragraph 3.h.); corrective actions associated with HCU bolting-

(paragraph 3.b.) and unique breathing air fittings (paragraph 3.c.).

The Team 'was favorably impressed with the . capability and enthusiasm

of the engineering personnel . involved and their strong cooperation

with the maintenance organization.

The Team completed additional inspections in two areas of engineering

support (duties of t systems engineers and DCR prioritization) by

review;of controlling procedures, discussions with. management and

- engineering personnel and review of documentation.

Findings  ;

The Team identified a lack of procedural definition regarding the

i. duties and responsibilities of systems engineers. Some definition is

provided by procedure '10AC-MGR-001-0S, Plant Organization Staff

Responsibilities and Authorities. However, this upper-tier procedure

does not provide specifics related to systems Engineers.

l

In some cases, the implementation of Design Change Requests (DCRs)

'

has not been timely. An example is DCR 80-440, "RCIC low speed

bypass 'line" which has been implemented on Unit 2 for several years

but is not yet implemented on Unit 1. Implementation was given a low

priority since it was considered to have little impact on reliable

^

1 - - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - - - _ _ - _ _ _ .

y  ;

-- -

,

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.l

...

L

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g 33

.

. plant. operation. Cognizant licensee personnel provided details on a

recently implemented DCR prioritization rationale, the downward trend

'

data'for open DCRs (22% reduction since March 1986),.and an informal ~

'

schedule of DCRs recommended for approval in 1990.

Conclusion-

The ' Team c'oncluded that additional specifics regarding systems

p

-

engineers duties and responsibilities should be added to the

procedures involved.

Th'e Team also ' concluded that' the presently implemented DCR

prioritization rationale and schedule were sufficient to resolved any

NRC concern.

The Team consensus was that technical rapport could be improved in

both program and implementation.

F m. Review of Licensee's Service Air System (Breathing Air System)

-

Requirements'

Licensee Technical Specification 6.11 states in part that

procedures for personnel radiation protection shall be prepared

consistent with the requirements of 10 CFR 20, and shall be

approved, maintained and adhered to for all operations involving

'

personnel radiation exposure.

10_ CFR 20, Apendix A, footnote (d), requires that' respirable air

shall be provided of the quality and quantity required in

accordance with NIOSH/MSHA certification (described. in

, 30 CFR Part 11) for atmosphere - supplying respirators.

30 CFR, Part 11, Subchapter b, subparts H and J require that

< , breathing air meet the applicable minimum grade requirements for

Type 1 gaseous air set forth in the compressed gas association

commodity specification for AIR, G-7.1 (Grade D or higher

quality).

Occupational Safety and Health Administration (OSHA) 1910.134,

" Respiration Protection" and NUREG 0041, " Manual of Respiratory

7.

Protection Against Airborne Radioactive Materials," include .

requirements to have air line couplings that are incompatible i

with outlets for other gas systems to prevent inadvertent

servicing of air line respirators with non-respirable gases or

oxygen.

,

e- .: a

.; 4 ; ' r

,. . _

, 1. -

L;

.,

, 34

f

"

ANSI Z-88.2-1969, Practices for Respiratory Protection,

.Section 5.3, Respirable Air and Oxygen for Self-Contained

'

Breathing Apparatus and Hose Type Respirators, also requires

air-line couplings to be incompatible with outlets for other gas

-sytems to prevent' inadvertent servicing of-air-line respirators

with nonrespirable gases or oxygen.

Unique Fittings

'

-

-Observations

The. team walked down the system from the air -intake to selected

systems outlets, and reviewed the following: historical back-

ground ilnformation for- the. system; operations. procedures .for

annunciwor response and abnormal operating' procedure; instru-

ment 'and service air maintenance; health physics procedures

~ relating to the supplied air respiratory protection program;

.

- and calibration records for the system's temperature monitors.

. Fin'ings

d

The licensee documented on Deficiency Card 2-87-659, October 6,

1987,.that quick disconnects on the Service Water-System outlets

were identical to those used on Service Air System outlets. The

root cause for the identified deficiency was "No gMdance .on

installation of quick disconnects." The ' licensee issued

guidance on the use of quick disconnects on December 11, 1987.

The guidance reported that quick disconnects were used on only-

the Demineralized Water System (P21), Service. Water System

.(P41), and the' Service Air System (p51). The guidance did not

address the. Instrument Air System (PS2).

The licensee issued another Deficiency Card 2-88-1452 on

March 16, 1988, identifying a Service Air System fitting on. a

Demineralized Water System outlet in Unit 2, High Pressure

Coolant- Injection ' (HPCI) ' room.' -The corrective actions taken *

referenced the Significant Occurrence Report (SOR) 2-87-659-185

that was written for the previously identified October 6,1987, .j

finding which'was closed in December 1987.

During tours of licensee's facilities on March 3, 1989, the

inspectors ' determined that identical fittings were on the

instrument air and service air lines. During the tours, the

team requested a health physics technician to accompany them.

When .the health physics technician was asked which system,

instrument air (P52) or service air (P51), should be utilized

to supply breathing air, the technician was unsure and reported

that he did not know. The service air lines (breathing air

lines) were not identified as service air-breathing air outlets

as recommended in the REA HT-0718 study in 1981.

= _ _ _ - - ._ _ N

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Conclusions

'

The team informed licensee personnel that failure to have

  • '

incompatible' fittings on the. Service Air. System (breathing air

system) was a violation of licensee Technical Specification 6.11

in.that the-licensee had failed to comply with the implementing.

references specified in licensee procedure 60AC-HPX-006-0S and

'that the. failure to implement- 60AC-HPX-006-0S occurred 1as a-

result of inadequate corrective actions for -deficiencies

identified by ~ the licensee in the HT-0718 study in 1981 and

two' Deficiency cards (2-87-659 in October 1987 and 2-88-1452

in ' March 1988). The inspectors stated that failure to take

u timely and adequate corrective' actions to prevent recurrence

was a violation of. the licensee's quality assurance program

Appendix B, Criterion XVI, Failure to Complete Adequate Correc-

tive Action 321,366/89-02-02.

'-

Failure to-Sample the Plant's Breathing A. System

'

Observations .

The team determined that licensee procedure 60AC-HPX-006-05

- required the licensee to provide Grade' D air or better as

prescribed by the Compressed Gas Association. The procedure

-also -requires that the respirable air be sampled monthly for

radioactivity. .The inspectors requested a review of the Grade D

and Radioisotopic Analyses made in the last 12 months. Licensee

procedure DI-RAD-03-1087N lists 'the locations and frequencies

for each sample. The licensee samples the respirable air

systems for Grade 0 air on a quarterly basis. The team

determined that the licensee had. completed the monthly isotopic

samples for radioactivity as required. However, the licensee

could not demonstrate that the Grade D sample on the air

compressor utilized to fill Self Contained Breathing Apparatus

(SCBA) had been made during the fourth quarter of 1988.

Conclusions

,

The inspectors informed licensee representatives that failure to

take a quarterly a1r sample and analyze it for Grade D air was a

violation of Technical Specification 6.11.

l

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Procedures for Sampling

Observations

The Team determined that the licensee's radiation protection

y procedures did not describe how the plant breathing air was

sampled and analyzed to versfy that the plant breathing air

lL systems meet the minimum requirements for Grade D air. When

licensee management was notified that there appeared to be a

_ ____

. _ _ . .__- _ -

ct -.

.

36

violation of licensee Tehenical Specifications, for failure

to have written procedures,.the inspectors were informed that a

site Quality Assurance (QA) Auditor had already identified the

procedure problem in an ongoing QA audit. The inspectors

interviewed the QA auditor and ' determined that the auditor had

begun a radiation protection program audit March 7, 1989 and had

discussed -the finding with health physics personnel. The

inspectors reviewed a Procedure / Request Development form that

had already been completed to address the deficiency. The Team

stated that a review of the licensee's corrective action.s

concerning the sampling and analyses of the plant's breathing

air system to meet Grade 0 requirements would be performed and

identified as Inspector Followup Item (IFI) 321,366/89-02-07,

Written Procedure for Sampling Breathing Air.

-

Breathing Air System Instrumentation

During the review of Service Air System High Temperature

instrumentation, the Team determined that the licensee was

verifying correct operability every five years plus or minus

five years. The inspectors discussed the calibration frequency

with licensee management and licensee representatives agreed to

increase the frequency to every 18 months.

n. Radiological Protection Program Interfaces

The Team reviewed the method and degree of interaction between the

radiation protection staff and other plant groups. In addition,

craft and operations personnel were interviewed relative to support

they received from the radiation protection staff and found that in

general, there appeared to be a good working relation between the

health physics group and other plant sections. The licensee had

established a shift coverage schedule, in which, all of the people

working rotating shifts did so together. Through interviews with

various shift personnel, the inspectors determined that most people

interviewed like the idea of working together routinely and thought

the schedule enabled the various work groups on a shift to work

together more as a team.

The Team determined that the licensee had a radiation specialist

assigned to the planning / controls section.

o. Control of Radioactive Material, Contamination, Surveys, and

Monitoring

Reviews of records and observations during plant tours revealed no

instances in which unsatisfactory controls were being exercised over

radioactive material, contamination, surveys or personnel monitoring.

The licensee had made improvements in controlling radioactive

materials and in reducing the total area contaminated.

_ _ _ - _ - _ . b

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37

p. Radiation-Protection Audits

e The Team discussed the audit 'and surveillance program related to

radiation protection and control of radioactive material with

licensee representatives and reviewed the following audits:

Quality Assurance Audit of Health Physics Program (88-HP-1)

L Quality Assurance Audit of Health Physics (88-HP-2)'

The audit findings identified program strengths and weaknesses.

Examples of the audit findings documenting program weaknesses

included but were not limited to:

Failure to perform adequate surveys

. Poor documentation of ALARA activities

. Inaccurate man-rem estimates

Inadequate guidance to require ALARA review of plant documents

The audits were .goed health physics appraisals, in-depth, and

appropriate in scope. The 11censee's audit program for radiation

protection activities is a program strength.

-q. As Low As Reasonably Achievable (ALARA)

10 CFR 20.1c states that persons engaged in activities under licenses

issued by the NRC should make every. reasonable effort to maintain

radiation exposures as low as reasonably achievable. The recommended

elements of an ALARA program are contained in Regulatory Guide 8.8,

Information Relevant to Ensuring that Occupational Radiation Exposure

at. Nuclear Power Stations will be ALARA, and Regulatory Guide 8.10,

Operating Philosophy for Maintaining Occupational Radiation Exposures

ALARA.

As documented above licensee radiation protection audits had

identified needs for improvement in tha ALARA area. Program ,

weaknesses identified included: l

Initial man-rem estimates for radiation work permits are ,

inaccurate. Errors in both the projected man-hour and dose

estimates have contributed to the problem.

Some aspects of ALARA Program are not well understood by plant

personnel.

At the time of inspection, most of the corrective action as a result

of licensee audits had not been implemented, however, the licensee

was in the process of strengthening its ALARA program. The licensee

was reviewing an ALARA training program to give plant workers

additional training that would enable the staff to better understand

methods to reduce exposures. The licensee was also requiring more

!

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- - - - - _ . _ - . . _ - _ . _ _

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38 1

,

involvement from section supervisors in setting ALARA goals and

guidelines were being developed to strengthen the Plant ALARA Review

Committee (PARC). Implementation of the proposed corrective actions

should strengthen the licensee's radiation protection program.

The licensee's 1988 person-rem per unit for Boiling Water Reactors

(BWRs) was 701 versus the 1988 national average of 511 person-rem per

unit. The licensee's three year average is 619 person-rem per

unit versus the national average of 551 person-rem per unit.

r. Maintenance Related Data

Observations

The Team examined the following data associated with maintenance

at Plant Hatch. Most of the data showed an improving trend in the

years up to 1987. In that year, record performance was achieved for

availability factor (over 80%), consecutive days on-line (143), ,

electrical generation (10,832 gigawatt-hours), forced outage rate l

(3.0%) and industrial. safety (10,880,000 man-hour without a lost-time

accident). In 1988, as shown in Table 1, most usta continued to

show acceptable performance and showed improvement over 1986 but in

some. areas performance was not as good as in 1987. The number of

reactor trips and ESF actuations in 1988 were above the industry

average, but within the acceptable range.

Table I, Maintenance Related Data

1988 Industry

Indicator, both units 1988 1987 1986 Average per unit

Availability Factor, % 7 81 - 52f 77

Forced Outage Rate, % 12.4 3.0 9. 3 11

Reactor Trips 10 8 11 2

ESF Actuations 6 5 4 2 ,

TS Violations 24 27' 43 i

SALP Rating, Maintenance 2 2 2

LERs .

38 27 77

NPRDS Failure Reports 693 460 173

Significant Occurrence

Reports 534 827 NA

Work Orders Backlog,12/31 1259 2400 3144

Radiation Exposure, Man-rem l

per unit 383 431 742 521 (1987)

Absenteeism, % 1.8 1.9 2.1

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Conclusion

The Team concluded that although some. ofL the historic data showed

poorer ' performance in 1988 than in 1987, the long-term trend is

improving and on balance the data indicate good performance.

s. -Root Cause Analysis-

The root cause analysis program at Hatch Nuclear Plant was evaluated

' with respect-to training, procedures, and implementation. . Interviews'-

were conducted with individuals who were involved'in tne development

of 'the program. and who are currently responsible for its

implementation. Specific areas inspected were training materials and

their application, procedures, MW0s (2-88-4850, 2-89-65, 2-88-704,

2-88-1810, 'and 2-88-1788), and significant equipment failures.

_

Additionally, one , manager who completed ~ the 40-hour root cause

analysis cour'se was interviewed and observed applying principles and

techniques covered during the. course.

Observations and Findings

During 1988, some managers and engineers received initial training to

familiarize them with concepts and methods used to conduct root cause

analyses.- The methods included MORT, event and' causal factors

analysis, fault tree analysis, change analysis, barrier analysis, and

Kepner Tregoe's . problem . analysis. The training consisted of an

eight-hour course on' root cause analysis. The course materials

included an instructor handbook (IT-IH-21100-00) and a student text

(IT-ST-21100-00).

Currently, a 40-hour course on root cause analysis is taught by EG&G

Intertech. This course was introduced December 1988. The course-

materials also include an instructor handbook and a student text

(IT-21300-01). The stated goal is to ensure that about 50

individuals (including engineers, supervisors, manager, general ~

l support personnel, security personnel, and mainten_ance personnel)

.

L

receive training on root cause analysis. The stated -expectation is

that :about. ten new individuals will recaive training on root cause

analysis each year. Each department nominates candidates for the

root cause analysis course.

l

Hatch Nuclear Plant has several procedures in place to address root

cause analysis. Procedure AG-MGR-27-0687N provides guidance for

personnel reviewing events necessitating root cause determination. -,

I The Team identified a weakness in this procedure concerning the i

lack of details on how to conduct a root cause analysis. Other

procedures relevant to root cause analysis include 10AC-MGR-004-05,

40AC-REG-002-05, and 10AC-MGR-012-OS. The first procedure assigns )

responsibility for root cause determination and provides guidance on

identifying significant deficiencies. The determination that a-

deficiency is significant necessitates a root cause analysis. The  ;

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- second procedure specifies significant events or conditions that

require reporting. The. third procedure ' provides specific guidance

for addressing significant or repetitive events (or conditions),

including the need for root cause determination.

Two approaches were used to assess the actual use of root cause

analysis in maintenance efforts at Hatch Nuclear Plant. In the

first approach, several pieces of equipment that had been previously

judged asi having'significant failures were the focal point.' These

significant equipment failures were investigated to determine if root

cause analyses were completed as required. The pieces of equipment

.were: 2E41-F006 (HPCI pump discharge valve), 2E51-F008 (RCIC Steam

Isolation. Valve), 2B31-R620 (master recirculation controller),

2B21-F013H . (safety relief valve), 2B21-F022B (air valve), and

2B21-F022C (air valve). For all of the equipment' failures except

one, it was .found that. root cause analyses had been completed and

were considered adequate. However, no root cause analysis was

conducted for valve 2E51-F003.

In the second approach, an individual was identified who had not only'

completed the 40-hour root cause analysis course, but also was

attempting to determine the cause of a failed pump. This individual

described and demonstrated principles and techniques taught in the

course- that were being applied to the failed pump problem. The

. observed process was considered a'dequate and seemed to reveal some

insights on the." weight"~that should be given to vibration, oil, and

wear particle analyses.

L0ne procedural weakness was noted regarding procedure

AG-MGR-27-0687N. The procedure lacks details on how to conduct a

root cause analysis. The Team further observed that an excessive

length of time was required to determine root cause of Feedwater Pump

leakage discussed in paragraph 4.x.

Conclusions

The root cause analysis program regarding - maintenance at Hatch

Nuclear Plant was adequately documented and seemed to. be well

implemented. LHowever, weaknesses were noted as discussed above.

Overall, the program was judged satisfactory,

t. Trending

The trending program at Hatch Nuclear Plant was evaluated regarding

established procedures and program implementation.

Observations and Findings

-

Hatch Nuclear Plant has two procedures in place to address trending

in the area of maintenance. The first procedure, DI-MNT-02-1085N, is

concerned with repetitive maintenance problems (for example, repeated

failure of the same piece of equipment) and is applicable to

maintenance engineering personnel.

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\. Trends were investigated for the main steam (B21) recirc (B31), CRD

filters (C11), HPCI (E41), and RCIC (E51), regarding equipment with

equal to (or greater than) five corrective work orders for the period

January 1,1988 to December 30, 1988. The equipment considered was

as follows: 2B21-F002A (4-way air valve), 2B21-F022B (2-way air

valve), 2B21-F022C (3-way air valve), 2B21-R614 (SRV temperature

h recorder), 2831-S001A and B (Recirc M-G Sets), 2C11-R003B (CRD

Filters), 1E41-FOC2 (HPCI Steam Supply Isolation Gate Valve),

IE41-C001 (HPCI Main and Booster Pump), 2E51-F007 (RCIC Steam Supply

Isolation Valve), 2E51-F045 (RCIC Steam Turbine Valve), and 1E51-F045

(RCIC Steam Turbine Valve).

The Team found that trend data for the equipment provided useful

information and except for the CRD Filters, the data indicated that

the subject equipment failed for a different reason each time. The

systems engineer pointed out that the problem with the high CRD

filter replacement rate during March 1988 on Unit 2 was found to be ,

related to start-up from a refueling outage. CRD takes suction from

the condensate system (carbon steel pipe). After a unit has been

shutdown two to three months, corrosion builds up in the condensate

system causing CRD filters to need replacing more of ten after an

1 outage.

The second procedure, DI-REG-08-1285N, describes the trending program

for deficiency cards (DCs), significant occurrence reports (SORS), -

and licensee event reports (LERs). The trend report for DCs and SORS

-

covering the period January 1, 1988 to December 31, 1988 was

examined. The equipment included the following: IC11-R018 (CRD

temperature recorder), IN21-C007 (condensate demineralized pump),

2W24-C021 (cooling tower fan), and 2N21-C002A (condensate booster

pump). It was found that the trend report was both adequate and ,

comprehensive, including a detailed breakdown of the type of

deficiency (e.g. , personnel related).

Although not explicitly covered by procedures DI-MNT-02-1085N and -

DI-REG-08-1285N, trending of NPRDS equipment failures were also

investigated. The NPRDS equipment failure analysis report for the

period January 1987 to June 1988 was examined. In addition to review

of the NPRDS report, a summary description was reviewed of all MWDs

for all systems with NPRDS component failure from Jar.uary 1,1988, to

December 30, 1988. The failed equipment included the following:

CRD-N26-23 (control rod), B31-K634A (controller), C11-R601 (pressure

indicator), C32-R607 (flow recorder), C32-K6008 (amplifier),

B31-N014D (transmitter), E11-C001A (pump), and B21-F010A (valve).

The subject trend report was considered a definite strength to the

overall Hatch Nuclear Plant trending program because it not only

provided useful data on specific equipment that had failed, but also

provided comparisons with the industry average.

.

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. Trends were~. investigated for the main steam (B21). recirc (B31), CRD

filters (C11)', HPCI (E41), and RCIC (E51), regarding equipment with

' equal to (or greater than)'five corrective work orders for the period

' January 1,1988 to. December 30, 1988. The equipment. considered 'was

as - .follows: 2B21-F002A '(4-way air valve); 2B21-F0228 (2-way air

"

valve) 2B21-F022C (3-way . air valve), 2B21-R614 (SRV temperature

recorder), 2B31-S001A and B (Recirc M-G . Sets), 2C11-R003B (CRD

Filters), 1E41-FOC2 (HPCI- Steam- Supply Isolation Gate. Valve),

IE41-C001f (HPCI Main and Booster Pump),. 2E51-F007 (RCIC Steam Supply

L

'

Isolation Valve), 2E51-F045 (RCIC Steam Turbine Valve), and IE51-F045

(RCIC Steam Turbine Valve).

The Team found . that trend data for the equipment provided useful

information and except.for the CRD Filters, the data indicated that

the . subject equipment _ failed for a different reason each time. The

systems engineer pointed out that the problem with the high CRD

-filter replacement rate during March 1988 on Unit 2 was found to be

related to start _up from a refueling outage. CRD takes suction from

~

the condensate system (carbon steel pipe). After a unit has been

shutdown two to. three months, corrosion builds up in the condensate

"

system causing CRD . filters to need replacing more often after an

outage.

The second procedure, DI-REG-08-1285N, describes the trending program

for deficiency cards (DCs), significant occurrence reports. (SORS),

and licensee event reports (LERs). The trend report for DCs and SORS

' covering the. period Janusey 1, 1988 to December. 31, 1988 was

examined. The equipment included the following: IC11-R018 (CRD

temperature recorder), IN21-C007 (condensate demineralized pump),

2W24-C021 (cooling tower fan), and 2N21-C002A (condensate booster

. pump). It was found that the trend report was both adequate and

comprehensive,- including - a detailed . breakdown of the type of.

deficiency (e.g. , personnel related).

Although not expl.icitly covered by procedures DI-MNT-02-1085N and

DI-REG-08-1285N, trending of NPRDS equipment failures were also

investigated. 'The NPRDS equipment failure analysis report for the-

period January 1987 to June 1988 was examined. In addition to review

of the NPRDS report, a summary description was reviewed of all MW0s

for all systems with NpRDS component failure-from January 1, 1988, to

December 30, 1988. The failed equipment included the following:

CRD-N26-23 (control rod), 831-K634A (controller), C11-R601 (pressure

indicator), C32-R607 (flow recorder), C32-K6008 (amplifier),

B31-N014D (transmitter), E11-C001A (pump), and B21-F010A (valve).

The subject trend report was considered a definite strength to the

overall Hatch Nuclear Plant trending program because it not only

provided useful data on specific equipment that had failed, but also

provided comparisons with the industry average.

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'

Interviews with maintenance management revealed that functional (or

post maintenance) test data'. are . trended to identify any adverse

trends. The team pointed out to the licensee that . trending NPRDS

data = with L respect. to failed components that can be attributed to

personnel error during previous maintenance is another trend that is-

recommended. This trend 'is readily available and could serve to

augment functional test trends.

Conclusions

The Hatch trending program in the area of maintenance was

satisfactorily documented through procedures and appeared to be well

implemented. The overall program was judged " good." This judgment

-was based on adequate. procedures that were in place and appropriate

implementation of the program. One recommendation for enhancing the

trending . program was noted. The recommendation concerned trending

NPRDS data regarding failed components that can be ' attributed to

previous maintenance. The benefits of such a trend would be

L two-fold: to augment trend data on functional tests and to identify

b

any adverse trends in this area.

u. Spare Parts

During the inspection, two MW0s were identified that required spare

parts: for final resolution. .The fi rst MWO, F.-89-00536, concerned

obtaining a motor' for the MSIV leakage control system. The second

MWO,. 1-88-8411, involved' obtaining a backup battery for the

programmable. controller in the demineralized building.

Observations and Findings

The resolution of the spare part issue for the MSIV system was

evaluated .by monitoring morning management sessions and interviewing

.the maintenance manager concerning this issue. There was some

difficulty in obtaining a spare motor because the manufacturer is no

longer in business. During the week of March 6, the motor arrived at

the plant and was installed, returning the MSIV system to operability

and thereby resolving a LCO. Currently, the motor that failed is

being refurbished and will-serve as a spare. The maintenance manager

indicated that parts that are no longer manufactured are a problem

'for Hatch Nuclear Plant and the industry at large. He also noted

that' the corporate office is supportive in resolving issues of this

kind.

The second-MWO, 1-88-8411, concerned obtaining a backup battery for

the programmable controller in the demineralized building. The

technician who replaced the battery indicated that the subject

battery was ordered and promptly received.

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Conclusions

i

The resolutions of the above described spare ' part issues were

considered good based on the continuous attention given by plant and i

corporate management to obtain the spare motor and the prompt

acquisition of the backup battery. i

v Document Control System for Maintenance I

The document control system for maintenance utilized at Hatch' Nuclear ,

Plant was evaluated with respect to these criteria: established,- 1

proceduralized, maintained, traceable, and updcted. .;

Observations and Findings

The Nuclear Plant . Management Information System' (NPMIS) has been

established, maintained, and is continuously updated, providing ' a

computer-based control system for processing MW0s. Procedure

DI-0AP-10-0588N provides guidance _for processing MW0s. Specific MW0s j

that were examined (that is, from initiation to closeout) through the 1

. NPMIS included the following: 1-88-01297 (failed SRV temperature

recorder), 2-87-03973 (replaced ASCO solenoid valve), 2-88-02235

(valve failed to close), and 2-88-02240 (valve air leak). It was

- found that MWO history and status are easily traceable through the

NPMIS. Since. the plant does not employ .a " trouble tag system",

checks were made to ensure' that the NPMIS included MW0s for failed

equipment that was observed during plant walkdowns. .With some

exceptions, it was confirmed that the NPMIS did ' include the subject

MW0s. Numerous NPMIS computer terminals were located throughout the

-plant in areas that seemed convenient for management, system

engineers, mair,tenance engineers, and support personnel.

Conclusion

The NPMIS was an effective system for not only documenting the

history and status of maintenance on equipment but also for trending

failed equipment. Based on the above findings and observations, the

system was judged " Good".

w. Control Room Annunciator Alarms

Control room annunciator alarms were evaluated for both Units 1 and 2

regarding the number of annunciators that are continuously lighted

and whether annunciators that should be cleared are being addressed

by the maintenance program.

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,

-0bservaticas and Findings

The control room was inspected on two different occasions. During

the inspections, it - was noted that only a few annur.ciators were

continuously lighted. Of these annunciators, the SAFETY / BLOWDOWN

VALVE LEAKING-annunciator, was investigated to determine how it. was

, being resolved. It was determined that the annunciator was in alarm

. resulting from 'a problem in the drywell. The problem was c.cheduled

to be, fixed during the ,iext forced outage. During the daily' morning

management -meetings, the number and causes of lighted annunciators

were. discussed. On ' February 28, 1989, the following annunciators

were reported: 1H11-P651, COOLING , TOWER OR~ DEEP WELL PUMP BKR

TRIPPED (several cooling tower fans tripped locally); 1H11-P700, WGT l

BLDG CHILLER B TROUBLE (blown gasket); IN62-P600, ABSORBER VESSEL

. TEMP HIGH (MWO 1-89-912); 2H11-P657 and 2H11-P654, TORUS WATER HI/ LOW l

LEVEL (due to venting with low level present); and 2H11-P700,  ;

REAC/RADW' BLDG COOLING TOWER BASIN HIGH LEVEL (operations l

investigating and deficiency card written).

{

Conclusion

Based Lon the 'above findings and observations, the number of

continuously ~ lighted annunicators were judged to be few and the l

subject annunciators appeared to be adequately addressed.  ;

i

x. . Condensate and Feedwater System (N21)  !

Obs'ervations

The. Team inspected ~ maintenance activities on the N21 system. The .

'

inspection included examination of a Summary List of 75 MW0s related. l

to repetitive corrective maintenace and 75 MW0s related to NPRDS I

equipment failures. Each of these - MW0s was discussed with the i

cognizant system engineer and a walkdown of the system, with emphasis i

on the' items requiring repeated corrective maintenance, was conducted j

with the system engineer. '

Findings, ,

!

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- Repetitive Tracking System

The system for tracking repetitive equipment failures was

developed by the Maintenance Engineering Supervisor to provide

guidance for prioritizing corrective maintenance work. The

tracking system uses the NPMIS te, sort those Master Parts List

(MPL) items for which five or more MW0s for corrective

maintenance (CM) were written in 1988. This list provided a

method for team inspectors to focus inspection effort on those

MPLs with potential maintenance problems.

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For the Ccndensate and Feedwater System (N23), the following

MPL's were listed:

MPL Number Number of MW0s Description

IN21 B006a 5 5th Stage Extraction Heater A

IN21.B006B 5 5th Stage Extraction Heater B

IN21 C005A 11 Reactor Feedwater Pump and

Turbine A

IN21 C005B 10 Reactor.Feedwater Pump and

, Turbine B

IN21 P001- 17 Condensate Polisher Control

Panel

2N21'C002A 7 Condensate Booster Pump

2N21 C005A 9 Reactor Feedwater Pump and

Turbine A

'2N21 C0058- 11 Reactor Feedwater Pump and

Turbine B

-

Feedwater Pump Leaks

During the system walkdown, sizable saal leaks wera noted on the

shafts of each of the four feedwater pumps. A. tray to catch

this water was installed below each pump with.a drain. tube to a

50 gallon . drum. A drain tube lead from the bottom of the drum

to the floor. drain. Drain tubes also lead from the seal weep

holes to the 50 gallon drum. Plastic funnels were installed to

catch leak water 'from flanges and fittings on pipes in the

feedwater pump rooms. Drain tubes from the plastic funnels lead

to floor drains.

The' seal leakage observed was not considered to be normal and a

consultant from the pump vendor (Byron-Jackson) was called in on

March 6, 1989, to analyze the problem. According to the vendor

representative the root cause of the problem was that the normal

seal water flow was routed back to the condenser hot well rather

than to the booster pump intake. The low pressure in the

hot well caused the seal water to flash into vapor, thereby

restricting liquid flow to the hot well. The vendor representa-

tive suggested that the excessive leakage could be decreased by

rerouting the seal water flow to the booster pump intake or by

increasing the size of the piping. Until these design changes

are made, the leakage may be decreased by careful adjustment of

the seal water controls.

-

Rebuild of Condensate Pump

The Team examined documentation associated with the repair of

Unit 2 condensate pump N21-C001B. The complete work order

oackages for the first and second rebuilds of the pump were

obtained. MWO 2-88-1906 was written on April 5, 1988, when high

L u _ ____ -- --__

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46

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vibration was noted and the pump shaft appeared to be out of

alignment. Worn bearings and wear rings on the pump shaft

were found. The pump shaft and bearings were replaced.

MWO 2-88-3177 was written on July 6, 1988, when the pump failed

again shortly after startup following the first rebuild. The

lengthy MWO packages (55 pages for the second rebaild) did not

provide a clear picture of the root cause of either failure nor

of the actual repair operations.

A further explanation was provided by the maintenance manager.

After the first failure of the pump, cracks were noted in the

section of the pump casing (52" in ' diameter and 104" long)

containing the suction and discharge flanges. This casing

section was rebuilt. The root cause of the second failure was

that the flanges for attaching the new casing section to the

motor and to the pump casing section were not properly aligned,

because instruments were not available in the maintenance shop

for accurately aligning such large-sized sections of casing.

When it was deduced by the maintenance manager that alignment I

was the problem, special equipment was designed and built for

checking the alignment of the casing flanges. The flanges were

found to be out of line. The alignment was corrected and the

pump was reassembled. It has been running without problems

since September 1988. The Team observed this pump in operation

with a maintenance engineer familiar with checking vibration and

alignment. Wire leads from the pump shaft bearing area for

attachment to a vibration measuring instrument were visible.

The pump appeared to be running smoothly.

A representative of the pump vendor was present during the first

and second rebuilds of the pump. The representative did not

recognize the alignment problem with the first rebuiid and was

surprised by the subsequent failure.

Conclusions

-

Repetitive Tracking System

The Team consensus was that the NPMIS and repetitive tracking

system is a programmatic strength (also see paragraph 4.v

above).

-

Feedwater Pump Leaks

The temporary provisions to route the seal water leaks, and

other pump room leaks, to the floor drains are unsightly and

constitute poor housekeeping practice, but do not represent

significant contamination or safety hazards. The pump room

leaks, except the seal leaks, will be corrected at the next

outage. Hatch management is moving toward a long-term solution

__

_- -_ _

,

,

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.1

, 4

,

47'

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of the seal leak problems-along the lines suggested by the pump.

vendor representative. No = definite . schedule' for corrective

action has.yet been established. Ideally, the licensee should

have discovered the' root.cause of. the leakage and corrc:ted it'

sooner, but the delay has not interfered with system operation .

nor resulted in a' safety hazard.

'

Rebuild of Condensate Pump

The Team consensus was -:that the . condensate ~~ pump rebuild ~

.

indicated la strong plant maintenance organization able to

"

~ analyze and. correct a' subtle and complex maintenance problem.

However, the . poor- description. of the -root cause analysis and

L corrective actions in the two " rebuild" MW0s is considered to

indicate. a weakness of the licensee's record keeping in the

maintenance area.

. S '. Evaluation of Maintenance Program

Based on the inspection ' details and.. inspection results of paragraphs 3

and 4 above, the. team' evaluated .the Maintenanc_e Program using the

guidance of NRC TI 2515/97. The below paragraphs detail the evaluation.

'a. Overall. Plant Performance Related to Maintenance - Direct' Measures

Rating - Good

Findings /0bservatio'ns

Review of Direct measures revealed an improving trend of most

performance indicators up to 1987. In that year, record erformance

was. achieved for availability - factor (over 80*0. consecut:vt v ..y s

v on-line (143), electrical generation (10,832 cigWatt-hours), forced

outage rate ( 3. 0*4) and industrial safety (10,880,000 man-hours

.without a lost-time accident).

Although some of the historic data showed poorer performance in 1988'

,

than 'in _1987, the long-term trend is improving and on balance the

data indicate good performance.

The general plant walkdowns found the plant to be in relatively good

material condition and L the team consensus was that the general

. quality :of housekeeping in the plant was good. As noted in

paragraph 4.a., some deficiencies were identified. On bal&nce, the

team 'does not regard the noted deficiencies as significant and

considers the overall condition of plant and housekeeping to be good.

--_ - _ _ __-

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Conclusion

,

L' .The overall plant performance related to maintenance as indicated by

l

historic data and observed in plant'walkdown inspections is good.

\ b. Ma'nagement Support of Maintenance

Rating -

7

Program: Satisfactory

Implementation: Satisfactory

Scope

. Management, support of maintenance was examined by reviewing and

, evaluating- (1) management- commitment to and involvement in

maintenance;. (2) management f organization and administration; and

(3) ' technical support provided to the maintenance organization.

f (1). Management Commitment and Involve 9ent

n Rating-

Program: Good

Implementation: Good

Findings / Observations

In general, the team found, during the inspections detailed in

paragraph 4. above, that the licensee had a good program 'for

application of industry intiatives. The inspection-revealed the

following examples of good application of industry initiatives:

few control room annunciator alarms that are continuously

lighted; the- NPRDS is used for trending' and equipment failure

history; motor operated valve motor' shaft keys are being

replaced; backseating of valves is no longer done on a routine

basis (IN; 87-40); policy has been established to remove PCBs

from 4160-600V . transformers by retrofilling with non-PCB

insulation; checks for silicon bronze carriage bolts (IN 88-11)

in - equipment identified in the IN as well as other related

equipment (e.g., SKV switchgear).

The following weaknesses were identified relative to application

of industry initiatives: Information Notice 88-42, " Circuit'

Breaker Failures Due to Loose Charging Spring Mounting Bolts,

was.not incorporated into the preventive maintenance-procedure;

the duties and responsibilities of the " systems engineer" is not

well defined; and the vendor's recommendation regarding PM on

- - _ _ _ _ _ _ _ _ - - _ _

_ _ _ _ _ ____-_

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4KV switchgear was not .followed. ' The sytems engineer related

and switchgear-related weaknesses are discussed .further in

'

.naragraphs 4.l. and 3.a., respectively. 1

Investigation of. management vigor and example indicated the.

'

following: management performs systematic area inspections;-

various morning meetings conducted by upper management serve to

n identify important maintenancelissues, follcwed by meetings with-

departmental managers and foremen to resolve the identified

'

. issues; training is generally excellent except that PM training:

on_4KV switchgear is not yet complete; and feedwater flow system

maintenance -replacing GEMAC transmitters . indicate that plant -

L aging is being addressed. The latter . finding is discussed  ;

.further in paragraph 4.c.

.

}

Conclusion

Based, on management's commitment to the application of industry

. initiatives, as . noted ..above, and observation of man'agement's

clear and active involvement in the maintenance program both the

program and its implementation were rated " good." Weaknesses in

'this inspection area were noted regarding .IN 88-42, the vendor  :

recommendation on SKV switchgear, 'and incomplete PM training on

SKV'switchgear.  ;

(2) Management Organization and Administration

.i

Rating -

.

Program: Not Evaluated

!

~ Implementation: Good  ;

1 a

!

Findings / Observation 1

Maintenance staffing level seemed adequate,' including the amount I

of technical- support provided; no adverse indicators of material

problems were found in the MWO review; various types of mainte-

nance activities (e.g., ISI, surveillance testing, diagnostic,

preventive, predictive, and corrective) have been implemented i

in the maintenance process; walkdown inspections are completed  ;

by management (e.g., Maintenance Superintendent and Plant l

Engineering Supervisor);' daily feedback is provided through j

morning meetings and staff meetings regarding maintenance issues ]

where improvement-is needed; numerous performance measurements i

(e.g., backlogs, reworks, and deferrals) are well identified 1

'

and implemented; and plant management appeared to be involved

in and aware of decisions regarding upgrades, plant agir.g, and l

work deferment.

i

l'

_ _ _ _-__ _ _ _ _ _ _ _ _ _ _ _ ._

_-_

_ _ _ _ _ _ _ , _ _

- - _ ._ _ . - -

,.

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[. .

50

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(

. The- computer-based maintenance work order system was well

4 implemented and judged to be a definite strength to the. overall

maintenance program. ' Specific- strengths included (a) the

capabilitymto trend repetitive equipment failures (b) the MPL

numbering system, and (c) the availability of numerous CRT

termi nal s_. This system is discussed in further detail in

paragraph 4.v.

Relative to definition of maintenance requirements, a weakness

was identified in that the . licensee was not following the vendor

technical manual regarding PM on 4KV switchgear (see paragraph-

3.a). . Additional . weaknesses were identified relative .to root

.cause analyses. The first concerned a feedwater. pump seal leak

and- the length of time required to- determine the cause of the

!

excessive' leakage (See paragraph 4.x.). The second involved a

MOV ; motor failure where root cause was not anlayzed (MWO

2-88-02612). Root cause analysis is discussed further in

paragraph 4.s.

Conclusion-

Based on the above inspection findings, management organization

and administration was' rated " Good." Some needed improvements

-

in this inspection area were noted with respect to following

,

"'

. vendor technical manuals and conducting root cause analyses.

The program for this inspection area. was not reviewed in

. sufficient detail and, therefore,'it was rated "Not Evaluated."

(3) Technical Supp' ort

Rating -

Program: . Satisfactory

Implementation: Satisfactory

q

Firidings/0 observations i

Formal and informal communication between technical support 'and

other organizations were not examined in detail. However,

indications are that communication is strong. Maintenance

information is communicated in the daily 7:30 AM meeting to 1

discuss the five principal operations to be performed that day. 1

A . weekly meeting projects maintenance work to be done in the )

next two weeks. These meetings are attended by about 30  :

maintenance, support and supervisory personnel including the

plant manager.

Good communication between maintensoce craftsmen, their foreman

and other support personnel was observed during the performance

of several maintenance jobs,

i

- _ _ _ _ _ _ _ - - - _ _

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Examination l of. Engineering Support . revealed that: the - major

engineering support for maintenance at Hatch .comes from the

4 maintenance engineering group reporting to the maintenance

-

manager ' for engineering support. The maintenance engineering

.

' '

group resolves routine engineering problems related to

maintenance, monitors preventive and predictive maintenance, and

</ performs trending analyses on repetitive ~ failures and on the

ratio :of preventive. to total maintenance. Less routine-

maintenance problems are sent to the system engineers for

analysis and resolution.

L

\ Maintenance engineers appear to be competent and enthusiastic in

completing their assigned. tasks. The Team also interacted with

system engineers during this inspection. It was clear that the

system engineers were thoroughly familiar with the maintenance

problems of their assigned systems and took active part in their

resolution. However, a need for better definition of systems

engineers duties and responsibilities was identified.

Examination of: QC revealed that: criteria for inspection and

aucit are Established and implemented, inspection / verification

is scheduled and accomplished, and corrective actions are taken

as necessary. The Team noted that plant QC inspectors were

present. during the performance of maintenance. and that MW0s

specified holdpoints for QC checks. In one instance, the QC

inspector miscalled the acceptability of a faulty weld patch

operation (see pragraphs 3.e. and 4.k.). Overall, this element

is rated good in program and implementation.

Radiological controls were examined and found satisfactory with

exception of procedures .related to breathing air sampling (see

paragraphs 3.d. and 4.m.)

Examination of maintenance safety revealed that: some

electrical procedures lacked sufficient safety instructions,

although the electricians actually observed good safety

precautions in performing their work. However, . a violation

involving breathing air was noted by the Team. Safety codes

repire the use of unique fittings on breathing air lines to

preclude non-respirable gas. The same type of fitting was

observed on instrument air lines subject to nitrogen use.

No deficiencies were observed involving hazardous materials,

fire protection or confined spaces.

The integration of regulatory documents was examined and two

related violations noted. First, loose bolts were observed on

CRD Hydraulic Control Units (related to regulatory documents

IN 87-56 and violation 321/86-20-02) (sce paragraph 3.b.).

Second, an inadequate procedure for insuring incorporation of

_ _ _ - _ _

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f

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r ' vendor information into. procedures was identified (related to

regulatory document Generic Letter 83-28) (see paragraph 3.a).

Conclusion

Based on the inspections and findings summarized above, the-

consensus of-the team for the Technical Support element is that

both the program and its implementa'. ion are satisfactory.

c. Maintenance Implementation

! ' Rating -

Program: Good

l Implementation: Good

Scope

The purpose of .this part ' of the . inspection was to determine the

,

quality. of the ' established controls and, more importantly, the

implementation of these~ controls. The controls established in four

areas were evaluated. These areas are (1)' Work Control, (2) Plant

Maintenance Organization, .(3) Maintenance Facilities Equipment and

-Materials Controls, and (4) Personnel Control. The effectiveness was

determined.through a review of completed work orders, procedures, and

other documentation associated with maintenance and training of

. maintenance personnel; physical observation of work in progress and

tools in stock; and discussions with all levels of personnel.

(1) ! Work Control

Rating -

Program: Good

Implementation: Good

Findings /0 observations

Review of work in progress in the field indicated that

appropriate authorizations were received; proper documentation

was issued; foremen observe the work in progress; personnel

appear competent- and properly qualified; procedures were

followed; and no major problems were identified during the

observation of work. However, a concern was identified

regarding lack of precise definition / details on MW0s 2-88-4862,

2-88-1906 and 2-88-3177.

.- - _ - - - _ _ _ _ - _ - - -

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This 'was aggravated by an . error regarding the type. of post-

+ maintenance testing required after revision of MW01-89-00722

on Estation service battery ' charge 10. These weaknesses are

further discussed in. paragraphs 4.e.(7), 4.x. and 4.e.(1).,

9 respectively.

e

I, ' Examination ~of the work order control system revealed a' program

in- place to . identify discrepancies - the Nuclear plant

Management Information System -(NPMIS). NPMIS is routinely

g updated by planner / schedulers during the MWO review and approval

cycle (see procedures DI-0AP-10-0588N and. 50AC-MNT-001-OS) and

'is an excellent tool for the analysis / trending / history of

maintenance activities. The NPMIS is further . discussed in

paragraph 4.v.

Review of equipment and maintenance history. records indicated:

maintenance - history is easily retrievable through NPMIS; work'

history is updated at the completica (closure) of the MWO, the

Master Parts List'(MPL)/ Equipment' Locator Index (ELI) is being

. updated and expanded; repair. time is tracked for each MWO; root

cause analysis could .be improved .(see paragraph 4.s); NPRDS is

used but not to the extent to yield maximum benefit - (see

paragraph 4.t.) and the MWO data form includes an input- for

NPRDS. .On. balance, the Team considered the equipment and

maintenance history records program to be a strength.

An ins'pection of the conduct of job planning revealed: the

safaty significance of an item to be repaired / replaced is the

first consideration; LCO items are' worked until completion;

drawings / technical manuals / procedures are included on the MWO;

the planner coordinates work between disciplines on a MWO; spare

parts are identified on - the MWO, when possible; personnel

requirements / qualifications are well documented and are known

or easily available to the foreman assigning work; and program /

procedures promote coordination and teamwork with ' system

Engineering / Technical Support.

Examination of the licensee's work prioritization controls

revealed that safety significance and the effect on safety by

BOP is considered and no safety significant items were found

that were not included in the work schedule.

By review of the licensee's maintenance work scheduling, it was

determined that: the maintenance backlog is being trended and

this- backlog appears to be decreasing; personnel are organized

in teams and rotated between day and night shifts so that new

-personnel are evenly dispersed and compensation occurs for work

loads in the various areas; the planning and control group of

the outage and planning department determines the schedule for

maintenance (except emergency maintenance) to reduce conflicts

and the NPMIS provides for MWO tracking.

= _

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54

The licenseei s establishment of backlog controls was reviewed

s and it was determined that PM maintenance activities are

sometimes deferred based on " sufficient written technical basis

~ for the deferral "(see procedure 50AC-MNT-007-05). The Team

.

examined several of these deferred PMs and- noted that the

majority were assocated with complex and expensive PMs on

. rotating equipment (examples: RHR pump motors IA and ID and

-. makeup wate pump 1A) which were authorized after an engineering

analysis of other predictive maintenance. data (i.e. vibration,

lubrication,etc.). The Team _ concluded that deferred PM's were

.

not adversely affecting backlog controls. Backlog controls

f' appear - to adequately acknowledge work significance, ' BOP

concerns, estimated manhours, and contribution to ALARA.

Backlogs are measured and trended, considered to be below

' '

industry average, - and receive adequate attention from plant

management. The Team consensus was that back'og' controls were a

j. programmatic strength.

An examination of maintenance procedures . revealed that

procedures 'are generally well conceived, thorough, technically

adequate and easy to use. However, some procedural problems

1 were noted regarding adequate tie with Section XI requirements, .

conduct of root cause analysis, and 4160 Volt switchgear pMs.

These are further discussed in paragraphs 3.f. , 4.s. , and 3.a. ,

respectively.

The Team consensus regarding maintenance procedures was that

some improvements were necessary in this area.

An examination of post-maintenance testing revealed that

post-maintenance testing criteria- have been established,

documented and implemented. However, the Functional Tests

recommended . by procedure 951T-0TM-001-0S are directed toward

component post-maintenance testing and do not necessarily assure

operational readiness. The operations supervisor on shift

(OSOS) and shift supervisor (SS) review the MWO-and may accept

the FT as a satisfactory method of proving operability or may

require additional operability testing. The Team did not

consider the- above aspects of the post-maintenance testing

program to be of concern. However, the Team observed at least

one instance of incorrect functional testing after revision of

MWO 1-89-00-00722 (see paragraph 4.e.(1)) and identified the

need for programmatic assurance in procedure 50AC-MNT-001-0S

that post-maintenance tests as required by ASME,Section XI, are

correctly imposed. These items are further discussed in

paragraphs 4.e.(1) and 3.f, respectively. The Team consensus

regarding post-maintenance testing was that some improvements

were necessary in this area.

f

. - - . - . - _ . - . . _ - - . - - . . - - - _. . _ , - - -

_ _

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"

The Team reviewed a sample of completed work control documenta-

-J

tion as. listed in Appendix B. This examination . established -

that a document review methodology is~ implemented and performed- i

in . a. timely manner. No' major anomolies/ discrepancies were

identified.

Conclusion

l'

Based on the inspection above, the consensus of the team, for

this element was'that the program and implementation were rated

good.

"(2) , Plant Maintenance Organization

Rating -

Program: Good

,

Implementation: Good

Findings / Observations

The review of the control' of. - Mechanical , Electrical, and

Instrumentation ~and ^ Control maintenance activities revealed

that a methodology has been established and implemented . to

identify the need for . maintenance and control. rework, vendor

technical manuals, procedures, materials, tools and personnel.

Items- such as assurance of system integrity, monitoring, use of

qualified parts, and personnel accountability are included. The-

Team noted general ' positive conditions such .as: small work

backlogs; PMs according to schedule; improving trends-on rework

. items; use of appropriate procedures; acceptable to good

equipment condition; and enthusiastic and well trained

personnel. Additional specific areas examined are as'follows:

-

Mechanical - work histories for several major - components

-(e.g. Unit 2 A and- B Recire M-G Sets, Unit 1 HPCI Main Pump

and Steam Supply Isolation Gate Valve, Units 1 and 2 RCIC

Steam to Turbine Valves -etc. (See paragraph 4.t.)) were

reviewed in detail. No major discrepancies were identified

with one ' exception - (failure to conduct a root cause

-

analysis after motor failure of RCIC Steam Supply Isolation

Valve MOV 2E51-F008). The Team also noted that an undue

length of time was required to reach an accurate root cause

analysis of Feedwater Pump excessive seal leakage. No

major repetitive failures were identified with exception of

multiple failures of CRD filters. These were adequately

explained as futher discussed in paragraph 4.t.

. _ _ _ _ _ _ _ _ _ _ _ . _

_ . _ _ . _. _-_

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-- ' Electrical - Review of work . history reports (4KV) and

.

special . historic . trend reports - indicated .that repetitive

' failures were not a . problem. :Further, the licensee trends

.

the condition of station batteries' (not a Technical

Specification requirement). However, the Team identified

weaknesses in that:

h

testing. of' the overcurrent- characteristic of

molded-case circuit breakers is not done (except for

penetration circuits)

preventive maintenance on 4KV switchgear is not

adequate since all vendor recommendations are not

incorporated into PM procedures. (See paragraph 4.a.

for details)

-

Instrumentation and Control - The Team noted a weakness -in

the: control of calibration of measuring and test equipment.

The control.is accomplished by a manual, monthly review of'

equipment. calibration cards. The computerized I&C

Automated Tracking System for Measuring and_ Test Equipment

was saidsto be deficient in that it counted 30 days only in

each month and caused calibration dates to' vary by three to

four days. This program should be. corrected and the card

system used as a backup. However, no s' pecific problems

were identified associated with the manual system.

The licensee's deficiency identification and control system

was reviewed. During plant walkdown inspections, only m'nor

deficiencies were found (see paragraph 4.a.) .which were not

previously identified in an MW0. The deficiency identification

and control program was considered to be a strength.

The Licensee's performance trending was examined and the

determinations were: (1) root cause analysis is adequate but

should be improved; (2) performance indicators are trended and

the majority were found 'to be better' than industry standards.

These were in overtime work, percentage of non-outage MW0s

greater than three months old; the ratio of highest priority

non-outage corrective MW0s to total non-outage MW0s and overdue

PMs.

Other trend information examined included: deficiency cards,

LERs, SORS and NPRDS failed components. The Team identified no

discrepancies in the above but does recommend the augmentation of

the presently conducted functional test trending with

information from NPRDS (See paragraph 4.t.).

The Team consensus was that performance o? maintenance trending

could be improved, especially with regard to root cause

analysis.

- _ _ _ _ _ _ _ - -

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The support. interfaces -were reviewed and. noted to be strong.

.o _ The Team noted good-cooperation between maintenance and other

organizations. Daily and 'long term. planning meetings appeared

, ,

to be a. strong point. However, the Team identified a lack of

procedural definition regarding the duties'and responsibilities

.of systems engineers. Procedure: 10AC-MGR-001-0S provides some

'

e definition but is 'not specific to systems engineers. The Team

consensus was that this level of deff nition should be added to

the program.

Conclusions

' Based on the inspection above,. the consensus of the team for

- this element' was. that. the program was . rated good and the

implementation was rated good.

.(3) Maintenance Facilities, Equipment and Materials Control

Rating -

Program: Good

Imp' lamentation: Good

' Findings / Observations

The Team found the following: maintenance facilities were

' located :as _ efficient 1y' 'as possible; maintenance supervisors'

offices were located close to the shops; maintenance shops

appeared to have most tools required for the work performed; and

parts and tools storage and: requisitions was well. organized and

_

calibration activities efficiently completed-(with exception of

the weakness.in calibration activities as discussed in paragraph

5.c.(2) . above); staging and laydown areas were adequate (with

exception of one area in the Un.it I turbine building); rigging

and scaffolding were' adequate; training and mockup facilities

.

appeared adequate; and the " Hot" and " clean" machine shops are

considered programmatic strengths. These are discussed further

in paragraph 4.g.

Conclusions

'

The Team consensus was that the program and implementation for

this area was rated good.

'

1

(5

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i

, .(4) Personnel Control

Rating -

.

Program: Good

. t. -

Implementation: Good

Findings /0 observations

Observations of' in process work and discussions. with craft

personnel indicated that the electrical, I&C, and mechanical

journeymen were knowledgeable and well trained for their jobs.

, TrainingL is discussed futher :in. paragraph 4.h. Staffing for

craftLpersonnel was considered adequate. Overtime work was

maintained within reasonable limits. 'The morale and atmosphere

of; teamwork displayed by craft personnel was considered above

,

average and is . reflected in low turnover. Maintenance

management .is ' considered qualified, . enthusiastic and

instrumental in' maintaining the. teamwork displayed by. craft.

Discussions with supervisors indicated that the maintenance

training program was in accordance with INPO requirements.

Craftsmen were not' " grandfathered",. but interim qualifications

were maintained until ' formal training could be scheduled.

Craftsmen . unable to satisfactorily complete' the formal

qualification requirements are considered not qualified for the..

area of concern.

However, the training department did not provide any training

for performing preventive maintenance of 4KV switchgear. At the

time of this inspection, a lesson plan for this was being

developed as part of the phase V of INPO. training program. This

omission was considered to be a fault, but training overall was

considered a programmatic strength.

System Engineers have 13-week Engineer-in-Training Systems

Course with four days per year followup. This was considered to

be adequate. However, as previously discussed, there is need

for improved definition of the duties r.nd responsibilities of

sytems engineers and additional training may be required.

,

Conclusion

Based on the inspection above, the team rated personnel control

" good" in both program and implementation.

_ _______

z - -- - - - - - -

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F

u L6. Exit' Interview

The . inspection scope and results were summarized on April 4,1989, with'. .

b those persons indicated in. paragraph 1. The team leader described the-

.

'

areas inspected and discussed in detail the - inspection results listed

E , below.; Proprietary information is not ' contained in this report.

Dissenting comments were not received from the licensee.

(0 pen)' Violation. 321,366/89-02-01,. Inadequate Administrative

, Procedure - Paragraph 3.a.

p,

L (0 pen) Violation 321,366/89-02-02, Failure to Complete Adequate-

L ' Corrective Action Paragraphs 3.b. and 3.c.

p

.(0 pen) Violation 321,3'66/89-02-03, Failure to Take Breathing Air

Samples - Paragraph 3.d.

(Closed)' . Violation " 366/89-02-08, Failure to Follow Acceptance

Criteria for Weld Patch on Reactur Building Roof Drain -

, ,  : Paragraph 3.e.

<

(0 pen) :IFI 321,366/89-02-04,- Programmatic Link' Between Maintenance

Procedures and ASME Section XI Requirements - Paragraph 3.f.

(0 pen) IFI 321,366/89-02-05, Inspection of RHR Hanger Weld Removal -

Paragraph 3.g.

'(0 pen) IFI 321,366/89-02-06, Design Verification .of Containment

Isolation Valves T48-F310 and T48-F311 - Paragraph 3.h.

(0 pen) IFI 321,366/89-02-07, Written' Procedure for Sampling Breathing

,

Air - Paragraph 3.1.

1

1

i

_ -_ _ _ __ _ _ L

pm j.s

,

- - - -

n

[ 9?

'

60

4

7. Acronyms and Initialisms

ALARA- -

As Low As Reasonably Achievable

ANI -

Authorized Nuclear Inspector

-ANII_ -

Authorized Nuclear Inservice Inspector

ASME -

American Society of Mechanical Engineers

BOP -

Balance of Plant

B&PV -

Boiler and Pressure Vessel Code

BWR -- Boiling Water. Reactor

CRD -

-Control Rod Drive

CM -

Corrective Maintenance

DC -

Deficiency Card

DCR -

Design Change Request

ELI -

Equipment Locator Index

FT -

Functional Test

General Electric

'

-

GE

GL. --

Generic-Letter

HCU -

Hydraulic Control Units

HP ,- Health Physics

HPCI -

High Pressure Coolant Injection-

IAS -

Instrument-Air System

I&C. --

Instrumentation and Control

IFI -

. Inspector Followup Item

IN -

NRC Information Notice

INPO -

Institute of Nuclear Power Operations

ISI -

Inservice Inspection

- LCO -

Limiting Condition for Operations

Licensee Event Report

~

LER -

LLRT -

Local Leak Rate Test

LPCI -

Low Pressure Coolant Injection

MCC -

Motor Control Center

M-G -

Motor Generator

,

MPL- -

Master Parts Lis'

MSIV -

Main Steam Isolat'on Valve

.MT -

. Magnetic Particle Test

MWO- -

Maintenance Work Order

NDE. -

Nondestructive Examination

NPMIS -

Nuclear Plant Management Information System

NPRDS -

Nuclear Plant Reliability Data System

-050S -

Operations Supervisor on Shift

PARC -

Plant ALARA Review Committee

PM -

. Preventive Maintenance

PPM -

Parts Per Million

PRA -

Probabilistic Risk Assessment

-PSIG -

Pound Per Square Inch Gage

PT -

'

Liquid Penetrant Test

PT -

Potential Transformer

QA

-

Quality Assurance

QC

-

Quality Control

_ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . -_---- -_-_ _ _______-__ _ _ _ - -

. _ _ - _ _ - -

s

...

61

.R&R -

Repair and Rariac'.inent

'RCIC -

' Reactor Cm e Isolat tun Cooling

RHR -

.Re. ;oual Heat Removal

SALP -

Systematic Assessment of Licensee Performance

SCBA -

Self Contained Breathing Apparatus

'

SER -

Safety Evaluation Report

SIL --

' Service Information Letter

SOR -

Significant Occurrence Report

SOER -

Significant Operating Experience Report

SS - '

Shift Supervisor

SSAC -

Station Service Air Compressor

TI -

Temporary Instruction

UVTA -

Undervoltage Trip Attachment

W -

Westinghouse Electric Corporation

- _ _ _ - - - _ _ _ - _ _ _ _

__-

,; .-.,

y

3 >

APPE'NDIX A _

,

LIST OF LICENSEE PROCEDURES REFERENCED / REVIEWED

PROCEDURE NUMBER TITLE

52PM-X43-006-1S, Rev.'0 Electric Fire Pump Cleaning and Inspection

52GM-MEL-022-0S Motor Shaft. Pinion Key Replacement

51GM-MME-0020 Rabuild of Waste Collector Pump

b 51-GM-MNT-0020

51GM-MNT-002-0S Maintenance Housekeeping and Tool Control

l- .

52PM-R22-01-0S, Rev. 3. _4160 Volt AC Switchgear and Associated Electrical

Components Preventive Maintenance

52PM-X43-006-IS. Electric Fire Pump Cleaning Inspection

- 345V-E11-001- RHR Pump Operability,

AG-MGR-27-0687N Root Cause Determination-

10AC-MGR-004-OS Deficiency Control System-

40AC-REG-002-0S Federal and State Requirements

10AC-MGR-012-0S' Plant Event Analysis and Resolution Program

- DI-REG-08-1285N DC, SOR and LER Trending Program

DI-MNT-02-1085N, Rev. 3 Maintenance. History and Trending Program

52CM-MME-001-05, Rev. 2 Repacking Valves and the Adjustment of Valve

Packing

52CM-MME-005-OS, Rev. 1 .Limitorque Valve Operator Models MB-0 through

SMB-4~

Mechanical Maintenance

- 52CM-MME-011-05, Rev. 2 Gate and Globe Valve Repair

52CM-MME-013-0S, Rev. O Purge and Vent Valve T-Ring Replacement

51GM-MNT-002-OS, Rev. 3 Maintenance Housekeeping and Tool Control

42SV-SUV-004-2S, Rev. 1 Safety Relief Valve ISI Test

10AC-MGR-003-0S, Rev. 9 Preparation and Control of Procedures

I

l

'

m_'_m___ l_ _ _ _ _ _

- -

- - - - - - - - - - - - - - -

7

,,

.,

'

a t

, Appendix'A 2 l

..

- 10AC-MGR-001-OS, Rev. 4 Plant Organization, Staff Responsibilities - and

Authorities

. AG-ENG-03-1185N, Rev. 1 GE Service Information Letters (SILs) and Rapid

Information ' Communication Service Information

Letters (RICSILS) Review and Tracking

'42EN-2NG-014-05, Rev. 1 ASME Section XI Repair Replacement Program

a 50AC-MNT-001-OS, Rev. 8 Maintenance Program

01-0AP-10-0588N, Rev. 0" Planning and Control Maintenance Work Order

Processing

' DI-MNT-10-0287N, Rev. O Int ,im Qualification Job Assignment

53PM-MON-001-0S', Rev. O Vibration Monitoring of Rotating Machinery

L 53PM-MON-002-05, Rev. O Lubrication Analysis

.50AC-MNT-007-OS, Rev.:1' = Preventive Maintenance Program

20AC-ADM-003-05, Rev. 2 Vendor Manual Control

01-TRN-29-0286N,-Rev. 0 Vendor Provided Training

26MC-MTL-003-0S, Rev. O Vendor Manual Review

295IT-0TM-001-OS, Rev. O .

Maintenance Work Order Functional Test Guideline

L AG-ENG-01-0786N, Rev. O Control for Technical Information Letters (TIL's)

'20AC-MTL-001-OS, Rev. O Procurement of Materials and Services

GEN-12750, Rev. 6 Qualification and Testing of nondestructive

Testing (NOT) Personnel

40AC-QCX-001-0S, Rev. 3 Quality Control Inspection Program

45QC-INS-004-OS,:Rev.1 Visual Examination Procedure, Piping and

Component

45QC-INS-005-0S, Rev. 1 Visual Examination Procedure for Structural Steel i

45QC-INS-006-OS, Rev. O Liquid Penetrant Examination Procedure

45QC-INS-008-OS, Rev. O Magnetic Particle Inspection

-45QC-QCX-002-05, Rev. 2 Quality Control Inspection Plans

!

i

1

- - _ - _ _ _ _ _ - _ _ __ i

_ _ - _ _ _ _ _

'

..

i ..

t

j Appendix A 3

,

450C-QCX-009-OS, Rev. O, Quality Control Document Review and Hold Point

Assignment

45QC-PQL-001-00S, Rev. 3 Qualification Of Inspection Personnel

A-MB-01, Rev. 1 Weld Inspection of B31.1 Component

QA-05-17, Rev. 4 QA Surveillance

31GO-OPS-006-05, Rev 1 Limiting Conditions For Operations (LCO)

42EN-ENG-010-OS, Rev. 2 Requisition Review for Quality Requirements

40AC-ENG-011-OS, Rev. 2 Environmental Qualification Program

55MC-PRO-001-OS, Rev. 2 Procurement Document Processing

26MC-MTL-001-0S, Rev. 2 Materials Receiving

'45QC-QCX-001-05, Rev. 2 Materials Receipt Inspection

50AC-MTL-002-0S, Rev. 2 Identification and Control of Material and

Equipment

55MC-MTL-003-05, Rev. 2 Material Identification and Issue Control

50AC-MTL-003-0S, Rev. 2 Warehouse Preservations, Handling, Shipping

Storage of Materials Equipment

26MC-MTL-002-05, Rev. O Preservation,. Storage and Handling of Material &

Equipment

42EN-ENG-009-05, Rev. 4 Equivalency Determination of Replacement Parts or

Materials

51GM-MNT-002-05, Rev. 3 Maintenance Housekeeping and Tool Control,

11/9/87

34AR-654-051-1, Rev. O Annunciator Response Procedure - Control Building

Service Air Trouble, 10/01/85

10AC-MGR-003-0S, Rev. 9 Preparation and Control of Procedures, 10/20/88

62RP-RAD-003-05, Rev. 1 Use and Care of Respirators

60AC-HPX-006-05, Rev. 3 Respiratory Protection Program

PROCEDURE NUMBER TITLE

62EV-SAM-005-05, Rev. 2 Monitoring Program for Detection of Releases Via

Unplanned Routes, 10/19/88

- - _ - -__ - - ____-_-. - i

._ . _ _ _ _ - _ . _ _ _ _ _ _ _ _ _ _ _-_ _ _ - _ _ - _ _ _ _ _ _ _ _ - _

_ _ _ _ _ - _ _ - _ ,

o

4

Appendix A 4

l

DI-RAD-03-1087N, Rev. I Survey / Inspection Frequency and Work Schedule,

8/8/88

34AR-700-040-2, Rev. O Annunciator Response Procedure, 8/23/85

34AB-0PS-020-2S, Rev. 4 Loss of Instrument and Service Air System,

12/12/88

- 34AB-0PS-020-IS, Rev 4 Loss of Instrument and Service Air System,

12/13/88

52PM-P51-001-1S, Rev. 1 Instrument and Service Air Maintenance, 2/1/89

i

I

i

,

l

l

.

.

I

- _ - _ _ _ _ _ _ - . - .

- _ _ _ _ .

.

APPENDIX B

List of Work Orders Reviewed

Work Order 'iumber Description

l

2-88-4802 Cot 11r.g Fan 2A2 Motor Changeout MPL #2W24-C002

2-88-4922 Inspect Brushes on Recirc Pump Motor Generator Sets

MPL # 2B31-S001A/B

2-88-1788 Valve Air Leak

2-88-01810 Valve Air Leak

1-88-08388 PM on Electric Fire Pump IX43-C001

2-89-00536 Repair MSIV

1-88-8411 Replace Battery for Demineralized Programmable

Controller

1-89-00227 Annunciator in Alarm For Safety / Blowdown Valve Leak

1-87-02710 Valve 2B21 - F019 Failed to Close

2-87-02714 Switches not Sensing Vacuum

2-88-01788 Valve Air Leak

2-88-01787 Turbine Building Vent Supply From Low Flow Alarm

2-88-02239 Valve Air Leak

2-87-04312 Water in Switch Internals

1-88-01286 Indicating Switch Failed to Respond

1-88-08388 Preventive Maintenance on Electric Fire

Protective Pump

1-89-308 Motor Shaft Pinion Key Replacement

1-89-309 Motor Shaft Pinion Key Replacement

2-89-400 Rebuild of Waste Collector Pump

2-88-1906 Rebuild Condensate Pump

2-88-1907 Rebuild Condensate Pump  !

- - - - l

_ - _ - _ - . _ _

"

1

.] '

,

..,

n .

Appendix B 2'

1

4 -

' Work Order Number  : Description

2-88-3177 Rebuild. Condensate Pump

2-89-540 Correct Seal Water Leak on Feedwater Pump

1-89-821. . Correct Seal Water Leak on Feedwater Pump

2-88-00460- Complete Rework on RCIC

steam supply Isolation valve 2E51-F007

2-88-01260 Changed torque switch settings on 2E51-F007.'

.2-88-01325 Changed Stem on Valve 2E51-F007

1-88-07113 . Change torque switch settings to repair cracked

yoke on HPCI Isolation Valve IE41-F002

2-88-04575_. Repair Coupling on Recirc M-G Set 2B31-S001A'

2-88-04345- ~ Repair oil mist eliminator.on Recirc M-G Set

,

2831-S001A

2-88-02384- Correct gage labeling on lube oil pump: headers on

Recirc M-G Set 2831-S001A-_

28-88-02226' Correct erratic tachomeier. on Recirc M-G Set  :

2831-S001A l

'2-88-02156 Repair pump outboard oil seal leak on Recirc M-G Set

2831-S001A

2-88 102155

~

Repair oil leaks from fluid drive filters.on Recirc

M-G Set 2B31-S001A-

2-88-02151 Repair check valve bonnet leak on Recir M-G Set

2831-S001A'

-2-88-02149 Repair fluid drive oil leak from 2" flange on Recirc

M-G Set 2B31-S001A

2-88-02132 Repair oil leaks from bearing plugs and sightglasses

on Recirc M-G 2B31-S001A

2-88-02067 Repair Binding scoop tube actuator on Recirc.M-G

Set 2B31-S001A

2-88-02060 Correct lack of pump speed runback after trip on

Recirc M-G Set 2831-S001A

Work-Order Number Description

_ _ _ _ _ _ - _ _ _ - _

g . _ _ _ __ .______ _ _

<,

. d

7 Appendix B 3

L2 -88-02152 Repair' bonnet and packing leaks on valves F154A and

F157A on Recirc M-G Set 2B31-S001A

2-88-04845 Repair lack of scoop tube positioner reset on Recirc

M-G set 2831-S001B

2-88-03468- Repair field breaker on Recirc M-G Set 2B31-S001B

2-88-02688 Repair tachometer on Recirc M-G Set 2831-S001B

2-88-02384 Repair lube oil suction header gages on Recirc M-G

Set 2B31-S001B

2-88-02159 Repair. fluid drive flange leak downstream of valve

F106B on Recirc M-G Set 2831-S001B

2-88-02157- ' Correct fluid drive sightglass leaks on Recirc M-G

Set 2831-S0018-

L2-88-02154 Repair pump outboard oil seal leak on Recir M-G Set

2831-S0018-

2-88-01342- Repair fan in M-G Set room of Recirc M-G Set

2B31-S001B

.2-88-02069 '* Correct high DP on CRD Drive water filter 2C11-D003B

2-88-01694' * Correct high DP on CRD Drive water filter 2C11-D003B

2-88-01606 * Correct high DP on CRD Drive water filter 2011-D003B

2-88-01592- * Correct high DP on CRD Drive water filter 2C11-D003B

2-88-01439 * Correct high DP on CRD Drive water filter 2C11-D003B

'2-88-01162 * Correct high DP on CRD Drive water filter 2C11-D003B

..

2-88-00522 * Correct high DP on CRD Drive water filter 2C11-D003B

  • Note: These were clearly identified as repetitive failures and were due to

initial poor water quality during start-up from refueling outage.

(

'l-88-67475 Repair bent coupling guard on HPCI pump IE41-C001

'

1-88-07248 Repair governor valve control circuitry for HPCI pump

1E41-C001

.1-88-05104- HPCI pump IE41-C001 tripped on turbine exhaust

l pressure - Repair as necertary

Work Order Number Description

w____________ - _ _ _ -

__ __ _ _ - _ _ _ - . - - _ _ -

t

(4 ; , .,

Q lll '

Appendix B 4

'

1-88-02513 Repair leak in seal water -line' on suction side of

- HPCI pump 1E41-C001

1-88-01733: Repair. gear box oil' leak on HPCI pump IE41-C001

"

1-88-01237- Replace missing alignment bolt on gearbox for HPCI

, pump 1E41-C001

2-88-00460 ~ Repair seat leakage on RCIC steam isolation valve

2E51-F007

2-88-00775 Reset Limitorque motor operator using MAC tester on

'

RCIC steam isolation valve 2ESI-F007

'

'

.

'2-88-00760' Resplice-cable for RCIC' steam isolation valve-

i 2E51-F007 at Penet' ration 2T52-X1050

2-88-01260 . Increase torque switch setting for RCIC steam

isolation valve 2E51-F007

2-88-01277 . Rotate Limitorque operator on RCIC steam isolation

valve 2E51-F007

~ 2-88-01325' ' Troubleshoot and repair RCIC' steam isolation

valve 2E51-F007

2-88-02575: Repair packing leak on RCIC ' steam isolation' valve

2E51-F007

2-88-02612 Replaced damanged motor on RCIC steam isolation valve

'

2E51-F008 (Note: motor meggered ok - root cause of

failure not completed)

2-88-01262 Repair damaged motor lead on RCIC steam isolation

valve 2E51-F008-

2-88-01240 Repair packing leak on RCIC steam isolation valve

2E51-F008

2-88-01213- Increase torque switch setting and re MAC test RCIC

steam isolation valve 2E51-F008

..

2-68-00625 Repair broken flex cable EEA90738 on RCIC steam

isolation valve 2E51-F008

2-88-00605' Replace brittle control leads on RCIC steam isolation

valve 2E51-F008

.

Work Order Number Description

I

-

_ _ _ _ _

gr = . .. ,

,

p ' . x 1 .: e

4 , ,

-

'

'

Appendir. B 5.

t

i

' L2-88-02695-  ; Repair faulty limit switch'on.RCIC steam to turbine.

valve 2E51-F045:

'

2-38-025811 Repair.mid position stop on closing for RCIC steam to-

turbine valve 2E51-F045

%i

12-88-01953 Repair leak-by on RCIC steam to. turbine valve

2E51-F045

'

2-88-01025 7 Adjust limit switch per MAC test on RCIC steam to

, turbine. valve 2E51-F045

-2-88-00231 Repair / replace Bellville washer pack on RCIC steam

to turbine valve 2E51-F045

1-88-08045 . Correct Faulty trip on RCIC steam to turbine valve

'1E51-F045

l-88-04251 Adjust declutch. lever and fingers on RCIC steam to

. turbine' valve 1E51-F045

o 1-88-04248' Adjust operator to prevent coasting into backseat on

RCIC steam to turbine valve 1E51-F045-

'

1-88-01311 Perform MAC test at system flow on'.RCIC steam to:

turbine valve IE51-F045

1-88-01310 Perform static MAC test on RCIC steam to turbine

valve IE51-F045

~1-88-00589 Correct-seat-leakage on.RCIC~ steam to turbine valve

'1E51-F045

2-86-3811 Verify torque of bottom bolts to 45-50 foot pounds for

Unit 2 HCUs

(

1-86-7330 Install missing flat washers and verify torque to

45-50 foot pounds for Unit 1 HCUs

'

1-88-5022 Modify reactor building RHR supports E11-RHR-H33, 34,

35, 293 and 274

2-85-1424 Weld patch on Rx building roof drain 2T55-RSD-5

2-89-00724 Torque back-to-back top plate cap screws to 15-25

foot pounds and confirm full thread engagement

for all Unit 2 HCDs

7 1-89-01077 Torque back-to-back top plate cap screws to 15-20

foot pounds and confirm full thread engagement for

all Unit 1 HCUs

-___ - _ _ - __ _ - _ -

_ _ _ _ _ _ _ _ _ _ _ _ _ - _ -

!

..

1

Appendix B 6

1-88-07300 Weld patt:h to repair valve IN71-F200 (FW001) l

2-89-0619 Fabricate and install motor base for surge tank pump

2G11-C015 (FW Nos. 1-8)

.

_ - - _.

- __ _ _ _ _ _ _ _ _ _ _ _ _- _______-_ ___-___ _ __-___

+.

.s.,

APPENDIX C

List of Components / Systems / Areas

Inspected During Walkdown Inspections

Unit 1 Main Generator

4160V Station Service Switchgear

IG 1R24-SO45

IB 1R22-S002

1C 1R22-S003

' IDL 1R22-S004

2A 2R22-5001

2B 2R22-5002

2C 2R22-S003

2D 2R22-S004

IE 1R22-S005

IF 1R22-S006

IG 1R22-S007.

2E -2R22-S005

2F 2R22-S006-

2G 2R22-5007

600V Station Service Switchgear

IB' 1R23-5002

1R23-5001

2A 2R23-S001

28 2R23-S002

Motor Control Center (MCC)

2D 2R24-S035

208V 1G 1R24-5045

250 VDC 2A 2R24-5021

600/208V 2A 2R24-S013

600/208V 2C 2R24-S011

600V 2E 2R24-5018B

600V 2E 2R24-S018A

250VDC 2B 2R24-S022

Five (5) diesel generators and associated batery rooms and electrical equipment

roomr.

Cooling tower electrical room

Cooling tower fan motor 2W24-C002 at tow 9r 4

l ' Inverters IR44-5002 and S003

Inverters 2R44-S002 and S003

l

l

t

b . ..

_--

- . _ . ._ . - . .

,' ;, (

Appendix <C ,

>

2-

l>

< _ Units I and 2 control- room and back panel areas

Unit 2 Recirc pump motor generator sets 2B31-S001A and B

l Backwash-Pump 2N21-C008

Condensate. Pump'2d21-C001A

'

. Condensate. Booster Pump 2N21-C002A~

,

Recirc MG Set 2831-S001B

Valve 2P42-F3006B

Lube 011: Circ Pump 2B31-S001B3

EHC'011 Rooms'(Unit 1) including EHC Purr.ps . IN32-C001A and 1N32-C001B and EHC

Coolers-

. Reactor.SBuilding Closed Cooling Water Heat Exchangers 2P42-B001A and 2P42-B001B

and Pumps 2P42-C001A and 2P42-C001B-

Backwash. Pump1 1N21'C008

,

. Unit 1: demineralized Valve. Nest

Condensate Pumps IN21' C001A', ~ 1N21-C001B, and :IN21-C001C

-

Unit 1 NE diag. and HPCI Room' including Main Pump IE41-C001.and

. Booster Pump IE41-C001

Unit li SE ' diag. including Pump Motors '1E11-C002A,1E11-C002C, and 1E11-C001A-

Unit?2'SE diag. HPCI Roon. including Main Pump 2E41-C001 and Booster Pump

2E41-C001-

FW Pump N21-C003A and general area

Electric Fire Protection Pump -1X43-C001 and. general area

Fire-Protection Jockey Pump IX43-C003 and general area

Unit 2 Loop'A RHR Pump 2E11-C002A;

discharge pressure gage 2E11-R003A;

suction pressure cage 2E11-R002A;

and nearby area

'

Unit 2 Core Spray Pump 2E21-C003A and Valve 2E21-F126A

Control Room and annunciator system for main steam

,

Unit 1: Turbine Building

QL _ _ _- _ - . - - _ - . - - _. 1

--_ _

-

.

Appendix C 3

Unit 1 and Unit 2 HCUs

Unit I and Unit 2 Reactor Buildings at 130 foot elevation

Unit 1 and Unit 2 Turbine Building east cableways

Unit 1 and Unit 2 Service Air System P51

Clean and Hot machine shops

Valves as listed below:

IZ43-F45-1AB 2P51-F087

IZ43-F45-2AD 2U43-F309C

IP42-F057 2P51-F098

IP41-F368B 2U43-F091

2U45-F092 2P41-F052B

2T48-F121 2P41-F070B

2T48-F120 2P41-F059

2T48-F014 2P41-F070A

2T48-F111 2P41-F050A

2C11-F002A

2C11-F047A

2C11-F046B

2C11-F005

m. ______