ML20137F645

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Insp Repts 50-321/97-01 & 50-366/97-01 on 970119-0222. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20137F645
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 03/24/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20137F607 List:
References
50-321-97-01, 50-321-97-1, 50-366-97-01, 50-366-97-1, NUDOCS 9704010171
Download: ML20137F645 (45)


See also: IR 05000321/1997001

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

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' Docket Nos: 50-321. 50-366

License Nos: DPR-57 and NPF-5

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Report No: 50-321/97-01, 50-366/97-01

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Licensee: Southern Nuclear Operating Company. Inc.

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Facility: E. I. Hatch Units 1 & 2

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! Location: P. O. Box 439

i Baxley. Georgia 31513  ;

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Dates: January 19 - February 22. 1997

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l Inspectors: B. Holbrook Senior P.esident Inspector i

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E. Christnot. Resident Inspector

, J. Canady Resident Inspector

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W. Miller. Reactor Inspector (Sections

F1.2. F1.3. F2.2. F2.4. F3, F5. F7. and F8 .;

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Approved by: P. Skinner. Chief. Projects Branch 2

Division of Reactor Projects

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Enclosure 2 '

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9704010171 970324 i

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EXECUTIVE SUMMARY

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Plant Hatch. Units 1 and 2

NRC Inspection Reports 50-321/97-01 and 50-366/97-01

This integrated inspection included aspects of licensee operations, j

engineering, maintenance, and plant support. The report covers a 5-week  ;

period of resident inspection. In addition, it includes the results of

an inspection by a regional reactor inspector in the area of fire l

protection.

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Ooerations  !

e The inspectors verified that the current revision of appropriate l

procedures was located at each of the Emergency Diesel Generators

(EDG). Housekeeping was superior in the EDG Building and good at

the intake structure. A previously identified pin hole leak at <

the Plant Service Water air release valve had not changed  !

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appreciably since its discovery in September 1996 (Section 01.2).

e The Unit 2 power reduction on January 23. was performed in  !

accordance with approved procedures, with adequate supervision and

management monitoring. Effective pre-job briefings were conducted  !

prior to the evolutions. Minor deficiencies.were identified in ,

operator alarm response and control room communications  ;

(Section 01.3).

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e The inspectors concluded that the Unit 1 shutdown due to pressure j

i boundary leakage was performed in a controlled manner using

L approved procedures. Supervisory and Shift Technical Advisor

oversight and support were evident (Section 01.4). t

i e The inspectors concluded that the requirements of selected

Technical Specification (TS) surveillances for the Unit 1 and

Unit 2 Standby Licuid Control (SBLC) System were met. The most

recently installec SBLC explosive valves for Units 1 and 2

contained charges from a certified batch (Section 02.1).

e Violation (VIO) 50-321. 366/97-01-01: Failure to Follow Procedure ,

- Multiple Examples, was identified. This example was for the  ;

failure to perform hourly fire watch patrols for fire zone 24A >

(Section 04.1).  ;

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Maintenance  ;

e For the surveillances observed, all data. met the required j

l acceptance criteria and the equipment performed satisfactorily.

The performance of the operators and crews conducting the

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surveillances was generally professional and competent. No

deficiencies were identified (Section M3.1).

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Enclosure 2 ,

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e Violation 50-366/97-01-02: Inadequate Procedure for Calibrating i

Unit 2 HPCI Time Delay Relay K14, was identified. The risk '

involved in performing the HPCI time delay relay calibration on

line was not procedurally identified for Unit 2. as it was'for  ;

l Unit 1. The troubleshooting by the engineering staff was  :

l conducted in a thorough and competent manner. The appro  !

! 10 CFR 50.72 reports were made to the NRC (Section M3.2)priate .

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e Violation 50-321, 366/97-01-01: Failure To Follow Procedures -  :

Multiple Examples, was identified. This example was for the  ;

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failure-to calibrate the Unit I relays associated with Design

Change Request (DCR) 96-55, for 4kV Bus 1F1 Transformer.  ;

l The inspectors also concluded that engineering and maintenance l

l personnel demonstrated inattention to detail and a lack of a

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questioning attitude to ensure that all required relay setting

changes were identified and completed. The inspectors concluded

that the technicians who identified the incorrect relay settings

were knowledgeable and demonstrated a questioning attitude

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i Enaineerina

e The inspectors concluded that the licensee was responsive to  !

correct potential problems identified in its system review in

response to Generic Letter 96-06: Assurance of Equipment

Operability and Containment Integrity During Design-Bases Accident

Conditions (Section E1.1).

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l s' The inspectors concluded that system logic reviews' conducted from

j 1989 through 1991' failed to identify that a portion of the 4160-

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volt alternating current (VAC) emergency switchgear logic had not

i been tested. This was considered to be an engineering oversight.

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The inspectors concluded that the licensee's immediate actions

were appropriate (Section E1.2).

e Violation 50-321. 366/97-01-01: Failure To Follow Procedure -

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Multiple Examples, was identified. This example was for failure

l to ensure that the Unit 1 Rod Worth Minimizer was enforcing the

L correct rod sequence mode (Section E2.1).

e Violation 50-321/97-01-03: Failure to Translate Original Design

Specifications Into Applicable Instructions, was identified. The

design specifications were for the replacement of the Residual

Heat Removal system vent- piping and valves during the last Unit 1

l refueling outage (Section E2.2).

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Enclosure 2

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e The inspectors also concluded that the licensee identified the

most probable cause for the weld failure that resulted in the

Unit 1 pressure boundary leakage. The repair was made with

management oversight, engineering input. quality control

inspections. and maintenance supervision (Section E2.2).

Plant Stiooort

e Health Physics control was excellent for drywell entry during the

forced outage on Unit 1. The observed use of three-part

communications by plant equipment operators was excellent.

Overall housekeeping on the 130-foot elevation and the 106-foot

elevation of the of the northeast diagonal w , satisfactory.

(Section R1.2)

e An observed representative sampling of Self Contained Breathing

Apparatus (SCBA) by licensee personnel determined that they were

functional. The technician Jerforming the inspection was

conscientious and knowledgea]le. Observed calibration stickers

were current. The requirements of the Emergency Plan, with respect

to the number of SCBA units and spare bottles available, were

maintained (Section R2.1).

e The inspectors concluded that the Emergency Preparedness Staff

Augmentation Drill conducted February 4 was not successful, as

described in the Hatch Emergency Plan. Although some items for

im3rovement were identified during a second drill conducted on

Fe]ruary 18. all Hatch Emergency Plan requirements were met. The

licensee initiated appropriate measures to determine root cause

and deveiop corrective actions (Section Pl.1).

e Violation 50-321. 366/97-01-01: Failure To Follow Procedure -

Multiple Examples, was identified. This example was for failure

to follow security procedures for weapon inventory (Section S1).

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e Violation 50-321, 366/97-01-01: Failure To Follow Procedure - l

Multiple Examples, was identified. This example was for storage  !

of waste oil transient combustibles in a safety-related area.  :

without a Transient Combustible Permit (TCP). The inspectors '

concluded that the administrative aspects of the TCP process of

the Fire Protection Program had deteriorated and was a weakness in  !

the fire protection program (Section F1.1). l

e The licensee was taking appropriate action to resolve the Thermo- ,

Lag issue at Hatch (Section F1.2). j

e Although damaged Kaowool assemblies were noted in several areas of

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the plant, the Kaowool installations provided to meet NRC fire

protection requirements were properly maintained (Section F1.3).

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Enclosure 2 I

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e The inspectors concluded that the repair activities for a fire i

header leak were performed in accordance with approved procedures. I

with supervisory oversight and engineering support. The system )

clearance, compensatory fire protection measures, and system i

restoration were satisfactory (Section F2.1). j

e There was no significant maintenance backlog on the fire l

protection systems. The material condition of the fire protection I

components, including the fire brigade equipment, was very good

(Section F2.2).

e Appropriate surveillances and tests were being performed on fire

protection features and systems. Appropriate evaluations were

also performed on the completed test results by the engineering j

group (Section F2.4).

e Violation 50-321, 366/97-01-04: Failure to Submit Special Report

on Degraded Fire Barriers, was identified. A special report on l

degraded fire barrier penetrations on the 112-foot elevation of  !

the control building, as required by Fire Hazards Analysis (FHA).

Section 9.2. Appendix B was not completed (Section F3).

e The fire 3rotection program implementing procedures were adecuate

and met t7e commitments to the NRC. However the procedures cid l

not requira adequate documentation to demonstrate that the fire l

l watch patrols required for degraded or inoperable fire protection

components were actually being performed. The licensee's policy

of not submitting special reports to the Safety Review Board (SRB) ,

for any degraded fire protection components listed in the FHA is  !

identified as a violation (Section F3). 1

e The fire brigade organization and training met the requirements of I

the site procedures. Performance by the brigades during the 1996

unannounced drills was satisfactory (Section F5).

e The audits and assessments made of the facility *,s fire protection

program were thorough and appropriate corrective actions were

taken to resolve the identified issues (Section F7).

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e The licensee's evaluations and corrective actions for reviewed '

Information Notices (ins) were appro]riate, except for IN 92-18.

l Potential Loss of Shutdown Capacity Juring a Control Room Fire.

The licensee's initial evaluation was very limited. The licensee

initiated an engineering request to perform a reanalysis, as part

of an industry wide issue, which will be completed in the Summer

! of 1997 (Section F8.1).  ;

Enclosure 2

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Reoort Details

Summary of Plant Status

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Unit 1 began the report period at 100% rated thermal power (RTP) and '

continued until January 29, when the unit was shutdown to identify and  !

repair an unidentified drywell leakage problem. The leak was

identified repairs were completed, and the unit was returned to 100%

RTP on February 4. The unit operated at 100% RTP until February 22. )

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when power was reduced to about 60% RTP to repair a water leak in the '

Isophase Bus Cooler. . Repairs were completed and the unit was returned  !

to 100% RTP later the same day. '

l Unit 2 began the report period at 100% RTP and continued until l

l January 23. when power was reduced to about 65% RTP to remove the A  !

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reactor feed pump turbine from service to replace the oil system filters J

and conduct a rod pattern adjustment. Power was returned to 100% RTP on l

January 24 and operated at that power level through the remainder of the  !

report period except for routine testing activities. l

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I. Operations l

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01 Conduct of Operations

01.1 General Comments (71707)

Using inspection Procedure 71707. the inspectors conducted

frecuent reviews of ongoing plant operations. In general, the

concuct of operations was professional and safety-conscious.

Specific events and observations are detailed in the section i

below.  !

01.2 Plant Tour of Emeraency Diesel Generator Buildino and Intake  !

Structure

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a. Insoection Scooe (71707) ,

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On January 28 the inspectors performed a routine tour of the

Emergency Diesel Generator (EDG) Building and the Intake

Structure. During the tour, the inspectors reviewed the l

procedures in the EDG Building, observed general housekeeping  !

conditions, and visually monitored the status of the 2D Plant

Service Water (PSW) Air Release Valve.  !

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b. Observations and Findinas

The inspectors performed a review of the )rocedures maintained in

the EDG Building for each of the EDGs. T1e inspectors verified

that the appropriate procedures were present and that they were

the current revision.

The inspectors observed that equipment stored in the storage room

on the north end of the EDG Building was arranged in a neat and

orderly fashion. The floors and walls of the building were

recently painted and the floors were in a high state of

cleanliness. The inspectors observed that drip pans containing an

absorbent material were placed under each diesel engine to catch

minor oil drips. The use of the drip pans provided a neat and

clean appearance under the diesel engines.

During a routine tour of the Service Water Intake structure the

inspectors visually examined the PSW Air Release Valve.

2P41-F332D. A very small amount of moisture was observed in the

area where a through-wall pin hole leak was identified in

September 1996. The previously identified leak did not appear to

have increased. The licensee continues to monitor the valve

daily. No housekeeping deficiencies were identified in the intake

structure.

c. Conclusions

The inspectors concluded that the current revision of the

appro)riate procedures were located at each of the EDGs.

Houseceeping was superior in the EDG Building and good at the

intake structure. The pin hole leak at the PSW air release-valve

had not noticeably changed since its discovery in September 1996. l

01.3 Power Reduction Unit 2

a. Insoection ScoDe (71707)

The inspectors observed licensee activities during the Unit 2

Jower reduction on January 23..The power level was reduced to 65%

RTP.for a control rod pattern adjustment and selected maintenance. .

The unit was returned to 100% RTP on January 24. l

b .~ Observations and Findinas

The inspectors observed Control Room (CR) activities c'uring the

power reduction. The inspectors attended the pre-job and As low i

As Reasonably Achievable (ALARA) briefing conducted price.to the 1

activities. The briefing was thorough with emphasis on command

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l and control, communications, procedure adherence, and dose

awareness. Questions raised during the briefing were fully

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discussed and answered.

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Among the procedures used by the operators were those associated

with power changes and system operations. The inspectors observed

that the procedures were the latest revisions. The observed

arocedural usage was in accordance with procedure 10AC-MGR-019-05: .

3rocedure Use and Adherence. Rev. O.  !

Command and control activities were good. Only necessary

personnel were in the control room and a low level of noise was

maintained. Minor deficiencies were identified in the areas of  ;

annunciator response, three-part communication, and use of the  !

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phonetic alphabet.

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An alarm. GENERATOR B LOCK 0UT. was received. The operator did not l

verbalize the alarm. The operator silenced the alarm and started

to review the Alarm Response Procedure (ARP). Prior to completing

the procedural review, the alarm reset. The operator replaced the

ARP and did not further persue the issue. The inspectors reviewed

the ARP for the Generator B Lockout alarm and observed that the

alarm normally indicates a significant problem with the

Recirculating System Motor-Generator (MG). The inspectors

considered the action taken by the operator of not informing other

crew members of an unexpected alarm or further pursueing the alarm

could have been better. The inspectors discussed these

observations with operations supervision.

c. Conclusions

The inspectors concluded that the power reduction was performed in  !

accordance with approved procedures, with adequate supervision and

management monitoring. Effective pre-job briefings were conducted  !

prior to major evolutions. Minor deficiencies were identified in

alarm response and control room communications.

01.4 Unit 1 Forced Outace Activities and Notification Of Unusual Event

a. Insoection Scooe (71707)

On January 28, the inspectors observed licensee activities during

the Unit 1 forced outage due to an increase in Drywell

unidentified leakage. The unit was returned to RTP on February 3.

b. Observations and Findinos

The inspectors documented previous observations of an increased

unidentified drywell leakage in Ins)ection Report (IR)

50-321, 366/96-14. At the end of tlat report period, the leakage

Enclosure 2

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rate was about 1.4 gallons per minute (gpm). On January 23, 1997.  !

leakage had increased to about 2.4 gam. The Technical i

Specification (TS) limit is 5 gpm. _icensee management ,

established an administrative limit of about 3 gpm to initiate l

actions for a unit shutdown. However, the licensee commenced an

orderly shut down on January 28, with leakage about 2.8 gpm.  !

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Power was reduced to 10% RTP and a drywell entry was made to

, identify the source of the leak. A weld on a 3/4-inch vent pipe,

! attached to a 20-inch Residual Heat' Removal.(RHR) shutdown cooling i

suction pipe, had a crack in it. Details on the weld failure. I

root cause.. and weld repair are documented in section E2.2 of this I

report. Following the identification that the leak was in the i

]ressure boundary, the licensee declared a Notification Of Unusual

Event (NOUE) at 8:59 a.m. on January 29. The NOUE was terminated

at 7:25 a.m. on January 30, following the completion of corrective l

maintenance activities to repair the leak.

The inspectors observed control room activities, attended pre-job

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briefings, and monitored ALARA discussions during the power

l reduction. All activities were performed in accordance with

i approved procedures with Shift Supervisor (SS) and Shift Technical

! Advisor (STA) oversight and support.

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During the shutdown, control room personnel discovered that the  !

Rod Worth Minimizer (RWM) was programmed to monitor the incorrect

rod sequence mode. Unit 1 was in control rod sequence B1 and the

RWM was programmed to monitor control rod sequence B2. The

inspectors discussed this deficiency with the reactor engineer and

operations personnel. The inspector's review of the RWM is

documented in section E2.1 of this report.

l Subsecuent to the shutdown, the operators commenced performing

l~ procecure 34S0-C11-005-1S: Control Rod Drive Hydraulic System. 1

l Revison 17. Section 7.3.14. Flushing CRD Collet Piston Seals in

Shutdown. The flushing was performed by local valve manipulations

to improve control rod withdrawal during startup. When control I

rod 30-31 was selected and flushed, the rod moved out of the core.

The control room operator stopped the rod at Josition 04 and i

inserted the rod to position 00 by using the Emergency In Switch.

The inspectors observed that approximately 130 control rods had i

been flushed, using the same procedure, prior to rod 30-31. The

procedure was stopped and was not performed on the remaining 16

control rods. The licensee suspected that crud may have gotten

into the rod drive mechanism causing the control rod to move out  ;

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of the core during the flushing activity. j

! The inspectors discussed the problem with engineering personnel.

i The inspectors were informed that General Electric (GE) personnel  ;

i had been consulted about the problem and agreed that crud may have ]

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" caused the problem. The ins >ectors were later informed by

engineering personnel that t1e procedure would be revised to valve

out the. control rods during this activity to prevent similar

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p problems. The inspectors reviewed the flushing procedure and

concluded that the specified lineup and activity. should not have

j' resulted in control rod movement. The inspectors did not view the

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rod movement a significant problem with respect to core

criticality.

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i c. Conclusions

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The inspectors concluded that the shutdown was performed in a

controlled manner using approved procedures. Supervisory and STA

l- oversight and support were evident.

i 02 Operational Status of Facilities and Equipent

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i 02.1 Standby Liauid Control Syster, Review

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j a. Insoection Scooe (71707) (71750)'

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The inspectors conducted a review of the Unit 1 and Unit 2 Standby

Liquid Control (SBLC) System to verify that selected Technical

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Specification (TS) surveillance requirements were met. The-

, applicable TS procedures and Final Safety Analysis Reports (FSAR)

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were also reviewed.

b. Observations an1_ findings

The inspectors reviewd selected surveillance requirements (SRs)-

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of TS 3.1.7 for Units 1 and 2. The corresponding TS bases were

also reviewed for both units.

The- following TS surveillance requirements and TS bases items were

verified for acceptability on both units:

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The sodium pentaborate solution volume versus concentration

and the solution temperature versus concentration

requirements every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

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The flow through one SBLC subsystem from the pump into the

redctor pressure vessel every 18 months on a staggered test

basis.

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Non-blockage of the heat traced piping between the storage

tank and the pump suction every 18 months.

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Proper batch certification for replacement charges for

explosive valve.

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l In verifying that the above TS and bases items were performed, the

inspectors reviewed the data packages for 3rocedures

, 34SV-C41-003-IS and 34SV-C41-003-2S: Stand)y Liquid Control j

Injection Test. Rev. 8 and Rev. 9 respectively. The Jackages for 1
the past three outages on each unit were reviewed. T1e inspectors

also reviewed the most recent data packages contained in

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procedures 52PM-C41-105-1S and 52PM-C41-105-2S: SBLC Explosive

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Valve Replacement. Rev. 6 and Rev. 6. respectively. MWO  !

i 2-94-3557. Test Fire Explosive Valve, was reviewed in conjunction i

! with the SBLC explosive valve replacement data package. This

! review verified that the most recently replaced charge for

explosive valves 1C41-F004A and 2C41-F004A were from a batch that

had been certified by having a charge from that batch successfully l

fi red. l

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l The inspectors reviewed Unit 1 and Unit 2 FSAR sections 3.8 and

7.4.2 respectively, and did not identify any deficiencies.

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j It was determined from a review of data packages that the

i requirements of the selected TS surveillances for the SBLC system

i were met. It was also verified that the most recently installed

j explosive valves for Units 1 and 2 have charges from a certified

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l 04.0 Operator Knowledge and Performance '

04.1 Hourly Fire Watch Patrol

a. Insoection Scooe (92901)  !

The inspectors performed followup activities for establishing and 4

conducting an hourly fire watch patrol for an inoperable cable

tray, i

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b. Observations and Findinas

Requirements for an hourly fire watch patrol was established on

January 16, 1997, for-Fire Zone 24A. located in the Unit 1 and

Unit 2 Cable Spreading Room. Fire Action 1-97-3 identified that

cable tray TMA8-10 contained damaged Kaowool and was inoperable.

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The inspectors reviewed information involving entries made into

Fire Zone 24A: operations shift manning sheets pertaining to fire

watches; and the Fire Hazard Analysis (FHA). Appendix B. Fire

Equipment Operating and Surveillance Requirements. The operations

shift manning sheets identified personnel who were assigned fire

watch duties during the shift.

Enclosure 2

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The inspectors identified from document reviews that entries into  !

Fire Zone 24A on four occasions exceeded the one-hour requirement

during the normal 12-hour shift. The following are entry interval

times: January 17,1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 34 minutes and I hour and 59

minutes; on January 18, 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 54 minutes; and on January 21.

7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> and 11 minutes.  !

Between the normal 12-hour operating shifts (shift turnover time),

the time Jeriods for numerous entries into Fire Zone 24A were ,

greater t1an 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The longest period observed between shift  !

l changes was on January 21. for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 42 minutes. i

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On several occasions )ersonnel who were not identified anywhere j

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on the shift manning sleets made hourly entries into Fire

Zone 24A. On numerous occasions, personnel not identified on the

L shift manning sheets as fire watch personnel made hourly entries

into Fire Zone 24A. On several occasions, entries into the fire

zone lasted for a total of 6 seconds.

! The FHA, Appendix B. Section 1.1.1. identified cable tray

enclosures as fire rated assemblies. Subsection 1.1.1.a states. in

part, with one or more required fire-rated assemblies inoperable.

l within one hour, establish an hourly fire watch patrol.  ;

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! The inspectors identified from these reviews and discussions that l

l the fire watch 3atrols were established but all patrols were not

performed on a lourly basis. In addition it is questionable if an

adequate )atrol was made during some entries into the areas due to

the lengt1 of time spent in the fire zone (6 seconds). Specific

actions to be completed during the fire watch patrol were not

identified and no documentation was required to identify that fire

watch actions had been taken.

The inspectors discussed these observations with licensee

managers. The ins)ectors were later informed that procedures or

instructions were )eing developed to clearly identify specific

instructions for the conduct of fire watch patrols and individual

accountability.

c. Conclusions

The inspectors concluded that the failure to enter Fire Zone 24A

! on an hourly basis is a violation of the FHA. Appendix B.

Section 1.1.1. This 1s. identified as Violation (VIO).

I 50-321. 366/97-01-01: Failure to Follow Procedure - Multiple

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Exam)les. This example was for a failure to perform hourly fire

i watc1 patrols.

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Enclosure 2

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_._. _ _ _ _ . . _ . _ . _ - . . _ ~ . _ _ _ . . . _ . _ . _ . _ _ _ _ . _ _ _ _ _

'

. .

.

i

8

.

08 Miscellaneous Operations Issues (92901)(92700)

08.1 (Closed) LER 50-321/96-10: Failure of the Turbine Oversoeed- '

Control Valve of the Hiah Pressure Coolant In.iection System.

This problem was discussed in IR 50-321. 366/96-10. No new issues

were revealed by the LER. This LER is closed.

r

II. Maintenance

l

'

M1 Conduct of Maintenance

M1.1 General Comments

l_

a. Insoection Scooe (62707)

l The inspectors observed or reviewed all or portions of the

following maintenance work order (MWO) activities:

-

MWO 2-94-3557: Test Fire Explosive Valve l

-

MWO 2-96-0004: Perform LC0/ BOP Calibration of the Listed  ;

Instruments Per Procedure i

-

MWO 1-97-0130: Restore Temporary Modification 1-96-041

-

MWO 2-97-0125: Perform Lugging / Terminations for 1R24-S026

b. Observations and Findinas  !

l

The inspectors found that the work was performed with the work )

l packages present and being actively used. I

c. Conclusions on Conduct of Maintenance

l Maintenance activities were generally completed thoroughly and

! professionally. No deficiencies were identified by the

inspectors.

l M3 Maintenance Procedures and Documentation

M3.1 Surveillance Observations

i

1

a. Insoection Scooe (61726_1 )

!

, The inspectors observed all or portions of the following Unit 1  :

( and Unit 2 surveillance activities:

!

- 34SV-C11-003-1S: Control Rod Weekly Exercise  !

j - 34SV-C51-002-1S: APRM Functional Test

l Enclosure 2

_ _ _ _ . _ _ . _ _ _ . . _. _ - -

.

.

9

b. Observations and Findinas

The inspectors observed that two licensed operators were present

at the control panel during the manipulations of control rods in

the performance of procedure 34SV-C11-003-1S, Rev. 10. Ed 1. The

use of the phonetic alphabet and three-part communications were

observed during the surveillance activities.

c. Conclusions

For the surveillances observed, all data met the required

acceptance criteria and the equipment performed satisfactorily.

The performance of the operators and crews conducting the

surveillances was generally professional and competent. No

deficiencies were identified.

M3.2 Relay Calibration Caused Unexoected Receiot of Annunciators and ,

'

Closina of Containment Isolation Valve

a. Insoection Scooe (62707)(37551)

The inspectors observed and reviewed licene2 activities following

inadvertent isolation of the Unit 2 High Pressure Coolant

Injection (HPCI) Vacuum Breaker Valve 2E41-F111. during the

performance of a routine surveillance.

b. Observations and Findinas

On January 25. the control room operators received the unexpected

alarms. HPCI LOGIC POWER FAILURE HPCI PUMP DISCH FLOW LOW. and

HPCI VACUUM BREAKER VALVE NOT FULLY OPEN, during the calibration

of time delay relay 2E41-K14. Also, the HPCI Vacuum Breaker valve

closed unexpectedly. Instrumentation and Control (I&C) personnel 1

were calibrating the relay in accordance with procedure

57CP-CAL-051-2S: GE Type CR2820B and ITE Gould Type J20T3 Delay

Relay Rev. 7. During the calibration, a wire was lifted that

caused the initiation of the unexpected alarms and valve closure.

The lifted wire was returned to its original location after the

unexpected initiations and_HPCI was restored to its standby

configuration.

Subsequent investigations by I&C and engineering personnel

determined that the HPCI automatic initiation capability was lost

during the short time that the wire was lifted, approximately

30 seconds.

The inspectors observed that the HPCI vacuum breaker valve is a

primary containment isolation valve and its logic initiation and

the HPCI inoperability were reported in accordance with the

requirements of 10 CFR 50.72.

Enclosure 2

_ .

_...__-___m.. . _ . _ _ . . - _ _

l .

' '

l .

10

l

Prior calibrations of the 2E41-K14 relay was normally performed

during refueling outages or at other times when the unit was off

line and the HPCI system was not available. The system engineer

informed the inspectors that he was not made aware that this

! calibration was scheduled to be performed online and that he would

t

not have recommended performing the calibration on line. The

inspectors were informed that this procedure was selected to be

! conducted on line. Maintenance personnel review of the procedure

to identify potential unit or system problems for online

performance of-the calibration procedure failed to identify the

.

above-referenced problems.

l

The inspectors also reviewed procedure 57CP-CAL-051-1S: G.E. Type

CR2820B and Square D Class 8501 Type LT Time Delay Relay. Rev. 7

Edition (Ed) 1. This is the similar procedure for Unit 1.

,

Attachment 2. Removal and Return to Service Instruction, states

l for the 1E41-K14 relay. " Remove only when HPCI is isolated or

l during refueling." The inspectors did not identify a similar type

statement in the Unit 2 procedure.

l The inspectors questioned licensee personnel about any other

l relays or components that were scheduled for on-line maintenance

l or work activities, which had the potential for causing the

initiation of similar unexpected events. The inspectors were

informed that a review was being performed to make such a

determination.

1

An Event Review Team (ERT) consisting of Engineering. Nuclear

Safety and Compliance (NSAC). I&C. electrical maintenance, and

training personnel conducted investigations to determine the cause

for the unexpected initiations. One aspect of the investigations

included the simulation of the relay configuration that caused the

closing of the HPCI Vacuum Breaker Valve.

On January 28. the inspectors observed a demonstration that

simulated the problem that caused the 2E41-F111 valve to

unex)ectedly isolate. The demonstration showed that the lifting

of tie wire on the relay caused a backfeed circuit that energized

an additional relay which resulted in closing the 2E41-F111 valve.

The inspectors reviewed calibration procedure 57CP-CAL-051-2S:

Loss of Function Diagram (LFD) 2-PCIS-15. Rev. 7. and associated

elementary diagrams. This review, in conjunction with the

engineers demonstration, provided an explanation for the closing

of the 2E41-F111 valve.

c. Conclusions

-

10 CFR 50. Appendix B. Criterion V. Instructions. Procedures and

Drawings requires that activities affecting quality shall be

1

i Enclosure 2

,

l

1

. ,

!

11

'

prescribed oy documented instructions procedures, or drawings of

a type appropriate to the circumstances and shall be accomplished

in accordance with these instructions, procedures, or drawings.

The failure to adequately identify activities affecting quality is

a violation of those requirements and is identified as Violation

50-366/97-01-02: Inadequate Procedure for Calibrating Unit 2 HPCI

Time Delay Relay K14.

The risk involved in performing the HPCI-time delay relay

calibration on line was not 3rocedurally identified for Unit 2 as

it was for Unit 1. The trou)leshooting by the engineering staff

was conducted in a thorough and com)etent manner. The appropriate

10 CFR 50.72 reports were made to t1e NRC.

M4 Maintenance Stuff Knowledge and Performance

M4.1 Incorrect Relav Calibration for DCR 96-055

a. Insoection Scoce (92902) (92903) l

On February 5 during the installation of Design Change Request

(DCR) 96-55, Motor Control Center (MCC) Breaker. Coordination

Resolution, for the B Emergency Diesel Generator (EDG) on Unit 2. 4

the licensee determined that relays IS32-K217-1. -2. and -3 for j

Unit 1 were set incorrectly. The DCR was to eliminate, for ,

certain postulated faults, possible mis-coordination between the l

safety-related supply breakers and downstream feeder breakers to

nonsafety-related loads. The inspectors reviewed licensee 3

documentation for work performed to install the DCR for l

MCC 1R24-S-26. The inspectors also observed work activities and l

reviewed the applicable procedures for the work activities. The j

inspectors reviewed an engineering evaluation concerning the

incorrect trip time setting of the Unit 1 overcurrent relays.

b. Observations and Findinas i

The ins)ectors observed from the review of the DCR. procedure

57CP-CA_-108-1S: GE IAC and Westinghouse C0 Overcurrent Relay,

Rev. 9, and the 4kV Bus 1F1 transformer Relaying Data Sheet. that

Attachment 2 of the procedure was used by the technicians to

adjust relays IS32-K217-1. -2. and -3. The relay adjustments were

made during the implementation of Temporarv Modification .i

(TM) 1-96-041. The activities involving the TM were documented in

Inspection Report (IR) 50-321, 366/96-14.

The inspectors found from the reviews that Attachment 2 of the i

procedure directed the technicians to change the relays from a

pickup setting of 7 to a new pickup setting of 5. This was i

indicated by a single line through the old setting and a new value i

Enclosure 2 ,

i

!

_

. ._ _ _ _ _ _ _ _ . _ _ _ . . . . . _ _ ... _ _ _ _ _ _ . _ . _ _

-

1

'

-

l .

12

written above or below the old setting. _Similar changes were

,

indicated for new values for the relay picku) acceptance criteria.  !

! However, no new changes were indicated for tie remaining relay ,

. adjustments that were required as a result of making the initial  !

l setpoint changes. Ap)arently the technicians only made the

! changes that were marced on the attachment. The technician did  :

! not make further adjustments to the remaining relay trip settings,

shich included the time delayed trip settings, as required by the

,

relay data sheet. -

t ,

! Engineering personnel failed to ensure that all data on the relay

i data sheet was changed to the new values. Maintenance personnel *

l transcribed the data that engineering personnel had changed on the  :

relay data sheet into the appropriate procedure attachment.

'

l

'

However, they failed to recognize that engineering personnel did

not make all the required changes. As a result, all required data

, was not transcribed.into the appropriate procedure attachment and ,

l the technician performing the work activities did not have '

l complete information to perform the required changes to all relay  :

settings.

'

'

The inspectors observed from the review of the engineering

evaluation that the licensee concluded that, with the incorrect  :

settings, down stream faults would not result in transformer

! damage. It was also concluded that for a severe internal fault '

'

theincorrectsettingscouldpotentiallyresultingreaterdamaf,e

to the transformer being protected. The transformer would stil ,

'

be damaged by a severe internal fault with the correct relay i

! settings. The licensee concluded that the time delayed setting  :

l

error had no safety significance. {

c. Conclusions  !

l

The inspectors concluded that the calibration of the relays was

'

not performed in accordance with procedure 57CP-CAL-108-15 and the i

i Relay Data Sheet. The improper calibration of the relays was l

identified as an example of VIO 50-321, 366/97-01-01: Failure To j

Follow Procedures - Multiple Examples.  ;

"

The inspectors also concluded that engineering personnel failed to

indicate all required relay setting changes for the work

activities. Maintenance personnel, who revised the procedure

attachment and completed the field work, failed to recognize that  !

the instructions were not complete. These examples demonstrated 1

inattention to detail and a lack of a questioning attitude. The '

,

inspectors concluded that the technicians who identified the  ;

incorrect relay settings were very knowledgeable and demonstrated

an excellent questioning attitude. l

.

'

Enclosure 2

i

, - -

. . . . . __ . . ._. _ - - . - - .-. _ .. .

. .

$

13

M8 Miscellaneous Maintenance Issues (92700) (92902)

M8.1 (Closed) VIO 50-366/96-13-05: Failure to Properly Perform TS

Surveillance 3.6.1.7.3.

The licensee responded to this violation in correspondence dated

December 19. 1996. The inspectors reviewed the res

procedure written for performing the surveillance,and ponse, the

observed

. the successful performance of the procedure on September 17. 1996.

4 Based upon the inspectors review of licensee actions this

'

violation is closed.

M8.2 (Closed) LER 50-366/96-04: Misinteroretation of Recuirements

Results in Missed Technical Soecifications Surveillance.

This item is discussed in paragraph M8.1 of this report. No new

issues were revealed by the LER. This LER is closed.

M8.3 (Closed) LER 50-321/96-13: Personnel Error Results In Missed

Technical Soecifications Surveillances

This item is discussed in IR 50-321, 366/96-14. paragraph 03.1.

3

No new issues were revealed by the LER. The inspectors verified

that the missed TS surveillance was completed for Unit 1 on l

January 29. 1997. following a unit shutdown. This LER is closed. l

III. Enaineerino l

l

El Conduct of Engineering  !

On-site engineering activities were reviewed to determine their

effectiveness in preventing. identifying, and resolving safety

issues, events, and problems.

4 E1.1 Review of Licensee Activities in Resoonse to Generic Letter 95-06:

Assurance of Eauioment Ooerability and Containment Intearity

Durina Desian-Bases Accident Conditions.

On January 27 the licensee issued their 120-day written response

to Generic Letter (GL) 96-06. Assurance of Equipment Operability

'

and Containment Integrity During Design-Bases Accident Conditions.

The licensee identified that containment air coolers may be

susceptible to water hammer and two phase flow, and that some  ;

isolation piping systems that penetrate primary containment may J

over pressurize due to fluid expansion during postulated accident '

conditions.

To prevent water hammer loads on the Unit 2 containment coolers,

the licensee's response indicated that they would prohibit

Enclosure 2

-. - -. . . . .-. . ...

-

.

.

14

operation of the coolers above the expected boiling temperatures

-

following a Loss of Coolant Accident (LOCA) or Main Steam Line

Break (MSLB) event. The inspectors reviewed procedure

31EO-EOP-100-2S; Miscellaneous Emergency Overrides. Rev. 5. Ed 1.

'

and verified that the procedure was revised to prevent operation

of the drywell coolers when drywell average temperature is equal

to or greater than 285 degrees Fahrenheit (F)

In response to the potential for thermally-induced over

pressurization of water filled isolation valves. licensee

representatives indicated that they would drain the Unit 1

demineralized water line between the isolation valves during the

next outage requiring a drywell entry. The inspectors reviewed

licensee actions following the Unit 1 forced outage that began on

January 28 and ended on February 3. The inspectors reviewed

4

procedure 34G0-0PS-028-1S: Drywell Closeout. Rev. 4. and verified

that the procedure contained steps indicating that the draining

, was performed. The steps were included as temporary procedure

3 change 97-16 and indicated that procedural steps to perform the

!

'

draining would be made permanent with the next revision of the

procedure.

l

The inspectors concluded that the licensee was responsive to i

correcting potential problems identified in its system review in  ;

response to GL 96-06.  ;

,

E1.2 Emeraency Diesel Generator (EDG) Switchaear Loaic

a. Insoection Scooe (92903)

As a result of GL 96-01. Testing of Safety-Related Logic Circuits,

corporate engineering discovered that a portion of the 4160 VAC <

emergency switchgear logic had not been tested. The inspectors I

reviewed the ap)licable procedures, monitored licensee activities.

'

.

and discussed t1e problem with engineering and licensee

management.

b. Observations and Findinas

'

1

The inspectors were informed by onsite engineering personnel that i

during the reviews for GL 96-01: Testing of Safety-Related Logic

Circuits, a portion of the logic for the lockout relays for the

six EDG switchgears, three per unit, had not been tested. Part of

the function of the lockout relays is to ensure that during an EDG

start and demand both the normal supply breaker and the alternate '

supply breaker open on their respective emergency electrical

switchgears. The opening of the breakers occurs prior to the EDG

breakers * closing onto their respective emergency switchgears.

Enclosure 2

- .-. . - _. - .- -. -- - -

.

15

i

This )revents the EDG breakers from closing onto an energized

switcigear.

t The portion of the logic that was not tested was the function

involving the opening of the alternate supply breakers. If the

alternate supply breakers failed to open, loads from the safety-

related busses from the EDGs would not be energized. The

inspectors were informed that the Logic System Functional Test

(LSFT) would be changed to test this function and that the revised

LSFTs would be performed during the next refueling outages.

As part of the immediate action, operations management issued

Operating Order Number 00-01-0297S. which states, in part, the

following:

!

Until the relay logic is tested, the following is applicable

to the 4160 VAC emergency busses:

1) Maintain each 4160 VAC emergency bus on the

> normal supply unless plant conditions require

powering it from the its alternate supply.

2) If any 4160 VAC emergency bus must be powered

from its alternate supply, the associated diesel

.

generator must be declared inoperable.

This limitation can be removed for each bus once its-

respective alternate supply breaker trip circuit is tested

satisfactorily.
The inspectors observed that, in accordance with plant procedure,

the Plant Review Board (PRB) concurred with the order on

February 13. 1997. The inspectors discussed operator training for

this problem with licensee training personnel. The inspectors did

-

not find evidence that operators received training for this

particular 3roblem. However, the operators received trair.ing on

numerous otler similar electrical problems. Based upon training

for similar problems and the cuality of electrical malfunction

procedures, the ins)ectors dic not view the lack of training on

-

this particular pro)1em as a safety significant issue.

The inspectors reviewed the licensee's initial response to the GL

dated April 12. 1996. That response stated that a comprehensive

review was performed from 1989 through 1991 to verify that

surveillance procedures properly implemented Technical

Specification (TS) testing requirements. The licensee

representatives also stated they planned to perform a review of

modifications to the logic circuits for the systems that have been

implemented subsequent to the previous review.

l Enclosure 2.

,

_ . _ . . _ . . _ _ _ . _ _ _ _ _ . . _ _ . . _ _ _ . - . . _ _ _ _ _ - . _ . . _ . _ _ .

.

'

t

16

The . inspectors held discussions with engineering concerning the

portion of the logic for the lockout relays for the six-EDG

switchgears that had not been tested and was not discovered during

the initial system logic review. Engineering personnel stated

that the breaker lineup was very unusual and was not considered

during the initial review. Engineering was not aware of

modifications to the system logic that would have initiated

additional reviews.

c. Conclusions

The inspectors' concluded that system logic reviews conducted from

1989 through 1991 failed to identify that a portion of the 4160

VAC emergency switchgear logic had not been tested. This was

considered to be an engineering oversight. Modifications had not ,

occurred to the system logic that would have initiated additional

licensee reviews. The inspectors concluded that the licensee

immediate actions were a)propriate. The licensee was required to

complete the requested G. actions prior to the first startup from

the first refueling outage commencing one year after the date of

the letter (April 1997).

E2 Engineering Support of Facilities and Equipment

.E2.1 Rod Worth Minimizer Mode Unit 1

a. Insoection Scoce (92903)

During the Unit 1 forced outage di.scussed in Section 01.4 of this

report the inspectors observed that the Rod Worth Minimizer (RWM)

was not in the correct Rod Sequence Mode (RSM). The inspectors

reviewed applicable procedures and discussed the problem with

operations and engineering personnel,

'

b. Observations and Findinas

-The inspectors observed portions of the control room activities

for the Unit 1 forced outage on January 29. The inspectors

observed that the RWM commenced enforcing actions for RSM B2. The

unit control rods were in RSM Bl. ,

The inspectors discussed the observation with the Reactor

Engineers (REs) on shift. The inspectors were informed by the REs

that the unit had been in the RSM B2 prior to the last sequence

exchange. The inspectors reviewed procedure 42CC-ERP-011-05:

Control-Rod Exchange, Rev. 8, which provided instructions for

performing control rod sequence exchanges during power operations.

. Section 7.2.28 of the procedure provided instructions for ensuring

that the RWM was changed to monitor the correct RSM.

.

Enclosure 2

[

l

. . - _ . . , - - - - _ . . , , . . . , . . -. - ,

,

17  ;

The inspectors also reviewed procedure 34G0-0PS-001-1S Plant

Startup, Revs. 25 and 29. for Unit 1 and Unit 2. respectively. The

inspectors observed that the procedures contained instructions to

ensure that the RWM was properly selected to the control rod

'

sequence.

The inspectors reviewed procedure 34G0-0PS-005-1S: Power Changes.

Rev. 19. Ed 1, and Rev. 20. Ed 1, for Unit 1 and Unit 2.

respectively. The procedures were used to decrease reactor power

for rod sequence changes at power. The inspectors observed that i

the procedure did not reference any other procedure or provide  !

instructions to ensure that the RWM was properly selected to the

correct rod secuence mode. The inspectors were informed that the  ;

procedure woulc be revised to include the proper guidance. j

The inspectors found from the review of the procedures,

discussions with the REs. and o)erations personnel that there was

no objective evidence that the RWM was changed to the correct RSM

following the previous rod sequence exchange.

c. Conclusions

The inspectors concluded that section 7.2.28 of the control rod

exchange procedure was not performed: or was performed and the RWM

was subsequently changed following the previous rod sequence

exchange. Failure to ensure that the RWM was enforcing the

correct rod sequence mode in accordance with section 7.2.28 of

procedure 24CC-ERP-011-05, is an example of VIO

50-321, 366/97-01-01: Failure To Follow Procedure - Multiple

Examples. The inspectors also concluded that the operating

procedures used to reduce power for rod sequence exchanges while

operating at power, did not require that the RWM be checked for  !

proper RSM.

E2.2 Reactor Pressure Boundary leak Unit 1 Drywell

'

a. Insoection Scooe (37551) (62703) (92903)

Unit 1 was shutdown on January 28 due to an increasing trend of

unidentified drywell leakage caused by a failed weld on a 3/4-inch

vent line. Details of the shutdown are discussed in section 01.4

of this report. The inspectors reviewed the As-Built drawing

S-01286, a hand sketch of a 3/4-inch pipe and half coupling welded

installation, MW0s 1-96-1045 and 1-97-0173. the weld process sheet  !

for MW0 1-97-0173, magnetic particle inspection and liquid

penetrant examination reports. and a Root Cause Analysis. The

inspectors discussed the initial construction installation.

replacement installation, and the repair installation of the vent

piping and valves with various licensee personnel.

Enclosure 2

.

'

.

18

b. Observations and Findinas

The inspectors observed from their reviews and discussions that a

socket weld on a 3/4-inch vent line connected to the Shutdown

Cooling (SDC) suction piping of the Residual Heat Removal (RHR)

system failed.

The inspectors observed that the as-built drawing. S-01286, showed

that the 3/4-inch vent pipe contained two valves in series. The

drawing clearly indicated the dimensions of the original .

construction installation. The distance between the half l

coupling, the location of the failed weld, and the first valve was

approximately two inches. MWO 1-96-1054. which was issued to

replace the vent piping and the two valves during the last Unit 1

refueling outage, did not specify any dimensions between the half

coupling and the first valve or any other dimension. The distance

between the half coupling and the first valve on that replacement i

installation, was approximately ten inches.

The repair installation, completed on January 29, by

MWO 1-97-0173. identified that the distance between the half

coupling and the first valve should be between 4 to 5 inches.

10 CFR 50. Appendix B. Criteria III. Design Control, requires, in )

part, that measures shall be established to assure that applicable

regulatory requirements for those structures, systems, and l

componeiits to which this appendix applies are correctly translated '

into specifications, drawings, procedures, and instructions. In

this case, specific requirements were not translated into

specifications, drawings, procedures, and instructions.

The inspectors observed that the Root Cause Analysis did not

conclusively determine the cause of the failure. Based on plant

history with this type of installation, engineering experience and

judgement, and input from the Architect Engineer, it appears that

the causes of the failed weld were a combination of weld anomaly

or discontinuity and high cyclic fatigue. Engineering experience

and vibration analysis for this particular installation indicated

that neither cause alone would have produced the failure.

Therefore, it is concluded that these factors probably combined to

produce the failure of the pressure boundary.

c. Conclusions

The inspectors concluded that design specifications documented on

Drawing S-01286 were not correctly translated into applicable

instructions for the replacement of the vent piping and valves.

This failure to translate the design specifications was identified

as Violation 50-321/97-01-03: Failure to Translate Original

Design Specifications Into Applicable Instructions.

Enclosure 2

. - - . . - . - - - - . - - . - . - - - . - .-.- - - - . - . _. ..

.

,

,

"

a .

1 i

.

3

'

19

i The inspectors also concluded that the licensee identified the

! most probable cause for the failure. The repair was made with  ;

management oversight, engineering input and quality control

'

.

I inspections, and was under maintenance supervision. 1

E8 Miscellaneous Engineering Issues (92700) (92903)

{

E8.1 (Closed) LER 50-321/96-09: Comoonent Failure Results in Manual  :

Reactor Shutdown.

!

! This LER was issued on June 19, 1996 when both Reactor Feed Pumps .;

on Unit 1 tripped. This problem was discussed in IR

'

,

! 50-321. 366/96-07. A capacitor shorted in a circuit board and )

- damaged the power supply for the logic systems. A less than 4

adequate design contributed to the event. Modifications to the  !

i systems will be performed during the next scheduled refueling  !

outages for both units. Based on the inspectors' review of l
licensee actions this LER is closed. 1

l

IV Plant Support

4

l R1 Radiological Protection and Chemistry Controls

i R1.1 Observation of Routine Radioloaical Controls

a. Insoection Scoce (71750)

l

'

.

General Health Physics (HP) activities were observed during the

i report period, including locked high radiation area doors. ) roper

radiological posting, and personnel frisking upon exiting tie

Radiological Controlled Area (RCA). The inspectors made frequent

! tours of the RCA and discussed radiological controls with HP

j

,

technicians and management. No deficiencies were identified.

I R1.2 Health Physics Control of Personnel Access to Unit 1 Drywell

4

j a. Insoection Scooe (71707) (71750)

, On January 29. the inspectors conducted a tour of the Unit 1

!

Reactor Building. The areas toured were the 130-foot elevation

and the 106-foot elevation of the northeast di gonal. Included in

this tour was the HP station that was setup for personnel entry

2

into the Drywell for the Unit 1 forced outage.

Observations and Findinas

'

b.

,i

^

The inspectors observed HP control for personnel access to the

drywell for scheduled work activities. HP personnel revealed
through conversation with the inspectors that they were

i

i Enclosure 2

.

_

'

.

20

knowledgeable of their job functions, security access requirements

to the drywell, and the work activities being performed.

The inspectors observed excellent use of three-part communications

by Plant Equipment Operators (PEOs) performing work activities

near the HP station.

c. Conclusions

HP control was excellent for drywell entry during the forced

outage on Unit 1. Observed PEOs* use of three-part communications

as excellent. Overall housekeeping on the 130-foot elevation and  !

che 106-foot elevation of the of the northeast diagonal was '

satisfactory.

R2.1 Insoection of Self Contained Breathina Aooaratus (SCBA)

a. Insoection Scooe (71750)  !

The inspectors reviewed procedure 62RP-RAD-003-0S: Use and Care of i

Respirators. Rev. 7. Ed 1. and observed a portion of the monthly i

inspection of Self Contained Breathing Apparatus (SCBA) equipment i

located in the main control room. The inspectors also reviewed

procedure 73EP-INS-001-OS: Emergency Equipment Inventory. Rev. 1.

b. Observations and Findinas

On February 12. the inspectors observed the inspection of SCBA

equipment by a Radiation Protection Technician. The technician

performed the inspection in accordance with the SCBA Monthly

Inspection Checklist. The checklist is an attachment to

Procedure 62RP-RAD-003-05.

The inspectors observed that 10 SCBAs were located in the Control

Room with 32 spare air cylinders. The inspectors observed the  :

inspection of a representative sampling of SCBAs in the Control

Room. The inspectors documented in Inspection Report

50-321. 366/96-15 that corrective lenses were available in the

control room for operators' use during emergencies that may

require the wearing of an SCBA.

The inspectors reviewed the documentation for the monthly

inspection of SCBAs used for radiological conditions. The

inspectors observed that 10 SCBAs with 32 spare bottles were

ins)ected in the Control Room. 10 in the Operation Support Center

witi 10 spare bottles and 2 SCBAs in the Technical Support Center.

All SCBAs and the spare bottles were acceptable. These numbers

satisfied the SCBA and spare bottle requirements for the Emergency

Plan (EP). as specified in procedure 73EP-INS-001-0S. The

inspectors also observed from the inspection documentation of the

Enclosure 2

_ _

-

_- _ . . . . ___ _ _ _ _ _ __-- _._. _. _ _ - - _-_ . - - - . -

'

'

.

l

! 21

23 SCBAs on the 112-foot elevation of the Control Building that

the SCBAs were acceptable. These SCBAs are not required by the

EP.

'

c. Conclusion

l

The representative sam) ling of SCBAs by licensee personnel

determined that the SC3As were functional and met procedural

acceptance criteria. The technician performing the sam) ling was  ;

l conscientious and knowledgeable about the equipment. 0) served

'

calibration sticker.s were current. The requirements of the EP, j

with respect to the number of SCBA units and spare bottles

available, were maintained.

l

i

'

P1 Conduct of Emergency Preparedness Activities

l Pl.1 EP Staff Auamentation Crill

a. Insoection Scooe (40500) (71750) (82301)

l

On February 4, the licensee conducted an off normal working hours  ;

Emergency Preparedness Staff Augmentation Drill. The drill was  ;

conducted to assess the ability to augment the existing onsite '

staff for a selected group of emergency response positions within

approximately 60 minutes from a simulated emergency during off ,

normal working hours. The drill required personnel to respond to

questions related to whether or not they were fit for duty and the

estimated time they would require to be able to report to the

site. Actual response to the site was not required. The '

,

inspectors reviewed the Emergency Plan, licensee documentation and

l assessment for an Emergency Plan Staff Augmentation Drill, and

participated in the performance of the drill.

b. Observations and Findinas

,

l The inspectors reviewed Table B-1, Minimum Staffing Ca)acity For l

l Emergencies, of the Emergency Plan and observed from tie results  ;

i of the licensee's documentation that the number of drill responses t

did not meet the requirements of Table B-1, i'able B-1 indicated  !

that a total of seven HP technicians was' required for minimum .

L

'

manning for the Internal Radiological Emergency Team (IRET). In

this case, four personnel were on shift and three additional  !

personnel that were required to meet the minimum staffing within  :

approximately 60 minutes, were not contacted. i

! The-licensee's initial assessment of the problem indicated that  ;

I

miscommunications between the Technical Su) port Center (TSC) i

!

HP/ Chemistry supervisor and the security slift captain resulted in .

a failure to initiate the required callout list

t

Enclosure 2 i

i

!

i

! ,

,. - _ ,

. _ _ , _ _ _ _ _ - _ _ _ _ _ _ _ . . . _ _ _ . ~ _ _ _ _ . _ . __ . _ _ .

'

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.

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22

Other deficiencies during the drill included a failure of the

Emergency Operations Facility (EOF) Support Coordinator and

Technical Support Center (TSC) Engineering Supervisor to complete l

their callout list. As a result, several . support positions were

not filled. The licensee documented the deficiencies and

initiated actions to complete a root cause determination. The

investigation was ongoing at the end of the inspection report

period.

On February 18. as part of the licensees corrective actions, a i

second Staff Augmentation Drill was conducted. The staff

augmentation satisfied the requirements of Table B-1. Minimum

'

Staffing Capacity For Emergencies, of the Emergency Plan, although  ;

some additional improvement items were identified.

c. Conclusions i

'

The inspectors concluded that the Emergency Preparedness Staff

Augmentation Drill conducted February 4, was not successful as

,

'

described in the Emergency Plan. Although some items for

im)rovement were identified during a second drill conducted on i

Fe]ruary 18. all Emergency Plan requirements were met. .The  ;

licensee initiated appropriate measures to determine root cause j

and develop corrective actions. j

S1 Conduct of Security and Safeguards Activities  !

'

,

I

! a. Insoection Scooe (92904) (40500)

l

l The inspectors reviewed the appropriate procedures and assessed ,

'

the licensees activities associated with the detection of an i

unattended security weapon.  !

b. Observations and Findinas

L

On February 19 the inspectors were informed that a security  !

supervisor had discovered a security weapon that was unattended.  !

The weapon was located inside a compensatory post structure  :

located within the protected area.  !

The inspectors were aware that a similar. situation occurred in t

August 1995. The ins)ectors discussed this problem with security i

management to gain.a Jetter understanding of the most recent  !

discovery. The inspectors were informed that about 12:12 a.m. on  !

i

February 19. a compensatory post was established due to poor  :

r

'

visibility in that general area. When the compensatory post was

secured at about 3:46 a.m., the weapon was not removed from the  !

'<

post and returned to the designated storage location. Security

supervision discovered the weapon during a routine tour of the

. compensatory post at about 1:58 p.m. on February 19.

- ,

Enclosure 2 j

4 ,

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i

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. . . _ _ _ ___ . _ _ _ _ _ _ _ _ . . _ . _ _ - _ . - _ _ - _ _

,

. ,

e

. i

i

i  :;

1

i 23 4

l The inspectors reviewed procedure 82SS-SEC-022-5S: Security l

Department Equipment Inventory, Rev. 2, and observed that the

procedure required an equipment inventory at a designated

,

i

-

frequency. The inspectors reviewed procedure 82SS-SEC-027-5S:  !

j Compensatory Officer Turnover Report, Rev. 4, which referenced

. Security Operations Order 96-01, dated January 31, 1996. The

"

,

Security Operations Order, which was implemented as part of.the

. corrective actions following the unattended weapon situation that  :

'

occurred in August 1995, required security personnel to conduct a

?

" hands on" (touch) inventory of security weapons at a designated

frequency. In this case, on five different occasions, the

.' weapons * touch inventory was not conducted and the unattended  ;

-

weapon was not detected.  !

,

c. Conclusions

4

The inspectors concluded that failure to conduct the required

equipment inventory was a failure to follow security procedure and

was identified as an example of VIO 50-321, 366/97-01-01: Failure

l to Follow Procedure - Multiple Examples.

S2 Status of Security Facilities and Equipment (71750)

The inspectors toured the protected area and observed that the

l' perimeter fence was intact and not compromised by erosion or

disrepair. The fence fabric was secured and barbed wire was

angled as required by the licensee's Plant Security Plan (PSP).

i

Isolation zones were maintained on both sides of the barrier and

were free of objects which could shield or conceal an individual.  ;

The inspectors observed that personnel and packages entering the

i protected area were searched either by special purpose detectors

- or by a physical patdown for firearms, explosives, and contraband.  !

! Badge issuance was observed, as was the processing and escorting  !

of visitors. Vehicles were searched, escorted. and secured as i

described in applicable procedures.  !

[ The inspectors concluded that the areas of security inspected met

the applicable requirements.

,

)

h F1 Control of Fire Protection Activities

i F1.1 Review of Transient Combustible Fire Loads

! i

, a. Insoection Scooe (71750) I

'

The inspectors reviewed procedure 40AC-ENG-008-05: Fire Protection

Program Rev. 8. Unit 1 and Unit 2 Fire Hazards Analysis (FHA),

and toured portions of the plant to verify proper implementation

) .of the procedures.

1

[ Enclosure 2

.

._ ,

_ _ . _ - - _ _ _ __

'

.

.

24

i b. Observations and Findinas

On February 12. the inspectors observed approximately 40 to 45

metal 55-gallon drums stored at the 112-foot elevation of the

control building. Labels on the drums indicated they contained

used oil, oil-water mixture, and oil sludge. The inspectors

reviewed the Unit 1 and Unit 2 FHA. Section 8.0. figure 7. and

observed that the location of the stored drums was in fire

zone 0007A.

The inspectors were informed by fire protection personnel that the

maximum fire loading for fire zone 0007A was about 420 gallons of

! oil. Due to the oil-water mixture in the drums the inspectors

were not certain how many gallons of oil existed in the drums.

The inspectors concluded that a maximum of eight full drums of

waste oil would exceed the maximum fire loading for the fire zone.

The inspectors were later informed that about 15 drums

(675 gallons) of oil existed in the oil-water mixture and that the

maximum fire loading of the fire zone was exceeded. The

inspectors observed that the fire zone was monitored by a fire

detection system but contained no fire suppresun system. Fire

suppression systems were located in the general vicinity.

The inspectors observed that procedure 40AC-ENG-008-0S, J

step 8.1.2.2. stated, in part, that unattended storage of any

! transient fire load in a safety-related area would require a i

transient combustible permit (TCP). The procedure step indicated

that the Control Building was a safety-related area. A discussion

with a fire protection engineer and a review of current TCPs  ;

revealed that no TCP was issued for the waste oil located in fire '

'

zone 0007A. The inspectors concluded that the unauthorized

storage of the waste oil in fire zone 0007A was a violation of l

, plant procedures and the FHA.

,

Section 3.5.3 of the FHA stated, in part, that administrative ,

! controls require all movement of transient combustibles in safety- 4

related structures to be approved by site fire protection

'

personnel. However, in this case, fire protection personnel did

not review the additional fire loading condition or issue a TCP..

l The inspectors observed that step 8.1.2.10 of procedure

, 40AC-ENG-008-0S stated, in part, that a record of approved TCPs

'

will be maintained by the issuer and that the computer program

represents the approved tracking system. The ins)ectors obtained

a list of 120 TCPs that were on the approved traccing system and

'

observed that 81 indicated that the TCP had expired. The

inspector.s discussed this problem with fire protection personnel.

The inspectors observed that the computer tracking system

maintained a running total of TCP fire loading until the TCP is

actually deleted from the tracking system. As a result the

Enclosure 2

i

l

l

--- - -- - ~_- . _ - . - _ _ - - - - . - - - - . . -

'

,

.

A

!

25

additional fire loading indicated on the expired TCPs was being -

taken into account for total fire loading in the specific fire

zone. All errors were in the conservative direction and presented

no safety significant prcblem. However, procedural steps were not

being performed to ensure that the TCP forms were completed and

turned in to appropriate personnel for proper tracking and  :

closure.

The inspectors were later informed that a fire watch had been  :

posted at the drum storage location and plans were being developed

to move the drums to one of two approved storage locations to

.

await proper disposal. An event review team (ERT) was initiated

l to review the problem and make recommendations ts prevent

recurrence.

,

c. Conclusions

The inspectors concluded that the unauthorized storage of the

40 to 45 drums of waste oil, oil-water mixture and oil sludge in

fire zone 0007A was a violation of plant- procedures and the FHA.

'This was identified as an exam)le of VIO 50-321. 366/97-01-01:

Failure To Follow Procedure - iultiple Examples.

l The inspectors also concluded that the administrative aspects of

!

the TCP process had deteriorated since the inspectors documented

similar deficiencies in-IR 50-321, 366/96-06. The administrative

aspects of the TCP process were identified as a weakness in the

fire protection program.

F1.2 Resolution of Thermo-Lao Fire Barrier Issue

a. Insoection Scooe (54704)

i

The ins)ectors reviewed the action taken to resolve the degraded

! Thermo _ag fire barrier issue at Hatch to determined if the

! licensee's action was consistent with commitments made to the NRC.

b. Observations and Findinas

g In 1991, the NRC identified that Thermo-Lag fire barrier material i

did not perform to the manufacturers specifications. NRC

'

Bulletin 92-01. " Failure of Thermo-Lag 330 Fire Barrier System to

Maintain Cabling in Wide Cable Trays and Small Conduits Free from

l Fire Damage," was issued which requested licensees with Thermo-Lag '

'

fire barriers to consider these fire barriers to be degraded and

-

take ap3ropriate compensatory measures- for the areas where the ,

Thermo _ag fire barriers were installed.

'

During 1993 and 1994, the licensee evaluated the results of data

,

from various tests performed by the nuclear industry on Thermo-Lag l

}

'

Enclosure 2

i

.

26

fire barrier installations. Based on the unfavorable results of

these tests, the licensee develo)ed a plan to eliminate the

reliance on Thermo-Lag for fire Jarriers at Hatch. A safe

shutdown methodology re-analysis was performed to identify the

components required for plant shutdown following an Appendix R

fi re. The plan specified the separation to be provided between  !

safe shutdown components to meet the separation requirements of '

10 CFR 50. Appendix R.Section III.G. This separation was to be  ;

provided by either rerouting cables or by the installation of.

additional fire walls. As of the date of this inspection, the  ;

licensee had initiated the implementation of this plan and most of t

the previously installed Thermo-Lag fire barrier materials had .!

been removed.  :

Initially, approximately 5.000 linear feet of electrical cable  ;

raceways were enclosed by Thermo-Lag fire barriers. Also, two '

fire walls of approximately 600 square feet were constructed of l

Thermo-Lag to separate redundant components. All of this ~

Thermo-Lag material had been removed, except' for the two fire

walls and the Thermo-Lag on approximately 300 linear feet of

electrical raceways. The licensee's re-analysis resulted in

approximately 10.000 linear feet of cable being re-routed.

The remaining Thermo-Lag installations are scheduled to be removed

and new fire walls constructed during 1997 and 1998. The

licensee's-letter to the NRC. dated March 28. 1995. stated that

the Thermo-Lag issue at Hatch would be resolved by the startup

from the Unit 2 Fall 1998 refueling outage. The NRC's response to-

this letter of June 29, 1995, indicated that this-schedule was

acceptable and requested that the licensea advise the NRC when the

modifications were completed. The current licensee's schedule

indicates that these modifications should be completed by the

Sumer of 1998.

In~the areas in which Thermo-Lag had been removed but electrical  ;

cables had not been rerouted or redundant components were not

provided with appropriate separation, the licensee was providing a

one-hour fire watch patrol to meet the compensatory measures of

the FHA. Section 9.2. Aopendix B. A discussion-of the fire watch

' program at Hatch is addressed in Sections 04.1 and F3 of this

report.

c. Conclusions ,

!'

The licensee was taking appropriate action to resolve the Thermo-

Lag issue at Hatch. i

!

Enclosure 2 ,

i

. . . . _ _ _ . _ . _ _ _ . _ . _ . . _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ . . . _ .

,

,

. i

'

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27  !

!

,

F1.3 Kaowool Fire Barrier Installations  !

( a. Insoection Scooe (64704) l

l The inspectors reviewed the application of Kaowool for fire ,

'

barriers at Hatch to determined if this application met the NRC's l

requirements and the licensee's commitments. i

b. Observations and Findinas  !

The inspectors reviewed request for engineering assistance

l (REA) HT-93630: Engineering Evaluation of Kaowool. This REA was 3

Jerformed to determine the minimum requirements for Kaowool at {

latch. This evaluation determined that Kaowool was installed for  !

the following three reasons:  :

-

To provide physical separation of redundant divisional i

raceways to meet the provisions of NRC Regulatory Guide

1.75.

-

To help reduce the combustible loadirg of specific plant I

areas. This was a commitment to the NRC during the fire

protection review of Hatch prior to the-issuance of 10 CFR

50 Appendix R.

-

To meet an Apaendix R exemption request for the Intake ,

Structure. T1e electrical cables ~ installed at the intake '

structure were enclosed within a Kaowool barrier in lieu of

3roviding automatic fire suppression for the entire

au11 ding. A closed head automatic water spray system was

provided for each service water pump.

The licensee's evaluation resulted in the development of a program

to maintain the Kaowool installations where required. Site

drawings were being revised to clearly indicate the electrical

raceways in which Kaowool was required. A program was being

developed to remove the Kaowool from accessible raceways where

this material was no longer required. The licensee stated that

all required Kaowool was to be properly maintained to perform its

design puroose.

In late 1996 following the idertification of installation

problems with Kaowool fire bari er installations at the Farley

Nuclear facility, the licensee performed Audit 97-SA-1 af the

l Kaowool fire barrier installations at Hatch. This audit found the

installation and surveillance program for Kaowool at Hatch to be

adequate. However, the Kaowool fire barriers in several plant-

, areas were noted to be damaged, indicating an apparent need for

'

the )lant staff to have an increased awareness as to the function

of t1is material. The audit report identified this issue as

! Enclosure 2

.

.

28

noncompliance finding AFR 97-SA-1/1. At the conclusion of this

inspection, this issue was being evaluated by the licensee to

determine the appropriate corrective action.

During plant walkdown inspections, the ins)ectors also noted

several areas containing damaged Kaowool tlat appeared to need

repairs. The licensee provided information that the identified

damaged Kaowool in these areas was no longer required for fire

protection.

c. Conclusion

Although damaged Kaowool assemblies were noted in several areas of

the plant, the Kaowool installations provided to meet NRC fire

protection requirements were properly maintained.

F2 Status of Fire Protection Facilities and Equipment

F2.1 Repairs to Fire Main Buried Pioe

a. Insoection Scooe (71750) (62707)  ;

The inspectors reviewed the applicable procedures. observed the

repair activities performed on a broken section of buried Fire ,

Main pipe and discussed the problem with licensee personnel. ]

.

'

b. Observations and Findinas

The inspectors identified from licensee documentation that on

January 19. 1997. the electric fire pump started on low pressure.

After the operators secured the electric fire pump, the jockey

pump would not hold pressure and the electric fire pump restarted.

Operators walked down the system piping and identified a fire main

header leak near the 20 Startup Transformer.

The inspectors observed, reviewed. and discussed with the licensee i

the activities associated with the repair of the Fire Main piping.

The craft personnel used procedure 450C-MNT-001-0N: Excavation and

Earth Work Quality Control. Rev. O, to remove the soil and uncover

the damaged piping in the area of the leak. The repairs consisted

of removing and re) lacing the section of damaged pipe. A coupling l

was used to mate tie old pipe with the new.

The inspectors reviewed the clearance. the compensatory fire

protection actions, and the system restoration. The clearance was

adequate with the applicable valves closed and tagged. The

l

compensatory fire protection actions were detailed and included

l the use of a towed trailer, on which was equipment with a header

manifold, valves, pressure indicators, and numerous lengths of

'

fire hoses. Temporary connections were made to a fire hydrant

Enclosure 2

l

._ .

.

t

29

located outside the clearance boundary and fire hoses were lined

up to the diesel building.

The inspectors observed that the system restoration was performed i

correctly. Following the repairs the inspectors did not observe

any leakage form the repaired section of piping.

c. Conclusions

The inspectors concluded that the repair activities were performed

in accordance with approved procedures with supervisory oversight

and engineering support. The system clearance, compensatory fire

protection measures, and system restoration were satisfactory. No

deficiencies were identified.

F2.2 Ooerability of Fire Protection Facilities and Eouioment

a. Insoection Scoce (64704)

The inspectors reviewed the maintenance history, open maintenance  !

work orders on the fire protection system, station deficiency

cards, and operations' list of out of service fire protection '

l equipment to determine performance trends. The fire protection i

!

'

systems were inspected to determine the material condition of the  !

plant's fire protection systems, equipment, and features. l

b. Observations and Findinas

Maintenance of Fire Protection Eauioment and Comoonents:

! As of January 21, 1997, a total of 21 work requests related to

!

fire protection components were open. These open work recuests

involved minor corrective maintenance work items which dic not

l affect the operability of the components. Of these work requests.

! 14 had been issued since December 1. 1996. Eight were issued in

1996 three in 1995, one in 1994, and one in 1993. The inspectors

concluded that there was no significant backlog of fire protection

maintenance items and that corrective maintenance was performed on

degraded fire protection components in a timely manner.

A review of the deficiency cards (DC) issued on fire protection

i

related discrepancies indicated that the licensee had a very low

,

threshold for the identification of fire protection related

deficiencies. The inspector's review of the deficiencies issued

for 1995 and 1996 indicated that these items had been assigned

appropriate corrective action and were being resolved in a timely

manner.

Enclosure 2

1

_

. _ _ , _ _ _ . _ _ _ _ _ _ _.___ _ .- _ _ _ s

.

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!

30

As of January 27, 1997. Operations' list of fire protection '

components out of service included only the degraded Thermo-Lag

fire barriers, one Kaowool fire barrier, and two penetration

seals. _ The licensee had assigned the appro)riate compensatory ,

measures, consisting of an hourly fire watc1 patrol for these

degraded fire protection features as required by the FHA. ,

The hourly fire watch 3atrols were assigned to non-licensed )lant

equipment operators. iowever. Procedure: 31G0-0PS-011-05. FiA

Operating Requirements. Rev. O. did not require that the date and i

time of each fire watch patrol be recorded or documented in order i

to verify that the fire watch patrols were actually being

performed. Additional information on this issue is included in

Section 04.1 and F3 in this report. .

NRC InsSection Report No. 50-321. 366/96-07 included the results  !

of an NRC review on a number of breaks in the fire protection  !

underground water supply piping. This review concluded that the  !

licensee had prioritized the work in repairing these leaks and

that the efforts to control leaks in the underground fire mains

were reasonable. Since that report, two additional leaks have i

occurred. One. leak was in a sup)1y pipe to a fire hydrant in the  ;

transformer yard. The other leac was in a 10-inch supply main l

near.-the fire pum) house. The licensee's evaluation determined l

that the most pro)able cause of these leaks was erosion due to

aging. These leaks were not of a significant magnitude to

implement any additional corrective action. However, the licensee j

planned to continue to monitor the system for future problems.

There have been approximately seven leaks within the past three

years which required major work. Based on this low number of

leaks the licensee's actions in this area continued to be

reasonable.

The inspectors toured the plant and noted that, with the exception

of the licensee identified degraded fire protection component, the

systems were operational, material condition was very good, and ~

the components well maintained.

Fire Briaade Eauioment:

The fire brigade turnout gear was stored on the 146-foot elevation

of the control building and in a fire equipment building located

outside the power block, adjacent to the fire pump house. A total l

of 46 complete sets of turnout gear, consisting of coats, pants, i

boots. helmets etc. , were provided. Normally, a maximum number l'

of approximately 20 fire brigade members can be expected to

respond in the event of a fire or other emergency. The inspectors

concluded that a sufficient number of sets of turnout gear was

provided.

I

Enclosure 2

. _ __

. _ _ . . ._. . . _ . - _ . . _ _ _ _ _ _ . _ _ . _ _ _ _ _ . _ _ . _ . ._ _ . . _ . . _ _ . _ . .

'

t

I

r

l 31  ;

l t

During previous emergency exercises, the fire brigade personnel

L had experienced problems in the receipt and transmission of radio

. messages. To correct this problem, an enhanced radio and battery

l. maintenance program had been implemented. .In addition, the radio  :

L batteries were being replaced every 120 days with batteries which j

had been completely discharged and recharged. These changes  :

'should assure that the fire brigade radios will be operable in the

l event of an emergency.

<

The fire brigade was provided with a motorized panel truck fully )

p . equipped with fire hose, nozzles, self-contained breathing

!

a)paratus and miscellaneous fire fighting equipment for use inside j

t1e protected area. In addition, a trailer equipped with fire  !

hose, fire nozzles, and miscellaneous fire fighting equipment was  !

provided outside the protected area. This trailer was available j

for use both inside and outside of the protected area.  !

The fire brigade equipment was properly stored and was well l

l maintained.  ;

c. Conclusions

t

Based'on the inspectors' review of maintenance records and .i

inspection of the fire protection components the inspectors j

concluded that there was not a significant maintenance backlog on  ;

the fire protection systems. In addition, the material condition  !

of the fire protection components, including the fire brigade i

equipment, was noted to be very 900d,

F2,4 Surveillance of Fire Protection Features and Eauioment

1

a. Inspection Scooe (64704)

j

'

The inspectors reviewed the following completed surveillance and i

test procedures:

-

42SV-FPX-002-05 Revision 6, Low Pressure C02 System

Surveillance Test (Annual). Completed October 10, 1996.

-

42SV-FPX-008-0S, Revision 0. Water Suppression System Flow

Test (3 Years). Completed May 17, 1996.

-

42SV-FPX-036-0S, Revision 2. Annual Fire Pumps Capacity

Test. Completed June 25, 1996.

i -b. Observations and Findinos

!

'

The completed surveillance tests of the fire protection systems

i reviewed by the inspectors were fcund to be well written and

j satisfactorily completed. The data obtained and recorded for each

1

l Enclosure 2

i

1

i

._ ..,_.._ , - - - _ _ . _ . . _ _ _ , ,

--. .-- - . - ..- . - . - .. .~ - - - - - .- .. - . . . - . . - -

'

.

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32

fire pump included multiple points on the pump curve to verify "

pump performance. The completed test procedures included an i

evaluation of the test results by the site fire protection system  ;

engineer.

c. Conclusions ,

Appropriate surveillances and tests were being performed on fire I

protection features and systems. Appropriate evaluations were '

.also performed on the completed test results by the engineering

group. ,

F3 Fire Protection Procedures and Documentation

l

'

a. Insoection Scooe (64704)

The inspectors reviewed the following procedures for compliance

with the licensee's requirements and guidelines:

-

40AC-ENG-008-0S, Rev. 8. Fire Protection Program  !

-

42FP-FPX-007-0S. Rev. O. Hot Work

-

DI-FPX-02-0693N. Rev. 3. Fire Fighting Equipment Inspection j

-

31G0-0PS-011-0S. Rev. O. FHA Operating Requirements

Plant. tours were performed to determine procedure compliance.

b. Observations and Findinas i

Procedure 40AC-ENG-008-OS and 42FP-FPX-007-0S established the i

administrative guidance used to implement the fire protection

program at Hatch. These procedures contained the requirements for ,

the control of combustibles. ignition sources, and fire brigade ,

organization and training. The procedures were satisfactory and

met the licensee's commitments.

!

The inspectors performed plant tours and noted that the  !

implementation of the site's fire prevention program for the

control of ignition sources, transient combustibles, and general

housekeeping was good, except as discussed in Section F1.1. for ,

the inappropriate storage of combustible liquids on the 112-foot

'

elevation of the Control Building.

The operability and surveillance requirements for the fire

)rotection systems and components previously located in the TSs

, lad been removed from the TSs and incorporated into the FHA. The

i inspectors reviewed the FHA and concluded that these requirements

!

were essentially the same as those previously listed in the TSs.

Enclosure 2 i

!

1

- -

-. ._ _.. . - . _ _ _ - -

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33

FHA Section 9.2. Appendix B. Item 1.1.1, requires inoperable fire

barrier assemblies to be repaired and restored to operable status

within 14 days or a special report is required to be submitted to

the licensee's Safety Review Board (SRB) within the next 30 days.

.

The licensee currently submits special reports only for degraded

4 fire protectDn components that could be directly related to an

Appendix R safe shutdown issue. Special reports were not being

provided for degraded fire protection components required to be

operable by the FHA but which were not directly related to an

Appendix R safe shutdown issue.

For example, two degraded penetration seals have existed in the

three-hour fire wall separating the control building from the east

cable way on the 112-foot elevation since November 3, 1995. This

fire wall is required by the FHA to separate the fire hazards in

the east cable way from the safety-related functions in the

control building. The licensee had implemented the appropriate '

compensatory measures for these degraded fire barrier  !

penetrations. The licensee did not consider that this degraded i

fire barrier warranted a special report since this fire wall did  !

not separate redundant safe shutdown components.

The licensee's failure to issue a special report on the degraded

fire barrier penetrations on the 112-foot elevation of the control

building. as required by FHA, Section 9.2. Appendix B, is

identified as VIO 50-321. 366/97-01-04: Failure to Submit Special

Report on Degraded Fire Barriers.

c. Conclusions

The fire )rotection program implementing procedures were adecuate I'

and met tie commitments to the NRC. However the procedures cid

not require adequate documentation to demonstrate that the fire j

watch patrols required for degraded or inoperable fire protection  !

components were actually being performed. The licensee's policy

of not submitting special reports to the SRB for any degraded fire

protection components listed in the FHA was identifled as a

violation.

F5 Fire Protection Staff Training and Qualification

a. Insoection Scooe (64704)

The inspectors reviewed the fire brigaue organization and

training, and the site's fire fighting preplans for compliance

with the facility's fire protection program and the NRC guidelines

and requirements.

Enclosure 2

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b. Observations and Findinas ,

The organization and tra-ining requirements for the plant' fire

brigade were established by Procedure 40AC-ENG-008-0S.

Section 8.2. The fire brigade for each shift was composed of a

fire brigade leader and at least five brigade members from -

operations. Additional brigade members were also provided from  ;

maintenance and health physics. The fire brigade members supplied

from operations met the minimum NRC five-man fire brigade staffing

rec uirements. The remaining fire brigade members provided ,

adcitional support. The fire brigade leader was a shift  !

supervisor or shift support supervisor. The other members from

operations were plant equipment (non-licensed) operators.

Each fire brigade member was required to receive initial. .

quarterly, and annual fire fighting related training and to '

satisfactorily complete an annual medical evaluation with

certification for participation in fire fighting activities. Each

member was required to participate in one announced training drill

per quarter. One of the drills conducted each year for each shift

was unannounced.

As of the date of this inspection, there was a total of 32

operations fire brigade leaders. 48 fire brigade members from

o)erations and 42 members from maintenance and heath physics on

tie plant's fire brigade .

The inspectors reviewed the training and medical records for the

fire brigade members and verified that the training and medical

records were up to date.

During this inspection the inspectors did not witness a fire

brigade drill. However, the drill results from the unannounced ,

drills conducted in 1996 were reviewed. These drills had been

reviewed by the licensee and were considered satisfactory. The  !

inspectors noted that a drill critique was performed following the

drills to discuss identified weaknesses.

c. Conclusions

The fire brigade organization and training met the requirements of

the site procedures. Performance by the brigades during the 1996

unannounced drills was satisfactory.

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F7 Quality Assurance in Fire Protection Activities

a. Insoection Scoce (64704) ~!

The following audit and self assessment reports were reviewed: ,

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QA Audit 96-FP-1 Annual / Biennial Fire Protection Audit of

March 11-22, 1996

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OA Audit 95-FP-1 Annual / Triennial Fire ' Protection Audit of

May 22 - June 9, 1995 ,

p b. Observations and Findinas

The QA audits of the' site'.s fire protection program were

, comprehensive and identified a number of findings and observations

i to enhance the facility's fire protection program. The inspectors

'

reviewed the audit findings from each OA report and the corrective

actions taken on the identified discrepancies. These items had

been resolved.

c. Conclusions

The audits and assessments made of the facility's fire protection

program were thorough and appropriate corrective actions were

taken to resolve the identified issues. '

F8 Miscellaneous Fire Protection issues

F8.1 Fire Protection Related NRC Information Notices (64704)

l

The inspector reviewed the licensee's evaluation for the following

NRC Information Notices (IN):

-

IN 92-18. Potential Loss of Shutdown Capacity During a

Control Room Fire I

!

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IN 92-28. Inadequate Fire Suppression System Testing

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IN 93-41. One Hour Fire Endurance Tests Results For Thermal

, Ceramics, 3M Company FS 195 and 3M Company E-50 Interam Fire  ;

j- Barrier Systems

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IN 94-28, Potential Problems with Fire Barrier Penetration

Seals l

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IN 94-31. Potential Failure of WILCO. LEXAN-Type HN-4-L.

Fire Hose Nozzles 1

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IN 95-36. Emergency Lighting

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!

The licensee's evaluations and corrective actions for these ins  !

were appropriate, except for IN 92-18. The licensee's initial '

evaluation of IN 92-18 completed May 15, 1992, was very limited.  !

On November 25, 1996, the licensee initiated an engineering i

request to perform a reanalysis of IN 92-18. This reanalysis was

in the initial stages of implementation and was scheduled to be

completed during the Summer of 1997. i

,

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V. Manaaement Meetinas

X.1 Management Changes

On February 19. 1997, the licensee announced the following

management changes that were effective immediately: 1

-

H.L. Sumner, from General Manager Plant Hatch to Vice- )

President, Plant Hatch

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P.H. Wells, from Assistant General Manager-0perations to l

General Manager. Plant Hatch i

-

J.A. Betsill, from Nanger-0perations to Assistant General

Manager-0perations, Plant Hatch -!

-- D.R. Madison, from Superintendent-on-Shift to Manager- i

Operations. Plant Hatch _;

,

X.2 Review of UFSAR Commitments

A recent discovery of a licensee operating its facility in a

manner contrary to the Updated Final Safety Analysis Report

(UFSAR) description highlighted the need for a special focused

review that compares plant practices, procedures and/or parameters

to the UFSAR description. While performing the ins)ections

discussed in this re) ort, the inspectors reviewed t1e applicable

portions of the UFSAR that related to the areas inspected. The ,

inspectors verified that the UFSAR wording was consistent with the '

observed plant practices, procedures, and/or parameters.

X.3 Exit Meeting Summary

The inspectors presented the inspection results to members of the

licensee management at the conclusion of the inspection on

,

March 4, 1997. The license acknowledged the findings presented.

An interim exit was conducted on January 31. 1997.

The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No

proprietary information was identified.

Enclosure 2

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X.2 Other NRC Personnel On Site  ;

On January 23 and 24. Mr. H.N. Berkow. Director. Project

Directorate II-2 and Mr. K. N. Jabbour. Senior Project Manager, i

Project Directorate II-3 and on February 11. Mr. J. R. Johnson.  ;

Director. Division of Reactor Projects and Mr. D. M. Collins.

Deputy Director (Acting). Division of Reactor Safety, conducted a

pre-Systematic Assessment of Licensee Performance visit to the  ;

site. They met with licensee management and supervisors to

discuss plant performance, licensee initiatives, and regulatory <

issues. They also toured various areas of the plant and discussed '

plant status and equipment performance with operations and craft

personnel.  ;

.

PARTIAL LIST OF PERSONS CONTACTED 4

Licensee

Anderson, J., Unit Superintendent

Betsill . J. , Assistant General Manager - Operations '

Coggin. C. . Engineering Support Manager '

Curtis. S. Unit Superintendent i

Davis. D., Plant Administration Manager '

Fornel. P., Performance Team Manager  !

Fraser. 0. Safety Audit and Engineering Review Supervisor j

Hammonds J., Operations Support Superintendent

Kirkley. W., Health Physics and Chemistry Manager

Lewis, J., Training and Emergency Preparedness Manager

Madison D. R.. Operations Manager

Moore. C.. Assistant General Manager - Plant Support

Reddick. R.. Site Emergency Preparedness Coordinator

Roberts.' P., Outages and Planning Manager

Sumner. H. , " ice President. Hatch Nuclear Operations

Thompson. J., Nuclear Security Manager

Tipps. S., Nuclear Safety and Compliance Manager

Wells P. , General Manager - Nuclear Plant

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying.

Resolving, and Preventing Problems

IP 61726: Surveillance Observations

IP 62703: Maintenance Observations

IP 62707: Maintenance Observations

IP 64704: Fire Protection Program

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 82301: Evaluation Of Exercises For Power Reactors

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IP 92700: Onsite Follow-up of Written Reports of Nonroutine

Events at Power Reactor Facilities

IP 92901: Followup - Operations

IP 92902: Followup - Maintenance / Surveillance

l IP 92903: Followup - Followup Engineering

IP 92904: Followup - Plant Support i

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ITEMS OPENED CLOSED, AND DISCUSSED

l Doened

50-321, 366/97-01-01 VIO Failure To Follow Procedure -  !

Multiple Examples

(Sections 04.1. M4.1, E2.1,

S1. F1.1).

50-366/97-01-02 VIO Inadequate Procedure for

Calibrating Unit 2 HPCI Time

Delay Relay K14  ;

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(Section M3.2).

50-321/97-01-03 VIO Failure to Translate Original

Design Specifications Into

Applicable Instructions

(Section E2.2). j

50-321, 366/97-01-04 VIO Failure to Submit Saecial

Report on Degraded rire

Barriers (Section F3).

Closed

50-321/96-10 LER Failure of the Turbine )

Overs)eed Control Valve of the i

High 3ressure Coolant

Injection System

(Section 08.1).

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50-366/96-13-05 VIO Failure to Properly Perform TS l

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Surveillance 3.6.1.7.3

(Section MS.1). ,

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50-366/96-04 LER Misinterpretation of

Requirements Results in Missed

Technical Specifications

l Surveillance (Section M8.2).

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Enclosure 2

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- 50-321/96-13 LER Personnel Error Results In

Missed Technical  ;

Specifications Surveillances-  ;

(Section M8.3). l

50-321/96-09 LER Component Failure Results in

Manual Reactor Shutdown 1

(Section E8.1). .l

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LIST OF ACRONYMS USED

ALARA- As Low As Is Reasonably Achievable

ASME - American Society of Mechanical Engineers  :

ARP - Alarm Response Procedure i

CFR - Code of Federal Regulations  ;

C02 - Carbon Dioxide -

- CR - Control Room-

DC - Deficiency Card

DCR - Design Change Request >

Ed - Edition

EDG - Emergency Diesel Generator ,

EOF - Emergency Operating Facility

E0P - Emergency Operating Procedure

EP - Emergency Plan ,

.

ERT - Event Review Team  !

F - Fahrenheit  ;

FHA - Fire Hazards Analysis '

FSAR - Final Safety Analysis Report -

GE - General Electric  !

GL - Generic Letter ,

GPC - Georgia Power Company l

GPM - gallons Jer minute

HP - Health P1ysics

HPCI - High Pressure Coolant Injection t

I&C - Instrumentation and Controls

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IN -

Information Notice

IR -

Inspection Report

IRET - Internal Radiological Emergency Team

LC0 - Limiting Condition of.0peration

LER - Licensee Event Report

LOCA - Loss of Cooling Accident

LSFT - Logic System Functional Test

MCC - Motor Control Center

MG - Motor Generator-

MSLB - Main Steam Line Break

MWO -

Maintenance Work Order

NOUE - Notice of Unusual Event

NRC - Nuclear Regulatory Commission

NRR -

- Nuclear Reactor Regulation

NSAC - Nuclear Safety and Compliance

Enclosure 2

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PCIS - Primary Containment Isolation System

PDR - Public Document Room

PE0 - Plant Equipment Operator

PM - Preventative Maintenance

PRB - Plant Review Board

PSP - Plant Security Plan

PSW - Plant Service Water System

0A - Quality Assurance

RCA - Radiological Controlled Area

RE - Reactor Engineer

REA - Request for Engineering Assistance

Rev. - Revision

RFP - Reactor Feedwater Pump

RG - Regulatory Guide

RHR - Residual Heat Removal

RP - Radiation Protection

RSM - Rod Sequence Mode

RTP - Rated Thermal Power

RWM - Rod Worth Minimizer

SCBA - Self Contained Breathing Apparatus

SBLC - Standby Liquid Control

SDC - Shutdown Cooling

SR - Surveillance Requirement

SRB - Safety Review Board

SS - Station Service and Shift Supervisor

STA - Shift Technical Advisor

TCP - Transient Combustible Permit

TM - Tem)orary Modification

TS - Tec1nical Specifications

TSC - Technical Support Center .

UFSAR- Updated Final Safety Analysis Report 1

VAC - Volts Alternating Current

VIO - Violation .

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Enclosure 2 l

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