ML20196J743

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Insp Repts 50-321/97-05 & 50-366/97-05 on 970518-0628. Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support
ML20196J743
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 07/25/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20196J633 List:
References
50-361-97-05, 50-361-97-5, 50-366-97-05, 50-366-97-5, NUDOCS 9708050042
Download: ML20196J743 (40)


See also: IR 05000321/1997005

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

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Docket Nos:

50-321. 50-366

License Nos:

DPR-57 and NPF-5

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Report No:

50-321/97-05'. 50-366/97-05

Licensee:

Southern Nuclear Operating Company. Inc. (SNC)

Facility:

E. I. Hatch. Units 1 & 2

Location:

P. O. Box 439

Baxley Georgia 31513

Dates:

May 18 - June 28, 1997

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Inspectors:

B. Holbrook. Senior Resident Inspector

E. Christnot. Resident Inspector

J. Canady Resident Inspector

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W. Kleinsorge. Reactor Inspector (Sections M1.2.

M2.1, M7.1. and M8.4 - M8.9)

G. Kuzo. Senior Radiation Specialist. (Sections

R1.2. R1.3. R2, R3 R5. R7. and R8)

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Approved by:

P. Skinner. Chief. Projects Branch 2

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Division of Reactor Projects

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Enclosure 2

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EXECUTIVE SUMMARY

E. I. Hatch. Units 1 and 2

NRC Inspection Report 50-321/97-05. 50-366/97-05

This integrated inspection included aspects of licensee operations.

engineering, maintenance, and plant support.

The report covers a 6-week

period of resident ins)ection; in addition. it includes the results of

announced inspections )y a regional reactor inspector and a radiation

protection / chemistry specialist.

Doerations

Plant procedures provided adequate instructions and Unit 2 operators

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took prompt and correct actions in response to a feedwater control

circuit swap from three element control to single element control.

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Engineering actions to troubleshoot the problem were appropriate

(Section 01.2).

The inspectors concluded that the failure to include Unit 1 plant

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service water strainer differential pressure instruments and their

associated setpoints in the instrument index was an oversight.

Equipment alignment, component operability, material conditions, and

housekeeping observed during an Engineered Safety Feature walkdown, were

acceptable.

Housekeeping for the diesel generator rooms was excellent

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(Section 02.1).

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An example of a violation for failure to follow procedure was identified

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for a clearance writer and two reviewers.

The clearance writer and

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reviewers failed to identify that the established clearance boundaries

affected other Emergency Core Cooling and support systems (Section

04.1).

The audit of Operations performance during the Unit 2 startup was

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conducted by trained ana qualified personnel.

Procedure requirements

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and audit techniques were clearly identified in the audit checklist

(Section 07.1).

Site management maintained good control of overtime.

Technical

Specification and procedural requirements were met (Section 08.1).

Maintenance

Routine maintenance activities observed were generally completed in a

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thorough and professional manner. Appropriated engineering and

supervisory oversight was provided (Section M1.1).

Equipment failures examined were generally appropriately addressed.

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item relating to the installation of an incorrect type of connector on

wide range monitor D11K621A was identified (Section M1.2).

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The licensee had made little progress in correcting the material

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condition deficiencies identified during the Maintenance Implementation

Inspection of October 1996.

As noted in October, the discrepant

material condition items were indicative of a lack of attention to

detail on the part of Operations and Engineering personnel who make

frequent tours to the areas (Section M2.1).

For the surveillances observed, all data met the required acceptance

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criteria and the equipment performed satisfactorily.

The surveillance

tests were conducted in accordance with procedures and with appropriate

oversight from supervisors and system engineers.

All involved personnel

were knowledgeable of the test and system performance requirements.

Overall performance was generally professional and competent (Section

M3.1).

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An example of a violation was identified for a failure to follow

procedure associated with sampling of fire-rated assemblies arid

penetration devices. Additional weaknesses were identified for the lack

of clarity of some surveillance procedural requirements and

administrative aspects of the fire protection program (Section M3.2).

A review of a licensee Safety Audit and Engineering Review audit reports

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'ndicated the audit was conducted by well qualified and trained

individuals (Section M7.1).

The licensee's actions taken or planned for other maintenance rule

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implementation inspection findings, were generally appropriate (Section

M8.9).

Enaineerina

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lne inspectors concluded that in general. engineering activities to

support plant operation were adequate (Section E1).

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Licensee personnel were actively pursuing a resolution of the concerns

discussed in Information Notice (IN) 92-18. Potential for Loss of Remote

Shutdown Capability During a Control Room Fire.

The established fire

watch patrols were appropriate (Section E2.1).

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The operation of Unit 2 with zero or low drywell-to-torus differential

pressure does not impact any safety function associated with the Primary

Containment.

All Technical Specification and Final Safety Analysis

Report requirements associated with torus-to-drywell vacuum breakers

were met (Section E2.2).

Plant Support

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In general, radiological controls and health physics activities were

adequate.

Minor deficiencies were discussed with technicians and

management personnel (Section R1.1).

Enclosure 2

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Radiological controls for high arid locked-high radiation areas were

maintained in accordance with Technical Specification requirements

(Section R1.2).

Contamination control associated with plant operation and maintenance

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activities continued to be a program weakness.

An example of a

violation for failure to follow procedure was identified for failure to

implement contamination control practices (Section R1.2).

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Transportation activities for radwaste and material shipments met

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10 CFR 71.5 and DOT 49 CFR 100-179 requirements (Section R1.3).

In general, the radiation monitoring system equipment was calibrated

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appropriately (Section R2).

Licensee programs to control, monitor and document liquid and airborne

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radionuclide effluent releases were maintained and implemented properly

(Section R3).

The Radiological Environmental Monitoring Program (REMP) sampling,

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analysis and reporting requirements were implemented effectively and

demonstrated minimal environmental impact (Section R3).

Projected offsite doses resulting from effluents were well within the

limits specified in the Offsite Dose Calculation Manual and 40 CFR 190

(Section R3).

An example of a violation was identified for the failure to implement

maintenance procedures to ensure that Radiological Work Permit

requirements and Health Physics coverage were adequate for the assigned

work activity.

A negative observation was identified for Health Physics

personnel failure to demonstrate a questioning attitude to ensure

radiological controls were adequate for an assigned work activity. A

negative observation was also identified for the failure of personnel to

identify and document several deficiencies surrounding a personnel

contamination due to poor radiological controls (Section R4.1).

Appropriate hazardous material training was provided to personnel

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handling and packaging radioactive materials for transport (Section R5).

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Audits of chemistry, radwaste and radiological control activities were

performance based with identified issues tracked and corrected

appropriately (Section R7.1).

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Counting room Quality Control activities were conducted in accordance

with approved procedures and demonstrated detector and analysis system

operability (Section R7.2).

Observed supervisory oversight by the inspectors of REMP activities by

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onsite personnel was minimal (Section R7.~2).

Enclosure 2

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The areas of security inspected met the applicable requirements (Section

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S2).

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Enclosure 2

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Report Details

Summary of Plant Status

Unit 1 began the report period at 100% rated thermal power (RTP).

Power was

reduced to about 80% RTP on June 21 to complete corrective maintenance for a

leak on a turbine extraction steam valve.

Power was returned to 100% RTP the

same day. The unit operated at 100% RTP for the remainder of the report

period, except for routine testing activities.

Unit 2 operated at 100% RTP throughout the report period, except for routine

testing activities.

I. Operations

01

Conduct of Operations

C1.1 General Comments (71707)

Using Inspection Procedure 71707. the inspectors conducted reviews of

ongoing plant operations.

In general, the conduct of operations was

professional and safety-conscious; specific events and observation are

detailed in the section below.

01.2 FeedWater (FW) Flow Control Unit 2

a.

Insoection Scooe (71707)

The inspectors were informed that Operations personnel had observed

sudden step changes in FW flow indications for channel A and channel B

on Unit 2.

During a routine tour of the control room on June 17. 1997

the inspectors also observed a sudden FW flow step change.

The

inspectors observed the operators' res)onse to the FW flow step change

and monitored licensee actions to trou)le shoot the problem.

The

ins)ectors also reviewed the applicable plant procedures for this

pro)lem.

b.

Observations and Findinas

Design Change Request (DCR)95-055 for the new FW control system was

installed on Unit 2 during the spring 1997. refueling outage. As a

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result of this DCR if a mismatch of about .5 million pounds mass per

hour between the FW flow sensing channels occurs. the FW control circuit

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shifts from three element control (reactor vessel water level. feedwater

flow, and steam flow) to single element control (reactor vessel water

level only).

The shift from three element to single element was

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designed to mitigate a transient following a FW flow transmitter

failure.

The DCR is scheduled to be installed on Unit 1 during the fall

1997, refueling outage.

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Enclosure 2

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The shift did not result in a plant transient and reactor level change

was negligible.

The inspectors observed that Operations personnel

res)onded using applicable plant procedures.

A review of procedures

34Al-603-132-2S. "Feedwater Control System Trouble." Revision (Rev) 2.

and 34-S0-N21-007-25. " Condensate and Feedwater System." Rev.29.

revealed that the procedures provided adequate instructions for

operators to respond to the problem.

The inspectors discussed the occurrences with Operations personnel and

were informed that the amount of time that the mismatch was present

varied. The FW flow variations lasted from about seven to forty-five

minutes.

The mismatches appeared to occur on a random bases and

included both increasing and decreasing changes.

Due to multiple occurrences, the operators placed the FW control system

in single element control.

The licensee formed a problem solving team

to review the mismatch. identify possible causes and make

recommendations for corrective actions.

Instrumentation to monitor

system performance was installed.

Near the end of the inspection period. Engineering personnel informed

the inspectors that the problem solving team was still evaluating the

problem and had not made recommendations to site management.

The team

concluded that actual FW flow differences existed.

The problem solving

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team determined that the difference in the A and B channel flow

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increased when Reactor Water Cleanup System (RWCU) was not in service.

These observations were made by the problem solving team when the RWCU

was out of service for corrective maintenance.

The RWCU was placed in

service following corrective maintenance and the FW control problem of

shifting from three element to single element control, due to a FW flow

mismatch, did not recur.

Operations personnel also observed a swap to FW single element control

during Main Steam Isolation Valve (MSIV) testing.

During this

surveillance test. the MSIVs were closed about 10%. resulting in a flow

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mismatch between the main steam lines that cas sensed by the FW control

circuit.

General Electric and corporate engineering personnel were

evaluating a change to the FW control circuit setpoints to lessen the

possibility of spurious swaps from three element to single element

control.

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The inspectors discussed with Operations management. the number of

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surveillance procedures that could cause a FW control circuit swap.

The

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inspectors were informed that some surveillance 3rocedures had been

identified and a review of other procedures was

aeing conducted.

The inspectors observed that all Operations personnel had not received

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specific instructions on what actions to take when surveillances were

identified that may cause a swap of the FW control circuit.

This was

discussed with Operations management.

Operations management later

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informed the inspectors that more detailed instructions were provided to

all Operations personnel.

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The inspectors discussed with Engineering personnel whether or not the

swapping of the FW control circuit had been identified during the DCR

review process or whether this-problem was unexpected.

The inspectors

were informed that the problem was unexpected and had not been discussed

.previously. -Engineering personnel planned to evaluate the results of

the problem . solving team's findings to determine what corrective actions

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will be required

c.

Conclusions-

Plant procedures provided adequate instructions and Unit 2 operators

took prompt and correct actions in response to the feedwater control

circuit swap from three element to single element control. The swap did

not result in a plant transient.

Engineering actions to troubleshoot

the problem were appropriate.

02

Operational Status of Facility and Equipment

02.1 Enaineered Safety Features (ESF) System Walkdowns

a.

Insoection Scooe (71707)

The inspectors used Inspection Procedure 71707 to walk down accessible

portions of the following ESF system:

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Plant Service Water (PSW), Divisions 1 and 2 (Unit 2)

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PSW for 1A. 1B. and 1C Emergency Diesel Generators (EDG).. Unit 1

The walkdown included a verification of valve alignment, condition of

components in service, and general housekeeping for the associated

areas.

b.

Observations and Findings

The ins)ectors reviewed applicable drawings and Instrument Setpoint

Index. Revision (Rev.) 47 for instruments that actuate control room

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alarms and automatic actions of the PSW strainers.

The inspectors

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observed that the set 3oint index for Unit 2 contained the necessary

instrumentation for t1e PSW motor operated strainers and indicated

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applicable instrument setpoints.

However, the inspectors could not

locate the Unit 1 corres)onding instruments and their applicable

instrument setpoints.

T1e inspectors discussed this issue with

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03erations and Engineering personnel.

The inspectors were informed that

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t1e Unit 1 instruments should have been included in the setpoint index.

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Enclosure 2

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The inspectors observed that the setpoints for strainer differential

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pressure instruments for both units were different.

The inspectors were

informed that the strainers for Unit 1 were of a different manufacturer

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than Unit-2 and that the instrument setpoints were different.

The

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inspectors verified that the Unit 1 instruments' setpoints were

consistent with engineering and vendor recommendations.

The inspectors were later informed that the onsite engineering group

issued As Built Notification (ABN)97-181 to add the applicable Unit 1

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instruments to the setpoint index.

c.

Conclusions

The inspectors concluded that the failure to include Unit 1 PSW strainer

differential pressure instruments and the associated setpoints in the

instrument index was an oversight.

Equipment alignment and com)onent

operability, material conditions, and housekeeping were accepta]le in

all areas inspected.

Housekeeping conditions for the EDG rooms were

excellent.

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04

Operator Knowledge and Performance

04.1 Clearance Deficiency for Unit 1 Core Soray (CS) System

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a.

Insoection Scooe (71707)

The inspectors reviewed procedure 30AC-0PS-001-OS. " Control Of Equipment

Clearances and Tags." Rev.15. equipment clearance 1-97-159. for the B

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loop of Unit 1 CS and reviewed licensee actions with respect to a

clearance deficiency.

b.

Observations and Findinas

On June 9,1997. Nuclear Safety and Compliance (NSAC) management

informed the inspectors that Unit 1 had entered TS action 3.0.3 due to

both loops of CS being considered inoperable.

The inspectors reviewed

operator logs, equipment clearance sheets and discussed the CS clearance

with clearance writers and Operations management.

The inspectors

observed from their reviews that clearance 1-97-159 was placed for

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maintenance activities on the IB loop of CS.

The clearance was placed

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and the required TS action statement was entered at 7:30 a.m.

At about

1:40 p.m.. control room operators received an alarm that indicated that

the 1A CS Jockey Pump system, which maintains the CS system full and

pressurized, had a low level.

This indicated that the A loop of CS

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might not be properly filled and vented.

Operators immediately declared

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the A loop of CS inoperable and initiated actions to fill and vent the

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system.

During the time both loops were declared inoperable. TS 3.0.3

was entered.

This TS action required that the unit be in Cold Shutdown

within the next 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />.

Following fill and venting activities, at

about 2:00 p.m. . operators declared the 1A loop operable and exited TS 3.0.3.

Enclosure 2

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The inspectors observed t at part of the clearance required closing the

1B CS pum) suction valve am racking out its electrical supply breaker.

Closing t1is valve isolated the inservice jockey pump suction source.

The correct action should have been to realign the jockey pump system to

the other CS loop and place the standby pump in service prior to

isolating the inservice jockey pump.

The clearance was developed by personnel from a maintenance team which

included experienced clearance writers.

The clearance form did not

contain, in Section 3. Amplifying Instructions. any caution or note

concerning a review of the inservice jockey pump suction source prior to

closing the CS pump suction valve.

The inspectors brought this problem

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to the attention of the personnel who write and modify computer

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generated clearances and a note was added for the computer generated CS

clearance form.

The inspectors observed that the computer generated clearance for the CS

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loop 1B was identical to the clearance that was implemented by

Operations personnel.

Neither contained any precautions concerning the

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jockey pump system. The inspectors discussed the clearance review

process with clearance writers.

The inspectors were informed that the

common practice and )rocedural recuirement for computer generated

clearances was for tie clearance crafter to verify the clearance using

plant drawings to confirm the clearance boundaries were accurate.

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this case. the review process was not adequate to identify the inservice

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jockey pump suction would be isolated and system alignment should be

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changed.

The clearance was reviewed and approved by two Senior Reactor

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Operators prior to being placed and the deficiency was not identified.

The licensee initiated an engineering review of the problem to determine

if the 1A loop of CS should have been declared inoperable.

Engineering

determined the 1A loop was not inoperable and applying TS 3.0.3 was a

conservative decision.

Engineering based their decision on a review of

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the TS required o)erability surveillance for the CS system fill and vent

and a review of t1e instrument design configuration.

Engineering

determined that about 2 gallons of water may have escaped from the 1A CS

loop between the time the inservice jockey pump was isolated and the

standby jockey pump was started.

The inspectors reviewed drawings of

the alarm piping with Engineering personnel and observed that the low

level alarm switch configuration was above the high point of the CS

system pipir,g.

A low water level in the alarm system piping occurred

and actuatt.d the low level alarm prior to any level decrease in the

primary system.

The inspectors concluded the licensee's determination

that the 1A CS system was operable was reasonable.

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The inspectors reviewed licensee performance for the past two years with

respect to clearance problems.

Clearance deficiencies were identified

in Inspection Report (IR) 50-321, 366/97-03 and a VIO was identified in

IR 50-321. 366/97-02 for operators' failure to identify correct

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cle5rance restoration steps.

The inspectors concluded that the

Enclosure 2

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circumstances surrounding the most recent clearance problem were

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different from the previous problems and would not have reasonably been

prevented by previous licensee corrective actions.

For the most recent clearance problem, the clearance drafter and two

clearance reviewers failed to implement steps 8.4.5 and 8.5.2 of

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procedure 30AC-0PS-001-0S.

The procedure ste)s required in part, that

the drafter of the clearance will determine tle required isolation

boundaries and fill out the equipment clearance sheet and that

appropriate system Drawings. Electrical Diagrams. Load Lists, and System

Operating Procedures will be used to determine the adequacy of the

proposed clearance.

In this case the clearance boundaries were not

adequate with respect to ensuring other Emergency Core Cooling Systems

(ECC) and support systems were not affected.

The inspectors were informed that Operations management established a

problem solving team to evaluate this and other recent clearance

problems.

They were to determine root causes and make recommendations

to prevent recurrence. Additionally, the clearance procedure was being

revised to clarify some steps and provide an overall general

enhancement.

c.

Conclusions

The clearance drafter and two clearance reviewers failed to properly

implement procedures to identify the correct clearance boundary for the

Unit 1 B loop of Core Spray.

As a result, other ECCS and support

systems (1A loop of Core Spray and the jockey pump system) were affected

by the clearance.

This failure to follow procedure was identified as an

example of Violation (VIO) 50-321. 366/97-05-01. Failure to Follow

Procedure - Multiple Examples.

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Quality Assurance in Operations

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07.1 Review of Safety Audit and Engineerina Review (SAER) Audit Report

a.

Insoection Scooe 71707

The inspectors reviewed SAER Report 97-SA-2 which was conducted by

licensee personnel to verify compliance with and the effectiveness of

the Quality Assurance program as applied to Reactor and Plant Startup of

Unit 2. following the spring refueling outage.

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b.

Observations and Findinas

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Licensee personnel conducted the audit between April 16 and April 23,

1997.

The audit focused on reactivity control, startup activities,

surveillances, communications, control room manning, and team

observations.

Operations management provided input for specific items

to be audited.

The audit was conducted for around-the-clock shifts

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during startup activities.

No audit findings or audit comments were

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identi fied.

The inspectors reviewed auditor training requirements and training

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records and verified the auditors were qualified to conduct the audit.

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The inspectors observed that the audit checklist and specific audit

items were based upon current plant procedures and department

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instructions.

Procedure requirements and audit techniques were clearly

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identified in the audit checklist.

The inspectors reviewed each audit element and assessed the audit

conclusions.

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c.

Conclusions

The inspectors concluded that the SAER audit of operations during the

Unit 2 startup activities was conducted by trained and qualified

personnel.

Procedure requirements and audit techniques were clearly

identified in the audit checklist.

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Miscellaneous Operations Issues

08.1 Use of Overtime (OT)

a.

Insoection Scooe (71707)(92901)

The inspectors reviewed Unit 1 and Unit 2 TS Section 5.0, Administrative

Controls, which establishes the requirements for OT use: Procedure 10AC-

MGR-020-0S. " Overtime," Rev.0: and the licensee's use of OT during the

spring 1997. Unit 2 refueling outage. The inspectors also conducted

reviews of OT for selected portions of the years 1995. 1996, and 1997.

The selected review for these years did not include OT used during

refueling outages.

The departments reviewed were Engineering, Security,

Maintenance. and Operations.

The inspectors discussed the results of

the OT review with applicable management personnel.

b.

Observations and Findinas

The review of OT during the spring refueling outage did not identify any

deficiencies.

The OT was controlled in accordance with TS and plant

procedures.

c.

Conclusions

The inspectors concluded that site management maintained good control of

overtime. Technical Specification and procedural requirements were met.

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II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a.

Insoection Scone (62707)

The inspectors reviewed the applicable procedures, work packages and

observed or reviewed all or portions of the work activities under the

following maintenance work orders:

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1-97-1077:

install seismic support for Residual Heat Removal

(RHR) Pump 1D electrical breaker

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1-97-0787:

change oil and meggar RHR Pump 1D motor

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1-97-1078:

install seismic support for RHR Pump 1B electric

breaker

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1-97-0507:

inspect end turn windings on the generator for the 1C

Emergency Diesel Generator (EDG)

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1-97-0270:

repair small fuel oil leak on 1C EDG

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2-97-1506:

change out Plant Service Water (PSW) Pump C mechanical

seal

b.

Observations and Findinas

The licensee removed loop 1B of the RHR system from service to perform

preventive maintenance. inspections, and implement a design change on

the RHR pump electrical breakers.

The inspectors observed that the design changes for breaker seismic

supports were im)lemented using work process sheets 97-011-E005 and

E006. items 33 t1 rough 38 only.

The installation and improvement of

seismic supports is an ongoing initiative for system upgrade.

The

implementation was performed with engineering and supervisory oversight.

The inspectors observed partial performance of and reviewed selected

maintenance work orders.

Applicable procedures were used and were

present at the work areas.

The inspectors discussed the activities with

workers. maintenance supervisors. and engineers.

All personnel were

knowledgeable of the work activities.

The required action statements

for Technical Specifications (TSs) out-of-service time were met.

The inspectors observed the routine generator end-turn winding

inspection of the 1C EDG.

The inspectors documented in previous

inspection reports that the inspections were routinely made due to

spacers between the windings becoming loose.

The inspection was

performed using the procedurally prescribed fiber optic and video

system.

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During the'last Unit I refueling outage the generator portion of the 1A

EDG was replaced.

The generator was sent offsite for a detailed

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inspection to determine if other EDGs should also be replaced.

The

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inspectors were informed that the results of the ins)ection indicated

that the removed generator was in good condition. T1e inspectors were

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also informed that, based upon the results of the offsite inspection of

EDG 1A there were no plans to replace the generators associated with

the 1C and the IB EDGs at this time.

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c.

Conclusions

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The inspectors concluded that maintenance activities completed were

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generally thorough and professional.

The inspectors observed

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engineering and supervisory oversight was provided when necessary.

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deficiencies were identified by the inspectors.

M1.2 Eauioment Failures

a.

Insoection Scoce (62700)

To evaluate the licensee's actions related to equipment failures, the

inspectors selected six Significant Occurrence Report (SOR) items.

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indicated below, to review for adequacy of: root cause determination;

determination of the extent of the problem: 10 CFR 50.65 evaluation; and

corrective actions taken and results achieved.

Commitment No.

Descriotion

C09700109

Failure of Reactor Core Isolation Cooling Valve

1E51F045 to open with control switch

C09700124

Standby Liquid Control Pump 1A tripped while

performing 34SV C41-002-1S

C09700130

Drywell Radiation Monitoring Wide Range Monitor

D11K621A spiking intermittently

C09700372

Cracked 3/4-inch RHR system socket weld adjacent

to 1E11-F3017/F3018

C09700771

Traversing Incore Probe (TIP) control unit 2C51-

1

J600-50 periodically fails the self test

l

C09701516

Valves 2G11-F003 and 2G11-F004 failed local leak

rate test

b.

Observation and Findinas

'

Drywell (DW) Radiation Monitoring Wide Range Monitor D11K621A was

reported, in C09700130. to be spiking intermittently. The licensee

4

Enclosure 2

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determined that spurious spiking was the result of corrosion on

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l

electrical connectors.

The connectors were subsequently replaced.

SOR

'

C09700130 stated in part: "The connectors outside the DW penetration for

i

l

2D11-K621A were found to be of the wrong type and were replaced in

01/97." When asked by the inspectors. how the wrong type of connectors

!

were installed. the licensee indicated that they did not know but would

i

find out.

Pending the outcome of~the licensee's investigation. this is

identified as Ins)ection Followup Item (IFI): 50-321, 366/97-05-02.

i

Installation of t1e Wrong Type of Connectors on Drywell Wide Range

Monitor D11K621A.

t

Equipment failures examined were appropriately addressed except as noted

above.

c.

Conclusions

l

Equipment failures examined were generally appropriately addressed.

!

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Housekeeoino and Material Condition

a.

Insoection Scone (62700)

During the Maintenance Rule Implementation Ins)ection, conducted in

October 1996 (NRC IR 50-321, 366/96-12). a num)er of housekeeping and

,

material condition discrepant items were noted. The team concluded that

'

these were indicative of lack of attention to detail by Operations and

Engineering personnel who frequently tour the areas.

To evaluate the

licensee's actions relative to those discrepant conditions, the

inspectors conducted a walkdown inspection of a portion of the plant

l

areas examined during the October 1996 inspection.

The specific areas

,

l

included: Diesel Generator Building 1B and 2A 4160 VAC Switch Gear

I

Rooms: Intake Structure: and Units 1 and 2 Cooling Tower Batteries.

b.

Observation and Findinas

The inspectors noted the following

The majority of the insulation associated with the traveling

.

l

screens was still in the same damaged / crushed condition noted in

October 1996.

The missing insulation noted in October 1996, had

been replaced. The licensee indicated that they were in the

process of generating a Modification that will replace the damaged

i

insulation and reroute the piping such that the piping will become

less attractive stepping locations. thus affording the new

insulation a better chance of remaining undamaged.

A number of fasteners continued to be missing or loose on the

!

guards and covers on the Traveling Screens.

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Enclosure 2

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Several electrical cabinet doors associated with the traveling 'r

screens continued to be improperly secured such that the weathe

'

stripping / environmental seal was not compressed thereby

i

potentially compromising the integrity of the components within.

Both Unit 1 service water strainers continued to leak., although to

1

=

l

,

a lesser extent than noted in October 1996.

~ Verdigris was-again noted on a number of terminals on the Unit 2

,

e

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Cooling Tower Batteries 2R425005.

L

l

In the switch gear rooms located in the EDG building the

l

inspectors noted ap3roximately ten panels that were improperly

l

secured such that t1e weather stripping was not compressed thus

l

not affording a proper seal

In addition, there were

approximately ten panel closure plate bolts that were not snug

tight, about four were stripped such that the bolt could be

removed without turning.

c.

Conclusions

The licensee had made little progress in correcting the material

condition deficiencies identified during the Maintenance Rule

Implementation Inspection of October 1996. As noted in October 1996,

the discrepant material condition items were indicative of a lack of

attention to detail by Operations and Engineering personnel who

frequently toured the areas.

M3

Maintenance Procedures and Documentation

M3.1 Surveillance Observations

'

a.

Insoection Scope (61726)

The inspectors reviewed the applicable procedures and observed all.or

portions of the following Unit 1 and Unit 2 surveillance activities:

e

34SV-E41-002-2S:

High Pressure Coolant Injection (HPCI) Pump

Operability

e

34SV-E41-002-1S:

HPCI Pump Operability

e

42SV-R42-007-05:

Battery Charger Capacity Test

b.

Observations and Findinas

l

The inspectors documented in previous inspection reports observations of

s)eed fluctuations for the HPCI turbine during surveillance testing.

i

!

Tlese observations were documented as Inspection Followup Item (IFI) 50-

!

321. 366/96-15-03.

Additional information is documented in Section M8.3

of this report.

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Enclosure 2

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12

During the recent surveillance activities, the inspectors observed

similar speed fluctuations.

Operators were aware that speed

fluctuations may occur and had discussed the issue during the pre-job

brief. The system engineer discussed system speed responses and stated

r

that some s]eed changes were normal and were to be expected.

The

inspectors lad discussed the speed changes with the system engineer and

Operations personnel prior to the surveillance and concluded that the

system engineer's explanation was reasonable.

The inspectors observed the battery charger test was for both chargers

for the EDG 1B battery.

The test was conducted in accordance with an

approved procedure and with oversight from the system engineer. All

involved personnel were knowledgeable of the system and test

requirements.

c.

Conclusions

For the surveillance activities observed, all data met the required

acceptance criteria and the equipment performed satisfactorily. The

surveillance tests were conducted in accordance with procedures and with

oversight from supervisors and system engineers.

All involved personnel

were knowledgeable of the test and system performance requirements.

Overall performance was generally professional and competent.

No

deficiencies were identified.

M3.2 Review of Unit 1 and Unit ? Fire Penetration Surveillances

a.

Insoection Scooe (61726)

The inspectors reviewed procedure 42SV-FPX-019-1S. Rev. 2 and 42SV-FPX-

019-2S. Revision (Rev.) 2. Penetration Seal Surveillance, and reviewed

licensee actions to complete the surveillance requirements. The

inspectors reviewed Units 1 and 2 Fire Hazards Analysis (FHA) to verify

correct implementation of the fire protection surveillance requirements.

b.

Observations and Findinas

The inspectors observed that Quality Control (OC) personnel generally

performed the surveillance procedures and fire protection engineers

reviewed and approved the procedures for acceptability.

The inspectors

observed that surveillance requirement 2.1.1 of the FHA required that

certain fire-rated assemblies and penetration sealing devices shall be

verified operable at least once per 18 months by performing a visual

inspection.

Section 7.7 ;f surveillance ]rocedures 42SV-FPX-019-1S/2S. stated in

part. that if any item in su)section 7.4 of the

3rocedure is marked

" Reject" or any other degradations were noted, t1e 10% sample of the

seals being surveyed is rejected, and a second 10% sample must be

requested from Fire Protection Engineering.

The second sample will be

Enclosure 2

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inspected in accordance with the steps of this procedure.

If the second

l

10% sample fails the surveillance procedure, additional 10% samples will

be inspected until a sample meets the acceptance criteria.

The inspectors observed that subsection 7.4 of the procedures included

the visual inspection acceptance criteria that was required to be met

for satisfactory completion of the surveillance.

The acceptance

criteria was identified in subsections 7.4.3.1 through 7.4.3.7.

Any

deficiencies were to be noted on Attachment 1 of the procedure and a

Deficiency Card (DC) was to be initiated.

The inspectors observed that

l

Attachment 1 contained a column where acc.cpted or rejecteo penetrations

'

were identified.

The inspectors reviewed the surveillance procedures for Unit 1 and Unit

2 that were completed between Jar;uary 30 cod April 21. 1997.

The

inspectors observed that four different types of penetrations were

identified as " rejected. " The inspectors ver1 M d that DCs and MW0s

were initiated to implement corrective actions f3r the rejected

penetrations. One penetration seal was misslag, one was not sealed on

one side, one contained holes and one contained spaces between the seal

and penetration boundary.

The inspectors reviewed surveillance procedures for both units since

A]ril 1991..

Each of the surveillance procedures identified degradations

tlat rendered some penetrations inoperable and required corrective

maintenance to restore the penetrations back to aerable status. The

inspectors verified that the correct Fire Actioi. Statement (FAS), for

penetrations that required FAS were implemented.

The inspectors were not provided ary documentation that a second 10%

sample of fire protection penetrations was no . conducted.

The

inspectors discussed this with fire protection engineering personnel.

The licensee stated that a second 20% sample had never been conducted.

The fire protection engineers interpretation of the procedurt step was

if the fire protection engineer detected a trend of a particular type of

penetration seal, a second 10% surveillance sample would be completed.

The inspectors concluded that this interpretation was not consistent

with the wording of the procedure.

The inspectors also identified everal procedure weaknesses. These

included the following:

-

Procedure 42FP-FPX-014-05. " Installation and Repair of Silicone

Foam Seals." contained specific irstallation requirements and

identified the required spacing ' atween multiple penetrations.

The procedure also identified tt

if penet ations were too

congested to complete a rejectici form.

The surveillance

procedure did not identify the s 'paration criteria requirement as

an item to review for surveillar,ce acceptance criteria.

.

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Enclosure 2

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Step 7.4.1 of procedure 42SV-FPX-019-1S/2S stated in part that

i

visual' inspection of each type seal includes, but will not be

,

l

limited to the items noted in steps 7.4.3.1 through 7.4.3.7.

The

I

procedure implied that other items may be observed for acceptance

i

'

criteria but provided no guidance for such items.

'

-

Step 7.4.3.2 of ' procedure 42SV-FPX-019-1S/2S stated in part.

(observe that) no apparent change in appearance or abnormal

degradation of seals and/or damming material.

The procedure

offered no guidance as to what constituted changes in appearance

l

or what abnormal degradation may include'.

-

Step 7.11 of procedure 42SV-FPX-019-1S/2S indicated the Fire

Protection Engineer will review the surveillance results and

perform a walkdown sample of penetration seals listed on

Attachment 1.

There were no procedure requirements to document

l

the sample walkdown, how many or which seals were reviewed or the

i

results of the review. The procedure did not indicate whether or

not seals that were identified as rejected or degraded should be

reviewed.

The inspectors observed that the last surveillances were com)leted for

l

Unit 1 and Unit 2 on abcat April 19. 1997.

The inspectors o) served that

3rocedure 42SV-FPX-019-IS for Unit 1. and 42SV-FPX-019-2S for-Unit 2.

-

l_

1ad incorrect cover sheets for the data package.

Unit 1 cover sheet was

'

on Unit 2 data and vice versa.

Inspectors brought this to the attention

of a fire protection engineer who corrected the problem.

l

As'of June 6.1997. fire protection engineers had not reviewed the

!

surveillances completed on A)ril'19.

The inspectors discussed with

Engineering management how t1e FHA reporting requirement to submit a

special report to the Safety Review Board within the next 30 days if an

inoperable penetration is not repaired within 14 days, was being met.

The-inspectors were informed that penetrations were usually repaired in

a timely manner however, this could be a potential vulnerability. The

problem was to be reviewed by Engineering personnel. The inspectors did

not identify problems caused by the delayed reviews.

The inspectors attempted to locate the previous 18 months surveillances

in document control. The document control clerk was unable to locate

,

the documents.

Fire protection engineering personnel had a copy of the

!

mrveillances in the office work location.

The inspectors were not able

L

to determine if the previous surveillances were ever submitted to

i

document control.

The inspectors documented a weakness in the administrative aspects of

the fire protection program in IR 50-321. 366/97-01. A Notice of

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Violation was also identified for failure to implement the FHA

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requirements for transient combustible permits. The above problems were

identified as additic.9el concerns of the administrative aspects of the

FP program implementation.

c.

Conclusions

The inspectors concluded that the failure to complete additional 10%

i

samaling of fire-rated assemblies and penetration devices in accordance

wit 1 section 7.7 of surveillance procedures 42SV-FPX-019-1S/2S and

section 2.1.1 of the Fire Hazards Analysis and Fire Protection Program

,

Surveillance requirements did not meet requirements. This was

,

identified as an example of VIO 50-321, 366/97-05-01, failure to follow

a

t

procedure - multiple examples.

Additional concerns were identified with

,

the clarity of some su'rveillance procedure requirements and with some

.

administrative aspects of the fire protection program.

4

M7

- Quality Assurance in Maintenance Activities

i

M7.1 .Audils

i

a.

Insoection Scoce (62700)-

'

To evaluate the licensee's Audit Program as it relates to maintenance,

the inspectors requested copies of all audits and self assessments

conducted in the maintenance area during the previous year.

The

inspectors reviewed the three audits provided.

l.

b.

Observations and Findinos

Audit 96-SPR-1. Audit of Special Processes, findings included.

incomplete weld sketches: Temporary Repair procedure not used; and Post

'

Weld Heat Treatment problems.

t

Audit 96-SA-4. Contractor Control

findings included: administrative

controls not satisfied: errors in the specification of ANSI Standards:

contractor pre-job briefings did not meet OSHA requirements: and

contractor Work Order procedural problems.

Audit 96-SA-8. Plant Housekeeping and Material Condition. findings

included: housekeeping deficiencies noted in U1 & U2 Turbine Buildings.

U2 Reactor Building. Control Room, and Laundry Storage Area: and tools

'

including wheeled carts were improperly stored in proximity of safety

related e

Appropriate corrective actions were taken or

planned. quipment.

.

c.

Conclusions

I

4

Maintenance was subjected to indcpendent audits, with appropriate action

'

taken for identified weaknesses.

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Enclosure 2

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M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) IFI 50-321. 366/96-14-04: Potential Deficiencies in the HPCI

l

Surveillance Procedure.

This item was opened pending additional

observations of operator and HPCI system performance during surveillance

,

l

activities.

The inspectors observed that the use of the Safety

l

Parameter Display System (SPDS) to monitor suppression pool temperature

during surveillance activities was consistent among the operating crews.

Engineering personnel informed the inspectors that the SPDS gives a more

accurate su)pression pool temperature indication than the safety related

recorder.

Based upon the inspectors' review of licensee's actions and

observations of the operators' consistent use of the SPDS. this item is

closed.

. Closed) Violation 50-321. 366/96-14-03: Failure to Implement

M8.2

(

Configuration Control Requirements - Multiple Examples.

The licensee

responded on February 4. 1997. by correspondence.

Additional examples

of this violation are discussed in Section E8 of this report.

The

licensee's res)onse indicated that a misleading label on the trip device

selector switc1 contributed to the incorrect setting.

Initial

corrective actions were discussed in IR 50-321. 366/96-14 (Section E2).

DCR 96-058 was implemented as part of the followup corrective actions.

Based upon the inspectors' review of licensee's actions, this violation

example is closed.

M8.3 (Closed) IFI 50-321. 366/96-15-03: Resolution of Reactor Core Isolation

Cooling (RCIC) and High Pressure Coolant Injection (HPCI) turbine speed

control drift.

During the report period the inspectors observed the

operation of the Unit 1 and Unit 2 HPCI system.

Part of the test was

for Inservice Testing (IST) purposes.

One requirement of the test was

to maintain the speed of the turbine at 3900 rpm plus or minus 1%.

The

inspators concluded, based on this observation and previous

observations, that during tests of the HPCI and RCIC systems the speed

will drift and did not result in a system operability concern.

The

inspectors observed that the plant operators had been made aware of

speed drifts.

Based on the inspectors' observations and review of

licensee actions, this item is closed.

M8.4 (Ocen) Violation 50-321. 366/96-12-01: Failure to Include All

Structures. Systems, and Components in the Scope of the Maintenance Rule

as Required by 10 CFR 50.65.

By letter dated December 19, 1996. the

licensee denied this violation.

Subsecuently, by letter dated March 5.

1997, the licensee stated that they hac determined that it was necessary

to resolve the issues discussed in their initial response of December

19. 1996.

The NRC responded by letters dated February 10. and April 2.

1997. As a result, the licensee indicated that they would include the

communications, non-appendix R emergency lighting. Appendix R emergency

l

lighting. and cooling tower systems to the maintenance rule program.

The licensee indicated that they would be in full compliance by

'

September 1. 1997.

This item remains open.

j

l.

Enclosure 2

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M8.5 (Ooen) Violation 50-321. 366/96-12-02: Failure to Establish Adequate

l

Performance Criteria for SSC Risk Significant Functions.

By letter

dated December 19, 1996, the licensee admitted that additional

performance criteria could have been established for the primary

containment and primary containment isolation, feedwater and condensate,

circulating water, electro-hydraulic control, and primary containment

i

'

chilled water systems.

The licensee has provided availability

performance criteria for those systems.

The licensee's letter dated December 19, 1996, denied that the

performance criteria for the AC and DC electrical and analog transmitter

trip systems were not 3roperly established.

Subsequently, by letter

dated March 5, 1997, t1e licensee stated that they had determined that

it was necessary to resolve the issues discussed in their initial

response of December 19, 1996.

The NRC responded by letters dated

February 10, and April 2,1997.

As a result, the licensee indicated

that they would establish appropriate additional performance criteria

for the AC and DC electrical and analog transmitter trip systems. The

licensee indicated that they would be in full compliance by September 1,

1997.

This item remains open.

M8.6 (Closed) Violation 50-321. 366/96-12-03: Failure to Follow Procedure for

.

Implementation of the Maintenance Rule.

By letter dated December 19,

1996, the licensee admitted to the violation and attributed it to

personnel error.

The licensee identified the failures as required by

the Maintenance Rule and conducted a root cause analysis on the

incident. The licensee determined that this was an isolated occurrence

and that the individual responsible. is no longer a licensee employee.

The inspectors determined that the licensee had conducted an

appropriate survey and determined the extent of the noncompliance, and

took appropriate actions to correct the condition and prevent its

recurrence.

M8.7 (Ocen) IFI 50-321. 366/96-12-04: Failure to Provide Adequate Procedure

for Implementation of Maintenance Rule Requirements.

The licensee

opened Action Item Tracking (AIT) No 96-2t>1 with a due date of January

j

5. 1998. AIT No 96-261 stated: Monitor the resolution of this issue by

)

the NRC and EPRI and once a position has been taken evaluate this

position and implement any corrective actions as necessary to bring

plant Hatch into compliance with regulatory requirements.

Regulatory

'

Guide (RG) 1.160, " Monitoring the Effectiveness of Maintenance at

Nuclear Plants." Rev.2, issued March 1997 paragraph 1.2. provided

specific guidance in the area in question. that of the role of

organizations, other than the Maintenance department, as it relates to

Maintenance Preventable Functional Failures (MPFF)s.

The licensee was

currently in the process of revising Administrative Control Procedure

ACP 40AC-ENG-020-05 Rev.2, " Maintenance Rule (10 CFR 50.65)

Implementation. " The licensee indicated that the guidance of RG 1.160,

Rev.2 Paragraph 1.2. will be incorporated in this revision.

This item

remains open.

Enclosure 2

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1

18

!

M8.8 (00en) IFI 50-321.366/96-12-05: Followup on Licensee Actions to Provide

Performance Criteria for Structures After Industry Resolution of this

Issue. The licensee opened AIT No 96-262 with a due date of January 7.

l

l

1998.

AIT No 96-262 stated: Monitor the resolution of the structural

'

monitoring issue by the NRC and EPRI.

Once a position has been taken

i

evaluate this position and implement any corrective actions as necessary

l

to bring plant Hatch's program into compliance.

RG 1.160. Rev.2. issued

'

March 1997, paragraph 1.5. provides specific guidance in the area in

question that of monitoring structures.

The licensee indicated that a preliminary draft of RG 1.160. Rev.2. was

used for guidance to write licensee document. Structural Monitoring

Program for the Maintenance Rule. Rev.1. dated September 1996.

It

should be noted that this document was available at the time of the

October 1996 Maintenance Rule Implementation Inspection.

notwithstanding. this IFI was opened as a result of that inspection.

Of concern to the inspectors was the fact that Structural Monitoring

Program for the Maintenance Rule. Rev.1, provides condition monitoring

acceptance criteria in vague terms e.g., potential significant

structural impact, considered serious, potentially significant, possible

structural impact, and structural integrity may eventually be

compromised. Where as Regulatory Guide 1.160. Rev. 2 provides guidance

in terms of the structure's ability to meet its design basis.

This item remains open.

M8.9 Licensee Actions Associated With Other Adverse Maintenance Rule

Imolementation Inspection findings

l

a.

Insoection Scooe (40500) (62700)

'

To evaluate the licensee's actions related to identified weakness and

other negative Maintenance Rule Implementation Inspection findings, the

'

inspectors examined the following:

b.

Observations and Findings

A weakness was identified in NRC Inspection Report 50-321, 366/96-

.

12 Section M1.6, associated with fragmented documentation for

review of problems and corrective actions for the Unit 2 primary

Containment Chilled Water System.

To address this issue the

licensee included in the monthly Maintenance Rule Report reference

)

to applicable documents for the (a)(1) systems e.g.

Clearance

'

No. . Deficiency Card No. . Significant Operating Report No. .

Maintenance Work Order No.. and Licensee Event Report No.

IR 50-321, 366/96-12, Section M1.4 identified that the licensee

.

had not established adequate performance criteria for several risk

significant SSC functions. balancing reliability and

!

Enclosure 2

.

19

unavailability for those functions would not be possible.

To

address this issue, the licensee reviewed all risk significant

SSCs and assured that each system included performance criteria

i

for both reliability and availability.

The systems to which

availability criteria was added included: primary containment

isolation, feedwater and condensate. circulating water electro-

1

hydraulic contiol. primary containment chilled water, primary

containment, ansi main steam.

Many findings or deficiencies discussed in audit notes were not

.

documented as findings or entered into the licensee's corrective

action program.

The lack of documentation of findings or

deficiencies was considt. red a weakness in the lice .ee's audit

process.

Comments in tne licensee's audit space were items that

were of only minimal significance for which no response was

expected.

To address this issue the licensee stopped the practice

of including comment:3 in audit reports.

The omission of two risk significant functions from the matrix was

.

considered a weakness.

The licensee indicated that they had

evaluated the two systems. and determined that the scoping of the

Remote Shutdown Panel (RSP) was appropriate.

They indicated that

they would amend the Maintenance Rule Scoping Manual to explain

the differences between the PRA assumptions for the RSP and the

scoping of the RSP.

The diesel generator building exhaust fan

system was still under evaluation.

The licensee indicated that

this issue would require a procedure modification.

The lack of assessments for non-risk significant SSC function

.

combinations was considered a weakness.

The licensee indicated

that they were comfortable with the situation as it now exists and

anticipate no changes in this area.

Misleading guidance regarding priorities following emergent

.

failures was considered a weakness.

The licensee indicated that

with their existing software, the existing guidance was the best

available.

The failure to perform a sensitivity analysis when initially

establishing reliability performance criteria was considered a weakness.

In addition, the failure to perform additional risk ranking using

Maintenance Rule performance criteria new data was considered a minor

weakness.

The licensee indicated that after they re-analyze their

safety assessment risk model they will re-do the risk ranking and

sensitivity analysis, currently planned to be completed in the first

quarter of 1998.

1

Enclosure 2

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c.

Conclusions

The licensee's actions taken or plance associated with other adverse

maintenance rule implementation ,nspectwn findings, were generally

appropriate.

III. Enaineerina

El

Conduct of Engineering (37551)

On-site engineering activities were reviewed to determine their

effectiveness in preventing, identifying, and resolving safety issues,

events and problems.

The inspectors concluded that in general, engineering activities to

support plant operation were adequate.

E2.1 Engineerina Followuo Concerning Electrical Short Circuits

a.

Insoection Scooe (92903) (71707)

Engineering personnel informed the inspectors that a recent additional

review of control room electrical systems for motor operated valves

revealed conditions described in Information Notice (IN) 92-18:

" Potential for Loss of Remote Shutdown Capability During a Control Room

.

Fire." The inspectors observed and reviewed the activities initiated by

corporate engineering, onsite engineering and Operations personnel to

i

correct the problem,

b.

Observations and Findinas

The licensee's initial evaluation of the IN was completed on May 15.

1992, and was very limited.

This inspector observation was documented

in Inspection Report 50-321, 366/97-01.

On November 25, 1996, the

licensee initiated an engineering request to perform a reanalysis of the

IN.

The most recent findings were a result of the reviews conducted

during the reanalysis.

The IN discusses control room short circuits, referred to as hot shorts,

that could result in valve actuation during some postulated fire

conditions.

The inspectors observed that two Design Change Requests (DCR). one per

unit, were developed and 16 Fire Action Statements (FAS) were

implemented.

The inspectors observed that DCR 97-016. for Unit 1 and

97-017 for Unit 2. identified the fire area / zones, the valves, by master

parts list designation, and the electrical circuits that were affected

as described in the IN.

The DCRs were scheduled to be implemented

during the next refueling outage for each unit.

Enclosure 2

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The inspectors reviewed the scope of the DCRs and observed that

corrective actions were to reroute cables to eliminate the possibility

of hot shorts occurring within a cable.

The inspectors were informed

that corporate engineering was still reviewing systems and components

that were affected and that the list of concerns would be adjusted as

necessary, based upon the additional reviews.

Additional actions of the

DCR's were the following:

DCR 97-016: correct six fire area / zones.15 valves, and 16

electrical circuits for Unit 1

DCR 97-017: correct seven fire area / zones. 34 valves, and 52

electrical circuits for Unit 2

The inspectors observed that in the scope of the modifications were

valves and electrical circuits in the Residual Heat Removal (RHR), High

Pressure Coolant Injection (HPCI) Reactor Core Isolation (RCIC), and

Plant Service Water (PSW) systems.

The inspectors observed that nine of the FASs were for Unit 1. 1-97-24

25, 26. and 43 through 48. and seven for Unit 2. 2-97-59 through 65.

The inspectors observed that FAS 1-97-24, 25 and 26 were issued on April

1

10, 1997, to address the control, cable spreading. and computer rooms

,

and the remainder of the FASs were issued on May 16.

The inspectors reviewed the FASs and observed that they were issued to

cover specific fire area / zones of the plant and contained both safety

and non-safety related equipment.

Among the FAS reviewed were the

'

following:

e

1-97-025:

the FAS was issued for fire area / zone 0024B. the

computer room, and was one of the initial FAS

e

1-97-043:

the FAS was issued for fire area / zone 1203F. the 130

foot (ft.) elevation of the reactor building south,

and contains circuits for valves in the Unit 1 RHR.

HPCI and RCIC systems

e

1-97-048:

the FAS was issued for fire area / zone 1205N. the 164

ft. elevation of the reactor building heating,

ventilation, and air conditioning room, and contains a

circuit for a valve in the Unit 1 RHR system

e

2-97-062:

the FAS was issued for fire area / zone 2205N. the 164

ft. elevation of the drywell chiller room, and

contains circuits for valves in the Unit 2 RHR and

RCIC systems

!

e

2-97-065:

the FAS was issued for fire area / zone 2205F

the 130

ft. elevation of the reactor building soutt. and

!

Enclosure 2

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contains circuits for valves in the Unit 2 RHR and

j

RCIC systems

The inspectors observed that the FAS required a one hour fire watch

patrol.

The inspectors reviewed the applicable Fire Hazards Analysis

and Fire Protection Program requirements and verified that the correct

FAS were implemented.

l

The inspectors discussed this item with cor) orate and onsite management

in terms of the 31 ant being outside design ) asis.

The inspectors also

'

inquired as to t1e reportability of this item under 10 CFR 50.72 or 10 CFR 50.73.

The licensee determined the deficient conditions were not

reportable. The inspectors reviewea the licensee's non-reportability

evaluation which stated in part, that "there is no indication that the

NRC intends licensees to report under this paragraph" (paragraph

'

(a)(2)(ii) of 10 CFR 50.73 and an additional reference to NUREG-1022

Part V), " events which are merely hypothesized to occur, particularly

when the hypothesis depends upon multiple layers of incredible

assumptions." Similar rationale was used for paragraph (a)(2)(v)/(vi)

of 10 CFR 50.73.

Pending the inspectors' detailed review of the reporting requirements,

this issue is identified as Unresolved Item (URI) 50-321. 366/97-04:

Determine the Reportability of Licensee Identified Deficiencies With

Respect to IN 92-18. Potential for Loss of Remote Shutdown Capability

During a Control Room Fire.

c.

Conclusions

.

The inspectors concluded that licensee personnel were actively pursuing

a resolution of the concerns discussed in Information Notice 92-18:

Potential for Loss of Remote Shutdown Capability During a Control Room

Fire.

Unresolved Item (URI) 50-321, 366/97-04: Determine the

Reportability of Licensee Identified Deficiencies With Respect to IN 92-

18. Potential for Loss of Remote Shutdown Capability During a Control

Room Fire, was identified.

The established fire watch patrols were

appropriate.

E2.2 Review of Unit 2 Drywell-to-Torus (DW/T) Differential Pressure

a.

Insoection Scooe (37551) (71707)

The inspectors reviewed documentation and held discussions with licensee

personnel concerning the circumstances associated with the zero or low

differential pressure (DP) between the Unit 2 drywell and torus.

b.

Observations and Findinas

The operating crew on Unit 2 observed that the DW/T DP was zero or very

low compared to its value prior to the Unit 2 spring refueling outage of

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Enclosure 2

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23

1997. A historical pattern of containment pressurization followed by

venting existed.

Based upon questions raised by the operating crew,

Nuclear Safety and Compliance (NSAC) conducted an evaluation to

l

determine the im]act of operating with a zero or discernibly small DW/T

DP.

Including w1 ether or not containment integrity existed based upon

the zero DP.

The inspectors reviewed the results of the NSAC's evaluation dated April

24. 1997.

The evaluation concluded the following:

The vacuum breakers between the drywell and torus were operable

e

with acceptable leakage characteristics,

There was no leakage from the primary containment that exceeds 10

e

CFR 50. Appendix J requirements, and

e

Low or zero DW/T DP does not impact any safety function associated

with the Primary Containment.

The NSAC's evaluation also indicated that a review of data confirmed

that the historical pattern of containment pressurization followed by

venting was observable until the drywell was inerted following the

recent Unit 2 refueling outage.

Since this refueling outage, the

drywell pressure remained fairly constant.

The licensee believes that

the fairly constant drywell pressure was due to less nitrogen leaking

into the drywell from the drywell pneumatic system as a result of the

maintenance performed on various drywell pneumatic valves during the

Spring 1997 refueling outage.

The inspectors reviewed the bases for Technical Specification (TS)

Surveillance Requiremerits 3.6.1.8.1 for the Suppression Chamber-to-

Drywell Vacuum Breakers.

The bases stated that with a closed indication

for the vacuum breakers and the DW/T DP remaining steady at zero, then

an alternate method for verifying that the vacuum breakers are closed

must be performed as outlined in the Technical Requirements Manual

(TRM), T3.6.1. , " Suppression Chamber to Drywell Vacuum Breaker Position

Indication." A review of TRM T3.6.1 by the inspectors indicated that

the alternate method was to demonstrate that the drywell-to-suppression

chamber (torus) DP can be maintained greater than 0.5 psid for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

without makeup.

The TS 3.6.1.8 required action time for this

confirmation was within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of discovery of the condition (zero DP)

and every 14 days thereafter.

The inspectors reviewed Surveillance Procedure 34SV-T48-004-25, "Drywell

to Suppression Chamber Leakage Test." Revision (Rev.) 2.

This procedure

had temporary change 97-168 incorporated on April 24, 1997, to add the

14 day requirement for DW/T torus vacuum breaker leakage test when

i

operating at zero DP between the drywell and torus.

The license is

l

performing this surveillance recommended every 14 days due to the zero

or discernibly l w drywell to torus DP.

!

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Enclosure 2

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The inspectors discussed with Operations supervision the use and testing

'

of the drywell/ torus differential pressure system. This system was

sometimes referred to as the " pump back" system. The pump back system

l

was originally designed to maintain the drywell pressure slightly higher

than the torus in order to lower the water column in the downcomer pipes

that. extend into the water in the torus.

The pump back system is not

,

used now due to the installation of additional reinforcements on the

-

torus.

-

!

Engineering personnel informed the ins)ectors that Design Change Request

4

(DCR)81-109 provided information on t1e additional reinforcements

installed on the torus that reduced its-susceptibility to the higher

.

L

loadings caused by the jet forces during initial: vent clearing following

i

l

a LOCA.

The inspectors verified that this DCR implemented

.,

reinforcements of the DW/T vent header and the downcomer legs.

Engineering also stated that the components necessary for automatic

o)eration of the system were " retired in place" on Unit 2 and was

plysically removed on Unit 1 under DCR 84-316.

L

The inspectors reviewed Unit 2 Final Safety Analysis Re) ort (FSAR).

!

Sections 3.8.2.8.2.3. DryweT1 to Pressure Suppression C1 amber Bypass

Area Tests. Supplement 3.88. Plant Unique Analysis of Mark 1 Containment

i

System and.6.2.1.2.1.6.1. Drywell to Suppression Pool Vacuum Breakers.

'he FSAR review provided no indications of requirements for the DW/T DP

(pump back) system.

i

c.

Conclusions

The inspectors concluded that the Unit 2 operation with zero or low DU/T

differential pressure does not impact any safety function associated

-

with the Primary Containment. All TS requirements associated with

torus-to-drywell vacuum breakers were met.

E8

Hiscellaneous Engir.eering Issues (92700) (92903)

E8.1

(Closed) Violation 50-321. 366/96-14-03: Failure to Implement

Configuration Control Requirements - Multiple Examples. The licensee

,

responded to this violation by correspondence dated February 4, 1997.

Based upon the inspectors' review of licensee actions, this item is

'

closed.

<

E8.2 1 Closed) LER 50-321/97-02: Less than Adequate Procedure Results in a

Condition Prohibited by the Technical Specifications (TS). This issue

,

was discussed in irs 50-321, 366/97-01 and 50-321. 366/97-03.

Based on

the inspectors' review of licensee actions. this LER is closed.

!

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Enclosure 2

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IV Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 Observation of Routine Radioloaical Controls

a.

Inspection Scooe (71750)

General Health Physics (HP) and radiological control activities were

observed during the report period.

This included locked high radiation

area doors, proper radiological posting, and personnel frisking upon

exiting the Radiological Control Area (RCA).

The inspectors made

frequent tours of the RCA and observed activities.

The inspectors concluded that in general, radiological controls and HP

activities were adequate.

Minor deficiencies were discussed with

technicians and management personnel.

R1.2 Radioloaical Controls

a.

Insoection Scone (83750)

j

Radiological controls associated with ongoing Radioactive Waste

(radwaste) processing operations and storage areas were reviewed and

evaluated by the inspectors.

Reviewed 3rogram areas included container

labels, area postings, high and locked-ligh radiation area controls, and

procedural and Radiation Work Permit (RWP) guidance.

Established

program controls and their implementation were compared against Updated

Final Safety Analysis Report (UFSAR) details and documented requirements

in ap)licable sections of Technical Specifications (TSs), and

10 CFR Part 20.

During the week of June 23. 1997, the inspectors made frequent tours of

the RCAs.

External and internal exposure controls and contamination

i

controls associated with specific radwaste processing and storage areas

were observed and evaluated in detail.

In particular, radiation control

activities associated with inspection and replacement of the Unit 1 (U1)

condensate filter elements performed in accordance with Maintenance Work

Order (MWO) Number (No.) 19701437. and RWP No. 097-0021. Rebuild \\ Replace

Filter Demins and Support. Revision (Rev.) 0, dated January 3. 1997.

were reviewed and discussed with responsible Health Physics (HP) staff

and supervisors.

The inspectors directly observed worker performance

and discussed results of radiation and contamination surveys conducted

for selected equipment and facility areas.

b.

Observations and Findinas

High and locked-high radiation area controls were verified to be

implemented in accordance with TS requirements.

Postings for

radiologically controlled areas were proper and in accordance with TS or

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Enclosure 2

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.

,

26

10 CFR 20 Subpart J requirements.

Containers holding radwaste,

contaminated materials and equipment were labeled in accordance with

,

10 CFR 20.1904 requirements.

Excluding U1 condensate maintenance

activities, radiation controls associated with ongoing radwaste.

processing, storage and shipping operations were adequate and conducted

in accordance with ap)licable RWPs and procedures.

In addition,

cleanliness and houseceeping within the radwaste processing and storage

1

areas.were considered to be acceptable.

i

During-facility tours on June 26. 1997, the inspectors observed the

'

following poor radiological and contamination control practices

associated with the U1 condensate demineralizer filter maintenance.

During disassembly of a containment tent used as an engineering control

tc prevent spread of airborne contamination. two workers were observed

.

standing in two 55 gallon drums located within the roped-off

contaminated work area.

The workers were physically stomaing on the

materials within the barrels to enhance com) action.

At t7e same' time,

!

rollup door T15 to the area was open, there)y allowing air flow into and

across the potentially contaminated work area into a non-coritmiiinated

t

area.

No engineering controls were established, no representative air

samples were collected, nor was the work performed under continuous HP

coverage.

Cognizant licensee representatives informed the inspectcrs

that the materials within the drums consisted of potentially

.

contaminated fabric which had been used to construct the tent

,

surrounding the U1 condensate filter maintenance area.

Subsequently,

'

the inspectors were informed that eight workers associated with the U1

condensate filter work activities were determined to be contaminated

externally, 3000 to 30000 disintegration per minute per probe area,

,

after conducting RCA exit surveys.

No' internal contamination was

detected for whole body counts conducted on the affected workers.

Gross

I

contamination surveys, large area masslin wipes, for areas outside of

'

the U1 condensate work area indicated contamination levels of 1000 to

.

100000' disintegration per minute per masslin wipe.

,

Review of the applicable RWP guidance and discussions of worker

knowledge with responsible HP personnel indicated that maintenance

!

workers were expected to be aware of potential contamination of the

enclosure material based on previous work experience.

Thus, disassembly

of the enclosure prior to completion of contamination surveys and decon

activities was not expected by the HP staff.

Based on their previous

similar work experience, the involved workers were expected to

understand precautions to minimize spread of contamination including

)

proper compaction of-contaminated material and preventing air flow

across a contaminated area.

In addition, the HP technician providing

i

'

intermittent coverage in accordance with the RWP was not informed that

the workers were going to dismantle the enclosure.

TS 5.4 recuired that written procedures be established implemented, and

maintainec covering activities delineated in Ap3endix A of Regulatory

Guide (RG) 1.33. Rev. 2. dated February 1978.

Regulatory Guide 1.33,

Enclosure 2

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Appendix A " Typical Procedures for Pressurized Water Reactor and Boiling

Water Reactors " Paragraph 7.e required radiation protection proradures

for Radiation Work Permit System and for Contamination Control.

Hulth

Physics procedure 60AC-HPX-004-05 " Radiation and Contamination

Control." Rev. 14. effective October 15, 1996, specified that HP will

take measures to minimize migration of high contamination to low or

uncontaminated areas: will initiate controls, to ensure the spread of

contamination is minimized: will perform non-routine radiation and

contamination surveys as required, to support operation and maintenance:

and will perform airborne surveys during radioactive work which is

expected to cause airborne radioactivity unless constant air monitors

are provided.

The inspectors identified the failure to implement proper

contamination controls, surveys and HP coverage for dismantling of the

U1 condensate demineralizer filter tent as an example of Violation (VIO)

50-321/97-05-01: failure to follow procedures - multiple examples.

c.

Conclusions

Radiological controls for high and locked-high radiation areas were

maintained in accordance with TS requirements

Contamination control associated with plant operation and maintenance

activities continued to be a program weakness with a violation of NRC

requirements identified.

The violation was an example of violation 50-

321, 366/97-05-01. Failure to Follow Procedure - Multiple Examples.

R1.3 Radioactive Waste and Material Transoortation Activities

'

a.

Insoaction Scope (86750. TI2515/133)

The incpectors reviewed RC program activities associated with packaging

and shipping of radioactive material and waste to either vendor

processing facilities or directly to a licensed burial facility.

The

review included evaluation and verification of radwaste classification

activities, and review of shipping documents.

In addition. the

inspection verified and evaluated implementation of revised 49 CFR Parts

100-179 and 10 CFR Part 71 regulations.

Records for radwaste and material shipments made between April 1 through

June 23, 1997, were reviewed and discussed.

In particular. selected

documentation associated with the following shipments were reviewed and

discussed with responsible licensee representatives.

e

Shipment No. 97-6007. Radioactive material. Low Specific Activity

(LSA). n.o.s.

7 UN2912. Fissile Excepted. April 28, 1997.

e

Shipment No. 97-1010. Radioactive material. LSA, n.o.s. 7. UN2912.

l

Fissile Excepted RQ. April 30, 1997.

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Enclosure 2

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28

e

Shipment No. 97-1012, Radioactive material . LSA. n.o.s. 7. UN2912.

Fissile Excepted. May 7. 1997,

e

Shipment No. 97-1014 Radioactive material . LSA

n.o.s. 7. UN2912.

Fissile Excepted R0. May 23. 1997.

Procedural guidance specified in Radiation Protection (RP) procedure.

62RP-RAD-011-05. " Shipment of Radioactive Material ." Rev.10. effective

June 23. 1997, was reviewed and evaluated against ap]licable

requirements in 10 CFR Part 20, 10 CFR Part 61. 10 C R Part 71 and the

revised 49 CFR Parts 100-179 and 10 CFR Part 71 regulations.

b.

Observations

The licensee's procedural guidance met applicable regulatory

requirements.

Recent revisions to 49 CFR Parts 100-179 and 10 CFR Part 71 regulations were implemented as required.

The inspectors verified

that changes to 49 CFR Parts 100-179 and 10 CFR Part 71 regulations were

incor] orated into approved procedures and implemented as required.

For

the slipping records reviewed, the inspectors verified that shipping

paper documentation was completed arid maintained as specified.

c.

Conclusions

Transportation activities for radwaste and material shipments met

10 CFR 71.5 and recently revised Department of Transportation (DOT)

1

49 CFR 100-179 requirements.

R2

Status of Radiological Protection and Chemistry Facilities and Equipment

R2.1 Radiation Monitor System Calibrations

a.

Insoection Scone (84750)

The inspectors reviewed and evaluated the adequacy of calibration

guidance and resultant data for selected Radiation Monitoring System

(RMS) process and area detectors.

Selected source and electronic

calibration data were reviewed and discussed for the following Unit 2

systems: drywell wide range monitor A and B. i.e., the Containment High

Range Monitors (CHRMs): liquid process: main steamline monitors and

main stack gaseous effluents.

The RMS calibration guidance and results were evaluated against

applicable sections of the FSAR, Technical Specification (TS) and

Offsite Dose Calculation Manual (ODCM) requirements.

In addition,

guidance for the CHRMs was compared against special calibration

requirements specified in NUREG 0737. Clarification of Three Mile Island

I

(TMI) Action Plan Requirements. Table II.F.1-3 Containment High Range

l

Monitors (CHRMs).

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Enclosure 2

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b.

Observations and Findinas

Excluding the CHRMs. no calibration concerns were identified.

Surveillances were conducted at the required frequencies and the

reported results were acceptable.

For the CHRMs data, the inspectors noted that the source used to conduct

the in situ calibration met the 1 -10 R/hr range specified in NUREG 0737. Table II.F.1-3.

However, the in situ calibration by electronic

signal substitution as specified in procedure 57SV-CAL-007-2S "Drywell

High Range Radiation Monitor Loop Calibration." Rev.1. was conducted

for four and not all of the six range decades above 10 Roentgens per

hour (R/hr) as specified in NUREG 0737. Table II.F.1-3.

Based on a

review of a similar issue at another Southern Nuclear Operating Company

nuclear facility, licensee representatives concluded that their test

data for four ranges demonstrated operability of the monitor.

Further.

no changes were made to meet the explicit requirements outlined in

,

NUREG 0737. Table II.F.1-3.

Licensee representatives were unaware if an

exemption was requested from meeting the specific requirements of

NUREG 0737. Table II.F.1-3. but planned to review appropriate licensing

information, and provide that information to the inspectors.

The

inspectors noted that the adequacy of their review of procedure guidance

to meet the ex) licit recuirements of NUREG 0737. Table II.F.1-3 would be

considered an Jnresolvec Item (URI) 50-321, 50-366/97-05-05, evaluate

adequacy of CHRMs electronic signal substitution calibrations following

additional review of the licensee response to Generic Letters 82-05 and

82-10 dated March 17, 1982 and May 5. 1982. respectively.

c.

Conclusions

In general. RMS equipment was calibrated appropriately.

The adequacy of the licensee's review to meet the CHRMs electronic

signal substitution to meet NUREG 0737 requirements was identified as an

URI: 50-321, 366/97-05-05: evaluate adequacy of CHRMs electronic signal

substitution calibrations following additional review of the licensee

commitments.

R3

Radiation Protection and Chemistry Documentation (83750, 84750)

a.

Insoection Scooe (83750. 84750)

The 1996 Annual Radiological Environmental 0)erating Report required by

TSs 5.6.2 and conducted in accordance with tie Section 4 of the ODCM

were reviewed and discussed with licensee representatives.

In addition,

results of the 1996 Anriual Radioactive Effluent Release Report submitted

in accordance with 5.6.3 were discussed in detail.

l

l

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Enclosure 2

30

In addition, the inspectors reviewed recent licensee evaluations

regarding a potential unmonitored liquid release pathway through the

Residual Heat Removal Service Water (RHR SW) heat exchanger system.

b.

Observations and Findinas

The inspectors verified that the 1996 Annual Radiological Environmental

Monitoring Program was implemented appro)riately and the report was

3repared and submitted in accordance witi TS and ODCM specifications.

or two radionuclides. Manganese-54 and Cobalt-60. measured in shoreline

sediment a few miles downstream of the plant discharge, doses were

insignificant fractions of the ODCM limits and represented

inconsequential doses to the environment and public.

No discernible

offsite effect was demonstrated from plant discharges to the environs.

The 1996 Annual Radioactive Effluent Release Report was submitted in

accordance with TS and ODCM requirements.

In general

1996 calculated

doses from effluents were less than 3 percent of the ODCM limits.

No

unplanned releases were identified in the report.

A licensee 10 CFR 50.59 screening evaluation was conducted for a

Jotential unmonitored liquid effluent release pathway through the RHR SW

leat exchanger system.

The licensee's evaluation determined that

potential release pathway would have negligible effect on offsite dose

results for both normal ard accident conditions.

The inspectors

verified ' hat appropriate administrative controls and sampling were

established to ensure any releases were monitored properly and were

within 10 CFR limits.

c.

Conclusions

,

Licensee programs to control, monitor and document liquid and airborne

radionuclide effluent releases were maintained and implemented properly.

'

The Radiological Environmental Monitoring Program sampling analysis and

reporting requirements were implemented effectively and demonstrated

minimal environmental impact.

Projected offsite doses resulting from effluents were well within the

limits specified in the Offsite Dose Calculation Manual and 40 CFP, 190.

R4

Staff Knowledge and Performance in Radiation Protection and Chemistry

R4.1 Maintenance Worker Contamination - Unit 1

a.

Inspection Scooe (92902) (92904l

On May 23. 1997, a maintenance worker became contaminated while

!

l

performing work activities in the Unit 1 torus area.

The inspectors

reviewed MWO 1-97-1186. Repair Leak per Attached Weld Sketch, radiation

work permits 097-0002 and 097-0003. procedures 51GM-MNT-025-05. " General

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Enclosure 2

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31

Welding Requirements For Pressure Boundary Applications," Rev. 4. ED 1,

50AC-MNT-001-05 " Maintenance Program." Rev. 24, 60AC-HPX-004-05.

" Radiation and Contamination Control." Rev. 14, 42FP-FPX-004-05, " Fire

Protection Reviews,~ Rev. 5, and Significant Occurrence Report, SOR

C09702718.

b.

Observations and Findinas

A welder was assigned to conduct a welding repair for a 1.5 inch crack

on a clean radiological waste pipe in the Unit 1 torus area. The

craftsman contacted HP personnel and was told that the area was

contaminated.

The craftsman and a fire watch dressed out in full anti-

contaminated clothing and proceeded to conduct the welding repairs.

After about 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of work the personnel exited the area for lunch.

Both workers conducted a contamination check using the personnel

contamination monitors.

The monitors alarmed indicating both workers

were contaminated.

A short time later, one worker was able to exit with

no contamination indicated.

The second worker was given a whole body

frisk which indicated contamination levels of 95,000 disintegrations per

minute (dpm) on his left shoe, 58,000 dpm on his face and 29,000 dpm on

his forearms.

After four showers, the contamination levels were reduced

to 6,000 dpm on his face. 4,000 dpm on his forearms and his shoes were

disposed of in radioactive trash.

The worker was excluded from the site and was allowed to go home with no

further decontamination.

HP personnel completed a personnel

contamination report and conducted bioassay analysis.

The analysis and

dose calculations revealed that the committed effective dose equivalent

was less than 1 millirem.

The post-event area survey report showed that

smearable contamination levels were as high as 120 mrad /100 square

centimeters.

HP personnel concluded that the smearable levels clearly

exceeded the capacity of single cotton protective clothing considering

the wet working conditions.

l

The inspectors observed that MWO 1-97-1186 specified that the work be

l

performed using RWP 097-0002.

The inspectors reviewed the RWP and

observed that the work conditions specified were routine breach, minor

i

mechanical / electrical /I&C support work.

The inspectors observed that

i

another section of the RWP indicated that no breach was allowed using

l

the protective clothing listed on the RWP.

It was management's

!

expectation that workers contact HP to discuss their specific job to

ensure HP coverage is correct.

The inspectors observed that the RWP was

'

not adequate for the specific work that was identified on the MWO

(welding under wet conditions).

i

l

The inspectors also observed that the RWP was written to cover multiple

!

conditions.

For example, the RWP specified that under certain

conditions booties, gloves, scrubs and hard hat may be appropriate.

Other work conditions listed were boots and gloves to inspect, if

conditioris allow, no protective clothing required for clean areas, and

Enclosure 2

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32

scrubs and single protective clothing may be appropriate for other work.

The inspectors observed that the RWP was written to cover multiple work

conditions and the individual worker was to determine if his specific

work condition was covered by the RWP. The inspectors observed that

broad based RWPs were a common practice.

The inspectors observed that the maintenance personnel who performed the

i

work did not use RWP 097-0002, which was specified on the MWO.

Instead.

l

RWP 097-0003 was used.

The inspectors observed that the work specified

on this RWP. in part, miscellaneous maintenance (no breach), inspection,

vibration readings, oil samples / add oil, crane movement, shaft voltage

reading, fire watch in high radiation / contamination areas. The

inspectors observed that the "WP was not adequate for the welding work

that was identified on MWO 1-97-1186. This RWP was also written in

broad terms similar to RWP 097-0002.

l

The inspectors were informed that HP staff personnel reviewed MW0s and

!

determined what RWPs should be used to conduct the specified work

l

activity.

In this case, an RWP update survey was requested by

,

!

scheduling personnel about two days prior to the scheduled work. The

i

updated survey was not performed and updated results were not available

i

for use. The inspectors were informed that the maintenance personnel

contacted the HP office and inquired about the radiological conditions

of the torus area.

HP personnel used a survey completed on May 19 and

j

informed the maintenance personnel that the contamination levels were

i

less than 1000 dpm per 100 square cm and that a single dress out of

j

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protective clothing would be sufficient. The inspectors were informed

'

that the maintenance personnel did not inform HP about the ty)e of work

j

to be performed (welding) or the extent of the job scope and iP

l

personnel did not inquire about the work. The inspectors concluded that

poor communications may have contributed to the problem.

j

The inspectors were informed that the HP technician usually assigned to

this maintenance team was not at work on the day these maintenance work

activities occurred and that this may have contributed to the problem.

l

The inspectors concluded that obtaining radiological work conditions to

ensure proper HP coverage for the assigned work was a fundamental work

'

i

requirement that was not performed.

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,

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The inspectors considered maintenance personnel failure to discuss the

planned work and job scope with HP personnel. to ensure that correct

radiological controls and processes were inplace for the ' signed work,

a failure to follow ste) 4.2.19 of procedure 50AC-MNT-001-oS.

" Maintenance Program."

Rev.24.

The procedure step required in aart.

that part of the responsibilities to implement the Maintenance

3rogram

.

was to identify the requirements for RWPs for authorized work.

Additionally. HP personnel failed to demonstrate a questioning attitude

with respect to determining what work was to be performed to ensure HP

l

coverage and RWP requirements were adequate.

This was identified as a

negative observation.

Enclosure 2

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33

The inspectors reviewed Significance Occurrence Report (SOR) C09702718

and observed that the report included root cause determination and

recommended corrective actions.

The root cause section of the report

stated in part, that the root causes were 1) inadequate communications

on the nature of the work between Maintenance and HP personnel. 2) upon

finding wet conditions, the worker did not notify HP personnel to

reassess the dress requirements. 3) HP technician assigned to the shift

team was on vacation contributing to the communications barrier.

The

inspectors concluded that the root causes identified were reasonable.

The inspectors followed up on deficiencies identified during their

review of the problem to determine if the deficiencies were identified

during the licensee's review for the SOR.

The ins)ectors observed that

l

no deficiencies were written for the following pro]lems.

The craftsman did not use the RWP specified on the MWO.

e

The RWP used by the craftsman was not adequate for the job.

e

The RWP specified on the MWO was not adequate for the job.

e

Although the SOR adequately identified the root cause of the

,

contamination problem, the reviewers failed to identify and document

'

other deficiencies. This was identified as a negative observation in

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the use of the deficiency card program.

The inspectors observed that there has been several recent individual

contamination events.

The inspectors questioned management personnel

about the 3erformance of HP personnel assigned to the maintenance teams.

A recent clange, since the implementation of maintenance teams, was that

HP coverage for maintenance work is generally provided by HP technicians

assigned to the particular maintenance team.

However, additional HP

personnel are available to provide additional support if needed.

The

inspectors were informed that an Event Review Team (ERT) was assigned to

review this particular contamination problem as well as other recent HP

and contamination problems.

The ERT was to determine if programmatic or

common problems exist for the events and to make recommendatior..; to

management for corrective actions.

This aspect of personnel

contaminations was identified as IFI 50-321, 366/97-05-03: Review of

Licensee's Root Cause Determination and Corrective Actions for Personnel

Contaminations.

c.

Conclusions

The inspectors concluded that a failure to implement maintenance

procedures to ensure that Radiological Work Permit requirements and

Health Physics coverage was adequate for the assigned work activity was

a violation for failure to follow procedure.

This violation was

identified as an example of VIO 50-321, 366/97-07-01: Failure to Follow

Procedure - Multiple Examples.

A negative observation was identified

for Health Physics personnel failure to demonstrate a questioning

attitude to ensure radiological controls were adequate for an assigned

l

Enclosure 2

_ _ _ _ . _ _ _ _ . _ . _ . -

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_ . _ . _ _ _ _ _ _ . . _ . . _ . _ _ . . . _

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34

,

,

work activity and for the failure of personnel to identify and document

.

several deficiencies surrounding the personnel contamination.

R5

Staff Training and Qualifications in Radiological Protection and

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Chemistry

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R5.1 Hazardous Material Trainino

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a.

Insoection Scone (86750. TI 2515/133)

l

Training provided to meet the requirements of 49 CFR Part 172 Subpart H

were reviewed and discussed with licensee representatives.

,

b.

Observations and Findinas

From review of training records, the ins)ectors verified that hazmat

training was provided to a new radwaste iP foreman.

From review of

training material presented. the inspectors confirmed that recent DOT

changes to shipping and packaging requirements were included in the

,

i

training.

c.

Conclusions

Appropriate hazmat training was provided to personnel handling and

,

packaging radioactive materials for transport.

R7

Quality Assurance in Radiation Protection and Chemistry Activities

.(83750, 84750)

R7.1 Audits

a.

Insoection Scooe (83750)

The inspectors reviewed and discussed audits of Health Physics.

Chemistry and Radioactive Waste program areas.

l

The inspectors reviewed and discussed the following Safety Audit and

Engineering Review (SAER) reports:

e

Audit Report 97-CH-1. Audit of Chemistry, dated March 12, 1997.

l

e

Audit Report 97-RW-1. Audit of Radioactive Waste Program, dated

March 25, 1997.

e

Audit Report 97-HP-1. Audit of Health Physics & Radiation

Protection Program dated June 2. 1997.

I

i

The inspectors assessed the scope, thoroughness and status of corrective

1

actions of the audits.

.

I

Enclosure 2

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35

b.

Observations and Ft,dinas

l

Audits consisted of interviews. record review and direct observations by

l

qualified audit personnel.

Audits were performance-based and the audit

contents were adecuate samples of program attributes.

The inspectors

verified that fincings were characterized appropriately in the reports,

were reviewed by licensee management and corrective actions appeared

adequate and timely.

c.

Conclusions

Audits of chemistry, radwaste and radiological control programs were

thorough and findings were corrected in a timely manner.

R7.2 Effluent Measurement and Radioloaical Environmental Monitorina Proaram

Ouality Control Activities

a.

Insoection Scooe (83750)

Counting room instrumentation quality control checks were reviewed and

discussed.

Minimum Detectable Concentrations (MDCs) for selected gaseous and

particulate radionuclides in airborne effluents were verified against

limits detailed in the ODCM.

Pesults of the 1996 Inter-laboratory Comparison Program for the

Radiological Environmental Monitoring Program (REMP) as required by

Section 4 of the ODCM were reviewed and discussed.

b.

Observations and Findinas

Quality control daily checks to verify system performance were conducted

for counting room instrumentation in accordance with licensee

procedures.

Based on detector efficiencies, sample volume and counting

'

time, the MDCs for the radionuclides reviewed met the established

detection criteria for airborne effluent measurements.

The inspectors noted and discussed the poor performance in REMP OC

analysis results. The report documented numerous examples of the cross-

check samples which were processed by an approved off-site laboratory

which exceeded normalized range or deviation warning and control limits.

The inspectors noted that no site representatives were knowledgeable of

the specific corrective actions being taken in regard to the REMP OC

sample analysis results.

Subsequent discussions indicated that

corrective actions appeared appropriate.

l

Enclosure 2

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36

c.

Conclusions

Counting room QC activities were conducted in accordance with approved

procedures and demonstrated detector and analysis system operability.

Supervisory oversight of the REMP OC activities by site personnel were

minimal.

R8

Miscellaneous Radiation Protection and Chemistry Issues (92904)

R8.1

(Closed) Insoection Followuo Item (IFI) 50-321. 366/96-10-10: review

licensee evaluations regarding gas geometry QC sample analyses and main

steam line monitor response biases.

In response to a lack of a gas QC

analysis in the laboratory QC program, procedure 64CH-0CX-001-05.

~ Quality Control for Laboratory Analysis." Rev. 3. Attachment 10 was

revised to include quantitative analysis of a gas quality control cross-

check sample on a biennial frequency.

For identified biases regarding

the main steamline monitors, the licensee procured a new NBS traceable

calibration source for calibration activities.

Results of the most

recent U2 MSL calibrations verified a significant reduction in the

identified bias.

Licensee representatives stated that additional

modifications to existing equipment were being evaluated to allow

adjustments to the system thereby improving accuracy of the readings.

Based on licensee actions, the inspectors noted this item would be

considered closed.

S2

Status of Security Facilities and Equipment (71750)

The inspectors toured the protected area and observed that the perimeter

'

fence was intact and not compromised by erosion nor disrepair.

The

fence fabric was secured and barbed wire was angled as required by the

licensee's procedures.

Isolation zones were maintained on both sides of

the barrier and were free of objects which could shield or conceal an

individual.

The inspectors observed that personnel and packages

entering the 3rotected area were searched either by special purpose

detectors or )y a physical patdown for firearms, explosives and

contraband.

Badge issuance was observed. as was the processing and

escorting of visitors.

Vehicles were searched, escorted and secured as

described in applicable procedures.

The ins)ectors concluded that the areas of security inspected met the

applica)1e requirements.

V. Manaaement Meetinas

X.2

Review of UFSAR Commitments

1

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

Enclosure 2

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37

practices, procedures and/or parameters to the UFSAR description.

While

performing the inspections discussed in this re) ort, the inspectors

reviewed the applicable portions of the UFSAR tlat related to the areas

inspected.

The inspectors verified that the UFSAR wording was

consistent with the observed plant practices, procedures, and/or

parameters.

X.3

Exit Meeting Summary

The inspectors presented the inspection results to members of the

licensee management at the conclusion of the inspection on July 11.

1997. The license acknowledged the findings presented. An interim exit

was conducted on June 6 and 27, 1997.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary.

No proprietary

information was identified.

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4

Enclosure 2

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

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Anderson, J. , Unit Superintendent

Betsill. J.

Assistant General Manager - Operations

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Breitenbach, C. Engineering Support Manager - Acting

Curtis. S.

Unit Superintendent

{

.

Davis., D.

Plant Administration Manager

Fornel. P.

Performance Team Manager

J

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Fraser. 0.. Safety Audit and Engineering Review Supervisor

Hammonds. J. , Operations Support Superintendent

Kirkley.

W.. Health Physics and Chemistry Manager

Lewis, J., Training and Emergency Preparedness Manager

Madison. D., Operations Manager

Moore

C.. Assistant General Manager - Plant Support

l

Reddick. R.. Site Emergency Preparedness Coordinator

'

Roberts. P., Outages and Planning Manager

Thompson,

J., Nuclear Security Manager

'

Tipps.

S., Nuclear Safety and Compliance Manager

Wells. P.. General Manager - Nuclear Plant

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying. Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62700: Maintenance Implementation

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

'

IP 83750:

Occupational Radiation Exposure

IP 84750:

Radioactive Waste Treatment, and Effluent and Environmental

Monitoring

IP 86750:

Solid Radioactive Waste Management and Transportation of

Radioactive Materials

IP 92700:

Onsite Follow-up of Written Reports of Nonroutine

Events at Power Reactor Facilities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance / Surveillance

IP 92903:

Followup - Followup Engineering

IP 92904:

Followup - Plant Support

TI 2515/133:

Implementation of Revised 49 CFR Parts 100-179 and 10 CFR Part 71

Enclosure 2

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ITEMS OPENED. CLOSED. AND DISCUSSED

Ooened

50-321. 366/97-05-01

VIO

Failure to Follow Procedure - Multiple Examples

50-321. 366/97-05-02

IFI

Installation of the Wrong Type of Connector on

Wide Range Monitor 011K621A

50-321, 366/97-05-03

IFI

Review of Licensee's Root Cause Determination

and Corrective Actions for Personnel

Contaminations

50-321, 366/97-04

URI

Determine the Reportability of Licensee

Identified Deficiencies With Respect to IN 92-

18. Potential for Loss of Remote Shutdown

Capability During a Control Room Fire

50-321, 366/97-05-05

URI

Evaluate licensee review and actions regarding

current CHRMS electronic calibration against

licensee commitments to meet NUREG 0737 Item

II.F.3-1

Closed

50-321. 366/96-14-04

IFI

potential deficiencies in the High Pressure

Coolant Injection (HPCI) surveillance procedure

50-321. 366/96-14-03

VIO

failure to implement configuration control

'

requirements - multiple examples

50-321, 366/96-15-03

IFI

resolution of RCIC HPCI turbine speed control

drift

50-321. 366/96-12-03

VIO

Failure to Follow Procedure for Implementation

of the Maintenance Rule.

50-321, 366/96-10-10

IFI

Review Licensee Evaluations Regarding Gas

Geometry QC Sample Analyses and Main Steam Line

Monitor Response Biases.

50-321/97-02

LER

Less than Adequate Procedure Results in a

Condition Prohibited by TS.

Discussed

50-321. 366/96-12-01

VIO

Failure to Include Ali Structures. Systems, and

Components in the Scope of the Maintenance Rule

!

as Required by 10 CFR 50.65

1

Enclosure 2

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50-321, 366/96-12-02

VIO

Failure to Establish Adequate Performance

Criteria for S.C. Risk Significant Functions

50-321. 366/96-12-04

IFI

Failure to Provide Acequate Procedure for

Implementation of Maintenance Rule Requirements

j

50-321. 356/96-12-05

IFI

Followup on Licensee Actions to Provide

Performance Criteria for Structures After

Industry Resolution of this Issue

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Enclosure 2

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a