ML20216E798

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Insp Repts 50-321/97-12 & 50-366/97-12 on 971228-980207. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20216E798
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 03/10/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20216E778 List:
References
50-321-97-12, 50-366-97-12, NUDOCS 9803180165
Download: ML20216E798 (55)


See also: IR 05000321/1997012

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-321. 50-366

License Nos: DPR-57 and NPF-5

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Report No: 50-321/97-12. 50-366/97-12

Licensee: Southern Nuclear Operating Company. Inc. (SNC)

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Facility: E. I. Hatch Units 1 & 2 i

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Location: P. O. Box 2010

Baxley. Georgia 31515

Dates: December 28, 1997 - February 7. 1998

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Inspectors: B. Holbrook. Senior Resident Inspector  !

J. Canady. Resident Inspector

C. Rapp. Team Leader (Sections E3.1 thru E3.12)

G. Kuzo. Senior Radiation Specialist (Sections

R1.1. R1.2. R5.1 and R7.1)

Accompanying Inspectors: T. Fredette. Resident Inspector

approved by: P. Skinner. Chief. Projects Branch 2

Division of Reactor Projects

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Enclosure 2

9803180165 980310

PDR

G ADOCK 05000321

PDR

EXECUTIVE SUMMARY

Plant Hatch. Units 1 and 2

NRC Inspection Report 50-321/97-12, 50-366/97-12

This integrated inspection included aspects of licensee operations.

engineering, maintenance, and plant support. The report covers a 6-week

period of resident inspection and region-based specialist inspection. In

addition, the results of an engineering inspection conducted at your corporate

headquarters in December 1997 are included.

Ooerations

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e Operator response to the 2A Emergency Diesel Generator (EDG) fire was

good. Maintenance evaluation of the cause of the fire and subsequent

recommendations for surveillance testing were also good (Section 02.1).

e The EDG procedural precautions contained ambiguity related to running the

EDGs unloaded, or at low load (Section 02.1).

e The inspectors concluded that the Nitrogen Supply System for the

Containment Atmospheric Dilution System (CAD) was operable. However, the

. system was not well-maintained. Violation (VIO) 50-366/97-12-02. Failure

to Implement Changes to Vendor Manual, was identified (Section 02.2).

l e The inspectors observed during a walkdown of the CAD system that the

Technical S)ecification (TS) surveillance requirements (SR) for both

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units were )eing met. All valve positions checked in the main control

l room and locally were in their required position (Section 02.2).

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l e An example of VIO 50-366/97-12-09. Failure to Follow Procedure - Multiple

Examples, was identified. Operations failed _to submit a timely

deficiency card for a frozen safety-related nitrogen pressure control

l valve (Section 02.2).

l e The Plant Review Board (PRB) organization and function met Updated Final

l Safety Analysis Report (UFSAR) requirements. The 10 CFR 50.59

l evaluations reviewed were thorough and detailed. Equipment reliability

and corrective action meetings were effectively focused. Equipment

problems were being corrected and management and PRB members demonstrated

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a strong safety focus for equipment availability and reliability

(Section 07.1).

Maintenance

e Maintenance personnel _and Plant Equipment-Operators exhibited excellent

procedural familiarity for the isolation of the instrument air supply

l outside the power block. Appropriate compensatory measures were taken

for the partially opened fire door to the Emergency Diesel Generator day

tank room (Section M1.2).

Enclosure 2

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e Instrumentation and Control personnel adherence to procedural

i instructions during reactor vessel water level reference leg backfilling

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activities was good and work activities were performed in a 3rofessional <

manner. Appropriate Technical Specification actions were tacen during l

these activities (Section M2.1). '

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e Maintenance and engineering personnel 3rovided excellent support for the

trouble shooting and repair of the 2C Emergency Diesel Generator

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following a failure to start. Procedures were used, supervisory

oversight was evident and all Technical Specification requirements were

met (Section M2.2).

e The inspectors concluded that the pre-test briefing for a High Pressure

Coolant Injection Test was satisfactory. An improvement was observed in

operato r.hree-part communications during the test. Supervisory

oversig:4 during the test was evident (Section M3.2).

e The 10 CFR 50.72 notification for the inoperable Unit 2 High Pressure

Coolant Injection System was appropriate. All the surveillance test

acceptance requirements were met (Section M3.2).

  • Due to a lack of attention to detail, a surveillance procedure frequency

change form was not submitted. This resulted in a failure to perform

weekly RPS channel test switch functional tests as committed to in a

General Electric (GE) Licensing Topical Report. This was identified as

NCV 50-321/97-12-03, Failure to Follow Procedure for Scheduling Weekly

Testing of RPS Scram Test Switches (Section M3.3).

Enaineerina

e The inspectors concluded that the licensee had taken the appropriate

action in addressing the 10 CFR 21 issue related to GE Type CR120 AD

relays (Section E2.1). I

e The inspectors concluded that engineering personnel demonstrated

excellent observations for problem identification on the Standby Liquid

Control and Standby Plant Service Water systems. Corrective actions were

timely; site maintenance and engineering and corporate engineering

support was excellent (Section E2.3).

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e The Significant Occurrence Report associated with the review of the

Traversing Incore Probe nitrogen purge valve issue was good. The

determination that the valve could be removed from the lis'/,9 of drywell

isolation valves was appropriate (Section E2.4).

e VIO 50-321, 366/97-12-05. Failure to Include Nitrogen Valves in a Test l

Program In Accordance with 10 CFR 50.Section XI of Appendix B. Test

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Cantrol, was identified (Section E2.5).

l e VIO 50-321, 366/97-12-06. Insulation on Nitrogen Supply Piping Not

l Installed in Accordance with Drawings, was identified (Section E2.5). I

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e The licensee's followup of the cycle-dependent SLMCPR issue was adequate.

The licensee was knowledgeable about the subject and took conservative

actions to correct possible safety deficiencies (Section 3.8).

e Although the RBM channels were operable during this period, and

administratively required after the licensee became aware of the problem._

the TS requirement was not implemented until after the licensee TS

-amendment request of May 9, 1997 (Section E3.12).

Plant Suncort

e Radiological controls for normal opnam e J for routine radioactive

waste (radwaste) processing, storage ar.c trannortation activities met-

procedur01. Technical Specification and 10 CFR Part 20 requirements

(Section R1.1).

e Current radiological environmental monitoring program (REMP) equipment.

instrumentation, and operations met Offsite D>se Calculation Manual

(ODCM) requirements (Section R1.1),

e The Radiation Protection Chemistry technician observed taking a drywell

grab sample was professional and knowledgeable of procedural

requirements. Procedural weaknesses were identified for guidance

associated with actions to take when noble gas readings exceed the

acceptance criteria (Section R1.3).

e A violation was identified for failure to dispose of licensed material in

accordance with 10 CFR 20.2001(a) requirements (Section R1.2).

e The limited use of automated gc.ma-sensitive equipment to conduct surveys I

of aggregate U1 Radwaste Building concrete debris released to the onsite  !

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landfill was identified as a program weakness (Section R1.2).  ;

e Technician'and management interpretations of radiation control procedural

requirements were inconsistent (Section R1.2).

  • Prior to June 1997, management oversight of the release of U1 Radwaste

building debris from the Waste Separation and Temporary Storage facility

was limited (Section r;.2). .

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o An example of VIO 50-321. 366/97-12-09. Failure to Follow Procedures -

Multiple Examples, was identified for a failure to follow procedures for

documenting release surveys (Section R1.2).

e No exposure rates above background were identified during confirmatory i

surveys of the two landfill trenches where the U1 Radwaste Building l

concrete debris was buried (Section R12).

Enclosure 2  !

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e The fission product monitoring (FPM) system trouble shocting activities

led by chemistry with maintenance. and operations support was not well-

planned or coordinated. The problem solving team convened by Nuclear

Safety and Compliance conducted an excellent investigation for the root

causes of the FPM and commercial grade oxygen analyzer problems. NCV 50-

321/97-12-08. Personnel Error Results in a Breach of Drywell Integrity,

was identified (Section R2.1).

e The investigations for personnel contamination reports were generally

adequate. The recommended corrective actions were not always thorough i

and comprehensive and some were narrow in focus. Some reports did not

have any recommended corrective actions (Section R3).

e Training provided to contract Health Physics technicians involved in

surveying. releasing, and disposing of U1 Radwaste Building concrete in

the onsite landfill was current and met procedural and 10 CFR Part 19 l

requirements (Section R5.1). I

o Licensee health physics technicians appropriately identified the disposal

of licensed material in the onsite landfill as a deficient radiological

condition (Section R7.1).

  • An example of a VIO 50-321. 366/97-12-09. Failure to Follow Procedures -

Multiple Examples, was identified for failure to follow administrative

control procedures for deficiency c;- d initiation (Section R7.1).

e Violation 50-321, 366/97-12-10 was identified for failure to maintain

decommissioning records in accordance with 10 CFR 50.75(g) requirements

(Section R7.1).

  • The inspectors concluded that the Self Contained Breathing Apparatuses

were being properly maintained. The emergency facilities were maintained

in a state of readiness and the telephone communications checks were

satisfactory (Section P2.1).

e The ins)ectors concluded that the areas of security inspected met the

applica]le requirements (Section S2).

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Reoort Details

Summary of Plant Statul

Unit 1 operated at 100% rated thermal power (RTP) for the report period.

except during routine testing activities.

Unit 2 began the report period at 100% rated thermal power (RTP). Power was

reduced to approximately 95% on January 6 for removal of the 2B 4th Stage-

Feedwater Heater from service to effect re

Separator Reheater (MSR) drain tank valve.Power pairs of

wasthe 2nd Stage

restored Moisture

to PJP on

January 7. The unit remained at 100% RTP for the remainder of the reporting j

period, except during routine testing activities.

I. Operations i

01. Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent reviews of ongoing plant operations.

In general, the conduct of operations was professional and safety-

conscious: specific events and observation are detailed below.

02 Operational Status of Facilities and Equipment

02.12A Emeraency Diesel Generator (EDG) Exhaust Manifold Fire

a. Insoection Scooe (71707)(92901)(37551)

The inspectors assessed licensee actions following an engine exhaust

manifold fire that occurred during a surveillance test of 2A EDG. A

review was conducted of maintenance and operations recommendations. fire i

incident reporting, and root cause determinations for this fire. I

b. Observations and Findinos

A fire occurred in the 2A EDG exhaust during a semi-annual test conducted

November 22, 1997. The EDG was run unloaded while maintenance personnel j

attempted to adjust and set the " Governor Not at Synchronous Speed" ~

annunciator switch. The EDG is designed to run for extended periods of I

time at no load: however. lube oil accumulates in the exhaust manifold if

the engine is run too'long with no load. During the annunciator switch

adjustment. the engine was run for more than 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> at no load. Lube I

oil collected in the exhaust manifold and subsequently leaked through a

manifold flange, soaking the insulation. and eventually ignited.

Operators reported the fire, secured the EDG. and took appropriate steps

to extinguisi the fire with hand held extinguishers. A fire incic'ent '

report was generated in accordance with DI-FPX-04-0694N. " Fire Incident

Reports." Revision (Rev.) 0. The inspectors reviewed the report and ,

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Enclosure 2  ;

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found that there was confusion.in documenting the actual source of the

fire. The report spec.fied fuel oil as the cause. However, discussions

with maintenance personnel stated that the cause was accumulated lube

oil. Operability of the EDG was not compromised. The fire caused slight

damage to the insulation.

The inspectors reviewed the licensee's procedures for running the EDGs.

All procedures include precautions for the operators to closely observe

engine operation, and to minimize running the engine for " extended

periods of time" at low loads. The EDG procedure precautions contained

ambiguity related to running the EDGs unloaded, or at low load. No clear

definition existed for " extended period of time." The inspectors

discussed this ambiguity with operations personnel. Maintenance

personnel had made informal recommendations to operations regarding

running the EDGs for surveillance purposes including surveillance testing

with maintenance 3ersonnel present to aid in observing and

troubleshooting a] normal EDG behavior. The licensee contacted the vendor

to determine an appropriate "exterded period of time" at low loada.

This issue is identified as Inspector Follow-up Item (IFI) 50-321,

366/97-12-01. Review of Operations. Maintenance and Engineering Actions

for Long-Term Resolution of Running the EDGs Unloaded or at Low Loads,

c. Conclusions

The inspectors determined that the response to the 2A EDG fire by i

operators was good. Maintenance evaluation of the cause of the fire, and  !

subsecuent recommendations for operations were also good. The EDG '

procecural precautions contained ambiguity related to running the EDGs

unloaded, or at low load.

02.2 Enaineered Safety Feature Walkdown

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a. Insoection Scooe (71707)

The inspectors reviewed selected parts of the nitrogen inerting system

for Unit 1 and Unit 2. The activity included a review of plant drawings

H-16000 for Unit 1 and H-26083 for Unit 2: procedures 34SV-SUV-011-IS.

" Primary Containment Integrity Demonstration." Rev. 1: 34SV-SUV-011-2S. i

" Primary Containment Integrity Demonstration." Rev. 8. ED 1: 34S0-T48- i'

002-2S, " Containment Atmospheric Control and Dilution." Rev 16:

34S0-T48-002-IS. " Containment Atmos)heric Control and Dilution." Rev.17. )

ED -1, and 52IT-MME-006-0S. " Safety Relief Valve 8ench Test Rev.14. The

ins)ectors conducted a system and component performance history review:

wal ced down parts of the. system to verify that valves were in the

recuired position: and verified that the Technical Specification (TS) and

Upcated Final Safety Analysis Report (UFSAR) requirements were met. 1

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b. Observations and Findinas

The Containment Atmosphere Dilution (CAD) system functions to maintain

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combustible gas concentrations within the primary containment at or below

the flammabi.ity limits following a postulated Loss of Coolant Accident

-(LOCA). Unit I has a safety-related CAD system and Unit 2 uses safety -

l- related hydrogen recombiners. A Unit 2 nitrogen supply. system supplies

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one of the two r@ uired Unit 1 CAD systems. The Unit 2 nitrogen system

is also safety-related.

The inspectors reviewed procedure 521T-MME-006-0S and observed that the

Applica3ility section of the procedure indicated that the procedure was

applicable, but not limited, to Units 1 and 2 safety relief valves. (SRV)

listed in Attachment 1. Eleven Unit 1 SRVs for the CAD system were

listed and one SRV (1T48-F072) was not listed. For Un;t 2. there were

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three SRVs listed and at least five SRVs indicated on plant drawing H-

26083 that were not listed. The inspectors did not find any plant

3rocedure that contained the required set point for any of the SRVs.

10 wever, the procedure required that valve name plate data be recorded

and used as a set point reference. The inspectors concluded that the

procedure was not specific but was adequate to perform the required

tests.

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The ins)ectors "eviewed Unit 1 TS 3.6.1.2 which required verification of

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each CA) subsystem manual power-operated, and automatic valve in the

flow path that is not locked, sealed or otherwise secured, to be in (or

can be aligned to) the correct position. The inspectors reviewed

procedures 345V-SUV-011-1S and -2S for Units 1 and 2. respectively, which

implemented the TS requirement. The inspectors observed that the

procedures did not contain the pressure control valves (PCVs) for the

flow path indicated on the drawings for both units. The inspectors

discussed this with licensee management and engineering person.nel. The

inspectors were informed that the procedure would be reviewed to

determine its adequacy. The inspectors concluded that the PCVs had the

potential to be inadvertently mispositioned but could be returned to the

correct position if required.

On January 20. operators placed the Unit 2 nitrogen storage tank on

manual pressure control because PCV F466 was frozen and would not control

tank pressure. The tank pressure is normally controlled by PCV F466 in

automatic. The inspectors were informed that on or about January 15.

operations personnel filled the nitrogen storage tank from a vendor tank

truck. The licensee believed that the tank may have been overfilled,

which caused the safety relief valve to open on January 20. Flow through

the relief valve caused excessive flow through the PCV. causing it to

freeze. Operations personnel opened the PCV bypass valve and controlled

tank' pressure in manual. The PCV was isolated, safety-tagged, and

removed from service so that it could thaw. The PCV was placed back in

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service on January 21. On February 1. the PCV would not control tank

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pressure and a relief valve lifted. The PCV valve was removed. repaired

and placed back in service on February 3.

The inspectors observed that when PCV F466 froze on January 20. no

deficiency card was initiated-to document the problem. The inspectors

,. reviewed procedure 10AC-MGR-004-05. " Deficiency Control System." Rev.10.

l and observed that step 8.3.1.1 requires, in ) art, that the person who

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identifies a deficiency is to report it to tie Plant Dispatcher within

! one hour. The inspectors observed that a deficiency was reported on

l about January 21 after the inspectors discussed the problem with

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operations supervision. This failure to identify a deficiency was

identified as an exam)1e of VIO 50-321, 366/97-12-09. Failure to Follow

Procedure - Multiple Examples. The failure to document deficiencies for

the nitrogen system was a previously identified 3roblem. A failure to

submit deficiency cards was also identified by tie NRC and is discussed

in Section R7.1 of this Inspection Report.

On February 1. operations personnel again observed that PCV F466 was not

properly controlling the Unit 2 nitrogen tank aressure. A deficiency

card was initiated for maintenance to disassemale, repair and reassemble

the PCV. The inspectors reviewed Maintenance Work Order (MWO) 2-98-356

and procedure 52PM-MME-012-05. " Fisher Pressure Regulator Valve

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Maintenance." Rev. 1. which was used to repair the PCV. The inspectors

observed that step 7.3.26 required the procedure user to contact the

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responsible engineering personnel to determine the operating pressure for

the applicable valve. Step 7.3.27 stated, in part, to adjust the

operating pressure of the valve in accordance with the operating pressure

determined in the previous step. In this case, maintenance personnel

failed to contact engineering to determine the operating pressure of the i

valve. Instead, they used information stated in procedure 34S0-T48-002- )

'2S, which indicated that the normal tank pressure was between 125 and 140

psig, to set the PCV pressure. The inspectors discussed this observation

with maintenance and operations personnel. The inspectors were informed

that the two steps ir the maintenance procedure would be marked not

applicable (N/A) due to the fact that the procedure user could determine

a pressure range (125 to 140) identified in system operating procedure

3450-T48-002-2S. Maintenance management informed the inspectors that the i

practice of marking procedure steps N/A would be reviewed for l

improvement. The inspectors concluded that marking the procedure steps l

N/A was allowed by procedure. However, using alternate means of '

determining system component setpoints was not a good practice.

The inspectors reviewed table 1-1 of the system vendor manual and

ob e yed that the pressure set point for PCV-1 (PCV F466) was listed as

145 psig. Maintenance personnel informed the inspectors that they had ,

l set the pressure for PCV F466 at about 132 asig. The system engineer

I informed the inspectors that the pressure s1ould be set at about 138 psig  :

I and that a higher pressure caused the relief valves to open on '

overpressure. However, in this case, the current set point would be i

satisfactory. Maintenance and engineering persorinel informed the i

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. inspectors that a desired pressure set point below the vendor manual

recommended value was recognized over a year ago. The vendor manual was

never revised to reflect the lower set point requirement based upon

system performance history. The inspectors reviewed 3rocedure

20AC-ADM-003-05 ' Vendor Manual Review and Control." lev. 4. and observed ]'

that step 8.7.1 states in part, that-individuals who identify a need for

a vendor manual change may submit the information as a proposed As-Built

Notice (ABN). per applicable procedure. This action was never completed.

and the requirement of 10 CFR 50.. Appendix B. Criterion VI,.to ensure

changes to the vendor document was not met. This. problem was identified

as VIO 50-366/97-12-02. Failure to Implement Changes to Vendor Manual.

The inspect ' review of procedures 34S0-T48-002-15 and -2S identified

that the i s page numbering for.some sections of the Unit 1 procedure

was not co- act. Operations supervision was informed of this

administrauve error.

The inspectors' review of procedure 30AC-0PS-001-0S. ' Control of

Equipment Clearances and Tags." Rev. 17. used to isolate PCV F466 for

repair, verified that the tags were properly placed. One minor

administrative error was observed in that the plant drawing referenced on

the clearance sheet was H20093 and the correct drawing was H26083.

Operations supervision was informed of this error.

Other problems associated with the Nitrogen Inerting System are discussed

in Section E2.5 of this report.

c. Conclusions

The inspectors observed that the TS surveillance requirements (SR) for

both units were being met. All valve positions checked in the main j

control room and locally were in their required position.

The inspectors concluded that the Nitrogen Supply System for the

Containment Atmospheric Dilution System was operable. However, the

system was not well maintained. VIO 50-366/97-12-02. Failure to i

Implement Changes to Vendor Manual, was identified.

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Also, a failure to identify a deficiency was identified as an example of i

VIO 50-321, 366/97-12-09. Failure to Follow Procedure - Multiple 1

Examples.

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07. Quality Assurance In Operations

07.1 Plant Review Board (PRB). Eauipment Reliability. Corrective Actions. and

Information Meetinos

a..Insoection Scooe (71707)(40500)

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Tlie inspectors reviewed Hatch Updated Final Safety Analysis Report

(UFSAR) section 13.4. Review and Audit, that describes the organization

and function'of.the PRB and section 13.4A. Edwin I Hatch-Units 1 and 2

Plant Review Board Charter, and verified that the specified actions and

requirements were being met. The inspectors verified that the equipment i

reliability. meeting addressed equipment with demonstrated deficiencies,

goals and standards for inclusion and exclusion into the program were

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being met, and management was informed of the identified deficiencies.

b. Observations and Findinas

The inspectors attended three PRB meetings. The inspectors observed that

appropriate members were in attendance with the required departments

represented. The inspectors observed that the meetings were held more ,

frequently than required by the UFSAR. Safety issues were discussed and I

procedure changes were reviewed. The 10 CFR 50 59 evaluations reviewed

by the inspectors were thorough and detailed.

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The inspectors attended one equipment reliability meeting (Reg-00401297),-

which focused on significant occurrence reports (SOR) initiated due to

equipment reliability problems. Three SORS were reviewed by Janel i

members for consideration for addition to the equipment relia]ility list.

Engineering support Jersonnel. presented an overview of their

investigation into tie equipment problems.

The inspectors also attended an information meeting which was part of

plant management's effort to meet with all site employees early in 1998.

The inspectors observed that among the topics discussed were:

organizational goals, management's expectations, regulatory compliance,

-industrial safety, im) roving appearance and housekeeplng, and improved

performance for healti physics and radiological controls. Plant

management clearly expressed expectations-for improved performance in all

areas of plant operations.

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c, Conclusions

The inspectors concluded that the Plant Review Board (PRB) organization

and function met UFSAR requirements. The 10 CFR 50.59 evaluations were

thorough and detailed. Equipment reliability and corrective action

meetings were effectively focused. Equipment problems were being

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Enclosure 2

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. corrected, management and PRB members demonstrated a strong safety focus

i for equipment availability and reliability. Plant management clearly

l' expressed expectations for improved performance in all areas of plant

operations.

l' II. Maintenance

M1 Conduct of Maintenance

! M1.1 General Comments i

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a. jnsDeCtion SCQDe (62707)

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! The inspectors observed or reviewed all or portions of the following work

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activities: i

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  • MWO 1-98-0205: Investigate Unit I high drywell oxygen

. MWO 1-97-2416: Clean and eddy current' test 1T41-8004B cooler.

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  • MWO 1-98-0088: Investigate EHC puna 18 failure to start

l- * MWO 1-98-0011: . Fire Pump 1B will not develop rated flow

l * MWO 1-98-0012:' Fire Pump 1B tripped on overspeed

l- * MWO 1-97-1737: Replace degrading relays

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b. Observations'and Findinas

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The inspectors found that the work was performed with the work packages

( present and being actively used.

c. Conclusions on Conduct of Maintenance

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Maintenance activities were generally completed thoroughly and

professionally. No deficiencies 'were identified by the inspectors.

M1.2 Reoair/Reolacemant of Instrument Air Line in Vicinity of Emeraency Diesel

Generator (EDG) Buildina

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a. Insoection Scope (62707)

.. The' inspectors reviewed validation procedure 51CM-MNT-001-05. " Isolation i

of Instrument Air Supply Outside the Power Block." and Maintenance Work j

L Order (MWO) 1-98-0058. These documents were associated with the repairs  !

to a. leaking instrument air line outside the power block. The inspectors  !

also observed portions of.the work activity and discussed the work  ;

activity with maintenance supervision, j

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p b. Observations and Findinas

On January 26. the inspectors observed work activities associated with

the repair / replacement of a section of underground instrument air piping.

The section of piping was replaced due to an air leak caused by

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corrosion. Components of Technical Specification (TS) systems that had

the potential of being affected by the work activities were the level

indication for the EDG storage tanks and the minimum flow valves for the

Plant Service Water and the Residual Heat Removal (RHR) Service Water

minimum flow valves.

The inspectors observed that Plant Equipment Oprators (PEO) supported '

maintenance personnel in the isolation of instrue, ant air headers and the

placement of clearance tags. The inspectors also observed the presence

of maintenance engineering support during the procedural isolation of

the instrument air headers and the connection of temporary tubing with

filters and pressure gauges by maintenance craft persons. The temporary

tubing was used to cross connect service air to instrument air.

The inspectors observed that procedure 51CM-MNT-001-0S provided guidance

for placing a temporary air hose from service air to an instrument air

connection in + e 2C EDG day tank room. This work activity resulted in

the inability to fully close the fire door associated with the room. The (

inspectors observed that the appropriate compensatory measures s)ecified j

in the Fire Hazard Analysis were taken for the partially opened EDG day -

tank room door.

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The inspectors observed from the review of MWO 1-98-0058, discussions

with maintenance supervision. and observance of the work activity that

approximately 25 feet of instrument air piping was replaced. The piping )

connection was fabricated outside of the excavated trench. The

inspectors were informed that the section of piping was re31 aced in order

to minimize the number of weld joints to be performed in t1e excavated

trench.

c. G.ggplusions

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Maintenance personnel and PEOs exhibited excellent procedural famillarity

for the isolation of the instrument air supply outside the power block. i

Appropriate compensatory measures were taken for the partially opened

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fire door to the EOG day tank room.

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Backfillf;? of Reactor Vessel Water Level Reference lag

a. Insoection Scoce (62707)(92902)

The inspectors reviewed procedure 57CM-MIC-002-15. "Backfilling of Water

Level Instruments." and Technical Specification 3.3.3.1. " Post Accident

Monitoring (PAM) Instrumentation." This review was associated with the

inoperability and backfill of a PAM reactor vessel water level channel.

Enclosure 2

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g 1

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Is 9

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~ b. Ob'servations and Findinas ,

l On December 30. the inspectors observed the backfilling of the reactor

pressure vessel (RPV) reference leg associated with water level

i

condensing chamber 1821-D002. This reference leg was backfilled due to -

abnormally high. level readings in the control room for indications from i

!

level transmitters (LT) 1C82-N110 and 1B21-N027.

L The inspectors observed that the Instrumentation and Control (I&C)

. technicians performed the backfill activity in accordance with procedure

l 57CM-MIC-002-1S. Subsequently. operations personnel performed a channel

check and confirmed. proper indication.

I

c. Conclusions

l

'

The I&C personnel adherence to procedural instructions was good and work '

activities were performed.in a professional manner. The appropriate TS

actions were:taken during this evolution.

M2.2 Emeraency Diesel Generator 2C Failure to Start

L

a, Insoection Scone (62707)

The inspectors observed part of the maintenance activities )ost

maintenance testing and operability surveillance on the 2C E E following q

l- , a failure to start during a surveillance conducted on January 20. The:

inspectors reviewed procedures 52SV-R43-001-05. " Diesel. Alternator and

Accessories Inspection." Rev.13; 34SV-R43-006-25. " Diesel Generator 2C

Semi-Annual Test." Rev. 14. ED 1: and 34SV-R43-002-25. " Diesel Generator

-

1B Monthly Test." Rev. 17. The inspectors reviewed the Unit 2 TS section

~ 3.8.1. AC Sources - Dperating, and verified that required actions were .

'

completed.

b. Ob_servations and Findinas

l

During a monthly operability surveillance on January 20. tha 2C EDG

L failed to start. This was the third EDG start failure since September

1997 and the second start failure for the 2C EDG. Previous EDG start

failures are discussed in Section E2.2 of Inspection Report 50-321.

366/97-11.

During trouble shooting and a subsequent EDG run maintenance personnel

observed that the fuel racks opened and then immediately closed. Further

trouble shooting led maintenance to suspect the governor to be the

problem. Some logic circuit wiring connectors were observed to be

cracked however a megger did nnt indicate that the wiring contributed to

'the problem. The wiring was repaired. the governor was re) laced. and

post-maintenance runs were com)leted to setup and adjust t1e governor.

The inspectors were informed tlat the governor will be sent to a vendor

for failure analysis. Nuclear Safety and Compliance (NSAC) personnel

Enclosure 2

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completed the recuired TS common cause failure determination and

initially concluced that the other EDGs were not affected by the failure

and issued documentation for the conclusion. However, following further

,

trouble shooting. NSAC rescinded the initial common cause failure letter

'

and informed operations personnel that the other EDGs may be affected by

the failure. Operations personnel then performed the TS-required

operability surveillances for the remaining EDGs. No problems were

identi fied. l

The inspectors observed part of the maintenance trouble shooting and l

repair activities. Procedures were used and supervisory oversight and

-engineering support were observed. The inspectors observed part of the

TS-required operability test of the remaining EDGs. The test acceptance

l criteria were met. The licensee increased the monitoring frequency by

running the EDG weekly as part of the corrective actions taken.

c. Conclusions

The inspectors concluded that maintenance and engineering 3rovided

excellent support for the trouble shooting and repair of t1e 2C EDG

following a failure to start. Procedures were used, supervisory

oversight was evident and all TS requirements were met. l

M3 Maintenance Procedures and Documentation

M3.1 Surveillance Observations (61726)

Insoection Scooe and Conclusions

The inspectors observed all or portions of six Unit ? and Unit 2

surveillance activities which included the following:

57SV-L51-003-05: Seismic Instrumentation FT & C. Rev. 4. Ed 1

+ 34SV-E41-002-2S: HPCI Pump Operability. Rev. 26

34SV-C71-002-IS: RPS Channel Test Switch Functional Test Rev. 5

For the surveillances observed, with noted exceptions, all data met the

required acceptance criteria and the equipment performed satisfactorily.

The performance of the operators and crews conducting the surveillances

was generally professional and competent.

M3.2 Unit 2 Hiah Pressure Coolant In.iection (HPCI) TemuorarilY Inocerable

Followina Surveillance

l a. Insoection Scooe (62707)(71707)

The ins ectors reviewed procedure 34SV-E41-002-2S. "HPCI Pump

Operabi ity". Rev. 26. and observed operators perform sections of the

surveillance procedure. The inspectors attended the pre-test briefing

and discussed observations with operatius management.

Enclosure 2

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b. Observations and Findinos

On January 27, the inspectors attended the pre-test briefing conducted

prior to the HPCI surveillance. The briefing was conducted by operations

personnel with maintenance engineering, health physics, and a member of

operations management in attendance. A Unit 1 supervisor was present and

conducted an " Observation For Excellence" checklist, routinely completed

to provide feedback to personnel for areas of improvement to ensure that

management's expectations are met. The inspectors observed some aspects

of the briefing that did not meet management's ex)ectations which were

not identified by the Unit 1 supervisor. These oaservations were

discussed with operations' supervision and management personnel.

About 20 minutes into the HPCI surveillance, the inspectors observed that

the " Torus Level High" alarm actuated several times. The alarm did not

seal in but flashed as if it had initiated then immediately reset.

Operators responded to the alarm used the alarm procedures, and

monitored the torus level indication in the control room. The indicated

torus level was below the level required to actuate the alarm. Shortly

thereafter, the "HPCI Pum) Discharge Flow Low" alarm actuated and the

operators observed that t1e HPCI suction swapped from the condensate

storage tank to the torus. This action is normal for a high torus level l

or low condensate storage tank level, The operators secured the HPCI 1

system and contacted maintenance to initiate trouble shooting activities

to determine why the suction swap occurred. The HPCI system ccntroller

was left in manual while the cperator described the issue to shift

supervision and maintenance perscnnel. Later, at the direction of the

superintendent of Shift (S05), the centroller was placed back in l

automatic. The licensee issued a 10 CFR 50.72 notification for the HPCI

being inoperable for the time the controller was left in manual.

Maintenance personnel calibrated the level instruments and found that one

channel had drifted slightly. However, the instrument was not i

sufficiently out of tolerance to have caused the suction valve to swap. '

0)erations, maintenance, and engineering did not specifically determine

t1e reason for the swap, but suspected contributing factors to be the

turbulence caused by exhausting steam and operating in the torus cooling

mode, differential pressure changes on the level transmitters caused by

the turbulence and, the sensitivity of the level transmitters.

1

On January 29 the inspectors observed operators complete the HPCI

surveillance test. All TS surveillance requirements were met and no

deficiencies were observed.

4

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c. Conclusions

.

The inspectors concluded that some aspects of the pre-test briefing did

not meet management's expectations. An improvement was observed in

f operator three-part communications. Supervisory oversight was evident.

J Enclosure 2

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The 10 CFR 50.72 notification for the inoperable HPCI system was

appropriate. Surveillance test requirements were met.

M3.3 Review of Reactor Protection System (RPS) Channel Test Switch Weekly

l Testina Reauirements

a. Insoection Scooe (61726) (71707)

l The licensee determined on December 30 that procedure 34SV-C71-002-1S had l

not been performed since the Unit 1 startup from the 1997 fall refueling

'

l

outage (November 21, 1997). The procedure is required to be performed '

weekly.

As a result, the inspectors reviewed Administrative Control Procedure

90AC-0AP-001-OS. " Test and Surveillance Control," Rev. 2: Surveillance

Procedure 34SV-C71-002-15, "RPS Channel Test Switch Functional Test "

Rev. 5: Technical Requirement Manual (TRM) Loss of Function Diagrams  !

(LFDs) 1-RPS-17 and 2-RPS-17. RPS Instrumentation Manual Scram for Unit I

and 2 respectively; and Technical Specification (TS) 3.3.1.1 RPS

Instrumentation for Units 1 ano 2. In addition, the 10 CFR 50.59

evaluation for a requested change of procedure 34SV-C71-002-1S was

reviewed and discussions were held with Operations and Engineering

personnel. <

b. Observations and Findinos

The LFD for Unit 1 indicates that the Manual Scram RPS logic is actuated

by the K15 relays and associated contactors. The automatic scram relays '

(K14) and associated contactors are not actuated during an actuation of

the manual scram pushbuttons on Unit 1. The LFD for Unit 2 indicates

that both the manual and automatic relays and associated contactors are

actuated during an actuation of the manual scram pushbuttons.

Surveillance Requirement 3.3.1.1.5 for both Units 1 and 2 requires that

the manual scram logic be tested weekly. The inspectors verified that

the TS-required manual scram surveillance arocedure (34SV-C71-004-1S/2S)

..fr each respective unit was performed weedy. Performance of the

procedure for Unit 2 tests both the K14 and K15 relays and associated

contactors. However, performance of the Unit 1 procedure only tests the

K15 relays and associated contactors.

The licensee had committed to testing of the K14 relays on a weekly basis i

as one of the requirements of Topical Report NEDC-30851P-A, " Technical

Specification Improvement Analysis for BWR Reactor Protection System," as

part of the new improved TS submittal. For compliance with the

requirement of this commitment. Rev. 5 of procedure 34SV-C71-002-15 was

implemented on November 17. 1997.

l Prior to implementation of the Power Range Neutron Monitoring (PRNM)

'

System on Unit I during the 1997 Fall Refueling Outage, the licensee took

l Enclosure 2

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13

credit for t ! sting of the K14 relays and contactors during the weekly

I APRM down scale surveillance. This surveillance was eliminated after

l implementation of the new PRNM system.

l

Licensee personnel responsible for the change of procedure 34SV-C71-002- i

1S did not submit the appropriate forms for updating the procedural

testing / surveillance' data base as required by procedure 90AC-0AP-001-05,

section 8.1. Test Control. There was no surveillance task sheet 2

f available to prompt performance of the test procedure. This failure to  !

, update the Surveillance Program Data Base for the performance of

l procedure 34SV-C71-002-15 constitutes a violation of minor safety

! significance and is identified as Non-Cited Violation (NCV)

50-321/97-12-03. Failure to Follow Procedure for Scheduling Weekly  ;

Testing of.RPS Scram Test Switches, in accordance with NUREG 1600.

Section VII.

The data base was subsequently updated with the first scheduled RPS Scram

Test Switch testing frequency beginning on January 16.

c. Conclusions

,

Due to a lack of attention to detail, a procedural change form was not

'

submitted for a procedural frequency change. This resulted in a failure

l to perform weekly twS channel test switch functional tests. A Non-Cited

Violation was identified for this problem.

l III. Enaineerina

l

El Conduct of Engineering

l On-site engineering activities were reviewed to determine their

l effectiveness in preventing, identifying. and resolving safety issues,

i events, and problems. In general, engineering support to operations,

maintenance, and plant support was excellent.

E2 Engineering Support of Facilities and Equipment

E2.1 Review of ootential 10 CFR 21. ReDortina of Defects and Noncomoliance.

l a. Insoection Scooe (37551)(92903.).

!

l The inspectors reviewed a 30-day report for a potential 10 CFR 21 defect

L identified at another facility. The potential defect was associated with

a potential failure of General Electric Type CR120 AD relays. The

inspectors reviewed and assessed the licensee's evaluation for

applicability at the Hatch facility in accordance with Regulatory

l

Compliance procedure 03RC-CPL-002-0S " Defects and Noncompliance."

Rev. 1.

Enclosure 2

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b. Observations and findinos

A potential 10 CFR 21 report identified at another facility indicated

that the potential failure of certain CR120 AD relays with specified date

codes was due to a manufacturing defect. Engineering personnel evaluated

this problem for applicability at Hatch in accordance with procedure

03RC-CPL-002-0S and found two safety-related replacement relays in the

warehouse that had not been installed. These relays have been placed on

hold pending replacement or testing instructions from General Electric.

None of the affected relays were identified as having been installed in

the piant.

c. Conclusions

The inspectors concluded that the licensee had taken the appropriate

action in addressing the potential 10 CFR 21 issue.

E2.2 Bgview of Unit 1 and Unit 2 Valves Not Included In The Inservice Testina

iTST) Procram

a. Insoection Scooe (37551)

On January 30, the inspectors were informed that corporate engineering

had identified twelve valves associated with the Plant Service Water

.

'

(PSW) makeup tn the Unit 1 and Unit 2 Spent Fuel Pools (SFP) which had .

not been incitmed in the IST program.

The inspectors reviewed Unit 1 and Unit 2 TS section 5.5 and deficiency

card (DC)98-382, and discussed the proposed corrective actions for the ,

valves that were not included in the IST 3rogram. The inspectors  !

reviewed Unit 1 UFSAR section 10.4. Fuel 2001 Cooling and Cleanup, and

Unit 2 UFSAR section 9.1. Fuel Stora r? and Handling.

b. Observations and Findinas

The inspectors reviewed DC 98-382 which documented the problem and

observed that the following valves were listed on the DC:

Manual valves that should be in the IST program for quarterly exercising:

1G41-F217

2G41-F040

1P41-F070A

1P41-F078

1P41-F103

2P41-F070A

2P41-F070B

2P41-F073

l

) Enclosure 2

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Power Operatad Valves that should be in the IST program for remote

indication verification every two years:

1G41-F041

L 2G41-F054.

l ' Check valves that should be in the IST program for quarterly exercising

i

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to the open position required to fulfill their design function:

IG41-F055

2G41-F055

Unit 1 and Unit 2 TS 5.5, Programs and Manuals, section 5.5.6, require an

,

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. Inservice Testing Program. Implicit in this requirement is that all

valves and components that are required to be tested under the program be

L

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included. American Society of Mechanical Engineers (ASME) Operations and

Maintenanca (C&M) code requires that active and passive valves which

_ mitigate the consequences of an accident be included in the IST 3rogram.

Plant Service Water is a safety-related seismic Class I system w1ich

provides makeup water to-the SFP.

,

i Nuclear Safety and Compliance (NSAC) personnel made an initial

j determination to prepare a 10 CFR 73 license event report (LER) based

l upon information in the DC. The determination to prepare the LER was

l based upon operations or conditions prohibited by plant TS. Operations

personnel also entered the appropriate required actions of the TSs.

l NSAC personnel informed the inspectors that additional reviews in

conjunction with the LER preparation will be performed to determine-

'

. whether the valves of concern should be placed in the IST program. The.

j results of this review will be documented in a Significant Occurrence

' Report. This issue was identified as inspector followup item (IFI)

50-321. 366/97-12-04, Review of IST Basis for PSW Makeup Valves to Spent

l Fuel Pool .

c. Conclusions

l Corporate engineering did a good job in identifying that various valves

were not included in the inservice test (IST) program. The licensee is

continuing the review of this informdtion to determine if these valves

should have been in the IST program. An IFI was opened to review this

issue upon completion of the licensee's action.

E2.3 Enaineerina Walkdown of Systems and Comoonents

,

! ' a. Insoection Scooe (37551)

The inspectors reviewed deficiencies. MW0s, and engineering evaluations

associated with deficiencies identified during a licensee walkdown of the

Standby Liquid Control (SBLC) and Plant Service Vater Systems. The

inspectors discussed the problems with engineering and management

j

Enclosure 2

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personnel, verified that corrective actions were completed, and assessed

system operability.

l

b. Qb.servations fpd Findinas

On December 29 the inspectors were informed by licensee management that  !

some bolts on the mounting flanges of the SBLC system test tanks (legs I

from the tank to the floor) were missing. The test tanks are for testing '

l. )urposes and are not' required for the system design function. Each tank

'

las three legs and each leg was designed to have four a m hor bolts

i embedded into the concrete as shown on plant drawing S1'352. For Unit 1.

l two legs had the required bolts and the third leg contened no bolts.

l For Unit 2. each leg had only two bolts. The licensee believed that this

i condition existed since initial construction. Corporate engineering was

not able to locate any engineering evaluation or assessment for the

existirig condition and performed the required seismic analysis. Site

!- personnel replaced all of the missing bolts. except for one bolt on each

l- unit, due to a physical ,bstruction which prevented their installation.

! .The inspectors reviewed the work Jackage, observed part of the ongoing

!

work activity and verified that t1e corrective actions were completed in

l a timely manner. The inspectors reviewed the preliminary safety

evaluation (the final evaluation was still being developed) which stated

l

that the currently installed anchor bolts and bolt configuration was not

a seismic concern and would not compromise the ability of the SBLC system j

to perform its safety function.

_

On February 5. during a walkdown of the standoy plant service water

l (SPSW) system engineering personnel identified that a small section

'

(about 18-20 inches) of plant service water piping on the supply to

Emergency Diesel-Generator (EDG) 1B had no missile protection. The

licensee believed that this condition had existed since initial

l construction. Operations declared the EDG inoperable and entered the  !

l required TS action statement. A temporary concrete barrier was

! . positioned to provide the required protection. Engineering was to  !

l develop a work plan to construct a permanent missile barrier. l

l

l The inspectors reviewed the reported deficiency. discussed the problem l

L with management personnel and observed that the temporary barrier would

l provide protection from a horizontal missile.  ;

i

c. Conclusions j

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The inspectors concluded that engineering personnel demonstrated  ;

excellent observations for problem identification on the Standby Liquid  !

Control and Standby Plant Service Water systems. Corrective actions were

timely: site maintenance and engineering and corporate engineering

support was~ excellent.

Enclosure 2

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E2.4 Removal of Traversina Incore Probe (TIP) Nitrogen Purae Valve from

_1stina of Primary Containment Isolation Valves

a. Jnsoection Scoce (37551) (92903)

' The inspectors reviewed surveillance procedure. 34SV-C51-005-05. " Stroke

Time Testing of NUMAC TIP Ball Valves Rev. 4. Significant Occurrence

Report (SOR) C0 97-3808 and held discussions with licensee personnel.

Additional documentation reviewed by the inspectors included. TSs

applicable to primary containment isolation valves (PCIVs), applicable

l sections of the Technical Requirement Manual (TRM), the UFSAR. Licensing

i

Document Change Request (LDCR) 98-02 and Southern Company Drawing H-

28993. Neutron Monitoring System, sheet 2 of 2. The documentation review

and discussions were associated with the listing of the TIP Nitrogen (N2) l

Purge Solenoid Valve (2C51-F3012) as a PCIV in the UFSAR and the TRM.

f

b. Observations and Findinas

The inspectors reviewed data packages associated with the performance of

l procedure 34SV-C51-005-0S and noted that the TIP Purge Solenoid valve

l 2C51.F3012 failed to remain closed following the perforriance of the

procedure on August 11, 1997. A deficiency card was written and the j

appropriate required action statement (RAS) of TS 3.6.1.3 Primary /

Containment Isolation Valves, was entered.

The licensee initiated a root cause review of the valve )roblem that was

l documented in SOR C0 97-3808. The inspectors reviewed t1e SOR and s

! Drawing H-28993 and noted that the TIP N 2 Purge Solenoid Valve is located

in the N 2S.upply line to the TIP indexing mechanism. The TIP indexing

mechanism 1s located inside the drywell. A N2 purge blanket is used to

minimize corrosion of the indexing mechanism. The valve is normally

I opened tc provide the N 2purge and closes on a Group 11 containment

,

isolation signal.

i

The inspectors were informed by licensee personnel that the force l

'

associated with the N 2 pressure in the line to the drywell is greater i

than the spring tension for the closing of the valve. The flow of the N 2 i

,

is o)posite to that of accident flow from the drywell. The pressure in i

l the 12 header to the valve is greater than the analyzed drywell pressure  ;

'

following a Loss of Coolant Accident (LOCA). Check valve 2C51-T3017 l

located in the TIP room. is also in the penetration flow path downstream l

of the TIP Purge Valve in the direction of N2 flow. The check valve i

prevents flow in the accident direction from the drywell. The licensee

concluded that the pressure of the 2N in the line provided an isolation l

boundary to the drywell in the event that the valve failed to remain

closed due to the N 2pressure following a LOCA. Unit I does not have ,

this problem because a pressure regulator is installed in the flowpath of '

the N2 line prior to the N Purge

2

Valve (1C51-3012).

Enclosure 2

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The inspectors reviewed an approved LCDR which removed the TIP Purge

Solenoid Valve from the TRM and UFSAR listing for PCIVs for Units 1 and

Unit 2. including a Request for Engineering Assistance (REA HT-97615) and

the 10 CFR 50.59 evaluation. This information supported the removal of

the TIP Purge Solenoid Valves from the TRM and UFSAR listing of PCIVs for

Units 1 and 2.

!

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c. Conclusions

I

The SOR associated with the review of the TIP nitrogen purge valve issue

l

was good. The determination that the valve could be removed from the

PCIV list in the FSAR and the TRM was appropriate.

E2.5 Valve Testina and Drawina Review of Containment Atmosobere Dilution (Ghp_1

System

,

]

a. Insoection Scooe (37551)

,

The inspectors reviewed selected components of the Nitrogen Inerting

System for Units 1 and 2. The activity included a review of plant

,

drawings H-16000 for Unit 1 and H-26083 for Unit 2. The inspectors

conducted a system and component performance history review and walked

down parts of the system,

b. Observations and Findinas ,

I

l The inspectors selected a sampling of Relief Valves (RVs) and Pressure

Control Valves (PCVs) and reviewed documentation associated with the CAD

system. This valve sampling and document review was done to determine

the testing frequency and the results of the testing. The inspectors

observed that of 16 valves selected on Unit 1. five valves were

identified as being on a 60-month testing frequency. There was no

history of testing for the remaining 11 valves and there was no task

l identified to perform testing. The testing of the five referenced valves

was required due to valve failure or replacement. None of the valves was i

tested as part of a routine testing or preventive maintenance effort. j

For Unit 2.12 valves were selected for review. Two valves were tested l

l due to repair or replacement following valve failure. One valve was I

identified as being on a 54-month test frequency. However, testing

records were not located for the remaining nine. Also, there was no task

identified to perform testing or preventive maintenance of the valves.

The inspectors discussed these observations with maintenance and 1

engineering aersonnel. The inspectors were informed that the RVs and '

PCVs for bot 1 units were not ) art of the routine testing program. There  ;

were no records to indicate tlat some of the v61ves were ever tested and

others were only tested following repair or replacement. 10 CFR 50.

Appendix B. Criterion XI. Test Control, requires, in part, that all 1

testing required to demonstrate that components will perform  ;

satisfactorily in service is identified and performed in accordance with i

written test procedures which incorporate the requirements and acceptance

Enclosure 2

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i limits contained in applicable design documents. The failure to

incorporate these com

50-321. '366/97-12-05.ponents

Failure tointo a testNitrogen

Include programValves

is identified as VIO

in a Test.

,

Program.

l

The ins)ectors walked down parts of the system on both units using

!

applica)le unit drawings. During the walkdown on Unit 1 and Unit 2 the

inspectors observed that a significant amount of ice had accumulated on

piping and some valves located at the nitrogen storage tanks. The manual

isolation valve for the Unit 1 tank was iced over. The inspectors

informed management. personnel of this observation and questioned if the

ice problem may be a seismic concern. The inspectors were later informed

that a deficiency card had been initiated and corporate engineering was

reviewing the problem for seismic concerns. The inspectors later

observed that the licensee had placed light- heaters in the tank

enclosures to thaw the valve.

l The inspectors' observed that all four of the safety relief valves on-

!

piping associated with the Unit 1 nitrogen storage tank were leaking

slightly. This observation was discussed with licensee management and

engineering personnel. Some engineers associated with the nitrogen

L system were aware of the leaking valves'. The inspectors'were informed

!

that the valves had been leaking for some time. The ins

view this as an immediate operability concern. However,pectors did not

it demonstrated

'

a lack of attention to material conditions of the system. The inspectors

did not identify that any deficiency cards had been initiated for the-

leaking safety relief valves. The inspectors observed that PC F469 on

]

_

Unit 2 had a small leak near the bottom of the valve. This leak had not

[ been identified previously by the licensee.

l Note 11 on plant drawing H-16000 for Unit 1 indicated that some piping )

from the nitrogen storage tank toward the steam vaporizer should have

been insulated. The inspectors observed that much of the piping was not

, insulated. Note 10 on plant drawing H-26083 for Unit 2 indicated that 1

l the piping from the nitrogen storage to the steam vapon zer should be  !

L insulated. The inspectors observed about 4 feet of insulation on )iping

i and one PCV was insulated at the front of the nitrogen storage tant.

Other piping at The storage tank area was not insulated as indicated on

plant drawings. The inspectors observed that the vendor manuals also

recommended that the piping be insulated.

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This failure to insulate piping as required by the design drawings was

identified as VIO 50-321, 366/97-12-06. Insulation on Nitrogen Supply

Piping Not Installed in Accordance with Drawings.

Following the inspectors' identification of the above problems, the

inspectors were informed that licensee management had initiated an Event

Review Team to review the system and previously identified problems.

Other problems identified with this system are also discussed in Section  !

02.2 of this report.

Enclosure 2

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L c. Conclusion

.The licensee.has exhibited a lack of attention to the material condition

! of these systems. DCs have not been generated to identify and correct

L w problems and routine maintenance and testing has not been performed. Two

l violations were identified.during this review: one for a failure to

l include nitrogen valves in a test program and one for a failure to meet

h

s

design drawing requirements.

.

E3 Etx.jineering Procedures and Documentation

Paragraphs E3.1 through E3.12 provide the results of a team inspection of

L various. fuel performance and managemerit issues. This inspection was

!

conducted at the Southern Nuclear Operating Company (SNC) corporate

offices the week of December 15, 1997.

,

E3.1 Core Thermdl Heat Balance

p a. Insoection Scoog (37550)

Due to recent fuel vendor notifications of discrepancies in the core

thermal heat balance calculation, the inspectors reviewed bounding

i calculations for discrepancies, root cause analysis, and corrective

, actions.

'

b. Findinas and Observations

i

In December,1995. General Electric (GE) notified the licensee that

! " unconsidered control. rod drive (CRD) bypass flow may result in

nonconservative heat balance calculations. In response,'the licensee

L opened SOR C09505439 to evaluate the CRD: bypass flow issue and other

L potential discrepancies in the heat balance calculation. The analysis

i showed that, while Plant Hatch was not susceptible to the CRD bypass-

l issue. ~other potential sources of error existed in the heat balance

l calculation. A root cause analysis showed that the impact of parameters

l not previously considered in the heat balance calculation was about.

l' O.6025 MW thermal. The licensee has added this value to the value for

- radiative heat losses in the heat balance calculation methodology.

M c. Conclusions

The inspectors concluded that the licensee *s re-evaluation of heat i

l

bal$nce calculation inputs contained in SOR C09505439 was a proactive

measure to minimize future discrepancies.

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L E3.2 BWR Peak Clad Temoerature

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a. Insoection Scoce'(37550)

The inspectors reviewed the licensee's peak clad temperature (PCT)

reporting due_to recent discrepancies in the fuel vendor's PCT analysis-

methodology. ,

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b. Findinas and Observations

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l , As reguired by 10 CFR 50.46(a)(3)(I), by letter dated January 13, 1997

the licensee informed the NRC that the sum of the changes and errors was

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-approximately 215 F. The licensee also stated that the 1986 SAFER /GESTR

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ECCS evaluation resulted in approximately 675 F of margin to the 2200*F

limit. The inspectors observed that the SNC Nuclear-Fuels Department

maintained a proceduralized process for complying with 10 CFR 50.46

reporting requirements for PWR nuclear units. However, no similar

2roceduralized process existed for BWR nuclear units. Because individual

3WR licensees were submitting the yearly report, the lack of procedures-

l for . tracking PCT changes at BWRs was an area for improvement.

k c. Conclusion

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n Although the licensee had not been susceptible to recent reports of

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inaccuracies in PCT. the inspectors noted that PCT changes for BWPs were

not proceduralized and tracked in a manner similar to PWRs.

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E3.3 Review of Nuclear Fuel Performance

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a. Jnsoection Scooe (37550)

! The inspectors reviewed fuel performance over the last four to six cycles

! of operation for both Units 1 and 2 and evaluated licensee efforts to 1)

l~ identify the root cause of fuel failures, 2) prevent future failures, and

l 3) mitigate effects when failures occur during operation.

b. Observai..ons and Findinas

Since fuel assembly failures occurred in both units in early cycles of

I operation due to crud-induced-localized corrosion (CILC), the licensee

l' became very aggressive in analyzing and preventing fuel assembly

l failures At the time of the inspection. Unit 1 was in Cycle 18 and

Unit 2 was in Cycle 14. The most recent fuel failures in Unit 1 occurred

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i- during Cycle 12, one fuel assembly failure due to debris, and two fuel

I assembly failures during Cycle 16 for unknown causes. Unit 2 had two

fuel assembly failures during Cycle 10 and three fuel assembly failures

f during Cycle 11. all due to debris. Following the Unit 2 fuel assembly

failures, the licensee shut down Unit 2 during Cycle 11 to remove one  !

failed fuel assembly and perform an examination of all fuel assemblies to

look for and remove debris. The debris found during the examination

Enclosure 2

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consisted of small steel turnings. All failed fuel assemblies were

removed from the core as were other fuel assemblies with evidence of

debris fretting. The licensee had inspected the failed fuel assemblies

from both units to determine the root cause of each failure and to

propose corrective actions.

The licensee had proactive fuel assembly failure prevention programs to

exclude debris and evaluate effectiveness of GE debris filter design in

lead use assemblies. The licensee also had a program to mitigate fuel

assembly failure degradation. Typical strategies used to mitigate

degradation were:

e shorten length of time for partial control rod insertion during

startup

e improveSfuelleakerdetectionfailedfueloperatingguidelines.

' e degradation resistant fuel design frequent interface with

industry, and

e vendors to learn new techniques.

c. Conclusions

The licensee maintains aggressive programs to eliminate and mitigate

effects of failures. The licensee also actively participated in industry

programs to prevent and mitigate failures.

E3.4 Lead Use Assemblies and Introduction of GE-13 Desian Fuel Assemblies

a. Insoection Scooe (37550)

The inspectors reviewed the licensee use of Lead Use Assemblies-(LUAs) to

evaluate new fuel designs. The inspectors also evaluated licensee

interface and interaction with the fuel vendor prior to introduction of

GE-13 design fuel assemblies into Unit 1 Cycle 18 and Unit 2 Cycle 14.

g b. Observations and Findinas

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The licensee does not introduce fuel design changes into its cores

without the following information and testing results.

LUAs testea in their own core, with data from at least two cycles of

operation vendor requirement to inform them of all design changes

(including minor ones) between the LUAs and the actual design to be used

for reloads demonstrated satisfactory performance of full reloads of new

design at other licensee plants.

>

The licensee monitored three cycles of operation of GE-13 LUAs in Unit 1

before loading a full reload. SNC performed several audits of the vendor

during design fabrication and reload licensing analyses prior to -

introducing the GE-13 design. The vendor audits by SNC were of

sufficient depth and breadth with good findings and followu SNC also

used check lists for design changes in areas of 1) nuclear.p.2)

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mechanical 3) core compatibility (mixed core issues), 4) core design,

5) o)erating strategy 6) analysis methods and analyses performance,

7) tiermal limits 8) technical specification changes, and 9) fuel

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reliability. They also conducted formal reviews.of reload design and

licensing from the preliminary to the final design phase and prior to

submittal of Reload Safety Evaluation and Core Operating Limit reports. i

and reload licensing calculations and documentation.

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c. Conclusions

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l The licensee had a very conservative philosophy toward introducing new

fuel designs into their cores. It waited until another. utility has i

already proven the design with a full reload, with satisfactory

performance, plus LUA use in its own cores with sufficient data to i

. substantiate performance. )

l

The licensee performed a thorough review of vendor design and analyses

information prior to the change to the GE-13 fuei design.

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l E3.5 Review of Asymmetric Ooeration j

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f a. Insoection Scoce (37550)

The inspectors reviewed the licensees evaluation of asymmetric power

operation during Unit 2 Cycle 11.

b. Observations and Findinas

During Unit 2 Cycle ll, a failed fuel assembly required the insertion of

l adjacent control rods to prevent further deterioration of the failed fuel

l assembly. The insertion of these control rods resulted in asymmetric

L

power operation for the remainder of Cycle 11. The inspectors reviewed

the licensee's technical evaluation dated April 28, 1993, that confirmed

the acceptability of continued operation with the adjacent control rods

inserted. In addition, the licensee provided copies of Section 3.4.2.8.

Symmetry, of GESTAR II [NEDE-24011-P-A-13), and NED0-20340-1. which

justified asymmetric power operation. A review of GESTAR II indicated

that the safety limit MCPR calculated by GE procedures was applicable for

both symmetric and asymmetric power operation. The inspectors reviewed

3D MONICORE P1 outputs for Unit 2 Cycle 11, before and after asymmetry

power operation was established. The location of the ten most limiting

fuel bundles did not change following the insertion of the adjacent

control rods and the MCPR values did not change significantly for the

asymmetric power condition.

A primary concern stated in the technical evaluation wat increased flow

through the failed fuel assembly due to depressing power around the

failed fuel assembly. Calculations indicated that the flow increase

would exceed the flow range of applicability for the GEXc correlation.

The licensee also evaluated this condition and concluded that the

Enclosure 2

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increased flow was acceptable and that the high-flow warnings generated )

by either'3D MONICORE or PANACEA simulations could be ignored. )

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The inspectors also reviewed cycle-specific calculations for Cycle 11. 1

The inspectors identified that the only analysis affected by the  !

asymmetric power operation was the Rod Withdrawal Error (RWE)

calculation. The licensee.had reanalyzed the RWE calculation using the )

asymmetric power operation conditions and demonstrated that the new RWE

analysis was bounded by existing limits. The licensee also evaluated the

effect on Cycle 12 core design due to asymmetric operation during

Cycle 11. The licensee concluded that Cycle 12 could be designed without i

adverse consequences. I

c. Conclusions

The evaluation of the asymmetric operation caused by a leaking fuel pin

during Cycle 11 was thorough and complete. The licensee properly

identified and resolved all major technical issues, including the impact

of increased bundle flow and the effect of asymmetric power operation on

Cycle 12 core design.

E3.6 3D MONICORE Ouality Assurance Procedures

a. Insoection Scooe (37550)

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.The inspectors reviewed the licensee's procedures used to' verify the

integrity of the Beginning of Cycle (BOC) data for 3D MONICORE.

b. Observations and Findinas

The inspectors reviewed the licensee's BWR Core Analysis Procedure.

BCA 50-100. 3D MONICORE BOC Wrapup Checkout, which documents the steps

taken by SNC to verify proper implementation of the BOC data for 3D

MONICORE. The procedure states that the responsibility for the integrity

of the BOC data belongs to the preparing organization (typically the fuel

vendor) and that the steps in procedure BCA-50-100 provided only

incremental quality assurance. The ins)ectors reviewed the design record

file for Unit 1 Cycle 18 and verified tlat the procedure was followed.

An interview with the licensee indicated that the licensee performed )

procedure BCA-50-100 for all cycles since the procedure was issued. The

licensee stated that normally the SNC BWR Core Analysis Group receives an

advanced copy of the final 3D MONICORE data which provided additional

time for the checkout process. However, in case of a delay in receiving

the final 3D MONICORE data from the vendor, the unit can proceed with an

initial approach to critical. SNC engineering would still have

sufficient time to verify the data because 3D MONICORE was not placed in

operation until about 25% rated thermal power.

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The licensee stated that it routinely finds problems with the 30 MONICORE

data provided by the vendor. Most of these )roblems were related to

limit settings..where different options may )e selected by the user.

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When errors were found, the differences were resolved with the vendor. '

l The licensee was interviewed regarding the applicability of 3D MONICORE

l methods to model 3 art-length rods and other features of advanced fuels

l such as GE-13. T1e licensee provided a copy of a GE letter MFN 059-89.

L JSC-8985. Application of Approved Methods to a New GE Fuel Design, dated

August 7. 1989. This letter discussed the application of NRC-approved

metnods to the GE-13 fuel design,

c. Conclusions

The inspectors found that the procedure for quality assurance of 3D

MONICORE data were technically adequate. A review of the documentation

for Unit 1 Cycle 18 indicated that the procedure had been followed.

E3.7 Doeratino Limit Uncertainty

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a. .Igspection Scone (37550)

The inspectors reviewed the cycle-dependent Safety Limit Minimum Critical- 1

Power Ratio (SLMCPR) evaluations for both Unit 1 and Unit 2. I

b. Observations and Findinas

The cycle-dependent SLMCPR evaluations resulted in different limiting

values for both units even though the operating strategy and fuel loading

patterns were similar. Unit 2 Cycle 13 had a SLMCPR value of 1.08 )

whereas Unit 1 Cycle 17 had a SLMCPR value of 1.06. The licensee stated

that they were aware of these differences and had questioned the vendor -

about them. The differences were finally attributed to a flatter power

distribution in Unit 2. The 0.02 safety limit difference between the two i

units remained for Cycles 14 and 18 even though the SLMCPR values

increased to 1.12 and 1.10, respectively, because of the fresh GE-13

design fuel loaded in those cycles.

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To investigate the above SLMCPR differences, the licensee used the TRACG l

code to determine if more-advanced best-estimate methods could be used to

determine the Operating Limit Minimum Critical Power Ratio (OLMCPR) more

accurately. Following established licensing procedures, the OLMCPR was

calculated by the addition of two components; the SLMCPR and the ACPR

which was estimated from the limiting transient calculation. The

licensee evaluated whether the OLMCPR could be calculated directly from a

statistical evaluation of a number of TRACG results. The inspectors

reviewed the results of this study which indicated that establishing a

OLMCPR directly from a number of statistical TRACG calculations was

feasible. Following this procedure the OLMCPR for Unit 2 could be

reduced by as much as 0.03 for Cycle 14. The licensed ODYN/TASC

Enclosure 2

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methodology yields an OLMCPR value of 1.35 whereas this valu can be

reduced to 1.32 if the TRACG statistical analysis were usec'

,

During review of the licensee's results, the inspectors noted that the I

uncertainty in the calculated ACPR ranged from 0.04 to 0.07. Thu

licensed ODYN/TASC methodology applies a fixed uncertainty of 0.01 to the ) ,

calculated ACPR which is significantly lower. Tne inspectors informed-

the licensee that this large discrepancy in uncertainties could

potentially result in a 0.06 penalty in OLMCPR. The inspectors were also

concerned with the lack of licensee or vendor follow up on this issue.

c. Conclusions

The inspectors considered the licensee *s actions to identify the observed i

differences in safety limit between essentially identical plant designs i

to be proactive. However, the inspectors were cor.cerned with the large

non-conservative difference between the OLMCPR uncertainty used in the

licensed ODYN/TASC methodology.and the uncertainty using the TRACG ,

methodology. Also, the inspectors considered the lack of licensee

followup with the vendor and/or NRC on this potential safety issue as an

area that could be improved.

E3.8 SNC Resoonse to Cycle-Decendent Safety limit MCPR Issue

a. Insoection Sroce (92903)

The inspectors reviewed the licensee's response to 10 CFR 21 nottfication

to potentially non-conservative SLMCPR calculations

b Observations and Findinos

By letter dated April 3, 1995. GE informed the NRC that GE intended to

replace the current SLMCPR generic analysis with a cycle-specific

analysis. As a result GE determined that the St.MCPR calculated using

the generic analysis could be non-conservative when applied to certain

actual core and fuel designs. As a result of this potential

non-conservative condition, the licensee imposed a temporary penalty of

0.03 in the SLMCPR for both Units 1 and 2. This penalty was reduced to

0.02 for Unit 2 and no penalty for Unit 1 once the cycle-dependent safety

limit calculation was . verified.

The inspectors reviewed several licensee documents related to the cycle-

dependent SLMCPR evaluation by the licensee. These documents contained

all correspondence between the licensee and GE. as well as internal

documents and communications, and topical reports. The inspectors

concluded that this issue was thoroughly documented by SNC and that the

licensee was knowledgeable of the subject and took conservative

, corrective actions. However, the inspectors were unable to determine if

the licensee could or should have anticipated these errors before the

vendor discovery. The ist.ue is identified as URI 50-321, 366/97-12-11.

Enclosure 2

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Timeliness of Identi'fication of SLMCPR Errors, pending additional review

by the NRC staff,

c. Conclusions

Based on discussions with licensee personnel and review of the

documentation the inspectors found that the licensee's followup of the

cycle-dependent SLMCPR issue was adequate. The licensee was

knowledgeable about the subject and took conservative actions to correct

possible safety deficiencies.

E3.9 Imolementation of Lona Term Stability Solution 00 tion III

a. Inspection Scooe (37550)

The inspectors discussed with licensee personnel the status of the

implementation of Long Term Stability Solution Option III. As part of

this discussion, the licensee provided a number of documents related to

the Option III implenentation.

b. Observations and Findinas

As a result of Generic Letter 94-02, the licensee committed to implement

BWROG Option III as a long-term solution to detect and su) press potential

reactor instabilities. By letter dated March 21, 1997, t1e NRC issued TS

Amendment Nos. 205 and 146 for Units 1 and 2. respectively. These TS

amendments allowed the licensee to install a new digital Power Range

Neutron Monitoring system which included Option III implementation.

By SNC letter dated June 20. 1997, the licensee requested an axtension of

the testing period for the Optb 'II hardware due to an unusually high

number of confirmation counts s false positives) from the 3eriod-

based detection system (PBDS). Ik 'icensee personnel stated tlat they

required additional time to "cune" the PBDS using less sensitive

settings. By letter dated September 12. 1997, the NRC approved the

licensee's request: however, the letter stated that the less sensitive

settings proposed by SNC would have to be reviewed separately.

During the Unit 2 Cycle 14 " tuning" tests, the licensee used less

sensitive settings and the longest confirmation observed was 4 counts.

Based on these results. the licensee proposed to use the less sensitive

settings. Because these settings are outside the previously approved

ranges, further NRC review was required. In response to a recuest for

additional information the licensee provided test data that cemonstrated

that the proposed settings were covered by the initial evaluation, but

that the sensitivity of these proposed settings is very low. The

inspectors reviewed the data and were concerned that the )roposed

settings would not provide a warning alarm before the hig1-amplitude

Option III scram would occur. Further discussions with licensee

personnel indicated that the problems observed during testing did not

Enclosure 2 j

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appear to have been communicated properly throughout the industry. 1

Specifically, the licensee appeared-to have solved the 3roblem "on their

own" without consulting other 0) tion III plants or the lardware vendor.

This was a concern because the )BDS sensitivity problems appear to be a j

generic issue and has been experienced independently by the Option I-A 4

plants.

c. Conclusions

The inspectors concluded that the licensee has 3 roper documentation of )

the Option III implementation d6ta. However, tie inspectors were '

concerned that the licensee does not a) pear to have communicated what

ap3 ears to be a generic problem with tie PBDS algorithm sensitivity to

otler Option III vendors and utilities.

E3.10 Review of Stability-Pelated Procedures

a. Insoection Scoce (37550)

The inspectors reviewed the licensee's BWR Core Analysis Procedure number

BCA-10-270. Stability Considerations, which documents the stability-

related considerations taken during reactor core management and reload

licensing activities. This procedure applied to both Unit 1 and Unit 2. ,

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b. Observations and Findinas

Prior to Option III im)lementation. Procedure BCA-10-270 specified that

both units follow the 3WROG Interim Corrective Actions dated June 6

1994. The )rimary recommendation of Procedure BCA-10-270 was to remain

within the )ounds of established operating experience. Specifically, the

procedure recommended that axial and radial )ower peakings be minimized,

that feedwater temperature be maintained wit 11n normal range, that

unusual xenon conditions (e.g., startup following a short shutdown) be

evaluated for their effect on reactor power distribution, and that

additional analyses be performed when a new fuel design was loaded into

the reactor core.

Following implementation of Option III. Procedure BCA-10-270 saecified

the actions taken during the reactor core anal.ysis to verify tlat the

o)erating margin due to instability events, detected and su) pressed by

tie OPRM scram system. were not limiting. The results of t ais

confirmatory analysis were reported in the Su)plemental Reload Licensing

Report and the OPRM values were supplied in tle COLR.

A review of Unit 2 Cycle 11 startup stability calculations indicated the

potential for out-of-phase instability. Even though the calculated

channel decay ratios were within the " core-channel ~ stability acceptance

region, the channel decay ratios were high. indicating that an out-of-

phase instability may occur.

Enclosure 2

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Procedure BCA-10-270 specifies that the form provided with Attachment 1

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may be used to help evaluate the new cycle for stability. However, an

interview with licensee personriel found that this form was not used.

L Licensee personnel stated that they planed to modify the procedure to

i require that the form be used to document their evaluation. Licensee

! personnel indicated that the customary procedure was to include the

stability evaluation as 3 art of the Cycle Management Report (CMR). The

inspectors reviewed the Jnit 2 Cycle 14 CMR (Rev.1). Section 4.2.

Reactor Thermal-Hydraulic Stability. The Unit 2 Cycle 14 CMR contained-

the results of three stability calculations which showed a core-wide

decay ratio of less than 0.29 and a channel decay ratio of less than

0.12. The analyzed condition was 35.8% rated power and 34% rated core

flow, which lies just outside the Unit 2 stability interim corrective 1

action exclusion region. l

The inspectors also reviewed CMR Section 4.2. Reactor Thermal-Hydraulic

Stability. Rev. O. for Unit 1 Cycle 18. This section did not contain any

documentation specific to the stability of the Cycle 18 reactor core,

which was the first cycle where GE-13 design fuel was used. The form

provided with Attachment 1 was not completed for this cycle. When

interviewed, licensee personnel stated that they had not performed a

cycle-specific stability evaluation because the results of Unit 2 Cycle

14 had shown a large margin (decay ratio less than 0.29) and that the

Unit I reactor core design was essentially identical to that of Unit 2

Cycle 14. However, no formal evaluation was conducted to demonstrate

that the Unit 2 Cycle 14 stability calculation applied to Unit 1 Cycle

18. The inspectors compared the Unit 1 Cycle 18 and the Unit 2 Cycle 14

reactor core designs and concluded that the stability evaluation was

technically adequate. However, the lack of a formal evaluation was

considered to be an area that could be improved.

The use of ODYSY for stability calculations was discussed with the

licensee. The licensee was aware that ODYSY is not approved for

licensing stability calculations and that these stability calculations l

were performed for operational purposes only. '

c. Conclusions

The Stability Considerations procedure BCA-10-270 adequately addressed

stability-related issues for new reactor cores. However the form  :

provided with Attachment 1 was not being used to evaluate the new cycle l

for stability. All relevant documentation relative to the stability for i

Unit 2 Cycle 14 was adequately covered by the CMR. The inspectors also  :

found that the stability evaluation for Cycle 18 of Unit 1 was i

technically adequate. However, there was no formal documertation of this

evaluation.

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E3.11 Licensee Oversiaht of Vendor Performance

a'. Insoection Scooe

At a' follow-up to concerns found during recent fuel vendor inspections,

the inspectors evaluated licensee programs to adequately oversee their

nuclear fuel vendor. General Electric. '

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The inspectors found that SNC has a comprehensive Quality Assurance (0A)

3rogram, from the Corporate 0A Policy and Guidelines to specific Nuclear

r uel (NF) Department

arocedures. The inspectors reviewed two detailed NF

0A audit reports for latch Unit 2. Cycles 13 and 14. In addition.: the

BWR audit logs from 1995 through 1997 were reviewed. The inspectors

found that 4 to 5 separate audits were oerformed for each reload core 6

design campaign. It was noted that a S4C Corporate Quality Services

audits of Nuclear Fuel in 1994 and 1996 also evaluated the BWR vendor

audit program, with no adverse findings.

c.. Conclusions

The ins >ectors found the Hatch licensee vendor oversight program to be a

strengt1 both in the formal 0A audits and follow-up activities with the

vendor.

E3.12 Rod WithdCpwal Error / Rod Block Monitor Ooerability Technical

Specifications

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a. Insoection Scooe (92903)

The inspectors reviewed the licensee *s res)onse and assessment of recent

vendor reported problems with the Rod Bloc ( Monitor (RBM) operability

requirement of TS'for the rod withdrawal error (RWE) event. j

b. Observations and Findinas

The inspectors evaluated the licensee's response to a GE letter dated

October 31, 1994, informing the licensee that the 1% plastic cladding i

strain limits should be considered for ARTS plants and that the strain  ;

limit would be met if one channel of the RBM remains operable. The '

inspectors noted that the GE Safety Reload Licensing Reports (SRLRs) for

Unit 1. Cycles 16 and 17. and Unit 2. Cycles 13 and 14, indicated the

necessary protective measures, but failed to clearly address the  !

conditions under which the RBM should be operable. During an inspection i

of the vendor. GE informed the NRC that its analyses showed that the

licensee's M0P screening limits had been exceeded, but the that the 1%

strain limits were not exceeded. Following this' inspection. GE issued a  ;

formal notification to all ARTS plants that at least one channel of RBM i

must remain operable to meet the 1% plastic cladding strain limits. In l

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April. 1997, the licensee submitted Licensee Event Report (LER)'

50-321/97-03. describing the discrepancy between GE RWE analyses-

procedures and the TS requirements and the corrective actions that were

taken.

In March 1995. GE began cycle-specific RWE. analyses for all plants and

fuel types. During the period when the potential existed for the MOP

, screening criteris to be exceeded, and before the detailed 1% cladding

strain analyses was completed, the TS.for Hatch Unit 1. Cycles 16 and 17

and Hatch Unit 2 Cycle 13 did not require the RBM operability. However,

the inspectors were not able to determine if the licensee could or should.

have been aware of this aroblem before formal notification by GE. This-

issue is identified as URI 50-321. 366/97-12-12, Timeliness of Amendment

of Technical Specifications, pending additional review by the NRC staff.

c. Conclusions

Although the RBM channels were operable during this period, and

administratively required after the licensee became aware of the problem,

the TS requirement was not implemented until after the licensee TS

amendment request of May 9. 1997.

E8 Miscellaneous Engineering Issues (92700) (92903)

E8.1 (Closed) Unresolved Item (URI) 50-321. 366/97-05-04: Determine the

Reoortability of Licensee-Identified Deficiencies With Resoect to IN 92-

18. " Potential for Loss of Remote Shutdown Caoability Durina a Control

Room Fire."

This URI was opened as a result of questions concerning the

reportability, under 10 CFR 50.72 and 50.73. of design and " hot short"

issues that were raised as a result of the licensee's review of IN 92-18.

The inspectors reviewed.the reportability requirements and the licensee's

rationale for not reporting-this issue. The inspectors reviewed NUREG-

1022. " Event Reporting Guidelines." and concluded that the licensee's

justification was sound. The " hot'short" scenario, as it relates to the

Hatch Units 1 and 2 design, was regarded as extremely remote. The

corrective action implemented through Design Change Recuests (DCRs) 97-

016 and 97-017 was reviewed. Updated lists of affectec motor-operated

valves were included in the DCR packages. The inspectors verified that

the complete list of valves was modified per DCR 97-016 during the Unit 1

Fall 1997 refueling outage. The updated list for DCR 97-017 (Unit 2), to

be accomplished in the Fall of 1998 was also verified. i

Based upon the inspectors review of the licensee's actions in response to

IN 92-18, and an assessment of the licensee's reportability

justification, this URI is closed

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E8.2 (Closed) URI 50-366/97-11-08: Unit 2 Failure to Meet General Desian

Criteria 56 for Procer Automatic Containment Isolation Valve Outside '

Containment.

This item is documented in Section E2.1 of IR 50-321. 366/97-11 and was

pending further NRC' review. The NRC conducted additional reviews of this

problem and acknowledged that both units have identical designs and that

3 resents little safety significance. The licensee's exemption request is

3eing reviewed by the NRC. Based upon the inspectors review of

licensee's actions and the minor safety significance of the problem, this

item is closed.

E8.3 (Closed) Licensee Event Reoort (LER) 50-321/97-04: Sinole Failure Renders

inocerable the RHRSW Lona-term Containment Heat Removal Mode.

This event is documented in section El.1 of IR 50-321, 366/97-07.

relating to licensee-identified inadequate cable separation issues. The

inspectors reviewed the licensee's corrective actions, which included

detailed walkdowns of the emergency 4160-volt switchgear and selected

control room panel circuits. Circuits that did not meet electrical

separation criteria were evaluated by the Architect-Engineer and found to

be acceptable. The inspectors reviewed the safety assessments, which

were thorough and detailed. Additional cable separation deficiencies

were corrected by Maintenance Work Orders (MW0s) to wrap cables with

S11 temp which is a qualified barrier and secured with tie-wrap.

Based on the inspectors review of licensee actions, this LER is closed.

IV Plant Support

R1 Radiological Protection and Chemistry (RP&C) Controls

R1.1 Conduct of Radiological Protection Controls (71750)(83750)(84750)

a. Insoection Scooe

Radiological controls associated with on-going routine Unit 1 (U1) and l

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Unit 2 (U2) operations were reviewed and evaluated by the inspectors.

Reviewed program areas included area postings and radioactive waste 4

(radwaste) and material container labels, high and locked-high radiation i

area controls, and procedural and radiation work permit (RWP)

implementation. In addition, operational status of offsite environmental

monitoring station equipment was verified.

The inspectors made frequent tours of Radiological Control Areas (RCAs)

and observed work activities in progress. In particular, radiation l

control practices and Health Physics (HP) staff activities were observed.

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Results of ongoing radiation and contamination survey results wes  ;

veri fied. Tours of selected offsite environmental monitoring stations i

j and direct observations of equipment operability were conducted.  !

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Established radiological controls were compared against ap)licable

sections of the Updated Final Safety Analysis Report (UFSAR) and the

applicable requirements specified in licensec procedures. Technical

Specifications (TSs). Offsite Dose Calculation Manual (ODCM), arid

10 CFR Part 20.

b. Observations and Findinas

Area postings and container labels were determined to be adequate for the

associated radiological conditions. Controls for high and locked high-

radiation areas were implemented appropriately. Dose rate and

contamination survey results were conducted with calibrated

instrumentation. Radiation and contamination surveys were conducted in 3

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accordance with approved procedures and results met regulatory

requirements.

No operational concerns were identified for the offsite Radiological

Environmental Monitoring Program (REMP) equipment. For the environmental

monitoring stations visited, thermoluminescent dosimeters (TLDs), and the i

surface water and air sampling equipment were verified to be in place.

calibrated properly and operational in accordance with procedural or ODCM

specifications.

c. Conclusions

Radiological controls for normal operations and for routine radwaste

processing, storage and transportation activities were maintained in

accordance with procedural. TS. and 10 CFR Part 20 requirements.

Current offsite radiological environmental monitoring program equipment,

instrumentation, and operations met procedural and ODCM requirements.

R1.2 Release of Material to the Onsite Landfill (83750. 84750)

a. Insoection Scooe

Radiation Protection program activities associated with the unconditional I'

release of materials from RCAs were reviewed and discussed. In

particular, the inspectors reviewed and discussed licensee actions

associated with review of NRC unresolved item (URI) 50-321, 366/97-10-06.

This item documented the release of potentially contaminated materials

from the Waste Separation and Temporary Storage (WSTS) facility area RCA  !

whicn subsequently were buried in the onsite landfill. The inspection l

included extensive interviews with licensee and contractor health physics

technician (HPT) staff. su)ervisors, and managers. Detailed reviews and  ;

discussions of the applica)le entries in the WSTS facility logbook were l

conducted. 1

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Enclosure 2

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34

The HPT staff's understanding and implementation of applicable procedures

were reviewed. The following Administrative Control (AC), Radiation

Protection (RP) and Health Physics Instrumentation (HI) procedures and

Health Physics Information Letter (HPLI) guidance regarding completion

and documentation of radiological surveys of materials released from

established RCAs for disposal. in the onsite landfill were reviewed and

discussed with responsible staff. ,

e Procedure, 60AC-HPX-007-0S, Control of Radioactive Materials,

Revision (Rev.) 4.

. Procedure, 60AC-HPX-004-05, Radiation and Contamination Control,

.Rev. 14.

. Radiation Protection (RP) Procedure 62RP-RAD-017-05, Release

Surveys, Rev. 6.

Rev. 9.

. -Procedure 62HI-0CB-056-OS, Waste Separation and Temporary Storage

Facility, Rev. 6.

.- Health Physics Information Letter Number (No.) 96-13. Rev. 1.

Calibration, Rev. 8. l

e Procedure 62HI-0CB-019-05, Geiger Counter Model E0120 Operation

and Calibration. Rev. 4.

Rev. 3.

The inspectors reviewed and discussed opplicable radiation and

contamination data, including. survey records of the pre-demolition U1

Radwaste facility floors and walls, drums containing radwaste building i

concrete debris released from the main power block RCA, concrete debris

released from the WSTS facility RCA, and qualitative gamma-spectroscopy

analyses of concrete rubble retrieved.from the onsite landfill during the

week of June 8, 1997. On January 14, 1998, the inspectors directly

observed and verified supplemental gamma surveys using a Ludlum Micro R

meter conducted at the two onsite landfill trenches where the U1 Radwaste

Building concrete deoris was deposited prior to June 10, 1997.

Inspection of staff training and licensee actions subsequent to

identification of the issue are documented in Sections ('SS) R5.1 and R7.1

of this report.

The established radiological controls and actions were compared against

applicable procedural guidance, and requirements of 10 CFR Parts 20 and

50, as applicable.  ;

.

Enclosure 2

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i^ .

.

b. Observations and Findinos

'

l . Based'on discussions with licensee and contractor HPTs and from review of

associated WSTS facility logbooks, the inspectors noted that the buried

material. concrete debris, was generated during construction of a

contaminated tool room in the Unit 1 Radioactive Waste (Radwaste)

building. Only concrete debris from the U1 Radwaste Building

132 foot (') elevation was transferred to Sealand trailers located

adjacent to.the WSTS building entry and within the facility's established

RCA. The concrete was processed for unconditional release within the

WSTS facility RCA and buried .in the onsite landfill between December 1.

1996, through June 10, 1997.

Pre-demolition radiological surveys of the U1 Radwaste Building '132'

elevation conducted between October through December, 1996, documented

that significant fixed surface contamination was present in the area.

Initial decontamination'of the concrete included removing and disposing

of the outer painted surfaces of the concrete walls and floor as

, radioactive waste. Survey records of drums of concrete rubble originally

designated for processing at the WSTS facility documented maximum dose-

rates of 20 millirad (mrad) contact and 0.7 mrad at one meter. No core

samples from the U1 Radwaste Building floors or walls were taken and

submitted for gamma spectroscopy analysis to evaluate potential internal

contamination on the internal surfaces of the walls or floors. Excluding

a single use of a sorting table gamma-sensitive monitor on June 6. 1997,

the concrete debris was hand-frisked using a Geiger-Mueller (GM) E-120

detector at the WSTS facility work area and segregated into clean and

contaminated material based on established guidelines. Subsequently, the

clean concrete material was placed into drums or boxes. Periodically

each drum or box of clean concrete was re-surveyed using a Ludlum Micro-R i

meter prior to release from the WSTS. facility RCA and transferred to the  !

onsite landfill. The concrete debris was placed into the open burial l

trenches: and re-surveyed prior to its being covered in the landfill j

trench.

In response to employee concerns regarding the adequacy of surveys of the {

concrete materials conducted at the WSTS facility RCA. a quality control '

check of the landfill trenches was conducted by the licensee on June 8, l

1997. Although the majority of concrete taken to the landfill was

buried licensee representatives identified several pieces of U1 Radwaste

building concrete either in, or adjacent to the landfill trench in use.

Approximately seven pieces of concrete were identified where traces of 3

surface paint had not been removed. Surveys of these concrete pieces  ;

resulted in count rates slightly above the licensee procedural release i

limits of 1000 disintegrations per minute (dpm) per probe area.  !

'Oualitative gamma-spectroscopy analyses conducted between June 9 through

. June 11, 1997. verified that Cobalt-60 and Cesium-137 radionuclides were

L associated with the concrete material. The inspectors noted that l

L 10 CFR 20.2001(a) requires, in part. disposal of licensed material only l

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by. transfer to an authorized-recipient as provided in section (5)

20.2006. The inspectors identified the disposal of. contaminated material

in the onsite landfill as Violation (VIO) 50-321.366.97-12-07. Failure

.

to Dispose of Licensed Material in Accordance with 10 CFR 20.2001(a)

Requirements. Individual surveys of the remaining pieces of unburied

concrete. approximately one-third of a drum, recovered from the landfill

, did not indicate any of the items exceeded the established release

limits. As of June 10. 1997, the licensee stopped disposal of U1

-

Radwaste Building concrete debris into the onsite landfill.

The identification of licensed material in the onsite landfill indicated

potential weaknesses in the use of the GM E-120 and Ludlum Micro R survey

instruments to unconditionally release the concrete from the WSTS

facility area. For example, core samples of the radwaste building

concrete floors and walls followed by gamma spectroscopy analyses were

not conducted to verify that the surveys of accessible surfaces were

representative of inaccessible areas. In addition to the pieces of

concrete having flat planar surfaces, the debris included irregularly

shaped pieces, small particles and dust, all of which were more

appropriately analyzed using supplemental gamma-sensitive automated

surveys of the aggregate materials to identify the low level radioactive

contamination. A gamma-sensitive automated Sorting Table was used on

June 6. 1997 for only one batch of material.

Inconsistencies and confusion regarding HPT and management understanding

of procedural methods and equipment availability for WSTS facility

operations were noted. For example. contract and licensee HPTs and

seva al first-line su3ervisors understood Section 7.1.2 of 62RP-RAD-017

Section 7.1.2 and HPI_ No. 96-13 to require the use of an automated

monitoring system, i.e., the SAM 9. for releasing the concrete materials

from the RCA. However. licensee management interprettt the procedure and

documented guidance to imply use of the equi) ment only if the SAM 9

detectors were established and assigned to t ie specific task. Also, the

inspectors noted-inconsistent responses among staff and management

regarding the specific procedures used for releasing m6terials. survey

instrument response times, and the need to take core samples for j

unconditionally releasing the concrete debris from the WSTS facility

area <

Prior to June 1997, licensee oversight of the release of concrete Gebris

from WSTS facility RCA was limited. Several licensee and contractor HPTs

stated that as a result of concerns regarding frisking of the material, a

request to use SAM 9 detectors to conduct surveys of the aggregate

concrete materials was discussed with direct supervisors but no actions

were taken. Review of Instrument and Calibr 'on Department records

indicated that SAM 9 detectors were calibrat and could have been made

available for use. Huwever, licensee manage wnt representatives stated

that they were unaware of the requests to use the SAM 9 equipment.

Enclosure 2

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Concernt, were also identified to licensee management regarding the

documentation and maintenance of applicable radiological surveys

conducted. Records of surveys conducted for release of concrete from the

WSTS facility RCA and at the landfill only documented results of direct

and smearable contamination levels of the concrete debris released to the

landfill . Based on discussions with several contractor technicians and

supervisors, gamma scintillation surveys of each drum or box of aggregate

concrete material were made as required by Section 7.5.1 of

62RP-RAD-017-0S prior to release from the WSTS facility area and also

after placement of the material in the landfill using a Ludlum Micro R

meter. Although procedure 62RP-RAD-008-0S recuired accurate and legibly

documented surveys to evaluate the present anc potential radiological

hazards and to comaly with the regulations of 10 CFR 20. results of the

final surveys of t1e aggregate materials released from the RCA and

subsequent to alacement in the landfill were not documented or

maintained. T1e inspectors identified this failure to follow

radioactivity control procedures in accordance with TS 5.4.1.a as another

example of VIO 50-321, 366/97-12-09. Failure to Follow Procedures -

Multiple Examples.

Licensee representatives statec that all unburied concrete had been

retrieved and the transfer of material to the landfill terminated. No

concrete rubble was observed during tours of the onsite landfill trenches

during the week of January 12, 1998. Measured exposure rates directly

above the two filled trenches where the concrete debris was buried were

similar to background values, approximately 10 micro-Roentgens per hour.

c. Conclusions

A violation regarding disposal of licensed material in the onsite

landfill was identified: Failure to Dispose of Licensed Material in

Accordance with 10 CFR 20.2001(a) Requirements.

The lack of automated gamma-sensitive ecuipment to conduct survey

aggregate concrete debris was identifiec as a significant program

weakness.

Technician and management interpretations of procedural requirements were

inconsistent.

Prior to June 1997. licensee management of the release of U1 Radwaste

Building debris from the WSTS facility was limited.

A violation of TS 5.4.1.a for failure to follow procedures for

documenting release surveys was identified as another example of VIO

50-321, 366/97-12-09. Failure to Follow Procedures - Multiple Examples.

No ex)osure rates above background were identified for the two landfill

trencies where the U1 Radwaste Building concrete debris was buried.

Enclosure 2

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L

RI.3 Fission Product Monitor Grab Samolina

a. Insoection Scooe (71750)

l

L The inspectors reviewed procedure 64CI-0CB-005-0S, " Fission Product

L Monitors," Rev. 2. Ed 1, and observed a chemistry technician perform a

grab sample of the drywell atmosphere. The inspectors also reviewed TS 3.4.5, RCS Leakage Detection Instrumentation. The drywell grab samples

were required per the TS due to the Fission Product Monitor (FPM) System

being inoperable.

b. Observations and Findinas

,

On January 15. the inspectors observed a radiological protection (RP)

chemistry technician take grab samples of the drywell atmosphere. This

activity was performed in accordance with Chemistry Instrumentation

Procedure 64CI-0CB-005-0S.

The inspectors observed that the noble gas activity for the grab sample l

obtained by RP chemistry at 9:00 p.m. on January 11 had an asterisked

notation, indicating that the acceptance criteria specified on the data

sheet had been exceeded. The statement "will monitor" was entered on the

data sheet as an explanation of the asterisk. The subsequent 12-hour

reading for the noble gas activity was within the acceptance criteria.

The asterisked notation on the data sheet indicated that the readings

would be monitored but that no compensatory measures beyond that required

for a normal reading were taken. The ins)ectors discussed this with RP

Chemistry supervision and were infornied tlat no compensatory actions were

taken for this reading because the subsequent 12-hour reading was within

the acceptance criteria and the total activities involved were relatively

-small

The inspectors observed from a representative sampling of control room

log entries that the RP chemistry department had notified control room

personnel of the drywell oxygen concentration. The inspectors noted that

the results of the noble gas sampling was not documented. The shift

supervisor informed the inspectors that the isotopic noble gas results

reported by RP chemistry personnel typically are not logged if they are

acceptable. Operations personnel were not aware of the noble gas reading

of January 11 which exceeded the acceptance criteria.

The inspectors were informed by chemistry supervision that the procedure

would be enhanced to provide clearer guidance for noble gas readings that

exceed the acceptance criteria.

l Enclosure 2

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c.. Conclusions

' The RP Chemistry technician observed taking a drywell grab sample was

professional and knowledgeable of procedural requirements. Procedural

weaknesses were identified for guidance associated with actions to be

taken when noble gas readings exceed the acceptance criteria.

R2 Status'of RP&C Facilities and Equipment

R2.1 Fission Product Monitorina (FPM) System Problems on Unit 1-

l

a.-Insoection Scooe (71/50)(37551)(92904J -

The inspectors reviewed system operating procedure 3450-D11-001-15.

" Fission Product Monitoring System.~ Rev.1. Ed 1: and chemistry

instrumentation ]rocedure 64CI-0CB-005-0S, " Fission Product Monitors."

Rev. 2. Ed 1. T1e inspectors also reviewed MWO 1-98-0057 and held

discussions with licensee personnel. The documentation review and

discussion were associated with the Fission Product Monitor System and

Commercial Grade Oxygen Analyzer (CGOA) problems.

b. Observations and Findings 1

The' inspectors observed that the licensee began trouble shooting .

activities associated with the Unit 1 FPM on January 8 as a result of i

'

abnormally The. licensee determined

frc"! troublehigh drywell

shooting Oxygen.hat

activities (0[)the

content.

control room reading for the

CGOA was affected when the FPM particulate pump 1011-C026 was operating.

This pump was replaced and the same effects were observed when the pump

was run. Continued troubleshooting activities icd the licensee to.

believe that an obstruction existed in the FPM drywell return line. It

was believed that the restriction caused a back pressure on the CGOA.

thus causing _it to read incorrectly high.

The' diagnostic activity for determining the location of the restriction l

to flow, invalved the monitoring of flows and pressures at the CGOA with '

all pumps running while individually opening serious valves to create a

vent )ath from the FPM drywell return line. The trouble shooting results  ;

led tie team to believe that the suspected obstruction was caused by  !

either the FPM outboard isolation valve 1D11-F052. or the inboard  ;

isolation valve 1D11 F050. 1

During this trouble shooting activity, the 1Dll-F131 containment manual l

test valve was opened as part of the diagnostic testing for venting the  ;

FPM drywell return line. Chemistry. maintenance. and operations i

personnel were performing the troubleshooting activity when the valve was  ;

opened. Chemistry personnel had the lead responsibility for the

'

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troubleshooting activity. The inspectors observed. from a review of

procedures 3450-D11-001-15. Attachment 2, FPM System Valve Lineup, and

I

,

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Enclosure 2

40

64CI-0CB-005-0S, Attachment 4. FPM Sam)le Panel Schematic, that the

normal position of manual test valve 1)11-F131 is closed.

Normally-closed valve 1011-F131 is on a 3/4-inch diameter capped pipe

that is connected to the main FPH return line to the drywell. The 3/4-

inch piping connects to the FPM return line between the drywell and the

inboard FPM isolation valve 1D11-F050. The cap on the end of the piping

that contained the ID11-F131 manual valve was removed by the

troubleshooting team prior to opening the valve. The valve was opened

for approximately.five minutes during the trouble shooting activity.

Drywell integrity was lost during the time that the valve was open. The

activities of removing the piping end cap and opening valve 1011-F131 was

not discussed with or approved by the Shift Su)ervisor (SS). The

ins)ectors were informed that overall troubleslooting methods and

tec1niques did not meet management's expectations. The opening of manual

valve 1011-F131 by the trouble shooting team that resulted in a breach of

drywell integrity was of minor safety significance and is identified as

NCV 50-321/97-12-08. Personnel Error.Results in a Breach of Drywell

Integrity, in accordance with NUREG 1600.Section VII.

Trouble shooting personnel concluded after opening valve.1D11-F131 and

removal of the end cap that an obstruction existed in or near the 1011-

F050 FPM Drywell isolation valve. The SS conservatively declared the

1011-F050 valve inoperable when Chemistry reported that an obstruction

ap) eared to be in or near the valve. The appropriate TS actions were

ta(en for the inoperable primary containment 1 solation valve. Chemistry

also began taking grab samples for 02 concentration and noble gas

activity in the drywell for the inoperable FPM system, as required by the

TSs. The inspectors observed the performance of a grab sampling activity

as discussed in Section R1.3 of this report.

Testing similar to a local leak rate test was performed by engineering

subsequent to the SS declaring the 1011-F050 valve inoperable. This

testing demonstrated the operability of the 1D11-F050 valve. The

ii.spectors observed portions of this testing activity. j

i

A problem solving team was convened by Nuclear Safety and Compliance to i

continue the investigation into the behavior of the FPM system and the '

high 0, readings on the CGOA. Early in the investigation, an engineer 1

suggested that the apparent obstruction may be the symptoms of the ,

normal, expected pressure drop in the return line. The engineer  !

demonstrated through calculations that the pressure drops observed in the  !

line during the previous troubleshooting activities could be accounted

for by the flow through drywell isolation valves 1D11-F050 and 1D11-F052.

Hence, the FPM return line obstruction theory was discontinued.

The problem solving team concluded that the FPM and CG0A systems are more

sensitive to pressure flow interactions than had been previously  !

understood. Small adjustments in pressures and flows on the FPM system

produced immediate. visible effects on the flows and pressures of the

Enclosure 2 .

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41

'

CGOA system. The teamed believed that the behavior of the FPM system and

the high 02 was due to a confluence of factors including incorrect

operation of the CGOA system, vacuum leaks. and degraded components.

As corrective actions for system operation, the following were undertaken

by the licensee:

Filters 1D11-D044 and 1D11-0045 were changed. New filter paper was

installed in the FPM system. New flow control valves were installed in )

the FPM system on both the particulate monitoring panel and the

iodine / noble gas panel. The FPM particulate monitor was checked and

found to be free of obstruction. The flows and pressures were set up on

the FPM and CGOA system in accordance with their operating procedures.

The FPM and CGOA systems were placed back in service on January 23 and

have operated with no problems since.

c. Conclusions

Trouble shooting activities by chemistry with maintenance and operations

support were not well-planned or coordinated. The problem solving team

convened by NSAC conducted an excellent investigation for the root causes

of the FPM and CG0A problems. A Non-Cited Violation for a personnel

error which resulted in a breach of drywell integrity was identified.

R3 RPC Procedures and Documentation

i

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a. Insoection Scooe (717501

The inspectors reviewed procedure 62RP-RAD-004-05. " Personnel

Decontamination." Rev. 8. five Personnel Contamination Reports (PCRs),

and discussed the licensee's assessment of the contamination problems and

recommended corrective actions with health physics (HP) supervisors. '

b. Observations and'Findinas

The inspectors observed that the procedure provided guidance as to when )

PCRs were required. One requirement was that for a personnel

contamination level greater than or equal to 10.000 dpm, a PCR would be

completed. - The inspectors observed that all five PCRs reviewed were for

contamination levels greater than 10.000 dpm. Personnel involved

included two from maintenance, two from health physics, and one from

chemistry. Two contaminations occurred in a designated clean area. For

these problems. one area was decontaminated and one area was roped off ,

and identified as a contaminated area. The inspectors observed that. 1

although the licensee has recently placed more emphasis on housekeeping

and decontamination activities, contaminations in a clean area is a

recurring problem. Two PCRs indicated that an improper work practice

was the root cause. The inspectors concluded that a third contamination  ;

j problem was also due to an improper work practice. In this case. '

I Enclosure 2 !

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maintenance activities included dry surface grinding which resulted in

contamination on the individual's face and mouth area. The PCR indicated

that the root cause was due to changing conditions that exceeded the-

capacity of protective clothing (PCs). The inspectors observed that the

grinding was discussed with HP supervision.

The inspectors observed that one section of the PCR was used to document

the investigation and corrective actions. Although the inspectors

observed that generally the investigation was adequate..they concluded

that the recommended corrective actions were narrow. For example, while

calibrating a conductivity cell in the lab without wearing gloves, one

individual become contaminated. There was no corrective action

documented. However. the PCR indicated the individual was asked what he

would do differently next time. For the maintenance person who become

contaminated during dry grinding. the corrective action was to add a

s)ecial instruction on the radiological work permit to require that all

a)rasive operations be performed wet and for workers to wear grinding

shields and facial protection. There were no recommendations for general

work practice improvement-(grinding work is generally skill-of-craft),

training, or discussion for shift briefings similar to recommendations

observed in other departments.  !

The inspectors observed that step 7.1.3.4 of procedure 62RP-RAD-004-0S 4

required, for certain conditions, that a more detailed investigation be l

completed. One of these conditions was that "three or more l

contaminations have occurred on a shift from the same location." The  !

inspectors discussed this observation with HP personnel to gain a better

understanding of management's expectations to reduce contamination i

events. HP personnel stated that the procedure would be reviewed. i

c. Conclusions

The inspectors concluded that the investigations for personnel I

contamination reports were generally adequate. The recommended  ;

corrective actions were not 6 ways thorough and comprehensive. Others l

were narrow.in focus and in some reports recommended corrective actions j

were not submitted. ,

R5 RP&C Training and Qualification (83750. 84750)

R5.1 Contractor Health Physics Technician Trainina

a. Inspection Scooe

Training provided to six contract HPTs involved with surveying.

unconditionally releasing, and subsequently transporting and disposing of

the U1 Radwaste Building concrete at the onsite landfill was reviewed.

The review included evaluation of applicable radiation protection program

'HPT study guides, verification of completion of training and an i

Enclosure 2

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assessment of contractor and licensee staff understanding of procedural

requirements.

l- The 3rovided training was reviewed against requirements specified in

L 10 C R Part 19 and Departmental Instruction (DI) DI-HPX-02-0286N. HP/ CHEM

l

New Employee Check-In Rev. 6.

b. Observations and Findinas

The training reviewed and tested technicians on ap)licable surveys. and

the control and release of materials from establisled RCAs. For the

contract HPTs involved in the WSTS facility RCA release activities,

training was determined to be current. Both contract and licensee HPTs

displayed appropriate knowledge of procedural guidance and details,

c. Conclusions

Training provided to contract HP technicians involved in surveying,

releasing. and disposing of U1 Radwaste Building concrete in the onsite

landfill was current and met procedural and 10 CFR Part 19 requirements.

R7 Quality Assurance in RP&C (83750, 84750) i

1

R7,1 Identification and Corrective Actions for Contaminated Material Released I

to the Onsite Landfill  !

i

a. Inspection Scooe

Licensee actions subsequent to verification that concrete rubble I

containing low levels of radio nuclides was released to the onsite i

landfill were reviewed and discussed. The review included interviews of ,

contractor and licensee HPTs. supervisors and managers, and a review of  :

the WSTS facility logbooks and deficiency control documents.  !

Program implementation and licensee actions were evaluated against .

3rocedural requirements specified in procedure 10AC-MGR-004-05.  !

Jeficiency Control System. Rev. 10.

b. Observations and Findinas

From discussions with cognizant licensee and contractor personnel, the

inspectors determined that initial concerns regarding the adequacy of  :

radiological surveys and the potential for release of licensed material

to the onsite landfill were identified during the week of June 2.1997.

On June 9.1997 licensee HPT staff identified approximately seven small

pieces of concrete rubble at the landfill. The rubble should have had

l

'

the green paint removed during decontamination activities. Surveys of

the subject pieces of rubble using a GM E-120 detector indicated count

,. - rates slightly exceeding 1000 disintegrations per minute (dpm) per probe '

area. Qualitative gama-scan analyses of the free-released pieces of

Enclosure 2

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concrete rubble conducted between June 9-11, 1997. verified low-level l

radioactive contamination from Cobalt-60 and Cesiumd37 radio nuclides.

From review of licensee commitment tracking data base, the inspec-t6rs

noted that although both HPTs. supervisors, and managers were aware of

the identified concerns during the initial weeks of June 1997 the issue

was not entered into the licensee's tracking system until August 9, 1997.

The inspectors determined that licensee HPT staff initially identified

their concerns to immediate supervisicn and subsecuently to upper

management. Licensee resolution documentation incicated that the

identified concern was treated as an expected statistical anomaly rather

than a deficient radiological concern because the contamination values

were near the release criteria, i.e., the survey instrumentation lower

limit of detection. The inspectors noted that the initial concern

included the adequacy of surveys for unconditionally releasing

potentially radioactive concrete debris from the U1 Radwaste Building and

that the positive gamma-scan analyses verified that at a minimum,

approximately seven ]ieces of the low-level contaminated concrete rubble

was transferred to t1e onsite landfill contrary to 10 CFR 20.2001(a).

The inspectors noted that Administrative Control (AC) procedure 10AC-MGR-

004-05 Deficiency Control System. Rev.10, required, in part, that an

identified deficiency be entered into the NUCLEIS computer system.

reported to the Plant Dispatcher or documented on a written deficiency

card within one hour. Conditions requiring completion of a deficiency

card included not meeting 10 CFR Part 20 regulations. The inspectors

noted that the disposal of licensed material in the onsite landfill met

the criteria for initi6 ting the deficiency card in a timely manner and

that the health physics section was responsible for initiating DCs

identifying low level waste mishap events. This issue was identified as

another example of a violation for failure to follow procedures. VIO 50-

321, 366/97-12-09. Failure to Follow Procedures - Multiple Examples.

Licensee actions taken in response to the identified concerns were

reviewed and discussed with responsible 1scensee representatives.

Although a statistical conclusion regarding the identification of a

" false negative" response was provided to both the NRC Resident

Inspectors and representatives of the State of Georgia. Environmental

Protection Division no estimation of the notential maximum quantities

and types of radionuclides which could have been placed into the onsite

landfill was presented. Based on this statistical interpretation,

licensee documents indicated that no additional actions were necessary.

The inspectors noted that 10 CFR 50.75(g) requires records of unusual

occurrences such as the spread of contamination in and around the site

which are important to the decommissioning of the facility to be

maintained. As of January 12, 1998. the licensee had not included the

information regarding the potential burial of radionuclide contaminants

in the onsite landfill in the site's decommissioning records. This issue

was identified as V10 50-321, 366/97-12-10. Failure to Maintain

Decommissioning Records in Accordance with 10 CFR 50.75(g) Requirements.

Enclosure 2

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c. Conclusions

Licensee HPTs appropriately identified the disposal of licensed material

in the onsite landfill as a deficient radiological condition.

An additional example of VIO 50-321. 366/97-12-09. Failure to Follow I

Procedure.s - Multiple Examples, was identified.

A violation. 50-321, 366/97-12-10, was identified for failure to maintain

decommissioning records in accordance with 10 CFR 50.75(g) requirements.

R8 Miscellaneous RP&C Issues (83750, 84750)

R8.1 .(Closed) Unresolved Item (URT) 50-321. 366/97-10-06: Review Licensee

Final Evaluation and Correctlye Actinns for Contam_inated Concrete Waste  ;

iaterials Released to the Onsite Landfill ,

Inspector review of this issue is documented in Sections R1.2. RS.I. and

R7.1 of this report. Based on these reviews, this item is closed.

P2 Status of EP Facilities, Equipment, and Resources

P2.1 Self-Contained Breathina Aooaratus (SCBA) Insoection

a. Insoection Scooe (71750)

The inspectors reviewed procedure 62RP-RAD-003-09. ~Use and Care of

Respirators." Rev. 7. ED 1. and observed a portion of the monthly

inspection of SCBAs designated for emergency use. The inspectors toured

emergency facilities to verify that they were in standby readiness and

conducted telephone communication checks.

b. Qbjervations and Findinas

The inspectors observed that personnel conducted inspections of SCBAs

stored in the 0)erations Su) port Center (OSC) without the use of a

procedure, checclist or otler guidance. The inspectors discussed this

observation with management personnel and were informed that procedure

62RP-RAD-003-0S was not a procedure that required continuous use. The j

SCBA inspections were generally performed as skill of the craft. The i

inspectors did not observe any deficiencies in the inspection process,

c. Conclusions

The inspectors concluded that the SCBAs were being properly maintained.

The emergency facilities were maintained in a sate of readiness and the ,

, telephone communications checks were satisfactory. l

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S2 Status of Security Facilities and Equipment (71750)  ;

The

fenceinspectors

was intact toured

and notthe protected area

compromised and observed

by erosion that the

or disrepair. kerimeter

he fence

fabric was secured and barbed wire was angled as required by the

licensee's Plant Security Program (PSP). Isolation zones were maintained

on both sides of the barrier and were free of objects which could shield

or conceal an individual. The inspectors observed that personnel and  !

packages entering the protected area were searched either by special )

purpose detectors or by a physical patdown for firearms. explosives and ,

contraband. Badge issuance was observed, as was the processing and l

escorting of visitors. The licensee searched. escorted, and secured

vehicles as described in applicable procedures.

The ins)ectors concluded that the areas of security inspected met the

applica)le requirements.

V. Manacement Meet _if.gs

X.1 Hanagement Changes  !

On January 10. 1998, the licensee announced the following management

changes that were effective immediately:

i

. P. E. Fornel, from Performance Team Manager to Plant Modification

and Maintenance Support Manager

  • M. H. Googe, from Operations Shift Supervisor to Performance Team

Manager

X.2 Review of UFSAR Commitments

A recent di.scovery of a licensee operating its facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

practices, procedures and/or parameters to the UFSAR description. While

performing the inspections discussed in this re] ort, the inspectors

reviewed the applicable portions of the UFSAR t1at related to the areas

inspected. The inspectors observed that the licensee have initiated a

UFSAR update change to remove the TIP Purge Solenoid Valve 1C51-F3012 and

2C51-F3012 for Units 1 and 2. res)ectively. from the UFSAR listing of

PCIVs. The inspectors verified tlat the UFSAR wording was consistent

with the observed plant practices, procedures, and/or parameters.

X.3 Exit Meeting Summary

The inspectors presented the inspection results to members of the

licensee management at the conclusion of the inspection on February 20.

1998. The licensee stated that the three violations proposed in the RP &

l C section would be denied. An interim exit was conducted on January 16,

1998. On. March 2 and March 3. 1998, teleconferences between NRC Region

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II management and Mr. S. Tipps. Manager, NSAC Hatch Nuclear Plant, were

conducted to address issues raised during a February 23, 1998. NRC/ Hatch

Nucleer Plant Management Meeting. The discussed issues involved.

. violations specifically associated with improper disposal. of licensed

material into the onsite landfill.

l. .

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. 'No proprietary

!

information was identified.

X.4 Other NRC Personnel On Site

i On January 12. Mr. H. N. Berkow. Director Project Directorate 11-2.

Division of Reactor Projects (DRP)-I/II. Office of Nuclear Reactor

Regulation (NRR): Mr. L. N. Olshan. Senior Project Manager Hatch. Project

Directorate II-2. DRP-I/II. Office of NRR; Mr. L. L. Wheeler. Senior

Project Manager, Non-Power Reactors and Decommissioning. Project

Directorate, Division of Reactor Program Management. Office of NRR: and

Mr. D. H. Jaffee. Senior Project Manager Vogtle. Project Directorate II-

2. DRP-I/II. Office of NRR. visited the site. They met with the resident

inspector staff to discuss licensee performance and regulatory issues.

They toured the facilities to observe equipment in operation and general

plant conditicns. They attended the morning management meeting and met i

licensee managemerit personnel. l

PARTIAL LIST OF PERSONS CONTACTED

Licensee

Anderson. J., Unit Superintendent .

Bets 111. J., Assistant General Manager - Operations

Bennett. D., Health Physics Superintendent .

Breitenbach, C.. Engineering Support Manager - Acting l

Carr, W., Environmental Services Manager. Corporate

Coleman..V.. Chemistry Supervisor

Curtis. S., Unit Superintendent

Davis. D., Plant Administration Manager

fornel. P., Plant Modification and Maintenance Support Manager

Fraser. 0.. Safety Audit and Engineering Review Supervisor

Googe. M. Performance Team Manager

Hammonds. J., Operations Support Superintendent

Kirkley. W.. Health Physics and Chemistry Manager

E Lewis, J.. Training and Emergency Preparedness Manager

Madison, D., Operations Manager

McCracken. D., Manager of Regulatory Engineering and Environmental l

Services. Corporate

Metzler. T., Nuclear Safety and Compliance Manager. Acting

Moore. C.. Assistant General Manager - Plant Support

Reddick. J., HP Su3ervisor Support

Reddick. R. , Site Emergency Preparedness Coordinator

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Riner. G., Plant Health Physicist

Roberts. P., Outages and Planning Manager

Smit'.1. D. , Chemistry Superintendent

Thonpson. J. , Nuclear Security Manager

finps. S., Nuclear Safety and Compliance Manager

Wells. P. , General Manager - Nuclear Plant

IMSPECTION PROCEDURES USED

IP 37550: Engineering

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying. Resolving.

and Preventing Problems

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations '

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 83750: Occupational Radiation Exposure

IP 84750: Radioactive Waste Treatment, and Effluent and Environmental

Monitoring l

IP 92700: Onsite Follow-up of Written Reports of Nonroutine Events at  !

Power Reactor Facilities l

IP 92901: Followup - Operations l

IP 92902: Followup - Maintenance / Surveillance  ;

IP 92903: Followup - Followup Engineering i

IP 92904: Followup - Plant Support i

ITEMS OPENED AND CLOSED  :

Ooened

50-321, 366/97-12-01 IFI Review of Operations. Mairtenance and I

Engineering Actions for Long-Term

Resolution of Running the EDGs  !

Unloaded or at low Loads

(Section 02.1).

50-366/97-12-02 VIO Failure to Implement Changes to Vendor

Manual (Section 02.2).

50-321/97-12-03 NCV Failure to Follow Procedure for

Scheduling Weekly Testing of RPS Scram

Test Switches (Section M3.3).

50-321. 366/97-12-04 IFI Review of IST Basis for PSW Makeup I

Valves to Spent Fuel Pool

(Section E2.2). j

50-321, 366/97-12-05 VIO Failure to Include Nitrogen Valves in

a Test Program In Accordance with 10

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CFR 50.Section XI of Appendix B. Test

Control (Section E2.5).

50-321, 366/97-12-06 VIO Insulation on Nitrogen Supply Piping

Not Installed in Accordance with

Drawings (Section E2.5)

50-321, 366/97-12-07 VIO Failure to Dispose of Licensed

Material in Accordance with

10 CFR 20.2001(a) Requirements

(Section RI.2).

50-321/97-12-08 NCV Personnel Error Results in a Breach of

Drywell Integrity (Section R2.1).

50-321, 366/97-12-09 VIO Failure to Follow Procedure - Multiple

Examples (Sections 02.2. R1.2, and

R7.1).

50-321, 366/97-12-10 VIO Failure to Maintain Decommissioning

Records in Accordance with

10 CFR 50.75(g) Requirements

(Section R7.1).

50-321, 366/97-12-11 URI Timeliness of Identification of SLMCPR

Errors (Section E3.8).

50-321, 366/97-12-12 URI Timeliness of Amendment of Technical

Specifications (Section E3.12).

Closed

50-321, 366/97-05-04 URI Determine the Reportability of

Licensee-Identified Deficiencies With

Respect to IN 92-18. ' Potential for

loss of Remote Shutdown Capability

During a Control Room Fire"

(Section E8.1).

50-366/97-11-08 URI Unit 2 Failure to Meet General Design

Criteria 56 for Proper Automatic

Containment Isolation Valve Outside

Containment (Section E8.2).

50-321/97-04 LER Single Failure Renders Inoperable the

RHRSW Long-term Containment Heat

Removal Mode (Section E8.3).

50-321, 366/97-10-06 URI Review Licensee Final Evaluation and

, Corrective Actions for Contaminated

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Concrete Waste Materials Released to

the Onsite Landfill (Section R8.1)

50-321/97-12-03 NCV Failure to Follow Procedure for

Scheduling Weekly Testing of RPS Scram

Test Switches (Section M3.3).

50-321/97-12-08 NCV Personnel' Error Results in a Breach of

Drywell Integrity (Section R2,1).

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