ML20151W078

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Insp Repts 50-327/88-20 & 50-328/88-20 on 880227-0318. Violations Noted.Major Areas Inspected:Control Room Observation & Operational Safety Verification Training,Maint Observations & Previous Insp Findings
ML20151W078
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 04/25/1988
From: Branch M, Jenison K, Long A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20151V938 List:
References
50-327-88-20, 50-328-88-20, NUDOCS 8805030290
Download: ML20151W078 (36)


See also: IR 05000327/1988020

Text

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NUCLEAR REGULATORY COMMISSION

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Report Nos.: 50-327/88-20, 50-328/88-20

Licenses: Tennessee Valley Authority

6N 38A Lookout Place

1101 Market Square

j Chattanooga, TN 37402-2801  ;

Docket Nos.: 50-327 and 50-328 License Nos.: DPR-77 and DPR-79 [

Facility Name: Sequoyah Units 1 and 2

Inspection Conducted: February 27, 1988 thru March 18, 1988

Project Engineers: O R . b my Vf2Sf?8

J. Brady, Project' Engineer D5te' Signed

G. Hunegs, Project Engineer

A. Long, Project Engineer

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Shift Inspectors: P. Harmon, Shift Inspector

F D. Loveless, Shift Inspector

[ W. Poertner, Shift Inspector ,

i G. Humphrey, Shift Inspector i

W. Bearden, Shift Inspector

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K. Ivey, Shift Inspector j

Shift Manager Approval: I 8 88

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V4 J'e nis on Shift Manager ' Date Signed

hf O d 36 TT

M. ~ Branch, Shift Manager Date Signed

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8805030290 880427

PDR ADOCK 05000327

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Summary

Scog:- This announced inspection involved onshift and onsite inspections

by the NaC Restart Task Force. The majority of exponded inspection

e2 fort was in the areas of extended contrcl room observation and opera-

tional safety verification including operations performance, system

lineups, radiation protection, and safeguards and housekeeping inspec-

tions. Other areas inspected included maintenance observations, review

of previous inspection findings, follow-up of events, review of licensee

identified items, and review of inspector follow-up items. During this

period there was extensive control room and plant activity coverage by

NRC inspectors and managers.

Results: Four violations were identified:

327,328/88-20-01, Three Examples: Failures to develop or

implement procedures (paragraphs 10 and 11).

327,328/88-20-02: Missed surveillance test for the #3 cold leg

accumulator (paragraph 10). l

327,328/88-10-03: Failure to comply with Technical Specifica-

tion Limi+'.ng Condition for Operations (paragraph ll.b.6).

327,328/88-20-04: Failure to ensure timely notification of the

NRC of a loss of safety functions (paragraph ll.b.10).

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rep 0RT DETAILS

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1. Persons Contacted

Licensee Employees

- *H. Abercrombie, Site Director

J. Anthony, Operations Uroup Supervisor

  • T. Arney, Quality Assurance Manager
  • R. Beecken, Maintenance Superintendent
  • R. Buchholz, Sequoyah Site Representative
  • J. Bynum, Assistant Manager of Nuclear Power

M. Cooper, Licensing Supervisor

H. Elkins, Instrument Maintenance Group Manager

R. Fortenberry, Technical Support Supervisor

J. Hamilton, Quality Engineering Manager

  • M. Harding, Licensing Group Manager
  • G. Kirk, Compliance Supervisor
  • J. La point, Deputy Site Director
  • L. Martin, Site Quality Manager

R. Olson, Hodifications

R. Pierce, . Mechanical Maintenance Supervisor

R. Prince, Radiological Control Superintendent

  • R. Rogers, Plant Operations Review Staff

M. Skarzinski, Electrical Maintenance Supervisor

E. Sliger, Manager of Projects

  • S. Smith, Plant Manager
  • S. Spenser. Nuclear Engineer, Compliance
  • J. Sullivaa, Plant Operations Review Staff Supervisor
  • B. Willis, Operations and Engineering Superintendent

NRC Employees

  • S. Ebneter, Director, Office of Special Projectu
  • F. McCoy, Startup Manager
  • K. Jenison, Shift Manager
  • M. Branch, Shift Manager
  • P. Skinner, Shift Manager
  • Attended exit interview

2. Exit Interview

The inspection scope and findinge were summarized on March 23, 1988,

with those persons indicated in paragraph 1. The Startup Manager

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described the areas inspected and discussed in detail the inspection

findings listed below. The licensee acknowledged the inspection

findings and did not identify as proprietary any of the material

reviewed by the inspectors during the inspection.

The f ollowing new items were identified:

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Violation (VIO) 327,328/88-20-01: Failure to develop or implement

procedures.

Example 1: Inadequate TS interpretation related to the

turbine driven auxiliary feedwater pump (AFW)

(paragraph 10).

Example 2: Inadequate TS interpretation related to the 2A-A

centrifugal charging pump (CCP) control switch

position (paragraph 11.b.2).

Example 3: Improper performance of the AI-5 Lead operator

Checklist, resulting in an improper verification

of centrifugal charging pump switch position

(paragraph 11.b.7).

Violation (VIO) 327,328/88-20-02: Missed surveillance test for the

  1. 3 cold leg accumulator (paragraph 10).

Violation (VIO) 327,328/88-20-03: Failure to comply with technical

specification 3.0.3 involving the loss of safety functions (para-

graph 11.b.6).

Violation (VIO) 327,328/88-20-04: Failure ensure timely notifica-

tion of notify the NRC of a loss of safety functions as required by

10 CFR 50.72.b.2.ili and AI-18, Plant Reporting Requirements (para-

graph 11.b.10).

An enforcement conference was held on March 17, 1988 and is dis-

cussed in paragraph 11.d of this report.

NOTE: A list of abbreviations used in this report is contained in

paragraph 13.

3. Sustained Control Room Observation (71715)

The inspectors observed control room activities and those plant

activities directed from the control room on a continuous basis for

the entire period of this report. The observation consisted of one

shift inspector per shift supported by one shift manager per shift

and other OSp management,

a. Control Room Actjvitics Including Conduct of Operations

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The inspectors reviewed control room activities and determined

that in some instances operators were not attentive and respon-

sive to plant parameters and conditions. These issues were

discussed at an enforcement conference held March 17, 1988 (see

paragraph 11.d). Operators were observed to employ communica-

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tion, terminology and nomenclature that was clear and f ormal.

In one instance operators were observed to perform an improper

relief prior to being discharged from their watch standing

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duties and were not attentive to plant operations (see viola- l

tion 327,328/88-20-01, discussed in paragraph 11).

b. Control Room Manning

The inspectors reviewed control room manning an6 determined

that TS requirements were met and a profeosional atmosphere was

maintained in the control room. The inspectcIs found the :4oise

level and working conditions to be acceptable. The inspectors

observed no horseplay and no radios or other non-job related

material in the control room. Operator compliance with regula-

tory and TVA administrative guidelines were reviewed. No

deficiencies were identified.

In addition, the control room appeared to be clean, unclut- r

tered, and well organized. Special controls were established

to limit personnel both in the control room inner area and in

the control room areas behind the back panels,

c. Routine plant Activities Conducted In or Near the Control Roem

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The inspectors observed activities which require the attention

and direction of control room personnel. The inspectors *

observed that necessary plant administrative and technical '

activities conducted in or near the control room were conducted

in a manner that did not compromise the attentiveness of the

operators at the controls. The licensee has established a SS '

office in the control room area in which the bulk of the

administrative activities, including the authorized issuance of

keys, take place. In addition the licensee has established HO,

WR, SI, and modification matrix functions to release the

licensed operators from the bulk of the technical activities

that could impact the per f ormance of their duties. These

matrixed activities were transf ormed into the WCC which is ,

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located in the TSC spaces.

d. Control Room Alarms and Operator Response to Alarms

In one instance, the inspectors observed that control room e

evaluations were not performed correctly utilizing approved

plant procedures (see paragraph 11). Control room alarms were  ;

responded to promptly with adequate attention by the operators

l to the alarm indications. Control room operators appeared to

i believe the alarm indications. None were identified by the r

l inspectors that were either ignored by the operators or

timed-out,

e. Fire Brigade

i The inspectors reviewed fire brigade manning and qualifications  !

Both manning and qualifications were found i

on a routine basis.

j to meet TS requirements.

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i f. Shift Briefing / Shift Turnover and Relief

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The inspectors observed that, in general, ROs completed turn-

over checklists, conducted control panel and significant alarm

walkdown reviews, and significant maintenance and surveillance

reviews priot to relief. The inspectors observed that, in

general, sufficient information was transferred on plant

status, operating status and/or events and abnornal system

alignments to ensure the safe operation of the unit. However,

the inspectors l'entified one instance where an insufficient

turnover occurred (see paragraph 11). Assistant SS relief was

conducted in the control room and sufficient inf or ma t ion

appeared to be transferred on plant status, operating status

and/or events, and abnormal system alignments to ensure the

safe operation of the unit. The inspectors identified one

instance when an Assistant SS failed to adequately brief the SS

(see paragraph 11). Assistant SS were observed reviewing shift

logbooks prior to relief.

Shift briefings were cenducted by the offgoing SS. personnel

assignments were made clear to oncoming operations personnel.

Significant time and effort were expended discussing plant

events, plant statua, expected shift activities, shift train-

ing, significant surveillance testing or maintenance activi-

ties, and unusual plant conditions,

g. Shift Logs, Records, and Turnover Status Lists

The inspectors reviewed the SS, STA, aad RO logs and determined

that in most cases, the logs were completed in accordance with

administrative requirements. In one case, however, the STA and

RO logs were concidered inadequate (see paragraph 11). In

addition, some improvement 18 needed in the timeliness of

, coz.ple'.on of the SS log. This was discussed with the licensee

at an e..forcement conference held on March 17, 1988.

The following logs were also reviewed:

Night Order Log

System Status Log

Configuration Control Log

Key Log

Temporarf Alteration Log

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h. Control Room Recorder / Strip Charts and Log Sheets

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! The inspector observed operators check, install, mark, file,

and route for review, recorder and strip charts in accordance

with the established plant processes. There were no events

j that caused the immediate control room review of recorder / strip

chart peaks during this inspection period. Control room and

plant equipment logsheets were found to be complete and legi-

ble; parameter limits were specified; and out-of-specification

parameters were marked and reviewed during the approval pro-

Cess.

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4. Manacement Activities

TVA management activities were reviewed on a daily basis by the NRC

shift inspectors, shift managers, and Startup Manager,

a. Daily Control of Plant Activities (War Room Activities)

The licensee conducted a series of plant activities throughout

each day to control plant routines. These activities were re-

ferred to by the !?.censee os War Room activities. War Room

activities were observed by the shift manager on a daily basis

and were found to be an adequate method to involve upper level

management in the day-to-day activities affecting the operation

of the units.

b. Observation of First Line Supervisor Activities

An increase in first line supervisor involvement in plant

activities was observed. First line supervisor response to

issues and events that occurred during the inspector period was

adequate,

c Management Response To Plant Activities and Events

Management response to the events that occurred during this

inspection period was conservative, well organized, and based

on a Sound technical grasp of the issues.

5. Site Quality Assurance Activities in Suncort of Operations

The inspectors reviewed the activities of the WCC which includes QA

oversight. No discrepancies were noted.

6. Chronoloav of Unit 2 Plant Onerations

At the beginning of the NRC Restart Task Force shift coverage, Unit

2 was in Cold shutdown (Mode 5) with tnree RCgs operating and the

2A-A RHR pump in service. The RCS was at 180 F and 370 psig.

i Pressurizer level was at 26 inches. All SGs were filled to the

operatir49 range, the condensate system was on long cycle recir-

culatisn, and there was a vacuun in the main condenser.

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On February 4, 1988, the NRC approved entry into Mode 4/3 (Hot Shut-

down/ Hot Standby). The plant was heated up using RCPs and entered

Mode 4 on February 6, 1988.

On February 10, 1988, RHR cooling was returned to service and the

licensee suspended all non-essential testing and maintenance for

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about 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. This was done following a series of events which

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included generation of a reactor trip signal, inadvertent MSIV

, closures and feedwater isolations, and a loss of the VCT level due

! to maintenance activities. During this period of licensee

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evaluation and corrective action, the MSIVs remained closed and the

unit was maintained in Hot Shutdown (Mode 4) using RCPs and RHR.

Prior to Mode 3 entry, approximately nine personnel errors had oc-  !

curred. None of the events resulting from those personnel errors r

represented significant safety concerns of their own accord and i

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collectively appeared to be typical of what one would expect at a

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Near Term Operating License Plant going through the same evolution.

During this inspection period the unit entered Mode 3 (Hot Standby)

on February 27 and was maintained in Hodg 3 with four RCPs opgrat- '

ing. The RCS was maintained between 350 F/1600 psig and 546

F/2250 psig. A number of events occurred during this inspection  !

period and are listed below:

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February 28: Two inoperable steam flow channels, in conjunc-

tion with the existing low-low Tave, resulted in the closure of ;

all four MSIVs.

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February 29: During perf ormance of SI-137.2, RCS Water Inven-

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tory, 2 gpm leakage was identified. The leakage was later

, deterr01ned to be due to RCS temperature variation. SI-137.2

was reperformed satisfactorily. ,

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March 1: A Unit 1 CVI occurrci due to spiking on the lower

compartment RMs.

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March 5: Val:<e 2-LCV-3-175 failed to stroke but the TDAFP was

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not declared inoperable. This resulted in violation

! 327,328/88-20-01, example 1 (see paragraph 10).

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March 6: Cumulative RCS leakage into the #3 CLA exceeded it of

the tank volume without boron concentration being verified as ,

j required by TS. This resulted in violation 327,328/88-20-02

(see paragraph 10).

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March 9: The control switch for the 2A-A CCP was in the PTL

! position while 2B-B CCP was also inoperable due to testing.

This resulted in two violations (327,328/88-20-03 and -04)

which are being evaluated for escalated enforcement (see

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! paragraph 11) and resulted in two of the three examples of

violation 327,328/88-20-01. ,

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March 10: Boron concentrations in the RWST and in the #3 cold

l leg accumulator were found to exceed TS limits. Both problems  ;

) were corrected within the time limits of the TS Action State-

! ments.

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March 16: The group M* mand step counter in the control room

failed to meve as control bank b was being inserted.

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l Detailed discussions of these events are contained in paragraphs 10

l and 11.

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7. Ooerational Safety verification (71707) Units 1 and 2

a. Plant Tours

The inspectors observed control room oporations; monitored

conduct of testing evolutions; reviewed applicable logs,

including the shift logs, night order book, clearance hold

order book, configuration log, and TACF log; conducted discus-

sions with control room operators; observed shift turnovers;

and confirmed the operability of instrumentation. The inspec-

tors reviewed the operability of selected emergency systems and

compliance with TS LCOs. The inspectors verified that mainte-

nance W0s had been submitted as required and that follow-up

activities and prioritization of work was accomplished by the

licensee.

Tours of the diesel generator, auxiliary, control, and turbine

buildings were conducted to observe plant equipment conditions,

including potential fire hazards, fluid leaks, excessive vibra-

tions, and plant housekeeping / cleanliness conditions.

The inspectors walked down accessible portions of the following

safety-related systems on Unit 1 and Unit 2 to verify operabil-

ity and proper valve alignment:

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Auxiliary Feedwater System

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Chemical Volume Control System

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Upper Head Injection System.

With the exceptions of the violations described in paragraphs

10 and 11, no problems were identified.

b. Safeguards Inspection

NRC inspection activities included a review of the licensee's

physical security program. The performance of various shif ts

of the security force was observed in the conduct of daily

activities, including protectec and vital area access controls;

searching of personnel and packages; escorting of visitors;

wadge issuance and retrieval; patrols; and compensatory posts.

In uidition, the inspectors observed protected area lighting,

and protected and vital area barrier integrity. The inspectors

verified interfaces between the security organization and both

operations and maintenance. Specifically, the shift inspectors

inspected security dur'ng the outage period and reviewed

licensee security event reports.

No violations or deviations were identified,

c. Radiation Protection

The inspectors observed HP practices and verified the implemen-

tation of radiation protection controls. On a regular basis,

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RWPs were reviewed and specific work activities were monitored t

to ensure the activities were being conducted in accordance

with applicable RWPs. Selected radiation protection instru- l

ments were verified operable and within calibration frequency. j

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The following RWPs were reviewed:

RWp 88-0-24: Minor Work.

RWP 88-1-29: Component Cooling Water System pump Repair. [

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No violations or deviations were identified.

8. Shift Surveillance Observations and Review (61726[  !

The inspectors observed or reviewed TS required surveillance testing

and verified that testing was performed in accordance with adequate  !

procedures; test instrumentation was calibrated; LCOs were met; test

results met acceptance criteria requirements and were reviewed by

personnel other thar the individual directing the test; deficiencies

were identified, as appropriate, and any deficiencies identified

during the testing were properly reviewed and resolved by management

personnel; and system restoration was adequate. For completed

tests, the inspector verified that testing frequencies were met and

tests were performed by qualified individuals.

The following activities were observed or reviewed:

SI-2: Shift Log. The inspector verified that the requirements of TS i

4.5.2a for valvec 2-FCV-63-1 and 2-FCV-63-22 are being adequately l

implemented by this SI. The inspector verified that the SI has been  ;

accomplished at the required frequency and no deficiencies were

noted.  ;

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SI-7.1: Diesel Generator AC Electrical Power Source Operability

Verification. This SI was observed by the inspector and no defi- i

ciencies were identified. i

SI-7.2: Diesel Generator Surveillance Frequency. This SI was

observed by the inspector and no deficiencies were identified.

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SI-11: Reactivity Control Systems Moveable Control Assemblies. The

inspectors observed portions of this SI. A review of problems '

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associated with this SI is contained in the events section (para-

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graph 10).

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SI-43: Rod Drop Time Measurement. The inspectors observed the

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performance of the SI, which was interrupted due to problems with

i the rod position step counter. A review of the problems is con- ,

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tained in paragraph 10.

I SI-90.82: Monthly Functional Test of Reactor Trip Instrumentation.

l This SI was observed by the inspector and no deficiencies were ,

identified. ,

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SI-111: Testing and Setting of Main Steam Safety Valves. This SI $

was observed by the inspector. No deficiencies were identifjed. -

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SI-127: RCS and pressur !zer Temperature and Pressure Limits. The

inspector observed portions of this SI during increase of tempera-

ture and pressure to ti e normal operating range. The purpose of

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this SI is to document compliance with surveillance requirements in i

order to provide reasonable assurance that unacceptable stresses ,

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af fecting system integrity will not occur and that operation in

excess of the limits is analyzed. No deficiencies were identified.

SI-130.1: Turbine Driven Auxiliary Feedvater Pumps. This SI tas ,

observed by the inspector. During the pump run, smoke came from the

outboard packing of the pump. The TDAFP was tripped and a WR ,'

written. Af ter packing repairs a second reperf ormance of this S'

was observed and no deficiencies were identified. 7

SI-137.1: Reactor Coolant Systems-Unidentified Leakage Measurement. l

This SI was observed by the inspector and no deficiencies were  !

identified. l

SI-137.2: RCS Water Inventory. This SI was observed by the inspec-

tor, and failed to meet the acceptance criterion that leakage be

less than than 1 gpm. It was determined that the failure to meet ,

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the acceptance criterion was due to not maintaining the RCS tempera-

ture constant (see paragraph 10). The 3I was rerun holding RCS i

temperature constant and the acceptance criterion was then met. No  !

further discrepancies were noted.

SI-166: Summary of Valve Tests for ASME Section XI. This SI was l

observed by the inspector and no deficiencies were identified.

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SI-166.6: post Maintenance Testing of Category A and B valves. The r

SI was observed being performed on valves 2-LCV-3-164 and I

2-FCV-1-15. In both cases the SI was satisfactorily completed and

no deficiencies were identified. i

SI-166.8: Increased Frequency Testing of Category "A" and "B" I

Valves. This SI was observed by the inspector. During the perfor-

mance of this test, valve 2-LCV-3-175 would not stroke. The details T

of this issue are discussed in paragraph 10.

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SI-166.32: AFW Check Valve Opening Test. This SI was observed and

the inspector noted that the TDAFP turbine sometimes oversped. The

cause of these overspeed trips was ir.vestigated by the licensee and i

resolved. Procedural changes to the TDAF Tests were reviewed. The  ;

test was changed to implement steam supply swapover in the automatic l

mode rather than manually. Auto swapover allows reset of the  !

trip / throttle valve (manual swapover does not reset) such that [

overspeed does not occur. The test was rerun successfully with no [

! overspeed. The licensee has determined that the overspeed was >

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caused by the manual swapover and the procedure change has corrected i

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the overspeed deficiencies. Review of the corrective actions by the

inspector performed on 1/3/88 revealed no discrepancies. No further

discrepancies were noted.

SI-196: periodic Calibration of UHI System Instrumentation. The

inspector observed this SI and noted that the hydraulic pressure

used to cycle the valve in this SI was 3130125 psig, although in

SI-744 hydraulic pressure is allowed to drop to the alarm setpoint

of 2970 psig. The inspector noted that a lower pressure would

increase the closing time of the valve. A follow-up inspection

performed subsequent to the inspector's initial observation deter-

mined that SI-196 is the test utilized by the licensee to satisfy

ASME Section XI valve timing test. ASME Section XI does not require

worst case testing (i.e. bleed to lowest expected pressure).

ST-228.2: Functional Test of RCP Undervoltage Relays. This SI was

coserved by the inspectors and no deficiencies were identified.

SI-230.2: Functional Test of RCP Underfrequency Relays. No defi-

ciencies were identified.

SI-276: Auxiliary Feedwater Automatic Control Valve Operability.

The inspectors reviewed this SI and no deficiencies were identified.

SI-298.2: Calibration and Functional Test of Condensate Storage Tank

Suction Header Pressure Switches to Auxiliary Feedwater System.

This SI was observed being performed on the 2B-D AFW pump r.4'ction

pressure switches. No deficiencies were identified.

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SI-488: RCS RfD Sensor Verification of Calibration. This SI was ob-

served at 525 F and at 447 F. No deficiencies were identified.

SI-720: Calibration of AFW Terry Turbine Controls. This SI was ob-

served by the inspector and the acceptance criterion was met, but

the inspector noted that the t:rbine tripped on overspeed. The

cause of the overspeed trips is discussed under SI-166.32 above.

SI-744: Monitoring of UHI Isolation Valves Accumulator Pressure.

The inspector observed performance of this SI and no deficiencies

were identified.

9. Shift Maintenance Observations and Review (62703)

a. Station maintenance activities of saf ety-related systems and

components were observed or reviewed to ascertain that they

were conducted in accordance with approved procedures, regula-

tory guides, industry codes and standards, and in conf ormance

with TS.

The following i te ms ve r e considered during this review: LCOs

were met while components or systems were removed from service;

redundant components were operable; approvals were obtained

prior to initiating the work; activities were accomplished

using approved procedures and inspected as applicable;

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procedures used were adequate to control the activity; trouble-

shooting activities were controlled and the repair record

accurately reflected what actually took place; functional

testing and/or calibrations were performed prior to returning

components or systems to service; QC records were maintained; ,

activities were accomplished by qualified personnel; parts and

materials used were properly certified; radiological controls l

were implemented; QC hold points were established where re-

quired and were observed; fire prevention controls were imple-

mented; outside contractor activities were controlled in -

accordance with the approved QA program; and housekeeping was

actively pursued.

b. Temporary Alterations  :

The following TACFs were reviewed: L

2-87-2001-30: Thermocouples in East and West Valve Vaults t

2-88-2005-68: Switching RCP RTDs from 2-TE-68-2A to

2-TE-68-2B (spare)

2-84-2039-03: Automatic Main Feedwater Bypass Valve.

No violations or deviations were identified.

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c. Work Requests [

The following WRs were reviewed: l

WR B257703 was initiated for inspection of 2D-B CCP gland bolt.

No deficiencies were identified.

WR 262113 was initiated for troubleshooting of steam flow i

indicator 1-3A. No deficiencies were identified.

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WR B262118 was initiated for troubleshooting on valve

2-LCV-3-164. Tb2 inspector observed the work in progress and .

no deficiencies were identified. During the troubleshooting,

it was determined that the problem was in the valve controller

rather than in the valve. ,

WR B262457 was initiated for electrical ground troubleshooting, ,

No deficiencies were identified.

WR B264214 was initiated for repairs to CCS pump 1-PHP-70-46.

The inspector observed the pump impeller being set up in one of

the machine shop lathes. An RA had been established around the

lathe, and RWp-1-29 was controlling work within this RA. The

inspector questioned the following practices:

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The lathe operator wiped his nose with the sleeve of his

j anti-contamination clothing (Anti-Cs). '

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- An assistant was outside the RA boundary ropes instead of

i

at the R A access area (i.e. the step-off pad).

}

-

13

,

.

.

-

The assistant was smoking as he handed tools across the RA

boundary.

The inspector discussed these issues with HP supervision, who

said they would ensure the lathe operator had not contaminated

his face. The Hp supervisor and the inspector reviewed CRI-1,

Radiological Control Program; RCI-14, Radiation Work permit

Program; SQA-205, Contamination Control; and RCI-15, Establish-

ing and Updating Radiological Signposting. None of these

documents gave guidance about where tools could enter the RA or

about sm3 king at the boundary of the RA.

The inspector also observed the condition of the RA around the

pump in the auxiliary building. There were no personnel ir. the

RA. At the time of the observation the RA had oily dirt on the

floor, numerous tools adrift, and several copies of procedures

lying around. Maintaining ras orderly helps prevent the

unnecessary spread of contamination. The inspector discussed

these issues with HP supervision, who agreed they were poor

work practices and directed that the work area be cleaned up.

WR B267164 was initiated to adjust the limit switches on valve

2-LCV-3-164. The inspectors reviewed work in progress and did

not note any discrepancies.

WR B267403 was initiated to repair valve 2-LCV-3-164, which had

been permitting approximately 100 gpm of flow when the valve

indicated closed in the auto position. The inspectors reviewed

work in progress and no deficiencies were identified.

WR B267451 was initiated to repair and calibrate 2-LCV-3-173.

The inspector observed work in progress and partial performance

of SI-75, the post maintenance test. No discrepancies were

noted.

WR B267767 was initiated to repair bearing leakage on the 23-B

AFW pump. No deficiencies were identified.

WR B26770 was initiated to repair a hydraulic leak on

2-FCV-87-23. No deficiencies were identified.

WR B271864 was initiated on the draindown pressure on

2-FCV-87-22. No deficiencies were identified.

WR B271886 was initiated on the draindown pressure on

2-FCV-87-24. No deficiencies were identified.

WR B275198 and WR 267353 were initiated to remove plugging from

the 2" line off the boric acid tank. The inspectors reviewed

work in progress and did not note any di60IepaneleS.

WR B275996 was initiated for repairs and testing of AFW SG

level contrc'. valve 2-LCV- 3-0156 A. No deficiencies were

identified.

14

__ _ _ _ _ _ _ _ _ _ _ _ _ _________ _ _ __.

WR B293849 was initiated to repair the governor valve on the

TDAFW. The inspector observed work in progress and no defi-

ciencies were identified.

] WR B296429 was initiated to replace the lockout relay on the ,

- 2A-A 6.9 KV shutdown board normal supply breaker. The inspec- ,

tor monitored a portion of the work activities. No discrepan-

cies were noted.  ;

!

,

No violations or deviations were identified during the inspec-

tions of work requests,

d. Hold Orders

The inspectors reviewed various Hos to verify compliance with

AI-3, Clearance Procedure, Revision 38, and to verify that the

H0s contained adequate information to properly isolate the

affected portions of the system being tagged. Additionally,

the inspectors inspected the affected equipment to verify that -

the required tags were installed on the equipment as stated on

the H0s. The following H0s were reviewed:

Hold Order E2uioment  ;

'

2-88-52 2-FCV-67-68 Motor Replacement

1-88-429 Boric Acid System ,

1-88-438 1A-A Motor Driven AFW pump ,

i

No violations or deviations were identified.  ;

10. Event Follow-un (93702, 62703)

On February 28, at approximately 8:00 p.m., steam flow channel #1 on

,

'

the #1 SG and steam flow channel #1 on the #3 SG were declared i

inoperable as a result of improper indication (i.e. indication of ['

steam flow when there was no steam flow) . TS 3.3.2.1 allows opera-

tion to continue if the inoperable channel is tripped. Accordingly,

to allow continued operation, the inoperable channels were tripped  ;

as prescribed in TS 3.3.2.1. This caused high steam flow indication

in two steam lines, which in conjunction with the existing low-low

Tave (less than 540 F), resulted in the closure of all four MSIVs.

The MSIVs were subsequently reopened, and the unit remained in Mode

3. The human f actors error will be evaluated as part of the LER

closure process.

'

,

On February 29, at approximately 2:00 a.m., during the perf ormance

! of SI-137.2, Reactor Coolant System Water Inventory, 2 gpm unclas-

sified leakage was identified. Until classification can be estab-

11shed, the leakage is considered unidentified. The licensee

declared an unusual event in accordance with their radiological ,
emergency plan. The high leakage rate was later determined to be

,

due to variation in RCS temperature during the leak rate test. The

test was reperformed at a constant RCS temperature and the retest ,

]

, .

.

15

,

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

!

i

data reflected a leakage rate well within TS acceptance criteria.

The unusual event was exited at 1:10 p.m. on February 29, 1988.

On M6rch 1, at 2:43 a.m., a Unit 1 CVI occurred due to spiking on

the lower compartment RM 1-RM-90-106 A&B. When the CVI occurred,

the RO blocked the RM signal. Troubleshooting determined the RM

signal to be the result of a clogged filter which caused relay

chattering and EMP spikes in the RM circuits. Containment venti-

lation and RMs were returned to service. At 3:45 p.m., the RMs

caused another CVI. Troubleshooting led to the same root cause as

before. The licensee is now changing the filters every four hours.

Permanent corrective action still needs to be developed.

On March 5, at approximately 10:30 p.m., TDAFP LCV 2-LCV-3-175 would

not stroke. TS 3.7.1.2 requires at least three independent SG AFW

pumps and associated flow paths be operable in Modes 1,2, and 3. ?S

3.0.5 states:

Whea a system, subsystem train, component or device is deter-

mined to be inoperable solely because its emergency power

source is inoperable, or solely because its normal power source

is inoperabic it may be considered operable for the purpose of

satisfying the requirements of its applicable LCO provided: (1)

its corresponding normal or emergency power source is operable;

and (2) all of its redundant system (s)........are operable, or

likewise satisfy the requirements of this specification.

TVA had interpreted TS 3.7.1.2 and had issued in 1984 a written

corporate position as TS Interpretation #8. Based on the interpre-

tation the TDAFP pump was agi declared inoperable. The 1984 TS

interpretation states that:

A recent incident involved the removal of a train B-B EDG from

service for maintenance and using LCO 3.0.5 to declare various

Llant equipment to be operable in relation to power supplies,

later that same day the TDAFP was declared inoperable. Howev-

er, confusion arose as to the operability of train B MDAFP,

since it was unclear if it still met the definition of 3.0.5

for ensuring all its redundant equipment was operabic. . . If

train B EDG is inoperable, then train "A" MDAFP must be opera-

ble and at least 3 SG's capable of being supplied from the

TDAFP.

The inspector questioned the validity of TS Interpretation 88 and

the decision not to call the TDAFP inoperable based upon the the

interpretation.

Further review by the inspector determined the following:

1) The failure of valve 2-LCV-3-175 to stroke during the

performance of SI 166.8, Increased Frequency Testing of

Category A and B Valves, was not entered in the RO,

Assistant SS or SS logs prior to shift relief. A log

16

t. .

{

entry was subsequently made after the inspecto: expressed

his concerns to the oncoming SS.

2) The failure of valve 2-LCV-3-175 was not entered in the SI

166.8 test director's chronological test log. The failure

of valve 2-LCV-3-175 to stroke was also not identified as

a deficiency in the SI 166.8 data package.

Valve 2-LCV-3-175 was successfully stroked at approximately 0120.

Therefore, although the TDAFp was not declared inoperable, the time

limit of the TS Action Statement was not exceeded and no violation

of TS occurred. The licensee has removed the TS interpretation book

from the control room until all the interpretations can be reviewed

for adequacy. The specific example of inadequate TS interpretations

is a violation of TS 6.8.1, which requires adequate procedures be

developed and implemented. This is violation 327,328/88-20-01,

example 1.

On March 6, at 8:00 p.m., the inspector determined that the licensee

had been routinely draining the #3 CLA due to inleakage from the RCS

and that RCS boron concentration was 2177 ppm. Review of TS 3.5.1.1

indicated that the upper limit for boron concentration in the CLAs

is 2100 ppm and that TS surveillance requirement 4.5.1.1.1.b re-

quires boron concentration to be verified within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after each

solution volume increase of greater than or equal to 1% of tank

volume. The inspector expressed concern to the SS that cumula-

tively, a 1% volume increase may have occurred as a result of the

RCS inleakage into #3 CLA. The SS immediately took action to

determine if a 1% volume increase had occurred as a result of RCS

inleakage and to obtain a boron sample. The boron sample analysis

was completed at 9:49 p.m. and indicated a boron concentration of

2085 ppm. The licensee determined that cumulatively the RCS

inleakage had increased the CLA #3 volume by greater than 1%. This

issue is identified as violation 327,328/88-20-02, Missed Surveil-

lance Test.

On March 9 it was determined that both CCps were inoperable for a 1

hour and 24 minute period. This event and the follow-up are de-

scribed in detail in paragraph 11 of this report.

On March 10, at 3:45 p.m. the Unit 2 RWST was declared inoperable

when its boron concentration was sampled and determined to be 2111

j ppm. This exceeded the TS 3.1.2.5.b.2 maximum of 2100 ppm. The

j licensee fed and bled the RWST to lower the boron concentration and

exited the LCO on March 11, at 12:12 a.m..

! On March 10, at 4:54 p.m. an Unusual Event was reported. A boron

sample on #3 CLA was 2101 ppm which exceeded the TS maximum boron

concentration of 2100 ppm. TS 3.5.1.1 requires the concentration to

,

be corrected within one hour or be in mode 4 within the next 5

i hours. The licensee commenced feed and bleed operations on the CLA.

1 At 8:25 p.m. the licensee began cooling down to enter mode 4 within

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. This initiation of cooldown necessitated a declaration of

'

an unusual event. At 9:40 p.m., a sample on 83 CLA indicated a

17

. .

i

!

!

l

boron concentration of 2079 ppm and a backup sample indicated 2080 l

ppm. At 10:10 p.m. the Unusual Event was terminated and the plant i

began a heatup to return to_527 F.  !

!

- On March 15, at 12:36 a.m., the licensee was conducting rod exercis-  ;

l es per SI-11, which requires stepping rod banks out 10 steps and i

'

j then back in. When attempting to step rod control bank D back in,

.

the licensee discovered that the rods had stepped in but the indi- )

cated position on the control room step counters had not changed. l

The licensee manually opened the RTBs as required by TS 3.1.3.3.  !

All equipment functioned and gperator actions were as expected. The '

reactor was stabilized at 535 F. Previous SI-11 rod exercises of '

shutdown banks A through D and rod control banks A through c had

i been completed without similar indication problems.

"

On March 17, at 6:69 a.m., the reactor was again tripped manually to i

'

comply with TS 3.1.3.3 when the step counters on bank B were ob- *

served to be inoperable while performing rod drop testing. Early

troubleshooting indicated a bad step counter, j

!

i

on March 18, at 2:30 p.m., control rod E-3 in shutdown bank C i

, appeared to be stuck on the bottom. The individual position indica-

tor appeared to stick, then responded. When bank C was reinserted

j and then withdrawn, rod E-3 stepped out with the bank. When the

j bank stopped at 10 steps withdrawn, rod E-3 appeared to f all slowly

! back to zero. The test was performed again, and rod E-3 appeared to ,

) fall as soon as the stepping out sequence was stopped. The problem

was later identified as a problem in the signal conditioning module

for the rod's position indicator. Repairs were effected and no  ;

further problems were observed.

i

11. Centrifugal Charging Pump 2A-A in Pull-to-Lock ,

I

'

a. Description of Event

! At 7:30 p.m. on March 9, 1988, during a walkdown of the Unit 2 L

control room panels, the inspector noted that the control

'

switch (HS-62-108A) for the 2A-A CCP was in the PTL position.

The inspector brought this condition to the attention of the

! control room operator and after brief discussion the operator

i put the switch back into the A-Auto position. During the above l

'

l discussion with the two operators in the control area the

i inspector considered that it was not common knowledge among the ;

i operators that the pump was not OPERABLE for Mode 3 while in t

! the PTL position (i.e. not capable of automatically starting on

I an accident signal). In fact, the operators indicated they r

! thought that the TS interpretation book allowed this switch '

j position while in Mode 3. The inspector indicated that he did

j not agree with the TVA interpretation and that the TS action  :

I

3

should have been entered while the pump was an PTL.

I

! i

'

Following the above discussion with the control room operators,

the inspector monitored the licensee follow-up actions for the

, l

!  !

18 l

[

'

L

.

event. Specifically, after resolving the initial safety

concern regarding the switch position, the inspector observed

the actions of the Ros, Assistant SS, STA and SS. The inspec-

tor was attempting to evaluate the effectiveness of communi-

cations among the above individuals in order to determine that

the proper level of- management was involved in the f ollow-up

actions. Af ter waiting approximately 30 minutes, at 8:00 p.m.,

the inspector asked the SS if he was aware of the problem

involving the 2A-A CCP being in PTL and determined that he had

not been informed of the problem.

The inspector requested the following information from the duty

SS:

-

When the 2A-A CCP was put in Pull-to-Lock

-

Whether the 2B-B CCP was OPERABLE during the period the

2A-A CCP was in PTL

-

If the 2A-A CCP was in PTL during shift turnover, and if

so, why the problem didn't get identified by the turnover

checklist

-

Why it took so long to notify the SS of the problem

-

If there was a TS interpretation that allowed the pump to

be considered OPERABLE in mode 3 with the switch in PTL

-

If there was a training problem on CCP OPERABILITY

After discussing the above event with the NRC Startup Manager

the inspector reviewed the Unit 2 operator log and determined

that:

1) At 1:11 p.m. on March 9, 1988 the ?B-B CCP was started for

engineering test associated with the speed increaser oil

system;

2) At 1:16 p.m. the 2A-A CCP was shutdown (although not

reflected by the log, this is the time the licensee later

determined the switch was put in PTL;

3) At 2:40 p.m. the 2B-B CCP was declared OPERABLE after post

maintenance testing. This review indicated that for a 1

hour and 24 minute period, between 1:16 p.m. and 2:40

p.m., both the 2A-A and 2B-B CCPs were inoperable and the

action of TS 3.0.3 was not followed.

A follow-up review of the March 9, 1988 Lead Operator System

Status checklist for Modes 1-4 (required by AI-5) was conducted

by the inspector. This review and follow-up conversation with

the SS revealed that during the 3:00 p.m. perf ormance of the

checklist the lead RO failed to recognize that the hand switch

(HS-62-108A) for the 2A-A CCP was in the PTL position. This

was demonstrated by a checkmark in the 3:00 p.m. entry space

next to the switch on the checklist. Later, after the inspec-

tor had identified the problem, the operator wrote over the

j checkmark with the inscription PTL and initialed the entry 'see

paragraph ll.B 6). Additionally, a review of the event

1

I

i 19

!

._-.

_ _ _ _ - _ - _ - _ _ _ _ __

.

description in the STA log indicated that the SS was immediate-

ly notified of the event by the operator. This was incorrect,

as the inspector had previously observed that the SS was not

promptly notified. (See the evaluation of concerns in section

11.B.9 of this report).

The SS requested that the PORS group perform a Root Cause

Evaluation of the event and the inspector provided a statement

to the PORS investigator. The inspector requested that the NRC

be provided with a copy of the investigation.

One additional issue arose when the reporting to the NRC (via

Red Phone) of the fact that both CCPs were inoperable for a 1

hour and 24 minute period was delayed until 10:08 a.m. on March

10, 1988. The inspector has concern that TVA may not have "Red

Phoned" the event at all if the site NRC personnel had not

intervened. This is based on the fact that the initial PRO

(2-88-74) did not address that the action of TS 3.0.3 was

exceeded. The PRO only indicated that LCO 3.0.3 "may" have

been entered without being recognized.

b. Evaluation of Concerns

1. Concern 01: Hand switch (HS-62-108A) for the 2A-A CCP

being in Pull-to-Lock not entered in LCO action log.

With the switch in PTL, the 2A-A CCP was inoperable (see

violatten 327,328/88-20-03, discussed in paragraph 11.B.6)

but the LCO of TS 3.5.2 was not indicated in the TS LCO

action log as required by AI-6, Log Entry and Review.

This failure to log a condition that was not recognized by

the operator as an entry into an LCO is not considered a

violation of procedural requirements since the condition

was not recognized by the operators as constituting

inoperability.

2. Concern #2: Several control room operators not aware that

in Mode 3 with the control switch in the PTL position the

2A-A CCP was inoperable, as defined by the TS.

The discussion between the control room operators and the

inspector indicated that the operators actually believed

that TVA has a TS interpretation that would allow the

switch to be in PTL. The inspector believes that the

operators, who were used to Cold Shutdown operations (i.e.

Mode 5), were relying on past knowledge and a TS interpre-

tation that allowed a charging pump to be in PTL and still

be considered operable for the boron injection flow path

while in Mode 5 or 4 only. Additionally, the operators

were not properly trained on the use of this TS interpre-

tation and were not referring to the control room proce-

dures or unit TS for their information. When the inspec-

tor questioned the switch position, the first place the

20

. .

.

operator went for the information was the TS interpreta-

tion book and not the NRC approved TS.

A subsequent review by the licensee of several interpreta-

tions in the TS interpretation book indicated that these

interpretations were in fact wrong and conflicted with the

current unit TS. The inspector requested that the

licensee pull the TS interpretation books from the control

room and training center until the interpretations had

been validated by the licensee.

Sequoyah Operating Licensee NO. DPR-79 requires the plant

to be operated in accordance with the TS. The use of TS

interpretations which conflict with the NRC - approved TS

constitutes a violation of TS 6.8.1 which requires ade-

quate plant procedures be established, linplemented and

maintained. This is violation 327,328/88-20-01, example 2.

s. Concern #3: Failure of the on duty RO, at the time of the

discovery of improper switch position, to promptly commu-

nicate the problem to the SS.

The NRC requires that the holder of a SRO license be on

duty in the control room during all nodes of plant opera-

tion. This SRO must be knowledgeable of the technical

aspects of the plant as well as being f amiliar with the

administrative requirements (including TS) required for

control of day-to-day operations. The technical knowledge

requirements of the SRO position are ensured by the

operator licensing process. Additionally, ANSI

N10.7-1976, which the licensee is committed to through

their QA Topical Report TVA-TR75-1A, requires the above

command function be established.

In order for the command function to be effective, commu-

nication of problems encountered by the RO must be timely

and effectively communicated to the SRO level so that

effective corrective and follow-up actions can be imple-

mented. AI-30, Nuclear Plant Conduct of Operations,

implies, but does not specifically state, that timely and

effective communication is essential. The inspector

consideres that this procedure (AI-30) should more specif-

ically address timely and effective communication of

problems up the operations chain.

4. Concern #4: Log entry made at the time the 2A-A CCP was

shutdown (i..e. 1:16 pm on March 9, 1988) did not reflect

tnat the control switch was put in PTL.

AI-6 requires that inf ornation pertaining to major equip-

ment operation be documented in the RO daily log. Howev-

er, the procedure does not specify the needed detail that

should be recorded. The event that occurred regarding the

2A-A CCP being placed in the PTL was not described in any

21

.

8 4

detail. In fact, only a simple statement that the "A CCP

shutdown IM notified to swap flukes to 2BB CCP" was

recorded in the log. Had the fact that the pump was

placed in PTL been recorded the review of the RO daily log

required by AI-5 may have discovered the inoperable

equipment.

5. Concern #5: Placing control switch in the PTL position

when the pump was secured.

SOI 62.1, Chemical and Volume Control System, which is the

operating instruction used to operate the 2A-A CCP, does

not state to put switch in PTL when stopping the running

pump. It is unclear whether or not the operator who

secured the 2A-A CCP on March 9 actually consulted the

procedure to operate this equipment or was sufficiently

knowledgeable of this requirements of this procedure.

This may have contributed to Violation 327,328/88-20-03.

6. Concern 06: Both CCP being inoperable for a 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 24 I

minute period and the action of TS 3.0.3. not followed.

At the time the 2A-A CCP was placed in the PTL position '

(i.e. made inoperable) the 28-B CCP was also inoperable,

in that its perf ormance had not been established subsc- .

'

quent to maintenance on its speed changer. With both

pumps simultaneously inoperable the action required by TS , 3.0.3 should have been followed. This required that  ;

within one hour, action be initiated to place the unit in i

a mode that did not require two operable centrifugal [

charging pumps. l

>

The failure to comply with the requirement of TS 3.0.3 (

resulted in a violation of TS requirements and involved  !

the loss of a safety function (i.e. high head injection i

and rapid boron injaction needed f or a LOCA and Main Steam l

Line Break Accident). This is violation 327,328/88-20-03. l

!

7. Concern 07: Failure to identify improper switch position  ;

for the 2A CCP during accomplishment of the March 9, 1988,

3:00 p.m. turnover checklist.

A review of the checklist wnich is required by AI-5 to be l

performed prior to shift turnover by the lead RO, indicat- l

ed that the control room handswitch for the 2A-A CCP

(HS-62-108A) was checkea as being in the proper position

(i.e. A-Auto). This constituted an improper performance

of the checklist, in that the actual position at the time

of the 3:00 p.m. verification was later verified to have  ;

been the PTL position. This is violation

327,328/88-20-01, example 3.

8. Concern 58: Improper Correction of the AI-5 checklist  ;

completed on March 9, 1988, i

l

i

22 i

-_ . , - -

_ _ - _ _ - __ _. _ __ . _ _ ._ _ _ _ _ _ _ _. .___

. .

On the March 9, 1988, AI-5 lead operator checklist, the

3:00 p.m. check mark entry for handswitch (HS-62-108A) had

been written over with the inscription PTL and initialed

by the operator. This method of correction of a OA record

is improper in that corrections should be made by drawing

a single black ink line through errors in the record so

that the incorrect information is still legible and the

person making the correction should initial and date the

correction. This improper record correction was promptly

corrected by the licensee.

9. Concern 19: STA log incorrectly indicating that the SS was

immediately notified of the event by the operator.

This was an incorrect statement in that the NRC inspector

notified the SS of the event after waiting approximately

30 minutes. Discussion with the STA involved indicated

that he had assumed that the SS was notified by the

Assistant SS. This incorrect STA log entry was discovered

and promptly corrected by the licensee.

10. Concern 510: Failure to ensure timely notification of the

NRC of a loss of safety functions (via ENS Red Phone) as

required by 10 CFR 50.72.b.2.111 and AI-18, Plant Report-

ing Requirements.

The event described in this report associated with having

both CCPs simultaneously inoperable meets the NRC thresh-

old of requiring a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> "Red Phone" report after identi-

fication of the problem. However, it took approximately

13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> to report the event after suspecting that both

pumps had been simultaneously inoperable. This is vi;la-

tion 327,328/88-20-04.

c. Concle tons

concerns 2, and 7, above constitute failures to either properly

develop or implement procedures as required by TS 6.8.1, and

were identified as examples of violation 327,328/88-20-01.

Concern 6, involving both CCPs being inoperable for a period in

excess of one hour and not complying with the Action Statement

required by TS 3.0.3, was identified as violation

327,328/88-20-03 and is being considered for escalated enforce-

ment.

Concern 10, regarding a failure to timely notify the NRC (via

ENS Red Phone) as required by 10 CFR 50.72.b.2.111 and AI-18

within four hours of the occurrence, was identified as viola-

tion 327,328/88-20-04 and is also being considered for escalat-

ed enforcement.

d. Enforcement Conference

23

.

On March 17, 1988 the NRC held an enforcement conference with

TVA to discuss concerns related to the apparent failure to ,

comply with TS 3.0.3 action requirements when both CCPs were [

INOPERADLE for a period of 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 24 minutes on March 9, i

'

1988. The meeting was opened by S. Ebneter, Director, office

of Special Projects, who along with F. McCoy discussed the NRC l

concerns with this specific event. TVA was requested to i

address their own investigation of this event along with other l

recent operational events that had occurred since approximately  !

January 14, 1988. TVA presented the requested information and .

I

provided a list of planned corrective actions to be implemented

both prior to and subsequent to plant startup. A copy of the t

material presented at the conference by TVA has been included I

as Appendix A of this inspection report. I

!

The NRC agreed with most of the TVA evaluation of the CCP  ;

event. However, there was a disagreement as to when TVA became l

aware that the 2A-A CCP was put in the PTL position when it was i

secured at 1:16 p.m. on March 9, 1988. TVA indicated that the

reason they took approximately 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> to report the violation i

of TS 3.0.3 was that they did not know for sure that the 2A  !

pump was inoperable at the same time that the 2B-B pump was i

inoperable. The inspector who discovered the problem consid- i

~

ered that the pump was put in eTL when it was secured at 1:16

p.m. This was based on discussicns with control room opera- -

tions personnel along with the pORS member who investigated the  !

event. Additionally, the PRO which was written approximately i

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> before the event was reported indleated that a viola-  ;

l tion of 3.0.3 may have occurred. The licensee agreed to ,

conduct further follow-up to evaluate the inspector's position.  !

The following prior-to-restart commitments were nade by the

l licensee: l

1

-

Controls will be established to limit interchanging

' operators from a cold shutdown unit to an operating unit.

-

AI-6, for operator log entries, is being revised to f

a delineate the level of detail for log entries such as

,

specifying switch positions. l

i

!

! -

AI-30, for operator communication, will be revised to

i specify required interface of operators during control  ;

board manipulations while switch positions are changed or i

j major equipment is taken out of service. f

I

!

i

- AI-5 will be revised to require a checklist completion ,

) (Appendix D1) for nonscheduled shift relief.  !

i

l -

A PORC review of f or mal TS interpretations is being I

i performed for technical adequacy and clarity. The TS i

l interpretation book has been removed from direct accesu to

operators until this review is complete. Additionally, i

.

!

I I

J  !

24

.

_ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ __ _

  • *  ?

i

i

.

l

l

'

the iteensee committed to have p0RC approval of any TS

interpretation prior to allowing its use by operators.  !

!

-

AI-5 will be revised to require the Assistant SS to

observe the main control board status f or abnormal condi- l

tions prior to assuming the shift. This observation will i

be documented in the Assistant SS log. (

- Senior Office of Nuclear power management are addressing i

operations personnel on the causes, conclusions, and i

corrective actions for the event.  !

l

-

Signs emphasizing plant operating mode will be placed in

the main control room and the auxiliary instrument room.  ;

'

,

!

-

The STA log entry at 8:20 p.m. and the AI-5, 3:00 p.m.

time entry will be corrected in accordance with plant [

procedures.

- Evaluate the duties of the Assistant SS and make necessary

changes to minimize his absence from the control room for  ;

administrative matters.

On March 24 the inspector verified that the prior-to-restart I

commitments made by the licensee in the enforcement conference j

were implemented. t

i

,

'

I

!

e

V

I

i

h

!

t

!

25

L

_ _ _ _ __ _ _ _ _ _ _ _ _

, _ _

. .

.

13. Shift Inspector Follow-un Issues

Issue Number Descriotion Status / Resolution

1/23/88-2-2 SI 166.12 needs to be Resolved. The licensee has

revised to reflect the implemented instruction changG

proper position of 88-0649 to require return to

valves HCV-74-36 and 31 service component positions.

2/15/88-2-1 Verify method of returning Resolved. SI-118 was

switches to service in appropriately revised.

SI-118,

2/16/88-2-1 Control room in- ~ tion Resolved. This item is con-

items : key con' shift tinuing to be monitored and

turnover check' 3 . and specific issues will be

SS log keeping .cices. addressed on a case-by-case

basis in subaequent reports.

2/16/88-2-2 Follow-up on discussion Resolved. Discussions and

items including key independent reviews indicated

control, shift turnover licensee ogrcms were

checklists, and logkeeping hdequate 69C will continue

to monit!

2/26/88-2-1 Evaluate new Work Control Currently under NRC review.

Group's effectiveness

regarding recognizing LCO

conditions

2/27/88-2-1 Review of improper Currently under NRC review.

operations of the COPS

2/28/88-1-1 SIS check valve leakage Currently under NRC review.

2/28/88-1-2 Main steam isolation ESF Resolved. Review ccmplete

actuation review and item to be reviewed

in depth in LER.

2/29/88-1-1 Review operator license Resolved. Review indicated

of an operator that the operator in question

was properly licensed.

2/29/C8-2-1 Repair TDAFP so it Resolved. The trips had been

does not inadvertently caused by inappropriate

trip on overspeed procedure steps. The pro-

cedure was changed and the

test rerun with satisfactory

results.

3/5/88-2-1 TVA to review the Resolved. This review is

validity of all TS complete. Twenty-seven out

interpretations prior to of ninety items were removed

Mode 2. from the control room.

26

t

__

_ _ - - - _ _ - __ -- - _ . . . _ . -- _ _ _ . - _ - _ _ _ _ - _ ___

- - _ _ _ - ____

. .

t

- 3/,7/88-2-1 Review PRO Report Resolved. The issue was

2-88 ' disposition discussed programatically

at 3/17/88 enforcement

conference.

.3/.7/88-2-2 . Follow events relating to. Resolved. _ Review is com-

2A-A MDAFP LCO :plete, and-an in-depth-

' review will be conducted

.on the LER.

3/7/88-2-3- Operability requirements Resolved. AFW instru-

of AFW instrumentation mentation'is considered

attendant-equipment.

- 3/8/88-1-l' Review the drawing Currently under NRC review.

control process in

SOEP 30 and SQEP 42 for

compliance with 10 CFR 50

Appendix B, Criterion VI

3/9/88-1-1 2A CCP in Pull-to-Lock Resolved. This item will

be tracked through vio-

lation 327,328/88-20-03

3/12/88-1-1 RCP #1 upper thrust Currently under NRC review.

bearing temperature alarm

problem

3/12/88-2-1- Determine that appropriate This is a non-restart item

measures for protection of and is currently under NRC

power block personnel for review.

radiography

3/12/88-2-2 Determine source of Resolved. Leak from

reddish fluid dripping snubber was repaired,

'

from overhead between #2 fluid cleaned up, the

and #3 SGs licensee is monitoring.

!

'

3/12/88-2-3 Evaluate PRO 2-88-81 Currently under NRC review,

dealing with no PMT after

[ work on 2-FCV-67-67

c.

.

'

3/14/88-2-1 Determine acceptability of Resolved. The test

pressure associated with pressure listed in SI-196

i. UHI valve testing was to ensure that valve

> accumulators were charged

to normal pressure after

other tests that reduced

accumulator pressure were

completed.

.

27

.

13. List of Abbreviations

AFW -

Auxiliary Feedwater

AI -

Administrative Instruction

ANSI - American National Standards Institute

AOI -

Abnormal Operating Instruction

ASME - American Society of Mechanical Engineers

CAQR - Conditions Adverse to Quality Reports

CCP -

Centrifugal Charging Pump

CCS -

Component Cooling System

CLA -

Cold Leg Accumulator

COPS - Cold Overpressure Protection System

CVI -

Containment Ventilation Isolation

EDG -

Emergency Diesel Generator

ENS -

Emergency Notification System

ESF -

Engineered Safety Feature

F -

Farenheit

HO -

Hold Order

HP -

Health Physics

IM -

Instrument Maintenance

LCO -

Limiting Condition for Operation

LCV -

Level Control Valve

LOCA - Loss of Coolant Accident

MDAFP- Motor Driven Auxiliary Feedwater Pump

MSIV - Main Steam Isolation Valve

NRC -

Nuclear Regulatory Commission

OSP -

Office of Special Projects

PMT -

Post Modification Test

PORS - Plant Operation Review Staff

PSIG - Pounds per Square Inch Gauge

PTL -

Pull-to-Lock

PRO -

Potentially Reportable Occurrence

QA -

Quality Assurance

QC -

Quality Control

RA -

Regulated Area

RCS -

Reactor Coolant System

RCP -

Reactor Coolant Pump

RHR -

Residual Heat Removal

RM -

Radiation Monitor

RO -

Reactor Operator

RTB -

Reactor Trip Breaker

RTD -

Resistance Thermal Devices

RTI -

Restart Test Instruction

RWP -

Radiation Work Permit

RWST - Reactor Water Storage Tank

SG -

Steam Generator

SI -

Surveillance Instruction

SS -

Shift Supervisor

SIS -

Safety Injection System

SOI -

System Operating Instructions

SRO -

Senior Reactor Operator

STA -

Shift Technical Advisor

TACF - Temporary Alteration Control Form

TAVE - Average Reactor Coolant

28

_ _ __ __., - _ . _ . _

. .,

.

-

.

TDAFP - Turbine Driven Auxiliary Feedwater Pump

TS -

Technical Specifications

TSC -

Technical Support Center

TVA -

Tennessee Valley Authority

UHI -

Upper Head Injection

VCT -

Volume Control Tank

WCC -

Work Control Center

WR -

Work Request

i

29

' .

. .

I

APPENDIX A

SUMMARY OF EVENTS

2A-A CCP FOUND IN PULL-TO-LOCK

+ -

,

DATE TIME ACTION

3/8/88 2154 28-B CCP WAS DECLARED INOPERABLE FOR REPAIRS.

'

ENTERED LCOs 3.1.2.4 AND 3.5.2.

3/9/88 0945 SHIFT REllEF OCCURRED. INCOMING OPERATOR HAD

5

SPENT TEN DAYS ON UNIT 1 BEFORE RETURNING TO UNIT 2.

. 3/9/88 1311 2B-B CCP STARTED FOR POST MAINTENANCE TEST.

3/9/88 1316 2A-A CCP WAS STOPPED AND PLACED IN PULL-TO-LOCK

BY OPERATOR.

3/9/88 1440 TEST ON 28-B CCP WAS COMPLETE AND PUMP DECLARED

.

OPERABLE. LCOs 3.1.2.4 AND ~3.5.2 WERE EXITED.

'; 3/9/88 1630 SHIFT REllEF TOOK PLACE. ONCOMING OPERATOR

ASKED ABOUT OPERABILITY OF THE 2A-A CCP IN

PULL-TO-LOCK POSITION. WAS TOLD PUMP OPERABLE.

3/9/88 1930 SECOND SHIFT RELIEF TOOK PLACE. 2A-A CCP WAS

FOUND IN THE PULL-TO-LOCK POSITION BY AN NRC

INSPECTOR. OPERATOR ENTERED LCO 3.5.2 AND

RETURNED 2A-A CCP TO A-AUTO MAKING PUMP

j OPERABLE. LCO 3.5.2 EXITED.

3 ~

3/9/88 2000 SHIFT SUPERVISOR WAS NOTIFIED OF EVENT BY NRC ,

INSPECTOR

I

. .

1

I.

If

t

L.. CONCLUSIONS

d

.-

  • OPERATOR DID NOT RECOGNIZE THAT PUTTING

l THE CCP HANDSWITCH IN PULL-TO-LOCK RENDERED

L THE PUMP INOPERABLE

L * TWO SUBSEQUENT SHIFT TURNOVERS DID NOT

L IDENTIFY THAT THE PUMP WAS INOPERABLE

s BECAUSE OF THE HANDSWITCH BEING IN

Tl PULL-TO-LOCK

  • HANDSWITCH POSITION WAS INCORRECTLY LOGGED

IN Al-5

L

..

h * INOPERABLE CONDITION OF 2A-A CCP WAS NOT

. IMMEDIATELY REPORTED TO SHIFT SUPERVISOR

  • STA LOG ENTRY FOR MARCH 9,1988, AT 2020 EST,

WAS IN ERROR

i * WRITE 0VER IN Al-5 BY OPERATOR IS CONTRADICTORY

TO THE REQUIREMENTS OF Al-7 FOR A OA DOCUMENT

i:

'l

.

' .

. .

.

ROOT CAUSES  !

l

,' o MANAGEMENT DID NOT ADEQUATELY CONSIDER THE POTENTIAL

AFFECTS OF TEMPORARILY ASSIGNING OPERATORS TO A COLD

'

'

SHUTDOWN UNIT AND BACK TO THE OPERATING UNIT (MODE 3).

  • MANAGEMENT DIRECTION REGARDING DETAIL OF OPERATOR

g LOG ENTRIES AND OPERATOR COMMUNICATION WAS NOT

j A0EQUATELY DESCRIBED.

  • Al-5 DOES NOT ADEQUATELY ADDRESS NONSCHEDULED

L SHIFT TURNOVERS.

I

1

4 PULL-TO-LOCK CCP IS NOT CONSISTENT WITH PLANT

-

MANAGEMENT PHILOSOPHY. i

  • DISCREPANCY EXISTS BETWEEN G01-3 AND TECHNICAL

SPECIFICATION 3.1.2.4 FOR CCPs NEEDED FOR REACTIVITY

CONTROL.

d

j

.-,

- - _ ._- _ - -__ _ __-._ - _ _ - - _ . - _ _ - - . _ _ - - - _ _ -

j

. .

.

_. CORRECTIVE ACTIONS '

'

(SLIDE 10F 2)

  • CONTROLS WILL BE ESTABLISHED TO LIMIT INTERCHANGING

OPERATORS FROM A COLD SHUTDOWN UNIT TO AN OPERATING

UNIT.

  • Al-6, FOR OPERATOR LOG ENTRIES IS BEING REVISED

TO DELINEATE THE LEVEL OF DETAll FOR LOG ENTRIES

SUCH AS SPECIFYING SWITCH POSITIONS.

.

( * Al-30, FOR OPERATOR COMMUNICATION WILL BE REVISED

TO SPECIFY REQUIRED INTERFACE OF OPERATORS DURING

3 CONTROL BOARD MANIPULATIONS WHILE SWITCH POSITIONS

ARE CHANGED OR TAKING MAJOR EQUIPMENT OUT OF SERVICE.

l * Al-5 WILL BE REVISED TO REQUIRE A CHECKLIST

i

COMPLETION (APPENDIX B1) FOR NONSCHEDULED SHIFT

REllEF.

,

  • A REVIEW OF FORMAL TECHNICAL SPECIFICATION

!

,

INTERPRETATIONS (TSI) IS BEING PERFORMED FOR

! TECHNICAL ADECUiCY AND CLARITY. TSI MANUAL HAS

BEEN REMOVED FROM DIRECT ACCESS TO OPERATORS UNTIL

THIS REVIEW IS COMPLETE.

  • Al-5 WILL BE REVISED TO REQUIRE THE UNIT SUPERVISOR

(SRO) TO OBSERVE THE MAIN CONTROL BOARD STATUS FOR

l

-

ABNORMAL CONDITIONS PRIOR TO ASSUMING SHIFT. THIS

OBSERVATION WILL BE DOCUMENTED IN THE UNIT SUPERVISOR LOG.

!

I

l

. .

_ CORRECTIVE ACTIONS

(SLIDE 2 0F 2)

T

  • EVALUATE G01-3 REQUIREMENT TO PUT A CCP IN PULL TO

LOCK BELOW 350 DEGREES F FOR COLD OVERPRESSURIZATION

PROTECTION.

  • SENIOR OFFICE OF NUCLEAR POWER MANAGEMENT

ADDRESSING OPERATIONS PERSONNEL ON THE CAUSES,

CONCLUSIONS, AND CORRECTIVE ACTIONS FOR THIS EVENT.

.

  • SIGNS EMPHASIZING PLANT OPERATING MODE WILL BE

PLACED IN MCR AND AUXILIARY INSTRUMENT ROOM.

l * TECHNICAL SPECIFICATIONS 3.5.3 (MODE 4) AND 3.1.2.4

I (MODES 1-4 REACTIVITY CONTROL) WILL BE EVALUATED

TO DETERMINE IF A CHANGE IS NEEDED TO CLARIFY

THE OPERABILITY REQUIREMENTS OF CCPS FOR MODE 4.

* TRAINING WILL BE GIVEN ON PROCEDURE CHANGES

AND TECHNICAL SPECIFICATION INTERPRETATION

CHANGES.

  • SCENARIOS EMPHASIZING THE USE OF TECHNICAL

SPECIFICATIONS WILL BE INCORPORATED INTO OPERATOR

'

L SIMULATOR TRAINING.

  • THE STA LOG ENTRY AT 2020 EST AND THE Al-5,

! 1500 TIME ENTRY WILL BE CORRECTED IN ACCORDANCE

WITH PLANT PROCEDURES.

l

I

l

l

_ _

y .

.

!

OPERATIONAL EVENT SUMMARY

-

-

, s

1. INADVERTENT ABI: (1-14-88)

.

2. PERSONNEL ERROR IN RETURNING TB SUMP RM TO SERVICE: (1-16-88)

"

3. INADVERTENT START OF (4) D/Gs: (1-27-88)

4. UNIT 1 CVI - WRONG UNIT / WRONG EQUIPMENT: (1-27-88)

5. FAILURE TO COMPLETE PMT ON ERCW RM: (1-30-88)

6. RX TRIP: (2-7-88)

..

7. TURBINE TRIP /FWl: (2-7-88)

8. FAILURE TO MEET SR RCS LEAKRATE: (2-8-8 8)

P 9. RCS LOSS OF INVENTORY - FCV-62-118 MISPOSITION: (2-9-88)

,

~ '

10. MAIN STEAM ISOLATION: (2-10-88)

11. LOSS OF NON-ESSENTIAL AIR IN CONTAINMENT UNIT 1: ' (2-10-88)

4

12. 1 A-A D/G TAGGED W/"B" CREVS INOP: (2-15-88)

L

l 13. COPS ACTUATION: (2-17-88)

l

14. MISINTERPRETATION OF CCS INDEPENDENT LOOPS: (2-26-88)

15. MSIV ACTUATION: (2-28-88) .

L 16. (2) UNIT 1 CVI: DUE TO EMI NOISE: (3-1-88)

l

17. TDAFW LCV NOT DECLARED INOP UPON SI-166.8 FAILURE: (3-5-88)

e

18. FAILURE TO DECLARE TDAFW VALVE (LCV) IHOP DUE TO COMMON

l SENSE LINE: (3-6-88)

19. NRC FOUND 2A-A CCP IN PULL TO LOCK: (3-9-88)

,

, , _ . . _ . , , . _ . . _ _ _ . . _ . _ _ , , . . . , . _ _ . , _ , - - . . . - - - - - - - - -

.

4 ,

EVENT CLASSIFICATION

PROCEDURAL INADVERTENT INADVERTENT

. DESCRIPTION NONCOMPLIANCE ESF ACTUATIONS LCO ENTRY

1 INADVERTENT ABI (1-14-88) X

2 TB SUMP RM (1-16-88) x

3 D/G START (1-27-88) y

4 UNIT 1 CVI (1-27-88) X X

5 ERCW RM (1-30-88) y

.

6 RX TRIP (2-7-88)

X X

,

7 TURBINE TRIP /FWI (2-7-88) X X

,' 8 RCS LEAKRATE (2-8-88) X X

,

FCV-62-118 POSITION (2-9-88)

-

10 MAIN STEAM ISOLATION (2-10-88) y y

11 LOSS OF AIR (2-10-88) X

. 12 CREVS INOP (2-15-88) X

,

13 COPS ACTUATION (2-17-88)

[ X

,

_

14 CCS LOOPS (2-26-88) y

i

15 MSIV ACTUATION (2-28-88) y

,

16 (2) UNIT 1 CVis (3-1-88) X

17 TDAFW LCV STROKE TIME (3-5-88) y y

(

,

TDAFW LCV SENSE LINE (3-6-88) x X

19 CCP IN PULL-TO-LOCK (3-9-88) X X