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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J3341999-10-19019 October 1999 Forwards Request for Addl Info Re Sale of Portion of Land Part of Oyster Creek Nuclear Generating Station Site Including Portion of Exclusion Area ML20217E0181999-10-0606 October 1999 Provides Nj Dept of Environ Protection Comments on Oyster Creek Nuclear Generating Station TS Change Request 267 Re Clarifications to Several TS Sections 05000219/LER-1998-011, Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts1999-09-30030 September 1999 Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts ML20216J7591999-09-30030 September 1999 Informs NRC That Remediation Efforts for Software Sys Etude & Rem/Aacs/Cico Have Been Completed According to Schedule & Now Y2K Ready ML20212J6721999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Oyster Creek Nuclear Generating Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216K1421999-09-29029 September 1999 Provides NRC with Name of Single Point of Contact for Purpose of Accessing Y2K Early Warning Sys,As Requested by NRC Info Notice 99-025 ML20217D1661999-09-27027 September 1999 Forwards Proprietary Completed NRC Forms 396 & 398,in Support of License Renewal Applications for Listed Individuals,Per 10CFR55.57.Encl Withheld ML20217B2531999-09-24024 September 1999 Informs That on 980903,Region I Field Ofc of NRC Ofc of Investigations Initiated Investigation to Determine Whether Crane Operator Qualification/Training Records Had Been Falsified at Oyster Creek Nuclear Generating Station ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A7921999-09-13013 September 1999 Forwards Second RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Issued on 950817 to Plant ML20212B5571999-09-10010 September 1999 Forwards Rev 11 to Oyster Creek Emergency Dose Calculation Manual, IAW 10CFR50,App E,Section V ML20211N2941999-09-0303 September 1999 Responds to NRC 990802 Telcon Request for Environ Impact Assessment of TS Change Request 251 Concerning Movement of Loads Up to 45 Tons with RB Crane During Power Operations ML20211J9831999-09-0202 September 1999 Discusses 990804 Telcon Re Sale of Portion of Oyster Creek Nuclear Generating Station Land.Requests Info Re Location of All Areas within Property to Be Released Where Licensed Radioactive Matl Present & Disposition of Radioactive Matl ML20211J6771999-08-30030 August 1999 Submits Response to NRC 990802 Telcon Request for Gpu to Provide Environ Impact Assessment for Tscr 251 ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211C0161999-08-19019 August 1999 Advises That Info Submitted by Ltr,Dtd 990618, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool, Holtec Rept HI-981983,rev 4,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211B9011999-08-18018 August 1999 Forwards Rev 0 to EPIP 1820-IMP-1720.01, Emergency Public Info Implementing Procedure ML20210U4341999-08-17017 August 1999 Responds to to Chairman Dicus of NRC on Behalf of Fm Massari Concern About Oyster Creek Nuclear Generating Station Not Yet Being Fully Y2K Compliant ML20210Q7331999-08-12012 August 1999 Responds to Re TS Change Request (TSCR)264 from Oyster Creek Nuclear Generating Station.Questions Re Proposed Sale of Property within Site Boundary & Exclusion Area ML20210L6311999-08-0606 August 1999 Discusses Licensee Response to GL 92-01,Rev1,Suppl 1, Rv Structural Integrity, for Plant.Staff Has Revised Info in Rv Integrity Database & Releasing as Rvid Version 2 ML20210D2801999-07-22022 July 1999 Submits Response to Administrative Ltr 99-02 Operating Reactor Licensing Action Estimates. Estimate of Licensing Actions Projected for Fy 2000 Encl.No Projection Provided for Fy 2001 ML20209H5001999-07-14014 July 1999 Forwards Revised TS Pages 3.1-15 & 3.1-17 Which Include Ref to Note (Aa) & Approved Wording of Note H of Table 3.1.1, Respectively ML20210U4411999-07-12012 July 1999 Forwards Article from Asbury Park Press of 990708 Faxed to Legislative Officer by Mutual Constitute Fm Massari Indicating That Oyster Creek Nuclear Generating State Not Fully Y2K Compliant ML20209G1451999-07-0909 July 1999 Forwards Rev 1 to 2000-PLN-1300.01, Oyster Creek Generating Station Emergency Plan. Attachment 1 Contains Brief Summary of Changes,Which Became Effective on 990702 ML20209E0821999-07-0707 July 1999 Forwards TS Change Request 269 for License DPR-16,changing Component Surveillance Frequencies to Indicate Frequency of Once Per Three Months ML20209B7501999-07-0101 July 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Generic Ltr 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Licensee Y2K Readiness Disclosure for Ocngs,Encl ML20196G1361999-06-23023 June 1999 Provides Status of Corrective Actions Proposed in in Response to Insp Rept 50-219/98-80 & Revised Schedule for Completion of Actions Which Are Not Yet Complete ML20196E6421999-06-22022 June 1999 Forwards Revised Pages of TS Change Request 261,dtd 990618. Replacement Requested Due to Several Dates Being Omitted on Certain Pages ML20195G6631999-06-0707 June 1999 Discusses 981204 Intiation to Investigate Whether Contract Valve Technician Was Discriminated Against for Raising Concern Re Use of Untrained/Unqualified Workers Performing Valve Repairs.Technician Was Not Discriminated Against ML20195G6541999-06-0707 June 1999 Discusses 981204 Initiation to Investigate Whether Contract Valve Technician,Was Discriminated Against for Raising Concern Re Use of Untrained/Unqualified Workers Performing Valve Repairs.Technician Was Not Discriminated Against ML20209B0561999-06-0404 June 1999 Informs That NRR Has Reorganized,Effective 990328.Forwards Organizational Chart ML20195D0551999-06-0303 June 1999 Forwards TS Change Request 226 to License DPR-16,permitting Operation with Three Recirculation Loops.Certificate of Svc & Tss,Encl ML20195C5511999-05-25025 May 1999 Forwards Book of Controlled Drawings Currently Ref But Not Contained in Plant Ufsar.Drawings Were Current at Time of Submittal ML20206N7711999-05-11011 May 1999 Forwards Rev 0 to Oyster Creek Emergency Plan, IAW 10CFR50.47(b) & 10CFR50.54(q).Changes Became Effective on 990413 ML20206H9441999-04-28028 April 1999 Forwards Application for Amend to License DPR-16,requesting Approval to Handle Loads Up to & Including 45 Tons Using Reactor Bldg Crane During Power Operations,Per NRC Bulletin 96-002 ML20206D3801999-04-26026 April 1999 Forwards Rev 11 to UFSAR, & Rev 10 to Fire Hazards Analysis Rept, for Oyster Creek Nuclear Generating Station, Per 10CFR50.712(e) ML20206B6991999-04-26026 April 1999 Forwards Copy of Rev 11 to UFSAR & Rev 10 to Oyster Creek Fire Hazards Analysis Rept. Without Fire Hazard Analysis ML20206C8261999-04-22022 April 1999 Submits Financial Info IAW Requirements of 10CFR50.71(b) & 10CFR140.21 ML20206A9931999-04-22022 April 1999 Forwards Number of Personnel & Person Rems by Work & Job Function Rept for Period Jan-Dec 1998. Included in Rept Is Listing of Number of Station,Util & Contractor Personnel as Well as Diskette Reporting 1998 Occupational Radiation ML20205P8411999-04-15015 April 1999 Forwards TS Change Request 267 to License DPR-16,modifying Items in Sections 2 & 3 of Ts,Expanding Two Definitions in Section 1 & Modifying Bases Statements in Sections 2,3 & 4. Certificate of Svc Encl ML20205P5381999-04-14014 April 1999 Ack Receipt of Re Request for Exception to App J. Intended Correction Would Need to Be Submitted as Change to TS as Exceptions to RG 1.163 Must Be Listed in Ts,Per 10CFR50,App J ML20205P9401999-04-12012 April 1999 Informs NRC That Gpu Nuclear Is Modifying Oyster Creek FSAR to Reflect Temp Gradient of 60 F & to Correct Historical Record ML20205P0651999-04-0909 April 1999 Discusses 990225 PPR & Forwards Plant Issues Matrix & Insp Plan.Results of PPR Used by NRC Mgt to Facilitate Planning & Allocation of Insp Resources 05000219/LER-1998-015, Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page1999-04-0505 April 1999 Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page ML20205J3281999-04-0101 April 1999 Discusses Arrangements Made on 990323 for NRC to Inspect Licensed Operator Requalification Program at Oyster Creek Nuclear Generating Station During Week of 990524 ML20205H1081999-03-31031 March 1999 Forwards Current Funding Status for Decommissioning Funds Established for OCNPP,TMI-1,TMI-2 & SNEC ML20205F0611999-03-25025 March 1999 Submits Info on Sources & Levels of Property Insurance Coverage Maintained & Currently in Effect for Oyster Creek Nuclear Generating Station,Iaw 10CFR50.54(w)(3) ML20205E1171999-03-24024 March 1999 Forwards Rev 39 to Oyster Creek Security Plan & Summary of Changes,Iaw 10CFR50.54(p).Rev Withheld ML20207F0331999-03-0404 March 1999 Forwards Insp Rept 50-219/98-12 During Periods 981214-18, 990106-07 & 20-22.Areas Examined During Insp Included Implementation of GL 89-10 & GL 96-05.No Violations Noted ML20207K2471999-02-25025 February 1999 Forwards Fitness for Duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Ny 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217E0181999-10-0606 October 1999 Provides Nj Dept of Environ Protection Comments on Oyster Creek Nuclear Generating Station TS Change Request 267 Re Clarifications to Several TS Sections 05000219/LER-1998-011, Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts1999-09-30030 September 1999 Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts ML20216J7591999-09-30030 September 1999 Informs NRC That Remediation Efforts for Software Sys Etude & Rem/Aacs/Cico Have Been Completed According to Schedule & Now Y2K Ready ML20216K1421999-09-29029 September 1999 Provides NRC with Name of Single Point of Contact for Purpose of Accessing Y2K Early Warning Sys,As Requested by NRC Info Notice 99-025 ML20217D1661999-09-27027 September 1999 Forwards Proprietary Completed NRC Forms 396 & 398,in Support of License Renewal Applications for Listed Individuals,Per 10CFR55.57.Encl Withheld ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212B5571999-09-10010 September 1999 Forwards Rev 11 to Oyster Creek Emergency Dose Calculation Manual, IAW 10CFR50,App E,Section V ML20211N2941999-09-0303 September 1999 Responds to NRC 990802 Telcon Request for Environ Impact Assessment of TS Change Request 251 Concerning Movement of Loads Up to 45 Tons with RB Crane During Power Operations ML20211J6771999-08-30030 August 1999 Submits Response to NRC 990802 Telcon Request for Gpu to Provide Environ Impact Assessment for Tscr 251 ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211B9011999-08-18018 August 1999 Forwards Rev 0 to EPIP 1820-IMP-1720.01, Emergency Public Info Implementing Procedure ML20210D2801999-07-22022 July 1999 Submits Response to Administrative Ltr 99-02 Operating Reactor Licensing Action Estimates. Estimate of Licensing Actions Projected for Fy 2000 Encl.No Projection Provided for Fy 2001 ML20209H5001999-07-14014 July 1999 Forwards Revised TS Pages 3.1-15 & 3.1-17 Which Include Ref to Note (Aa) & Approved Wording of Note H of Table 3.1.1, Respectively ML20210U4411999-07-12012 July 1999 Forwards Article from Asbury Park Press of 990708 Faxed to Legislative Officer by Mutual Constitute Fm Massari Indicating That Oyster Creek Nuclear Generating State Not Fully Y2K Compliant ML20209G1451999-07-0909 July 1999 Forwards Rev 1 to 2000-PLN-1300.01, Oyster Creek Generating Station Emergency Plan. Attachment 1 Contains Brief Summary of Changes,Which Became Effective on 990702 ML20209E0821999-07-0707 July 1999 Forwards TS Change Request 269 for License DPR-16,changing Component Surveillance Frequencies to Indicate Frequency of Once Per Three Months ML20209B7501999-07-0101 July 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Generic Ltr 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Licensee Y2K Readiness Disclosure for Ocngs,Encl ML20196G1361999-06-23023 June 1999 Provides Status of Corrective Actions Proposed in in Response to Insp Rept 50-219/98-80 & Revised Schedule for Completion of Actions Which Are Not Yet Complete ML20196E6421999-06-22022 June 1999 Forwards Revised Pages of TS Change Request 261,dtd 990618. Replacement Requested Due to Several Dates Being Omitted on Certain Pages ML20195D0551999-06-0303 June 1999 Forwards TS Change Request 226 to License DPR-16,permitting Operation with Three Recirculation Loops.Certificate of Svc & Tss,Encl ML20195C5511999-05-25025 May 1999 Forwards Book of Controlled Drawings Currently Ref But Not Contained in Plant Ufsar.Drawings Were Current at Time of Submittal ML20206N7711999-05-11011 May 1999 Forwards Rev 0 to Oyster Creek Emergency Plan, IAW 10CFR50.47(b) & 10CFR50.54(q).Changes Became Effective on 990413 ML20206H9441999-04-28028 April 1999 Forwards Application for Amend to License DPR-16,requesting Approval to Handle Loads Up to & Including 45 Tons Using Reactor Bldg Crane During Power Operations,Per NRC Bulletin 96-002 ML20206B6991999-04-26026 April 1999 Forwards Copy of Rev 11 to UFSAR & Rev 10 to Oyster Creek Fire Hazards Analysis Rept. Without Fire Hazard Analysis ML20206D3801999-04-26026 April 1999 Forwards Rev 11 to UFSAR, & Rev 10 to Fire Hazards Analysis Rept, for Oyster Creek Nuclear Generating Station, Per 10CFR50.712(e) ML20206C8261999-04-22022 April 1999 Submits Financial Info IAW Requirements of 10CFR50.71(b) & 10CFR140.21 ML20206A9931999-04-22022 April 1999 Forwards Number of Personnel & Person Rems by Work & Job Function Rept for Period Jan-Dec 1998. Included in Rept Is Listing of Number of Station,Util & Contractor Personnel as Well as Diskette Reporting 1998 Occupational Radiation ML20205P8411999-04-15015 April 1999 Forwards TS Change Request 267 to License DPR-16,modifying Items in Sections 2 & 3 of Ts,Expanding Two Definitions in Section 1 & Modifying Bases Statements in Sections 2,3 & 4. Certificate of Svc Encl ML20205P9401999-04-12012 April 1999 Informs NRC That Gpu Nuclear Is Modifying Oyster Creek FSAR to Reflect Temp Gradient of 60 F & to Correct Historical Record 05000219/LER-1998-015, Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page1999-04-0505 April 1999 Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page ML20205H1081999-03-31031 March 1999 Forwards Current Funding Status for Decommissioning Funds Established for OCNPP,TMI-1,TMI-2 & SNEC ML20205F0611999-03-25025 March 1999 Submits Info on Sources & Levels of Property Insurance Coverage Maintained & Currently in Effect for Oyster Creek Nuclear Generating Station,Iaw 10CFR50.54(w)(3) ML20205E1171999-03-24024 March 1999 Forwards Rev 39 to Oyster Creek Security Plan & Summary of Changes,Iaw 10CFR50.54(p).Rev Withheld ML20207K2471999-02-25025 February 1999 Forwards Fitness for Duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Ny ML20206S2541999-01-20020 January 1999 Confirms Resolution of Thermo-Lag Fire Barriers in Fire Zones OB-FZ-6A & OB-FZ-6B (480 Switchgear Rooms) IAW Previous Commitments Contained in Gpuns Ltrs to NRC & 971001 ML20199J2631999-01-18018 January 1999 Requests That Listed Changes Be Made to Correspondence Distribution List for Oyster Creek Generating Station ML20199D0271999-01-11011 January 1999 Requests Listed Addl Info in Order to Effectively Review TS Change Request 264 Re Ownership of Property within Exclusion Area ML20199A6521999-01-0707 January 1999 Notifies That Reactor Operators G Scienski,License SOP-11319 & D Mcmillan,License SOP-3919-4 Have Terminated Licenses at Oyster Creek Nuclear Generating Station, Effective 990101 ML20198T1061999-01-0606 January 1999 Forwards Rev 15 to Gpu Nuclear Corporate Emergency Plan for TMI & Oyster Creek Nuclear Station. with Summary of Changes Which Reflect Use of EALs Approved in NRC Ltr to Gpun on 980908 & Other Changes Not Related to Use of New EALs ML20198K0331998-12-23023 December 1998 Forwards Change Request 268 for Amend to License DPR-16. Amend Would Change TS to Specify Surveillance Frequency of Once Per Three Months ML20198H0181998-12-22022 December 1998 Forwards Attachment Addressing New Info & Modifying 980505 Submittal Re Request for Change to Licensing Bases for ECCS Overpressure,In Response to NRC Bulletin 96-03, Potential Plugging of ECCS by Debris in Bwrs ML20198H8521998-12-16016 December 1998 Dockets Completion of Physical Inventory Performed in July 1997,as Addl Info to Nuclear Matl Balance Rept Submitted on 980416 ML20196H4461998-12-0202 December 1998 Provides Final Response to NRC GL 96-01, Testing of Safety-Related Logic Circuits ML20196B4471998-11-23023 November 1998 Provides Required Response 2 to NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers in Bwrs. During Recently Completed 17R Refueling Outage,New Strainers Were Installed ML20195J8451998-11-12012 November 1998 Forwards Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan, as Change Previously Made Without Appropriate Notification to NRC ML20195C7201998-11-11011 November 1998 Forwards 120-day Required Response to GL 98-04, Potential for Degradation of ECCS & CSS After LOCA Because of Construction & Protective Coating Deficiencies & Foreign Matl in Containment, ML20195E1221998-11-10010 November 1998 Notifies NRC of First Time Usage of Code Case N-504 & Inclusion Into OCNGS ISI Program,As Accepted by RG 1.147, Inservice Insp Code Case Acceptability ML20155J6851998-11-0505 November 1998 Forwards TS Change Request 266,to Modify Safety Limits & Surveillances of LPRM & APRM Sys & Related Bases to Ensure APRM Channels Respond within Necessary Range & Accuracy & Verify Channel Operability ML20155H5641998-11-0202 November 1998 Informs That Bne Has No Comments on Proposed Change 259 to Ts,Correcting Required Water Level in Condensate Storage Tank So That Design Basis Is Correctly Implemented ML20155G3741998-10-29029 October 1998 Forwards Response to NRC 980619 RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L2551990-09-14014 September 1990 Advises of Preparation for Final Refueling Outage to Complete Second 10-yr Interval for Inservice Insps ML20059F5121990-09-0505 September 1990 Requests Exemption from Filing Requirement of 10CFR55.45(b)(2)(iii) to Allow Submittal of NRC Form 474, Simulator Facility Certification, After 910326 Deadline & to Allow Administering of Simulator Portion of Test ML20059F7441990-08-31031 August 1990 Forwards Util Review of NRC Backfit Analysis for Hardened Wetwell Vent.Nrc Analysis Does Not Support Conclusion That Hardening Existing Vent Is cost-beneficial Mod for Plant ML20059E9061990-08-30030 August 1990 Forwards Response to 900808 Request for Addl Info Re NRC Bulletin 90-002, Loss of Thermal Margin Caused by Fuel Channel Box Bow ML20059G1841990-08-29029 August 1990 Ack NRC Request to Perform Type C Testing During Unscheduled Outage,As Plant Conditions Will Allow.Type C Exemptions Should Remain in Effect Until New Outage Start Date ML20059C8231990-08-27027 August 1990 Advises That SPDS Enhancements Described in Completed,Per 900628 Request.Offline & Online Testing Completed & Enhancements Considered to Be Operational ML20059C8571990-08-24024 August 1990 Provides Results of Evaluation of Ability to Meet Acceptance Criteria for Eccs,In Response to 900804 Notice of Violation. Plant Meets Acceptance Criteria Contained in 10CFR50.46 W/ Valve Logic Design Deficiency in Containment Spray Sys ML20063P9521990-08-0909 August 1990 Advises That Response to NRC 900523 Request for Assessment of Hazardous Matl Shipment Will Be Sent by 910531 ML20058N0781990-08-0909 August 1990 Submits Info Re pressure-temp Operating Limits for Facility, Per Generic Ltr 88-11.Util Recalculated Adjusted Ref Temp for Each Belt Line Matl as Result of New Displacement Per Atom Values ML20058L9521990-08-0303 August 1990 Forwards Rev 2 to Security Contingency Plan.Rev Withheld (Ref 10CFR73.21) ML20058L9551990-08-0303 August 1990 Responds to SALP Rept 50-219/88-99.Although Minor,Several Factual Errors Noted.Dialogue Promotes & Identifies Areas Where Improvements Should Be Made ML20056A2071990-07-30030 July 1990 Forwards Response to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Record Review Performed & Sys Walkdowns Completed to Assemble Requisite List ML20058N9911990-07-20020 July 1990 Partially Withheld Response to NRC Bulletin 90-002 Re Loss of Thermal Margin Caused by Box Bow (Ref 10CFR2.790(b)(1)) ML20055H7961990-07-20020 July 1990 Advises of Change to Preventive Maint Program for Electromatic Relief Valves.Rebuild Schedule Will Be Modified to Require Rebuilding Two or Three Valves During Refueling Outage & Remaining Valves During Next Refueling Outage ML20055J0481990-07-19019 July 1990 Requests 2-wk Extension for Submittal of Response to Re Installation of Hardened Wetwell Vent W/ Appropriate Extension Period to Be Decided Pending Outcome of 900724 Meeting Discussion W/Bwr Owners Group ML20064A1221990-07-11011 July 1990 Discusses 900710 Telcon W/Nrc Re Util Corrective Actions in Response to NRC Finding That Operator Received Passing Grade on Administered Requalification Exam in 1989 Should Have Received Failing Grade.Corrective Actions Listed ML20055F8491990-07-10010 July 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 188,reducing Low Condenser Vacuum Scram Setpoint ML20043H7471990-06-21021 June 1990 Confirms Telcon W/A Dromerick Re Util Plans to Inspect CRD Hydraulic Control Units During Plant Walkdown to Address USI A-46, Seismic Qualification of Equipment in Operating Nuclear Power Plants. Walkdown Planned in Oct 1992 ML20043H2301990-06-14014 June 1990 Documents Licensee Commitment to Improve Seismic Restraints for Diesel Generator Switchgear Encls,Per 900613 Telcon W/ Nrc.Engineering Will Be Finalized & Mods Completed Prior to 900622 ML20043F7581990-06-0707 June 1990 Responds to Request for Info Re Util Compliance W/Generic Ltr 88-01 & Insp Plans for Upcoming 13R Outage.Frequency of Insp of Welds Classified as IGSCC Categories C,D & E Will Not Be Reduced During 13R Outage ML20043C2461990-05-25025 May 1990 Forwards Rev 7 to EPIP 9473-IMP-1300.06 & Rev 4 to Radiological Controls Policy & Procedure Manual 9300-ADM-4010.03, Emergency Dose Calculation Manual. ML20043C5801990-05-25025 May 1990 Provides Descriptions & Conclusions of Three Remaining Issues of SEP Topic III-7B.Issues Include,Evaluation of Drywell Concrete Subj to High Temp & Thermal Transients ML20043B2981990-05-21021 May 1990 Responds to NRC 900420 Ltr Re Violations Noted in Insp Rept 50-219/90-06.Corrective Actions:Incident Critique Rept Incorporated as Required Reading for Appropriate Operations Personnel & Change Made to Procedure 201.1 ML20043D0701990-05-17017 May 1990 Provides NRC W/Addl Info Re SPDS & Responds to Concerns Raised During 900117 & 18 SPDS Audit Documented in 900130 Ltr ML20043B3901990-05-0909 May 1990 Responds to NRC 900408 Ltr Re Violations Noted in Insp of License DPR-16.Corrective Actions:Two Narrow Range Drywell Pressure Monitoring Instruments to Be Provided During Cycle 14R Refueling Outage,Per Reg Guide 1.97,Category 1 ML20042G7071990-05-0808 May 1990 Forwards Summary of Initiatives & Accomplishments Re SALP, Per 891031 Commitment at mid-SALP Meeting.Plant Div Responsibilities Now Include Conduct of Maint Outages & Emergency Operating Procedure Training Conducted ML20042G2291990-05-0707 May 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 180,revising Tech Specs Re Fuel cycle-specific Parameters ML20042G2601990-05-0404 May 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 187,revising Tech Specs to Accommodate Implementation of 24-month Plant Refueling Cycle ML20042E9431990-04-20020 April 1990 Forwards Revised Epips,Consisting of Rev 7 to 9473-IMP-1300.01,Rev 4 to 9473-1300.11 & Rev 2 to 9473-ADM-1319.04.Deleted EPIPs Listed,Including Rev 3 to 9473-1300.19,Rev 2 to 9473-1300.21 & Rev 5 to 9473.1300.24 ML20042E6371990-04-16016 April 1990 Informs of Plans to Install Safety Grade Check Valve in Supply Line Inside Emergency Diesel Generator Fuel Tank Room Coincident W/Replacement or Repair of Emergency Diesel Generator Fuel Oil Tank ML20042E5001990-04-13013 April 1990 Forwards Rev 1 to Topical Rept 028, Oyster Creek Response to NRC Reg Guide 1.97. ML20012E8711990-03-28028 March 1990 Lists Property Insurance Coverage,Effective 900401,per 10CFR50.54(w)(2) ML20012D4391990-03-19019 March 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 186,allowing Idle Recirculation Loop to Be Isolated During Power Operation by Closing Suction,Discharge & Bypass Valves ML20012B6781990-03-0202 March 1990 Requests Exemption of Specified Local Leak Rate Test Intervals to Include Next Plant Refueling Outage Scheduled for Jan 1991,per 10CFR50,App J ML17347B5881990-03-0101 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. Info Covers Time Spent by Key Power Plant Managers in Responding to Operational Insps & Audits ML15217A1031990-02-28028 February 1990 Forwards Semiannual Radioactive Effluent Release Rept for Jul-Dec 1989 for McGuire Nuclear Station Units 1 & 2 & Revised Process Control Programs & Offsite Dose Calculation Manuals ML18094B3221990-02-28028 February 1990 Forwards Executed Amend 14 to Indemnity Agreement B-74 ML20011F3821990-02-26026 February 1990 Confirms Amount Electronically Transferred to Us Dept of Treasury,Nrc on 900223 for Payment of NRC Review Fees of 10CFR50 Applications & 10CFR55 Svcs Per 10CFR170,for Period of 890101-0617 for Listed Invoices ML20012A1501990-02-23023 February 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 184,removing 3.25 Limit on Extending Surveillance Intervals,Per Generic Ltr 89-14 ML20006G0621990-02-22022 February 1990 Forwards Revised Proprietary Pages to DPC-NE-2004, Core Thermal Hydraulic Methodology Using VIPRE-01, Reflecting Minor Methodology Changes Made During Review & Approval Process.Pages Withheld ML20006G0101990-02-21021 February 1990 Discusses 900110 Meeting W/Nrr Re 13R Insp Criteria for RWCU Welds Outboard of Second Containment Isolation Valve. All Welds Required 100% Radiography Based on Review of Piping Spec.Response to Generic Ltr 88-01 Will Be Revised ML20011F2571990-02-21021 February 1990 Advises That 891003 Request for Appropriate Tech Specs for Chlorine Detection Re Control Room Habitability,Not Warranted ML20011F6641990-02-20020 February 1990 Responds to NRC 900122 Notice of Violation & Forwards Payment of Civil Penalty in Amount of $25,000.Corrective Actions:Change Made to Sys Component Lineup Sheets in 125- Volt Dc Operating Procedure to Include Selector Switches ML20006F5931990-02-20020 February 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 177.Amend Changes Tech Spec 4.7.B to Include Battery Svc Test Every Refueling Outage & Mod of Frequency of Existing Battery Performance Test ML20006E9071990-02-16016 February 1990 Discusses Plants Design Control Program.Util Adopted Concept of Design Change Implementation Package (Dcip).Dcip Will Contain or Ref Design Change Notice Prepared Per Approved Procedures ML20006E1441990-02-16016 February 1990 Forwards Suppl to Rev 1 to Updated FSAR for Braidwood Station,Units 1 & 2 & Byron Station,Units 1 & 2,per 881214 & 891214 Submittals ML20006F9181990-02-15015 February 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 183,permitting No Limitation on Number of Inoperable Position Indicators for 16 ASME Code Safety Valves During Power Operation ML20006E4201990-02-14014 February 1990 Requests NRC Approval for Use of Alloy 690 Steam Generator Tube Plugs for Facility,Prior to 900301,pending Final ASME Approval of Code Case for Alloy 690 ML20011E6151990-02-12012 February 1990 Forwards Revs 1 to Security Plan & Security Training & Qualification Plan & Rev 2 to Security Contingency Plan. Salem Switchyard Project Delayed.Revs Withheld (Ref 10CFR73.21) ML20011E4991990-02-0606 February 1990 Discusses Liability & Funding Requirements Re NRC Decommissioning Funding Rules & Verifies Understanding of Rules.Ltr from NRC Explaining Liability & Requirements of Rule Requested 1990-09-05
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s q a FCc Div of Complunce Jersey Central Powdh & Ligilt Com puny M ADISoN AVENU E AT PUNCH BOWL Ro AD e MoRRISToWN, N. J. 07960 e 533 6111 February 9, 1968, Dr. Peter A. bbrris, Director Division of Reactor Licensing United States Atomic Energy Commission Washington, D. C. 20515 4
Subject:
Oyster Creek Reactor Vessel Repair Program i
9
Dear Dr. Morris:
We have, throughout the past several weeks, discussed on 6 several occasions with you and your staff, as well as the ACR3, the problems associated with the reactor vessel at Oyster Creek. These t discussions, which have been in the nature of interim stat,us reports, supplemented by Amendment 29, Status Report on Reactor Vessel Repair Program, have been aimed at maintaining communication with the Commission and its consultants relative to this problem.
Our contract,or, the General Electric Company, has developed a
. repair program along the lines set forth in the attached summary report which, you will note, General Electric states will be amplified by its i detailed report submitted within about one month. We have advised
-General Electric that we have no objection to their proceeding with the
- repair program, and we understand that initial activities have begun.
i We and our consultants plan to review very carefully the detailed 2
implementation of that repair program, including tne quality control, inspection and test procedures employed by General Electric Company. We plan to submit, in the form of an amendment to the Oyster Creek operating
! license application, the detailed report submitted by General Electric Company.
2 /,2 f f Sincerely,
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'i" 9004080102 690106 iN PDR ADOCK 05000219 (f g. ,
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G H] E RfL kj E LE CTRIC NUCLE A R ENERGY C D M P A il Y DIVISION 175 CURTNER AVE.. SAN JOSE, CAUF. 95125 . . AREA CODE 408, TEL 297-3000. TWX No. 910 338-0116 February 2, 1968 RAII-63-105
,. l [h Jersey Central Project: Req. 303-91700 ,N
Subject:
Oyster Creek Reactor Vessel Repair Program
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Mr. G. H. Ritter, Vice President i/
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Jersey Central Power & Light Company '
x /W Madison Avenue at Punch Bowl Road N". N
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Dear Mr. Ritter:
General Electric investigation of the Oyster Creek reactor vessel probica has now developed to a point where we have completed the evaluation phases and are embarking on actual repair activities based upon the findings from such earlier activity. Our investigations conclude that the problem is, in fact, in the nature of that stated in earlier reports to you; namely, chemical activation of the surface of sensitized stainless steel stub tube caterial contained generally within high stress areas of the stub tube, the presence.of defect containing field welds between the stub tubes and control rod housings, and minor defects contained within the welds between several of the in-core instru-cent tubes and the vessel.
Investinations Careful and extensive exanination of all areas of the reactor vessel have been carried out using liquid dye penetrant, ultrasonic and visual techniques. The scope and result of these exaninations are summarized as follows:
- 1. Performance of carefully controlled dye penetrant examinations have revealed localized intergranular cracking in 123 stub tubes at the point of maximun stress, which is adjacent to the ' shop weld betueen the pressure vessel vall and the stub tube. Preliminary tests re-ported in Amend ent 29 identified crack indications in 108 stub tubes at this location; the additional indications were minor in nature and were located near the center of the vessel where inspection is difficult and were of the type previously detected and reported.
- 2. Indications of shallow linear and non-linear rounded type defects have been found on the surfaces of 43 stub tubes by careful dye penetrant examination. These indications do not correlate with stress profiles, do reveal grain boundary attack, penetrate to a 5/32 inch depth in the maximum case and are extremely fine.
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2- February!2, 1968
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- 3. The field welds joining the stub tube and the control rod drive housings have been thoroughly surveyed using both dye penetrant and ultrasonic techniques. These studies indicate some level of defect--either porosity or localized lack of complete fusion--in each of the 137 field welds.
, 4. While not a major problem, slag inclusions were detected in a number ., ,
of the welds attaching the flux monitor tubos to the reactor vessel bottom head through dye penetrant examinations and probe-grinding operations, i~ 5. Subsequent to investigation of the aforementioned probica areas in the reactor vessel, further investigation of highly streuced areas or locations in which contaminants could potentially collect uere initiated.
These arcas, which included recirculation suction piping, instrument nozzles, head spray welds, and various n'rcas in the shroud support cone
, to the vessel welds, displayed no indications of defec.ts througn dyc penetrant and ultrasonic examinations with the exception of three (3) ,
minor surface indications located on internal surfaces of the vessel recirculation suction nozzic transition wcld which were removed by shallow surface grinding. No defects were found in any other arcas of the reactor vessel, with the exception of some minor localized wcld lap 3 indications at the intersection of the stub tubo shop wcld and the j cladding which will be removed. >
Evaluations Based upon the facts set forth above, intensive' evaluation of the reactor vessel defect problem was initiated by General Electric, 1ts technical consultants, and Combustion Engineering, the reactor vessel supplier. These evaluations were broken down into specific functional phases aimed at investigation of metallurgical factors and perforuance of chemical and design analyses.
In the area of metallurgy, physical samples were taken from representative reactor ,
vessel stub tube shop welds, stub tubes proper, and field welds. These sampics were taken in locations indicating major defects, as well as locations which were expected to be representative of general stub tube conditions. Metallography relating to these samples was evaluated by both General Electric and Combustion-Engineering and their respective consultants. Results of this metallography indicated the presence'of intergranular attack of the stub tube areas both a djacent to the shop wcld locations and in localized arcas of the stub tubes proper.. Metallography of the field welds which join the stub tube to drive
-housings showed indication of lack of complete fusion and, in some cases, porosity within the wcld proper.
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G E N E R A L ih) E LE CTRIC l I
Mr. G. H. Ritter- February 2, 1968 l
The preliminary evaluation set forth in Amendment 29 which indicated that the subject problem appeared to be a combination of problems associated with welding of the field welds and stress assisted corrosion of the stub tubes has been
, fully verified by studies and evaluations conducted since issuance of the Amendment. A comprehensive survey has been conducted of the environment to which the vessel was subjected during its fabrication and field installation history. Although it has not been possible to establish a specific corrodant responsible for the problem, several chemicals which potentially have been in contact with the reactor vessel have been evaluated. Among these were those associated with shop fabrication operations, both shop and field hydrostatic testing, and field assembly and cleaning activities.
In order to evaluate as effectively as possible the potential chemical contamin-ants associa'ted with the observed intergranular attack of the vessel stub tube material, control samples were taken of liquids collected in various local areas of the reactor vessel, as well as samples of the chemical solutions utilized in reactor vessel cleaning operations. Investigation was also made of materials utilized during shop fabrication operations and other environments to which the vessel was subjected throughout both its shop and on-site life.
Samples exposed to chemical c1 caning solutions comparable to those actually utilized at Oyster Creek displayed sc0 evidence of, intergranular attack af ter a period of 160 hours0.00185 days <br />0.0444 hours <br />2.645503e-4 weeks <br />6.088e-5 months <br /> at a temperature of 180*F.
All samples tested indicated freedom from attack with the exception of those sensitized 304 stainless steel material samples stressed above yield and sub-jected to aqueous solutions containing chlorides as lou as ten parts per million E^'*[
at a temperature of 180*F. Such cracking was incurred in laboratory samples after exposure to the above conditions for forty-eight hours.
A careful evaluation of: stress profiler, has been conducted by General Electric, Combustion Engineering, and the Teledyne Corporation. In general, these evaluations conclude that:
- 1. The highest operating tensile stresses occur in the cold pressurized condition.
- 2. The stresses tend to be compressive in nature at the hot operating condition.
The shop weld between the stub tube and the vessel head included weld metal in excess of that required by design. Experience and measurements of the distortion indicate that the field weld between the stub tube and the CRD. housing applied fabrication induced strains which exceed the elastic' limit of the material on the " free" length of the " hill side" on the outer. rows of the stub tubes. ,
Experience also indicates that increasing the " free" length of the stub tube-will reduce the fabrication strains. . As a result of this conclusion, excess weld metal will be removed in selected areas. .
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GEllERAL$ ECTRIC Mr. G. H. Ritter February 2,1968 Repair Action Based upon the investigative and evaluation actions set forth above, decisions have been made to effect repair of the Oyster Creek reactor vessel as follows:
- 1. The stress-assisted intergranular cracks in the stub tube at the shop weld to stub tube juncture have been removed by grinding. Even though stress analyses indicate that only those ground configurations which exceed 3/16 inch in depth require deposition of weld metal, all ground configurations will be restored with 308L weld metal.
- 2. The fine cracks observed in the stub surfaces have been removed, lloweve r ,
these cracks are extremely fine in many cases and it is not possible to guarantee that all such cracks have been removed. While remote, it is '
also possible that remaining undetected cracks could bear a corrodant which in time could further propagate. To provide insurance against ,
this remote eventuality, stub tube surfaces will be clad with a 308L weld metal overlay. This material is significantly more resistant than sensitized 304 stainless steel to stress-assisted corrosion attack.
- 3. As stated previously, the tensile strains resulting from fabrication or the cold pressurized condition are reduced as the " free" length of the stub tube is increased. The shop welds will be contour-machined to provide a minimum of 1/2 inch between the top of the shop weld and ]
the bottom of the field weld.
4 .' Some level of defect, porosity or lack of complete fusion, is indicated in the field welds through the combination of dye penetrant and ultrasonic testing methods. It is difficult to establish with assurance the real significance of these findings in each instance. In the interest of (
advancing the Oyster Creek program, all field welds attaching the thimble to.the stub tubes will be removed and replaced.
- 5. Slag ' inclusions in the flux monitor guide tube welds will be removed and the welds repaired with application of Inco 182 weld material.
In the composite, this program of modification and repair consistently, we believe, reflects a conservative opproach to the integrity of the Oyster Creek pressure vessel and fully restores the pressure vessel to at least the )
original design and design intent. I We are initiating immediately the aforementioned repair action at Oyster Creek excepting those tuo specific stub tube locations which the Coc ,1ssion previously requested be retained in their original state. At an appropriate time when the repair schedule demands, these two stub tubes will also be repaired.
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Mr. C. II. Rit te r February 2, 1)68 Preparation of procedures and plans in support of this program is nearing l completion. These procedures and plans, as developed, will be available for k, review with AEC Compliance personnel on site as the work progresses. t!e will further provide to the Ccamission and to the ACRS a final report in detail of the information supplied above. This report will be filed with the Co:maission in the form of an amendment to the Oyster Creek operating license application.
Sincerely, R. A.c~ . k\~O )-
Huggins Principal Project Engineer Oyster Creek Project RAH:sa i
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