IR 05000412/1987059

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Insp Rept 50-412/87-59 on 870908-11.No Violations Noted. Majors Areas Inspected:Startup Test Program Review & Power Ascension Test Witnessing
ML20236A142
Person / Time
Site: Beaver Valley
Issue date: 10/08/1987
From: Eapen P, Wen P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20236A137 List:
References
50-412-87-59, NUDOCS 8710220064
Download: ML20236A142 (4)


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U.S. NUCLEAR REGUUJORY: COMMISS7.ON REGION Iu e

Report No~.

50-412/87-59 Docket'No.

50-412 License No.

NPF-73'

Licensee:

Duquesne Light Company Post Office Box 4 Shippingport, Pennsylvania-15077

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Facility Name:

' Beaver Valley Unit'No. 2

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Inspection At:

-Shippingport, Pennsylvania'

Inspection Conducted:

LSeptember 8-11, 1987 Inspector:

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/0/8/87 P.-C. Wen, Reactor Engineer, Special Test

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Pr grams Sec on EB, DRS M

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j Approved f~-67

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v r Dr. P. K. Eapen,~ Chid (/ Special Test

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Programs Section,'EB, DRS-l l

Inspection Summary:

Inspection on September 8-11, 1987 (Inspection Report No. 50-412/87-59)

l Areas Inspected: Startup Test Program review and Power. Ascension Test Witnessing.

Results: No violations were identified.

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DETAILS.

1.0' Persons Contacted Duquesne Light Company

  • J. Godleski, TCT Engineer
  • D. Hunkele, Director, QA Operations
  • J. Johns, Supervisor, QA Surveillance T. F. McGourty, Principle Engineer
  • T. P. Noonan, Assistant Plant Manager
  • R. G. Williams, Principle Engineer
  • G. Zosack, Compliance engineer j

T. G. Zyra, Director, Site Test and Plant Performance l

U.S. Nuclear Regulatory Commission

  • J. Beali, Senior Resident Inspector L. Prividy, Resident Inspector The inspector also contacted other administrative and technical licensee personnel during the course of the inspection.
  • Denotes those present at the exit meeting held on September 11, 1987.

2.0 Power Ascension Testing

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2.1 Startup Test Program i

The licensee performed two major transient tests (Main Steam l

Isolation Valve Closure Test and Loss of Power Test) during this

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inspection period (September 8-11, 1987). After completing

startup testing through 50% power plateau, the un.it was shut down on September 11, 1987 for a planned mini maintenance outage, i

The Load Rejection Test (IST-2.04.06) at 50% power level was deleted.

Instead, a 10% load swing test was performed at'50% power.

This test change was approved by the Joint Test Group (JTG) and Onsite Safety Committee (OSC). Additionally, load rejection test at 50%

power level is not one of the regulatory positions in Regulatory Guide 1.68.

The inspector had no questions.

2.2 Test Witnessing

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The inspector witnessed entire portions of the tests described below.

These tests were observed against the attributes identified in Inspection Report 50-412/87-55, section 2.2.

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f Main Steam Isolation Valve (MSIV) Closure Test (IST-2.21A.02)

This test was performed on September 9, 1987 at 30%' power level by)

simultaneous 1y' closing all.3 MSIVs.. -Upon MSIVs closure,- the: steam-generator levels shrunk from. normal (~41%) to' low-low. level, and

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caused reactor trip. The actions'of the control room operators-following the reactor trip.were:in accordance'with established:

procedures.

The MSIVs.were. reopen to restore the normal path of'

decay heat removal; the unit was' stabilized shortly'in.accordance with plant. procedure.

Preliminary test.results indicated that;all MSIV closure times met the test acceptance criteria-(5 seconds /from

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the time the valve received the signal to the time:the valve' fully closed). However,:the feedwater' flow and_the associated steam.

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generator level control did not respond. adequately.

The licensee and

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reactor vendor were evaluating' the: test results.

The inspector:wil1<

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l-follow this in a future inspection.

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l Loss of Power Test (IST-2.04.03)

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On September 9, 1987 with the reactor at approximately 30%, the.

i licensee performed a loss of. power test.in accordance with test-procedure IST-2.04.03, " Verification of Plant Performance.Following a Turbine Trip Coincident with'a Los of Offsite Power ~at Load." 'The l

inspector observed the test briefing between the test. engineers and-

operations personnel' prior to the conduct.of the test.

The' test-

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briefing was thorough and comprehensive..The' inspector 'also verified '

that the required prerequisites'had been completed.

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Prior to the test, auxiliary electrical load was being supplied by Unit Station Service Transformers TR-2C and TR-20.

The-test'was initiated by manually tripping the turbine generator. 'The emergency diesel generators, loading sequence, and plant system's responded as designed. As part of the test, electric power to the 'RCPs'was -

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removed and the plant went into-natural circulation.

During t_his

test the performance of the Turbine-Driven Auxiliary Feedwater Pump

was also verified.

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Preliminary results indicated that the plant responded as designed following the turbine trip with no offsite power. However, such l

equipment problems as the malfunction of the plant paging. system were

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identified. The licensee is currently evaluating test results.. The.

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inspector will follow this in a future ' inspection.

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i Summary The licensee conducted these transient tests in accordance with approved test procedures by highly qualified test personnel. These tests met the test objectives.

No unacceptable conditions were identified.'

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3.0 Independent Verification

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During the loss of power test, the inspector independently verified the l

plant response.

For' example, the inspector assured that the reactor-

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entered natural circulation by observing that (1) there was ~approximately.

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19 F - ' difference between T and T temperatures (2) T and incore hot cold hot q

thermocouple temperatures were tracking closely and (3) there was i

sufficient subcooling within the reactor.

4.0 QA/QC Interface j

i The licensee QA Surveillance Group continuously provided test coverage

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for the startup test program. During this ' inspection-period, the

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I inspector noted that QA personnel were actively following startup pro--

gram tests. Appropriate surveillance ' reports WEre issued.

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No unacceptable conditions were identified.

l 5.0 Exit Meeting

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An exit meeting was held on September 11, 1987 to discuss the inspection scope and findings, as detailed in this report (see paragraph 1.0 for attendees).

l At no time during this inspection was written material provided to the i

licensee.

Based on the NRC Region I review of this report and discus-

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sions held with the licensee representatives'at the exit, it was I

determined that this report does not contain information subject to 10 CFR 2.790 restrictions.

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