ML20057E833

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Insp Repts 50-334/93-21 & 50-412/93-22 on 930824-0927. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance,Engineering,Plant Support & Safety Assessment/Quality Verification
ML20057E833
Person / Time
Site: Beaver Valley
Issue date: 09/30/1993
From: Lazarus W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20057E829 List:
References
50-334-93-21, 50-412-93-22, NUDOCS 9310130212
Download: ML20057E833 (21)


See also: IR 05000334/1993021

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U. S. NUCLEAR REGULATORY. COMMISSION

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REGION I -

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Report Nos.

93-21

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93-22

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Docket Nos.

50-334

50-412

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License Nos.

DPR-66

NPF-73

Licensee:

.;Duquesne Light Company _

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One Oxford Center

301 Grant Street

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Pittsburgh, PA 15279

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Facility:

Beaver Valley Power Station, Units 1 and 2

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Location:

Shippingport, Pennsylvania-

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Inspection Period:

August 24 - September 27,1993

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Inspectors:

Lawrence W.~ Rossbach, Senior Resident Inspector L

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Peter P. Sena, Resident Inspector

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Scot- A. Greenlee, Resident Inspector

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. Richard A. Rasmussen, Reactor Engineer, RI

Gordon E. Edison, Project Manager,' NRR

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Approved by:

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W'%rdfhief, Reactor Projects Section 3B

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Inspection Summary

This inspection report documents the safety inspections conducted during day and backshift

hours of station activities in the areas of: plant operations; maintenance and surveillance;

engineering; plant support; and safety assessment / quality verification.

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9310130212 931001

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EXECUTIVE SUMMARY

Beaver Valley Power Station

Report Nos. 50-334/93-21 & 50-412/93-22

Plant Ooerations

Operators at Unit 2 completed a plant shutdown to mode 5, for the unit's fourth refueling

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outage, in a professional, competent, and safe manner. Two weaknesses were noted in plant

procedures during the shutdown.

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The licensee's scheduled Unit 2 motor operated valve testing, which would have placed one

of the emergency diesel generators out of service just prior to the refueling outage without

verifying a net safety benent. Upon further discussion with the NRC and internal review,

the licensee rescheduled the testing to the outage.

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Maintenance

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Good job site performance and oversight were observed during maintenance activities.

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Performance during all observed surveillance activities was satisfactory. On two occasions,

spurious alarms were received at Unit 2 when instrumentation and control test equipment was

installed in the plant. The licensee determined that the cause was a combination of test

equipment design and installation technique. Adequate corrective actions were taken to

prevent recurrence.

Non-outage maintenance backlog was reviewed and found to be appropriately prioritized and

managed by the licensee.

The licensee failed to perform 18 month calibrations on four gaseous effluent process flow

rate monitors. The failure to perform the calibrations is a violation (50-412/93-22-01) of

technical specifications. The cause of the violation appeared to be an inadequate tracking

system for calibration due dates.

Engineering

The licensee demonstrated excellent initiative, and good technical insight during the

investigation and resolution of two generic issues: (1) gas accumulation in the Unit I low

head safety injection piping; and (2) the possibility of high head safety injection pump run-

out during the transfer from cold leg to hot leg recirculation following a large break loss of

coolant accident.

Station modification procedures were generally found to be of good quality, except in the

case of design equivalent changes. Design equivalent change procedures were not covered in

sufficient detail.

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Executive Summary

A review of the 10 CFR 50.59 process showed that the 10 CFR 50.59 evaluations were

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thorough and indicated that the licensee was committed to the process.

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Plant Sunnort

Fifteen temporary fire seals were found in the Unit I charging pump cubicles. The seals

were installed in 1989, and were not controlled by the licensee's temporary modification

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program. The seals were evaluated as satisfactory and will be replaced with permanent seals

during the next refueling outage.

Chemistry support and corrective actions were good for a high gas concentration in the

Unit I reactor coolant system.

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TABLE OF CONTENTS

EXECUTIVE SUMMARY

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TABLE OF CONTENTS

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1.0

MAJOR FACILITY ACTIVITIES

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2.0

PLANT OPERATIONS (71707, 71710) . . . . . . . . . . . . . . . . . . . . . . . . . .

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2.1

Operational Safety Verification . . . . . . . . . . . . . . . . . . . . . . . . . . .

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2.2

Safety System Walkdowns . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

2.3

Unit 2 Pre-Outage Emergency Diesel Generator (EDG) Maintenance.

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2.4

Unit 2 Diesel Air Start Piping Configuration . . . . . . . . . . . . . . . . . . . 3

2.5

Unit 2 Shutdown for Refueling . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

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3.0

M AINTENANCE (62703, 61726, 71707)

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3.1

Maintenance Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

3.1.1 Inoperable Unit 1 Control Rod Assemblies

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3.2

Surveillance Observations

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3.3

Spurious Alarms During Surveillance Testing . . . . . . . . . . . . . . . . . . 7

3.4

Maintenance Backlog and Inoperable Unit 2 Velocity Probes

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4.0

ENGINEERING (37001, 90712, 92700, 71707, 92702)

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4.1

Review of Written Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

4.2

Gas Accumulation in the Unit 1 Low Head Safety Injection Piping . . . .

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4.3

10 CFR Part 21 Notification . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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4.4

(Closed) Violation (412/92-07-01) Diesel Sequencer Relay Failures . . . .

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(Closed) Violation (412/93-09-03) Missing Pipe Support Brackets . . . . .

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4.6

Review of Beaver Valley 10 CFR 50.59 Process

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5.0

PLANT SUPPORT (71707)

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5.1

Radiological Controls .

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Security . . . . . . . . . . . . . .

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5.3

Housekeeping . . . . . . . . . . . .

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5.4

Unit 1 High RCS Gas Concentration . . . . . . . . . . . . . . . . . . . . . . .

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6.0

ADMI NISTR ATI V E . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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6.1

Preliminary inspection Findings Exit

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6.2

Attendance at Exit Meetings Conducted by Region-Based Inspectors

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6.3

NRC Staff Activities

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DETAILS

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1.0

MAJOR FACILITY ACTIVITIES

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Unit 1 operated at full power throughout this inspection period without any significant

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operational events.

Unit 2 operated at full power from the beginning of this inspection period until August 29

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when end oflife coast-down began. The licensee reduced power to 75% on September 3 and

to 65% on September 10 as part of the coast-down, and to enable pre-outage maintenance on

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various secondary components. Unit 2 was shut down on September 17, as previously

scheduled, to begin the unit's fourth refueling outage. Mode 5 (cold shutdown) was entered

on September 19.

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PLANT OPERATIONS (71707,71710)

2.1

Operational Safety Verification

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Using applicable drawings and check-offlists, the inspectors independently verified safety

system operability by performing control panel and field walkdowns of the following

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systems: river water, diesel starting air, and residual heat removal. These systems were

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properly aligned; however, a difference was noted between the Unit 2 diesel starting air

system configuration and the system prints. This is discussed in more detail in Section 2.4

of this report. The inspectors observed plant operation and verified that the plant was

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operated in accordance with licensee procedures and regulatory requirements. Regular tours

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were conducted of the following plant areas:

Control Room

Safeguards Areas

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Auxiliary Buildings

Service Buildings

Switchgear Areas

Turbine Buildings

Access Control Points

Intake Structure

Protected Areas

Yard Areas

Spent Fuel Buildings

Containment Penetration Areas

Diesel Generator Buildings

Containment Building

During the course of the inspection, discussions were conducted with operators concerning

knowledge of recent changes to procedures, faciUty configuration, and plant conditions. The

inspectors verified adherence to approved procedur:s for ongoing activities obsen'ed. Shift

turnovers were witnessed and staffing requirements confirmed. The inspectors found that

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control room access was properly controlled and a professional atmosphere was maintained,

Inspectors' comments or questions resulting from these reviews were resolved by licensee

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personnel.

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Control room instruments and plant computer indications were observed for correlation

between channels and for conformance with technical specification (TS) requirements.

Operability of engineered safety features, other safety related systems, and onsite and offsite

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power sources were verified. The inspectors observed various alarm conditions and

confirmed that operator response was in accordance with plant operating procedures.

Compliance with TS and implementation of appropriate action statements for equipment out

of service was inspected. Logs and records were reviewed to determine if entries were

accurate and identined equipment status or de0ciencies. These records included operating

logs, turnover sheets, system safety tags, and the jumper and lifted lead book. The

inspectors also examined the condition of various fire protection, meteorological, and seismic

monitoring systems.

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2.2

Safety System Walkdowns

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The operability of the Unit I high head safety injection (HHSI) system and the Unit 2 low

head safety injection (LHSI) system was verified by performing detailed walkdowns of the

accessible portions of the systems. The inspectors conGrmed that system components were

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in the required alignment, hangers and supports are made up properly, instrumentation was

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valved in with appropriate calibration dates, as built prints reDected the as-installed system,

essential support systems were operational, and the overall material condition was

satisfactory. Specific observations are discussed below.

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Unit i HHSI

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The accessible portions of the HHSI inspected included suctions from the refueling

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water storage tank, LHSI, and emergency boration and charging pump discharge to

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the hot legs and cold legs (via the baron injection tank). No major discrepancies

were identiGed. Minor housekeeping items and valve leakage deficiencies were

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turned over to licensee personnel for resolution.

The inspector identified a 250 mR/hr hot spot (on contact) adjacent to CH-148

(charging pump IC suction isolation from LHSI). The dose rate was less than 100

mR/hr from a distance of 18 inches. This hot spot was not present one week earlier

as indicated by the licensee's last survey map of this area. Health physics toscrael

subsequently initiated proper action to adequately post this area. Follow-up surveys

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by health physics personnel in all three charging pump cubicles did not identify any

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other new radiation hot spots.

The inspector identified 15 temporary Ere seals in the charging pump cubicles (pump

suction and discharge piping penetrations). These temporary seals were installed in

1989, but were not included in the quality services unit's recently developed periodic

inspection program for temporary seals, nor were these seals controlled via the

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licensee's temporary modification program because the work orders were closed.

These seals were subsequently inspected and evaluated by engineering as being

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satisfactory. Maintenance work requests have been initiated to replaced the temporary

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seals with permanent Gre seals during the next refueling outage. The inspectors were

satisfied with the licensee's actions.

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Unit 2 LHSI

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No significant discrepancies were found. Several minor de6ciencies were turned over

to the licensee for resolution.

2.3

Unit 2 Pre-Optage Emergency Diesel Generator (EDG) Maintenance.

Duquesne Light Company scheduled motor operated valve testing on one of the Unit 2 EDG

service water valves prior to the unit's fourth refueling outage. The testing would have

required the licensee to enter a 72-hour shutdown technical specification action statement.

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This would have been necessary because all service water would have been isolated from the

EDG in order to test the valve.

The inspectors asked Duquesne Light Company to explain the safety benefit associated with

doing the testing prior to the outage. The licensee explained that they wanted to perform the

test prior to the outage primarily because of outage scheduling conflicts. Duquesne Light

Company was reminded of the NRC's position that performance of preventive maintenance

on-line, rather than during shutdown, should improve safety by making equipment more

reliable, and should be warranted by operational necessity, not just by the convenience of

shortening a refueling outage. Moreover, the licensee should be able to justify such an

expectation of improved safety. Duquesne Light Company subsequently rescheduled the

testing to the refueling outage.

2.4

Unit 2 Diesel Air Start Piping Configuration

During a routine walkdown of the Unit 2 diesel air start system, the inspectors determined

that the system configuration was not as shown on the system diagram, and not as described

in the plant operating manual. The difference involved piping which supplies air to boost the

fuel racks during diesel startup. During a normal diesel start, air pressure boosts open the

fuel racks to provide adequate fuel for starting. The Beaver Valley system diagram shows

that air for the fuel rack boost is supplied from a point just downstream of the main air start

valves. The actual con 6guration is such that the air comes from downstream of the air start

solenoid valves. The air start solenoid valves supply air which opens the main air start

valves on diesel start signal.

This difference in con 6guration only has implications in the event of a local manual start. If

the diesel fails to start because the air start solenoid valves will not open (e.g., during a loss

of 125 V d.c. control power), the operators are trained to start the unit manually, by opening

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one of the main air start valves. The system print configuration showed that the fuel racks

would get boost air if a main air start valve was opened manually. The actual configuration

would not allow for boost air on a manual start.

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The licensee contacted the diesel vendor (Colt) about the diesel air start piping configuration.

The licensee was told that the piping design configuration was changed back in the late 1970s

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because of overspeed concerns, and was delivered to the site that way. The vendor also

stated that the governor should build up enough oil pressure to open the fuel racks on a

manual diesel start; however, the start would be slower than a start with boost air.

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Duquesne Light Company is going to change their documentation to reflect the current air

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start piping configuration.

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2.5

Unit 2 Shutdown for Refueling

On September 17, 1993, Dnquesne Light Company started a Unit 2 shutdown for the plant's

fourth refueling outage. Th; shutdown started from approximately 65 percent power at

7:10 p.m. The unit entered Mode 5 at approximately 12:35 a.m. on September 19.

The inspectors observed a significant part of the plant shutdown and cooldown. The

operators completed the rea; tor plant mode changes in a professional, competent and safe

manner. This included hardling several minor problems, such as a failed source range

nuclear instrument, a feedv ater regulating valve which did not fully close, and a blocked

residual heat removal system sample line. The nuclear shift foreman also noted a problem

with Abnormal Operating Procedure (AOP) 2.2.1, " Nuclear Instrumentation Malfunction."

The AOP was not consistent with the technical specification actions for a failed source range

nuclear instrument channel. The Operations Manager initiated actions to resolve the AOP

deficiency.

3.0

M AINTENANCE (62703, 61726, 71707)

3.1

Maintenance Observations

The inspectors observed and reviewed selected maintenance activities to assure that: the

activity did not violate Technical Specification Limiting Conditions for Operation and that

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redundant components were operable; required approvals and releases had been obtained

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prior to commencing work; procedures used for the task were adequate and work was within

the skills of the trade; activities were accomplished by qualified personnel; radiological and

fire prevention controls were adequate and implemented; QC hold points were established

where required and observed; and equipment was properly tested and returned to service.

The maintenance work requests (MWRs) and preventive maintenance procedures (PMPs)

listed below were reviewed. The observed activities were properly conducted without any

notable deficiencies unless otherwise indicated.

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MWR 022427

In-plant Computer Input Verification

MWR 023095

Rod Control Troubleshooting (see Section 3.1.1)

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MWR 011732

Charging Pump (CH-P-1B) Alignment

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PMP 018526

Charging Pump (CH-P-1 A) Bearing Inspection

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During the 'A' charging pump inboard bearing inspection, the bearing clearances were found

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to be out of speci6 cation (>.006 inches) using plastigage measurement. Subsequent

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micrometer readings of the bearing sleeve inner diameter and shaft outer diameter were

within specification. Thorough action was initiated by maintenance supervision to resolve

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this discrepancy. This included coctacting the vendor for additional guidance, performing a

blue check of the bearing sleeve seating surface, and plastigage measurements between the

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bearing housing and bearing sleeve. The bearing was subsequently replaced and tested

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satisfactorily. The inspector also noted proper foreign material exclusion controls practiced

by the workers. During the 'B' charging pump alignment, good on-site job support and

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oversight were provided by the maintenance foreman. This exacting process was

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methodically completed by the workers and resulted in a satisfactory vertical and horizontal

alignment.

MWR 020395

Replace low Head Safety Injection (LHSI) Pump P21 A Inboard and

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Outboard Seals

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The inspectors noted good job site performance and supervision during the replacement of

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the LHSI pump mechanical seals. Quality control and radiological controls coverage were

also good. Some minor problems were noted with the seal replacement procedure

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(2 CMP-llSIS-P-21 A-B-lM, " Low Head Safety Injection Pump Overhaul"). Some of the

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procedural steps and illustrations did not rc6cct the actual conGguration of the pump. The

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licensee identified and corrected most of the deficiencies by issuing a revision to the

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procedure prior to the start of the job. Another procedure deficiency, involving pump

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bearing configuration, was identified during the job, and was within the skill of the craft to

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work through using the technical manual. The licensee is pursuing a procedure change to

reflect the correct bearing con 6guration. The procedure was a product of the licensee's

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procedure upgrade process, but the quality was not typical of their upgraded maintenance

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procedures.

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3.1.1 Inoperable Unit 1 Control Rod Assemblies

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On September 18, 1993, during monthly control rod movement testing, two sets of rod banks

failed to move on demand. Speci6cally, shutdown bank 'A' (group 2) and control bank 'C'

(group 2) would not step in or out while in manual control. There was no indication of rod

movement by either the analog rod position indication or primary voltage changes. All other

rod banks tested satisfactorily. At the time of this incident, these eight rods were in the fully

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withdrawn position. At 12:45 p.m., the shift supervisor declared these rods inoperable and

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correctly applied Technical Speci6 cation 3.1.3.1. Per the technical specifications, it is

incumbent upon the plant to verify the trippability of the inoperable control rods within I

hour. If the trippability of the inoperable rods could not be veri 6ed, then emergency

boration would be required since the technical specification shutdown margin would not be

satis 6ed.

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Immediate assistance was provided by the instrumentation and controls (I&C) department for

troubleshooting of the rod control system. The inspectors observed these efforts and at 1:38

p.m., the I&C foreman identified a control system failure. The bank select in power cabinet

'2AC' was determined to be electrically stuck in the control bank 'A' position. Thus, when

either shutdown bank 'A' or control bank 'C' was selected by the reactor operator. control

bank 'A' rods would respond to the demand signals. The inspector concluded that the

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licensee's determination that the rods were trippable was appropriate. Multiplexing relay

MXR1 was replaced per MWR 023095 to allow for proper bank selection. The operability

of the rods was restored by 3:55 p.m. following successful surveillance testing. However,

on September 20, I&C personnel identified that power cabinet '2AC' had again incorrectly

selected control bank 'A'.

This identification was a result of I&C personnel attempting to

determine the root cause of MXR1 relay being electronically stuck. I&C identi6ed that a

signal conditioning card, which provides input to MXR1, had failed. This card has been

replaced and the rods returned to operable status. The licensee has shipped the failed card to

Westinghouse for further evaluation.

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Overall, the I&C foreman demonstrated excellent system knowledge and good

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troubleshooting efforts to diagnose the failure during the limited time constraints. These

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efforts by the I&C foreman in verifying the trippability of the rods is commendable, as it

averted the need for an emergency boration. Good follow-up action by the I&C director,'per

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root-cause analysis, resulted in the identi6 cation of the rods again being inoperable and the

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initiation of proper corrective action.

3.2

Surveillance Observations

The inspectors witnessed / reviewed selected surveillance tests to determine whether properly

approved procedures were in use, details were adequate, test instrumentation was properly

calibrated and used, technical specifications were satisfied, testing was performed by

qualified personnel, and test results satisfied acceptance criteria or were properly

dispositioned. The operational surveillance tests (OSTs) and Beaver Valley Tests (BVTs)

listed below were reviewed. The observed surveillance activities were properly conducted

without any notable deficiencies unless otherwise indicated.

l OST-7.2

Boric Acid Transfer Pump (1CH-P-28) Operational Test

IOST-7.5

Centrifugal Charging Pump (ICH-P-1B) Test

LOST-36.1

Diesel Generator No.1 Monthly Test

IOST-24.4

Turbine Driven Auxiliary Feed Pump Test (lFW-P-2)

During OST 24.4, the auxiliary feedwater (AFW) system engineer initiated the use of

visicorder instrumentation for enhanced monitoring of the turbine governor based on past

industry experience. The parameters specifically monitored are turbnx speed, governor

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valve position, and pump discharge pressure. The inspectors considered this a good practice

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to monitor governor performance and ensure high reliability. Also during this surveillance

test, the inspectors noted boric acid buildup on the piping Dange for auxiliary feedwater flow

transmitter FT-FW-100B. A boron concentration of between 5 and 10 ppm is maintained in

the steam generators. Although this concentration is minimal, deposits of boric acid crystals

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are highly concentrated and may be very corrosive for carbon steel. A deficiency tag was

previously hung to identify the leak and generate a work request. However, the boric acid

buildup was not identi6ed for prompt cleanup to minimize its corrosive effects.

IBVT 8.3.1

Incore Movable Detector Flux Mapping

The reactor engineers demonstrated excellent knowledge of the flux mapping procedure and

equipment. During the procedure, the 'C' incore detector acted erratically. The reactor

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engineers quickly identified the faulty incore detector. Maintenance personnel promptly

responded to check the accessible portion of the equipment. After a brief evaluation, the

reactor engineers decided to continue the map using another detector via the emergency path.

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The reactor engineers ensured the requirements of Technical Specification 3.3.3.2, regarding

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the maximum number of faulty detector thimbles, were met. The procedure was well written

with good use of prerequisites, precautions, contingencies and notes.

OST 2.24.2

Motor Driven Auxiliary Feed Pump 2FWE*P23A

2BVT 1.21.2

Trevitest Method for Main Steam Safety Valve Setpoint Check

2BVT 1.11.3

SI Accumulator Discharge Check Valves Full StroM Tat

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2OST1.1

Control Rod Assembly Partial Movement Test

2OST 2.11.1

Imw Head Safety injection Pump [2 SIS *P21 A] Test

2OST 2.36.15

4 kV and 480 V Emergency Bus Undervoltage Test

OST 2.42.2

Shutdown Margin Calculation

OST 2.2.3

Nuclear Source Range Channel Functional Test

3.3

Spurious Alarms During Surveillance Testing

On September 1 and 2,1993. Unit 2 operators received spurious alarms during

instrumentation and control equipment surveillance testing. The spurious alarms were not

functionally related to the equipment being tested. The licensee conducted an investigation

into the events. They found that the same individual was involved in both occurrences, and

the cause was a combination of test equipment design and installation technique. Some test

equipment connectors were configured such that they could easily short across the pins of the

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mating connector. Shorting across mating connector pins while installing the test equipment

caused the spurious alarms. The mating connectors are mounted on circuit cards which are

used only during testing.

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The licensee modified the test connectors to reduce the possibility of shorting the mating

connector pins during installation. Additionally, the events were discussed with all

instrumentation and control personnel who use the associated test equipment. The inspectors

concluded that there was no safety consequence associated with the two events, and the

licensee's actions in response to the events were appropriate.

3.4

Maintenance Backlog and Inoperable Unit 2 Velocity Probes

The inspectors reviewed the Unit 1 and Unit 2 non-outage maintenance backlog to ensure

that safety related maintenance activities were being appropriately prioritired and managed by

the licensee. The inspectors found that, overall, maintenance backlog management was

adequate. The inspectors did note a problem involving technical specification (TS) required

calibrations. A maintenance work request (MWR) was generated to calibrate two Unit 2

ventilation stack velocity probes. The velocity probes were used to measure process flow

rate from the condensate polishing building and waste gas storage vault ventilation systems.

The probes must be calibrated at least once every 18 months according to Technical Specification 4.3.3.10, " Radioactive Gaseous Effluent Monitoring Instrumentation

Surveillance Requirements." The MWR to calibrate the probes was more than 3 months old

at the time of the inspection, so the inspectors asked when the calibrations were due. The

licensee subsequently found that both probes were past due for calibration (including the 25

percent maximum extension allowed by TS 4.0.2). Condensate polishing building ventilation

probe was last calibrated on May 15, 1990; and, the waste gas storage vault ventilation probe

was last calibrated on June 6,1990. The licensee promptly declared the velocity probes out

of service, and commenced estimating process flow for the associated discharge paths every

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4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> as required by TS.

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The inspectors reviewed the circumstances associated with the licensee's failure to calibrate

the velocity probes. The inspectors found that the licensee did not have a formal system to

track ventilation system velocity probe calibration due dates. Additionally, some of the

personnel responsible for scheduling the calibrations thought the quarterly channel functional

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tests were meeting the 18-month calibration requirements.

The licensee looked at the calibration status for all velocity probes at Unit I and Unit 2.

They found the following additional problems:

(1)

The Unit 2 elevated release process flow rate monitor was past due for calibration

(last performed on March 30, 1989) from February 15, 1991, to April 20,1993.

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(2)

The Unit 2 plant ventilation system process flow rate monitor was past due for

calibration (last performed on April 1,1989) during the period from February 17,

,

1991, to April 30, 1993.

The failure to calibrate the four Unit 2 velocity probes as required by TS, without taking

appropriate compensatory measures, is considered a violation (50-412/93-22-01). Unit 2 has

a total of five ventilation system velocity probes which have TS requirements. Four of the

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probes were discussed above. The fifth probe is used for monitoring ventilation How from

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the decontamination building. This probe had not been calibrated since August 17, 1990;

however, the decontamination building ventilation fans had been on clearance since October

16, 1991. TS do not require the gaseous release monitoring systems to be operable if

process flow is not present.

The licensee was able to conservatively calculate releases via the four active release paths

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during the period when the flow rate monitors were past due for calibration. The licensee

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does not use the actual process flow rate in their calculations. Instead, they use the

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maximum achievtle flow rate for the system.

4.0

ENGINEERING (37001, 90712, 92700, 71707, 92702)

4.1

Review of Written Reports

1

The inspectors reviewed Licensee Event Reports (LERs) and other reports submitted to the

NRC to verify that the details of the events were clearly reported, including accuracy of the

description of cause and adequacy of corrective action. The inspectors determined whether

further information was required from the licensee, whether generic implications were

indicated, and whether the event warranted further onsite followup. The following LERs

were reviewed:

Unit 1:

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93-12 Plant Entry into Mode 2 with an inoperable Hydrogen Analyzer

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This event was discussed in NRC Inspection Report 93-16.

Unit 2:

93-08 Engineered Safety Feature Actuation Due to Loss of Emergency Response Facility

Substation

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This event was discussed in NRC Inspection Report 50-412/93-17.

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The above LERs were reviewed with respect to the requirements of 10 CFR 50.73 and the

guidance provided in NUREG 1022. Generally, the LERs were found to be of high quality

with good documentation of event analyses, root cause determinations, and corrective

actions.

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4.2

Gas Accumulation in the Unit 1 Low Head Safety injection Piping

The licensee had identified the presence of undissolved gas in the 'A' train low head safety

ujection (LHSI) piping. This identification was a result of the licensee's review of

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Information Notice 88-23, Supplement 4 (dated December 18,1992), " Potential for Gas

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Binding of High Pressure Safety injection Pumps During a Design Basis Accident." The

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information notice discussed the principle gas source as being from reactor coolant that leaks

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past the reactor coolant system cold leg check valves into the LHSI piping which

depressurizes and cools so that gases come out of the solution.

Ultrasonic examination of the LHSI piping identified about 2.2 cubic feet of gas in the

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recirculation mode transfer piping (i.e., charging pump suction from LHSI pumps). This

amount is minimal compared to the 108 cubic feet discussed in the information notice. .An

engineering evaluation concluded that these gases would not effect the operability of the high

head safety injection pumps. The gas void would be compressed by about 50 percent due to

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the discharge pressure of the LHSI pumps. An evaluation of the fluid dynamics of this

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two-phase flow concluded that the gas void would be broken down into smaller voids (less

than f inch in diameter) prior to entering the charging pump suction. The maximum

allowable gas void has been defined as 8.1 cubic feet based on the engineering evaluation.

The inspectors also reviewed the inservice testing results of the cold leg check valves

(SI-10, 11, 12, 23, 24, 25) and noted that all valves exhibited zero leakage on May 29,

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1993. Follow-up monitoring of the LHSI piping has not identified any increase in the size of

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the gas void. Thus, it is possible that the gac void may be due to an improper fill and vent

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of the LHSI piping following the recent refueling outage as opposed to check valve leakage.

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The licensee is appropriately planning to continue monitoring the gas void. Contingency

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plans are available to vent the piping if needed. Overall, engineering personnel initiated

proper action in response to the information notice. The engineering evaluation was

thorough and con e sufficient basis for its conclusions.

4.3

10 CFR Part 21 Notification

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On September 10,1993, the licensee notified the NRC of a 10 CFR Part 21 issue regarding

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a possible run-out condition of the charging pumps under a specific condition. Previously,

on July 14, Duquesne Light Company received a Westinghouse nuclear safety advisory letter

(NSAL 93-12) for evaluation of 10 CFR Part 21 applicability. For Unit 1, the licensec

determined that following a large break loss of coolant accident (LOCA), a rtm-out condition

of a single high head safety injection (HHSI) pump could occur during the transfer to hot leg

recirculation. Emergency operating procedure ES 1.4, transfer to simultaneous hot leg and

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cold leg recirculation, is entered 14.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after the LOCA. This procedure directs

operators to initiate hot leg injection from the HHSI pumps, isolate the boron injection tank,

then isolate cold let injection from the HHSI pumps. The low head safety injection (LHSI)

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pumps remain lined up to supply both the HHSI pumps and cold leg injection. If a loss of

train 'A' power is proposed as the single active failure, then the remaining 'B' HHSI pump

would be aligned for both hot leg and cold leg recirculation since the cold leg injection could

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not be isolated via its motor operated valve. Continued operation of the remaining HHSI

pump in this parallel flowpath will lead to pump run-out conditions. Manual operator action

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to locally close the affected motor operated valves is not taken credit for, since these valves

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would be in a high radiation area due to containment sump recirculation.

As corrective action to prevent this condition, the licensee has changed ES 1.4 to alert

operators not to establish hot leg injection if the boron tank cannot be isolated (i.e., no

power available to train 'A' isolation valves). Instead, operators are instructed to consult the

technical support center. However, hot leg injection is still necessary to elimi7 ate boron

precipitation in the reactor vessel and thus maintain long-term core cooling. Thus, long-term

corrective actions are under development to establish LHSI hot leg injection or throttle the

HHSI pump discharge valves to prevent run out during simultaneous hot leg and cold leg

injection. The Unit 1 Operations Manager has delineated the change to ES 1.4 in the night

order book and has required all operators to read and understand this procedure change.

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The 10 CFR Part 21 notification also stated that Unit 2 was susceptible to the same pump

run-out condition as Unit 1. This, however, was only a very remote possibility. The

emergency procedures at Unit 2 required the operators to secure the HHSI pumps prior to

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changing the valve lineup from cold leg to hot leg recirculation. The HHSI pumps would

then be restarted after the lineup change was complete. Consequently, the only way to

establish parallel injection paths with the HHSI pumps running, was to deviate from the

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emergency procedures. The Unit 2 emergency procedures were changed to give the

operators specific guidance for problems encountered while shifting from cold leg to hot

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recirculation (because of a loss of power to one train).

The inspectors were satisfied with the licensee's immediate corrective actions. Duquesne

Light Company was the first utility to report this 10 CFR Pan 21 concern to the NRC. This

action is indicative of the licensee's continued proactive approach toward review of generic

issues. The timeliness of the licensee's review was acceptable, as it was completed within

the 10 CFR Part 21 criteria.

4.4

(Closed) Violation (412/92-07-01) Diesel Sequencer Relay Failures

The licensee was issued a notice of violation on June 17, 1992, which involved the failure to

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establish adequate design control measures for verifying the adequacy of a vendor-

recommended change to emergency diesel sequencer relays. The vendor-recommended

change resulted in the application of excessive voltage across the sequencer circuitry and

subsequent relay failures. This change was different than the qualified design configuration.

The vendor, in this case. was not a 10 CFR 50, Appendix B vendor as the relays were

purchased as commercial grade items.

]

The inspector reviewed the adequacy and completeness of the licensee's long-term corrective

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action to prevent recurrence. The licensee has improved procedures on meeting

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documentation requirements where verbal input from vendors is used as the basis for any

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technical decision or modification. Engineering procedures for design change control,

engineering speci6 cations, and design verifications have been updated to include the

following:

Changes to vendor supplied designs should be evaluated to ensure that quali6 cation

testing is appropriate for the modified design, including commercial grade equipment

procured for Quality Assurance Category I applications.

Changes to vendor supplied designs made with the vendor's concurrence must be

documented with a confirmation letter sent to the vendor.

Training of engineering personnel on these issues has been completed.

The licensee also performed a review of design change packages involving Class lE

electrical equipment (of the last 5 years). No deviations from the qualified design

configuration were identified. Several deficiencies were, however, identified which involved

the lack of commercial-grade dedication or quality documentation. The scope of this review

was sufficient as evidenced by licensee identi6 cation of quality deficiencies. The noteworthy

examples involving commercial grade items installed in Class 1E equipment include:

two breakers which provide 480 V AC input to the four uninterruptible power supply

(UPS) units;

static switches which transfer 120 V AC vital bus power supplies between the normal

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(UPS) and the alternate supply (480/120 V AC voltage regulator); and

two 120 V AC vital bus breakers which supply both trains of the inadequate core

cooling instrumentation system.

4

The static switches have been replaced and design changes have been initiated to correct the

other deficiencies. The inspectors did note, however, ths.t a timely documented basis for

continued operability (BCO) was not prepared when these issues were Crst identified in

December 1992. Generic Letter 91-18 states that the licensee should make an operability

determination and take follow-up corrective action upon the discovery of non-conforming

conditions where the qualification of equipment is called into question. Furthermore, the

concepts of operability and restoration of qualification should be treated separately to ensure

that the operability determination is focused on safety and is not delayed by the decisions or

actions necessary to plan or implement the corrective action (i.e., restoring ful1

_

qualification). At the end of this report period, the formal BCO was being finalized. The

licensee's Manager of Nuclear Safety indicated that additional training would be conducted

on this concept to improve their applications of Generic Letter 91-18. Overall, the inspectors

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were satisfied with the licensee's corrective actions to prevent recurrence in response to the

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madequate design control measures. This violation is closed.

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4.5

(Closed) Violation (412/93-09-03) Missing Pipe Support Brackets

On May 25,1993, the licensee was issued a violation for inappropriate corrective actions

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associated with a missing pipe support bracket on the 21B high head safety injection pump

lube oil system. The licensee allowed the deDeient condition to exist from October 29,

1992, until April 15, 1993, when a similar condition was identified by the NRC.

The licensee concluded that the missing bracket was not corrected in a timely manner

because ofimproper coding of the maintenance work request (MWR), and failure by

personnel reviewing the MWR to identify the error. The deficiency was coded for a

miscellaneous system instead of the safety injection system. The licensee reviewed the MWR

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control program and concluded that adequate provisions were available to identify the

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improper coding, if the provisions were followed. Thus, the licensee's actions to prevent

recurrence were: (1) to reemphasize proper review of MWRs; and (2) to schedule training

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to reenforce the need for accurate identification and reporting of degraded and

nonconforming conditions.

The inspectors reviewed the licensee's non-outage maintenance backlog for evidence of other

improperly dispositioned deficiencies. No other instances were found. The inspectors

concluded that the licensee's corrective actions to prevent recurrence were adequate. This

violation is closed.

4.6

Review of Beaver Valley 10 CFR 50.59 Process

The licensee's procedures for controlling modifications at both units, the training records

related to training of their staff in the requirements of 10 CFR Part 50.59, logs of setpoint

changes and temporary modi 6 cations, and several modification packages including the

associated safety evaluations were reviewed.

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The licensee's station modi 6 cations are organized into three categories: design changes,

design equivalent changes, and administrative changes. Design changes include major

modifications, minor modi 6 cations, setpoint changes, temporary modiDeations and computer

system changes. Design equivalent changes are intended to include changes to structures,

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systems or components for which design requirements remain unchanged. Administrative

changes include UFSAR updates, technical specification changes, and other changes to

documents such as operating procedures, valve lists or administrative changes to drawings.

With the exception of design equivalent changes (DECs), all of these changes are controlled

with approved procedures which are generally of good quality. Some guidance for handling

DECs is included in Figure 6.4 of Nuclear Engineering Administrative Procedure 2.13,

whose stated purpose is to control the preparation and processing of technical evaluation

reports. However, there is no procedure to identify purpose, applicability, responsibilities,

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references, and to organize and detail restrictions, instructions and requirements for design

equivalent changes.

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The 10 CFR 50.59 training program was revamped in mid-1990 because of problems with

earlier 10 CFR 50.59 evaluations and resulting pressure from the Onsite Safety Committee

(OSC). This demonstrated good internal self-monitoring and a commitment to the 10 CFR 50.59 process. Training records indicated that about 150 persons rnaintained their 10 CFR 50.59 training current (within the past 2 years) and another 100 persons had completed initial

or partial training since mid 1990. All members of the engineering assurance group, which

performs most of the 10 CFR 50.59 evaluations for major modifications, had received

training within the past year. Two out of three persons who perform a similar function for

most tech spec changes also were current in their training. The licensee also stated that

Onsite Safety Committee (OSC) and Offsite Review Committee (ORC) managers involved in

10 CFR 50.59 program oversight and managers who oversee no significant hazards

evaluations received 10 CFR 50.59 training through the Technical Personnel Training

program.

Logs were being properly maintained in the control room for setpoint changes and for

temporary modifications (TMODs) including jumper connections and lifted leads. These logs

were found to be updated, reviewed on a quarterly basis, and the number of temporary

modifications is trended. A significant reduction in the number of outstanding TMODs

occurred during 1992 at both units.

The following operational surveillance test procedure changes, TMODs, and design change

packages were reviewed:

OST 1.39.l A, Rev 33,11/1/90,10 CFR Part 50.59 Evaluation, Unit 1, Weekly Station

Battery Check, Battery No.1.

TMOD l-90-026,3/10/88, Install Temporary Power Supply for Betz Equipment to Cooling

Tower (Unit 1).

TMOD l-90-017,4/13/89, Remove Internals from Check Valve AS-7 (Unit 1)

TMOD 2-90-31,6/2/88, Maintain on-line the Circulation Water Pumps During a Chilled

Water Low-Temperature Trip (Unit 2)

TMOD 2-90-53,2/10/89, Modification to the Unit 2 Control Building Ventilation Filters

DCP No.1546, Rev. O,1/14/91, Replacement of Station Air Compressors (Unit 1)

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DCP No.1377, Rev. O,5/13/90, Auxiliary Feedwater System Design Pressure Change

(Unit 2)

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The 10 CFR 50.59 evaluations were thorough and indicated the licensee is committed to the

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10 CFR 50.59 process.

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5.0

PLANT SUPPORT (71707)

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5.1

Radiological Controls

Posting and control of radiation and high radiation areas were inspected. Radiation work

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permit compliance and use of personnel monitoring devices were checked. ' Conditions of

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step-off pads, disposal of protective clothing, radiation control job coverage, area monitor

,

operability and calibration (portable and permanent), and personnel frisking were observed

!

on a sampling basis. Licensee personnel were observed to be properly implementing their

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radiological protection program.

5.2

Security

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Implementation of the physical security plan was observed in various plant areas with regard

to the following: protected area and vital area barriers were well maintained and not

compromised; isolation zones were clear; personnel and vehicles entering and packages being

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delivered to the protected area were properly searched and access control was in accordance

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with approved licensee procedures; persons granted access to the site were badged to indicate

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whether they have unescorted access or escorted authoriration; security access controls to

vital areas were maintained and persons in vital areas were authorized; security posts were

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adequately staffed and equipped, security personnel were alert and knowledgeable regarding

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position requirements, and that written procedures were available; and adequate illumination

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was maintained. Licensee personnel were observed to be properly implementing and

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following the Physical Security Plan.

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5.3

Ilousekeeping

Plant housekeeping controls were monitored, including control and storage of flammable

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material and other potential safety hazards. The inspectors conducted detailed walkdowns of

accessible areas of both Unit I and Unit 2. Housekeeping at both units was acceptable.

5.4

Unit 1 Iligh RCS Gas Concentration

On August 24,1993, routine chemistry sampling identined a high total gas concentration in

the reactor coolant system (RCS) in excess of 60 cc/kg. The gas was mainly comprised of

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dissolved hydrogen and possibly ammonia. The licensee maintains the specifications for

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dissolved hydrogen between 25 - 50 cc/kg. The upper limit is based on limiting primary

water stress corrosion cracking ofInconel 600 steam generator tubing. Degasification of the

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RCS was initiated per the recommendation of the chemistry staff. The RCS gas

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concentration was successfully reduced to 40.9 cc/kg following 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> of degasification.

Licensee investigation revealed that argon activity had doubled on August 24. This is an

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excellent indicator of air intrusion into the RCS. The licensee believes it is possible that air

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may have been introduced while returning the chemical volume and control system to service

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following maintenance. Mixed bed demineralizer CH-I-1 A was drained between August 8

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and 20 to allow for maintenance on isolation valve CH-9. Overall, the chemistry personnel

conducted a thorough investigation and initiated proper action to restore RCS gas

concentration to within specification.

6.0

ADMINISTRATIVE

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6.1

Preliminary Inspection Findings Exit

At periodic intervals during this inspection, meetings were held with senior plant

management to discuss licensee activities and inspector areas of concern. Following

conclusion of the report period, the resident inspector staff conducted an exit meeting on

September 28, 1993, with Beaver Valley management summarizing inspection activity and

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findings for this period.

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6.2

Attendance at Exit Meetings Conducted by Region-Based Inspectors

During this inspection period, the inspectors attended the following exit meetings:

Inspection

Reporting

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Dates

Subject

Report No.

Inspector

8/26/93

Unit 1 Licensed Operator Requal Exams 93-19

R. Temps

9/03/93

Station Blackout Rule Implementation

93-80/80

J. Trapp

9/10/93

Emergency Preparedness Program

93-20/20

L. Eckert

6.3

NRC Staff Activities

Inspections were conducted on both normal and backshift hours: 48.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of direct

inspection were conducted on backshift; 28.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> were conducted on deep backshift. The

times of backshift hours were adjusted weekly to assure randomness.

R. Barkanic, Pennsylvania Department of Environmental Resources, and T. Reeves, Ohio

Emergency Management Agency, visited the site and the inspectors on September 7 and 8 to

accompany the emergency preparedness program inspection.

G. Edison, Project Manager, Nuclear Reactor Regulation (NRR), visited the site and the

inspectors from August 23 to 27 to evaluate the licensce's 10 CFR 50.59 activities as

discussed in Section 4.6.

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Four East Europeans visited the inspectors to become familiar with the NRC inspection

program. Gyula Fichtinger, Atomic Energy Commission, Hungary, and Yordan Hari7anov,

Committee on Uses of Atomic Energy for Peaceful Purposes, Bulgaria, visited the inspectors

from August 23 to September 2. Milan Musak, State Office of Nuclear Safety, C7ech

Republic, and Miroslav Lipar, Nuclear Safety Authority, Slovak Republic, visited the

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inspectors from August 30 to September 2. The visitors toured the site and discussed the

inspection program with the inspectors. The visitors also accompanied the inspectors on

inspections 50-334/93-19,21, and 80 and also 50-412/93-22 and 80.

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