ML20058Q022
ML20058Q022 | |
Person / Time | |
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Site: | Beaver Valley |
Issue date: | 12/15/1993 |
From: | Durr J, James Trapp NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20058Q014 | List: |
References | |
50-412-93-81, NUDOCS 9312280038 | |
Download: ML20058Q022 (41) | |
See also: IR 05000412/1993081
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l f c.- . .. < * U. S. NUCLEAR REGULATORY COMMISSION :] REGION 1 ! AUGMENTED INSPECTION TEAM REPORT ' ' INSPECTION OF E ~ERGENCY DIESEL GENERATOR LOAD F- QUENCER FAILURES 1 . REPORT / DOCKET NOS. 50-412/93-81- -j .i - LICENSE NO. NPF-73 ] LICENSEE: Duquesne Light Company ) One Oxford Center ; 301 Grant Street 1 Pittsburgh, PA 15279 * FACILITY: Beaver Valley Unit 2 INSPECTION DATES: November 9-19,1993 , INSPECTORS: J. Calvert, Reactor Engineer, RI - ! S. Greenlee, Beaver Valley, Resident Inspector E. lee, Electrical Engineer, NRR .. R. Skokowski, Reactor Engineer, RI { ! TEAM LEADER: n.a Co IQ.- 11- 30 James hf/Trapp, Teani feader Date . Engineering Branch, DRS I APPROVED BY: MoA . iMJ J f acqup'. Durr, Chief N / Dat( ~ -l /,Engmeering Branch DRS- , .{ ! ! , i I ., i f ! , i i ; 931228003B 931221 l PDR ADDCK 05000412 i G- PDR. .! . - . 'l
. . EXECUTIVE SUMMARY ',
The scope of the Augmented Inspection Team (AIT) inspection was provided by the Region 1 Regional Administrator in the Augmented Inspection Team Charter. The team was tasked with conducting a detailed review of the circumstances surrounding the failure of both emergency diesel generator load sequencers during routine surveillance testing. Specifically, the team was tasked with developing a detailed sequence of events, evaluating the root cause determination, assessing the effectiveness of the corrective actions, and evaluating the safety significance of the event. The emergency diesel generator load sequencers automatically place vital safety-related equipment in service if normal power is lost to the emergency busses. Following restoration of power to the emergency busses by the emergency diesel generators, the load sequencer timer / relays are used to load safety-related equipment onto the emergency busses in discrete timed steps. The original load sequencers used electro-mechanical timer / relays to generate the timed steps. The electro-mechanical timer / relays were replaced with digital microprocessor based timer / relays during the second refueling outage, in November 1990. During the third refueling outage, in April 1992, routine surveillance tests identified three of the eight microprocessor timer / relays in each sequencer train had failed. The failures were caused by a modification made to the timer / relays that continuously energized the clock circuits. The root cause for the failures was inadequate design control. The NRC conducted an enforcement conference regarding this failure and issued a Severity Level III violation and - a Civil Penalty (NRC Inspection Reports 50-412/92-07 and 50-412/93-22). The failed timer / relays were replaced and the clock circuits were appropriately modified such that the microprocessor timer / relays were only energized during sequencer operation. On November 4,1993, during the performance of the Operating Surveillance Test 36.3, " Emergency Diesel Generator Automatic Test," the Train-A, 2-1 emergency diesel generator (EDG) load sequencer failed to automatically load safety-related equipment onto the emergency bus. Subsequent bench testing conducted with the suspect relays was not - successful in identifying the cause of the failure. An evaluation of the sequencer logic circuit by the licensee's engineering staff identified two relays, one in the sequencer circuit and one in the solid state protection system, whose malfunction had the potential to cause the symptoms observed during the surveillance test. Both suspect relays were replaced and the surveillance test was successfully repeated on November 5,1993. On November 6,1993, during the perforrnance of the Operating Smveillance Test 36.4,
Emergency Diesel Generator Automatic Test," the Train-B, 2-2 emergency diesel generator load sequencer failed to automatically load safety-related equipment onto the emergency bus. Diagnostic test equipment had been installed on the load sequencer and provided pertinent-
information on the failure mode. The cause of the sequencer failure was a failed safety injection reset microprocessor timer / relay (762EGSBA). This timer / relay resets the load
sequencer when a safety injection signal occurs during a loss of offsite power event. A
contact from this timer / relay failed to open, which caused the load sequencer to " lock-up" and fail to automatically load safety-related equipment onto the emergency bus.
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. The failure of both einergency diesel generator load sequencers would prevent automatic
initiation of the emergency core cooling system in the event of an accident with a loss of normal power. In the event that the load sequencers were to malfunction during an accident with a loss of normal power, manual operator actions, in accordance with the emergency operating procedures, would be required to mitigate the consequences of the event. , However, for some postulated accidents, manual operator actions might not have been adequate to satisfy the design criteria for the emergency core cooling systems. The team concluded that the common cause failure of multiple trains of a safety system required to - mitigate the consequences of an accident was a significant event. l The microprocessor operated timer / relays failed due to voltage spikes introduced through the timer / relay contacts. The voltage spikes were generated by the auxiliary relays that are controlled by the timer / relays. These spikes were generated when the electrical circuit to the coil of an auxiliary relay were opened, resulting in the generation of an " inductive kick," or voltage spike. The " lock-up" of the microprocessors resulted in the failure of the timcr' relays. The failure of the timer / relays caused the malfunction of the load sequencers. The exact failure mechanism internal to the microprocessors was not known at the conclusion of this inspection. . A modification of the emergency diesel generator sequencers was implemented to reduce the magnitude of the voltage spikes. The modification installed diodes around the auxiliary relays to reduce the magnitude of the voltage spikes. Nine voltage spike suppression diodes were installed in each emergency diesel generator load sequencer. The post modification testing identified a deficiency with the installation of the diodes. The installation of the diodes increased the drop-out time of the relays, which caused the auxiliary feedwater pump to start at the wrong sequence step. The auxiliary feedwater pump starting circuits and the sequencer logic circuits were modified to correct this problem. The team concluded that the modification that installed the microprocessor timer / relays was ' inadequate. The design control for the selection and review for suitability of the Automatic Timer and Controls Company (ATC) timer / relays for this application was not adequate. The modification design inputs should have identified the potential for voltage spiking by the ' auxiliary relays. This design input should then have been translated into the equipment specification and the dedication testing specification. The delay in auxiliary relay drop-out time caused an auxiliary feedwater pump to start at the wrong sequence step following the installation of the diodes. Further design changes were required to correct this problem. The team concluded that the implications of the installation of the diodes on relay tirning was ; not thoroughly evaluated. The team concluded that the actions taken to correct the auxiliary feedwater pump starting logic problem and :he installation of diodes to suppress voltage spikes were acceptable. j ! l iii l i i
. . TABLE OF CONTENTS * . Page : EXECUTIVE SUMMARY ...................................... ii 1.0 INSPECTION S COPE . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 , 2.0 DETAILED INSPECTION FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . 2 2.1 Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 2.2 Event Description . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 i 2.3 Safety Significance .................................. 4 2.4 Imad Sequencer Operation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4 2.5 Root Cause Failure Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5 2.5.1 Sequencer Imgic Failure . . . . . . . . . . . . . . . . . . . . . . . . . . . 5 2.5.2 Microprocessor Timer / Relay Failure . . . . . . . . . . . . . . . . . . . 6- 2.5.3 Engineering Process and Root Cause . . . . . . . . . . . . . . . . . . . 7 2.6 Corrective Actions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8 2.6.1 Suppression Diode Installation . . . . . . . . . . . . . . . . . . . . . . 8 2.6.2 Auxiliary Feedwater Pump Logic Change . . . . . . . . . . . . . . . . 9 2.6.3 Post Modification Testing . . . . . . . . . . . . . . . . . . . . . . . . . 11 2.7 Equipment Qualification .............................. 12 2.8 Generic Implications ................................ 13 2.9 Com mitmen ts . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15 2.10 Conciusi on s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15 3.0 EXIT M EETING . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16 APPENDIX A - Persons Contacted APPENDIX B - Sequencer Operation ATTACHMENT 1 - Augmented Inspection Team Charter ATTACHMENT 2 - Exit Meeting Slides FIGURE 1 - Simplified Sequencer logic Diagram - Pre-Modification FIGURE 2 - Simplified Sequencer Irgic Diagram - Post-Modification iv
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DETAILS 1.0 INSPECTION SCOPE , The scope of the Augmented Inspection Team (AIT) inspection was provided by the Region 1 Regional Administrator in the Augmented Inspecdon Team Charter (Attachment 1). , ' Generally, the team was tasked with conducting a detailed review of the circumstances surrounding the failure, during routine surveillance testing, of both the Train-A and Train-B emergency diesel generator load sequencers. Specifically the team was tasked with: . * Conducting a thorough and systematic review of the circumstances surrounding the t failure of the diesel generator load sequencers. * Collecting, analyzing and documenting factual information to determine the causes, conditions, and circumstances pertaining.to the failures, including the adequacy of commercial dedication qualification testing of the relays and the adequacy of the licensee's corrective actions in response to a previous failure of this circuitry.- * Evaluating modification controls, design changes, and surveillance testing which may have contributed to the failures. ; * Evaluating the licensee's review of and response to the failures, including implemented and proposed corrective actions. * Assessing the safety significance of the failures and communicating to Regional ~and Headquarters NRC management the facts and safety concerns related to problems identified, including single failure vulnerabilities and impact on other safety-related equipment, generic implications and the need for communication of generic issues to , other licensees. l ; In addition to the team charter, the NRC issued a Confirmatory Action Letter (1-93-020) on November 9,1993, to confirm verbal commitments made by the licensee to the NRC j regarding this event. Specifically, the letter documented the following actions: (1) The. quarantine and suspension of testing of the relays and components, which may have caused ; ' the failure of the emergency diesel generator load sequencers, until resumption is authorized by the AIT team leader; and (2) Maintain Unit 2 in the cold shutdown mode until you receive authorization from the Regional Administrator, NRC Region I. l . ; I J j
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2.0 DETAILED INSPECTION FINDINGS , 2.1 Background The emergency diesel generator load sequencers automatically place vital safety-related ' equipment in service in the event that normal power is lost on an emergency bus. If a ' postulated accident were to occur concurrently with a loss of normal power, then the load sequencers would also automatically place the emergency core cooling system equipment , inservice. The load sequencer timer / relays are used to distribute the loads being placed on the emergency electrical bus in six discrete timed steps over a 1-minute period. A total of eight timer / relays are installed in each emergency diesel generator load sequencer. The original emergency diesel generator load sequencer timer / relays were Model ATC 305E electro-mechanical timer / relays manufactured by the Automatic Timer and Controls Company, Incorporated. During the first refueling outage, in 1989, difficulty was encountered with obtaining the necessary set-point repeatability with the electro-mechanical timer / relays. An engineering evaluation was completed to widen the set-point tolerances, thus allowing the Model 305E timer / relays to satisfy the acceptance criteria. Based on th~e performance of the timer / relays during the first outage, the decision was made to replace these timers during the second refueling outage.
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During the second refueling outage, in November 1990, the original timer / relays were replaced with digital Model 365A microprocessor based timer / relays manufactured by the Automatic Timer and Controls Company, Incorporated. The timer / relays were procured as commercial grade components and dedicated by Wyle Laboratories for Class-1E service. To improve the timer / relay performance, the clock circuits were continuously energized on some of the timer / relays in accordance with vendor recommendations. The load sequencers functioned properly during surveillance testing conducted following this modification. During the third refueling outage, in April 1992, roatine surveillance tests identified three of the eight timer / relays in each sequencer train had failed. The failures were caused by the , modification made to the timers that continuously energized the clock circuits. Continuously energizing the clock circuits caused overheating and the failure of a resistor in the timer / relays. The clock circuits had been continuously energized to improve the timer / relay - . set-point accuracy.
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The timer / relay configuration was changed based on the vendor's recommendation, but verification of the adequacy of this recommendation was not thoroughly tested or analyzed. The cause of the failures was attributed to inadequate design control. The NRC conducted l an enforcement conference regarding this issue and issued a Severity Level III violation and a l Civil Penalty (NRC Inspection Reports 50L412/92-07 and 50-412/93-22). The failed i timer / relays were replaced snd the clock circuits were modified such that the timer / relays
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were only energized during sequencer operation. The load sequencers tested satisfactorily during the eighteen month surveillance tests conducted at the end of the outage. l
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2.2 Event Description On November 4,1993, during the performance of Operating Surveillance Test 36.3, " Emergency Diesel Generator Automatic Test," the Train-A,2-1 emergency diesel generator (EDG) load sequencer failed to automatically load the emergency core cooling system equipment on the emergency electrical bus as designed. The routine surveillance test, which r is conducted on an eighteen month interval, involved simulating a loss of normal power concurrent with a safety injection signal. During the test, the EDG started and reenergized the associated emergency bus; however, safety-related equipment did not automatically ! sequence onto the bus as expected. Approximately two minutes following the failure, the safety injection (SI) signal was manually reset. Resetting the safety injection signal caused the safety-related equipment to begin sequencing onto the emergency bus. The surveillance test was terminated and trouble-shooting activities were initiated. . Bench testing of the relays was not successful in identifying the cause of the failure. An evaluation of the sequencer logic circuit by the licensee's engineering staff identified two relays, one in the sequencer circuit and one in the solid state protection system, whose malfunction had the potential to cause the symptoms observed during the failed surveillance test. Both suspect relays were replaced, and diagnostic test equipment was installed to monitor the load sequencer operation. The operating surveillance test was successfully , repeated on November 5,1993. The diagnostic test equipment did not identify any component failures during this test. , ) On November 6,1993, during the performance of Operating Surveillance Test 36.4, " Emergency Diesel Generator Automatic Test," the Train-B, 2-2 emergency diesel generator load sequencer failed to automatically load emergency core cooling system equipment on the ' bus as designed. Diagnostic test equipment had been installed on the load sequencer and provided pertinent information on the failure mode of the sequencer. The cause of the sequencer failure was identified as the safety injection reset relay (762EGSBA). This relay [ ' resets the load sequencer if a safety injection signal occurs during a loss of normal power event. A contact from this relay failed to open, which caused the load sequencer to ." lock- up" and failed to automatically load equipment onto the emergency bus. Surveillance testing ' activities were suspended and an evaluation was initiated to determine the cause for the failure. ; The operations staff notified the NRC of this failure of multiple trains of a safety' system in , accordance with 10 CFR 50.72(b)(2)(i) on November 6,1993. In response, the NRC l dispatched an Augmented Inspection Team on November 8,1993, to review this event. l . i 1 ,
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2.3 Safety Significance
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The failure of both emergency diesel generator load sequencers would prevent automatic initiation of the emergency core cooling systems in the event of an accident with a loss of normal power. The automatic initiation of the emergency core cooling systems would have functioned correctly for a postulated accident without the loss of normal power. The load sequencers would also have functioned correctly and loaded safety-related equipment in the event of a loss of normal power without an accident. In the event that the load sequencers were to malfunction during an accident with a loss of normal power, manual operator actions, in accordance with the emergency operating procedures, would be required to mitigate the consequences of the event. The manual actions include locally resetting the motor-control-centers. Resetting the motor-control-centers is required to restore service water to the emergency diesel generators, the high head safety injection pump coolers and to operate essential emergency core cooling system valves. For some postulated accidents, , manual operator actions may not have been adequate to satisfy the design criteria for the emergency core cooling systems (10 CFR 50.46). The team concluded that the common cause failure of multiple trains of a safety system required to mitigate the consequences of an accident was a significant event. At the time of the identification of this failure, Beaver Valley, Unit 2, was in cold shutdown
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and the automatic initiation of the emergency core system was not required. However, the susceptibility of the timer / relays to this failure mechanism appears to have existed since the
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microprocessor timer / relays were installed in 1990. 2.4 Load Sequencer Operation
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The emergency diesel generator load sequencers automatically load safety-related equipment i onto the 4 kV emergency busses following the detection of an undervoltage or degraded 1 voltage conditions on the emergency busses and restoration of power. Additional emergency core cooling system equipment would be placed in service by the load sequencer if the loss of power were to occur concurrently with an accident. The safety-related equipment is ) loaded onto the diesel generators in six discrete, timed steps, over a 1-minute period, to l prevent overloading the diesel generators. The function of the Train-A and Train-B load i
sequencers is identical. Therefore, only the Train-A sequencer operation will be described. In the event that power is lost to an emergency bus, the associated emergency diesel generator will automatically start, and the diesel output circuit breaker will close to provide j
emergency power to the bus. The load sequencer blocks the automatic start function of ; equipment on the bus so that loads are place onto the diesel generator in a timed sequenca. ] When the EDG output circuit breaker closes, the load sequencer master relay (3-EGSA.AX) ] energizes (See Figure 1). The master relay starts seven timer / relays that start the timintf of i
sequencer steps 2 through 7. The first step is when the EDG output breaker closes and the ! seventh step resets the sequencer after 1 minute. i ) i I I .
, * . 5 When the timer / relays for steps 2,3,5 and 6 time-out, they energize an auxiliary relay, which initiates sequencing of specified loads onto the emergency bus. The step 4 timing l relay is slightly different. When it times-out, it energizes a second timer / relay. This slave timer / relay energizes an auxiliary relay for 2 seconds, during which time an auxiliary feedwater pump and/or a quench spray pump may start. The auxiliary feedwater pump and the quench spray pump may also start any time after step 7. Step 7 is the. final step in the sequencer, and it resets the load sequencer by deenergizing the master relay (3-EGSAAX). - The load sequencer is designed to reset following a safety injection (SI) or a Phase-B containment isolation (CIB) signal. The reset is required because the loads required during a SI or CIB are different than those required for a loss of normal power alone. Therefore, by . resetting the load sequencer, the appropriate equipment is automatically placed in service. If the sequencer receives a reset signal after it has started running, loads already connected to the bus will remain operating. The reset of the load sequencer occurs when the SI reset , timer / relay or the CIB reset timer / relay are energized. These relays are energized by engineered safety feature actuation system. Each train of the load sequencer has eight Automatic Timer Controls, Model 365A microprocessor timer / relays. The microprocessor timer / relays are used for SI and CIB reset,' , sequence steps 3-6, sequencer reset, and the step 4 slave timer. The step 2 timer is a Model ITE-62K timer / relay manufactured by Asea Brown Boveri (ABB). The Model ITE-62K timer / relay is used for step 2 because of the additional accuracy needed in the timing of this step. All of the auxiliary relays in the sequencer circuits are Model RXMH-2 electro-mechanical relays. The RXMH-2 relays were manufactured by Asea Brown Boveri. A detailed description of the load sequencer operation is provided in Appendix B of this inspection report. A simplified logic diagram of the load sequencer circuit is provided in ' ' Figure 1. 2.5 Root Cause Failure Analysis ; 2.5.1 Sequencer Logie Failure - The configuration and operation of the Train-A and Train-B EDG load sequencers are identical; therefore, only the Train-A sequencer operation and failure will be described. The , licensee installed diagnostic test equipment on the 2-2 emergency diesel generator load sequencer prior to the performance of the operating surveillance test. Following the failure of the load sequencer, the information collected from the diagnostic test equipment was analyzed to determine the cause. i t
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: 6 - The cause of the load sequencer failure was determined to be the malfunction of the safety injection microprocessor timer / relay (762-EGSAA) that is used for sequencer reset. Specifically, the microprocessor timer / relay time delay contact opened after a 1/2 second time delay and then inadvertently m-closed a very short time later (approximately 30 , milliseconds). Closing of the 762-EGSAA time delay contact energized the 3-EGSAAX4 > relay, which " locked-out" (deenergized) the load sequencer master relay and prevented further load sequencer operation. The diagnostic test equipment also identified that a large negative voltage spike resulted from deenergizing the auxiliary relay (3-EGSAAX4) coil. The auxiliary relay coil (3-EGSAAX4) deenergized when the microprocessor timer / relay (762-EGSAA) time delay contact (762- ' TDO) opened. The spike was generated by the sudden change in current in the auxiliary relay coil (inductor). The rise and fall times of the voltage spike were very fast and the amplitude of the voltage spike was in excess of 1100 volts at the 762-TDO contact. The - voltage spike was transmitted back into the input, power line, and electronics of the microprocessor timer / relay (762-EGSAA) by the arc shower process across the 762-TDO . contact. The resulting electronic interference caused the microprocessor to malfunction and y reclosed the 762-TDO contact. 2.5.2 Microprocessor Timer / Relay Failure The licensee conducted a series of bench tests of the microprocessor timer / relays to obtain ' additional information regarding the failure. The test setup used both a microprocessor timer / relay and an auxiliary relay. These relays were tested in a circuit configuration identical to the in-plant configuration. The results of these bench tests indicated an i intermittent failure mode of the microprocessor timer / relays. i The 2-1 load sequencer was temporarily modified to allow the performance of in situ testing of the sequencer without starting the safety-related loads. The results of this in situ testing ) indicated an intermittent failure mode of the microprocessor timer / relay (762-EGSAA). These in situ tests were instrumented to provide information regarding the magnitude and ; location of the voltage spikes that occurred during sequencer operation. The licensee also conducted failure analysis tests internal to the microprocessor timer / relay. ! The tests concluded that the failure was due to microprocessor malfunction. The cause of : microprocessor malfunction was attributed to the negative voltage spikes which were , ' generated when the internal relay deenergized the auxiliary relay coil. The internal relay and contacts (762-TDO) were mounted on the same printed circuit card as the electronic parts and the microprocessor. Consequently, the negative voltage spikes affected the microprocessor and electronic circuitry through an indeterminate transient process involving i the internal relay. The exact transient mechanism was not determined at a level below the ! ~ circuit board indications. The timer / relay vendor engineer stated that symptoms of a microprocessor failure were that the time display malfunctions and the internal timed relay : deenegizes, thus causing the normally closed internal timed relay contact to close. Since the l ,
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. 7 normally closed contact were used in the auxiliary relay circuit, the result was that the , auxiliary relay would not be deenergized as required at the end of the microprocessor controlled time delay. This description matched the failure analysis indications. The vendor ! engineer also stated that the probable cause was due to the inductive discharge of energy , across the contacts of the internal relay. This would cause transient arcing and could generate electronic interference internal to the timer / relay, which could cause the microprocessor to malfunction. The inductive energy discharge transient across the contacts ; is called arc shower and is always a direct consequence of interrupting an inductive current. The licensee plans to send a microprocessor timer / relay to the vendor for additional failure analysis of the electronic circuitry. , Diode suppression of the voltage spikes at the auxiliary relay removed the cause of the are shower effect and allowed the microprocessor timer / relay to function properly. The . + effectiveness of diodes in suppressing the voltage spikes created during the deenergization of the auxiliary relays was determined by testing. The microprocessor timer / relay and auxiliary relay were bench tested in the in-plant configuration with the addition of a diode installed in parallel with the coil of the auxiliary relay. The results of these tests showed no failures after approximately 80 operations and indicated a significant reduction in the magnitude of the negative voltage spikes. : The team noted that test results were frequently not well documented. However, the root cause evaluation described and summarized all the testing in a comprehensive, logical manner. 2.5.3 Engineering Process and Root Cause To determine the root cause of the failure of the emergency diesel generator (EDG) load sequencer the team evaluated the load sequencer circuit design, the failed microprocessor timer / relay (762-EGSAA), and the engineering process for design control. The licensee's engineering personnel did not suspect that voltage spikes, that normally result from deenergizing auxiliary relays, would present a problem in this application of the microprocessor timer / relay. This was based on their interpretation of the vendor's data sheet, which did not contain any information or precautions that indicated susceptibility of the microprocessor timer / relay to voltage spikes associated with deenergizing auxiliary relays. The licensee did not conduct any confirmatory testing, analysis, or wTitten justification that independently verified the vendor's implied statement concerning the non- susceptibility of the microprocessor timer / relay to voltage disturbances. The team noted that the vendor's data sheet did not discuss noise suppression when using the contacts to control direct current (de) powered relays. But there were precautions stated for the auxiliary relay. In the auxiliary relay data sheet, the protection of electronic circuits against the auxiliary relay coil inductive voltage type transients was covered along with details of diode - suppression' techniques.
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The modification process and the 10 CFR 50.59 safety evaluation for the modification that installed the microprocessor timer / relays did not list or evaluate inductive spiking as a possible failure mechanism for the microprocessor timer / relays, even though the possibility of spiking existed. Since no suppression techniques were included in the modification, 1
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voltage spikes would, therefore, be present and should have been evaluated. The previous * failure of the load sequencer in 1992 was attributed to weak design control. At this time, an opportunity was missed to conduct additional design reviews of this modification to determine if other design control deficiencies existed. The team reviewed the post modification test data from the initial design change and , determined that the data did not provide information on load sequencer voltage spikes. The licensee's root cause determination concluded that a more rigorous post modification test may have identified this failure mode. The team concluded that the effects of the inductive voltage transient which caused arc showering, due to the interruption of an inductive current, were inadequately evaluated in the design process. This resulted in a sequencer design with an inherent failure mechanism that had an extremely high potential for the introduction of a common cause failure. Therefore, the team attributes the root cause of this event to an inadequate engineering evaluation of the susceptibility of the microprocessor relay / timer to the installed electromagnetic interference (EMI) service conditions. The evaluation did not encompass the
EMI sources (such as fast transient voltage spikes / arc shower in this case) or the effect of
those EMI sources on the replacement component. 2.6 Corrective Actions 2.6.1 Suppression Diode Installation Minor design change package (MDCP) number 2057 was developed to prevent the malfunction of microprocessor timer / relays 162-EGSAAX1,762-EGSAA,862-EGSAA,162- EGSBAX1, 762-EGSBA and 862-EGSBA, while the microprocessor timer / relays are deenergizing their respective auxiliary relays. This was accomplished by the installation of inductive voltage transient suppressors across nine auxiliary relay coils in each sequencer i train. The sequencer timer / relays and auxiliary relays are located in power panel PNL* SEQ 244 for Train-A and in power panel PNL* SEQ 254 for Train-B. The applicable ! portions of the schematics showing the pre-modification and post-modification configurations of the EDG loading sequencer are provided in Figures 1 and 2 of this inspection report, respectively.
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. .. - __ _. - _ . ' . . ! . 9 ; ; The suppressors consisted of diodes which were installed in parallel with the auxiliary relay ' coils to suppress the voltage spikes created when the relay coils are deenergized. The l i suppressor type selected was an ABB terminal base mounted, RTXE with the type 2 assembly.' These diodes were designed for use with the ABB RXMH-2 type coil relays and j _ other ABB type relays. The purpose of these diodes, as explicitly stated in the published ABB relay data sheets, was "to obtain a dropout delay for de relays or to protect electronic ! -; circuits against transients." ! t The 10 CFR 50.59 safety evaluation worksheet associated with the modification was , ' reviewed. The safety evaluation identified that the only parameters affected by this change were the voltage and the timing associated with the operation of the sequencer relays. The safety evaluation stated that the addition of a diode to the coil of the ABB RXMH-2 relay . delays the dropout time by approximately 20 milliseconds. The safety evaluation concluded : that this 20 millisecond delay was not significant compared to the required accuracy of the . sequencer, which is on the order of 200 milliseconds. However, the conclusion that the 20 l millisecond time delay would not affect sequencer operation was incorrect. A problem with , the auxiliary feedwater (AFW) pump start sequence was identified during the performance of the functional test, 20ST-36.3. With the exception of this relay timing problem, the team ! determined that the MDCP and associated 10 CFR 50.59 evaluation were adequate. j The installation and initial testing of the suppressors for the Train-A load sequencer was - l completed on November 14, 1993, with the final post-modification testing completed on ; November 16, 1993. The Train-B diode suppressors were installed and subsequently tested j
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on November 17,1993. In addition to the installation of the suppressors, microprocessor , timer / relays 762-EGSAAX, 862-EGSAAX, and the 862-EGSBAX were replaced. ]f 2.6.2 Auxiliary Feedwater Pump Logic Change { l During the performance of the diesel generator 2-1 functional test 20ST-36.3, " Emergency j Diesel Generator Automatic Tests," the auxiliary motor driven feedwater (AFW) pump .- ! inadvertently started immediately following the closure of the EDG output circuit breaker, ; rather than at load sequencer step 4. Load sequencer Step 4 equipment is supposed to load - i 15 to 17 seconds after the emergency diesel output circuit breaker closes. The licensee j determined that the cause of the inadvertent start was a delay in the deenergization of : auxiliary relay 162-EGSA.AX, at the beginning of the loading' sequence. The delay in the ! deenergization of the 162-EGSAAX relay was introduced by the addition of diode l suppressors and was not identified during the development of the modification. The AFW. 3l pump starting logic is identical for Train-A and Train-B; therefore, only the Train-A starting .l logic will be described. l 3 : l .I - - - - . . - . . ..
. 10 AFW Pumo Startine Imcic Operatim The motor driven auxiliary feedwater pump starting logic consisted of three contacts in series that were all required to close to start the AFW pump. (Not to be confused with the simplified schematic in Figures 1 and 2.) These contacts were closed when voltage was available on the emergency bus, when the load sequencer auxiliary relay 162-EGSAAX was energized (sequencer step 4), and when a safety injection signal was present. The load sequencer relay 162-EGSAAX was normally energized and deenergized when the EDG output circuit breaker closed. This logic was designed to deenergize the 162-EGSAAX relay i before the voltage sensing relays on the emergency bus picked-up following power , ' restoration by the EDG. Deenergizing the 162-EGSAAX relay opened a contact in the AFW pump starting logic that prevented starting the AFW pump prior to sequencer step 4. At sequencer step 4, the 162-EGSAAX relay energized and started the AFW pump. AFW Pumn Starting Impic Failure After the failure of the functional test, the licensee reviewed the AFW pump starting circuit to determine why the AFW pump inadvertently staned at sequencer step 1 rather than at step 4. During step 1 of the loading sequence, the safety injection (SI) contact in the AFW pump starting circuit was closed. The two additional contacts in the starting circuit were the 162-EGSAAX contact from the sequencer and the voltage available on the emergency bus
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contact from the bus voltage sensing relays. To prevent premature starting of the AFW pump, the 162-EGSAAX relay must deenergize prior to the voltage available on the bus ' sensing relays pick-up. This developed a race between the two relays. The installation of the suppressor diodes around the 162-EGSAAX relay caused a delay in the drop-out time of the 162-EGSAAX relay. This delay allowed the emergency bus voltage relay contacts to close prior to the opening of the 162-EGSAAX contacts, thus starting the AFW pump. The modification which installed the diode suppressors did not assess the effect of the delay in auxiliary relay drop-out time on the sequencer operation. The associated safety evaluation identified that the expected delay in relay drop-out was approximately 20 milliseconds. The safety evaluation correctly stated that this would not adversely affect the overall delay time in : loading safety-related equipment. However, the safety evaluation did not document the effect that this would have on the AFW pump start circuit. In addition the functional test measured l the actual delay in relay drop-out time to be approximately 70 milliseconds. j i Corrective Actions ) In response to this failure, the licensee performed a detailed review of the sequencer circuit < and verified that no other potential start logic problems existed. In order to correct the failure associated with the AFW pump starting circuit, the licensee initiated an Engineering Change Notice (ECN) to modify the AFW pump starting circuitry such that the 162- EGSAAX relay would not be energized prior to load sequence step 4. The design change u l
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prevents the possibility of having the three AFW pump starting circuit contacts closed prior to sequencer step 4. The 162-EGSAAX relay would be energized for 2 seconds at step 4 of the load sequence. An additional change to the AFW pump start circuit was required to provide a second AFW pump a start signal after the final sequencer step. . Conclusion The implications of the installation of the diode suppressors on the relay timing were not < thoroughly evaluated. Following the installation of the suppressors, the delay in slave relay drop-out time caused the AFW pump to start at the wrong sequence step. An additional ! design change was required to correct this problem. The team concluded that the actions taken by the licensee to correct this probicm were acceptable. However, the team considered the inadequate evaluation of the suppressor installation on relay timing as another example of ' a weak design control process. 2.6.3 Post Modification Testing , After the installation of the suppressors, the modification design change package required the performance of sequencer testing to verify that the microprocessor timer / relays and the auxiliary relays were functioning properly. The modification design change package required j that each sequencer train be tested a total of 30 times. Fifteen cycles were to be initiated by . loss of normal power with an SI signal. The remaining fifteen cycles were to be initiated by loss of normal power with a CIB signal. The first and last run for each set of fifteen cycles , were to be instrumented to allow for engineering review of the associated traces. - In addition to the testing required for the completion of the modification, other in situ tests were performed to verify that the installation of the of the suppression diodes allowed for proper sequencer operation. In total, approximately 200 in situ tests were performed with no failures. Whereas, in situ testing performed prior to the installation of the suppressors , ' indicated a failure rate of approximately 35%. These post-mooification tests verified the operation of the sequencer for loss of offsite power conditions, separately, and with a SI signal or a CIB signal. Approximately 20% of these tests were instrumented to verify that the voltage spikes were adequately suppressed, and to verify that the suppression diodes showed no signs of degradation. The licensee also performed the Operating Surveillance Tests 20ST-36.3 and 20ST-36.4, " Emergency Diesel Generator Automatic Tests,"_ prior to declaring the sequencers operable. The team observed portions of these tests and determined that they were acceptable to demonstrate system opembility. , , < ? ,
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2.7 Equipment Qualification ATC Timer Relay Dedication The Beaver Valley Unit 2 Updated Final Safety Analysis Report, Table 8.1-1, lists the Institute of Electrical and Electronic Engineers Standard (IEEE) 323-1974, " Standard for > Qualifying Class 1E Equipment for Nuclear Power Generating Stations," as acceptance criteria for Class IE components. This standard was used as guidance for the dedication of the ATC Model 365A microprocessor timer / relays. The microprocessor timer / relays were procured as comme,cial grade items in the spring of 1990 and installed in the load sequencers in the fall of 1990. The dedication of the . l timer / relays as Class 1E components was controlled through the licensee's engineering design change process rather than through the commercial dedication program. The design change package stated that the following actions were necessary to dedicate the relays: e A review and evaluation by a third party 7f the Class 1E environmental qualification
of the microprocessor timer / relays. The review and evaluation was to be governed by IEEE 323-1974 (as interpreted by NUREG-0588, Rev.1) and the seismic qualification requirements of IEEE 344-1975. The environmental qualification parameters specified in the procurement document were: temperature, pressure, humidity, cumulative radiation dose, aging, and seismic forces. ! ,
- An initial calibration and checkout of the relays prior to installation.
* A continuity test of the relay circuits to ensure that they were wired properly. * A functional test of each sequencer circuit. '
The third party review and evaluation was complete by Wyle Laboratories. The review was thorough, and provided adequate justification for qualification of the relays as specified in the procurement specification. However, the following deficiencies were noted in the licensee's overall qualification package for the microprocessor timer / relays (the combination of Wyle's testing and the onsite testing) when compared to the requirements ofIEEE 323-1974:
e Electromagnetic interference (EMI) was not considered as part of the relay qualification. The term EMI encompasses both external (or radiated) EMI and circuit induced EMI. Section 6.2(2) of IEEE 323-1974 states that Class 1E qualification shall include electromagnetic interference. ; .
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. 13 * IEEE 323 requires specification of the equipment operating environment. The licensee indicated weakness in this area as illustrated by the following: (1) The equipment performance specifications did not define the transient range of ' voltage under which the relays were expected to operate. (2) The circuit configuration specified in the procurement specification was not the actual configuration used for all the relays. Some of the installed relays were ' wired with their clock power supplies continuously energized.' The configuration qualified by Wyle had the relays energized only when the sequencer was called on to operate. This eventually. led to failure of the relays as discovered in the spring of 1992. This deficiency was covered by Enforcement Action 92.-085. ; * The qualification documentation was not organized in a auditable form as specified in Section 8 of IEEE 323-1974. The documentation supplied by Wyle was thorough; however, the post-modification test results were not incorporated in the qualification documentation. Following the sequencer railures on November 4 and 6,1993, the licensee modified the sequencer design and performed supplemental testing to provide reasonable assurance that the ATC timer / relays installed in the load sequencers would operate as designed. They did not, however, develop an auditable qualification package for the relays. Additionally, no documentation was developed to indicate the status of the ATC timer / relays in the warehouse. The licensee's spare microprocessor timer / relays underwent third party review by Farwell & Hendricks, Inc. Since the spare microprocessor relays do not have auditable qualification documentation, and have not received rigorous testing like the installed relays, their Class IE qualification requires documentation. Supnression Diode Dedication The team reviewed commercial grade evaluation, D-905786, for the suppression diodes. The critical characteristics defined by the licensee were appropriate for the intended application of ' the suppression diodes. Additionally, the commercial grade evaluation contained appropriate calculations to support the selection of the critical characteristics. 2.8 Generic Implications Beaver Valley Specific .j In addition to the microprocessor timer / relays installed in the sequencers, four additional , ATC-365A microprocessor timer / relays are installed in the recirculation spray (RSS) pump starting circuits. These timer / relays start the RSS pumps 628 seconds after the receipt of a containment isolation phase-B (CIB) signal. A failure of the "D" RSS pump occurred during , i I
14 t the performance of surveillance testing during the week of November 1,1993. The timer / relay staned the "D" RSS pump at the time the CIB signal was simulated and did not delay the pump start for 628 seconds. The timer / relay was removed from the circuit for further investigation and bench testing. During bench testing,125 Vdc was inadvertently applied directly to the timer / relay without a voltage dropping resistor. The voltage dropping ' resistor was required to reduce the supply voltage to the timer / relay from the 125 Vdc to the design voltage of 24 Vdc. As a result of this error, the timer / relay was destroyed and was not available for further testing. A new timer / relay was installed in the RSS pump staning circuit and a functional test was successfully performed. The team considered the licensee's inadvertent damaging of the failed RSS pump microprocessor timer / relay as an example of weak troubleshooting practices. Functional test 2BVT1.13.5, " Recirculation Spray Pump Test," was performed, with diagnostic test equipment installed, to determine if voltage spikes were affecting the performance of the RSS pump microprocessor timer / relays. The test identified one negative , voltage spike at the microprocessor timer / relay input from the RSS pump breaker trip coil. During accident conditions, the RSS pump would not be tripped until the CIB signal had ; - been reset. When the CIB signal is reset, the RSS pump microprocessor timer / relays are isolated from the RSS pump starting circuit. Therefore, any RSS pump breaker trip coil induced voltage spikes would not adversely affect the microprocessor timer / relay ability to start the RSS pump. In order to determine if any other solid-state electronic relays had been installed at the Beaver Valley Power Station, the licensee reviewed the category one design change packages (DCPs) implemented over the past five years. This review identified four DCPs that installed solid-state electronic relays. The relays installed by these DCPs were determined to have adequate documentation regarding transient immunity that enveloped the expected .,! transients conditions, or had been appropriately tested for surge withstand capability, fast transient and EMI susceptibility. Therefore, these relays should be suitable for their installed , application. Industry Generic Implications The team determined that the load sequencer failures at Beaver Valley have generic implications. The generic issue is that licensees must conduct a thorough design review when replacing discrete component electrical devices with digital, microprocessor based l electronic devices. Specifically, licensees need to conduct a detailed case-by-case design , f review to assure that the digital, microprocessor based replacement equipment is compatable for the specific application. This review is necessary since solid state electronic equipment is
l generally more susceptible to damage from system disturbances than their electromechanical
predecessors, particularly with respect to electromagnetic interference and other power
l supply instabilities.
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15 2.9 Commitments The first three commitments listed below were provided in the licensee's letter to the NRC, ; ' dated November 18, 1993. In addition, the licensee staff stated that a review would be * conducted to evaluate the feasibility of additional sequencer testing, and the commercial ; grade dedication package documentation for microprocessor timer / relays would be upgraded. It is the team's understanding that the licensee plans to do the following: 1. An ATC timer / relay will be sent to the manufacturer for failure analysis. ! 2. An evaluation of the licensee's capability to identify and specify modification tests * which detect functional degradation of modified equipment will be conducted. Until completion of the evaluation, Engineering Assurance and System Engineers will review modification packages prior to installation and will concur with the modification testing requirements. t ' 3. Engineering guidelines will be developed which address engineering requirements for the application of digital solid state components as replacements for non-digital components. 4. A review will be conducted to determine if additional testing of the emergency diesel generator sequencers is feasible and appropriate. 5. The qualification package for the ATC timer / relays will be upgraded to satisfy the IEEE-323-1974 standards. Documentation of the EMI type testing conducted on the , ATC relay will be included in the commercial grade qualification package.- , 2.10 Conclusions The modification which installed the Model 365A ATC microprocessor timer / relays was ! inadequate. The design control for the selection and review for suitability of the ATC j timer / relays for this application was not adequate. The modification design inputs should have identified the potential for voltage spiking by the auxiliary relays. This design input should then have been translated into the equipment purchase specification and the dedication testing specification. * I The implications of the installation of the diodes on relay timing was not thoroughly evaluated. The delay in the slave relay drop-out caused an auxiliary feedwater pump to start ; at the wrong sequence step following the installation of the diodes. Further design changes , = were required to correct this problem. The team concluded that the actions taken to correct this problem were acceptable. ; ! t l
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The installation of the diodes to suppress voltage spikes was an acceptable corrective action. The team independently verified the test results and concluded that this modification makes , the emergency diesel generator load sequencer operable. Test control and trouble-shooting of the failed relays was weak. For example, the failed relay from the recirculation spray pump was inadvertently destroyed, preventing further investigative testing.
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The corrective actions taken in response to the April 1992 clock failures were adequate. , However, an opportunity to further evaluate the selection of the microprocessor timer / relays for this service application was missed at this time. The team concluded that the failure mechanism and corrective actions taken in response to the clock failures were independent of the current timer / relay failures. The qualification documentation for the ATC 365A timer / relays was incomplete. The documentation did not address electromagnetic interference issues and was' not put together in j an organized and auditable format as specified in IEEE-323-1974. 3.0 EXIT MEETING The team met with those denoted in Appendix A, on December 2,1993, to discuss the - ] preliminary inspection findings which are detailed in this report. The exit meeting was open j for public observation and the NRC answered public questions following the exit meeting. I The slides used at the exit meeting are provided as Attachment 2 of this inspection report.
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- APPENDIX A
Persons Contacted .; Duquesne Light Comoany , , * P. Bienick Project Engineer * L. Freeland General Mgr. Nuclear Operations * K. Grada Mgr. Quality Services Unit . * K. Halliday Director, Electrical Engineering * F. Lipchick Sr. Licensing Supr. ! ' * D. McBride System Engineer * D. McLain Mgr. Maintenance Engineering and Assessment * T. Noonan Gen. Mgr., Nuclear Engineering and Safety ~ * D. O'Neil Gen. Mgr. Public Affairs * J. Sasala Director, Nuclear Communication ' * R. Scheib ANSS Unit 2 * J. Sieber Sr. Vice President - Nuclear Power Division * M. Siegel Mgr. Nuclear Engineering Department . * G. Storolis NSS Unit 2 * D. Szucs Sr. Engineer, Nuclear Safety * G. Thomas Division Vice President - Nuclear Service * N. Tonet Mgr. Nuclear Safety i * G. Zupic Supr. Reactor Engineering ! U. S. Nuclear Regulatory Commission - * G. Edison Project Manager, NRR 1 * C. Miller Deputy Division Director, DRS * L. Rossbach Sr. Resident Inspector - Beaver Valley QLhn * G. Morris Video Photographer * J. Musala Reporter * B, Shaw DLC-retired * R. Barkanic Nuclear Engineer, Pa. State DER /BRP Asterisk (*) denotes those present at the exit meeting conducted on December 2,1993. The persons contacted list is not a comprehensive list of every individual contacted but provides the principal staff associated with this event. ;
APPENDIX B . SEQUENCER OPERATION
The following provides a description of the function of the emergency diesel generator load sequencer operation. The Train-A and Train-B load sequencer operations are identical; therefore, only the Train-A sequencer operation will be described. A simplified logic diagram of this circuit is provided in Figure 1 of this inspection report. Secuencer Operation 1. A loss of offsite power will result in the opening of the normal supply circuit breakers
to the emergency bus and the automatic start of the associated emergency diesel- generator. The opening of the normal supply circuit breaker to the emergency bus l will cause the 52S-ENSAC contact to close. ;
2. Following the EDG attaining rated speed and voltage, the EDG output circuit breaker
closes and contact 52S-ECPAA closes. This energizes master relay,3-EGSAAX, j because the 69-EGSAA and the 3-EGSAAX4 contacts are normally closed. Once the master relay is energized, its associated contacts in the circuits for the slave ' timer / relays are closed allowing the loads to sequence on in the proper order.
3. When an SI signal is present, contact SIS-K610XA would close. 4. The closing of contact SIS-K610XA provides power to the microprocessor timer / relay
762-EGSAA.
5. When microprocessor timer / relay 762-EGSAA energizes, its timer operation is
started, and its normally open 762-INST contact closes.
6. At the closing of contact 762-INST, the SI/CIB reset relay, 3-EGSAAX4, energizes. 7. When relay 3-EGSAAX4 energizes, its normally closed contact in the master relay
circuit opens, deenergizing the master relay and consequently all ofits slave timer- relays.
8. At 0.5 seconds after energization of the 762-EGSAAX microprocessor timer / relay
(step 3 above), its normally closed 762-TDO contact opens, deenergizing the SI/CIB reset relay, 3-EGSAAX4. The 762-TDO contact stays open until the 762-EGSAAX . L microprocessor timer / relay is reset (i.e. deenergized). '
9. When the 3-EGSAAX4 relay deenergizes, its normally closed contact, which was
opened as described in step 5 above, recloses and reenergizes the master relay, 3- EGSAAX, and all its slave timer / relays. Energizing these slave timer / relays allows ! the safety equipment to load in the proper sequence. ; , h I
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. k , k h 1 L - ATTACHMENT 1 , AUGMENTED INSPECTION TEAM CIIARTER i . I i ,f 1 i , k h I T e i ;
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>S Moe + , UNITED STATES 8 'h NUCLEAR REGULATORY COMMISSION T, gy j REGloN I 0, g 475 ALLENDALE FioAD KING OF PRUSSIA. PENNSYLVANIA 1940G1415 %....[.,d Docket No. 50-412 NOV 9 1993 MEMORANDUM FOR: Marvin W. Hodges, Director, Division of Reactor Safety ' FROM: Thomas T. Martin, Regional Administrator SUBJECT: AUGMENTED INSPECTION TEAM CHARTER FOR REVIEW OF COMMON MODE FAILURE OF THE EMERGENCY DIESEL GENERATOR LOAD SEQUENCERS AT BEAVER VALLEY yNIT 2 On November 4,1993, during the load sequencing test of the 2-1 emergency diesel generator (EDG), the load sequencer malfunctioned in such a manner as to prevent automatic loading of the EDC. On November 6,1993, a load sequencer malfunctioned on the 2-2 EDG. Subsequent testing revealed that a common-mode problem exists that may have prevented either EDG from loading automatically. In order to assess the safety significance of the issue, I have determined that an Augmented Inspection Team (AIT) should be initiated to review the causes and safety implications associated with these malfunctions. The Division of Reactor Safety (DRS) is assigned the responsibility for the overall conduct of this Augmented Inspection. Jim Trapp, Team Leader, DRS, is appointed as Augmented Inspection Team 12ader. Other AIT members are identified in Enclosure 2. The Division of ! Reactor Projects (DRP) is assigned the responsibility for resident and clerical support, as necessary; arid the coordination with other NRC offices, as appropriate. Further, the Division ' of Reactor Safety, in coordination with DRP is responsible for the timely issuance of the inspection report, the identification and processing of potentially generic issues, and the identification and completion of any enforcement action warranted as a result of the team's review. Enclosure 1 represents the charter for the Augmented Inspection Team and details the scope of the inspection. The inspection shall be conducted in accordance with NRC Management Directive (M D) 8.3, NRC Inspection Manual 0325, Inspection Procedure 93800, Regional Office Ins'.ruction 1010.1, and this memorandum. ' Thomas T. Martin Regional Administrator Enclosures: 1. Augmented Inspection Team Charter ; 2. Team Membership i l 1
' , .. - . . ' , . +z . * Marvin W. Hodges 2 cc w/encls:
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J. Taylor, EDO J. Sniezek, OEDO T. Murley, NRR J. Calvo, NRR C. Rossi, NRR W. Butler, NRR F. Miraglia, NRR C. McCracken, NRR J. Wermiel, NRR. W. Russell, NRR J. Wiggins, NRR A. Thadani, NRR B. Grimes, NRR S. Varga, NRR B. Boger, NRR E. Jordan, AEOD D. Ross, AEOD V. McCree, OEDO W. Kane, DRA, RI R. Cooper, DRP, RI W. Lanning, DRP, RI . C. Miller, DRS, RI , W. Lazarus, DRP, RI W. Hehl, DRSS, RI S. Shankman, DRSS, RI L. Rossbach, SRI, Beaver Valley G. Edison, NR.R C. Sisco, DRS, RI L. Bettenhausen, DRS, RI J. Linville, DRP, RI K. Abraham, PAO, RI M. Miller, SLO, RI .
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, . ENCLOSURE 1 ,- AUGMENTED INSPECTION TEAM (AIT) CIIARTER The general objectives of this AIT are to: 1. Conduct a thorough and systematic review of the circumstances surrounding the failure , ' of the diesel generator load sequencers. 2. Collect, analyze, and document relevant factual information to determine the causes, conditions, and circumstances pertaining to the failures, including the adequacy of ; commercial dedication qualification testing of the relays and the, adequacy of the - ; licensee's corrective actions in response to a previous failure of this circuitry (IR ' q 50-412/92-07). ; , 3. Evaluate the licensee's review of and response to the failures, including implemented and l proposed corrective actions. ! , 4. Assess the safety significance of the failures and communicate to Regional and -l Headquarters management the facts and safety concerns related to problems identified, , including single failure . vulnerabilities, impact on other safety systems, generic -! ! implications and the need for communication of generic issues to other licensees. 5. Evaluate modification controls, design changes, and surveillance testing which may have I contributed to the failures. : 6. Prepare a report documenting the results of this review for the Regional Administrator within thirty days of the completion of the inspection. j , i > > i , . Y ! . [
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, .; i I a , . - ENCLOSURE 2 3; 4 AIT MEMBERSHIP ; James Trapp, AIT Irader, Division of Reactor Safety (DRS), Region I (RI) i ! John Calven, Reactor Engineer, Division of Reactor Safety (DRS), IU i Scott Greenlee, Resident Inspector, Beaver Valley Unit 1, DRP, RI , , Richard Skokowski, Reactor Engineer, DRS, RI - . Eric Lees, NRR : Other NRC personnel, consultants, or contractors will be engaged in'this AIT, as needed. ! , ' ~$ . ! i . t : - i i e f . ! i , . r i * . l , 'd '!
! , ., . t ! 1 i s j : , t : l , ') I ! -) i ATTACIIMENT 2 I ! ! 4 AUGMENTED INSPECTION TEAM i EXIT MEETING SLIDES- ! l ] i i l I I
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. ' . : powou, ! % i E g, ..!.../ l AUGMENTED INSPECTION TEAM BEAVER VALLEY UNIT 2 EMERGENCY DIESEL GENERATOR LOAD i SEQUENCER FAILURES : I NRC INSPECTION 50412/93-81 ! EXIT MEETING ; , DECEMBER 2,1993 10 a.m. l * EXIT MEETING BETWEEN NRC AND LICENSEE. , * NRC WILL ADDRESS PUBLIC QUESTIONS ! REGARDING TEAM FINDINGS. l ) 1 1 ! I
. - _ - - _ . . . . . ' . l BEAVER VALLEY UNIT 2 - LOAD SEQUENCER FAILURES j INSPECTION SCOPE ! . I e CONDUCT A THOROUGH AND SYSTEMATIC . REVIEW OF THE CIRCUMSTANCES l SURROUNDING THE FAILURE. l e COLLECT AND ANALYZE FACTUAL : -l INFORMATION,-INCLUDING THE COMAERCIAL GRADE DEDICATION-OF THE l FAILED TIMER / RELAYS. L
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e REVIEW THE ADEQUACY OF THE : CORRECTIVE ACTIONS TAKEN IN RESPONSE - TO THE PREVIOUS SEQUENCER FAILURE. l l e REVIEW THE PROPOSED CORRECTIVE i ACTIONS. ! ! e EVALUATE THE MODIFICATION AND ANY j SURVEILLANCE TESTING THAT MAY HAVE l CONTRIBUTED TO THIS FAILURE. : e ASSESS THE SAFETY SIGNIFICANCE OF THE l FAILURES. ! ! e DETERMINE IF TIHS EVENT HAS GENERIC i I IMPLICATIONS. a 2 ; i
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A _s 4 ..- ,. - . 1 - i ' BACKGROUND . : * EAERGENCY DIESEL GENERATOR LOAD 1 ! SEQUENCER AUTOMATICALLY STARTS : EQUIPMENT REQUIRED TO MITIGATE TIE 1 CONSEQUENCES OF AN ACCIDENT WHEN i OFFSITE POWER IS LOST. " * ORIGINALLY TIE TIMER / RELAYS WERE ATC MODEL 305E AND WERE NOT MICROPROCESSOR BASED. l * DURING REFUELING OUTAGE (RFO) 2, IN 1990, . TIE TIAER/ RELAYS WERE REPLACED WITH ! MICROPROCESSOR BASED ATC MODEL 365A i TIAER/ RELAYS. - * IN 1992 SIX ATC TIAERS WERE IDENTIFIED AS - FAILED DUE TO INTERNAL CIRCUIT CLOCK
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FAILURES. * THE NRC ISSUED A SEVERITY LEVEL III VIOLATION AND CIVIL PENALTY IN RESPONSE ' TO TIE ATC TIAER/ RELAY CLOCK FAILURES. l ! ; 3 ) ! I l ..
- .. : ' l .' EVENT DESCRJPTION * ON NOVEMBER 4,1993, DURING ROUTINE SURVEILLANCE TESTING, THE 2-1- EMERGENCY DIESEL GENERATOR LOAD SEQUENCER FAILED TO FUNCTION. 1 * ATC TBER/ RELAY 762 WAS REPLACED AND ' THE SURVEILLANCE TEST WAS SUCCESSFULLY COMPLETED. , e ON NOVEMBER 6,1993, DURING ROUTINE ; SURVEILLANCE TESTING, THE 2-2 l EMERGENCY DIESEL GENERATOR LOAD SEQUENCER FAILED TO FUNCTION. ; * THE LICENSEE NOTIFIED THE NRC OF THE I FAILURES ON NOVEMBER 6,1993. , * IT APPEARED THAT A COMMON CAUSE FAILURE HAD AFFECTED MULTIPLE TRAINS OF A SAFETY SYSTEM. , ' * AN AIT WAS DISPATCHED BY T11E NRC ' REGIONAL ADMINISTRATOR. AND ARRIVED' ONSITE ON NOVEMBER 9,1993.- . 4 .
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! SAFETY SIGNIFICANCE i e THE DIESEL GENERATOR LOAD' SEQUENCER l WOULD NOT AUTOMATICALLY START j EMERGENCY EQUIPAENT. f I * THE FAILURE WOULD ONLY OCCUR DURING A LOSS OF OFFSITE POWER WHEN A SAFETY ! INJECTION WAS REQUIRED. . < E * MANUAL OPERATOR ACTIONS WOULD BE ' REQUIRED TO LOAD SAFETY-RELATED , EQUIPhENT. . ' * RESETTING OF THE MOTOR-CONTROL- CENTERS WOULD REQUIRE OPERATOR ' ACTIONS FROM OUTSIDE TIE CONTROL ROOM. . * TIE TEAM DETERMINED THAT THE SAFETY SIGNIFICANCE OF THIS EVENT WAS HIGH ' BECAUSE A COMMON CAUSE FAILED REDUNDANT TRAINS OF SAFETY-RELATED EQUIPAENT. l 5 l I . _ - _ .
, ; i 'l'. DIESEL-GENERATOR SEQUENCER: LOGIC 1 ., . ; +125YDC ! ' CLOSES WHEN DIESEL f CLOSES ON SAFETY ' OUTPUT BREAKER CLOSES / INJECTION SIGNAL ./ CLOSES , ' / f WHEN TIMER j RELAY STARTS P ! CLOSES WHEN SL A VE REL A Y ; , JEGSAA : y X4 l- DE-ENERG/ZES / l
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l / / ' OPENS //2SECOND ; AFTER T/MER RELAY: STARTS , t [ t MASTER ATC TIMER SLAVE l ; RELAY l RELAY RELAY , .; 3EGSAA 3EGSAA- ' : X 762EGSAA X4 ' y i , 9 , . k e , 9 COMMON l ! t c . - -,
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l i ; * A NUMBER OF BENCH AND INSITU TESTS ! WERE PERFORMED TO DETERMINE THE j CAUSES OF THE EQUIPMENT FAILURE. : ! ; * DIODES WERE INSTALLED AROUND T11E ; SLAVE RELAYS TO REDUCED THE MAGNITUDE- i OF THE VOLTAGE SPIKES CAUSED BY THE l DROPOUT OF THESE RELAYS. > * THREE ATC TIAER\ RELAYS IN THE ! ' SEQUENCER WERE REPLACED WITH NEW TIMER / RELAYS. ; ; * POST MODIFICATION TESTING IDENTIFIED A ! ' PROBLEM WITH THE AUXILIARY FEEDWATER PUMP STARTING LOGIC. : * ADDITIONAL SEQUENCER AND PUMP _ l STARTING LOGIC DESIGN CHANGES WERE l ! REQUIRED TO ELIMINATE T11E AUXILIARY. FEEDWATER PUMP LOGIC PROBLEM. ' t * EXTENSIVE POST MODIFICATION TESTING OF THE LOAD SEQUENCERS WAS CONDUCTED TO i DEMONSTRATE OPERABILITY AND' : RELIABILITY. , ; 6 q ,
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: *i : ^ GENERIC IMPLICATIONS , ! . . * THE LICENSEE REVIEWED DESIGN CHANGES MADE TO BOTH BEAVER VALLEY 1 AND 2 TO VERIFY NO SIMILAR CONDITIONS EXISTED. j . ! . * A DESIGN CHANGE MADE TO THE r RECIRCULATION SPRAY PUMP LOGIC WAS ; IDENTIFIED AS CONTAINING SIMILAR ATC - TIMER / RELAYS. ! r * THE SPIKES IDENTIFIED IN THE ) RECIRCULATION SPRAY PUMP LOGIC WERE : DETERMINED TO NOT AFFECT ATC l TIMER / RELAY OPERATION. , ! . . . * THE NRC IS CURRENTLY PLANNING TO ISSUE AN INFORMATION NOTICE DESCRIBING.THIS ! EVENT. I i l I 7 .1 l ! ! l
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..4
- COMMITMENTS : -i ! * . A FAILURE ANALYSIS WILL BE CONDUCTED ON AN ATC TIAER/ RELAY. { ' * THE FEASIBILITY OF ADDITIONAL SEQUENCER TESTING WILL BE INVESTIGATED. ; .; * THE QUALIFICATION PACKAGE FOR TIE ATC TIAER/ RELAYS WILL BE UPGRADED. ; * AN EVALUATION OF POST MODIFICATION ; TESTING WILL BE CONDUCTED. .j * ENGINEERING GUIDELINES FOR. l REPLACEMENTS WITH DIGITAL SOLID STATE ; COMPONENTS WILL BE DEVELOPED. : l , , , 8 ; ;
. . _ - , - . CONCLUSIONS ^ !
e' THE MODIFICATION THAT INSTALLED THE
MODEL 365A, ATC TIMER / RELAYS WAS ! INADFQUATE. ! '
- A WE AK TECHNICAL UNDERSTANDING OF TIE
MODEL 365A TIMER / RELAY LIMITATIONS, j APPLICATIONS AND SPECIFICATIONS BY THE ENGINEERING DEPARTMENT WAS TIE ROOT ! CAUSE FOR THIS FAILURE. ! :
- THE CORRECTIVE ACTION THAT INSTALLED !
DIODES TO SUPPRESS TI-E VOLTAGE SPIKES ! WAS ACCEPTABLE. i ,
- TROUBLE-SHOOTING ACTIVITIES AND ll
TESTING FOLLOWING THE FAILURE WERE j POORLY PLANNED AND WERE FREQUENTLY NOT FORMALLY DOCUAENTED. , . ^
- THE QUALIFICATION DOCUMENTATION FOR
THE ATC TIAER/ RELAYS WAS INCOMPLETE. -
- TIE CORRECTIVE ACTIONS TAKEN IN
RESPONSE TO THE PREVIOUS CLOCK CIRCUIT FAILURE WERE APPROPRIATE AND WERE INDEPENDENT OF T11E CURRENT FAILURE. 9 - ! i
.
: . : ENFORCEMENT ACTIONS : . ; * AN NRC ENFORCEMENT CONFERENCE WILL : BE SCHEDULED TO DISCUSS THE EVENTS AND CIRCUMSTANCES SURROUNDING THE 1 FAILURE OF THE EMERGENCY DIESEL , GENERATOR LOAD SEQUENCERS. ; . $ , a : ! ! ! , , i : 10 : , ,
. - Figure 1 > " 12241-E-12A Sh.1 (Simplified) - Before Modification t 3_ TDO /'! ] /52S. ENSAC EGS y/ 2 Soc 74 '162 ! AAX5 - - - - 52S. EGS\ -- ECPAA , kt-- :AA tI -- l 1 .# IX1 SIS L. ClO ~ 1 ; K610XA I 125 T- K618XA g Sc2 3 _z69- 1 2 ww gg [[ EGSAA GSAA /-EGSAA __ y _ __ { w' . ..... . . . . . . . . . . . ~...... .... l _ , _ j : /- gg, -- / EGSAA g TDO TDO / EGSAA ' l '. 3 3 DD 762 3- 862- 162- j O FI ', EGSAA EGSAA EGSAA EGSAA EGSAA EGSAA f t..... .......: j X XS m X4j W RXMH2 (Typical) X / ... ..... ... / 1 / ,7 - _ y/.EGS - 1- _/ 1- EGS _/ y EGS 1 _ f ,2 1- EGS _/ j EGS 1-' _/_. y 1- EGS AAX [ AAX AAX AAX AAX AAX l , TDC -- 162 . TDO _ _ 62 TDC -- 362 TDC -- 462 TDC 562.- TDC -- 662- , 15 Sec -- EGSAA 5 Sec -- EGSAA 20 Soc EGSAA 40 Sec -- EGSAA 60 See EGSAA_ 0.5 Sec -- EGSAA 125 g "d Step 4 ' Step 3 Step 5 Stop 6 Reset Stop 2 gg .
4 m.w ! !
" dB 182- ' EGSAAX1 c2h 3c2 EGSAA 4c2 EGSAA s62 EGSAA sc2 EGSAA EGSAA)
L m Xj X X X X
. Timers for 62,162,362,462,562,662 not shown '"jfy" , ,
. .____________-_._m._a -- - _osa .1-u -u =w _ ___m .......--m._.,.-mw ewe.,.~... ve-., _-w.. .g =,ev.r.. - - + - - e,.=. # w .we.e, =woew.v....+.-,ow-s- - es ow. r -r .,,,g.aw-w_,. -,,..c.w,, _ ww. r erw,,
. , .. . . Figure 2 - 12241-E-12A Sh.1 (Simplified) - After Modification ' 52S- TDO j - f ENSAC ./- 2 Soo , - l102. g 3 - 52S- :EGS{ - -- ECPAA - Imt -- !AA '\ l - SIS CIB -~ , 'j yj ii T- KG10XA 7- KGleXA I g _', SAA- - GSAA EGSAA b b b Removed ...... j . . . . . . . . . . . . . . ....... j _ __ I - Z 3- - 7G2- - 862- ! / N I l - gg, -- 74 <E E j i cos^^ 66 ' - ,. 3 6d .,e2 ee2 ,p 3 O R EGSAA EGSAA EGSAA ]{ EGSAA ]{ EGSAA ]{ ; t..... ........... ..... 2 X X5 m X4 m RXMH2 (Typten!) EGSAAI][/ X ,/ j ~ - ~ ~ EdS y EdS EdS ' EdS EdS' EdS AAX AAX AAX AAX AAX AAX l / i TDC -- 162 TDO -- 62 TDC -- 362 TDC -- 462 TDC 562 TDC -- 662 15 Sec - EGSAA 5 See -- EGSAA 20 Sec -- EGSAA 40 Soc -- EGSAA 60 Seo EGSAA 0.5 See -- EGSAA 125 " Step 4 Step 3 Step 5 Stop 6 Reset Step 2 ygg . \i 66 162 EGSAAX1 c2 EGSAA )( sc EG]2 4c2 EGSAA 3( ' 58h2 EGSAA) 3( oc2 EGSAA3( m X X) 2( X Xf .X \ 'Umers br G2,162,362,462,562,662 not shown ',"j,[**," -
._. , }}