ML20211Q579

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Insp Rept 50-412/99-07 on 990720-29.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering
ML20211Q579
Person / Time
Site: Beaver Valley
Issue date: 09/07/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20211Q563 List:
References
50-412-99-07, NUDOCS 9909150098
Download: ML20211Q579 (29)


See also: IR 05000412/1999007

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U.S. NUCLEAR REGULATORY COMMISSION

REGION I

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Licensee No. NPF-73

Report No. 99-07

Docket No. 50-412

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Licensee: Duquesne Light Company

Post Office Box 4

Shippingport, PA 15077

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Facility: Beaver Valley Power Station, Unit 2

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inspection Period: July 20 through 24,1999 - On Site

July 25 through 29,1999 - In Office Review

inspectors: Brian J. McDermott, Team Leader

Christopher G. Cahill, Reactor Engineer

Barry S. Norris, Senior Reactor Engineer

Geoffrey A. Wertz, Resident inspector

Approved by: Wayne D. Lanning, Director

Division of Reactor safety

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9909150098 990907

PDR ADOCK 05000412

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EXECUTIVE SUMMARY

A Special Team inspection was chartered to evaluate the operators' actions and equipment

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response following a diesel generator failure at Beaver Valley (BV) Unit 2 on July 16,1999. The

Team also reviewed the circumstances that resulted in biofouling of the safety-related service

water system before, and after, the electrical event. (The team charter and an event timeline

are included as attachments to this inspection report).

On the basis of its independent review, the Team agreed with the licensee's root cause

determinations regarding the diesel generator failure and the failure of operators to take the -

expected actions in response to a loss of seal cooling for two reactor coolant pumps (RCPs).

Although Duquesne Light Company (DLCo) had not completed its own review of the service

water degradation at the conclusion of the on-site inspection, the Team agreed that adequate

short term corrective actions had been taken to support restart of the plant.

The major findings and conclusions of this inspection were:

Operations

The BV Unit 2 operating crew failed to recognize that all seal cooling for two RCPs was lost and

consequently, they did not implement actions specified in an alarm response procedure to

. protect the seals. The importance of these actions was not emphasized in training or indicated

by the human factoring of the control room annunciators. The failure to implement this

procedure is a violation which has been entered in the licensee's corrective action program and

is being treated as a non-cited violation consistent with the NRC Enforcement Policy. The

operating crew did, however, respond well to a loss of one 4 kV emergency bus and effectively

mitigated potential equipment problems. (Section O1.2)

The licensee's 1997 Probability Risk Assessment shows that reactor coolant pump seal failures

contribute 50% of the total core damage frequency for BV Unit 2. This risk insight was not

previously used to identify improvements in plant procedures, operator training, or control room

alarm human-factors that would assist with mitigation of this risk significant event. (Section

01.2)

The licensee failed to develop procedures for loss of emergency power, as required by

Regulatory Guide 1.33 and the Technical Specifications. Although Operations department

personnel knew procedure guidance was lacking in this area, the " loss of bus" procedure had

not been identified as a required procedure. This violation has been entered in the licensee's

corrective action program and is being treated as a non-cited violation consistent with the NRC

Enforcement Policy. _ (Section 03.1)

Maintenance

Macro biological fouling (biofouling) in the service water piping that supplies the diesel generator

was not detected during a biocide treatment on July 7. Seven days later, a rapid and substantial

- - degradation of service water flow occurred during an unrelated diesel generator surveillance

' test. The management team was slow to understand the effects of the July 7 biocide treatment

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- for common mode failure and failed to protect EDG 2-1 from heat exchanger fouling. This series

of events resulted in Emergency Diesel Generator 2-2 being inoperable for longer than the 72-

hour allowed outage time of the Technical Specifications. Additionally, the initial plan for EDG 2-

2 operability restoration was incomplete, until challenged by the inspectors. This apparent

violation of Technical Speedications is being considered for escalated enforcement action.

(Section M2.1)

In 1995, the licensee developed a plan for the prevention of biofouling in the service water

system. Although plans for the type of biocide treatments were established, frequencies for

those treatments were not included in the plan. Subsequently, the licensee failed to perform

these treatments consistently and frequently enough to be effective. An increase in the Zebra

mussel population at the service water intake structure in 1998 was a missed opportunity to

identify this problem. This apparent violation of Quality Assurance requirements for Corrective

Action is being considered for escalated enforcement action. (Section M2.2)

The licensee failed to provide adequate acceptance criteria in its procedure for bulk chemical

treatments of the service water system. Specifically, the emergency diesel generators were not

monitored to assess the impact of biofouling dislodged during the treatment. The lack of

acceptance criteria, coupled with the simultaneous treatment of both service water trains,

created the potential for a common mode failure and a significant reduction in safety margins.

The failure to develop an adequate procedure for bulk chemical treatments is an apparent

violation of Quality Assurance requirements and is being considered for escalated enforcement

action. (Section M2.3)

On July 7, a chemistry technician failed to follow the procedure for sampling of the service water

system during a bulk chemical treatment activity. As a result, the intended biocide concentration

was not applied to the "A" train of service water. This failure to follow procedures is being

treated as a Non-Cited Violation, consistent with Appendix C of the NRC Enforcement Policy.

(Section M2.3)

Enoineerina )

The licensee identified the most probable cause of the EDG 2-2 failure on July 16 as an

intermittent control relay contact in the voltage regulator circuit. A questioning attitude

throughout the engineering evaluation and root cause analysis was observed, and the licensee

made effective use of the vendor support. The voltage regulator repairs and retest were

appropriate. Long term corrective actions recommended by the Event Response Team are

reasonable actions to prevent recurrence of the relay failure. (Section E1.1)

Equipment aligned to the 4 kV emergency bus that was affected by the EDG 2-2 failure

responded as expected during the low voltage condition which existed for approximately 75

seconds. The licensee's engineering evaluations for loads that were running, or received start

signals, were technically sound. In addition, electrical tests were used to confirm the condition

of the affected equipment. (Section E1.2)

The licensee conducted adequate troubleshooting of the EDG 2-2 local control switch anomaly

that resulted in an unexpected start. Intermittent contact resistance during operation of a local

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control switch was identified as the most probable cause, after other possibilities were

eliminated through testing and design reviews. Appropriate short term actions were completed

and, long term corrective actions will be addressed by the licensee's corrective action process.

(Section E1.3)

The safety-related 125 voit batteries and DC system responded normally during the loss of

power to their chargers. TS requirements for the DC distribution system were appropriately

implemented. The licensee's engineers provided a reasonable assessment of the batteries'

performance during this event and concluded that the battery discharge rates were within their

design. An inspector followup item was opened to review the DC system's capability during a

loss of battery charging event that requires a plant shutdown. (Section E1.4)

The licensee appropriately evaluated the operational condition of the reactor coolant pump seals

after the loss of all seal cooling (concurrent loss of both seal injection and thermal barrier flow).

Based on plant data taken before, during, and after the event, the licensee determined no

significant heat up of the seals occurred. (Section E1.5)

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TABLE OF CONTENTS

EXEC UTIVE SU MMARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . i1

Summary of Plant Status . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1, Operat ions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 General Comments on the Event . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.2 Operators' Response to the Event . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

03 Operations Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

03.1 Lack of a Procedure for the Loss of an Emergency Bus. . . . . . . . . . . . 4

11. M airite n a nce . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M2 Maintenance and Material Condition of Facilities and Equipment. . ..... .... 5

M2.1 EDG 2-2 Service Water Flow Degradation . . . . . . . . . . . . . . . . . . . . . . 5

M.2.2 Program for Prevention of Macro Biological Fouling . . . . . . . . . . . . . . 7

M2.3 Service Water Chemical Treatment Procedure . . . . . . . . . . . . . . . . . . . 9

ll!. Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 1

E1 Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ....... 11

E1.1 Root Cause Determination for EDG 2-2 Failure . . . . . . . . . . . . . . . , . 11

E1.2 Effects of Under Voltage on Emergency Bus 2DF . . . . . . . . . . . . . . 12

E1.3 ~ Unexpected Restart of EDG 2-2 . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

E1.4 - Loss of Charging for Battery 2-2 and Battery 2-4 . . . . . . . . . . . . . . . . 14 .

E1.5 Loss of Seal Cooling for Two Reactor Coolant Pumps . . . . . . . . . . . . 16

- V. Management M eetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

X1 Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

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LIST OF ACRONYMS USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

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ATTACHMENT A - SPECIAL INSPECTION TEAM CHARTER '

ATTACHMENT B - EVENT TIMELINE

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Report Details

Summary of Plant Status

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On July 14 at Beaver Valley (BV) Unit 2, the service water cooling flow to Emergency Diesel

Generator (EDG) 2-2 degraded to less than its design basis flow during a surveillance test. On

July 16, EDG 2-2 was started and synchronized to the grid through emergency bus 2DF for a

post maintenance test following the cleaning of its heat exchanger. During this test, a diesel

generator failure occurred which resulted in a loss of power to emergency bus 2DF and its

associated loads. The plant was shut down on July 18 after it became apparent that EDG 2-2

could not be declared operable within the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> period allowed by the Technical l

Specifications.

After completing a review of the equipment and operator issues associated with this event, i

Duquesne Light Company (DLCo) management concluded that the appropriate short term

corrective actions had been taken to support restart of the plant. On July 26, operators

commenced a reactor startup sequence for BV Unit 2.

1. Operations ,

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01 Conduct of Operations'

01.1 General Comments on the Event

NRC Region I management chartered a Special Team inspection to review tha l

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circumstances surrounding the EDG failure of July 16. In addition, the Team was

chartered to review the biofouling discovered in the service water system on July 14 and

July 21. The Team's charter and a sequence of events are included with this report as

Attachments A and B, respectively. ,

An initial NRC assessment determined that the risk significance for a 2-hour loss of one j

4 kV emergency bus was a small reduction in safety margin. Operators restored RCP

seal cooling in less than three minutes and significantly decreased the associated risk of l

an RCP seal loss-of-coolant-accident. Likewise, EDG 2-2 being inoperable for l

approximately 5 days was determined to be of small risk significance. During the 5 day l

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period, the redundant EDG, off-site power, and a 4 kV cross-tie to BV Unit 1 were

available. This risk assessment, in part, was the basis for initiating the Special Team

inspection.

Based on the results of this inspection, the Team noted that the failure to implement an

adequate biofouling treatment program cculd have resulted in a common mode failure of

both EDGs, for a period of up to 14 days prior to detection. In this scenario only the off-

site power and the 4 kV cross-tie would have been available. An NRC assessment of

this scenario determined that it would result in a significant reduction in safety margins.

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' Topical headings such as Oi, M8, etc., are used in accordance with the NRC standardized ,

reactor inspecten report outline. Individual reports are not expected to address all outline topics.

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01.2 Ooerators' Response to the Event

a. Inspection Scope (93702)

The inspectors reviewed the operator recovery actions associated with the loss of one

4kV emergency bus. The assessment included reviews of the licensee's Event

Response Team (ERT) report, the operator logs, the sequence of events recorder, and

the station procedures. Additionally, interviews were conducted with the operators,

training instructors, the ERT members, and senior station management.

b. Observations and Findinos

On July 16,1999, BV2 was at 100% power, conducting a full load surveillance test of the

2-2 emergency diesel generator (EDG). At 5:29 pm, one of the tie breakers (2F7)

between the 4 kV emergency bus (2DF) and normal 4kV bus opened. The operators

subsequently observed low voltage on the 4 kV emergency bus and opened the EDG's

output breaker (2F10). This de-energized the 4 kV emergency bus and the "B" train of

emergency equipment. Of immediate concem were the loss of Battery Chargers 2-2 and

2-4 (requiring a TS 3.0.3 required shutdown), and the loss of the "B" charging pump for

inventory control and reactor coolant pump seal injection.

The crew correctly diagnosed the plant conditions and the Assistant Nuclear Shift

Supervisor (ANSS) prioritized the operators' actions. Specifically, the plant operator

(PO) was directed to attempt to restore electrical power to the 4 kV emergency bus, and

the reactor operator (RO) was told to restore charging. The "A" charging pump was

manually started and seal injection was restored within 2 minutes and 45 seconds. After

verifying that no faults were indicated on 4 kV emergency bus 2DF, operators restored

its normal power supply (approximately two hours later).

The ANSS recognized that there was no abnormal operating procedure (AOP) to

address the loss of s 4 kV emergency bus. After the plant was in a stable condition, the

ANSS directed the operators to review the control panels and to ensure that all of the

alarms were expected. During this event approximately 120 annunciators had alarmed.

The RO subsequently identified that cooling flow to the thermal barrier heat exchanger

had been lost for the "B" and "C" RCPs when their attemating current (AC) powered

supply valves were de-energized. The ANSS then told the Shift Technical Advisor to

review the alarm response procedure (ARP) for loss of seal injection. This ARP required

operators to immediately trip the reactor, and to secure the affected RCPs within 2

minutes. The ANSS informed the NSS of the missed actions. Based on the fact that

seal injection was recovered within three minutes, and following an initial review of RCP

parameters, the ANSS (with NSS concurrence) considered the RCPs operable and

concluded that the actions in the ARP were no longer required. The ANSS then

requested a formal engineering evaluation of the seals.

During NRC interviews, the operators stated that they were not aware of the potential for

loss of all seal cooling to certain RCPs, with the loss of a single 4 kV bus. Also during

interviews, the ANSS told the inspectors he knew that a concurrent loss of seal injection

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and thermal barrier flow required an immediate reactor trip. The inspectors concluded

that the failure to recognize that all seal coding was lost (and implement the required

immediate actions for protection of RCP seals) is significant and indicative of a weakness

in the training program.

Notwithstanding the condition of the pump seals, the failure to implement the actions

contained in ARP A2-4D, " Reactor Coolant Pump Seal Trouble," for a concurrent loss of

seal injection flow and thermal barrier cooling flow is a violation of the Beaver Valley,

Unit 2 TS, Section 6.8.1, requiring the implementation of procedures. This Severity Level

IV violation is being treated as a Non-Cited Violation (NCV), consistent with Appendix C

of the NRC Enforcement Policy. This violation is in the licensee's torrective action

program as CR 991752. (NCV 50-412/99-07-01)

The licensee determined the root causes for the operators failing to reference the ARP

were: (1) there was no mechanism to aid in identifying alarms that require prompt

operator actions, and (2) the operation's standard for response to a multi-alarm event did

not address prioritizing ARPs. Corrective actions included: (1) development of a

prioritization scheme for the annunciators, and (2) training on the new scheme with an

emphasis on the need to ensure that all annunciators are understood during an event.

These corrective actions were applicable to both Units.

The inspectors compared the actual plant response to that observed in the plant specific

simulator and noted no significant differences. After review of the ERT's final report

(issued July 24,-1999) and independent reviews, the inspectors concluded that the I

licensee had generally performed a good root cause evaluation. However, the

inspectors also considered the lack of training on the required, immediate actions to

protect RCP seals, and prevent an RCP seal LOCA, a significant problem.

The BV Unit 2 Probability Risk Assessment (PRA) Update Report, dated October 31,

1997, discussed the fact that a loss of both sources of cooling to the reactor coolant

pumps (RCPs) subjects the pump seals to full reactor coolant system temperatures. The

elevated temperatures cause a degradation of the RCP seals and would eventually lead

to a small break loss-of-coolant-accident (typically referred to as an RCP seal LOCA).

According to the licensee's PRA report, RCP seal LOCAs contribute 50% of the total

core damage frequency (CDF) for Unit 2. The inspectors determined that the licensee

did not effectively use this risk insight to improve the timeliness and reliability of

mitigating operator actions. Specifically this information had not previously been used to

improve procedures, training, or control room alarm human-factors.

c. Conclusion

The BV Unit 2 operat;ng crew failed to recognize that all seal cooling for two RCPs was

lost and consequently, they did not implement actions specified in an alarm response

procedure to protect the seals. The importance of these actions was not emphasized in

training or indicated by the human factoring of the control room annunciators. The failure

to implement this procedure is a violation which has been entered in the licensee's

corrective action program and is being treated as a non-cited violation consistent with the

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violation consistent with the NRC Enforcement Policy. The operating crew did, however,

respond well to a loss of one 4 kV emergency bus and effectively mitigated potential

equipment problems.

The licensee's 1997 Probability Risk Assessment shows that reactor coolant pump seal

failures contribute 50% of the total core damage frequency for BV Unit 2. This risk

insight was not previously used to identify improvements in plant procedures, operator

training, or control room alarm human-factors that would assist with mitigation of this risk

significant event.

03 Operations Procedures and Documentation

O3.1 Lack of a Procedure for the Loss of an Emeroency Bus

a inspection Scope (93702)

The inspectors determined that neither BV Unit had procedures for a loss of an

emergency electrical bus. The inspectors discussed the issue with station management,

assessed the immediate corrective actions, and performed an independent assessment

to determine if other procedures were required.

b. Observations and Findinos

As noted in Section O1.2 of this report, the ANSS knew there was no procedure to

address the loss of a 4 kV emergency bus. Through interviews, the inspectors lesmed

that operators and operations managers knew of this deficiency. The drafting of a " loss

of bus procedure" had been initiated several years ago, but was never finished.

NRC Regulatory Guide 1.33 (RG1.33), " Quality Assurance Program Requirements

(Operation)," lists typical procedures used at nuclear facilities, including loss of electrical

power. Technical Specification requirements for both BV Units require procedures to be

developed for activities covered in RG 1.33. After the inspectors discussed this with

licensee management, a CR was initiated. The licensee had not previously recognized ,

the lack of this procedure as a failure to meet their TSs. l

For corrective action, the licensee developed four AOPs for each Unit and trained all the

crews prior to them assuming the shift. The new procedures cover: Loss of 4kV

Emergency Bus, Loss of 480V Bus, Loss of Vital Bus, and Loss of 125VDC Bus.

The inspectors observed portions of the simulator development and validation of the )

AOPs, reviewed the final procedures and the associated training package, and

discussed the development of the procedures with plant management. The Plant

Manager indicated that further consideration will be given to adding more detail to these

initial procedure revisions based on future bench-marking with other utilities. The

inspectors considered the new procedures, training, and plans for bench-marking to be

acceptable.

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The inspectors also asked whether any other procedures required by RG 1.33, Appendix

"A", Section 6, were missing from either BV Unit. The licensee reviewed existing

procedures against the RG 1.33 list and concluded that no other procedures were

missing. The inspectors performed an independent review and no discrepancies were

identified.

Technical Specification Section 6.8.1, for both BV Units, requires written procedures to

be established covering the activities in Appendix "A" of RG1.33, Revision 2, February

1678. The failure to develop procedures required by Section 6.c of Appendix "A" of

RG1.33 is a violation of TS 6.8.1 for both Units. This Severity Level IV violation is being

treated as a Non-Cited Violation (NCV), consistent with Appendix C of the NRC

Enforcement Policy. This violation is in the licensee's corrective action program as

CR 991764. (NCV 50-334/99-07-02 & NCV 50-412/99-07-02)

c. Conclusion

The licensee failed to develop procedures for loss of emergency power, as required by

Regulatory Guide 1.33 and the Technical Specifications. Although Operations

department personnel knew procedure guidance was lacking in this area, the " loss of

bus" procedure had not been identified as a required procedure. This violation has been

entered in the licensee's corrective action program and is being treated as a non-cited

violation consistent with the NRC Enforcement Policy.

11. Maintenance

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 EDG 2-2 Service Water Flow Deoradation

a. Inspection Scope (62707,93702)

During a surveillance test for EDG 2-2 on July 14, operators found that the SW flow to

the EDG had decreased from about 1500 gpm to below the design basis minimum flow

of 1170 gpm after fifteen minutes. The EDG was declared inoperable and a

maintenance inspection discovered about 3 gallons of biological fouling (primarily Zebra

mussels) blocking approximately 90% the heat exchanger's tube sheet. The inspectors

reviewed the details of the event, the duration of the degraded condition, and the safety

implications associated with the cause of the degradation.

b. Observations and Findinos

On July 7, the licensee performed a bulk chemical treatment of the service water system

in accordance with procedure 2-OM-30.4.M, Revision 7, the treatment program for all

biofouling. On July 14, the initial flow of SW to EDG 2-2 during a surveillance test

resulted in the rapid accumulation of Zebra mussels in the EDG's heat exchanger. The

minimum SW flow to the EDG heat exchangers specified in the Updated Final Safety

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approximately 1070 gpm, prior to the operators stopping the test. EDG 2-2 was declared

inoperable on July 14 at 9:57 p.m. Sections M2.2 and M2.3 of this report provide

additional detail regarding the causes of this event.

Station management met on July 15, after cleaning the EDG 2-2 heat exchangers, to

develop a plan to restore EDG 2-2 to operable status. At the conclusion of this meeting, l

the approved post maintenance test required SW flow through EDG 2-2 for 30 minutes.

If SW flow remained above 1300 gpm at the end of the test, EDG 2-2 would be declared

operable. In addition, SW flow would be established through EDG 2-1 for 30 minutes per

day for one week to evaluate the potential for a common mode failure. The inspectors

determined that the EDG 2-2 restoration plan and EDG 2-1 monitoring plan were

incomplete. The acceptance criteria permitted flow degradation from the normal 1550

gpm to 1300 gpm in 30 minutes to be acceptable for EDG 2-2 operability. These plans

did not address the 7 day ECG mission time as described in the Updated Final

Safety Analysis Report (UFSAR). The acceptance criteria did not consider

appropriate heat exchanger flow characteristics. Specifically, SW flow would

appear normal as the first 20-40% of the tube sheet became fouled, but drop off

more rapidly as additional Zebra mussel shells accumulated to block the remaining

portion of the tube sheet. Station personnel had not identified the source of the

macro biological fouling and did not address the potential for further biological

fouling accumulation on various heat exchangers. The inspectors discussed these ,

issues with station management. The licensee agreed that the EDG restoration and

monitoring plans had been incomplete and required revision.

The revised SW flow test acceptance criteria did not include the effect of river

water level or SW system pressure on the minimal SW flow to the EDG heat

exchangers. When questioned by the NRC inspectors, the system engineer

developed a curve of system flow versus pressure which addressed these

parameters. However, this curve was not provided to operators until three days

after the monitoring period began. The inspectors determined that not having timely

and accurate acceptance criteria to support an operability determination was a

weakness. In addition, the management team was slow to understand the effects of the

July 7 biocide treatment for common mode failure. The July 22 biocide treatment,

performed to remove Zebra mussels and Asiatic clams from the SW system

inadvertently fouled the EDG 2-1 heat exchangers and made the EDG inoperable,

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Based on information from the licensee's engineers, and their consultant, Zebra mussels

are expected to detach from the piping within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> after the application of a toxic i

concentration of blocide. A toxic concentration was achieved in the "B" service water

header on July 7 at 1:00 p.m. (Section M2.3 discusses why a toxic concentration was not

achieved in the "A" header). However, the problem was only revealed after sufficient

flow to move the detached mussels occurred during the EDG 2-2 surveillance test.

Following cleaning and reassembly of the EDG 2-2 heat exchangers on July 16,

operators observed stable SW flow, sufficient to support EDG 2-2 operability. Based on

this information, the inspectors determined that EDG 2-2 was inoperable due to

inadequate SW flow from July 9 at 1:00 p.m. until July 16 at approximately 5:30 p.m.

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Technical Specifications (TS) 3.8.1.1 requires both EDG's to be operable with the mactor

in Operating Mode 1. The L!miting Condition of Operation for one EDG out of service

requires the EDG to be restored to an operable condition within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Contrary te

the above, EDG 2-2 was inoperable from July 9 until July 16 due to inadequate SW fi . -

with the reactor in Operating Mode 1. The failure to meet TS 3.8.1.1 is an apparent

violation. (eel 50 412/99 07 03)

c. Conclusions

Macro biological fouling (biofouling) in the service water piping that supplies the diesel

generator was not detected during a biocide treatment on July 7. Seven days later, a

rapid and substantial degradation of service water flow occurred during an unrelated

diesel generator surveillance test. The management team was slow to understand the

effects of the July 7 biocide treatment for common mode failure and failed to protect EDG

2-1 from heat exchanger fouling. This series of events resulted in Emergency Diesel

Generator 2-2 being inoperable for longer than the 72-hour allowed outage time of the

Technical Specifications. Additionally, the initial plan for EDG 2-2 operability restoration

was incomplete, until challenged by the inspectors. This apparent violation of Technical

Specifications is being considered for escalated enforcement action.

M2.2 Proaram for Prevention of Macro Bioloaical Foulina

a. Insoection Scope (62707,93702)

l

The service water system has periodically been treated for biofouling since 1995. On '

July 7, the service water system was chemically treated. Seven days later, EDG 2-2 was

declared inoperable after a rapid service water flow reduction occurred during a

surveillance test of the EDG. Subsequent inspection of the EDG's heat exchanger

revealed an accumulation of Zebra mussels that had been dislodged from the service

water piping by a chemical treatment performed on July 7. The inspectors reviewed the

licensee's program for prevention of biofouling, the availability of industry information,

and potential precursors for this event,

b. Observations and Findinas

in 1990, the licensee recognized the potential for the plant to be affected by Zebra

mussels and pro-actively assigned an individual to obtain industry information and

develop a comprehensive strategy. Information was gathered from industrial sites in

proximity to the Beaver Valley plant and from plants that were experiencing more

advanced Zebra mussel infestations. A Zebra Mussel Working Group was formed which

included representatives from Operations, System Engineering, Chemistry and an

outside consultant. The group completed a Zebra Mussel Control Plan at the same time  ;

the first Zebra mussel was identified at the intake structure in October 1995. l

The 1995 Zebra Mussel Control Plan included cleaning the service water intake bays, I

routine biocide treatments and bulk blocide treatments. The proposed " routine" blocide

treatments consisted of short duration applications (2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />), performed several times  ;

4

1

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d

8

per week, to prevent immature mussels from attaching and growing within the piping

system. The " bulk" treatments were intended to kill any attached mussels before they

grew large enough to affect service water system components. The plan also identified

the optimum river water temperatures for Zebra mussel growth. However, the Working

. Group did not establish requirements for the scheduling or frequency of the bulk

treatments. The inspectors also noted that the plan did not contain any measures to

assess or validate the effectiveness of the treatments.

A sharp increase in Zebra mussel density at the service water intake bays was identified

by the licensee in February 1998 and was documented in CR 980451. The Zebra

Mussel Working Group was convened to re-assess the 1995 recommendations.

However, the inspectors determined that the recommendations did not change based on

a review of the meeting minutes and discussion with the group's leader.

The mussels removed from the EDG 2-2 heat exchanger were up to 1.25 inches in

length. The licensee, with the help of a consultant, determined these mussels were  !

approximately 1.5 years old (indicating they originated around February 1998). The j

licensee's review of the biocide treatment over the past 2 years found that the routine

biocide treatments were not consistently performed. In addition, the bulk biocide

treatments, such as the one performed on July 7, were not being performed frequently

enough to be effective. From 1995 to 1997, the Unit 2 service water system received 1

two treatments per year. In 1998 and this year, only one treatment was performed.

The inspectors determined that the Zebra Mussel Control Plan and Working Group's

meeting minutes both reflected a good awareness of industry experience. However, the

licensee did not take adequate steps to implement the corrective actions outiined in the

Zebra Mussel Control Plan in that the frequency for application of the routine and bulk

biocide treatments was not specified. In addition, the 1998 increase in Zebra mussel

population at the service water intake structure was a missed opportunity to identify the

need for more prescriptive action. The failure to implement adequate corrective actions

to prevent the intrusion and accumulation of Zebra mussels in the service water system

is an apparent violation of 10 CFR 50, Appendix B, Criterion XVI, " Corrective Actions."

(eel 50-412/99-07-04)

Senior site management involvement after the plant shutdown on July 18 resulted in a I

more focused review of the biocide program. Emphasis was placed on protecting safety i

related trains in the future by not treating both trains simultaneously. These deficiencies

and other improvements were identified and captured in CR 991848. Although the

details of the licensee's long term corrective action plans were not available at the close

of this inspection period, reasonable short term actions, which included multiple bulk ,

I

biocide treatments of the service water and EDG branch lines with flushing, cleaning and

extended flow monitoring, had been implemented to ensure service water system

operability for restart of the plant.

.

.

9

c. Conclusions

in 1995, the licensee developed a plan for the prevention of biofouling in the service

water system. Although plans for the type of biocide treatments were established,

frequencies for those treatments were not included in the plan. Subsequently, the

licensee failed to perform these treatments consistently and frequently enough to be

effective. An increase in the Zebra mussel population at the service water intake

structure in 1998 was a missed opportunity to identify this problem. This apparent

violation of Quality Assurance requirements for Corrective Action is being considered for

escalated enforcement action.

M2.3 Service Water Chemical Treatment Procedure

a. Insoection Scope (62707,93702)

On July 14, a rapid and significant service water flow degradation occurred in the EDG 2-

2 heat exchanger due to an accumulation of biofouling (primarily Zebra mussels). The

inspectors reviewed the chemical treatment procedure (2-OM-30.4.M, Revision 7) to

evaluate the adequacy of the procedure and the controls applied to this maintenance

activity.

b. Observations and Findinas

The service water system at Beaver Valley Unit 2 consists of two redundant trains. Each

train consists of a 36 inch main header that supplies large heat loads and a 12 inch

branch line that supplies smaller safety-related loads such as the EDGs, safeguards

area room coolers, and the control room ventilation. EDG 2-1 and 2-2 are supplied from

the "A" and "B" service water headers, respectively.

The service water system chemical treatment process is initiated by injecting a biocide

(Betz Deabom Powerline 3627) into the "A" and "B" service water pumps' suction. After

the biocide injection is started, its concentration is adjusted based on samples taken

from the main service water headers, downstream of the component cooling heat

exchangers. Operators then align various standby heat exchangers for flow so that they

are treated with the biocide. This process did not provide for flushing of standby heat l

exchangers (including the EDGs') following exposure to the blocide.

On July 21, after the plant was shut down, the licensee performed another bulk biocide

treatment of the service water system. On July 22, service water flow was established

through EDG 2-1 and its heat exchanger rapidly became fouled with Zebra mussels. i

The licensee did not expect this to hapoen because they believed the biofouling was an

isolated problem in the "B" service water header's branch line to EDG 2-2.

i

Subsequently, the licensee realized that on July 7, a chemistry technician failed to follow

the procedure for sampling of the service water system during a bulk chemical treatment '

activity. As a result, the intended blocide concentration was not applied to the "A" train of i

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10

service water. This error was fortuitous because it precluded the simultaneous

degradation of both emergency diesel generators. However, this error was the result of

a procedure violation.

Chemistry procedure C.M. 2-3.79C, " Service Water System," Revision 1, requires

personnel to " contact the control room to determine which (CCP) heat exchanger (s) are

in service..." when sampling the service water system. On July 7, the technician did not

contact the control room and incorrectly presumed which heat exchangers were in

service. The failure to follow procedures for maintenance on safety-related equipment is

a violation of T.S. 6.8.1.a. This Severity Level IV violation is being treated as a Non-

Cited Violation, consistent with Appendix C of the NRC Enforcement Policy. This

violation is in the licensee's corrective action program as CR 991801.

(NCV 50 412/99-07-05)

The inspectors' review of the chemical treatment procedure found that it did not provide

quantitative or qualitative acceptance criteria that would ensure required flow to the

EDGs after the bulk biocide treatments. Cumulatively, the licensee's failure to properly

implement the treatment program, coupled with the procedure guidance that called for

simultaneous treatment of both service water headers, created a credible potential for

common mode failure of the EDGs. Monthly surveillance tests for the EDGs are

performed on a staggered basis (one EDG is run every 14 days). Because the bulk

treatments were not scheduled in relationship to the EDG surveillances,14 days could

have passed before a routine EDG surveillance would have detected a common mode

problem.

The inspectors determined that a common mode service water system failure, coupled

with a 14-day period prior to discovery, would result in a significant reduction of safety

margins. It was fortuitous that EDG 2-2 was tested only 7 days after the bulk biocide

treatment; and, it was also fortuitous that both service water trains were not chemically

treated, as planned.

10 CFR 50 Appendix B, Criterion V, " Instructions, Procedures and Drawings," requires in

part, that, procedures include appropriate acceptance criteria for determining that

important activities have been satisfactorily accomplished. Chemical treatment

procedure 2-OM-30.4.M, Revision 7, did not contain quantitative or qualitative

acceptance criteria for service water flow to the EDGs nhor the treatment activity. The

failure to establish adequate acceptance criteria for tNa procedure is an apparent

violation of 10 CFR 50 Appendix B, Criterion V. (eel 50-412/99-07-06)

c. Conclusions

The licensee failed to provide adequate acceptance criteria in its procedure for bulk

chem! cal treatments of the senrice water system. Specifically, the emergency diesel

_ generators were not monitored to assess the impact of biofouling dislodged during the

treatment. The lack of acceptance criteria, coupled with the simultaneous treatment of

both service water trains, created the potential for a common mode failure and a

significant reduction in safety margins. The failure to develop an adequate procedure for

11

bulk chemical treatments is an apparent violation of Quality Assurance requirements and

is being considered for escalated enforcement action.

On July 7, a chemistry technician failed to follow the procedure for sampling of the

service water system during a bulk chemical treatment activity. As a result, the intended

biocide concentration was not applied to the "A" train of service water. This failure to

follow procedures is being treated as a Non-Cited Violation, consistent with Appendix C

of the NRC Enforcement Policy.

Ill. Enaineerina

E1 Conduct of Engineering

E1.1 Root Cause Determination for EDG 2-2 Failure

a. Inspection Scoce (93702.)

The inspectors reviewed engineering documents and field practices to assess the

licensee's root cause determination and corrective actions in response to the failure of

EDG 2-2 and tripping of the 4 kV tie breaker 2F7. In evaluating the licLnsee's response

to this event, the inspectors attended several licensee management meetings, system

engineering troubleshooting meetings, and reviewed the ERT report, and CR 991749

entitled " Loss of Unit 2,2DF Emergency Bus."

b. Observations and Findinos

Overall, the inspectors determined that the licensee's root cause analysis was conducted

in a professional and timely manner. The licensee's troubleshooting efforts were

hampered by the fact that they were unable to reproduce the failure during static testing

or subsequent EDG runs (loaded and unloaded). The voltage regulator and associated

~

sub-components performed properly during a half hour run on July 17,1999, and an ,

extended fullload run on July 21,1999. The licensee promptly sought support from

several vendors to assist in the diagnosis of the EDG failure. The licensee's

detemiination that the voltage regulator lost communication from the Signal Mixer Output

Card was independently supported by the vendors. The inspectors observed that the

licensee was very effective in the management of the vendor support.

The licensee concluded that the initiating eve. A was a loss of the voltage regulation due

to an intermittent control relay contact in the EDG 2-2 voltage regulator power amplifier.

The loss M the volta 0e regulation caused the generator output power factor to increase.

The increasing power factor resulted in a rise in ground current above the expected ,

setpoint value of protection relay 50-VF207G. This relay in turn opened the 2F7 tie j

, breaker, separating the emergency bus (2DF) and EDG from the nonsafety-related bus l

(2D) and %6 gde

l

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12

Through extensive engineering and troubleshooting the licensee determined that an

intermittent control relay contact in one of three control relays,90FC, 90X or 43(K1),

could have resulted in the observed event. The licensee replaced the three suspected

relays and retested EDG 2-2 (Work Order 99-213186-000). The inspectors reviewed the

retest requirements and observed portions of the retest and found the licensee's actions

to be acceptable.

The licensee recommended long term corrective actions under CR-991749. These

recommended actions include changes to the EDG monthly surveillance procedures that

will provide performance trending and monitoring for the suspected relays. Additionally,

the licensee has planned to perform a failure analysis for the removed relays and review

the results with the vendor to determine if additional preventive maintenance should be

incorporated.

c. Conclusion

The licensee identified the most probable cause of the EDG 2-2 failure on July 16 as an

intermittent control relay contact in the voltage regulator circuit. A questioning attitude

throughout the engineering evaluation and root cause analysis was observed, and the

licensee made effective use of the vendor support. The 'voltage regulator repairs and

retest were appropriate. Long term corrective actions recommended by the Event

Response Team are reasonable actions to prevent recurrence of the relay failure.

E1.2 Effects of Under Voltaae on Emeroency Bus 2DF

a. Inspection Scoce (93702)

The inspectors reviewed the actual response of electrical equipment powered from the

2DF bus during the EDG 2-2 failure and compared it to the expected response. The

inspectors also reviewed the licensee's investigation and final disposition regarding the

condition of equipment affected by this event.

b. Observations and Findinas

i

l

A low voltage condition existed on the 4 kV emergency bus (2DF) from the time the 4 kV

'

tie breaker automatically tripped until operators opened the EDG 2-2 output breaker.

The voltage on bus 2DF stabilized at approximately 2100 volts (% of rated voltage) and  !

lasted for a duration of approximately 75 seconds. The expected response of a motor to

a decrease in voltage would be to lose speed, stall or overload. At the start of the event,

Service Water Pump "B" and the Charging Pump "B" were running. During the low l

voltage condition the two pumps slowed down, as was expected. This was indicated by '

their respective control room alarms, "SWS HDR B PRESS LOW' and "RCP 21 A SEAL

INJ FLW LOW" l

During the transient, Safety injection Pump "B" and Component Cooling Pump "B"

received expected start signals and sequenced onto the bus due to the degraded

voltage condition. The licensee determined that the pumps' breakers closed and the

I

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13

pumps probably started, but did not reach full speed due to the low voltage condition.

During starting, the motors behave as constant ir ;sdance loads. This reduces the

starting current proportional to the motor terminal .< Mage. The fact that the motors did

not trip supports the licensee's evaluation that the motors probably started but did not

reach full a, peed. Extended operation of these motors at reduced voltage possibly would

have resulted in the motors tripping on over-current. Due to the short time that these

motors were operated in a low voltage condition, no over-current trips were observed.

In addition to the engineering evaluations, the licensee satisfactorily completed electrical

testing (bridge and megger checks) of the affected equipment under work orders 99

213211-000,9921259-000,99-123266-000 and 99-213267-000. The inspectors found

that the licensee's conclusions were technically sound and that they promptly confirmed

the condition of the affected equipment.

c. . Conclusion

Equipment aligned to the 4 kV emergency bus that was affected by the EDG 2-2 failure

responded as expected during the low voltage condition which existed for approximately

75 seconds. The licensee's engineering evaluatioi.: for loads that were running, or

received start signals, were technically sound. In addite electrical tests were used to

confirm the condition of the affected equipment. l

E1.3 Unexpected Restad of EDG 2-2

a. Inspection Scope (93702)

On July 16, EDG 2-2 unexpectedly started when its control circuit was placed in the local

control mode during recovery from the electrical transient. The inspectors walked down

portions of the EDG 2-2 starting system, reviewed engineering documentation, and

observed portions of the field investigation to assess the licensee's root cause

determination and corrective actions.

b. Observations and Findinas

On July 16, during the emergency bus 2DF degraded voltage event, EDG 2-2 was

manually secured from the control room by means of the emergency stop buttons.

Operators decided that the engine should be secured locally to minimize the possibility of

spurious restarts. An equipment operator was directed to place the " Auto - Local" switch

at the diesel control panel in the " Local" position. This is a two position switch that, by l

design, will block all automatic EDG start signals in the " Local" position. However, the l

EDG immediately restarted when the control switch was placed in the " Local" position.  !

Minutes later, the local control switch was retumed to the " Auto" position and the EDG  !

was secured from the control room.

The licensee promptly initiated an investigation of the event as described in the Event l

Response Team charter. The licensee conducted testing of the switch circuit (CR

991755 and wo* order 99-213246-001). The testing included wiring verifications and

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14

)

switch functional testing. Additionally, the licensee verified the functionality of the start

circuit by placing the local control switch in the " Local" position and inserting an

emergency start signal. The circuitry functioned as designed and did not start the

engine. The licensee determined that no deficiencies existed in the starting circuit or

local control switch.

The licensee concluded that a momentary breaking and remaking of the " Auto" contacts

occurred in the local control switch while it was being placed in the " Local" position. This

was identified as the most likely cause of the unexpected EDG start. Switch operating

technique may have caused the contact cycling. However, this could not be confirmed

based on interviews with the operator. The licensee initiated long term corrective actions

under CR 991748 to review this event, and proper switch operation technique, in

operator training.

The inspectors interviewed the system engineer and reviewed the test results against the

Updated Final Safety Analysis Report (UFSAR) logic diagram numbers 7.4-31 through

7.4-37 and EDG 2-2 elementary diagram numbers 10080-E-12K,12241-E-12M8 and

12241-E-12N9. The inspectors found the test results to be consistent with the diagrams,

c. Conclusion

The licensee conducted adequate troubleshooting of the EDG 2-2 local control switch

anomaly that resulted in an unexpected start. Intermittent contact resistance during

operation of a local control switch was identified as the most probable cause, after other

possibilities were eliminated through testing and design reviews. Appropriate short term

actions were completed; and, long term corrective actions will be addressed by the

licensee's corrective action process.

E1.4 Loss of Charoino for Batterv 2-2 and Batterv 2-4

a. Insoection Scooe (93702) .

l

The inspectors interviewed the system engineer and reviewed the event operations logs I

and surveillance test to determine if the battery performed as expected and if the

licensee properly executed the Technical Specification (TS) requirements for the DC

system,

b. Observations and Findinos

l

The loss of the emergency bus 2DF at 5:29 p.m. on July 16 resulted in the loss of power

to the chargers for two safety-related batteries. Batteries 2-2 and 2-4 supply vital buses

generally associated with the "B" train of safety-related plant equipment.

The licensee promptly recognized that this condition required a plant shutdown. A loss

of two battery chargers is outside the scope of TS requirements for the DC system, and

therefore TS 3.0.3 required operators to place the reactor in the " hot standby" condition

within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. Without the chargers, the batteries began discharging to supply their

15

respective DC loads. After approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, power was restored to the chargers.

However, neither battery could meet the operability limits of TS 3.8.1 and therefore the

plant shutdown continued. Battery 2-4 recovered to above the TS Category "B" limits for

operability after approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 8 minutes, and Battery 2-2 after about 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

and 43 minutes. The shutdown due to battery related problems was terminated at 10:18

p.m. on July _16.

The surveillance data available for this event was collected after the battery chargers

were returned to service and therefore loaded battery data was not captured. Post ,

discharge surveillances showed that Battery 2-2 pilot cell (#49) read 2.0055 VDC with a  !

specific gravity of 1.192, and Battery 2-4 pilot cell (#9) read 2.0135 VDC with a specific

gravity of 1.208. The licensee estimated that the load on the batteries during the three

hours of the event was approximately 150 amps for the 2-2 battery and approximately 40

amps for the 2-4 battery. These discharge rates are within the battery design, as

specified in the 125 volt DC Design Document (2-DBD-39, Revision 3, Section 5.1.1.b)

and the Updated Final Safety Analysis Report (Section 8.3.2.1.3).

The design basis for BV Unit 2 includes the ability to withstand the single failure of one

battery or one DC bus. During the July 16 event, two battery chargers became

inoperable and their associated batteries began to discharge. A TS 3.0.3 shutdown was

initiated in response to this event. At some point in time, the two batteries became

" inoperable" when their pilot cell voltage and specific gravity decreased below TS

requirements. However, during the July 16 event both batteries remained functional until

their chargers were restored. All of the instruments or relays powered from the batteries

remained in their apprcpriate state.

Battery 2-2 and 2-4 are designed for a 2-hour discharge under design basis accident

conditions. If the battery chargers are not recovered, it may be possible for the two

batteries to discharge below the point of being functional during the 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> that TS 3.0.3 I

would allow to reach hot standby, This issue was discussed with licensing and

engineering personnel during a conference call on August 5. The potential for two

batteries to become non-functional prior to completing the plant shutdown is being l

evaluated by the licensee. An Inspector Follow-up item will be opened to track NRC

review of the licensee's final evaluation. (lFl 50-412/99-07-07)

c. Conclusion

The safety-related 125 volt batteries and DC system responded normally during the loss

of power to their chargers. TS requirements for the DC distribution system were

appropriately implemented. The licensee's engineers provided a reasonable

assessment of the batteries' performance during this ewnt and concluded that the

battery discharge rates were within their design. An inspector follow-up item was

opened to review the DC system's capability during a loss of battery charging event that

requires a plant shutdown.

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E1.5 Loss of Seal Coolina for Two Reactor Coolant Pumos

a. Inspection Scooe (93702)

The inspectors reviewed the licensee's engineering evaluation for continued operation of

'ne reactor coolant pumps after the coincident loss of seal injection and thermal barrier

flow. The inspectors also conducted an independent assessment of the risk associated

- v&h the concurrent loss of both cooling sources.

b. phy rvations and Findinas

After restoring charging flow using the "A" charging pump, operators discovered that

both seal injection and thermal barrier cooling had been lost for almost three minutes to

the "B" and "C" RCPs. An engineering evaluation was performed based on

temperatures and flows recorded before and after the event.

RCP A RQ_P_R RCP Q Qng

Pre-Event Readina (a 5:00 om)

Seal #1 leakoff temperature: 150 165 167 <210*F

Pump bearing temperature: 126 139 131 <184*F

Seal #1 leakoff flow: 2.4 2.3 2.7 1 - 5 gpm

Event and Post-Event Maximum Temperatures

and Minimum Flow (5:29 om- 9:00 nm)

Seal #1 leakoff temperature: 153 175 175 <210*F ,

Pump bearing temperature: 130 148 139 <184*F l

Seal #1 leakoff flow; 2.2 1.7 2.5 1 - 5 gpm l

Post-Event Steadv State Readinas (10:00 om)

Seal #1 leakoff temperature: 147 167 167 <210*F

Pump bearing temperature: 123 138 132 <184*F

Seal #1 leakoff flow: 2.5 2.3 3.0 1 - 5 gpm

Pre and post-event readings were consistent, and the transient readings were well within

the allowable limits. In addition, the licensee ensured that the limits being used for the

allowed time without seal injection and thermal barrier flow were consistent with the

guidance provided by the vendor (Westinghouse) and an independent contractor

(Brookhaven National Laboratory). The licensee's evaluation concluded that the RCP

seals and the pump bearings suffered no consequences from the short duration loss of

cooling. The inspectors assessed the engineering evaluation, independently reviewed

the pump parameters and the vendor and contractor recommendations, and considered

the conclusion to be acceptable.

17

The inspectors noted the BV Unit 2 RCP seals have high-temperature O-rings and

floating ring sea!s. This information has not been credited in the Unit 2 Probability Risk

Assessment. The extent to which these components may have played a roll in the

minimal change in seal temperatures and seal leakoff had not been evaluated by the

licensee at the conclusion of the inspection. The licensee's efforts for the short term

were focused on the current seal condition. During the Nuclear Safety Review Board

review of the ERT report, the licensee's design engineers indicated that a re-evaluation

of the CDF contribution for RCP seal LOCAs would be considered. The licensee's

preliminary evaluation indicated that the RCP seal LOCA contribution to CDF should be

reduced. The licensee's final evaluation of the RCP seal performance during this event

will be reviewed by the NRC at a later date. (IFl 50-412/99-07-08)

The ERT identified that the component cooling supply valves for the RCP's thermal

barriers are DC powered at BV Unit 1. This design difference woul'd preclude the total

loss of RCP seal cooling should a loss of one 4 kV emergency bus occur on Unit 1.

Condition Report (CR) #991818 was initiated to review the potential design deficiency at

Unit 2. As an immediate corrective action, the associated surveillance test procedures

were revised to ensure the in-service charging pump is powered from the opposite train

during EDG testing.

c. Conclusion

The licensee appropriately evaluated the operational condition of the reactor coolant

pump seals after the loss of all seal cooling (concurrent loss of both seat injection and

thermal barrier flow). Based on plant data taken before, during, and after the event, the

licensee determined no significant heat up of the seals occurred.

V. Manaaement Meetinas

X1 Exit Meeting Summary

The team met with licensee representatives periodically throughout the inspection and at a

debriefing prior to leaving the site. Following the in-office review of materials collected during

the inspection, and exit meeting was conducted on July 29,1999 by telephone call. At that time,

the purpose and scope of the inspection were reviewed, and the preliminary findings were

presented. The licensee acknowledged the preliminary inspection findings.  ;

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18

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

eel 50-412/99-07-03 Diesel Generator Inoperable for Longer Than 72-hours

eel 50-412/99-07-04 Failure to Implement Corrective Actions for Biofouling

eel 50-412/99-07-06 Inadequate Procedure for Chemical Treatment

IFl 50-412/99-07-07 Battery Capability During Shutdown for Two Inoperable Chargers

IFl 50-412/99-07-08 RCP Seal Performance During July 16,1999 Loss of Seal

Cooling

Ooened/ Closed

NCV 50-412/99-07-01 Failure to implement Alarm Response Procedure

NCV 50-412/99-07-02 Failure to Develop Procedure for Loss of Emergency Power

NCV 50-412/99-07-05 Failure to Follow Procedura for Service Water Sampling

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LIST OF ACRONYMS USED

AC Altemating Current

ANSS Assistant Nuclear Shift Supervisor

AOP Abnormal Operating Procedure

ARP Alarm Response Procedure

'BV Beaver Valley

CDF Core Damage Frequency

CFR Code of Federal Regulations

CR Condition Report

DBD Design Basis Document

DC Direct Current

DLCo Duquesne Light Company

EDG Emergency Diesel Generator

eel Escalated Enforcement item

ERT Event Response Team

IFl inspector fo!iow-up item I

kV kilovolt  !

LCO Limiting Condition for Operation I

LOCA Loss of Coolant Accident

NCV Non-cited Violation

NNS Nuclear Shift Supervisor

NRC Nuclear Regulatory Commission

PO Plant Operator

PRA Probability Risk Assessment

RCP Reactor Coolant Pump

RO Reactor Operator

RPS Reactor Protection System

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI unresolved item

VIO ' Violation

I

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.

ATTACHMENT A '

July 23,1999

MEMORANDUM TO: Wayne D. Lanning, Director, Division of Reactor Safety

A. Randolph Blough, Director, Division of Reactor Projects

FROM: Hubert J. Miller ORIGINAL SIGNED BY:

Regional Administrator

SUBJECT: SPECIAL INSPECTION TEAM CHARTER - FAILURE TO TRIP

REACTOR AS REQUIRED BY ALARM RESPONSE

PROCEDURE AND MULTIPLE EQUIPMENT PROBLEMS AT

BEAVER VALLEY UNIT 2

You are directed to perform a Special Team Inspection review of the causes, safety implications,

and associated licensee actions which led to multiple equipment problems and the failure of

operators to trip the reactor as required by an alarm response procedure at Beaver Valley Unit 2

on July 16,1999. The basee for the NRC concern involve several equipment and operator

performance issues that are not currently understood.

DRS is assigned responsibility for the overall conduct of this inspection. DRP is assigned

responsibility for resident inspector and clerical support and coordination with other NRC offices.

Brian McDermott is designated as the onsite Team Leader. Team composition is described at

the end of this memorandum. Team members will work for Mr. McDermott and are assigned to

this task until the report is completed.

OBJECTIVES

The general objectives of this team inspection are to:

a. Conduct a timely, thorough, and systematic review of the circumstances surrounding the

events, including the sequence of events that led to and followed the July 16,1999, loss

of the 2DF emergency bus which resulted in the interruption of RCP seal water flow and

thermal barrier cooling.

b. Collect, analyze, and document relevant data and factual information to determine the

conditions and circumstances surrounding these equipment and operator performance

issues, and the appropriateness of the response to the events by the licensee's

operating staff.

c. Investigate the equipment issues which occurred prior to, during, and after the loss of the

emergency bus; including failures or problems with the EDG, emergency bus and

, breakers, service water flow, battery and chargers, and reactor coolant pump seal

cooling flow.

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Wayne D. Lanning - 2

A. Randolph Blough l

d. Assess the safety and risk significance of the events and communicate to Regional and  !

Headquarters management the facts and any safety concems related to the problems

identified.

e. Evaluate licensee management's review of and response to the events and corrective

actions taken.

SCOPE OF THE INSPECTION

The team should identify and document the relevant facts and determine the probable causes of

the events. It should also critically examine the licensee's response to the event.

The team should:

a. Develop a detailed chronology of the events.

b. Identify safety issues, problems and concerns with equipment, personnel performance,

processes and procedures, and management response.

Potentialitems to be considered:

e Licensee staff actions before, during, and following the events, including operator

actions, procedure adequacy and usage during a loss of RCP seal cooling.

e' Configuration controls, including previous modifications, and event related

system alignments.

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e Management oversight and administrative controls in place be'iore, during, and

following the events.

l e Coordination of maintenance and operations activities before and during the l

l events.

l e Adequacy and implementation of troubleshooting procedures.

c. Determine the root causes of the events, where practicable, as a result of the team's

l evaluation and document equipment problems, faiiures, and/or personnel errors which

i directly or indirectly contributed to the event or complicated the response.

d. Determine the expected response of the plant due to the loss of the vital bus and

compare it to the actual response.

e. Determine the adequacy of the initial responses of the operations and technical support

staffs to the events.

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f. Determine the effectiveness of the Event Review Team (ERT) assessment and

evaluation of the events and the subsequent technical specification required shutdown,

including the ERT effectiveness in communicating the results to licensee management.

g. Understand the scope and direction of the licensee's ERT. Assess the quality of the

investigation, including disposition of issues and findings of the ERT. Determine

management's use of ERT findings relative to restart of Unit 2, continuing operation of

Unit 1, and identification of effective corrective actions.

h. Determine the relationship of previous events or precursors, if any, to this event,

including actions taken to address service water heat exchanger fouling by clam and

musse shells,

i. Verify that the licensee has identified and effectively addressed issues that affect start-up

of Unit 2 and the continuous operation of Unit 1.

J. Determine the potential generic implications of this event.

CONDUCT OF THE INSPECTION

The team should understand the scope and direction of the licensee's investigation and

assessments of the events, and their initial response. Through sampling and independent

verification, the team should use information collected by the ERT. The pace and nature of

team activities should be gauged to assure its assessments are independent of the licensee's

and that, where practicable, they do not unduly impact licensee efforts.

SCHEDULE

The Special Inspection Team shall be dispatched to Beaver Valley, Unit 2 so as to arrive and

commence the inspection on July 20,1999. A written report on this inspection shall be provided .

to me within 45 days of completion of the onsite inspection. The team leader shall provide daily l

status calls to the team manager.

TEAM COMPOSITION

The assigned team members are as follows:

Team Manager: Wayne Lanning, DRS

Onsite Team Leader: B. McDermott, DRP

Onsite Team Members: B. Norris, DRS

C. Cahill, DRS

G. Wertz, DRP

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ATTACHMENT B

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Beaver Valley EDG 2-2 Cooling Degradation and Electrical Failure

Date Time Event

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7/7 Unit 2 service water (SW) trains "A" and "B" treated for biofouling

7/14 EDG 2-1 Surveillance Test (~ 2 hr. run), supplied by "A" SW train.

2132~ EDG 2-2 Surveillance Test begins, supplied >1500 gpm by "B" SW train.

2147 . Service water flow to EDG 2-2 decreases from initial reading to 1070 gpm

(1170 gpm design basis minimum flow)

2157 EDG 2-2 secured and declared inoperable, Technical Specification (TS) 72 hr

period to restore the EDG begins

7/15 1141 Three gallons of zebra mussels removed from the EDG 2-2 heat exchanger

7/16 1324 SW flow through EDG 2-1 initiated for confidence check based on zebra

mussels discovered in EDG 2-2

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1628 EDG 2-2 started and loaded to 4400 KW for post maintenance test following

heat exchanger cleaning

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1729 Normal power supply breaker to emergency bus 2DF trips open

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unexpectedly. Bus 2DF and EDG 2-2 voltage observed at half of normal.

1730 Operator opens EDG 2-2 output breaker based on degraded voltage and

l manually trips EDG from control room

1730 Emergency bus 2DF de-energizes, major equipment affected: running

j- charging pump "B" lost resulting in loss of all reactor coolant pump (RCP)

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seal injection flow; component cooling to "B" and "C" RCPs isolates; and

battery chargers for batteries 2-1 and 2-1 de-energized.

1730 Vital DC buses 2-2 and 2-4 auto swap to battery supply with no loss of

function.

TS 3.0.3 is entered due to loss of two battery chargers.

~1733 "A" charging pump manually started, seal injection flow restored to all RCPs.

1800 Emergency bus DF loads put in pull-to-lock in preparation for restoration.

1815 EDG 2-2 put in " Local" by operator at local panel and EDG auto starts.

Operator is unable to trip EDG from local panel. " Local-Auto" switch put back

in " auto" and EDG is secured from the control room

j 1912 Load reduction commenced for TS 3.0.3 required shutdown

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1941 Normal power restored to emergency bus 2DF and loads are restored during

the next 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

2030 Charger for Battery 2-4 restored

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2035 Charger for Battery 2-2 restored

2115 Batteries 2-2 and 2-4 tested. Did not meet TS Category "B" values required

for operability. TS 3.0.3 shutdown continued. j

2138 Battery 2-4 meets Category "B" allowable values.

TS 3.0.3 exited, TS shutdown still required for 1 battery inoperable.

2218 Battery 2-2 meets Category "B" allowable values.

Plant shutdown terminated, reactor power held at - 60%.

TS 72 hr clock for EDG 2-2 restoration still counting down.

7/17 2021 Plant shutdown continued, based on expectation that EDG 2 2 would not be

l restored within the TS allowable 72 hr period.

2157 TS 72 hr period to restore EDG 2-2 ends,6 hr clock to be in Hot Standby 4

begins.

7/18 0206 Plant is in Mode 3, Hot Standby

1721 Plant is in Mode 5, Cold Shutdown

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