ML20050B648

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Monthly Operating Rept for Mar 1981
ML20050B648
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 04/03/1981
From: Connell C
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML20050B647 List:
References
NUDOCS 8204070073
Download: ML20050B648 (6)


Text

.

OPERATING DATA REPORT DOCKET NO.

50-286 DATE 4-3-81 COMPLETED BY C. ConnoJ1 TELEPHONE ({14) 739-8200 OPERATING STATUS Notes

~ -

1. Unit Name: ndian Pnine__Nn_1 ni, clew pnrgy pinne
2. Reporting Period:

March 1981

3. Licensed Thermal Power (51Wt):

1025

4. Nameptste Rating (Gross $1We):

1013 S. Design Electrical Rating (Net 51We):

965 926

6. Sf aximum Dependable Capacity (Gross MWe):

891

7. Slaximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report. Give Reasons:

,c NONE

9. Power Level To Which Restricted. lf Any (Net 51We):

NA

10. Reasons For Restrictions. lf Any:

This Month Yr. to.Date Cumulative 744 2,160 40,201

11. Hours In Reporting Period
12. Number Of Hours Reactor Was Critical 6.0 734.7 27,484.7 0
13. Reactor Reserve Shutdown Hours

. 0 0

14. Hours Generator On Line 0

728.7 26,431.8 0

0 0

15. Unit Reserve Shutdown Hours 0

2,074,821 69,706,091

16. Gross Thermal Energy Generated (MWH) 0 604,010 22,195,511
17. Gross Electrical Energy Generated (MWH) 0 579,583 21,293;743
18. Net Electrical Energy Generated (MWH1 0

33.7 65.7

19. Unit Service Factor 0

33.7 65.7

20. Unit Availability Factor I 'q 0

30.1 M

21. Unit Capacity Factor (Using MDC Net) 0 27.8 a4.9 U
22. Unit Capacity Factor (Using DER Net) 100 66.3
  • -12.6
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date and Duration of Eacht:

^

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Ac'hihed '

INITIA L CRITICA LITY N/A N/A INITIAL ELECTRICITY N/A.__

N/A COMMERCIAL OPERATION N/A N/A s

NU I 040 00 OO2OJ O

R

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AVI:ItAGl: D AILY UNII l'0Wl:lt 1.1. VEL i

DOCKET NO.

Sn-28f.

leidi;in Poi nt UNIT 180.3 4-3-81 DATE COMPLETED BY C. Conne11 TELEPl!ONE 914-739-8200 f4 arch 1981 MONTil DAY AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)

(MWe Net) as O

j7 0

0 0

2 18 0

0 3

39 4

0 20 0

0 0

5 21 6

0 22 0

0 3

0 7

0 0

8 24 9

0 25 0

0 0

10 26 11 0

27 0

0 0

12 28 13 0

29 0

14 0

30 15 0

33 0

0 16 INS 7 RUCTIONS On this format. list the aserage daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77)

=

UNITSIIUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-286 UNIT NAME Indian Point Unit, 8.

DATE 4-1-91 REPORT MONTil March 1981 COMPLETED llY

c. connel1 TELErilONE (9141 733-8200 1

1 f*3 E. ?

3 Y

Licensee

,E-r, 1,

Cause & Corrective No.

Date g

gg g

jg5 Event g?

9 Action to

$E 5

H

3. i5 =g Report a mU EL Present Recurrence u

O 02 10131 P

744 A

3 N/A IIA Turbin One L-1 blade failed on the 31 low pressure turbine causing significant turbine blading and, condenser tube damage. Damaged turbine blades were repaired / replaced. All three low pressure turbines were inspected and any suspect blades sere replaced.

Damaged condenser tubes have been plugged.

I 2

3 4

F: Forced Reason:

Method:

Exhibit F Instructions S: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Data Il-Maintenance of Test 2 Manual Scram.

Entry Sheets for Licensee C Refueling 1 Automatic Scram.

Event Report (Ll'R) Fde(NUREG-i D Regulatory Restriction 4 O her(Explain) 0161)

E-Operaint Training & License Examinatiorr F Administrative 5

G-Operational Eirur (Explain)

Exhibit 11-Same Source P)/77)

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2HOffrilLY Malt 1TEllAt1CE REPORT March 1901 Honth

DATg, W.R.

8 EQUIPMEtrP MALFUNCTION CORRECTIVE ACTIOt1 3-03 I-1852 Component Cooling line flange Leaking Gasket Renewed Gasket to #34 RCP 2-25 I-1835 RCS Valve 455 B Gasket Leak Renewed Gasket 3-06 I-1854 Mov 536 Defective Limitorque Operator Renewed Operator 3-05 I-1857 CVCS Valve 1844/1846 Worn Packing Replaced Packing 3-07 I-1820 Valve 891 C Defective Ring Terminal Connection Renewed R1ng Terminal 3-07, I-1848 SI valve 887 B None Replaced oper, w/Enviornmentally Qualified Operator 2-18 I-1809

  1. 32 I A Compressor Compressor Knocks Readjusted Crosshead Clearances 3-03 I-1800 "34 RCS Standpipe Valve Valve leaked through Repaired valve 3-02 I-1849 32 Fan Cooler Unit Cooler Leak Repaired leak by soldering 2-28 I-1837 Prim. Sample Valve 955A Packing Leak Renewed Valve 2-24 I-1833 Polar Crane Crlmped Auxiliary Hook Cable Renewed Cable 2-26 I-1830 32 Boric Acid Transfer Pump Mechanical Seal Leaks Replaced Mechanical Seal and Pump Internals e

d

a a SUMfGRY CF OPEPATING EXPERZENCE MARCH 1981 Indian Point Unit 3 was shutdown for the entire reporting period.

Completed main turbine repairs, inspection, and reassembly. The reactor was brought critical on March 30 at 2135 hours0.0247 days <br />0.593 hours <br />0.00353 weeks <br />8.123675e-4 months <br /> and shortly there after shutdown because of " drifting

  • problems with the individual rod position indicators. This problem was resolved and the reactor brought critical again at 1943 hours0.0225 days <br />0.54 hours <br />0.00321 weeks <br />7.393115e-4 months <br /> on March 31.

As the main turbine was being brought up to speed there was a turbina trip on an electrical fault.

The fault was determined to be located in #32 nain transformer. The transformer is being disconnected in preparation for returning to service on #31 main transformer.

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