ML20207B605

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Forwards Corrected SALP Repts 50-245/85-98 & 50-336/85-98 for Mar 1985 - May 1986.Util Comments Re Refueling & Outage Mgt Area Valid.Category 1 Rating Assigned
ML20207B605
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 12/04/1986
From: Murley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Opeka J
NORTHEAST NUCLEAR ENERGY CO.
Shared Package
ML20207B611 List:
References
NUDOCS 8612110002
Download: ML20207B605 (2)


See also: IR 05000245/1985098

Text

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DEC 0 41986

Docket Nos. 50-245; 50-336

Northeast Nuclear Energy Company

ATTN: Mr. J. F.- Opeka

Senior Vice President - Nuclear

Engineering and Operations Group

P. O. Box 270

Hartford, Connecticut 06141-0270

Gentlemen:

Subject: Systematic Assessment of Licensee Performance (SALP) Reports 50-245/85-98

and 50-336/85-98, and Your Reply Letter Dated November 5, 1986

This refers to the Millstone Unit 1 and 2 SALPs for the period from March 1, 1985

through May 31, 1986. The SALP reports were initially forwarded to you by our

August 29, 1986 letter (Enclosure 1). On October 2, 1986, at a management meeting

on the Millstone site, we discussed the SALPs with you and your staff (see Enclo-

sure 2 for attendees). We have reviewed your written comments (Enclosure 3) and

herewith transmit the final SALP reports (Enclosure 4).

After the October 2, 1986 management meeting, we concluded that your comments about

assigning a grade to'the Unit 1 Refueling and Outage Management area were valid

and re-examined that area. After supplementing the observations with relevant

observations from other SALP areas, the SALP board assigned this area a Category

1 rating.

We noted your extensive comments on the Unit 1 Maintenance and Modifications area.

While we acknowledge the points you make, we still have an overall concern about

the scram solenoid valves, the main turbine mechanical pressure regulator, the

emergency gas turbine (EGTG), and the three scrams related to this area. We modi-

fied the SALP evaluation to reflect the role of faulty replacement parts on EGTG

performance, but our review also affirmed the Category 2 rating assigned to this

area.

For the Unit 2 SALP of the Plant Operations area, you commented that Licensee Event

Reports (LERs) need address failed components only when such failures occur. We

agree. As a matter of clarification, the NRC concern developed from the LERs re-

viewed is about identifying the manufacturer and model of failed components so that

information recipients can take more timely actions.

We have also made minor corrections to the SALPs. These did not result in any

changes in the associated SALP ratings.

We appreciate your responses to the SALP comments and your discussion of plans to

improve performance. Thank you for your cooperation.

Sincerely,

T

8612110002 861204 Drigi'nal signed by

PDR ADOCK 05000245 Ito as E. Murley,

O PDR Thomas E. Murley

_ Regional Administrator

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Northeast Nuclear Energy Company 2

DEC 0 41986

Enclosures:

1. NRC Letter, T. E. Murley to J. F. Opeka, Dated August 29, 1986

2. SALP Management Meeting Attendees, October 2, 1986

3. NNEco Letter, J. F. Opeka to T. E. Murley, Dated November 5,1986

4. Region I Systematic Assessment of Licensee Performance (SALP)

Report 50-245/85-98; 50-336/85-98

cc w/encis:

E. J. Mroczka, Vice President, Nuclear Operations

W. D. Romberg, Station Superintendent

D. O. Nordquist, Manager of Quality Assurance

R. T. Laudenat, Manager, Generation Facilities Licensing

Gerald Garfield, Esquire

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC) -

NRC Resident Inspector

State of Connecticut

Chairman Zech

Commissioner Roberts

Commissioner Asselstine

Commissioner Bernthal

Commissioner Carr -

Vandana Mathur, McGraw-Hill Publications (2 copies)

bec w/encls:

Region I Docket Room (with concurrences)

Management Assistant, DRMA (w/o encl)

DRP Section Chief

J. Shea, LPM, NRR

T. Murley, RI

T. Martin, RI

W. Kane, RI

S. Ebneter, RI

R. J. Bores, DRSS

J. Shediosky, SRI, Millstone 3

P. Swetland, SRI, Haddam Neck

! M. McBride, RI, Pilgrim

K. Abraham, RI (2 copies)

NRC Management Meeting Attendees

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ENCLOSURE 1

gf asc%'c, UNITED STATES

E " . ,., ^g NUCLEAR REGULATORY COMMISSION

j REGION I

0,, 531 PARK AVENUE

KING oF PRUSsl A, PENNSVLVANIA 194M

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Docket Nos. 50-245 MG29 N

50-336

Northeast Nuclear Energy Company

ATTN: Mr. J. F. Opeka

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Senior Vice President - Nuclear

Engineering and Operations Group

P. O. Box 270

Hartford, Connecticut 06141-0270

Gentlemen:

Subject: Systematic Assessment of Licensee Performance (SALP) Report Numbers

50-245/85-98 and 50-336/85-98

On July 28, 1986, the NRC Region I SALP Board reviewed and evaluated the perform-

ance of activities associated with the Millstone Nuclear Power Station, Units 1

and 2. These assessments are documented in the enclosed SALP Board Reports. You

will note that much of the performance analyses are the same for both units in the

arees of Radiation Controls, Emergency Preparedness, Security and Safeguards, As-

surance of Quality, and Training and Qualification Effectiveness. Common assess-

ments are included in both reports to make each unit's SALP Report complete.

A meeting at the site to discuss these assessments will be scheduled. That meeting

is intended to provide a forum for candid discussions relating to the performance

evaluation.

At the meeting, you should be prepared to discuss our assessment and your plans

to improve performance, particularly in the radiation protection area. Any com-

ments you may have regarding our report may be discussued at the meeting. Addi-

tionally, you may provide written comments within 30 days after the meeting.

Following our meeting and receipt of your response, the enclosed reports, your re-

sponse, and a summary of our findings and planned actions will be placed in the

NRC Public Document Room.

Your cooperation is appreciated.

Sincerely,

-.

Thomas E. Murley

Regional Administrator

Enclosures:

1. NRC Region I SALP Report 50-245/85-98

2. NRC Region I SALP Report 50-336/85-98

3. Northeast Utilities Letter B11979 dated March 13, 1986.

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Northeast Nuclear Energy Company 2

G291995

cc w/encls:

E. J. Mroczka, Vice President, Nuclear Operations

W. D. Romberg, Station Superintendent

D. O. Nordquist, Manager of Quality Assurance

R. T. Laudenat, Manager, Generation Facilities Licensing

Gerald Garfield, Esquire

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of Connecticut

bec w/encls:

Region I Docket Room (with concurrences)

Management Assistant, DRMA (w/o encl)

DRP Section Chief .

J. Taylor, IE

T. Murley, RI

S. Ebneter, DRS

T. Martin, DRSS

E. McCabe, DRP

E. Conner, DRP

D. Holody, RI

P. Lohaus, RI

J. Shea, NRR

D. Jaffe, NRR

SALP Board Members

DRS Branch Chiefs

DRSS Branch Chiefs

DRP Branch Chiefs

K. Abraham, RI (2 copies)

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ENCLOSURE 2

MILLSTONE UNITS 1 AND 2 SALP MANAGEMENT MEETING

WATERFORD, CONNECTICUT

OCTOBER 2, 1986

Northeast Nuclear Energy Company

W. Ellis, Chairman and Chief Executive Officer

W. Fee, Executive Vice President - Nuclear Engineering and Operations

J. Opeka, Senior Vice President - Nuclear Engineering and Operations

E. Mroczka, Vice President - Nuclear Operations

C. Sears, Vice President - Nuclear and Environmental Engineering

W. Romberg, Station Superintendent

J. Stetz, Unit 1 Superintendent

S. Scace, Unit 2 Superintendent

J. Kelley, Station Services Superintendent

M. Black, Simulator

K. Burton, Unit 3 Operations Supervisor

E. Foster, Unit 2 Engineering

R. Kacich, Licensing Supervisor

R. Laudenat, Licensing Manager

D. Nordquist, Nuclear and Environmental Engineering

R. Palmieri, Unit 1 Operations Supervisor

R. Place, NUSCo Nuclear Safety Engineer ..

P. Prezekop, Unit 1 Engineering

J. Shea, Unit 1 Project Manager

J. Kangley, Radiation Services Supervisor

B. Granados, Health Physics Supervisor

R. Graves, Haddam Neck Superintendent

R. Asafaylo, Quality Services Supervisor

J. Smith, Unit 2 Engineering Supervisor

G. Baston, Nuclear and Environmental Engineering

W. Renfro, Nuclear and Environmental Engineering

R. Harris, Nuclear and Environmental Engineering

J. Sullivan, Health Physics

G. Closius, Quality Assurance / Quality Control

E. Debarba, Generator Engineering

F. Dacimo, Unit 2 Maintenance

U.S. Nuclear Regulatory Commission

T. Murley, Regional Administrator

T. Martin, Director, Division of Radiation Safety and Safeguards

E. McCabe, Chief, Reactor Projects Section 38, Division of Reactor Projects

A. Thadani, Director, PWR Project Directorate #8, Office of Nuclear Reactor

Regulation (NRR)

D. Jaffe, Licensing Project Manager, Millstone 2, NRR

T. Rebelowski, Senior Resident Inspector, Millstone 1 and 2

G. Grant, Resident Inspector, Millstone 1 and 2

F. Casella, Resident Inspector, Millstone 3

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ENCLOSURE 3

NORTHEAST UTILITIES o.n.r.i Ome.. . s.io.n sir..i. e.rnn. Conn.ciicui

l En EcN'*Y*$ P.O. BOX 270

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HARTFORD. CONNECTICUT 06141-0270

L L J 7.'.~. '7d".U,"," ~, (203) 665-5000

November 5,1986

Docket Nos. 50-245

50-336

B12312

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Dr. Thomas E. Murley, Regional Administrator

Region i

U. S. Nuclear Regulatory Commission

631 Park Avenue

King of Prussia, PA 19406

Gentlemen:

Millstone Nuclear Power Station, Unit Nos. I and 2

Systematic Assessment of Licensee Performance

The Staff recently forwarded the SALP Board Reports (I) for the 15-month period

ending May 31, 1986, for Millstone Unit Nos. I and 2. Subsequent to receipt of

the SALP Board Reports, a meeting was held on October 2,1986 between

members of the Staff and members of Northeast Nuclear Energy Company

(NNECO).

.

The purpose of this letter is to respond to and comment on the findings of the

SALP Board with particular emphasis on the Board recommendations for the

individual evaluation categories. The responses to the Board's recommendations

for Millstone Unit No. I and Millstone Unit No. 2 are contained in Attachments

A and B, respectively, to this letter. This response was due to be submitted on

November 3,1986. In a telephone conversation with a member of your staff on

November 3,1986, NNECO was granted an extension to November 5,1986, for

the submittal of this letter.

NNECO takes very seriously the ratings and recommendations given by the Board

as an input into the continuing process of evaluating and improving our overall

performance. As reflected by our comments and observations during the October

2, 1986 meeting, we generally concur with the Board's observations and

previously have taken or are taking steps to address the concerns identified, it

remains our objective to achieve Category I ratings in all functional areas for

subsequent SALP evaluations, and the attachments to this letter describe some

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of the steps we will be taking to fulfill that objective.

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T.E. Murley letter to 3.F. Opeka, "SALP Report Nos. 50-245/85-98 and

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L 50-336/85-98," dated August 29,1986.

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We trust that the actions presented in the attachments addressing the concerns

of the Board and our general comments will be considered in subsequent SALP

evaluations. We will be updating you regarding the status of implementing the

corrective actions discussed herein prior to the next SALP evaluation.

Very truly yours,

NORTHEAST NUCLEAR ENERGY COMPANY

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J.F. Opeka '

Senior Vice President

.

By: C.F. Sears

Vice President

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Docket No. 50-245

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. Attachment A.

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Northeast Nuclear Energy Company

Millstone Unit No.1

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Response to SALP Report -

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Functional Area: PLANT OPERATIONS

Board Recommendation: None.

Response:

The report states that weaknesses were noted in the " correction of Isolation

Condenser valve motor-operator problems." We suggest that the term " motor-

operator" be deleted since the problem was with the valve itself and not the

motor-operator.

We will continue to evaluate the need for a full-time onsite fire protection

coordinator, as was suggested in the report.

The report mentions various weaknesses identified in LER preparation. We are in

the process of reviewing NRC's report from AEOD on this issue dated July 21,

1986. This is the first formal feedback from the NRC on Millstone LERs.

Identified weaknesses will be addressed.

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Functional Area: RADIOLOGICAL CONTROLS

Board Recommendation: Improve radiation worker training to stress worker

awareness of and compliance with Health Physics procedures. Improve the

effectiveness of the ALARA program. Strengthen assurance of quality in the

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transportation area.

Response:

This functional area contained numerous criticisms, the majority of which we

agree with. The SALP Board recommendations identified three major areas of

concern, namely radiation worker training, effectiveness of the ALARA pro-

gram, and assurance of quality in the transportation area. As a result of the

difficulties experienced in this area, NU has initiated changes to the

occupational radiation exposure controls program, the ALARA program, and the

radioactive waste management program.

The radiation exposure controls program changes being made are in both the

training and accountability areas. Radiation worker training is administered as a

part of our General Employee Training. This training of all radiation workers at

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NU, is modified annually to include lessons learned from the previous year, as

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weil as NRC/INPO and NU significant findings from the previous year. Since

most of our radiation workers, including contractors, have previously worked at

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our facilities and received such training, it is expected that these annual

reinforcements will heighten the awareness of these indivic'uals in this area. NU

also believes that supervisors are a key ingredient in assuring radiation worker

protection. Accordingly, we have reminded supervisors of their responsibility to

be fully cognizant of the tasks that they assign to their employees and

contractors. This includes providing all the tools, equipment, knowledge and

controls, such that these individuals can complete their tasks safely, efficiently

and in a high quality manner.

To provide the impetus to ensure that training and supervisory reinforcement are

effective, a program to monitor and enforce radiological practices will be

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developed and implemented by March 1,1987.

Regarding the Exposure Reduction and ALARA program, NU has recently

initiated a number of further actions in an attempt to lower collective exposures

to levels consistent with INPO goals.

Our efforts regarding Exposure Reduction Initiatives have been continuing and

are expected to yield paybacks in person-rem reduction. They include methods

to reduce dose rates and work scope, and improve worker efficiency. These

initiatives are currently receiving a multidiscipline (engineering, construction,

operations and ALARA-involving home office and site personnel) review for

prioritization and incorporation into the short-term (1 to 2 years) and long-term

(2 to 5 years) Soals program.

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It should be noted that, over the past few years, Millstone Unit No. I has been i

among the best domestic BWRs in regard to total occupational exposure. .

The radioactive waste management program has received considerable attention

since the formation of a special committee to review the entire radwaste

program. The results of that committee's efforts have led to the following

changes:

o The on-site radwaste handling group is being reorganized to provide a

dedicated, permanent staff with greater resources for implementation of

the program. The supervisory position was upgraded to attract and retain a

more skilled individual. Assistant supervisor and station technician post-

tions were created to assist with program administration. The authorized

working staff was doubled to reduce the number of contractors involved

with radwaste activities. It is expected that this organization will be fully

implemented and staffed by the end of 1986.

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o The training of radwaste handling and quality control personnel to increase

their knowledge of radwaste manifest preparation, shipping and burial

regulations is continuing. Radwaste supervisory personnel have attended,

or are scheduled to attend, a training program in shipping preparations,

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classifications and burial regulations offered by Chem-Nuclear. The

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program includes a trip to the Barnwell, South Carolina facility aimed at

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Increasing the supervisors' awareness of radwaste shipment from the

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receiver's perspective.

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o NEO Procedure 6.07, " Quality Assurance and Quality Control in Station

Radioactive Material Processing, Classification, Packaging, and Transpor-

tation," defining quality aspects of the radwaste shipping process, has been

issued. Implementation of this procedure has resulted in meaningful

quality checks of the entire shipping process.

o Reactivation of the Radwaste Review Committee with an expanded

charter which includes transportation issues has occurred.

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o Increased attention by the quality organization through additional audits

and surveillances will be utilized to ensure the effectiveness of the

proposed corrective actions.

o A proposal for the formation of a dedicated home office engineering staff

to address broad radwaste issues such as volume reduction, burial alloca-

tion, radwaste system engineering, decontamination and decommissioning

has recently been approved for implementation in 1987.

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It is our expectation that these significant forward steps will resolve the

difficulties we have experienced in the radiological controls area.

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Functional Area: MAINTENANCE AND MODIFICATIONS

Board Recommendations: None.

Response:

We believe that the SALP Report in several limited respects does not accurately

reflect Millstone Unit No. I performance in this functional area. In the summary

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of this section, the report states that "much outstanding maintenance work was

noted and the environmental qualification program was well implemented, but

there were significant problems with the scram solenoid pilot valves, with the

emergency gas turbine generator, and with the main turbine mechanical pressure

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regulator. These indicate a need to more effectively assure that aging and/or

obsolescent equipment is replaced and, where appropriate, redesigned so as to

minimize the effect upon and challenges to safety systems." Additional

information regarding each of these three items is provided belows

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t 1. Scram Solenoid Pilot Valve Rework

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During the 1985 Refueling Outage, 45 scram solenoid pilot valves were

' reworked. The valves were selected as part of our continuing program to

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replace Buna-N material. This has been a routine maintenance and upgrade

activity during recent refueling outages. During control rod scram testing

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valves, three valve failures were experienced. Two of these valves had

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been rebuilt durin5 the outage. The SALP Report considers inadequate

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testing of the valves after rework and before power operation to be a

prime factor in these failures.

Contrary to this conclusion, adequate retest was a serious concern and was

discussed at length prior to performing the work. Since valve performance

affects control rod scram times, selection of the valves to be rebuilt, in

addition to other factors, was made based on the ability to perform scram

timing on those valves after the outage (by June,1986) without signifi-

cantly impacting plant capacity factor or introducing a possibility of

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challenges to safety systems. In-place retests cannot be adequately

performed during the outage because of the potential for subsequent

control rod drive seal damage that could occur when the reactor vessel is

not pressurized.

It was noted in the SALP Report that " discussions with maintenance

personnel revealed a high level of knowledge about current maintenance

activities. This included the scram solenoid rework effort. . . ". Again,

this comment recognizes the planning and attention to detail that went

into overall performance of this task.

The SALP Report also references our commitment to rebuild the remaining

solenoid valves by June, 1986. In the context of the report, this ,

commitment is presented as being an NRC mandate due to our rework

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schedule not being timely. Contrary to the above, it should be noted that

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this commitment was our initiative based on what we believed to be timely

completion of a rework program.

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In conclusion, we do not believe that the SALP summary reflects a true

understanding of our performance of this task, nor does it present a valid

conclusion in identifying our pro 6 ram as a significant problem. It should in

no way serve to lessen the SALP rating in this category. Instead, it should

serve as an example of our ability to effectively plan and carry out

maintenance activities, to react to unexpected conditions encountered

during performance of these activities, and to plan and perform appropri-

ate corrective measures.

2. Gas Turbine Performance

On November 27, 1985, the Gas Turbine received a start signal and failed

to start. Investigation revealed that the Gas Turbine tripped on high

exhaust temperature. The " root cause" of this event was a failure of the

Air Start Regulator Valve. This valve had just been installed prior to the

failure. The valve that failed had been rebuilt by the manufacturer and all

associated Q.A. documentation was in order. This valve was installed in

response to an SEP commitment to the NRC to replace governor controls

on a routine basis.

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On January 13, 1986, while performing an operational readiness demonstra- .

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tion af ter maintenance but before declaring the Gas Turbine operable, the

Gas Turbine failed to start. Preliminary information indicates that the

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event was due to a fault in the Electric Governor Regulator. This Electric

Governor Regulator had been installed on January 8,1986 as a result of a

preventative maintenance program. All Q.A. documentation was in order,

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and the testing of the Gas Turbine was the re-test for the EGR replace-

ment.

It is apparent that the two Gas Turbine failures were not due to our

inability to replace aging equipment. The second failure was caused by and ,

detected during the retest following s routine chanbeout of a governor

component. These failures shculd not even be included in this report, since

the failures were attributable to the replacement components which were

installed to preclude unanticipated failures.

Credit for proper routine maintenance efforts should be given. An example

of such an effort was the re-adjustment of the Servo-limiter that was

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performed on August 21, 1986. However, maintenance and routine

activities, "which may have prevented a failure," are very hard to

document and thus hard to credit.

The SALP Report states that our " procedures, training, trending of

equipment characteristics, and management overview have been increased,

but these actions were primarily responsive ones." We recognize that there

have been problems related to the Gas Turbine Generator. In the past, and

especially since 1982, we have made continuous changes in our procedures

and programs to increase the reliability of the machine. We have been

very successful in this effort, as can be seen from system performance

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improvement. Further experienced-based improvements to our programs

are being made, but to say that these actions are solely responsive ones is

both inaccurate and invalid. Instead, they demonstrate our ability to

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develop effective monitoring and maintenance pro 6 rams, to implement

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these programs, and to make changes to these programs based on new data 1

and operational experience. It should be recognized also that, since this

system is unique to Millstone Unit No.1, we are developing our programs

based on Millstone Unit No. I experience only, rather than from an industry

data base. Under these conditions, more frequent program changes and

longer program development times are expected. We believe that our

actions related to the Gas Turbine Generator have been both effective and

justified, and therefore do not provide reason for lessening the sal.P rating

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in this category.

3. Mechanical Pressure Regulator Performance

on February 5,1986, the Mechanical Pressure Regulator (MPR) System

failed, causing a pressure oscillation resultin6i n a reactor scram. Mainte-

nance, which included planned replacement of the sensing bellows gasket

and the inspection of a snubber valve, had been performed on the MPR

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during our recent 1985 refueling outage. During this refuel outage, the

, snubber valve was found to have some slight contamination and was

cleaned. Following the reactor scram, the MPR was adjusted, tested, and

returned to service. Additional work on the MPR was scheduled for the

next outage. -

On May 21, 1986, while shutting down for a planned turbine rotor

inspection, a manual scram was initiated when reactor pressure began to

oscillate due to the malfunction of the MPR. Operator initiation of a

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manual scram was a conservative response by the operator to this

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situation. Planned maintenance was again performed on the MPR, which

included an inspection of the snubber valve as well as modifications to the

rate adjustments. The snubber valve had been clogged with a foreign

substance. The valve was cleaned and returned to service. The MPR was

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adjusted, tested, and returned to service. As an added preventative

measure, the snubber valve was scheduled for replacement.

On August 28, 1986, the snubber valve was replaced. The valve that was

removed was once again clogged. Further investigation revealed that the

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nickel plating had been worn off the valve. This most likely is the result of

steam passing through the valve when the MPR had a faulty gasket. The

valve had not been replaced earlier due to long lead times in obtaining

spare parts. Future inspections and preventative maintenance of the new

valve are planned to preclude future misoperation due to internal clogging

of the component. An investigation into the source of the clogging is

continuing. We are confident that the root cause is not associated with

aging components.

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The attention given to this system has been greatly increased over the past

several years. We are presently in a transition state, going from what once

was complete vendor support to an in-house maintenance program for this

system. In all cases, we have utilized experts from various manufacturers

and have followed their maintenance recommendations. It should be noted

here that actions taken to date have resulted in a marked improvement in

MPR operation. We believe that we will now begin to see a system

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reliability improvement associated with program enhancements. In gener-

al, we believe that this is another example of our ability to make effective l

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program changes to improve plant reliability and reduce the probability for

challenges to safety systems. MPR performance is not related to an ,

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inadequate maintenance program to replace aging components, and should

not serve to lessen the SALP rating in this area. l

Additional Maintenance Programs

The report does not give credit to upgrade programs that have helped to

increase our reliability. Some examples of these programs are listed

below.

Reactor Recirculation System

' A. Recirculation Speed Control components were replaced.

B. The installation of a new type of Motor Generator Field Brush with

significantly longer . operating life to minimize brush wear was

completed.

C. A program to test the Motor Generator is ongoing.

D. A new Motor Generator Field was procured.

i E. The existing Motor Generator Field was re-built.

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A-13

Feedwater and Drains System

A. Heater Bay Positioner upgrades to improve performance and reliabil-

Ity have been completed.

B. Periodic Feedwater Control Valves Positioner changeouts are

ongoing.

C. The installation of additional Feedwater Flow Transmitters to im-

prove plant monitoring capability has been completed.

D. The installation of new Reactor Level Transmitters has been com-

pleted.

E. The installation of new Reactor Pressure Transmitters has been

completed.

F. A program to replace Feedwater Control System components is

ongoing.

G. Routine performance checks of the following are ongoing:

1) Feedwater Control Valves and their lock-ups

2) Moisture Separator Drain System

3) Feedwater Heater Controls.

Gas Turbine Generator

l

A. Gas Turbine Regulator components have been replaced to improve

reliability.

B. A dehumidifier was installed in the regulator compartment to prevent .

corrosion damage to regulator components.

,

C. The Gas Turbine batteries were replaced.

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A-14

D. The Gas Turbine . Generator Rotor was replaced when inspection

revealed possible insulation problems.

Electrical Systems

A. Routine checks of the Main Generator Regulator are ongoing.

B. Routine checks of the station transformers to monitor performance

are ongoing.

C. Routine checks of the 4160 volt motors are ongoing. -

D. The calibration of all protective relays is ongoing.

E. A program to calibrate station time delay relays has been instituted.

F. The station 125V batteries have been replaced.

G. The Neutron Monitoring System batteries have been replaced.

H. All solenoids on the Main Turbine have been replaced.

I. Contact inte5rity tests of pressure switches are ongoing.

Balance of Plant

t

A. A balance of plant vibration monitoring program was initiated for all

rotating plant equipment.

B. Improvements to plant air systems to minimize potential for cross-

contamination of plant components were implemented.

C. Improved condenser leak detection methods to reduce personnel

radiation exposure and minimize plant capacity factor impact have

been implemented. ,

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A-15

D. A Service Water System inspections program to improve reliability

has been implemented.

E. The Service Water Strainer isolation valves were replaced.

F. The screen wash strainer body was replaced and the internals were

coated to increase component lifetime.

This list is incomplete, but is representative of the type of program development

and plant improvements that are being implemented at Millstone Unit No.1.

Based on them and on similar programs like them, we believe they should provide

a highly favorable impact on the overall SALP rating in this category.

Based on our review of the SALP Report and our perception of our performance,

we have not identified a basis for an overall rating of Category 2 in the area of

Maintenance and Modifications. It appears that the NRC assessment of items 1, -

2 and 3 above could be altered based upon the information contained in this

letter. We believe that the Millstone Unit No. I rating for this functional area

should be Category 1.

It should also be noted here that Millstone Unit No. I completed 374 days of

continuous power operation during the assessment period. Our success in

implementing successful maintenance and modification-related tasks is directly

reflected in this accomplishment. As plants get older, it is expected that

-

1

attention to detail in planning and performance of component maintenance must

increase. Our operating accomplishments, capacity factor and availability

demonstrate our success in these areas. The capacity factor for Millstone Unit

j No. I was 81.2% for this SALP period (93.4% capacity factor not counting

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A-16

refueling period). This compares favorably with the average capacity factor for

US BWRs during 1985, which was 54.3 (1) The forced outage rate for Millstone

Unit No. I was very low, namely,1.7%, while the rest of the industry averaged

11.9

(1) " Operating Units Status Report," dated January,1986.

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in Functional Area: SURVEILLANCE

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Board Recommendation
None.

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No comments.

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Functional Area: EMERGENCY PREPAREDNESS '

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Board Recommendation: Reassess effectiveness of commitm'e nt' tracking sys-

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Response:

There was no discussion in the SALP report relating to this recommendation.

However, it should be pointed out that a comprehensive; commitment follow

system is used for all drill and exercise critique findings. ~ This is periodically

updated. In addition, there are emergency preparedness (EP) surveillance

tracking systems to ensure that periodic emergency fac!!ity anc equipment test:

are accomplished. A station Administrative Control Procedure will be effective

in November,1986 to formalize this EP surveillance system. We suggest that

the NRC review the above systems at a future date.

.

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i Functional Areat SECURITY AND SAFEGUARDS

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Board Recommendation: None.

Response:

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No comments.

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Functional Area: REFUELING AND OUTAGE MANAGEMENT

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Board Recommendation: None.

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Responses s,

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This section of the SALP Report reflects what we believe to be an accurate

,

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representation of our performance during the 1985 Refueling Outage. No rating

~

was given due to what the inspectors determined to be insufficient time for

'

j'; performing an accurate evaluation.

As noted in the SALP Report, significant activitics were performed during the

,

period from October 25, 1985 to December 23, 1985. These activities included

weld overlay repair of the jet pump instrumentation vessel nozzles and isolation

condenser steam supply lines, replacement of safety-related valve motor oper-

ators with environmentally qualified units and the replacement of the emergency

gas turbine generator rotor. Not mentioned in the report, but considered by us

,

to b'e significant in nature, was cleaning of the recirculation pump MG set fields.

ThiC task was planned based on trending of component performance, and

.\k

demonstrates our ability to anticipate and correct situations that, if left

unattended, could result in signicant losses in unit availability and capacity

'

s factor. All major activities were completed with no significant problems, as ,

, noted in the report, due to planning and good communication during performance

,

of the work.

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A-21

The report also makes mention of our on-line management decisions that were

instrumental in effective implementation of piping repair activities. These

activities occurred without major impact on the outage duration because we

anticipated the piping problems and planned accordingly.

Although 32 hours3.703704e-4 days <br />0.00889 hours <br />5.291005e-5 weeks <br />1.2176e-5 months <br /> of inspection time represents only 2% of the total inspection

time that was expended to assess our performance, we believe it to be sufficient

in providing a rating in an area in which every aspect of our performance was

found to be outstanding. If more inspection time would have been available, we

believe that it would only strengthen the assessment made in the report.

Additionally, because of the manner in which refueling and outage management

data are presented to inspectors (e.g., published reports, daily updated schedules

and log books, etc.), assessments made in this area are not expected to require

the same number of inspection hours as would be required in other areas. Not

providing a rating for a functional area where we believe a Cr.tegory I rating is

deserved sends a negative signal to Millstone Unit No. I personnel involved in

this area. We would request that a rating be provided based on the inspection

performed. We firmly believe the correct rating is Category 1.

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A-22

Functional Area: ASSURANCE OF QUALITY

Board Recommendation: None.

Response:

This functional area is a synopsis of the assessments in the other nine areas. The

responses for the other functional areas address specific actions which are being

taken to minimize and/or eliminate problems in those areas.

,

As stated in our response to Maintenance and Modifications, we believe that we

have good programs to assure quality performance of aging equipment and

adequate post-maintenance testing. As is stated in our responses to both the

Radiological Controls and the Training and Qualification Effectiveness func-

tional areas, we are taking significant measures to improve worker adherence to

and endorsement of routine radiation protection controls. We will continue to

take measures to improve our assurance of quality in all areas.

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A-23

Functional Area: TRAINING AND QUALIFICATION EFFECTIVENESS l

Board Recommendation: None.

Response:

Since the end of this SALP period, four of ten training programs have been

accredited by INPO. The four operator training programs, for non-licensed

operators, reactor operators, senior reactor operators and shif t technical ad-

visors, received accreditation from INPO on August 21, 1986. On October 1,

.

1986, the Self-Evaluation Reports for the remaining six training programs were

submitted to INPO. INPO reviews and site accreditation visits for these six

programs are not expected to be completed until well into 1987. Although not

yet accredited, these training programs are already in place, with most of the

lesson plans complete. Including all four nuclear units at NU,1533 training

programs are scheduled for 1987.

The Nuclear Training Department undertook a major reorganization during the

SALP period to meet the corporate goal of " training excellence." The training

.

staff (which has tripled since 1984) is committed and dedicated to the develop-

ment and delivery of superior quality training in all operator and technical

,

disciplines. We expect these efforts to result in performance-based improve-

1

i ments of the job incumbents. Some of the changes that have been implemented

to re-orient operator and technical training include:

. - - - - -

A-24

(1) Installation of the Millstone Unit No. I Simulator

o On-site reverification testing was completed in May,1986.

o Availability of the simulator has resulted in significant enhancements

to Licensed Operator Training Program and provided opportunities to

support other station activities.

o Since July,1986, the simulator has been used to support the Licensed

.

Operator Requalification Program. It is anticipated that the simu-

lator will be used to support approximately 50 percent of licensed

operator requalification training in future years.

o ' The simulator has been integrated into both Reactor Operator and

Senior Reactor Operator Initial Training Programs. The simulator

portions of these programs, each consisting of approximately 200

hours, began on September 29, 1986, and is currently ongoing. A

Senior Reactor Operator upgrade class is currently scheduled to begin

approximately February 2,1987.

(2) I&C Technician Understanding of Technical Specifications

o The Instrument and Controls (l&C) instructional staff prepared and

delivered in May, 1986, a four hour presentation of Technical

specifications to 100% of the Millstone Unit No. I and 2 I&C

Department's Technician staff.

.

. . A-25

.

(3) Radweste Transportation and Handling

As was stated in our response (2) to Combined Inspection No. 50-245/86-06,

50-336/86-06, and 50-213/86-04, several corrective steps to avoid radwaste

shipping problems are being taken.

Additional training has been provided to individuals involved in the

shipment of radioactive waste to assure suitable proficiency in the area of

transportation of radioactive material.

Title Dates

o NUS training session for Radwaste Handlers 03/31/86 - 04/01/86

o NUS training session for Radioactive 04/02/86 - 04/04/86

Materials Supervision, Shippers and QA/QC

Inspectors

o NUSCO Training Department course of 07/14/86 - 07/18/86

radioactive materials shipping 07/21/86 - 07/25/86

o CNSI Workshop on Radioactive Waste 05/28/86 - 05/30/86

Packaging, Transportation and Disposal

- attended by Radioactive Materials

Handling Supervisor

(2) J.F. Opeka letter to T.E. Murley, " Response to I&E Inspection No. 50-

245/86-06,50-336/86-06 and 50-213/86-04," dated August 21,1986.

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A continuing training program for Radwaste personnelis being developed.

o- The Health Physics section of the Technical Training Branch of the

Nuclear Training Department will complete a job analysis and pro-

cedure based task analysis in accordance with procedure NTM-1.06,

" Systematic Instructional Design" for the following areas: Radwaste

Handlers, Radwaste Supervision and Station Technician (R/W), and

Radwaste QA/QC by February 28,1987.

o A set of instructional objectives resulting from this analysis effort

will be produced and approved by the Training Program Control

Committee for Radwaste by March 30,1987.

o A performance based cor.tinuing training program consisting of

classroom and on-the-job training will be developed by July 30, 1987

and completely implemented prior to December 31,1987.

(4) At our request, INPO conducted an accreditation assistance visit at NU on

August 25-26, 1986, to review and make recommendations on our accredi-

tation efforts for the radiological protection technician training program.

,

. (5) The following items represent additional enhancements to our training

.

program:

o An electrical switchgear and motor control center lab has been created.

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o Two new instrument and controls labs have been established.

o Full-scale mock-ups for reactor coolant pump seal replacement training

have been procured for all four nuclear units.

o A full diesel engine has been procured for diesel overhaul maintenance

training.

o A full chemistry lab including all of the instrumentation used on all four

nuclear units has been established.

o A gamma spectroscopy lab has been built.

o A fully equipped and staffed graphics department has been established to

suppo-t the training department,

o A fully equipped technical library has been established.

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Functi'n-1 Ar a: LICENSING ACTIVITIES l

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Board Recommendations: None.

Response:

No comments.

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_ Docket No. 50-336

Attachment B

Northeast Nuclear Energy Company

Millstone Unit No. 2

Response to SALP Report

.

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November,1986

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B-1

Functional Area: PLANT OPERATIONS

Board Recommendations: None.

Response:

We will continue to evaluate the need for a full-time onsite fire protection

coordinator.

.

The report mentions various weaknesses identified in LER preparation. Millstone

Unit No. 2 has reviewed the NRC's report from AEOD on this issue dated July

21, 1986, evaluating suggested improvements and specifically reviewin5 the two

,

" principle weaknesses" identified in the report summary: (1) failure to provide an

'

assessment of the safety consequences and (2) the lack of identified failed

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components.

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Concerning the failed component deficiencies, the report referenced 5 of the 10

l LERs reviewed as not having completed the failed component fields. NUREG-

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1022, including its supplements, requires that the failed component field be left

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blank if the event is not attributable to a failed component. Mr. Hebdon, the '

<

author of the 10CFR50.73 rule, confirmed this method of LER preparation at an

.

NRC/ Utility Symposium in 1985. Therefore, this identified weakness is un-

founded.

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The safety assessment, though implied in the LERs, was not specifically

identified or annotated as a safety assessment of the event. Therefore, in an

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effort to clarify LERs in the future, Millstone Unit No. 2 will adopt an outline

format in its LER preparation. This should eliminate the weakness as described

in the evaluation and ensure consistency in its LERs.

In addition to the proposed outline format, the entire evaluation by the NRC was

discussed with Millstone Unit No. 2 engineering department personnel to ensure

completeness in future LERs.

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Functional Area: RADIOLOGICAL CONTROLS

Board Recommendations: Improve radiation worker training to stress worker

awareness of and compliance with Health Physics procedures. Improve the

effectiveness of the ALARA program. Strengthen assurance of quality in the

transportation area.

Response:

..

See Millstone Unit No. I's response.

It should be noted that Millstone Unit No. 2 has had high exposure primarily

because of extensive steam generator repair requirements.

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Functional Area: MAINTENANCE AND MODIFICATIONS

Board Recommendations: None.

Response:

No comments.

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Functional Area: SURVEILLANCE

Board Recommendation: None.

Response:

The report discusses 2 violations occurring during the performance of the Local

Leak Rate Test (LLRT) program for Millstone Unit No. 2. The following actions

.

have been taken to ensure that similar violations do not occur in the future:

.

o Af ter the last LLRT was performed, a complete review of the program was

undertaken. This included a review of procedures, forms, and equipment

used during the LLRT program. The outcome was a revision to the

procedures and forms and an upgrade in equipment and its maintenance. In

order to address the finding on lack of calibration, each test requires the

operator to verify calibration dates prior.to the start of the test. In order

to address the finding on failure to follow procedures, the procedures were

.

clarified to provide clear direction and the operators were familiarized

with the use of the procedures.

'

o A discipline engineer has been assigned on a full-time basis the direct

responsibilitly of supervising the performance of the 1986 LLRT program.

His duties include assuring procedural compliance and scrutinizing every

aspect of the program for weak points or areas of uncertainty. He reports

directly to the Operations Supervisor.

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o The same discipline engineer mentioned above will recommend long-term

improvements to the LLRT program. It is anticipated that additional

procedural upgrades and procurement of state-of-the-art equipment will

ensure not only a program that complies with present regulations, but also

a LLRT program that could be a model for other facilities.

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Functional Area: EMERGENCY PREPAREDNESS

Board Recommendation: Reassess effectiveness of commitment tracking sys-

tem.

Response:

See Millstone Unit No. I's response.

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Functional Area: SECURITY AND SAFEGUARDS

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Board Recommendation: None.

Response:

No comments.

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Functional Area: REFUELING AND OUTAGE MANAGEMENT

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Board Recommendation: None.

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Response:

In the Facility Perforrnance table on page 6 of the report,it is incorrectly stated

that a Category 2 rating was assigned for the previous SALP period for the

Refueling / Outage Management functional area. A Category I rating was

actually assigned.(I)

,

, (1) See the T.E. Murley letter to J.F. Opeka, " Systematic Assessment of .

Licensee Performance," dated May 20,1985, page 5 of Millstone Unit No. ~

2's report. -

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-Functional Area: ASSURANCE OF QUALITY

Board Recommendation: None.

Response:

As stated in the report, this functional area is a synopsis of the assessments in

the other nine areas. The responses for the other functional areas address

specific actions which are being taken to minimize and/or eliminate problems in

those areas. We will continue to take measures to improve our assurance of

quality in all areas.

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Functional Area: TRAINING AND QUALIFICATION EFFECTIVENESS

Board Recommendation: None.

Response:

See Millstone Unit No. I's response.

.

(1) Installation of the Millstone Unit No. 2 Simulator

,

o Training on the simulator began on August 12,1985.

o Availability of the simulator has resulted in significant enhancements

to Licensed Operator Training Program and provided opportunities to

support other station activities.

o The simulator is being used to support the Licensed Operator

.

Requalification Program. It is anticipated that the simulator will

continue to be used to support approximately 50 percent of licensed

operator requalification training.

o The simulator has been integrated into both Reactor Operator and

Senior Reactor Operator Initial Training Programs. The simulator ,

i portions of these programs consist of approximately 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> and

!

[ 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, respectively. A licensed operator class and a licensed

operator upgrade class, each including simulator training, were

'

completed on July 3,1986.

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Functional Areat LICENSING ACTIVITIES

Board Recommendations: None.

Response:

No comments.

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