IR 05000369/1988009: Difference between revisions

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{{Adams
{{Adams
| number = ML20153F521
| number = ML20195H121
| issue date = 04/29/1988
| issue date = 06/16/1988
| title = Insp Repts 50-369/88-09 & 50-370/88-09 on 880319-0422. Violations Noted.Major Areas Inspected:Operations,Safety Verification,Surveillance Testing,Maint Activities & Followup on Previous Insp Findings
| title = Ack Receipt of 880531 Ltr Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-369/88-09 & 50-370/88-09
| author name = Orders W, Peebles T
| author name = Brownlee V
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =  
| addressee name = Tucker H
| addressee affiliation =  
| addressee affiliation = DUKE POWER CO.
| docket = 05000369, 05000370
| docket = 05000369, 05000370
| license number =  
| license number =  
| contact person =  
| contact person =  
| document report number = 50-369-88-09, 50-369-88-9, 50-370-88-09, 50-370-88-9, NUDOCS 8805100356
| document report number = NUDOCS 8806280221
| package number = ML20153F513
| document type = CORRESPONDENCE-LETTERS, NRC TO UTILITY, OUTGOING CORRESPONDENCE
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 1
| page count = 12
}}
}}


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    - UNITED STATES
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[in Rio I o,^  NUCLEAR REGULATORY COMMISSION REGION il h8Y h , g
  ,  .101 MARIETTA STREET. ATLANTA GEORGIA 30323
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Report Nos.: 50-369/88-09 and 50-370/88-09 Licensee: Duke Power Company        l 422 South Church Street      !
Charlotte, NC 28242      !
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Docket Nos.: 50-369 and 50-370  License Nos.: NPF-9 and NPF-17
, Facility Name: McGuire 1 and 2 Inspection Conducte g  arch 19, 1988 - April 22, 1988 Inspector [  AM/      ;
  <'w;mrders, Senior)dsidentInspector    /Da4V 5fgneo Accompanying Personnel: D. Nelson      ;
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R. Croteau      !
Approved by:E A. Peebles, SectiorAChief
    /    /[4 D&te'5igned
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,  DivisionofReactorFrojects
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SUMMARY    !
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Scopt, This routine unannounced inspection involved the areas of operations    :
. safety verification, surveillance testin  maintenance activities, and
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follow-up on previous inspection findings, g,      i
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Results: In the areas inspected three violations were identified. One    I violation was identified which ir$cluded two examples for failora to follow    !
procedure during safety valve testing and an inadequate procedure for slave    !
relay testing. A second violation was identified which involved an inoperable    l component cooling train and the *. aird violaticr. involved a failure to perform    i post maintenance testing which rendered a nuclear service water train    ,
inoperabl j 1          1 l
J s          I I          I l  8805100356 880429        i
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PDR ADOCK 05000369
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REPORT DETAILS Persons Contacted Licensee Empicyees
*T. McConnell, Plant Manager i 8. Travis, Superintendent of Operations
* Suple, Superintendent of Maintenance B. Hauilton, Superintendent of Technical Services R. Sharpe, Compliance Engineer J. Boyle, Superintendent of Integrated Scheduling L. Firebaugh, OPS /NPE/MNS
*S. LeRoy, Licensing, General Office
*D. Baxter, OPS /MNS/NPD
*S. Copp, Planning Engineer R. Panner, Compliance    :
J. Snyder, Performance Engineer
*N. Atherton, Compliance
; W.Reeside}AEEngineerOperations R. White,  Engineer
*G. Gilbert, MNS/NPD
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Other licensee employees contacted included construction craftsmen, technicians, operators, mechanics, security force members, and office personne * Attended exit interview Exit Interview (30703)
The inspection findings identified below were summarized on April 22, i 1988, with those persons indicated in paragraph 1 above. The following items were discussed in detail:
l 1  (OPEN) Violation 370/88-09-01, Failure to follow procedure for Pressurizer Code Safety Valve Testing and Inadequate Procedure for Slave Relay Testing. (Seeparagraphs5and9).
 
  (OPEN) Violation 369/88-09-02,
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Train Due to Inoperable Nuclear Service Water (RN) Valv See Inoperable Co
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paragraph 10).    !
l (OPEN) Vio1rion 369/88-09-03, Inoperable RN Train Due to a Failure to Test RN-2 (See paragraph 10).
 
The licensee representatives present offered no dissenting comments, nor did they identify as proprietary any of the information reviewed by the inspectors during the course of their inspectio l
 
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' Unresolved Items An unresolved item (UNR) is a matter about which more information is required to determins whether it is acceptable or may involve a violation or deviation. There were no unresolved items identified in this repor . Plant Operations (71707, 71710)
The inspection staff reviewed plant operations durir:g the report period to verify conformance with applicable regulatory requirements. Control room logs, shift supervisors' logs, shift turnover records and equipment removal and restoration records were routinely aerused. Interviews were conducted with plant operations, maintenance, clemistry, health physics, and performance personne Activities within the control room were monitored during shifts and at
!  shift cMnges. Actions and/or activities observed were conducted as
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prescribed in applicable station administrative directives. The complement of licensed personnel on each shift met or exceeded the minimum required by Technical Specification Plant tours taken during the reporting period included, but were not limited to, the turbine buildings, the auxiliary building, Units 1 and 2 electrical equipment rooms, Units 1 and 2 cable spreading rooms, and the
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station yard zone inside the protected are During the plant tours, ongoing activities, housekeeping, security, equipment status and radiation control practices were observed.
 
Use of overtime by operations was reviewed to verify cornpliance with TS requirement Documentation showed that the maximum overtime limits were exceeded approximately nine times in 1987-1988, primarily for outage support. It is allowable to exceed the maximum limits for very unusual circumstance Operations Management Procedure 1-7, Shift Manning and Overtime Requirements, requires that overtime worked in excess of guidelines be authorized in advance by the station manager or his designee (another high level of management). The inspector noted that in September of 1987 two instances of exceeding the maximum overtime limits were not authorized in advance. The licensee received a violation for this issue (see Inspection Report 369, 370/87-26) in the September 1987 period and corrective actions have been take Unit 1 Operations Unit 1 began the reporting period at full power. On March 23, 1988, the unit emerienced a saurious safety injection (SI), main steam isolation ar,d reactor tr p. The spurious SI signal was generated in a Solid State Protection Syetem (SSPS) caLinet containing the circuitry for A train low steam line pressure SI and main steam isolation. Licensee technicians had just completed testing in this l
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cabinet and were closing the door. The spurious signal occurred when the door was shut. All A train SI components actuated and the hiah head pump injected into the primary coolant system. Main steam'
isolation and feed water isolation occurred, generating a turbine trip and resultant reactor tri Operators determined that the SI was inadvertant and secured the injection in approximately nine minutes. No major problems occurred during the transient. All A train SI components functioned as designed during the transient, except that the reactor trip was caused by the turbine trip above P-8 instead of directly by the SI actuation as would be expected. The cause for this was determined later and is discussed below. During the event a low steam generator level in the C steam generator caused auxiliary feedwater (CA) to initiate a second tim After the unit was stabilized, Instrumentation and Electrical (IAE)
technicians attemnted to determine the cause of the SI signal. The spurious signal was duplicated several times by agitating the SSPS cabinet. However, the signal could not be repeated following the shutting of a nearby heavy door. Further investigation could not determine the exact cause of the problem. The licensee considers that a sina11 piece of loose wire or other conductor had shorted or
 
grounded the circuitry u)on agitation of the cabinet. According to
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the licensee, the additional agitation conducted during trouble-shooting, and finally the shutting of the nearby door served to vibrate the conductor away from the electrical centacts. A thorough cleaning of the cabinet was performed. This arod'ned some small wire fragments which could have caused what the l'censee postulates. The licensee also considers that the points of contact occurred in the low steamline pressure SI circuit downstream from the point where the reactor trip function branches off, thereby causing the SI to initiate without causing a direct reactor trip. Following the cleaning a complete functional surveillance was performed with no problem The unit was restarted and achieved full power the ,
following da No similar problems in SSPS have develope On March 27, load was decreased to 86 percent power due to decreased load demand on the grid and was back at full power at 1247 a.m. on i March 2 Later on March 28 power was reduced to 46 percent to
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support removal of a voltage regulator control drawe Unit 1 returned to 100 percent power on March 2 ,
i On April 16, Unit I was manually tripped from 100 percent power due to decreasing le<el in the C steam generator (SG) caused >y the C feed regulating nice (FRV) failing shut. The C FRV shut due to a
"  blown fuse on a wd controlling the valve. The card was later tested and found to be the cause of the blown fuse. Auxiliary feed I
water (CA) auto started on low steam generator levels but 1SA-49, steam supply from the 8 SG to the turbine driven CA pump, did not indicate open due to problems with the position indicating limit i switche The valve was actually ope The limit switches were
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adjusted, tha' FRV card was replaced, and the unit returned to 100 t percent power oa April 18.
 
l Unit 2 Operations    _
Unit 2 operated at full power for the entire period. The SI on Unit !
i  1, discussed above, did lowever affect Unit 2. Due to the alignment of the common portion of the Nuclear Service Water (RN) System, the ,
operating Unit 2 RN train was isolated by the single train SI on Unit '
l Had both SI trains on Unit 1 actuated, the common portion of RN would have realigned to ensure continued RN operation on Unit Various Unit 2 component temperatures elevated, but Unit 2_ operators
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diagnosed and corrected the problem in time to prevent any additional a  required action No violations or deviations were identifie . Surveillance Testing (61726)
Selected surveillance tests were analyzed and/or witnessed by the inspector to ascertain procedural and performance adequacy and ccnformance with applicable Technical Specifications.
 
Selected tests were witnessed to ascertain that current written approved procedures were available and in use, that test equipment in use was
;  calibrated, that test prerequisites were met, that system restoration was ,
;  completed and test results were adequat l Detailed below are selected tests which were either reviewed or witnessed:
PROCEDURE  EQUIPHENT/ TEST
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PT/0/A/4150/05 Pressurizer Safety Valve.Setpoint Test PT/1/A/4403/007 RN 1A Flow Balance Test  i PT/2/A/4200/28A SSPS Slave Relay Tests  l PT/1/A/4208/03A Train 1A NS Heat Exchanger Performance Test PT/1/A/4252/018 CA Pump IB Performance Test PT/1/A/4601/088 SSPS Train B Periodic Test  l PT/1/A/4403/018 RN Train IB Performance Test PT/1/A/4403/01A RN Train 1A Performance Test PT/1/A/4206/01A NI Pump 1A Performance Test PT/1/A/4252/01A CA Pump 1A Performance Test PT/1/A/4204/01B ND Pump 1B Performance Test PT/2/A/4209/01A NV Pump 2A Performance Test PT/2/A/4206/01A NI Pump 2A Performance Test PT/0/A/4350/38 125 VDC Battery Service Test See paragraph 9 for further information conce ning PT/0/A/4150/0 !
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On March 22 at 10:02 AM, a procedure error in a performance seriodic test procedure caused re-alignment of power sources to severa' Unit 2  '
non-safety containment ventilation systems. A step in grocedure  i PT/2/A/4200/28A, Slave Relay Test, directs the opening of a sliding link" :
to prevent ventilation units from tripping during the test. This occurs in the section of the procedure that tests slave relays in the Train A Safety Injection SSPS circuitry. The step specifies opening sliding link H-3 in cabinet 2ATC8. When the system was actuated in a subsecuent step, ,
several non-safety containment ventilation systems experiencec a shunt trip to re-align their power sources to non-safet The affected systems were lower containment ventilation (VL)y, buse Upper Containment Ventilation (VU), and Control Rod Drive Mechanism Cooling" Ventilation (VR). These non-safety systems are designed to "load shed in the event of an ESF actuation to lessen the electrical load on safety system power sources. The loid shed took 31 ace because the wrong sliding link was specified. A step at the comp:etion of the test specifies closing sliding link I-2 in the same cabinet. I-2 is the correct sliding link that should have been opened originally. Having the wrong sliding link open during the test did not othenvise adversely effect the test or plant operatio The procedure is therefore error constitutes an apparent an examp/88-09-01).le of an inadequate proce violation. (370 The licensee states that the procedure error occurred in a recent re-write of the procedure, but has no explanation for why it occurred. Another case of an unexplained procedure change occurred recently in an operations procedure which was discussed in NRC inspection report 50-369,~370/88-0 In that case two procedure steps were interchanged during re-write. A violclion was issued for that occurrence, but the licensee's corrective action appeared to be limited to the operations organization where the problem occurred. When the corrective actions and lessons learned are shared with other departments, similar problems may be prevente . MaintenanceObservations(62703)
Routine maintenance activities were reviewed and/or witnessed by the resident inspection staff to ascertain procedural and performance adequacy and conformance with applicable Technical Specification The selected activities witnessed were examined to ascertain that, where a3plicable, current written approved procedures were available and ir use, t1at prerequisites were met, that equipment restoration was completed and maintenance results were adequat No violations or deviations were identifie . Follow-up on Previous Inspection Findings (92702)
The following previously identified items were reviewed to ascertain that the licensee s responses, were applicable, and licensee actions were in compliance with regulatory requirements and corrective actions have been
 
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complete Selective verification included record review, observations, and discussions with licensee personne (CLOSED) Violation 369, 370/85-06-0 Failure to Take Prompt Corrective  I Action to Notify Operations Personnel of Potential Degradation of Auxiliary Feedwater System and Correct Improper Valve Installatio .
Nuclear Station Modifications (NSM's) were completed by July 21, 1985 which installed temperature monitors to detect check valve leakage and replaced the stop check valves with a different design valve. The completed NSM's were reviewed and selected check valves were physically verified to be in place by the inspecto The violation was initially denied but the NRC determined that the violation occurred as stated in the
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Notice of Violation. The corrective actions stated in the response have been completed and this item is close (CLOSED) Inspector Followup Item 369, 370/86-28-04, Testing of Safety Valve Procedure PT/0/A/4150/05, now contains instructions on observing the trend of safety valve lift setpoint See section 9 for more information on this P ,
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  (CLOSED) Unresolved Item 369/86-28-07, Blocking of Safety function This issue dealt with blocking of the low pressure safety injection signal when a safety valve opened and caused excessive blowdown while in hot standby, Mode The licensee has reinforced the policy of not blocking automatic safety actuations except when directed by approved procedures or 10 CFR 50.54(x). This : tem is' close (CLOSED) Violation 369, 370/86-28-01, failure to Repor Corrective actions have been taken and this item is close . Licensee Event Report (LER) Followup (90712, 92700)
The following LER's were reviewed to determine whether reporting require-  l ments have been met, the cause appears accurate, the corrective actions  i appear appropriate, generic applicability has been considered, and whether  !
t1e event is related to previous events. Selected LER's were chosen for more detailed followup in verifying the nature, impact, and cause of the event as well as corrective actions taken.
 
l (CLOSED) Licensee Event Report 369/86-17, Both Trains of Hydrogen Mitigation System Inoperable. Multiple failures of hydrogen ignitors during quarterly surveillance testing resulted in both trains of the hydrogen mitigation system being declared inoperable. The licensee has  l evaluated the life expectancy of the ignitors and estimates six years as a  l conservative life expectancy. Corrective action includes replacing the  I ignitors every four year (CLOSED) Licensee Event Report 370/86-03, Unidentified Reactor Coolant Leakage Due to Leaking Valves Resulting in Shutdown. Four valves were  l found to be leaking and subsequently repaired, i
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  (CLOSED) Licensee Event Report 370/86-06, Failure to Maintain Required Boration Flow Path Due to Personnel Error. The event was discussed in an operations staff aeeting and shift supervisor meetin (CLOSED) Licensee Event Report, 370/86-19, Missed Surveillance on Essential Auxiliary Power System Corrective actions have been completed and this item is close (CLOSED) Licensee Event Report 369/87-02, Both Trains of Containment Spray System Inoperable. This event resulted in violation 369/87-04-01 and corrective actions are being tracked in followup to the violatio . Pressurizer Safety Valve Setpoint Testing During a review of the completed data sheets for PT/0/A/4150/05, Pressurizer Safety Valve Setpoint Test, it was noted that the maintenance personnel signing the data sheets for satisfactory lift checks were not the personnel who were trained to perform the tests. In a letter to the NRC dated July 22, 1987, the licensee committed to allowing only specially trained personnel to work and test these valves. This commitment was made -
in response to violation 369/86-28-06 which involved a primary system safety valve opening at a pressure outside the T.S. limit. The tests in question were performed on September 14, 1987; June 11, 1987 and June 13, 198 The licensee stated that the qualified individuals were present but non qualified individuals signed the data sheet for the qualified individuals. The licensee stated that in the future the data sheets will
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be clearly annotated if a non qualified person signs for a qualified person and the data sheet will contain the name of qualified person performing the tes Another problem with the test performed on pressurizer code safety valve 2NC1 on June 11, 1987, was discovere The data sheet for this test listed a lif t pressure of 2513 psi for the second lift of the valve. The procedure specified that each lift must be within the TS required range of 2485 psig plus or minus 1 percent (2461 to 2509). The other lift pressures were within the required band and the average of the three lifts was also within the required range. This is a second example of an apparent violation (370/88-09-01) of T.S. 6.8.1 for failure to properly implement the written procedure for pressurizer safety valve setpoint testing. Corrective actions for violation 369/86-28-06 should have
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prevented this violation from occurring in that personnel were trained on the specific requirements. Contributing to the violation was the fact that the data sheet did not clearly specify that each lift must be within the required band.
 
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The licensee initiated a Problem Investigation Report when this item was brought to their attention by the inspector. The Itcensee has stated that the maintenance and quality control personnel involved believe the actual lift setpoint was in the required band but the data was incorrectly recorded. All parties state they were aware each lift was required to be i
 
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within plus or minus 1 percent of 2485 psig. The proposed corrective
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actions include changing the procedure, counciling the persons involved, '
and expediting the development of a training program in this are ;
During the review Power Research of the p(ressurizer Institute EPRI) Reportsafety valve NP-4235, Setsetpoint test, Electric point Testing of !
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Safety Valves Using Alternative Test Methods, was reviewe This EPRI report was prepared to present the results of tests performed and to
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correlate alternate test methods for safety valve tests to testing using i  full pressure steam as the test medium. The full pressure steam test method most closely simulates the actual conditions which the valve  '
experiences in the system. It is noted, however, that McGuire has loop seals in the lines from the pressurizer to the code safety valves so steam
;  is not actually on the valves. The licensee uses an alternate test method j  using nitrogen as the pressure medium rather than stea The EPRI test >
results appear to indicate that:
1 Tolerance bands using the nitrogen test method need to be much  .
tighter than plus or minus 1.0% in order to assure the valve will '
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lift at TS recuired 2485 plus or minus 1.0% psi while installed in !
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the system. The licensee currently uses a plus or minus 1.0%  i tolerance band using nitroge The actual valve lift setpoint using steam will be lower than the 3  setpoint using nitroge It was discovered that generic correlations '
could not be made to relate nitrogen tests to actual in place lift
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setpoints; however, correlations on a valve-by-valve basis can be -
made with a higher degree of confidenc The method for determining ,
;  the valve correlations is given in Appendix E of the EPRI report.
 
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The licensee currently does not use any correlations to correct the !
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lift point using nitrogen to the lift point using a steam mediu j
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T.S. 3.4.2.2 requires that pressurizer code safety valves have a lift  i setting of 2485 psig plus or minus 1 percent and the lift setting pressure i'
i  shall correspond to ambient conditions of the valve at nominal operating t
temperature and aressure. Based on the information available in EPRI  !
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Report NP-4235, it is not clear that the pressurizer code safeties would lift within the TS required range at normal system operating temperature i and pressure. The licensee has indicated that the EPRI report does not i  take into consideration the fact that McGuire has loop seals in the lines
)  to the pressurizer code safetie According to the licensee, the ,
y  temperature of the water at the code safety is 140 degrees F and testing :
at Wyle Laboratories has confirmed direct correlation between nitrogen j  lifts under ambient conditions and nitrogen with 140 degree F water at the i i
valve inlet. The licensee stated that Catawba and Oconee send their
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pressurizer code safeties to Wyle to have hot lifts performed since  i neither have loop seal This item was still being rev'ewed at the end of the inspection perio I
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10. Nuclear Service Water Valves Inoperable On March 9,1988, during a system walkdown a licensee engineer discovered Unit 1 Nuclear Service Water (RN) valve 1RN1908, (RN to component cooling (KC) heat exchanger 18 throttle valve) to be inoperable. A travel stop that limits the maximum 03en position of the valve had become repositioned toward the closed direction and was found to be loose. If the valve had been called upon during an Engineered Safety Features (ESF) actuation, the repositioned stop would have prevented required RN flow to the KC heat exchanger from occurring, and would have possibly prevented the KC system from adequately cooling critical com)onents in a design basis acciden The travel stops are precisely set curing RN system flow balance tests designed to balance RN system flow among all the RN heat loads, including K The licensee estimates that RN flow to the KC heat exchanger would have been reduced approximately 1500 gpm below the required 6000 gpm in the event of an ESF actuation. The licensee considers that the heat removal capability of the 8 train of KC, although impaired, was adequate due to low RN temperature and the clean condition of the KC heat exchanger. This hypothesis is based on design engineering analysis. Upon discovery, the licensee declared the KC train inoperable and took prompt action to restore the travel stops to the most recent tested position.
 
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The last RN flow balance test was conducted on January 29, 1988, at which time the valve stops were adjusted. The licensee could not produce any documentation or evidence of authorized work conducted on 1RN1908 that may have affected the travel stop positions since this last test. It is known
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that the travel stops have been routinely used to secure the valve in the i shut position to facilitate isolation for other work. A work recuest usual'y documents these occasion The licensee concluded that tie hex nuts securing the travel stop had vibrated loose allowing the stop to drift in the closed direction. In normal operation the valve is throttled significant'ly in the closed direction with the travel stop performing no function, thus it was free to drift upon loosening of the nut Technical Specification 3.7.3 requires that both trains of KC be operable during operation in Modes 1, 2, 3, and 4. One train may be inoperable for -
up to 72 hours in these mode The mis positioned travel stops on IRN1908 resulted in train B of KC being technically inoperable from the last documented position of the valve on January 29, until the discovery of the problem on March 9. This is an apparent violation (369/88-09-02) of the action statement requirements of Technical Specification 3. In an unrelated event, on March 28, 1988, the licensee determined that i valve IRN-21, RN Strainer IA automatic backwash valve, underwent maintenance on February 4,1988, without subsequent retest. This valve is
 
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,'  designed to automatically open upon high differential pressure across the l 1A RN strainer thereby allowing backwash flow to clean the strainer. This i flow is diverted from the total A train RN flo Upon an ESF signal, !
RN-21 shuts, if open, to ensure that all RN flow is supplied to ESF heat loads cooling critical components in accident situations. A packing
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adjustment was performed on RN-21 on February 4,1988, under a work request to investigate and correct a packing lea The work request incorrectly identified that a retest was not require Maintenance personnel tightened the packing but determined that the )acking leak could not be stopped without over tightening the packing there)y impairing valve stroke. The work request had a contingency to be re-scheduled until an outage if tightening the packing was unsuccessful. The work request was !
returned to planning for this purpose. Contributing to this problem was the fact that maintenance clearance was also deemed to be not required which resulted in operations being not fully informed of the extent of work being conducted on the valv j
. Technical Specification 4.0.5 states that testing to ASME Code require- !
ments is required to properly retest ESF components following maintenance. ;
Station Directive 3.2.2, Identifying and Performing Plant Retesting, ;
implements these requirements by identifying the components and types of !
maintenance that require retests as well as identifying the retest j require RN-21 is identified as a component requiring retes !
Adjustment of stem packing is an example of maintenance requiring retes In tnis case a valve stroke timing test should have been performed since '
the valve is required to shut within 60 seconds upon receipt of an ESF signa !
On March 28, 1988, the licensee detected the error on the work request and immediately added RN-21 to the TS Action Item Log for RN train A which was :
currently declared inoperable for unrelated reasons. The performance of a stroke timing test at that point could have determined valve operability, '
however, add"tional packing adjustment took place first. During the subsequent stroke timing test, the valve failed to shut. Licensee review of operator aids computer (OAC) data revealed that the valve was actually required to automatically open and shut numerous times between February 4 and March 28 to correct high strainer differential pressur ,
Typical i stroke times on these occas'ons, as recorded by the OAC, show that the ,
valve shut well within the maximum time permitted, (approximately 10 l seconds vs maximum 60 seconds) The licensee has stated that it is likely 5 that satisfactory results would have been obtained had a formal stroke timing test been conducted after the initial packing adjustment. It was i likewise hypothesized that the valve would have performed its safety j function during the time of unknown inoperability. The licensee considers l that the final packing adjustment caused the valve to fail to shu Technical Specification 3.7.4 requires that two trains of RN be operable in modes 1, 2, 3, and 4. One train may be inoperable for up to 72 hours in these modes. The failure of the work request to aroperly identify that a retest was required caused the requirements conta:ned in TS 4.0.5 to be omitted. This resulted in RN-21 and thus train A of RN to be inoperable from February 4 to March 28, 1988. Mitigating factors, however, lessen the significance of the RN-21 inoperability. The total flow diverted with RN-21 open is approximately 700 gpm. This amount is a small portion of the total RN flow of greater than 12,000 gpm available from one train
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f during accident condition Also, RN temperature during the time of inoperability was in the range of 40 to 50F, well below the design temperature of 78F. Design engineering evaluation indicates that ample heat sink existed for A train RN to perform its safety function. The prime concern and root cause of this particular event is the failure to retest as described above. This item is identified as an apparent violation (369/88-09-03) of Technical Specification 4. The inoperability of the two RN valves discussed above occurred over an extended period of time resulting in numerous occasions when both trains of RN or the systems they support were rendered inoperable. Most notable is the overlapping period (February 4 to March 9) when both RN valves were inoperable rendering both trains of KC inoperable. The NRC recognizes the mitigat;ng factors discussed above and considers the safety significance of these specific events to be minima However, had conditions been less favorable or other components been involved, the safety significance ,
could have been much greater. The NRC is particularly concerned with '
the events associated with the RN-21 problem from the stand 30 int of maintenance work control and retesting. The inspectors have initiated a thorough study of the work control process to determine if sufficient controls are in place to prevent missed retests and unknown inoperabili- i ties of safety system component . Ground Water Detection    ;
On April 12, 1988, NRR technical staff reviewed the Groundwater Monitoring System and conducted a walkdown of selected monitoring wells ( Auxiliary Building East and West wall exterior monitors, Auxiliary Building north wall interior monitors PP-51, QQ-56 and PP-61), and Auxiliary Building drain sump "C". System operators and surveillances were found to be consistant with T.S. 3.4. 7.13 requirements. On April 13, 1988 design calculations of hydrostatic and buoyancy influences and overturning potential for the Auxiliary Building, Reactor Buildings, and Diesel Generator Buildings were audited at licensee's corporate engineering offices. This review is part of the NRC's review of Duke's request for l Technical Specifications 3.4.7.13 changes dated January 27, 198 ;
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Revision as of 02:47, 6 November 2020

Ack Receipt of 880531 Ltr Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-369/88-09 & 50-370/88-09
ML20195H121
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 06/16/1988
From: Brownlee V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Tucker H
DUKE POWER CO.
References
NUDOCS 8806280221
Download: ML20195H121 (1)


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