ML20153F521

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Insp Repts 50-369/88-09 & 50-370/88-09 on 880319-0422. Violations Noted.Major Areas Inspected:Operations,Safety Verification,Surveillance Testing,Maint Activities & Followup on Previous Insp Findings
ML20153F521
Person / Time
Site: Mcguire, McGuire  Duke Energy icon.png
Issue date: 04/29/1988
From: William Orders, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20153F513 List:
References
50-369-88-09, 50-369-88-9, 50-370-88-09, 50-370-88-9, NUDOCS 8805100356
Download: ML20153F521 (12)


See also: IR 05000369/1988009

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- UNITED STATES

[in Rio I o,^ NUCLEAR REGULATORY COMMISSION

REGION il

h8Y h , g

, .101 MARIETTA STREET.N.W.

ATLANTA GEORGIA 30323

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Report Nos.: 50-369/88-09 and 50-370/88-09

Licensee: Duke Power Company l

422 South Church Street  !

Charlotte, NC 28242  !

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Docket Nos.: 50-369 and 50-370 License Nos.: NPF-9 and NPF-17

, Facility Name: McGuire 1 and 2

Inspection Conducte g arch 19, 1988 - April 22, 1988

Inspector [ AM/  ;

<'w;mrders, Senior)dsidentInspector /Da4V 5fgneo

Accompanying Personnel: D. Nelson  ;

R. Croteau  !

Approved by:E A. Peebles, SectiorAChief

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D&te'5igned

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, DivisionofReactorFrojects

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SUMMARY  !

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Scopt, This routine unannounced inspection involved the areas of operations  :

. safety verification, surveillance testin maintenance activities, and

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follow-up on previous inspection findings, g, i

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Results: In the areas inspected three violations were identified. One I

violation was identified which ir$cluded two examples for failora to follow  !

procedure during safety valve testing and an inadequate procedure for slave  !

relay testing. A second violation was identified which involved an inoperable l

component cooling train and the *. aird violaticr. involved a failure to perform i

post maintenance testing which rendered a nuclear service water train ,

inoperable. j

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l 8805100356 880429 i

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PDR ADOCK 05000369

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REPORT DETAILS

1. Persons Contacted

Licensee Empicyees

  • T. McConnell, Plant Manager

i 8. Travis, Superintendent of Operations

  • H. Suple, Superintendent of Maintenance

B. Hauilton, Superintendent of Technical Services

R. Sharpe, Compliance Engineer

J. Boyle, Superintendent of Integrated Scheduling

L. Firebaugh, OPS /NPE/MNS

  • S. LeRoy, Licensing, General Office
  • D. Baxter, OPS /MNS/NPD
  • S. Copp, Planning Engineer

R. Panner, Compliance  :

J. Snyder, Performance Engineer

  • N. Atherton, Compliance
W.Reeside}AEEngineerOperations

R. White, Engineer

  • G. Gilbert, MNS/NPD

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Other licensee employees contacted included construction craftsmen,

technicians, operators, mechanics, security force members, and office

personnel.

  • Attended exit interview

2. Exit Interview (30703)

The inspection findings identified below were summarized on April 22, i

1988, with those persons indicated in paragraph 1 above. The following

items were discussed in detail:

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1 (OPEN) Violation 370/88-09-01, Failure to follow procedure for

Pressurizer Code Safety Valve Testing and Inadequate Procedure for

Slave Relay Testing. (Seeparagraphs5and9).

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(OPEN) Violation 369/88-09-02,

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Train Due to Inoperable Nuclear Service Water (RN) Valve. See Inoperable Co

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paragraph 10).  !

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(OPEN) Vio1rion 369/88-09-03, Inoperable RN Train Due to a Failure

to Test RN-21. (See paragraph 10).

The licensee representatives present offered no dissenting comments, nor

did they identify as proprietary any of the information reviewed by the

inspectors during the course of their inspection.

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3. Unresolved Items

An unresolved item (UNR) is a matter about which more information is

required to determins whether it is acceptable or may involve a violation

or deviation. There were no unresolved items identified in this report.

4. Plant Operations (71707, 71710)

The inspection staff reviewed plant operations durir:g the report period to

verify conformance with applicable regulatory requirements. Control room

logs, shift supervisors' logs, shift turnover records and equipment

removal and restoration records were routinely aerused. Interviews were

conducted with plant operations, maintenance, clemistry, health physics,

and performance personnel.

Activities within the control room were monitored during shifts and at

! shift cMnges. Actions and/or activities observed were conducted as

prescribed in applicable station administrative directives. The complement

of licensed personnel on each shift met or exceeded the minimum required

by Technical Specifications.

Plant tours taken during the reporting period included, but were not

limited to, the turbine buildings, the auxiliary building, Units 1 and 2

electrical equipment rooms, Units 1 and 2 cable spreading rooms, and the

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station yard zone inside the protected area.

During the plant tours, ongoing activities, housekeeping, security,

equipment status and radiation control practices were observed.

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Use of overtime by operations was reviewed to verify cornpliance with TS

requirements. Documentation showed that the maximum overtime limits were

exceeded approximately nine times in 1987-1988, primarily for outage

support. It is allowable to exceed the maximum limits for very unusual

circumstances. Operations Management Procedure 1-7, Shift Manning and

Overtime Requirements, requires that overtime worked in excess of

guidelines be authorized in advance by the station manager or his designee

(another high level of management). The inspector noted that in September

of 1987 two instances of exceeding the maximum overtime limits were not

authorized in advance. The licensee received a violation for this issue

(see Inspection Report 369, 370/87-26) in the September 1987 period and

corrective actions have been taken.

a. Unit 1 Operations

Unit 1 began the reporting period at full power. On March 23, 1988,

the unit emerienced a saurious safety injection (SI), main steam

isolation ar,d reactor tr p. The spurious SI signal was generated in

a Solid State Protection Syetem (SSPS) caLinet containing the

circuitry for A train low steam line pressure SI and main steam

isolation. Licensee technicians had just completed testing in this

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cabinet and were closing the door. The spurious signal occurred when

the door was shut. All A train SI components actuated and the hiah

head pump injected into the primary coolant system. Main steam'

isolation and feed water isolation occurred, generating a turbine

trip and resultant reactor trip. Operators determined that the SI

was inadvertant and secured the injection in approximately nine

minutes. No major problems occurred during the transient. All A

train SI components functioned as designed during the transient,

except that the reactor trip was caused by the turbine trip above P-8

instead of directly by the SI actuation as would be expected. The

cause for this was determined later and is discussed below. During

the event a low steam generator level in the C steam generator caused

auxiliary feedwater (CA) to initiate a second time.

After the unit was stabilized, Instrumentation and Electrical (IAE)

technicians attemnted to determine the cause of the SI signal. The

spurious signal was duplicated several times by agitating the SSPS

cabinet. However, the signal could not be repeated following the

shutting of a nearby heavy door. Further investigation could not

determine the exact cause of the problem. The licensee considers

that a sina11 piece of loose wire or other conductor had shorted or

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grounded the circuitry u)on agitation of the cabinet. According to

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the licensee, the additional agitation conducted during trouble-

shooting, and finally the shutting of the nearby door served to

vibrate the conductor away from the electrical centacts. A thorough

cleaning of the cabinet was performed. This arod'ned some small wire

fragments which could have caused what the l'censee postulates. The

licensee also considers that the points of contact occurred in the

low steamline pressure SI circuit downstream from the point where the

reactor trip function branches off, thereby causing the SI to

initiate without causing a direct reactor trip. Following the

cleaning a complete functional surveillance was performed with no

problems. The unit was restarted and achieved full power the ,

following day. No similar problems in SSPS have developed.

On March 27, load was decreased to 86 percent power due to decreased

load demand on the grid and was back at full power at 1247 a.m. on i

March 28. Later on March 28 power was reduced to 46 percent to

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support removal of a voltage regulator control drawer. Unit 1

returned to 100 percent power on March 29. ,

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On April 16, Unit I was manually tripped from 100 percent power due

to decreasing le<el in the C steam generator (SG) caused >y the C

feed regulating nice (FRV) failing shut. The C FRV shut due to a

" blown fuse on a wd controlling the valve. The card was later

tested and found to be the cause of the blown fuse. Auxiliary feed

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water (CA) auto started on low steam generator levels but 1SA-49,

steam supply from the 8 SG to the turbine driven CA pump, did not

indicate open due to problems with the position indicating limit i

switches. The valve was actually open. The limit switches were

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adjusted, tha' FRV card was replaced, and the unit returned to 100 t

percent power oa April 18.

l b. Unit 2 Operations _

Unit 2 operated at full power for the entire period. The SI on Unit  !

i 1, discussed above, did lowever affect Unit 2. Due to the alignment

of the common portion of the Nuclear Service Water (RN) System, the ,

operating Unit 2 RN train was isolated by the single train SI on Unit '

l 1. Had both SI trains on Unit 1 actuated, the common portion of RN

would have realigned to ensure continued RN operation on Unit 2.

Various Unit 2 component temperatures elevated, but Unit 2_ operators

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diagnosed and corrected the problem in time to prevent any additional

a required actions.

No violations or deviations were identified.

5. Surveillance Testing (61726)

Selected surveillance tests were analyzed and/or witnessed by the

inspector to ascertain procedural and performance adequacy and ccnformance

with applicable Technical Specifications.

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Selected tests were witnessed to ascertain that current written approved

procedures were available and in use, that test equipment in use was

calibrated, that test prerequisites were met, that system restoration was ,
completed and test results were adequate. l

Detailed below are selected tests which were either reviewed or witnessed:

PROCEDURE EQUIPHENT/ TEST

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PT/0/A/4150/05 Pressurizer Safety Valve.Setpoint Test

PT/1/A/4403/007 RN 1A Flow Balance Test i

PT/2/A/4200/28A SSPS Slave Relay Tests l

PT/1/A/4208/03A Train 1A NS Heat Exchanger Performance Test

PT/1/A/4252/018 CA Pump IB Performance Test

PT/1/A/4601/088 SSPS Train B Periodic Test l

PT/1/A/4403/018 RN Train IB Performance Test

PT/1/A/4403/01A RN Train 1A Performance Test

PT/1/A/4206/01A NI Pump 1A Performance Test

PT/1/A/4252/01A CA Pump 1A Performance Test

PT/1/A/4204/01B ND Pump 1B Performance Test

PT/2/A/4209/01A NV Pump 2A Performance Test

PT/2/A/4206/01A NI Pump 2A Performance Test

PT/0/A/4350/38 125 VDC Battery Service Test

See paragraph 9 for further information conce ning PT/0/A/4150/05.

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On March 22 at 10:02 AM, a procedure error in a performance seriodic test

procedure caused re-alignment of power sources to severa' Unit 2 '

non-safety containment ventilation systems. A step in grocedure i

PT/2/A/4200/28A, Slave Relay Test, directs the opening of a sliding link"  :

to prevent ventilation units from tripping during the test. This occurs

in the section of the procedure that tests slave relays in the Train A

Safety Injection SSPS circuitry. The step specifies opening sliding link

H-3 in cabinet 2ATC8. When the system was actuated in a subsecuent step, ,

several non-safety containment ventilation systems experiencec a shunt

trip to re-align their power sources to non-safet The affected

systems were lower containment ventilation (VL)y, buses.

Upper Containment

Ventilation (VU), and Control Rod Drive Mechanism Cooling" Ventilation

(VR). These non-safety systems are designed to "load shed in the event

of an ESF actuation to lessen the electrical load on safety system power

sources. The loid shed took 31 ace because the wrong sliding link was

specified. A step at the comp:etion of the test specifies closing sliding

link I-2 in the same cabinet. I-2 is the correct sliding link that should

have been opened originally. Having the wrong sliding link open during

the test did not othenvise adversely effect the test or plant operation.

The procedure

is therefore error constitutes

an apparent an examp/88-09-01).le of an inadequate proce

violation. (370

The licensee states that the procedure error occurred in a recent re-write

of the procedure, but has no explanation for why it occurred. Another

case of an unexplained procedure change occurred recently in an operations

procedure which was discussed in NRC inspection report 50-369,~370/88-04.

In that case two procedure steps were interchanged during re-write. A

violclion was issued for that occurrence, but the licensee's corrective

action appeared to be limited to the operations organization where the

problem occurred. When the corrective actions and lessons learned are

shared with other departments, similar problems may be prevented.

6. MaintenanceObservations(62703)

Routine maintenance activities were reviewed and/or witnessed by the

resident inspection staff to ascertain procedural and performance adequacy

and conformance with applicable Technical Specifications.

The selected activities witnessed were examined to ascertain that, where

a3plicable, current written approved procedures were available and ir use,

t1at prerequisites were met, that equipment restoration was completed and

maintenance results were adequate.

No violations or deviations were identified.

7. Follow-up on Previous Inspection Findings (92702)

The following previously identified items were reviewed to ascertain that

the licensee s responses, were applicable, and licensee actions were in

compliance with regulatory requirements and corrective actions have been

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completed. Selective verification included record review, observations,

and discussions with licensee personnel.

(CLOSED) Violation 369, 370/85-06-04. Failure to Take Prompt Corrective I

Action to Notify Operations Personnel of Potential Degradation of

Auxiliary Feedwater System and Correct Improper Valve Installation. .

Nuclear Station Modifications (NSM's) were completed by July 21, 1985

which installed temperature monitors to detect check valve leakage and

replaced the stop check valves with a different design valve. The

completed NSM's were reviewed and selected check valves were physically

verified to be in place by the inspector. The violation was initially

denied but the NRC determined that the violation occurred as stated in the

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Notice of Violation. The corrective actions stated in the response have

been completed and this item is closed.

(CLOSED) Inspector Followup Item 369, 370/86-28-04, Testing of Safety

Valves. Procedure PT/0/A/4150/05, now contains instructions on observing

the trend of safety valve lift setpoints. See section 9 for more

information on this PT. ,

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(CLOSED) Unresolved Item 369/86-28-07, Blocking of Safety functions. This

issue dealt with blocking of the low pressure safety injection signal when

a safety valve opened and caused excessive blowdown while in hot standby,

Mode 3. The licensee has reinforced the policy of not blocking automatic

safety actuations except when directed by approved procedures or

10 CFR 50.54(x). This : tem is' closed.

(CLOSED) Violation 369, 370/86-28-01, failure to Report. Corrective

actions have been taken and this item is closed.

8. Licensee Event Report (LER) Followup (90712, 92700)

The following LER's were reviewed to determine whether reporting require- l

ments have been met, the cause appears accurate, the corrective actions i

appear appropriate, generic applicability has been considered, and whether  !

t1e event is related to previous events. Selected LER's were chosen for

more detailed followup in verifying the nature, impact, and cause of the

event as well as corrective actions taken.

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(CLOSED) Licensee Event Report 369/86-17, Both Trains of Hydrogen

Mitigation System Inoperable. Multiple failures of hydrogen ignitors

during quarterly surveillance testing resulted in both trains of the

hydrogen mitigation system being declared inoperable. The licensee has l

evaluated the life expectancy of the ignitors and estimates six years as a l

conservative life expectancy. Corrective action includes replacing the I

ignitors every four years.

(CLOSED) Licensee Event Report 370/86-03, Unidentified Reactor Coolant

Leakage Due to Leaking Valves Resulting in Shutdown. Four valves were l

found to be leaking and subsequently repaired,

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(CLOSED) Licensee Event Report 370/86-06, Failure to Maintain Required

Boration Flow Path Due to Personnel Error. The event was discussed in an

operations staff aeeting and shift supervisor meeting.

(CLOSED) Licensee Event Report, 370/86-19, Missed Surveillance on

Essential Auxiliary Power Systems. Corrective actions have been completed

and this item is closed.

(CLOSED) Licensee Event Report 369/87-02, Both Trains of Containment Spray

System Inoperable. This event resulted in violation 369/87-04-01 and

corrective actions are being tracked in followup to the violation.

9. Pressurizer Safety Valve Setpoint Testing

During a review of the completed data sheets for PT/0/A/4150/05,

Pressurizer Safety Valve Setpoint Test, it was noted that the maintenance

personnel signing the data sheets for satisfactory lift checks were not

the personnel who were trained to perform the tests. In a letter to the

NRC dated July 22, 1987, the licensee committed to allowing only specially

trained personnel to work and test these valves. This commitment was made -

in response to violation 369/86-28-06 which involved a primary system

safety valve opening at a pressure outside the T.S. limit. The tests in

question were performed on September 14, 1987; June 11, 1987 and June 13,

1987. The licensee stated that the qualified individuals were present but

non qualified individuals signed the data sheet for the qualified

individuals. The licensee stated that in the future the data sheets will

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be clearly annotated if a non qualified person signs for a qualified

person and the data sheet will contain the name of qualified person

performing the test.

Another problem with the test performed on pressurizer code safety valve

2NC1 on June 11, 1987, was discovered. The data sheet for this test

listed a lif t pressure of 2513 psi for the second lift of the valve. The

procedure specified that each lift must be within the TS required range of

2485 psig plus or minus 1 percent (2461 to 2509). The other lift

pressures were within the required band and the average of the three lifts

was also within the required range. This is a second example of an

apparent violation (370/88-09-01) of T.S. 6.8.1 for failure to properly

implement the written procedure for pressurizer safety valve setpoint

testing. Corrective actions for violation 369/86-28-06 should have

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prevented this violation from occurring in that personnel were trained on

the specific requirements. Contributing to the violation was the fact

that the data sheet did not clearly specify that each lift must be within

the required band.

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The licensee initiated a Problem Investigation Report when this item was

brought to their attention by the inspector. The Itcensee has stated that

the maintenance and quality control personnel involved believe the actual

lift setpoint was in the required band but the data was incorrectly

recorded. All parties state they were aware each lift was required to be

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within plus or minus 1 percent of 2485 psig. The proposed corrective

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actions include changing the procedure, counciling the persons involved, '

and expediting the development of a training program in this area.  ;

During the review

Power Research of the p(ressurizer

Institute EPRI) Reportsafety valve

NP-4235, Setsetpoint test, Electric

point Testing of  !

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Safety Valves Using Alternative Test Methods, was reviewed. This EPRI

report was prepared to present the results of tests performed and to

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correlate alternate test methods for safety valve tests to testing using

i full pressure steam as the test medium. The full pressure steam test

method most closely simulates the actual conditions which the valve '

experiences in the system. It is noted, however, that McGuire has loop

seals in the lines from the pressurizer to the code safety valves so steam

is not actually on the valves. The licensee uses an alternate test method

j using nitrogen as the pressure medium rather than steam. The EPRI test >

results appear to indicate that:

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a. Tolerance bands using the nitrogen test method need to be much .

tighter than plus or minus 1.0% in order to assure the valve will '

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lift at TS recuired 2485 plus or minus 1.0% psi while installed in  !

the system. The licensee currently uses a plus or minus 1.0% i

tolerance band using nitrogen.

b. The actual valve lift setpoint using steam will be lower than the

3 setpoint using nitrogen. It was discovered that generic correlations '

could not be made to relate nitrogen tests to actual in place lift

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setpoints; however, correlations on a valve-by-valve basis can be -

made with a higher degree of confidence. The method for determining ,

the valve correlations is given in Appendix E of the EPRI report.

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The licensee currently does not use any correlations to correct the  !

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lift point using nitrogen to the lift point using a steam medium. j

T.S. 3.4.2.2 requires that pressurizer code safety valves have a lift i

setting of 2485 psig plus or minus 1 percent and the lift setting pressure i'

i shall correspond to ambient conditions of the valve at nominal operating

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temperature and aressure. Based on the information available in EPRI  !

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Report NP-4235, it is not clear that the pressurizer code safeties would

lift within the TS required range at normal system operating temperature i

and pressure. The licensee has indicated that the EPRI report does not

i take into consideration the fact that McGuire has loop seals in the lines

) to the pressurizer code safeties. According to the licensee, the ,

y temperature of the water at the code safety is 140 degrees F and testing  :

at Wyle Laboratories has confirmed direct correlation between nitrogen

j lifts under ambient conditions and nitrogen with 140 degree F water at the i

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valve inlet. The licensee stated that Catawba and Oconee send their

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pressurizer code safeties to Wyle to have hot lifts performed since i

neither have loop seals. This item was still being rev'ewed at the end of

the inspection period. I

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10. Nuclear Service Water Valves Inoperable

On March 9,1988, during a system walkdown a licensee engineer discovered

Unit 1 Nuclear Service Water (RN) valve 1RN1908, (RN to component cooling

(KC) heat exchanger 18 throttle valve) to be inoperable. A travel stop

that limits the maximum 03en position of the valve had become repositioned

toward the closed direction and was found to be loose. If the valve had

been called upon during an Engineered Safety Features (ESF) actuation, the

repositioned stop would have prevented required RN flow to the KC heat

exchanger from occurring, and would have possibly prevented the KC system

from adequately cooling critical com)onents in a design basis accident.

The travel stops are precisely set curing RN system flow balance tests

designed to balance RN system flow among all the RN heat loads, including

KC. The licensee estimates that RN flow to the KC heat exchanger would

have been reduced approximately 1500 gpm below the required 6000 gpm in

the event of an ESF actuation. The licensee considers that the heat

removal capability of the 8 train of KC, although impaired, was adequate

due to low RN temperature and the clean condition of the KC heat

exchanger. This hypothesis is based on design engineering analysis. Upon

discovery, the licensee declared the KC train inoperable and took prompt

action to restore the travel stops to the most recent tested position.

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The last RN flow balance test was conducted on January 29, 1988, at which

time the valve stops were adjusted. The licensee could not produce any

documentation or evidence of authorized work conducted on 1RN1908 that may

have affected the travel stop positions since this last test. It is known

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that the travel stops have been routinely used to secure the valve in the i

shut position to facilitate isolation for other work. A work recuest

usual'y documents these occasions. The licensee concluded that tie hex

nuts securing the travel stop had vibrated loose allowing the stop to

drift in the closed direction. In normal operation the valve is throttled

significant'ly in the closed direction with the travel stop performing no

function, thus it was free to drift upon loosening of the nuts.

Technical Specification 3.7.3 requires that both trains of KC be operable

during operation in Modes 1, 2, 3, and 4. One train may be inoperable for -

up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in these modes. The mis positioned travel stops on IRN1908

resulted in train B of KC being technically inoperable from the last

documented position of the valve on January 29, until the discovery of the

problem on March 9. This is an apparent violation (369/88-09-02) of the

action statement requirements of Technical Specification 3.7.3.

In an unrelated event, on March 28, 1988, the licensee determined that i

valve IRN-21, RN Strainer IA automatic backwash valve, underwent

maintenance on February 4,1988, without subsequent retest. This valve is

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,' designed to automatically open upon high differential pressure across the l

1A RN strainer thereby allowing backwash flow to clean the strainer. This i

flow is diverted from the total A train RN flow. Upon an ESF signal,  !

RN-21 shuts, if open, to ensure that all RN flow is supplied to ESF heat

loads cooling critical components in accident situations. A packing

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adjustment was performed on RN-21 on February 4,1988, under a work

request to investigate and correct a packing leak. The work request

incorrectly identified that a retest was not required. Maintenance

personnel tightened the packing but determined that the )acking leak could

not be stopped without over tightening the packing there)y impairing valve

stroke. The work request had a contingency to be re-scheduled until an

outage if tightening the packing was unsuccessful. The work request was  !

returned to planning for this purpose. Contributing to this problem was

the fact that maintenance clearance was also deemed to be not required

which resulted in operations being not fully informed of the extent of

work being conducted on the valve. j

. Technical Specification 4.0.5 states that testing to ASME Code require-  !

ments is required to properly retest ESF components following maintenance. ;

Station Directive 3.2.2, Identifying and Performing Plant Retesting,  ;

implements these requirements by identifying the components and types of  !

maintenance that require retests as well as identifying the retest j

required. RN-21 is identified as a component requiring retest.  !

Adjustment of stem packing is an example of maintenance requiring retest.

In tnis case a valve stroke timing test should have been performed since '

the valve is required to shut within 60 seconds upon receipt of an ESF

signal.  !

On March 28, 1988, the licensee detected the error on the work request and

immediately added RN-21 to the TS Action Item Log for RN train A which was :

currently declared inoperable for unrelated reasons. The performance of a

stroke timing test at that point could have determined valve operability, '

however, add"tional packing adjustment took place first. During the

subsequent stroke timing test, the valve failed to shut. Licensee review

of operator aids computer (OAC) data revealed that the valve was actually

required to automatically open and shut numerous times between February 4

and March 28 to correct high strainer differential pressure.

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stroke times on these occas'ons, as recorded by the OAC, show that the ,

valve shut well within the maximum time permitted, (approximately 10 l

seconds vs maximum 60 seconds) The licensee has stated that it is likely 5

that satisfactory results would have been obtained had a formal stroke

timing test been conducted after the initial packing adjustment. It was i

likewise hypothesized that the valve would have performed its safety j

function during the time of unknown inoperability. The licensee considers l

that the final packing adjustment caused the valve to fail to shut.

Technical Specification 3.7.4 requires that two trains of RN be operable

in modes 1, 2, 3, and 4. One train may be inoperable for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

in these modes. The failure of the work request to aroperly identify that

a retest was required caused the requirements conta:ned in TS 4.0.5 to be

omitted. This resulted in RN-21 and thus train A of RN to be inoperable

from February 4 to March 28, 1988. Mitigating factors, however, lessen

the significance of the RN-21 inoperability. The total flow diverted with

RN-21 open is approximately 700 gpm. This amount is a small portion of

the total RN flow of greater than 12,000 gpm available from one train

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during accident conditions. Also, RN temperature during the time of

inoperability was in the range of 40 to 50F, well below the design

temperature of 78F. Design engineering evaluation indicates that ample

heat sink existed for A train RN to perform its safety function. The prime

concern and root cause of this particular event is the failure to retest

as described above. This item is identified as an apparent violation

(369/88-09-03) of Technical Specification 4.0.5.

The inoperability of the two RN valves discussed above occurred over an

extended period of time resulting in numerous occasions when both trains

of RN or the systems they support were rendered inoperable. Most notable

is the overlapping period (February 4 to March 9) when both RN valves were

inoperable rendering both trains of KC inoperable. The NRC recognizes the

mitigat;ng factors discussed above and considers the safety significance

of these specific events to be minimal. However, had conditions been

less favorable or other components been involved, the safety significance ,

could have been much greater. The NRC is particularly concerned with '

the events associated with the RN-21 problem from the stand 30 int of

maintenance work control and retesting. The inspectors have initiated a

thorough study of the work control process to determine if sufficient

controls are in place to prevent missed retests and unknown inoperabili- i

ties of safety system components.

11. Ground Water Detection  ;

On April 12, 1988, NRR technical staff reviewed the Groundwater Monitoring

System and conducted a walkdown of selected monitoring wells ( Auxiliary

Building East and West wall exterior monitors, Auxiliary Building north

wall interior monitors PP-51, QQ-56 and PP-61), and Auxiliary Building

drain sump "C". System operators and surveillances were found to be

consistant with T.S. 3.4. 7.13 requirements. On April 13, 1988 design

calculations of hydrostatic and buoyancy influences and overturning

potential for the Auxiliary Building, Reactor Buildings, and Diesel

Generator Buildings were audited at licensee's corporate engineering

offices. This review is part of the NRC's review of Duke's request for l

Technical Specifications 3.4.7.13 changes dated January 27, 1988.

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