ML20211E798

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Insp Repts 50-369/97-16 & 50-370/97-16 on 970712-0827. Violations Being Considered for Escalated Eas.Major Areas Inspected:Review of Aspects of Problem Involving Inoperable Unit 2 Ice Condenser Lower Inlet Doors
ML20211E798
Person / Time
Site: McGuire, Mcguire  
Issue date: 09/16/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20211E787 List:
References
50-369-97-16, 50-370-97-16, NUDOCS 9709300271
Download: ML20211E798 (9)


See also: IR 05000369/1997016

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U.S. NUCLEAR REGULATORY COMMISSION

REGION 11

Docket Nos.

50 369 and 50-370

License Nos.

NPF 9 and NPF-17

Report No:

50-369/97-16 and 50 370/97-16

Licensee:

Duke Energy Company

Facility:

McGuire Nuclear Station. Units 1 and 2

Location:

12700 Hagers Ferry Rd.

Huntersville, NC 28078

Dates:

July 12 - August 27, 1997

Inspectors:

M. Sykes, Acting Senior Resident inspector

M, Franovich, Resident inspector

Approved:

C. Ogle, Chief, Project Branch 1

Division of Reactor Projects

9709300271 970916

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Enclosure

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EXECUTIVE SUMMARY

McGuire Nuclear Station

NRC Inspection Report 50-369/97 16 and 50-370/97-16

This special inspection reviewed aspects of a problem involving inoperable

Unit 2 ice condenser lower inlet doors.

Enoineerina

The immediate corrective actions regarding the inoperable Unit 2 lower

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ice condenser doors were adecuate.

However, long-term corrective

actions for both Unit I and lnit 2 were not established.

An apparent violation was identified concerning the failure to comaly

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with Technical Specification requirements for the operability of t1e ice

condenser inlet doors on Unit 2 for an unknown period of time during

operation in Modes 1. 2, 3, and 4.

An apparent violation was identified concerning the failure to perform

adequate corrective actions in accordance with 10 CFR Part 50 Appendix B

Criterion XVI, in light of relevant industry operating experience at

another ice condenser facility and operational events at the McGuire

facility.

A preliminary review of industry experience and site-specific

operational events indicated that prior opportunities may have existtJ

to implement corrective actions to prevent the occurrence of the event

at the McGuire facility.

Enclosure

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Report Details

Summary of Plant Status

Unit 1 began the period at 100 percent rated thermal power.

On July 12.

power was reduced to approximately 95 percent to realign the number 3 turbine

stop valve to its normal position.

Unit 1 operated at 100 percent for the

remainder of the reporting period.

Unit 2 began the 3eriod in Mode 5 (cold shutdown) for a forced outage to

repair a failed 2) reactor coolant pump motor. While shutdown, the licensee

determined that 10 of 48 ice condenser lower inlet docrs were inoperable

because of upward ice condenser floor movement.

The licensee rep 61 red the

failed reactor coolant pump motor and the lower ice condenser inlet doors and

returned Unit 2 to power operations on July 22.

On August 4. power was

reduced to approximately 95 aercent to complete moderator temperature

coefficient measurements.

T1e unit was returned to 100 percent power on

August 5. where it continued to operate for the remainder of the reporting

period.

Review of Updated Final Safety Analvsis ReDort (UFSAR) Commitments

While performing inspections discussed in this report. the inspectors reviewed

+5 applicable portions of the UFSAR that were related to the areas inspected.

. e inspectors verified that the UFSAR wording was consistent with the

observed plant practices, procedures. and/or parameters.

III. ENALNURING

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Conduct of Engineering

El.1

Inonerable Unit 2 Ice Condenser Lower Inlet Doors

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Inspection Stone (37551)

The inspectors reviewed the facts and circumstances related to a failure

to comply with Technical Specification requirements for the operability

of the Unit 2 ice condenser inlet doors.

On July 17. 1997, with the

unit in Mode 5 (cold shutdown) for a forced outage, the licensee

discovered that 10 of 48 lower inlet doors were inoperable for an

unknown period of time since the arevious Unit 2 refueling outage.

The

affected doors were mechanically )ound because the concrete floor raised

to the point where metal flashing interfered with the doors.

Prior to

restart of Unit 2. the inspectors reviewed the immediate corrective

actions initial root cause evaluations, and applicability of the

problem to Unit 1. The inspectors also reviewed station documents,

reviewed the UFSAR and design basis documents, and interviewed plant

personnel. On August 15. the licensee submitted licensee event report

(LER) 50 370/97-03 to address this event in accordance with the

requirements of 10 CFR 50.73.

Enclosure

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Observations and Findingi

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Ice Condenser System Desian

The ice condenser is a passive accident mitigation system that contains

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approximately 2.5 million pounds of borated ice.

Because the McGuire

containment has a low design pressure capability of approximately 15.0

psig, the ice condenser system condenses steam and sup3resses pressure

to ensure containment integrity during an accident.

T1e system, which

consists of ice contained within an array of approximately 1.940

baskets, has lower inlet. intermediate deck, and top deck doors that

allow passage of steam released from an accident.

Forty eight (48) lower inlet doors, which are contained in 24 bays (two

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doors per bay), are located in the lower compartment.

The inlet doors

will passively open when a differential pressure of approximately one

pound per square foot (PSF) exists between the lower containment and the

ice bed.

The design function of the lower inlet doors is to uniformly

open during a loss of coolant accident (LOCA) or steam line break in

containment 50 that the thermal energy released into the containment is

evenly absorbed by the borated ice.

These doors are adjacent to the ice

condenser floor structure.

In each bay, a thin layer of metal flashing

surrounds the bottom of the doors' frame and protects small bags of

insulation.

The ice condenser floor consists of a four inch wear slab layer of

concrete imbedded with glycol cooling coils.

The floor is cooled by one

of two floor cooling pumps that circulate glycol through the cooling

coils.

A protective layer of ice is normally on the floor.

Beneath the

wear slab is an insulation layer of foam-concrete. Combined, the floor

structure and the cooling system minimize heat entering the ice

condenser from the lower crane wall and equipment room; thereby

minimizing ice sublimation rates.

Secuence of Events

During a forced outage on July 12. several Unit 2 ice condenser inlet

doors actuated due to depressurization of upper containment when

personnel entered the containment through the upper airlock.

Through

visual ins)ection. Operations personnel discovered that one inlet door

was 12 incies open and another door was off its seat.

No ice melted

from the event: however. Operations declared the ice condenser

inoperable and a work order was developed to determine if a test of the

doors would be required prior to entry to Mode 4.

This condition was

reported to the NRC on July 12, 1997, in accordance with the reporting

requirements of 10 CFR 50.72.

On July 15. the licensee retracted the notification based on their

interpretation that a valid engineered safety feature actuation of the

lower inlet doors had not occurred since a substantial number of the

Enclosure

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- doors did not open.

On July 16. a retest of the doors was required when

maintenance personnel noticed abnormal conditions (i.e.. door bulging)

in the ice condenser.

On July 17, with Unit 2 still in Mode 5. the licensee determined that 10

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of 48 lower ice condenser inlet doors in eight of the 24 bays (two doors

per bay) were incapable of opening at a torque less than or equal to

that specified in Technical Specitications.

In Modes 1, 2. 3. and 4,

Technical Specification section 3/4.6.5.3.1 requires that the torque to

initially open each door be less than or equal to 675 inch pounds. The

inlet doors were tested per Station Procedure PT/0/A/4200/32. Periodic

Inspection of Ice Condenser Lower inlet Doors. and were found to require

more than the 15.5 lbs opening force limit (which correlates to the

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Technical Specification limit cue to the testing method).

Three of the

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5. 6, 8. quired at least 80 lbs of force to open. Inlet doors in bays 2.

doors re

and 19 through 22 were affected. On July 18. 1997, the licensee

reported this condition to the NRC in accordance with the requirements

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of 10 CFR 50.72.

The licensee's investigation revealed that the affected doors were

dragging on flashing between the floor and the bottom of the doors.

The

licensee attributed the door binding to upward movement of the floor

where the floor (wear slab) appeared to be raised by approximately 0.75

inches above its normal height. The licensee a ho discovered that ice

normally on the floor had disappeared and the floor cooling system was

degraded.

Immediate Corrective Act %n1

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Before restart of Unit 2 on July 21. 1997, immediate corrective actions

included a modification to remove a portion of the flashing that

interfered with the doors.

This left a minimum clearance of at least

2.25 inches in every bay between the floor and the remaining flashing.

occurred),perational data from Sequoyah (where a similar problem

Based on o

this modification should provide a sufficient gap under a

worst case floor movement for the remainder of the operating cycle.

The

licensee also performer' baseline measurements of the floor to monitor

future floor growth. A small amount of the bagged insulation that the

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flashing was protecting was also removed.

Removal of the insulation

increases ice sublimation rates: however, the licensee determined that

sufficient ice mass existed in the ice condenser for the remaining two

months in the fuel cycle.

The inspectors concluded that the 10 CFR 50.59 evaluation for the minor modification was adequate.

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Several of the Unit I lower ice condenser doors were examined by use of

a video camera that was lowered through the intermediate deck doors down

to the wear slab.- Video surveillance did not reveal deformation of-

flashing or concrete heave.

The inspector reviewed videos of both Unit

I and Unit 2 to verify the licensee's surveillance results.

Floor ice

and beam cooler frost were significantly present in the Unit 1 ice

condenser.

The licensee also reviewed historical ice basket data,

determining that Unit 1 did not have significant ice melt events

comparable to the Unit 2 events discussed below.

On August 19. the

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Enclosure

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system engineer informed the inspector that removal of the door frame

flashing on Unit I was placed on the Unit 1 forced outage list to be

performed at the next opportunity as testing warrants.

Anoarent Cause. Review of Industry Experience. and Operatinn Exoerience

Water intrusion, freezing, and expansion in the floor concrete coupled

with subsequent freeze and thaw cycles are the likely phenomena causing

the concrete to hea/e upward. The licensee identified several Unit 2

0)erational events and design attributes that may have contributed to

t7e problem. Two events in 1993 resulted in some of the ice melting.

The first event involved feedwater valve 2CF-130, where a maintenance

error caused high temperature and pressure feedwater to be released into

containment. The second event involved a loss of offsite )ower event

where reactor coolant was released into containment when t1e pressurizer

relief tank rupture disk ruptured.

In 1994, the licensee intentionally

performed an aggressive wall panel defrost in Unit 2 ice condenser bays

18 through 24 that may have also introduced water into the concrete

flooring. Additionally, the licensee postulated that the design of the

floor cooling system did not account for localized heat loads from the

steam generators.

On July 20, 1997, the licensee discovered that the performance of the

floor cooling system was degraded for some period of time following the

last Unit 2 refueling outage.

Video surveillance of Unit 2 revealed

that no ice was present on the concrete wear slab, and virtually no

frost was present on the beam cooler lines that remove residual heat.

Normally, a protective coat of at least 0.25 inches of ice is on the

floor and heavy frost is accumulated on the beam coolers.

The lack of

ice and frost on these components was a self-revealing condition

indicative of degraded floor cooling system performance.

Together,

these events may explain the concrete heave in the bays that were

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affected.

On July 29, the inspectors interviewed the ice condenser system

engineer.

The inspectors questioned the system engineer on past

corrective actions at McGuire to address a similar event that occurred

at the Sequoyah facility in 1992. Apparently. McGuire personnel in 1992

did not perceive that the floor problems at Sequoyah applied to McGuire

because:

(1) the concrete floor at Secuoyah was severely cracked and

the floor noved in multiple planes; anc (2) water intrusion at Sequoyah

was the result of intentional floor defrosting and floor cleaning

practices that were not performed at the McGuire facility.

The inspectors also asked if any baseline measurements of floor

dimensions or special efforts to monitor floor growth were established

in view of both the Sequoyah event and the ice melt events that had

occurred at McGuire since then.

No floor measurements had been taken,

nor was additional monitoring-established beyond the regular Technical

Specification required door surveillances that are performed once every

eighteen months.

In 1992, the licensee did examine the condition of the

wear slab and concluded that the cracking expe enced at Sequoyah was

not evident at McGuire.

The licensee also stated that, unlike what was

Enclosure

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experienced at Sequoyah. the current condition of the Unit 2 floor

indicates movement in a single slane. The inspectors noted that the

licensee did not determine if t7e Sequoyah floor cracking had exhibited

movement in a single plane before the severe cracking of the concrete

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occurred.

During the July 29 interview the system engineer informed the

inspectors that the setpoint for the temperature controlled glycol / floor

cooling flow valve had drifted from 12*F to 19'F.

The licensee believes

that this degradation aggravated the condition of the floor: however.

the licensee maintained that the ice on the floor did not melt.

The inspectors interviewed the instrumentation and controls (I&C)

engineer and ice condenser system engineer on the procedare usS1 to

calibrate the glycol bleed controller for floor cooling. The inspector

expressed concern that inadequate performance of the floor cooling

system may create a source of water (from ice normally on the floor)

that could be absorbed Dy the concrete. The 1&C engineer informed the

inspector that the system had never been calibrated and is run to-

failure.

The licensee also postulated that the floor ice had sublimated

away and did not melt as evidenced by boron residue on the floor.

However, the inspectors' examination of the video also revealed boron

residue streams near the floor drains. which may indicate that an ice

melt had occurred.

The inspectors also questioned if a mispositioned valve may have

inadvertently isolated glycol to the floor cooling coils during

maintenance and train swaps. Some plant drawings indicate that the idle

pump had its associated discharge valve normally closed.

Operations

responded that the train swap practice for the floor cooling system did

not require valve closure and the valves were not referenced in the

procedure for train swaps.

On August 19 the inspector identified information in the UFSAR

regarding the consequences of water on the floor of the ice condenser.

UFSAR section 6.2.2.1.3 states that ..the effects of water on the floor

and insulation [are) negligible."

The licensee initiated PIP-0M 97-

3070 to incorporate into the UFSAR industry and site-specific experience

regarding water intrusion and temperature swing effects,

Preliminary Review of Safety Sianificance

To evaluate the short-term containment res)onse, the licensee performed

special scoping loss of coolant accident ( 0CA) analyses using the

GOTHIC computer code to demonstrate that the ice condenser would have

)erformed its safety function during design basis accidents.

Up to 16

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) locked doors were assumed for a range of pipe break sizes.

The results

demonstratedthatgeakcontainmentsteampressureswouldnotexceedthe

design pressure.

ihe inspector performed a preliminary review of LER

50-370/97-03 and noted to the licensee that an evaluation of post-

accident hydrogen (e.g.. degraded core, radiolysis of core and sump

water, corrosion of aluminum and zinc. etc.) nad not been performed.

/ccording to UFSAR section 6.2.7. 12 igniters are located in the ice

Encicsure

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condaser. The inspectors were concerned that blockage of tra lower

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inlet doors may impact the distribution of hydrogen in containment and

reduce the hydrogan mitigation systeT s effectiveness in preventing a

detc.nable concentration during an accident.

The licensee acknowledged

the inspector's concern.

C.

(onclusions

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The inspectors concluded that the licensee's immediate corrective

actions regarding the inoperable Unit 2 lower ice condenser doors were

adequate. At the end of the inspection period. long-term corrective

actions for both Unit I and Unit 2 were not established.

As a result of the degraded condition, two apparent violations were

identi fied.

The first apparent violation is related to a failure to

comply with iechnical Specification requirements for the operability of

^he ice condenser inlet doors on Unit 2 for an unknown period of time

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W rino o pratica in Modes 1. 2, 3. and 4.

This is identified as

cr;arent da),nion (EEI) 50 370/97-16-01. Failure to Comply With

Technical ipecificatieri Requirements for Ice Condenser Lower Inlet

Doors.

The second apparent violation is related to a failure to perform

adequate corrective actions in accordance with 10 CFR Part 50 Appendix B

Criterion XVI, in light of relevant industry operating experience at

another ice condenser facility and operational events at the McGuire

facility. A preliminary review of industry experience and site-specific

operational events indicates that prior opportunit.es may have existed

to implement :orrective actions to prevent the occurrence of the event

at the McGuwe facility. This is identified as EEI 50-370/97-16 02.

Failure to Implement Effective Corrective Actions to Prevent Ice

Condenser Lower Inlet Door Binding.

Enclosure

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Y. Management Heetinos

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Exit Heeting Summary

The inspectors 3 resented the inspection results to members of licensee

management at tie conclusion of the inspection on August 7.1997. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary.

No proprietary

iaformation was identified.

On August 27. a phone exit was held between

the acting branch chief and the site vice president to inform the

licensee of the two apparent violations.

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Enclosure

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

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Barron B.

Vice President. McGuire Nuclear Station

Cross, R.. Regulatory Compliance

Dolan. B.. Manager. Safety Assurance

Geddie. E., Manager. McGuire Nuclear Station

Herran. P.. Manager. Engineering

Cash. M., Manager. Regulatory Compliance

Thomas, K.. Superintendent. Work Control

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Travis. B. . Manager. Mechanical-Systems Engineering

Tuckman

M., Senior Vice President. Nuclear Duke Power Company

Spada. R.. System Engineer. McGuire Nuclear Station

Knost. J., System Engineer. McGuire Nuclear Station

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S. Shaeffer. Acting Chief. Branch 1. Division of Reactor Projects

M. Sykes. Acting Senior Resident Inspector. McGuire

M. Franovich. Resident Inspector. McGuire

INSPECTION PROCEDURES USED

IP 375S1:

Onsite Engineering

ITEMS OPENED CLOSED, AND DISCUSSED

OPENED

50 370/97-16-01

EEI

Failure to Comply With Technical

Specification Requirements for Ice

Condenser Lower Inlet Doors.

50-370/97-16 02

eel

Failure to Implement Effective Corrective

Actions to Prevent Ice Condenser Lower

Inlet Door Binding.

Enclosure

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