ML20149E452

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Insp Repts 50-327/87-65 & 50-328/87-65 on 871006-1105. Violations Noted.Major Areas Inspected:Operational Safety Verification,Including Operations Performance,Sys Lineups, Radiation Protection,Safeguards & Housekeeping Insps
ML20149E452
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 12/22/1987
From: Jenison K, Mccoy F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II), NRC OFFICE OF SPECIAL PROJECTS
To:
Shared Package
ML20149E379 List:
References
50-327-87-65, 50-328-87-65, IEB-83-01, IEB-83-1, NUDOCS 8802110055
Download: ML20149E452 (34)


See also: IR 05000327/1987065

Text

UNITED STATES

[v.0tg% NUCLEAR REGULATORY COMMISSION

y" REGION 11

g j 101 MARIETTA STREET,N.W.

O r ATLANTA, GEORGt A 30323

'+9 . . . . . ,o

Report Nos.: 50-327/87-65, 50-328/87-65

Licensee: Tennessee Valley Authority

500A Chestnut Street

Chattanooga, TN 37401

Docket Nos.: 50-327 and 50-328 License hos.: DPR-77 and DPR-79

Facility Name: Sequoyah Units 1 and 2

Inspection Conducted: October 6, 1987 thru Novembir 5, 1987

Lead Inspector: N]/8. M /of/2//87

K.M.Jenison,SeniorReg#intyspect)r Date Si'gned

Accompanying Inspectors: P. E. Harmon, Resident Inspector

D. P. Loveless, Resident Inspector

W. K. Poertner, Resident Inspector

W. C. Bearden, Resident Inspector

M. W. Branc , Sequ h Restart Coordinator

Approved by:

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F. R. McCoy, Chief, Projects Section 1

/ /M.:2[F 7

Date SVgned'

DivisionofTVAProjects

SUMMARY

Scope: This routine, announced inspection involved inspection onsite by the

Resident Inspectors in the areas of operational safety verification including

operations performance, system lineups, radiation protection, safeguards and

housekeeping inspections; maintenance observations; review of previous

inspection findings; followua of events; review of licensee identified items;

review of IE Information Notices; and review of inspector followup items.

Results: Three violations were identified.

(327,328/87-65-01), Inadequate Corrective Actions paragraph 12

(327,328/87-65-02), Inadequate Response Time Test - paragraph 6

(327,328/87-65-03), Failure to Adequately Control Changes to

Control Room Orawings paragraph 3

One unresolved item was identified.

(327,328/87-65-04), Surveillance Discrepancies - paragraph 13

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REPORT DETAILS

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1. Licensee Employees Contacted

H. L. Abercrombie, Site Director

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J. T. La Point, Deputy Site Director

  • L. M. Nobles, Plant Manager
  • B. M. Willis, Operations and Engineering Superintendent
  • B. M. Patterson, Maintenance Superintendent

R. J. Prince, Radiological Control Superintendent

  • M. R. Harding, Licensing Group Manager

L. E. Martin, Site Quality Manager

D. W. Wilson, Project Engineer

R. W. Olson, Modifications Branch Manager

J. M. Anthony, Operations Group Supervisor

  • R. V. Pierce, Mechanical Maintenance Supervisor

M. A. Scarzinski, Electrical Maintenance Supervisor

  • H. D. Elkins, Instrument Maintenance Group Manager

R. S. Kaplan, Site Security Manager

J. T. Crittenden, Public Safety Service Chief

  • R. W. Fortenberry, Technical Support Supervisor
  • G. B. Kirk, Compliance Supervisor

D. C. Craven, Quality Assurance Staff Supervisor

J. H. Sullivan, Regulatory Engineering Supervisor

J. L. Hamilton, Quality Engineering Manager

D. L. Cowart, Quality Engineering Supervisor

H. R. Rogers, Plant Operations Review Staff

R. H. Buchholz, Sequoyah Site Representative

M. A. Cooper, Compliance Licensing Engineer

Other licensee employees contacted included technicians, operators, shif t

engineers, security force members, engineers and maintenance personnel.

  • Attended exit interview

2. Exit Interview

The inspection scope and findings were summarized with the plant manager

and members of his staf f on November 5,1986. Three violations described

in this report's summary paragraph were discussed. No deviations were

discussed. The licensee acknowledged the inspection findings. The

licensee did not identify is proprietary any of the material reviewed by

the inspectors during this inspection. During the reporting period,

frequent discussions were held with the Site Director, Plant Manager and

other managers concerning inspection findings.

During the exit interview plant management committed to revising A01-27,

Control Room Inaccessibility, per paragraph 3 below, in order to meet the

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guidance of regulatory guides 1.68.2 and 1.68.

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3. Licensee Action on Previous Inspection Findings (92702)

(Closed) Unresolved Item (URI) 327, 328/87-24-02, Control of Temporary

Changes to Drawings. This URI has been determined to constitute a

violation. Drawings in the control room are marked by the modifications

engineers immediately following the completion of physical changes to the

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plant's as-built condition. These temporary drawing changes ~ consist of

red marks for additions to the drawings, and green marks to designate

removals. During the inspection described in IR 327, 328/87-24, several

instances were identified where errors were introduced to the control room

drawings by the modifications engineers when they marked up the drawings.

10 CFR 50, Appendix B, Criterion VI requires that changes to documents

(including drawings) be reviewed for adequacy and approved for release by

authorized persons. This requirement was not met in that changes to

primary control room drawings were routinely made with no verification or

review by second parties. _This is a violation VIO 327,328/87-65-03.

(Closed) URI 327, 328/87-08-02, Abnormal Operating Instruction (A01)

Personnel Required for Remote Shutdown. The inspector reviewed A01-27,

Control Room Inaccessibility. The procedure describes actions to be taken

should the control room become uninhabitable. The procedure requires the

dispatching of more personnel than are required as a minimum on-shift in

TS 6.2.2.a. Appendix A of 10 CFR 50 requires in GDC 19 that equipment at

appropriate locations outside the control room be provided with a design

capability for prompt hot shutdown of the reactor, including necessary

instrumentation and controls to maintain the unit in a safe condition

during hot shutdown. This criteria is addressed in regulatory guide (RG)

1.68.2, Initial Startup, Nuclear Power Plants. This RG states that

startup testing should demonstrate that the number of personnel available

to conduct the shutdown operation is sufficient to perform the many

actions required by the procedure in a timely, coordinated manner.

Startup test documentation, as described in item SU-1.2A of Table 14.1-3

in the final safety analysis report (FSAR), was reviewed. In addition,

the following issues, identified in inspection report 327, 328/87-08, were

also reviewed:

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Whether there is sufficient personnel and guidance to perform a safe

and orderly shutdown from outside the control room with a minimum

shift crew per the TS.

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Whether procedures are adequate to address the limiting case of

minimum shift manning.

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Whether the initial startup test was performed utilizing the

personnel indicated in the procedure or the TS minimum, and whether

the procedure was adequate.

The inspector walked down the procedure utilizing licensed personnel and

determined that the plant could be shutdown using minimum shift crew.

However, performance with a minimum crew would require some step sequence

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modifications ; to A01-27. A draf t update to A01-27 was prepared and

reviewed making it possible to run with minimum shift crew. During the

exit interview, plant management committed to revising A01-27 in order to

meet the guidance of regulatory guides 1.68.1 and 1.68.

The inspector cid determine that the initial startup test utilized normal

shift manning as opposed to the minimum shift crew in TS. This action to

use the normal shif t manning was according to the TVA commitment set in

the FSAR. This item is closed.

(0 pen) Violation (VIO) 327, 328/86-37-06, Containment Sump Leve' Test

Deficiencies. The inspector reviewed this issue which involved a

prolonged history of test deficiencies with respect to the calibration of

the containment sump level transmitters. These particular transmitters

were identified as being out of TS tolerance six times during the

surveillances conducted between 1984 and 1986. The NRC identified that

the licensee did not initiate a quality assurance document identified as a

corrective action report (CAR). Failure to initiate a CAR was identified

as a violation and the cover letter for inspection report 327, 328/86-37-

stated that, "violation 327, 328/86-37-06 was also identified and is

described in paragraph 13 of the enclosed inspection report. This

additional violation is under consideration for escalated enforcement

action. Accordingly, a notice of violation addressing this particular

violation is not being issued at this time, and therefore no response to

this violation is required." The cover letter for the inspection report

further stated that "the number and characterization of violations

described in paragraph 13 of the enclosed inspection report may change as

a result of further NRC review".

The licensee's corrective actions with respect to the containment sump

level transmitters included issuance of a condition adverse to quality

report (CAQR) CAQR-SQP870043 and the establishment of a plant tracking and

trending program under standard practice SQM-58, maintenance history and

trending. The general adequacy of the QA .CAQR and the maintenance

tracking and trending processes are subjects of separate NRC inspections.

The specific issues dealing with the identification of the containment

sump level transmitters as a condition adverse to quality and tracking and

trending of those specific material deficiencies appear to have been

adequately addressed by the licensee. This item will remain open, pending

escalated enforcement action.

(Closed) VIO 327, 328/86-39-01, Failure to Report Computer Program Errors.

This violation involved the use of incorrect axial flux curve and rod bow

penalty data in monthly surveillances of incore reactor parameters. In

response to the violation, the licensee wro;e a licensee event report

(LER) 322 '86-004 which was closed in NRC inspection report 327, 328/87-08.

The LER appears to address adequate correctivt action to violation 327,

328/86-39-01. The inspector examined the root cause of this issue in

detail and evaluated the corrective action witt respect to the security

and accuracy of data being placed into saist3 related plant computer

systems in general and the INCORE program in particular. In LER 328/86-004 the licensee committed that before installing vendor-supplied

data into sof tware in the future, verification will be provided that the

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- correct data is being used. This is accomplished through an independent-

verification process, This_ item'is closed.

(Closed)URI 327,.328/87-30-03, Reactor Coolant-System Sight Glass Design.

The design .of the sight _ glass .used to indicate . reactor ' coolant system

(RCS) inventory level during partial- loop drain down ' conditions was-

questioned by the NRC inspection staff as well as the licensee'.s nuclear

manager's review group (NMRG) following the RCS spill event of January 28,

1987. Several design deficiencies were . identified and later determined

by the NRC . not to be safety related. In particular, the monitoring

arrangement using a TV camera and monitor was not well designed to allow

the control room operator to readily determine the level in the sight

glass. Resolution of the above deficiency and .several other minor defi-

.ciencies is scheduled during the next refueling outage for each unit. The

corrective actions are presently being tracked under the licensee's

tracking and reporting of open items system '(TROI). The actual site

glass modifications will be reviewed when the appropriate reviews and

corrections have been accomplished during the unit 2 cycle 3 outage. This

item is closed.

(Closed) URI 327, 328/87-30-04, Change to TS Basis. Sequoyah issued

Technical Specification (TS) basis change 87-14 directly to 'the NRC.

without a nuclear safety review board (NSRB) review. The licensee's

position is that the TS basis is not an actual part of the TS as defined

by 10 CFR 50.36(a). Therefore, TVA's position is that changing the basis

does not require an NSRB review. NRC approval of the change to the TS

Basis was issued on August 18, 1987. .The inspector . discussed the

licensee's position with OSP Technical Programs management, and determined

that this generic issue is currently under NRC review. TVA indicated

that they would have the NSRB perform such reviews until such time this

generic issue is resolved. This item is closed.

-(0 pen) VIO 327, 328/86-73-04, Failure to Properly Evaluate the Generic

Applicability at Other Nuclear TVA Facilities of Conditions Adverse to

Quality (CAQ). The violation pertained to the adequacy of engineering

evaluations. Deficiencies identified included Bellefonte CAQR BLN4929,

dated June 30, 1986. Sequoyah did not properly analyze the cause of the

CAQR and did not have documentation for justification of the determination

that the CAQR did not apply to Sequoyah. TVA gave as reasons for the

violation "the failure on TVA's part to provide adequate and sufficient

problem descriptions and detailed information in the assessment of the

potential generic condition as recorded in the P&CE memorandum so that

other TVA facilities could properly assess the generic implications of the

cited conditions." Their corrective action includes a revision 3 to YVA's

t nuclear quality assurance menual (NQAM) part I, Section 2.16, which

requires generic reviews to be completed af ter root caJse analysis and

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recurrence control actions have been determined. This was implemented

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July 1, 1987. TVA further revised procedures for more controlled and  ;

centralized requirements for the conduct and timing of generic reviews.

The inspector reviewed CAQRs at Sequoyah that have been determined by TVA

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to be generic. This was a random review of CAQRs initiated by Sequoyah

and by other plants. The foll_owing deficiencies were noted.

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CAQR number WBP870420 was initiated on June 6, 1987, at Watts Bar and

concerned the storage of electrical cabies in the warehouse and craft

storage area at Watts Bar. The CAQR listed 8 items to address and

gave as the root cause of the CAQ, "inadequate procedures for cable

transactions and storage which lead to personnel being trained

incorrect." On August 1,1987, the generic review sheet was signed

with a determination that this CAQ did not exist at Sequoyah. The

justification was based on inspection of cable storage areas and

addressed the 8 items, but failed to address the root cause, i.e. ,

inadequate procedures and training.

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CAQRs WBP870420 and BFQ870375 attachment 7 CAQ generic review sheets

were not properly reviewed. NQAM Part 1, Section 2.16, step 10.3

states," the justification for determining that a CAQ is not generic

shall be documented. The individual who prepares the justification

shall provide a dated signature, and the individual's supervisor

shall approve the justification by dated signature." On August 1,

1987, the same individual signed WBP 870420 as reviewer and as

supervisor of reviewer. On June 26, 1987, the same individual signed

BFQ 870396 as reviewer and as supervisor of reviewer. This is a

failure to follow procedures.

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On July 9,1986, Bellefonte (BFN) identified a CAQ and initiated SCR

BLN4929. The root cause of this CAQ was an operator attempting to

close the diesel generator (D/G) output breaker out of phase.

Sequoyah misidentified the root cause. The recommendations made at

Bellefonte to prevent recurrence are: (1) additional simulator

training for operators, (2) review of the incident with operators,

and (3) addition of a permissive synchronize and voltage check scheme

on the diesel generator output breaker.

Sequoyah CAQR SQP870943, signed on July 2, 1987, states in the

description of proposed disposition, that "items 1 and 2-POTC

provides D/G simulator training during RO certification. Operators

are already aware that the D/G should be in phase before

synchronization. No additional training is proposed. Item 3, we do

not recommend adding an interlock to the D/G breaker. This accident

appears to have been due to human error and was an isolated

incident." The recommended actions at Sequoyah appear to be

inconsistent with those at Bellefonte. Further, NQAM Section 1,

Part 2.16 step 10.5.2 states "for CAQs determined to be generic,

affected organizations should communicate with each other in the

development of corrective action plans to ensure that, when

appropriate, such plans are consistent."

Further inspections of the generic review issue will be conducted prior to

the startup of either unit. This violation remains open.

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(Closed) 327, 328/87-06 observation MEB-8, Inconsistent Equipment

Qualification Temperature. Calculation NEB 811007235 had been prepared to

analyze a deficiency in the pre-operational test results for the turbine

driven auxiliary feedwater pump (TDAFW) room ventilation system and to

provide suggestions to reduce the temperature rise in the room. The

calculation uses a temperature rise to 125 degrees F, which the

calculation states is the equipment qualification temperature. This is_

not consistent with plant data sheet, 47E235. TVA recalculated the room

heat loads in 844870609010, dated April 10, 1987, and the required air

flow rates in B44870716007, dated July 16, 1987. The conclusion is that

the installed exhaust' fans are adequate to meet the requirements of normal

operation and LOCA, with and without loss of offsite power, with a maximum

of 110 degrees F in the room. The corrective action in PIRSQNMEB8773 is

to change FSAR section 9.4.2.2.7 to delete the room temperature rise

criterion and to replace it with a maximum room temperature of 110 degrees

F. This corrective action appears to be an adequate response to NRC's

concern. This item is closed.

(Closed) 327, 328/87-06 observation GEN-1, Substantiated Condition for a -

CAQ. Nuciaar engineering procedure (NEP)-9.1, Corrective Actions, revised

July 1, 1986, defines the controlled system within ONE to document,

evaluate and resolve conditions adverse to quality (CAQs). NEP-9.1 was

being revised to agree with the corporate QA procedure, NQAM, Part I,

Section 2.6, which includes in the definition of CAQs the statement that

"unsubstantiated conditions are not defined as CAQs," The concern was

that this statement had the net effect of eliminating a set of CAQs that

had previously been identified and resolved. NEP-9.1, Revision 2,

Section 2.2, dated June 30, 1987, eliminates the questionable statement

from the definition. Section 1.lb of NEP-9.1, Revision 2, provides for a

problem identification report (PIR) system to document problems, and

potential problems that are not CAQs as defined. The licensee's action

resolves the concern. This item is closed.

(Closed) 327, 328/87-14 observation 6.19, 480 Volt Board Room Air Handling

Unit Control Logic. Cut-out switches had been installed in each of the

heating, ventilation and air conditioning (HVAC) systems for the 480V

board room and the 6.9KV shutdown board room to shut off the room's

cooling system on a high temperature signal in the room. The NRC concern

was that the close location of the temperature sensors was such that a

common mode failure could disable all cooling. CAQR871011 for the 480V

board room and CAQR871279 for the 6.9KV shutdown board room were issued to

disconnect the room high temperature cut-out switches since the switches

had been installed for economic reasons to protect equipment in the event

of refrigerant loss, and had no safety function. ECN7263 followed up on

this item and the switches have been disconnected. This item is closed.

(Closed) VIO 327, 328/87-02-02, Failure to Establish, Maintain and

Implement Safety-Related Procedures. This violation resulted from three

engineered safety feature (ESF) initiations reported in licensee event

reports (LERs) 328/86-08, 328/86-09 and 328/86-10, and from observations

of the performance of general operating instruction (G01)-6H, Freeze

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Protection. The violation consisted of an inadequate work plan (WP),-

instrument maintenance instruction, G0I documents, and personnel errors

during procedure performance. The inspector reviewed TVA's corrective

actions detailed in the June 12,-1987 written response to this violation

and in the LERs. The specific procedural errors and weakt. esses have been

corrected. Site procedures such as surveillance instructions have been

through an extensive review process and are now developed and revised

using checklists and a writer's guide. Maintenance procedures are

currently undergoing a similar process. Personnel involved in the

specific incidents have been reinstructed and more extensive training has

been conducted regarding adherence to procedures. The licensee's

corrective actions appear to be adequate. This item is closed.

(Closed) VIO 327, 328/86-68-05, paragraph c, Section 2.4.5, deficiency

D-2,4-6, Loose and Broken Flexible Conduits. NRC inspectors reviewed the

July 16, 1987 TVA response to this portion of the violation and the

corrective action taken. All discrepancies except the loose conduit on

valve 2-FSV-30-14 were addressed in NRC report 87-57. Electrical

maintenance request 8234106 completed corrective action on valve

2-FSV-30-14. NRC inspectors performed field inspection of the valve and

found corrective action to be adequate. This violation is closed.

(0 pen) URI 327, 328/86-68, section 2.4.10 U-2,4-2, Flamastic Thickness on

Cable Trays. NRC report 327, 328/86-68 noted saveral areas in

safety-related cable trays that had flamastic thicknesses in excess of the

1/4-inch that was assumed for ampacity derating due to thermal loading. '

During discussions between NRC inspectors and site management. TVA

committed to an examination of the as-installed flamastic thicknesses at

Sequoyah. The TVA draft commitment was reviewed by the NRC and

discussions were held with TVA's department of nuclear engineering

personnel. TVA sampled flamastic thicknesses at 68 node locations of the

720 total node locations associated with class 1E control power and power

cable trays. The node locations were selected by random number

generation. Actual flamastic thickness examination identified 16 cables

that had thicknesses in exce;* of 1/4-inch, but that no thickness exceeded

1/2-inch. Calculation SQN-t2-025 was performed on all class 1E control

power and power cables based on a thickness of 1/2-inch. The results

indicated that only three cables (2PL3091A, 2PL40918, and 2PL4958A) would

be inadequately sized if the flamastic exceeded the 1/4-inch maximum

assumed thickness. A supplemental field walkdown measured flamastic  ;

thickness at 22 locations on these three cables. The supplemental

walkdown identified that only one cable (2PL4901B) of the three has a

flamastic coating exceeding 1/4-inch. That cable was determined to be r

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adequate because it was a normally deenergized alternate feeder; it was

routed in a mild environment; the flamastic coating exceeded 1/4-inch for

only part of the length of the c4ble; and the ampacity reduction was only

0.67% below full load current. NRC performed inspections on cable trays

that had been previously identified as having thickness greater than

1/4-inch and noted that the trays were control and signal cable trays. A

satisfactory re-inspection of class ?E control power and power cable trays

was conducteci by TVA. The licensea's corrective actions appear to be

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adequate. However, this item remains open pending review of the final TVA

resolution memo B25 87-1029-008 and tracking numbers NCO 87-0029-002 and

NCO 0484-005.

(Closed) URI 327, 328/85-45-18, Provide Complete Description of Corrective

Actions Taken To Preclude Circumstances Which Resulted In The Installation

of Upper Head Injection (UHI) Level Switches With Incorrect QA Level

Designations. The licensee identified in PRO-2-85-008 that 3 UHI level

switches did not have proper documentation of seismic qualification and QA

level designation. The subject switches were replaced and a review

commenced on both IE components that had been replaced and components in

stock in the warehouse. NRC report 327, 328/86-48 reported status of the

review and the ongoing resolution of 138 components that had inadequate

seismic qualification documentation. NRC report 327, 328/87-37 provided

further status and reported that not all devices that required replacement

had been replaced. TVA has completed the review and replacement of

required items that are documented in TVA memorandum, D. W. Wilson,

DNE/H. L. Abercrombie/0NP dated March 19, 1987. NRC inspectors reviewed

seismic and QA level designation documentation for the devices and found

them to be acceptable. This item was reviewed against the NRC enforcement

criteria, and was determined to be licensee identified. Therefore, this

item is closed.

(Closed) URI 327, 328/87-24-01, Drawing Control. TVA administrative

instruction (AI)-25, part I, Drawing Control After Unit Licensing,

revision 20, details the methods utilized by Sequoyah for control of

drawings. This procedure has been revised in response to NRC concerns

regarding drawing control. AI-25 provides definition; of the various

drawings; responsibilities for control of drawings; procedures for

receipt, inspection, filming, distribution, and filing; guidelines for

determination of primary drawings and utilization of drawing criteria.

AI-25 specifically addresses guidelines for selection of those drawings

considered primary drawings (ie. , required in the control room for safe

startup, operation and shutdown of the Unit. Appendix 1 to AI-25 lists

those drawings considered to be primary. Included in Appendix 1 are

drawings designated as critical drawings (required for technical support

center and Chattanooga emergency operations center). Primary drawing

changes will be controlled by the operations group manager and the plant

manager as provided in AI-25. This procedure was approved by the plant

operations review committee (PORC) on September 25, 1987. The primcry

drawings in the control room are required to be inventoried against

Appendix 1 of AI-25 annually. Currently, the site document control

section is ensuring prima./y drawings are maintained up to date. This URI

is closed.

(Closed) VIO 328/85-28-05, Accumulator Boron Concentration out of TS

Limit. The following actions were accomplished by the licensee: caution

statements were added to the "drain" and "fill" portions of 501-63.1,

concerning the potential for uncertainties of boron samples taken during

these processes; and a training letter was issued to licensed personnel,

discussing the occurrence and the 501 revision. The licensee's actions

appear to be adequate. This item is closed.

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(0 pen) URI. 327, 328/87-18-01, Potential for Secondary Bridging, Potential

Use of Flammastic As An Alternative To Solid Barriers, and The Lack of

Criteria for Separation of Safety-Related conduits. This unresolved item

contains three ~ specific examples related to the three generic concerns

stated above. The examples include a divisional cable that was misrouted

in a non-divisional tray, two non-divisional cables that were misrouted in

a divisional tray, and a division A conduit that was routed nearly in

contact with an uncovered division B tray. The concern for potential

secondary bridging (a non-divisional cable routed with one division and

then routed with the opposite division elsewhere in the plant) results

from the indeterminate path of the misrouted cables. A second potential

for secondary bridging existed in free air routing which is not documented

in cable routing records. Long vertical runs of flammastic cable bundles

in the cable spreading room contain both divisional and non-divisional

cables. Because routing is not documented in free air, the potential for

secondary bridging exists. TVA has instituted a change to the cable

routing computer program which adds free air nodes to the cable tray

system. A change in the computer program will prohibit routing a

non-divisional cable which has been run with a divisional cable, from

being routed with the opposite division. This action is adequate to

satisfy the concern regarding secondary bridging in free air. The concern

for secondary bridging due to misrouting of cables in cable trays is not

resolved and requires further review. Documentation reviewed indicated

that the non-divisional cables running in the divisional tray had been

corrected by condition adverse to quality report (CAQR) SQP870702 which

changed the routing cards for the misrouted cables. As a result of the

CAQR, a category D FCR (5572) was written and completed to change the

routing cards. This example is closed. The potential use of flammastic as

a fire barrier which is prohibited by subparagraph 8.3.1.4.2, but was

allowed by section 4.2.9 of Sequoyah design criteria SQN-DC-V-12.2, has

been corrected. A design input memo (temporary change to the design

specification) entitled, Design Input Memo On Separation Of Electrical <

Equipment And Wiring Design Criteria, SQN-OL-V-12.2, dated June 25, 1987, '

added information to the design snecification that precludes use of

flamastic as a fire barrier. This generic issue is closed. The

conduit / cable tray separation criteria issue is not resolved and will be  ;

the subject of further review. Items that remain open include the

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divisional cable that is routed in a non-divisional tray, the potential

for secondary bridging due to misrouting of cables in cable trays, and

both the example and the generic concern regarding the lack of criteria

for conduit / cable tray separation. The correction of the divisional cable

that is in the non-divisional tray, and the potential for secondary

bridging due to misrouting of cables in cable trays will be followed up

under violations 87-52-01 and 02. The conduit / cable tray separation issue  :

is a startup item and will be followed under URI 87-18-01. Accordingly,

this item remains open.

(Closed) Violation 327, 328/86-68-05, paragraph d, section 2.4.14,

deficiency 0-2.4-16, Pipe Support Discrepancies. TVA's July 16, 1987,

response to this violation and completed corrective actions were reviewed. .

Field change requests (FCRs) were issued to document the as-built clamp

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gap and change weld sizes and configuration. Space plates were added to

correct the potential rotation problem with the one snubber and bracket to

. clamp assembly and weld data sheets documented that six undersized welds

were built up to drawing requirements. Programmatic changes related to

procedure adherence by-craft technicians and- quality control-(QC)

inspectors, detailed in the Sequoyah nuclear performance plan and

elsewhere, have addressed the root causes of this violation. TVA's

corrective actions are adequate and this portion of the violation is

closed.

4. Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations. One unresolved item was identified during this inspection,

and is identified in paragraph 13.

5. Operational Safety Verification (71707)

a. Plant Tours

The inspectors observed control room operations, reviewed applicable

logs, conducted discussions with control room operators, observed

shift turnovers, and cor. firmed operability of instrumentation. The

inspectors verified the operability of selected emergency systems,

and verified compliance with Technical Specification (TS) Limiting

Conditions for Operation (LCO). The inspectors verified that

maintenance work orders had been submitted as required and that

followup activities and prioritization of work was accomplished by

the licensee.

Tours of the diesel generator, auxiliary, control, and turbine

buildings, and containment were conducted to observe plant equipment

conditions, including potential fire hazards, fluid leaks, and

excessive vibrations and plant housekeeping / cleanliness conditions.

The inspectors walked down accessible portions of the safety

injection system on Unit 2 to verify operability and proper valve

alignment.

No violations or deviations were identified,

b. Safeguards Inspection

In the course of the monthly activities, the inspectors included a

review of the licensee's physical security program. The performance

of various shif ts of the security 6rce was observed in the conduct

of daily activities including protected and vital area access

controls; searching of personnel and packages; badge issuance and

retrieval; patrols and compensatory posts; and escorting of visitors.

11

In addition, the inspectors observed protected area lighting,

protected and vital areas barrier integrity. The inspectors verified

an interface between the security organization and operations or

maintenance. Specifically, the resident inspectors: responded to

bomb W eats, fires, etc. ; interviewed individuals with . security

concerns; inspected security during outages; reviewed licensee

security event report; visited central or secondary alarm stations.

No violations or deviations were identified.

c. Radiation Protection

The inspectors observed health physics (HP) practices and verified

implementation of radiation protection control. .On a regular basis,

radiation work permits (RWPs) were reviewed and specific work

activities were monitored to ensure the activities were being

conducted in accordance with applicable RWPs. Selected radiation

protection instruments were verified operable and calibration

frequencies were reviewed.

During a tour of the auxiliary building the inspector identified two

separate deviations from the licensee's health physics procedures.

These involved dress out noncompliances which were minor in nature

and did not result in any personnel contamination or overexposure.

The licensee currently has a long term health physics corrective

action effort in progress which includes improvements in dress-out

and frisking issues. The two issues were discussed with operations

3

section management, NRC m,'nagemnt, and Sequoyah site management,

during the exit conducted for this inspection period. Sequoyah

health physics management initiated two radiological incident reports

(RIR) et the time the two noncompliances were identified by the

inspector. The inspector will review the resolution of RIR 87-24

dated October .6,1987, and RIR 87-23 dated October 16, 1987, after

completion of licensee corrective action. The inspector had no

further questions.

No violations or deviations were identified.

, 6. Monthly Surveillance Observations (61726)

The inspectors observed / reviewed the TS required surveillance testing

'

Tisted below and verified that testing was performed in accordance with

adequate procedures; that test instrumentation was calibrated; that L%

were met; that test results met acceptance criteria requirements and were

reviewed by personnel other than the individual directing the test; that

deficiencies were identified, as appropriate, and that any deficiencies

identified during the testing were properly reviewed and resolved by

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management personnel; and that system restoration was adequate. For

complete tests, the inspector verified that testing frequencies were met

and tests were performed by qualified individuals.

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a. SI-166.36, Diesel Starting Air Valve Test

SI-7, Electrical Power System: Diesel Generators

The above two surveillances were performed in tandem with a test

director in charge of SI-166.36 and an_ auxiliary unit operator (AV0)

in charge of SI-7. During the performance of the two surveillances

the test director of SI-166.36, assumed that the AVO performing SI-7

would record a piece of data that was necessary .for the performance

of SI-166.36 (the time for the diesel to reach and attain 900 rpm).

After the diesel generator had been started and was running at the

required rpm, the test director realized that the AVO was not

required by SI-7 to record the time it took the diesel to reach the

required speed. The test director retrieved the information from an

alternate data source (control room operator) without repeating the

diesel generator starting sequence. The inspector had no further

questions.

b. SI-94.5, Reactor Trip Instrumentation Refueling Outage Channel

Calibration. Portions of this SI were observed and the inspector had

no questions.

c. SI-98.1, Channel Calibration for Engineered Safety Feature

Instrumentation (Steam Flow & Pressure).

IMI-99 CC 9.108, Offline Channel Calibration of Loop 3 Steam

Generator Steam Pressure Channel II.

On October 7, 1987, the inspector observed testing in progress on CC

9.10B of IMI-99. The inspector noted that a step in the procedure

was signed off stating that the precautions and prerequisites of

FT/CC-9 were completed. FT/CC-9 was not at the work site and the

technician that had signed it off stated that she knew what the steps

were. The following were stated:

(1) Assure double person signoff for critical steps

(2) Notify operations prior to starting work

(3) Place orange stickers in the control room alarm windows

(4) Assure other loops are in service as necessary

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At a later date the inspector determined that the precautions and

prerequisites of FT/CC-9 were somewhat different than what he had

been told. The actual procedure stated the following:

3. PREREQUISITES

3.1 Copy of functionti test or channel calibration procedure

and its associated data sheet (s).

3.2 Provide adeouate communication between instrument

locations.

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3.3 Equipment required - see data sheet of functional test or.

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channel calibration being performed.

3.4 For channel calibrations only, calibration data card for

each instrument listed in component list at the beginning of

each channel calibration procedure.

4. PRECAUTIONS

4.1 Calibration date on test instruments must be current.

4.2 Test may be performed on only one protection set at a time. '

When one protection set is being tested, the remaining

protectior, sets must be in nornal (untripped) mode.

4 . 'J Notify shift engineer of maintenance, calibration, ' or

functional test to be performed.

4.4 Instrumentation and test equipment must be energized at

least the minimum length of time to achieve stability in

accordance with applicable manufacturers instruction manual'.

4.5 If during any at power test, a related reactor protection  ;

channel trip is actuated from another protection set, the test j

must be terminated and all channels returned to normal i

(untripped) condition.

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4.6 Control systems are to be placed in the manual control mode i

before any change is made in a channel defeat and/or channel

transfer switch position. After the change is made, the control

system may be returned to automatic control.

4.7 Observe all posted health physics precautions obtaining a

special work permit when required or if work to be performed ,

could result in changes in radiation levels in work area. Tools ,

or equipment being moved from contaminated to regulated zones or

from regulated to clean zones must be surveyed by health physics

l unit prior to removal.

4.8 Use IMI-118 for backflushing and filling of possible

contaminated instrument lines.

l 4.9 Loops containing Barton transmitters, Models 763 and 764, ,

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used in conjunction with the Foxboro 610A power supply shall be

l- de-energized prior to switching the analog channel test to

l normal, and then re-energized af ter placing the test switch in ,

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the normal operating position.

Although no violation of the procedure was observed, there was an  !

appearance that the procedure was being performed without appropriate '

controls. The inspector discussed with licensee management the

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importance of 'the technicians either knowing explicitly, through

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p'. training, their responsibilities or having a copy of an approved,

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t d. SI 247.900,,E691neered Safety Features Response Time' Verification

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1 ', , During review of SI-247.900,. Engineered Safety Features / Response Time

/

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Verification, the inspector determined that the SI does not meet the

2 - requirements of TS 4.3.2.1.3. TS 4.3.2.1.3 requires that containment

spray responsa ' time be demonstrated to be within the limit at least

- once per 18 months. The inspector determined that the time period

for the containment spray pump start interlock . to close was not

included as part of the response time for the containment spray

isolation valve to open. The pump start interlock must be satisfied

before valve movement will begin. TVA procedures bypassed this

interlock during response time testing. The failure to have an

adequate SI to measure containment spray response time is identified

as violation 327,328/87-65-02.

7. Monthly Maintenance Observations (62703)

Station maintenance activities of safety-related systems and components  !

were observed / reviewed to ascertain that they were conducted in accordance I

with approved procedures, regulato y guides, industry codes and standards, ,

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and in conformance with TS.

The following items were considered during this review: LCOs were met

while components or systems were removed from service; redundant

components were operable; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; procedures used were adequate to control the

activity; troubleshooting activities were controlled and the repair record

c, accurately reflected what actually took place; functional testing and/or

calibrations were performed prior to returning components or systems to

service; quality control records were maintained; activities 'were

accomplished by qualified personnel; parts and materials used were

properly certified; radiologicdl controls were implemented; QC hold points <

were established where required and were observed; fire prevention '

controls were implemented; outside contractor force activities were

controlled in accordance with the approved Quality Assurance (QA) program;

and housekeeping was actively pursued.

a. Work Request (WR) B298870; Maintenance on Temperature Monitor

TM-68-43K  :

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During the performance of the above corrective maintenance, the i

technicians implemented configuration control through the use of

instrument maintenance instruction IMI-134, Configuration Control of

Instrument Maintenance Activities. When this maintenance was [

' observed the TM-68-43K circuit card had been placed into its cabinet

and troubleshooting was in progress. The configuration indicated on

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the IMI-134 data sheet did not indicate the placement af the circuit

card into the cabinet.

IMI-134 section 3.2.7 states that the technician is to list on the

data sheet (work performance sheet) any configuration changes. "This

includes: jumpers, wire lifts, inhibits, temporary instrument

settings, unbolting flanges, disconnecting tubing and pipe fittings,

temporary connection, etc."

During this troubleshooting period, the configuration work

performance sheet did not accurately reflect the configuration of the

equipment covered by the work activity or the trouble shooting that

was conducted due to the fact that the card was in the rack when the

configuration log indicated it was out of the rack. This is due '.o

the licensee policy of logging the card one time for trouble shooting

and then removing and reinstalling the card at will to accomplish

that troubleshooting. The corporate maintenance u.anager had

identified a similar programmatic issue involvina adequate functional

testing of equi 7 ment after maintenance is performed. During a

meeting which was attended by the plant maintenance supe ri nter. den t ,

corporate maintenance manager, and NRC management, it was agreed thn.t

selection of adequate post maintenance testing (PMT) deperded en in

accurate understanding of the troubleshootino that was conoucted and

the cor. figuration changes that occurred in the equipment. This issue

will not result in a violation because the equipment was out of

service during this periud and the licensee had previousi/ identified

tha need for functional testing and was implementing corrective

action when this issue was identified. The inspector had no further

questions,

b. Preventive Maintenance (PM) 0961-068; Main Control Room Recorder

2-M-5

Portions of the 2-REC-068-VAR scaling were observed by the inspector.

The PM referenced the vendor's manual and indicated that the scaling

shculd be accomplish " within the limits set by the vendor. The

va' car set the scaling limits between zero and fif ty milli-amps on

tne wand type indicator pens. The inspector observed that the

technicians had apolied cixty milli-amps to one of the indicator

pens. The techniciins had applied the sixty milli-amps to the pen in

order to mo(6 it aside and had decided that the additional amperage

would not damage the recordar. This particular equipment is not a

critical safety system component (CSSC) and therefore the require-

ments of TS 6.S.1 do not apply and no violation will be issued. This

issue was discussed with the plant maintenance superintendent, the

corporate maintenence superintendent, NRC management and other plant

management. The inspector had no further questions.

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c. ' Work r4quett B28468-d; Calibration of Indicating Instruments for

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480 volt Shutdown Board (282-B)

This item was' performed to validate the voltage, amperage, and watt

~

meters for the 480 volt shutdown boards. - All three meters were found.

within ttlerar.ce. .No adjustments were necessary,

d. hork Plan-(VP) 12360; Fire Protection Connections to the Control Room

Computer.

On Septerrber 28, 1987, the inspector observed work in progress on WP

12360. This WP implements a portion of engineering change notice

(ECN) L5841 on connections between fire detection panel 0-L-633 and

the. plant computer. An engineer was in charge of testing and was

acting as'the test director. Procedures were out and being followed

, by the Individuals performing the WP. The engineer and testing

personnel appeared to be knowledgeable of the work and their

responsibilities. The inspector had no further questions. l,

Ho violations or deviations were identified.

3. Licenneo Event Report (LER) Followup (92700)

The fel;owing LERs were reviewed and closed. The inspector verified that:

reporting requiremente. had been met; causes had been identified;

corrective actions appeared appropriate; generic applicability had been

considered; the LER forms were complete; the licensee had reviewed the t

merit; no unreviewed safety questions were involved; and no violations of .

regulations or TS condition had been identified. [

a. Closed LERs

_

LER 327/86-044 Inadequate Verification of ECCS Flow. As previously

s'.ated i n report 87-36, the remaining required licensee action in

this matter way to revise procedure SI-137.3 to include reactor i

coolant pump (RCP) seal differential pressure requirements. Revision

4 to this procedure was approved on May 29, 1987. NRC review of the r

revised procedure reveals that the necessary changes have been

adequately incorporated. This item is closed. p

LER 327/87-001, Trip Setpoints for Air Circuit Breakers (ACBs)

Incorrect. The tri; setpoints for ACB's on shutdown boards that feed

control and auxiliary building vent boards were incorrect due to a

desig, error. ECN L6SS3 has been issued and the loads have been

! analysed to deterc.11ne proper trip setpoints. WP 12636 has been

issueo and is being worked. The work required to satisfy this LER *

has heq c v.pleted. Licensee's corrective actions appear to be ,

acce; trble. This. item is closed, i

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LER ??.7/87-On, Fa dure to Cycle Test Six Fire Protection Valves per

TS Surveillance Requirement 4.7.11.1.d Due to an Inadequate

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Procedure. The inspector reviewed revision 11 to surveillance

instruction SI-172, Fire System Testable Valve Cycling, and verified

that the six valves have been included. These valves are not

critical safety system components per SQA-134, Critical Structures,

Systems and Componeras (CSSC) list. The inspector also reviewed

completed data sheets indicating these valves had been satisfactorily

cycle tested per SI-172 on August 5, 1987, This item is closed.

LER 327/87-035; Diesel Generator 2B-B Start During Replacement of

Fuses. The licensee was unable to reproduct the event. Subsequent

testing verified that all diesel generators started as required when

a fuse was removed. Conclusion: event may have been generated by

momentary high impedance in relay (ES28Y) circuit causing only that

relay to pickup. Licensee's investigation and results appear to be

adequate. This issue is closed.

LER 327/87-038; 6.9.KV Circuit Breakers Not Tested. The 6.9 KV

circuit breakers for pressurizer control heaters that are used to

protect IE busses from faults on non-1E loads have not been tested

.. because of an engineering oversight. The licensee has generated

surveillance instruction (SI) 737-1A, 18, 2A, 2B to cover TS

surveillance requirement 4.8.3.3 for the 6.9 KV pressurizer control

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heater circuit breakus. Thes~e' h n e been completed. Licensee's

corrective actions appear to be acceptable.

LER 327/87-042; Inadvertent Starting of The Fire Pumps During a loss

of Coolant Accident. The licensee submitted an information LER to

identify a potential problem with the shutdown power capabilities at

the Sequoyah plant. The licensee determined, as a result of an

electrical calculation program review, that an event could occur

which was not analyzed for in the final safety analysis report. This

event was a loss of coolant accident concurrent with the inadvertent

starting and running of the station fire pumps. The licensee

determined that starting the fire pumps concurrent with a LOCA could

potentially degrade the auxiliary electric power system voltage and

thereby prevent safety related equipment from performing its intended

function. The NRC is reviewing this and other issues in the

electrical calculations design review process to determine if the

potential problems identified by the licensee are adequately

resolved. The licensee determined that no immediate corrective

action was necessary because of the mode condition of each of the

units. Long term licensee corrective action will include

administrative compensatory measures on the control of the unit 2

fire pumps. During its operational readiness inspection, the NRC

will examine all administrative compensatory measures employed by the

licensee prior to the startup of either units. The generic issue of

compensating issues for degraded auxiliary electric power systems

will be addressed as a topic in the NRC operational readiness

inspection 327, 328/87-73. This LER is closed.

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LER 327/87-024;-2-FCV-74-3 Exceeded Allowable Stroke Time. .The. local

stroke time of a flow control valve 2-FCV-74-3 exceeded the maximum

allowable stroke time due to an inadequate procedure. The inspector

reviewed the stroke time test results for 2-FCV-74-3, which showed an

acceptable local and remote test after maintenance on June 12, 1987.

TVA's review data comparing the most recent local stroke times for

all power operated valves which did not identify any additional

discrepancies, was also reviewed. A review of the applicable

surveillance instructions indicated that they have been revised to

require comparison of local stroke times to the maximum allowable.

The licensee's corrective actions appear to be adequate. This item

is closed.

LER 327/87-023; Ir.spection of Ice Condenser Assemblies. Inspection

of the ice condenser vent assemblies has not been performed in

accordance with the TS due to lack of guidance in the surveillance

instruction. The licensee determined that the total requirements of

TS surveillance requirement 4.6.5.3.2.b was not being met due to ice

condenser vent assemblies being incorrectly interpreted as being the

intermediate deck doors. This interpretation did not support an

inspection of the vent curtains for free movement. The immediate

corrective action was to verify free movement of the vent curtains.

Long term corrective action revised surveillance instruction

(SI)-108 Ice Condenser Doors, to provide proper guidance for

ensuring free movement of the vent curtain during conduct of the TS

surveillance requirement. The inspector reviewed revision 9 to

SI-108 and found that it contained adequate guidance for ensuring

free movement. of the vent curtain in step 6.2.4. The licensee's

corrective action appears adequate. This item is closed.

LER 327/87-046; Possible Dilution of The Emergency Core Cooling

System During Large Break LOCA Events. This LER was issued by the

licensee for information only. The licensee is currently reviewing

the possible safety implications that a given plant configuration

would have on a post-LOCA long term cooling condition. The concern

involves the possibility tnat nonborated water from such sources as

the essential raw cooling water system, high pressure fire protection

system, primary water system and component cooling water system will

affect the long term shutdown capability of the unit. This issue is

being handled as a startup item by the licensee. The potential

generic issue has been transferred to the NRC, Office of Special

Projects for disposition. This LER is closed.

b. Reviewed LERs which Remain Open

LER 327/87-030; Blown Fuse in Emergency Start Circuits Result in

Spurious Emergency Diesel Generator Starts on Two Occasions. A

review of the fuses indicates that the f ailed fuses came from

(FLAS-5) lot no. 3. As of July 13, 1987, 69 FLAS-5 fuses have failed

with 67 confirmed from lots 2 and 3 and two indeterminate. A change

in manufacturing process was initiated (between lots 3 and 4) by the

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. manufacturer as improvements in the production process. The licensee

is in the process of changing out all FLAS-5, lot 2 and 3 fuses. The

emergency diesel generator, emergency start circuit fuses have been

verified or replaced with fuses from lots manufactured after lot' 3.

The licensee's corrective actions appear to be acceptable. This

issue remains open pending completion of NRC review of the fuse-

replacement program.

(0 pen) LER 327/86-039 Surveillance Requirements Not Performed

Because of Inadequate Procedures. Licensee event report (LER) 327/96-39 reported that procedures were not adequate to test all

interlock functions of the reactor trip system interlocks. Reactor

trip, P-4 permissive (technical specification 4.3.1.1.2, Table

3.3-1.22G) or to test the ice condenser inlet door position at the

local panel during- the functional test (technical specification 4.6.5.3.1). NRC inspectors reviewed surveillance instruction SI-108,

Ice Condenser Doors. The procedure had been revised to include

verification of the inlet door position at the local panel as

required by the technical specification. This item is closed.

Surveillance instruction SI-268-3, periodic verification of the P-4

interlock, was written and provides required testing for the "turbine

trip on reactor trip" function of the reactor trip P-4 permissive.

Testing of the "main feedwater valve closure on low reactor coolant

system average temperature with reactor trip" function of the reactor

trip, P-.4 permissive interlock is in the process of being evaluated.

A draft technical specification interpretation entitled "technical

specification interpretation log No. 94 revision 1-definition of

total interlock function" dated October 7, 1987 was written and

discussed the total interlock function as including the process

input, solid state protection system (SSPS) logic (if any), and

output function. The output function would include verifying the

output of the logic circuitry including the energizing of the SSPS

master relays for ESF permissives and verifying the logic through-the

output of the SSPS undervoltage card for reactor trip permissives.

The requirement to test the slave relay output contacts as a

surveillance instruction (SI) requirement of the technical

specifications is the issue under TVA review. The P-4 permissive

slave relay contact for the main feedwater valve closure is presently

tested but not by a technical specification surveillance instruction.

This item will remain open sending review of TVA action concerning

the slave relays.

(0 pen) LER 327/86-048; Inadequate Verification of ECCS Flow Due to

Procedural Inadequacy. As previously stated in report 87-36,

procedure SI-260.2.1 is to be instituted and procedure SI-260.2 is to

be revised to ensure that Centrifigal Charging Pumps are tested under

conditions as specified in the TS. Completion of these actions is

not required for Unit 2 restart, but is required for restart of

Unit 1. Conversations with licensee personnel reveal that these

corrective actions are not yet complete. This item remains open.

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(0 pen) LER 328/87-041 revision 1, Loss of RHR Flow Resulting From

Mispositioning of a Breaker Due to Personnel Error. A student

assistant unit operator (AVO) opened a circuit breaker .while

performing a routine surveillance to verify alignment of breaker 2 on

the 120 VAC vital instrument power board 1-IT. Licenste's actions

prevented damage to RHR and flow was restored within 4 minutes. The

student AVO was counselled on the necessity for good communications,

of following procedures (attention to detail) and the consequences of

failure to do so. The licensee's specific corrective actions appear

to be acceptable. The generic issue of allowing student operators to

unilaterally operate plant equipment will be reviewed at a later'

date. This item remains open.

(0 pen) LER 327/86-042, Two Surveillance Requirements Not Performed

~

Because of Inadequate Procedures. As previously stated in report

87-36, the licensee has requested relief from American Society of

Mechanical Engineers (ASME), section XI, subsection IWP-3100, for

several safety related pumps because of possible damage to the pump

by throttling the pump miniflow recirculation valves during testing.

Current information -obtained from the licensee indicates that the

granting of such relief is in the final approval process at NRC, and

will be issued in the near future. This item remains open until the

relief request is granted.

(0 pen) LER 327/86-020, Failure to Perform a TS Required Quarterly

Functional Test. As previously stated in report 87-36, procedures

SI-244, Periodic Functional Tests of Radioactive Effluent Monitoring

Instruments and 51-244.2, Peridodic Functional Tests of Radioactive

Effluent Monitoring Instruments were to be revised to include a

functional test for channel F-15-43. These procedures have been

revised by the licensee. However, NRC review has identified several

questions concerning the adequacy of the tests. These questions are;

(1) the procedures provide no guidance as to what position flow

control salve FCV-15-43 is to be lef t upon completion of the test;  ;

(2) is flow indicating controller FIC-15-43 required to function in

both "auto" and "manual" modes, or in the "manual" mode only. The

latter question is due to conflicting statements in licensee ,

generated reports. Attachment 1 to PRO 3-86-031, under "additional i

comments", stated "F-15-43 is used for auto isolation flow control", '

while the "analysis of event" section of the LER report states that

"this instrument provides only an a'.rm on the plant process

computer" and that "the flow channel does not provide an isolation

function"; and (3) presently,51-244 requires that this channel in

unit 1 be tested in the "manual" mode only, while ?I-244.2 requires

that both "manual" and "auto" modes be tested in Unit 2. As a result

of these questions, additional information and/or action is required

from the licensee before this item can be considered complete. This

item remains open.

(0 pen) LER 327/87-027; Surveillance Requirement Was Not Fulfilled

Because Four Essential Raw Cooling Water (ERCW) Valves Were Not

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Verified in the Correct Position. This event occurred because the

subject valves were only verified to be in the correct position

(throttled) every 90 days in accordance with surveillance instruction

(SI-682), ERCW Flow Balance Valve Position Verification. Technical

Specification surveillance requirement 4.7.4.a required them to be

verified in the correct position every 31 days. These valves had

been verified to be'.in the open position every 31 days in accordance

with SI-33, "ERCW Valves Servicing Safety-Related Equipment." TVA

concluded that because the valves were tagged as throttled valves and

the knowledge of plant operators, these valves had remained in the

throttled position. Corrective action was to delete the four subject

valves from SI-33 and revise SI-682 to ensure that these valves are

verified in the correct position every 31 days. SI-682 was also to

be rerun prior to restart.

The NRC inspector confirmed that SI-33 and SI-682 have been revised

as indicated. However, review of the pertinent documentation has

resulted in the following concerns related to the performance of

these sis and the evaluations of discrepancies identified.

The LER analysis does not address the question of how operators

could sign off 51-33, verifying valves in the opsn position, if

they were in fact in a throttled position.

  • A review of SI-682 data packages performed in 1986 and 1987

indicates that a number of valves have been found improperly

positioned at each inspection. Hispositioning ranged from one

turn or less . to the completely opposite position from that

specified (for open or closed valves). Numerous potential

reportable occurrence (PRO) reports have been generated with no

apparent identification or correction of the root cause. PRO

investigations do not appear to be accurate or adequate.

Completed SI-682 data packages had not always listed improperly

positioned valves in a deficiency log and there were inadequate

dispositions of the discrepancies (June, September and December

SI-682 performances).

The plant operations review staff (PORS) is reviewing these concerns

and is performing an indepth root cause analysis. Pending NRC review

of this reassessment by TVA this item remains open.

9. Sequoyah Requalification Program Corrective Actions

Two license examiners of Region II's Operator Licensing Section conducted

an unannounced inspection of Sequoyah's corrective actions for

deficiencies noted during the December 1986 requalification examination.

Of particular interest were actions taken to upgrade training of Reactor

Operators on the bases for steps in the Emergency Operating Procedures

(EOPs).

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On October 8-9, 1987, the inspectors observed ongoing requalification

training for a group of operators, involved in the last week of the 1987

requalification cycle. This consisted of simulator and classroom

training, a ' final written examination and a graded simulator evaluation.

Lesson plans, examination questions and simulator scenarios utilized in

requalification training were also reviewed with the focus being on E0P

related areas.

The findings of this inspection are as follows:

a. The requalification lesson plans for E0P training contained learning

objectives which specifically addressed questions asked on previous

NRC examinations and did not incorporate any further objectives which

would be appropriate for this training. The objectives should be

i

more broadly based to cover the pertinent topics within the lesson

l plan, not just previously asked NRC examination questions,

b. Specific requalification lesson plans did not exist for coverage of

individual emergency procedures. It was nr.ted that some questions

related to procedural bases were developed, however, there were no

requalification learning objectives associated with these questions.

Lesson plans utilized in the hot license training program were

reviewed and could readily be adapted to the requalification program,

'

c. The written examination questions utilized for evaluating the

requalification training in E0P usage were phrased exactly the same

as the learning objectives. No other questions were developed to

examine this area, and further effort should be conducted to create a

broader sample of questions to ensure a valid examination can be

generated for each requalification group.

d. Simulator training covered the learning objectives, however, the

instructor-to-student ratio for training sessions was 1:5 and for

final evaluations was 2:4. Consideration should be given to

improving this ratio in order to provide more attention to

individuals within the crew and equalize the burden on the

instructors to control the simulator scenario as well as evaluate the

operators.

During this inspection, the corrective actions initiated by the

facility were identified and their implementation was found to be

adequate. As noted above, however, further effort is required to

improve requalification training on the E0Ps. These findings were

presented to facility staff members at an exit meeting on October 9,

1987.

10. Plant Operations Review Committee (PORC) (40700)

The inspector conducted a functional review of the PORC which performs as

the onsite safety review committee. This functional review was intended

to evaluate if the activities of PORC could support the heatup and

u-----______-._-.------- - - - - - - _ _ _ _ _ - - - - - - - - - - - - - - . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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23

eventual startup of unit 2. The site is currently changing to a qualified

reviewer concept as a result of TS change 87-34. This review however, has

been conducted prior to the implementation of the TS change. The

inspectors observed the PORC review proposals which affected nuclear

safety including issuance of plant procedures and changes thereof,

modifications to systems and equipment, and unreviewed safety question

determinations (USQDs). The inspectors attended PORC meetings conducted

on October 7, 8, 13, 14, 26, and 28. The inspectors had the following

comments:

One plant modification reviewed by PORC on October 8, 1987,

addressing manholes which held safety related cables, was presented

to PORC without an approved USQD. PORC rejected the modification.

' One plant special maintenance instruction (SMI) addressing thermal

excursion of piping had been rejected by a previous PORC. The

observed PORC was not aware of why the SMI had been rejected and had

to request information from the individual that was presenting the

SMI to explain why the previous PORC meeting had rejected it. This

is an example of a loss of continuity with respect to PORC oversite

activities. In addition, the individual presenting the SMI stated

that the thermal property being tested for would result again because

of a lack of a program to control field routed lines and conduits

with respect to thermal interference. The SMI was rejected by PORC

a second time.

No violations or deviations were identified.

11. IE Bulletins (92701)

IE bulletins (IEB) are documents issued by the NRC which require certain

specific actions of the addressee. The inspector has reviewed the actions

taken by the licensee as a response to the below listed IE bulletins. The

inspector verified that: corrective actions appeared appropriate; generic

applicability had been considered; the licensee had reviewed the event and

that appropriate plant personnel were knowledgeable; no unreviewed safety

questions were involved; and that violations of regulations or TS

conditions did not appear to occur.

IEB 83-01, Salem Anticipated Transient Without Scram. The inspector

reviewed licensee response dated March 4, 1983, A27 830304 010, and

maintenance instruction MI-10.9, Removal, Inspection, Lubrication, and

Replacement of Control Rod Drive MG Set, Reactor Trip, and Bypass Circuit

Breakers. After a review of the supporting documentation and the

implementation of the actions required initially by this bulletin the

licensee's actions were determined to be adequate. This item is closed.

12. Inspector Followup Items

Inspector Followup Items (IFIs) are matters of concern to the inspector

which are documented and tracked in inspection reports to allow further

-

24

review and evaluation by the inspector. The following IFIs have been

reviewed and evalcited by the inspector, ~The inspector has either

resolved the concern identified, determined that the licensee has

performed adequately in the area, and/or determined that actions taken by -

the licensee have resolved the concern,

t

.(Closed) IFI-327/87-11-01, Employee Concern Program (ECP) Element 11301,

Design of Plates Rev. 6. The inspector determined that the specific

concerns addressed in this item were to be closed out by the safety

evaluation report (SER) to be completed by NRC. This item is redundant to

that closure process. Therefore, this item is closed and element report

11301 will remain open until the issuance of the SER.

(Closed) IFI 327/87-11-03, Pipe / Fittings As Related To Construction. This

i is part of the on going employee concern element report 17105 Revision 2.

Parts of the essential raw cooling water system were changed from carbon

steel to stainless steel without a quality seismic analysis being

performed. This has now been accomplished by the civil section of TVA's

division of nuclear engineering. IFI 327/87-11-03 is redundant to element

report 17105 Revision 2 which will be addressed by the NRC in an SER. The

following references were reviewed: (1) TVA's Engineering Change Notice .

L-5009; (2) Memorandum from H. L. Abercrombie to D. W. Wilson dated,

February 6, 1986, (RIMS B 25 870312040); (3) Memorandum from

J. A. Southers to Sequoyah Engineering Project Files dated March 25, 1987,

- (RIMS B 25 870325048); and (4) Memorandum from D. C. Hatcher to Sequoyah

Engineering Project Files dated, April 8,1987, (RIMS B 25 870408078).

This IFI is closed. The element report 17105 will remain open pending

issuance of the SER.

(Closed) Observation 327,328/87-06-EEB-1, Battery and Charger Sizing.

This observation was related to errors in the calculation for sizing of

the class 1E batteries. The NRC design calculation review team _ reviewed

TVA's revised calculations and found them acceptable. This calculation '.

was performed using a maximum inverter load of 17.5 KVA instead of its

name plate rating of 20 KVA. TVA's electrical engineering branch informed

the team that they intend to establish design and administrative limits to

keep inverter loads less than 17.5 KVA. TVA also committed to reevaluate

sizing criteria for the battery and charger whenever the DC system load ,

changes. Design criteria procedure SQN-DC-V-11.6 has been changed to

include in step 1.2.1 system description. . ."The maximum allowable load to

each inverter is 15 KVA." Also, drawings 45N703-2, 45N703-3, 45N703-4,

and 45N706-1, 45N706-2 45N706-3, 45N706-4, and 45N703-1 have been revised

to include the note "although each vital inverter is rated to deliver 20

KVA, the maximum design load on each is 15 KVA." Sequoyah engineering

,

procedure SQEP-09 has been revised to adequately require a calculation for ,

the battery and charger whenever a change in loading of the DC system '

'

occurs. Also, assumption 2.7 in calculation procedure SQN-CPC-004

addresses calculating inverter lord at 17.5 KVA and a design limit of 15

KVA. Licensee action on this item is Adequate. This item is closed. ;

,

f

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25

(Closed) IFI 327, 328/85-26-02, Ice Condenser Door Blocks. This inspector

followup item addressed the control of the devices used to block shut the

ice condenser intermediate doors when the units were in modes 4 and 5.

The devices are controlled through the use of work requests and verified

through routine auxiliary unit operator performance. This item is closed.

(Closed) IFI _ 327, 328/86-69-02, - Effluent Releases In Accordance With

Surveillance Instruction- SI-400.2. On November 19, 1986, a ten minute

transfer was conducted from the high crud tank B to the turbine building

sump without the appropriate setpoint change adjustment to the in-line

radiation monitor. 0-RM-90-225, being performed _as required by

surveillance instruction SI-400.2, Condensate-Demineralizer Waste Effluent-

To The Turbine Building Sump - Periodic Continuous Releases. The system,

by design, provides for a pathway from the tank to cooling tower blowdown

which goes immediately to the river. In this case, however, the transfer

was made to the turbine building sump which is only released itself-

through another monitored pathway. The interpretation given_ the

inspector from the OSP technical staff was that a release occurred only

if it went directly to the environment. Therefore, the transfer of

,

'

liquid from the high crud tank to the turbine building sump was not

considered to be a release even though it left the radiological

controlled area.

The licensee discovered this occurrence 10 minutes into the event and the

transfer was immediately terminated. Once this condition was. discovered

the licensee complied with the action statements of Technical

Specification 3.3.3.9 for this event. Additionally, licensee samples

reflected that the activity of the transferred water was within the

release limits of Technical Specification 3.11.1.

Personnel involved were reinstructed in the requirements of SI-400.2 for

setpoint changes on rad monitors at a January 7,1987 safety meeting.

In addition, the individual involved was privately counselled in

following procedures. Because this issue was identified by the licensee,

the licensee took immediate corrective actions, and no release to the

environment occurred, no violation will be issued and IFI 327,

328/86-69-02 is closed.

i (Closed) IFI 327, 328/86-28-19, Unanalyzed Installation of Piping

Insulation. This item involved the processing of nonconformance report

SQN-QAB-8105 and the necessity to determine if pipe insulation affected

the structural integrity of safety related piping. The issue was

addressed by the Watts Bar nuclear plant employee concerns task group

(ECTG) and in a letter (Brown /Abercrombie, T25 870106 855) dated

January 6, 1987. No structural issues as a result of insulation appear to

exist at Sequoyah. This item is closed.

(Closed) IFI 327, 328/86-71-08, Surry Plant Feedwater Line Rupture.

Following the Surry feedwater line rupture this IFI was opened to ensure

that the licensee initiated a program to evaluate the occurrence of wall

thinning in the feedwater system. The licensee initiated a voluntary

l

. _ - _ -

1

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26

,

program employing various inspection and testing techniques. This

voluntary program was implemented prior to the issuance of IEB 87-01,

Thinning of Pipe Walls In Nuclear Power Plants, dated July 9,1987. The. ',

liconsee responded to the bulletin- in - a letter (Gridley/NRC,

L44 870918 806) dated September 18, 1987. All further NRC. questions

concerning the adequacy of the licensee's feedwater system pipe -thinning

will be addressed within the bounds of the IEB. This item is closed.

(Closed) IFI 327, 328/84-24-04, and 327, 328/86-60-07, Generic Fittings. '

This item was initially closed in inspection- 327,328/86-15- and

subsequently reopened in inspection 327, 328/87-43 to reevaluate all i

aspects of the seal table tube ejection event. The inspector reviewed the

licensee's evaluation of the generic (mixed) fittings as ~ contained in

problem identification report (PIR) SQNEEB87131. This PIR referenced a

report from Singleton Materials Engineering Laboratory (SME). This report

was conducted to determine the adequacy and safety of compression fitting

assemblies which were installed contrary to manufacturers' recommendations-  ;

'

and/or using mixed manufacturer fitting components. The SME report

concluded that regardless of various improper assembly techniques, the  ;

assembly is acceptable if the joint was assembled to leak tightness as >

displayed during hydrostatic testing or in-service leak checking. Various

low-amplitude (service) vibration and high amplitude (seismic) vibration

tests were performed, as well as axial tension (pullout) tests to support t

this conclusion. The licensee has performed walk-down inspections of  !

various plant areas and found no leaking fittings on instruments or drain F

lines, A procedure (MMT-28) was written to implement formal fitting i

assembly requirements. Site personnel have been trained in the use of

this procedure and are scheduled for periodic retraining. This item is

closed.

(Closed) 327, 328/87-06 Observation EEB-3,120V AC and DC Solenoid Valve

Voltage. This observation noted that electrical calculations of cable ,

impedance do not consider cable slack, high ambient temperature, and drops  !

, across connections. Additionally, assumptions are not listed in a  !

dedicated section. TVA's technical justification is documented in  !

"

B43870529908 and is included in TVA's response to the NRC dated July 2,

1987. Nuclear engineering procedure (NEP)-3.1, Calculations, requires t

assumptions to be listed and documented and includes a sample format. The  ;

licensee's response, as described in the July 2, 1987 letter, is adequate.

This item is closed. .

!

(0 pen) 327, 328/86-27 0.3.3-1, Pipe Support Friction Design. This item ,

described TVA's failure to analyze pipe supports for friction forces due t

to thermal displacements. TVA has responded to the NRC in letters dated  !

July 28, 1986, December 31, 1986 and August 21, 1987, with a program to (

evaluate 60 randomly selected supports on major systems. Design criteria a

SQN-DC-V-24.2 Supports For Rigorously Analyzed Category I Piping, defines .

the requirements used in the evaluation program. The general, restart I

criteria contained in volume 2 of TVA's nuclear performance plan (NPP) [

have been made specific to pipe supports in CEB-CI 21.89, Modification i

Priorities for Pipe Supports on Rigorously Analyzed Category I Piping,

r

!

I

i

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, , , - , - - - .,, - - - - _ . . -

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27

These criteria have been transinitted to the NRC in a letter dated,

August 31,. 1987, and will be used to determine whether an action is

required pre-or/ post-startup. This item will remain open until the

evaluations are complete.

(Closed) IFI 327, 328/87-02-06, Review Supplemental Report on Glycol Valve

Stroke Failure. The inspector reviewed revision 1 to LER 327/084-070.

, TVA's further investigation into the valve failure concluded that failure

was due to a buildup of sediment on the stem, was an isolated incident and

that no further action was required. The maintenance history of all

valves of this type were reviewed by this inspector. Total failure to

operate has not been a problem with these valves. Maintenance attention

to these valves has been increased and improved since the incident. This

inspector also reviewed the complete history of stroke times for the two

valves that failed and the work requests that overhauled them after

failure. No degradation trends in stroke times were apparent, either

before or after the event. Although the inspector does not concur that

the f ailure to operate in this event can clearly be blamed on "sediment

buildup," the f ailure does appear to be an isolated case. This item is

closed.

(Closed) 327, 328/86-55 observation 6.15, Testing of 0.5 Second Time Delay

Relays. This item noted that the 0.5 second time delay relays on critical

safety systems component (CSSC) systems had not been calibrated. TVA had

transmitted to the NRC reportable occurrence report SQR0-50-327/871010 on

February 27, 1987, which stated that a QA audit had found that numerous

relays, switches and controllers had not been identified on any procedure

to require calibration. Revision 1 to Maintenance Instruction MI-13.1.3,

Setpoint Verification and Calibration for Time Delay Relays Associated

with Load Shedding logic, was issued on June 9,1987, and these relays

have now been calibrated. TVA has committed, in its response to NRC, to

incorporate the subject instrumentation into Sequoyah standard practice

SQE-8, Control of Installed permanent Process Instrumentation, by

December 31, 1987. The licensee's actions are satisfactory and this item

is closed.

(Closed) VIO 327, 328/86-68-05, paragraph c, section 2.4.4 deficiency

0-2.4-5, Loose Debris in Valves 2-FCV-1-17 and 2-FCV-1-18. NRC inspectors

reviewed the July 16, 1987 TVA response to this portion of the violation

and the corrective action taken. The loose debris in the limit switch

area of the valves was corrected under work plan 12305. Licensee action

on these items is adequate. This portion of the violation is closed.

(Closed) IFI 327, 328/86-48-05, Reportable Occurences. Ten potential

reportable occurrences (PR0s), identified by the licensee, with the status

of corrective actions were reviewed by the inspector. Five of the items

were reported as completed, the remaining five were reported as in

progress. The five items still in progress are:

Item 3 - MOV (CSSC) MOVATs testing

Item 7 - Pressurizer instrumentation

. .

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_ _ _ _ _ _ _ .

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28

Item 8 -1RHR switches

Item 9 - Backfill instrument sensing lines procedures t

'

Item 10 - Condenser vacuum exhaust flow monitor

The_ licensee assigned Sequoyah Activities List (SAL) tracking numbers to *

the above items as follows:

Item 3 - SAL-0317

Item 7 - SAL 0023' .

Item 8 - SAL 0699

Item 10 - SAL 0699

Item 9 was assigned a corporate commitment tracking system (CCTS) number

NCO 870114003 and NCO 870114005. All items are reported as complete for

Unit 2 except item 9 (NCO 870114003) which is being evaluated by TVA

licensing for satisfactory completion per the commitment. A third

commitment, evaluation of outgassing of sense lines for devices required

to operate during and after design basis accident (DBA) was not provided

for review. Discussions with TVA personnel indicated that the outgassing

~

evaluation was not part of this PRO concern. Based on the above, and

TVA's completion of the procedures required for backfill, this item is

closed.

(Closed) IFI 327,328/86-49-05, Apparent Deficiency of Adequate

Instrumentation to Monitor Cooling Water to the Emergency Diesel

Generators (EDGs). A valid emergency start, coincident with a blackout

could result in severe damage to the EDGs under certain operational ERCW

conditions (reliance on cross connect system). Sequoyah has taken steps

to reduce the risk by implementing attachment 1, page 3 of OSLA-30, dated

June 11, 1985. This attachment requires the EDG to be made inoperable if

normal emergency raw cooling water (ERCW) supply is removed from service.

It also requires the assigning of a dedicated operator for the EDG's, if

two (2) trains are made inoperable by the action. This corrective action

should eliminate damage to the EDGs, due to administrative action making

ERCW unavailable. A review of the FSAR did not locate a requirement for

flow measurement of ERCW to the EDGs. The generic issues associated with

this issue will be addressed under "compensatory measures for defeated

safety functions" during the NRC operational readiness review. This item

is closed.

(Closed) IFI 327, 328/84-43-06, Training For Reactor Vessel Head Vent

(RVHV) System. The training for the RVHV system was reviewed as part of a

, recent emergency operation procedures insepetion conducted November 2

through 5,1987. However, during a review of Sequoyah action list (SAL)

Ite'n 13, NRC inspectors noted that there were several discrepancies with

the operation of the RVHV system. The discrepancies were noted in the

performance of work plan (WP) 10597 which was written to perform post

modification testing (PMT) of the system. This PMT tested the operability

i of the RVHV system. During the performance of this PMI many exceptions

l and deficiencies were noted. The testing to prove the operability of the

system was conducted in October of 1983. All deficiencies except for one

l

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!

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29

was addressed by a department of nuclear engineering document entitled.

Interim Review and Approval of Post Modification Test Results, PMT-39,

dated June 6, 1986. The final discrepancy, a change to the controller to

provide more accurate valve position for-the head vent throttle valves, is

to be completed under ECN 5160 during - a future outage. The post

modification testing ECN 2777 along with workpackage 19597 was closed out

on a partial modification completion form which included an attached USQD

dated January 13, 1987. During the inspectors review of. the test

deficiencies and associated documentation, it was noted that during

testing when the block valve (2-FSV-68-395) was opened, both throttle

valves (2-FSV-68-396, 2-FSV-68-397) inadvertently opened to 6D% of full

~

open and then shut within about 5 seconds. This inadvertent opening was

noted during the resolution of deficiency DN-6 in work package 10597,

PMT-39, Appendix 0, Deficiencies and Exceptions. However, the inadvertent

opening did rot appear to have been made part of the deficiency reviewed

by DNE in either the PMT or USQD evaluation. A review of the functional

restoration guides (FR-I.3, revision 0, page 9 and 10, and FR-H.1, page

10) indicated that the procedures do not address the system- abnormality.

During discussions with the TVA staff, TVA indicated that the problem with -

this target rock valve was well known. However, when questioned by NRC

inspectors, some control room operators were not aware of the problem.

The NRC inspectors requested the licensee address the following concerns:

a. Why does the ACTION / EXPECTED RESPONSE column, step 19 of SQNP FR-I.3,

Unit 1 or 2, revision 0, page 9, and step 13 RESPONSE NOT OBTAINED,

SQNP FR-H.1, Unit 1 or 2, revision 1, page 10, not provide

precautions or describe the expected system response?

b. Provide documentation which indicates that the vendor has evaluated

the fact that the Target Rock throttle valves may "pop" open when

subjected to inlet pressure transients.

c. Verify that DNE agrees that the valve performance is acceptable and

documented by an unreviewed safety question determination (USQD).

d. Provide documentation that the problem has been addressed to the

operating crew.

Items (a) and (d) above, regarding the functional restoration guides

and training on valve response, was addressed by the recent NRC E0P

inspection. Item (b) above was addressed by the licensee by providing

the inspector with copies of Target Rock report #2866, Solenoid Valve

Response to Inlet Pressure Transient (December 17, 1980), along with

ASME publication 81-PVP-39 (April 1981). Item (c) above was addressed

by the licensee by providing the inspector a copy of the test deficiency

review and approval memorandum (D. W. Wilson to H. L. Abercrombie,

RIM B25 860606 012). .

The inspectors reviewed the above information and determined that items

(a), (b), and (d) were adequately addressed. However, item (c) above was

~

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_ _ _ _ _ ___ _______

i

30

determined to be a violation of corrective action requirements, in that,

the department of nuclear engineering review of the test deficiencies

documented in deficiency report 2-PT-789 (dated April 12, 1984) did not

specify that emergency procedures should be changed and personnel trained

to cope with the described condition. Additionally, the evaluation of the

test deficiency did not reference the vendor's test report as

justification for accepting the test deficiency. This item, which involved

questionable performance of equipment is identified as a violation of the

10 CFR part 50, appendix B requirements for effective corrective action,

and is identified as violation 327, 328/87-65-01.

(Closed) IFI 328/86-62-04, Review of Final Revision of AI-19, part IV,

plant Modification After Licensing, To Ensure Time Commitments for ECN

Closecut and Drawing Update Is Established. During a review of the

transitional design change program conducted in November 1986, and

June 1987, (inspection reports 327, 328/86-62 and 327, 328/87-42) the

inspectors identified a weakness in the new program. Specifically, there

was no commitment on TVA's part to ensure timely closure of ECNs. This

issue was seen as a significant weakness, because the lack of timely

closure was determined by TVA and the NRC to be a contributor to past

design control problems. Additionally, the inspectors determined that

without timely closure of ECNs the requirements of 10 CFR 50.71, which

requires the annual update of the FSAR to be current within 6 months of

the modification, could not be assured. The licensee determined that it

would take approximately 6 months to complete the closure of the ECNs from

the point of field completion and operations acceptance of the

modification. This time commitment was established by revision 24 of

AI-19, part IV and appears to reflect the actual time needed by the

licensee to complete all reviews and closure effort. However, this 6 month

closure of the ECNs will not ensure that the requirements of 10 CFR 50.71

are satisfied. Specifically, TVA uses the closure of the ECN and not the

field completion of physical work, as the starting point of updating the

FSAR. This process could cause as much an 18 montF lag between the actual

plant configuration and the FSAR.

The above issue was discussed with the licensee and a commitment to start

the FSAR update process at field completion vs. ECN closeout was made by

the licensee. However, the licensee should have changed the FSAR update

process as part of the transitional design control program based on

corrective action report (CAR) 86-04-21 and the findings in inspection

report 327, 328/86-62. This lack of complete correct've action is

identified as a violation of 10 CFR part 50, appendix B, criterion XVI and

is a second example of violation 327, 328/87-65-01. IFI 328/86-62-04 is

closed.

13. Restart Test

a. SI-26.2B Loss of Offsite Power With Safety Injection D/G 2B-B

Containment Isolation Test, Revision 14, and STI-78, D/G 2B-B Load

Sequence Tes'., Revision 0. STI-78 was performed in conjunction with

51-26.28. N1C inspector > observed the performance of all of STi-78

_ _ _ _ _ _ _ _ _ _ _ _ - _

31

and test 1 and test 2 of SI-26.28. Test sequence 1 and test sequence

2 tested loading / shedding and safety injection / phase B actuation.

NRC intpectors attended the shift turnover briefing prior to the

testing. The of f going and on-coming shift supervisors discussed

plant rctivities for the previous shift, maintenance activities

perfo'.meri during the previous ibif t and the performance of the load

shnding, and the containment isolation test. NRC inspectors

6 tended a second briefinn for the on-coming operating crew for the

performance of the test. The briefing covered personnel assignments,

location of personnel, comrnur;ications, and the details of how the

timing would be conducted. The importance of good comsunication was

stressed by the shift supervisor. Each person responsible for

sections of the test was given highlighted copies of applicable

sections of the test. The following observations were noted during

the testing:

-

All pressurizer heaters were energized rather than just group B

and C heaters as specified by the test procedure. The assistant

test director told the unit operator to energize pressurizer

heaters. The unit operator energized all heaters and then

questioned the assistant test director as to whether he wantd

all heaters on. The lineup was promptly restored to the co' rect

lineup. The unit operator did not, like other test per:,onnel,

have a copy of the test procedure to check his pn cicular

actions. During subsequent steps it was noted that the unit

operator was careful in requesting information on what switches

and controls to operate by number. However, he was not given a

copy of the test. Having a copy of the procedure c>r repeating

back exact verbage of the step would have prevented the

occurrence.

-

During the initiation of the safety injection (SI) signal all

personnel were on nation to start recorders from a countdown

and "go" signal from the assistant test director. The assistant

test director did not check to see that the unit operator was

ready, consequently all recorders were started on the "go"

signal, but the safety injection signal was not activated. The

test was delayed to change paper in the recorders and rerun the

step. The test director was not directly overseeing this

portion of the test which may have contributed to the error.

-

During the tests, the unit operator secured an SI pump with the

SI signal still inserted. This resulted in the SI pump stopping

and immediately restarting. The assistant test director noted

the mistake and reminded the unit operator to place the pump in

the "lockout" position. The pump was secured due to isolation

l valve leakage that was increasing pressurizer level. Securing

the pump was not part of the test procedure, but was allowed by

precautions in the procedure to control plant parameters.

l

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32

.

- Loads normally powered from vital inverter 1-4 was inadvertently

deenergized during the test when the 6.9KV shutd(wn board was

blacked out in step 6.2.8. During the shift turnover briefing,

it was discussed that maintenance was being performed on the 1-4

vital inverter. It was not brought out that the inverter was

powered from its maintenance supply (the 480V shutdown board)

5 nor that the maintenance supply would be deenergized during the

blackout of the 6.9 KV shutdown board. When power was lost, the

,

CO 2 fire doors for the 2B-B board room tripped. This caused

s

r considerable confusion in the control room as the cause was not

known. The test was stopped ano eventually it was determined

E that the vital inverter had been deenergized. The problen could

h have been prevented by a careful review of the effects of plant

maintenance on testing that was to be conducted.

i The following material deficiencies or potential material

jr deficiencies were noted during the testing:

a

f -

The 28-8 diesel exhaust fans did not restart when the diesel

-

started and returned powec to the 6.9KV shutdown boards. The

J probable cause was determined to be a f ailure of relay R1X2. A

work request was written to investigate and correct the cause of

the failure. The relay problem did not effect continuing the

test and was noted as a test deficiency.

-

During a review of the recorder data from the recorder connected

to the 6.9KV shutdown board, it was determined that the recorder

1 had stopped working during the SI activation test.

4 Investigation revealed that a lead had become loose causing the

malfunction. The malfunction resulted in having to rerun a

section of STI-78, Load Shedding. Steps 6.5.3 through step

r 6.5.6 had to be repeated. These steps pertained to the

simultaneous starting of a main fire pump and containment spray

_

pump on the 6.9KV shutdown board that was being supplied by the

,, 2B-B diesel generator. The inspector determined that the

licensee's actions were in compliance with AI-47.

s

-

One procedure problem was noted with 51-26.28, step 6.2.2.2 in

f[w resetting the phase A isolation signal. The step read to reset

the phase A isolation signal using reset button HS-30-63D rather

than using HS-30-630 and HS-30-63E. The result was that some of

the relays in the following steps were not deenergized as

-

required by the procedure. The test was stopped while a

temporary change to the test procedure was obtained. The test

was recommenced after the temporary change was processed and

approved.

-

During the test the 2B-B diesel generator fuel oil transfer pump

did not restart as expected upon a low day tank level. The 2B-1

diesel generator fuel oil transfer pump was tagged out for

maintenance. Fuel oil to support the diesel during the test was

. . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

,

33

transferred manually. The licensee is investigating why the

fuel oil transfer operation did not function as expected. The

failure of the fuel oil transfer pump to start did not affect

the performance of the test.

The discrepancies identified during the performance of the above

. testing activities was discussed during the exit. meeting with

Sequoyah plant management. The NRC will further review these

discrepancies under unresolved item (URI) 327, 328/87-65-04.

b. Followup of open Sequoyah activity list (SAL) item 51 L-finger Gap

Adjustment (MI-11.2A). This SAL item addressed the resolution of

Limitorque valve maintenance regarding adjustment of limit switch

L-fingers. The inspector reviewed the limitorque vendor manuals

available in Sequoyah document control facility. No provisions or

reference to the process of measuring the gap or bending the

L-Fingers could be found in the manuals reviewed. The vendor manuals

do suggest that the geared limit switches should be replaced as an

assembly. The diagrams pictured show the L-fingers as part of the

assembly. Discussions with TVA personnel indicated that the vendor

is planning to include the measurement of the L-finger gap in future

maintenance instructions. TVA also presented a Commonwealth Edison

internal memo that, in part, states: the vendor. Limitorque, has

addressed the concern of insufficient contact pressure by inspection

of the L-finger gap and bending the L-finger to achieve a 1/32-inch

nominal gap. This issue is closed.

.

L.