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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20084K4981976-10-0505 October 1976 Updates AOs 50-265/74-3,50-265/74-13,50-265/74-16 & 50-265/74-19 Re low-low Reactor Water Level Switch LIS-2-263-728 Failure.Surveillance Interval Changed to Monthly.Switch Installation Delayed Pending Analog Trip Sys ML20084S2291975-12-19019 December 1975 Supplementary Ao:Four Temp Switches Were Found to Trip at Values Exceeding Tech Specs Limits.Caused by Sensors Placed Too Closely to HPCI Turbine & Steam Piping.Different Temp Sensor Will Be Installed ML20084S5561975-11-19019 November 1975 Preliminary Ao:On 751109,traversing Incore Probe (TIP) Ball Valve 2 Failed to Close.Manual Attempts to Close Valve Failed.No Cause Stated.Addl Info Will Be Submitted in AO 50-265/75-45 ML20084S5851975-11-17017 November 1975 AO 50-265/75-44:on 751107,RCIC Turbine Tripped.Caused by Failure of Hydraulic Fluid servo-valve Actuator.Actuator Replaced & Overspeed Trip Mechanism Repaired ML20084S5731975-11-10010 November 1975 Preliminary Ao:On 751107,reactor Core Isolation Cooling (RCIC) Sys Turbine Tripped.Caused by Failure of Hydraulic Fluid servo-valve actuator.Servo-valve Actuator Will Be Replaced.Addl Info Will Be Submitted in AO 50-265/75-44 ML20084S5931975-10-30030 October 1975 Ao:On 751029,RHR Sys 2 Supply from Emergency Diesel & Core Spray Sys 2 Bus/Logic Power Failure Alarms Received.Caused by Switch 12 in Off Position.Switch Returned to on Position. Addl Info Will Be Submitted in AO 50-265/75-43 ML20084S6021975-10-28028 October 1975 AO 50-265/75-42:on 751018,differential Pressure Across B Train of Standby Gas Treatment Sys Exceeded Tech Spec Limit. Caused by Fouling of High Efficiency Prefilter.Filter Changed & Tested Satisfactorily ML20084S6191975-10-27027 October 1975 AO 50-265/75-41:on 751018,while Performing Monthly Diesel Generator Surveillance Test,Diesel Generator Reactive Power Meter in Control Room Pegged Full Scale.Megawatt Output Load Erratic.Operator Tripped Diesel.Caused by Equipment Failure ML20084S7771975-10-24024 October 1975 AO 50-265/75-38:on 751014,weld Exams Indicated Crack on B Loop of Rx Recirculation Discharge Bypass Line.Caused by Intergranular Stress Assisted Corrosion.Both Bypass Lines Will Be Removed ML20084S6471975-10-24024 October 1975 AO 50-265/75-40:on 751016,while Performing Routine Surveillance,Three High Drywell Pressure Scram Switches Found to Exceed Tech Spec Limit.Apparently Caused by Instrument Drift.Pressure Switches Recalibr & Tested ML20084S6741975-10-24024 October 1975 AO 50-265/75-39:on 751016,one Bergen-Patterson & Two Grinnell Hydraulic Snubbers Found W/Empty Oil Reservoirs. Apparently Caused by Equipment Failure.Snubbers Will Be Repaired or Replaced ML20084S6121975-10-20020 October 1975 Telecopy AO 50-265/75-42:on 751018,differential Pressure Across B Train Particulate Filters of Standby Gas Treatment Sys Exceeded Tech Specs.Caused by Smoke from Small Fire Created by Onsite Welders.Work Request Issued ML20084S2071975-10-20020 October 1975 Telecopy Ao:On 751020,radwaste Discharge Batch 3709 Discharged at Rate Which Exceeded Tech Spec Limit.Further Info to Be Provided in AO 50-254/75-22 ML20084S6291975-10-18018 October 1975 Telecopy AO 50-265/75-41:on 751017,during Monthly Surveillance Testing of Diesel Generator,Electrical Flash Burned Out Diode Rectifier Array of Generator Exicitation Circuitry.Output Breaker Tripped.Generator Inoperable ML20084S6561975-10-17017 October 1975 Telecopy AO 50-265/75-40:on 751016,during Routine Monthly Surveillance,Three High Drywell Pressure Switches Found to Exceed Tech Spec Limit.Cause Not Stated.Instruments Recalibr & Tested Satisfactorily ML20084S6831975-10-17017 October 1975 Telecopy AO 50-265/75-39:on 751016,two Grinnell & One Bergen-Patterson Hydraulic Snubbers Found Defective.Cause Not Stated.Work Request Issued for Repair ML20084S7821975-10-17017 October 1975 AO 50-265/75-37:on 751007,minor Leakage from B Feedwater Flush Line Observed.Caused by Equipment Failure.Flush Line Being Repaired ML20084S2181975-10-15015 October 1975 Telecopy Ao:On 751014,two High Drywell Pressure Scram Switches Found in Isolated Condition.Further Info to Be Provided in AO 50-254/75-21 ML20084S7681975-10-14014 October 1975 Telecopy Ao:On 751014,crack Indication Confirmed on B Loop in heat-affected Zone on Pipe Side of pipe-to-weldolet Weld. Repair Plans Incomplete.Addl Info Will Be Submitted in AO 50-265/75-38 ML20084S7851975-10-0707 October 1975 Telecopy Ao:On 751007,pipe Crack Found on Feedwater Flush Line 2-3206B-4-C at Main Feedwater Line 2-3204B-18-C.Minor Leakage Did Not Affect Reactor Inventory.Repairs Initiated. Addl Info Will Be Submitted in AO 50-265/75-37 ML20084S0391975-08-31031 August 1975 Telecopy Ao:On 750830,while Performing Monthly RCIC Operability Surveillance Test RCIC Would Not Reach Normal Conditions.Possibly Caused by Overspeed Mechanism.Required Testing of HPCI Sys Initiated ML20084R9871975-08-31031 August 1975 Telecopy of AO 50-265/75-36:on 750831,during Shutdown, Instability Was Experienced on Feedwater Control Sys Which Caused 3/4 Inch Drain Lines to Sever from Low Flow Feedwater Regulating Valve.No Radioactive Matl Released ML20084S0041975-08-31031 August 1975 Telecopy Ao:On 750830,while Testing Operability of HPCI Sys, Auxiliary Oil Pump Kept Tripping & HPCI Turbine Failed to Start.Orderly Shutdown Was Initiated.Further Info to Be Provided in AO 50-265/75-35 ML20084S0651975-08-25025 August 1975 Telecopy Ao:On 750825,oil Separator Overflowed Into Spray Canal Releasing Contaminated Water.Caused by Rainfall. Remaining Water in Oil Separator Being Discharged as Controlled Batch Release ML20084S0991975-08-25025 August 1975 Telecopy Ao:On 750824 Grinnel Snubber Had Empty Fluid Reservoir & Bergen-Paterson Snubber Had Leaking Accumulator. Replacement Parts Installed Prior to Reactor Startup on 750825.Further Info to Be Provided in AO 50-265/75-32 ML20084S1831975-08-18018 August 1975 Telecopy Ao:On 750817,following Maint Outage,Reducer of Low Flow Feedwater Regulating Valve 2-643 Severed Due to Vibration.Unit Manually Scrammed & Reactor Level Maintained W/Rcic Sys ML20084S2471975-08-15015 August 1975 AO 50-254/74-19:on 750805,reactor High Pressure Scram Switch 1-263-55A Was Isolated.Caused by Switch Left Isolated After Completion of Previous Month Testing.Establishment of Administrative Control Over Valves Initiated ML20084S2231975-08-13013 August 1975 Telecopy Ao:On 750812,ECCS Low Pressure Permissive Sensor PS-2-263-52A Discovered in Isolated condition.PS-2-263-52A Put Into Svc & All Switches Satisfactorily Functionally Tested.Further Info to Be Provided in AO 50-265/75-30 ML20084S2221975-08-11011 August 1975 Telecopy Ao:On 750809,standby Liquid Control Pump 1A Produced Flow Rate Below Tech Spec Limit.Caused by Premature Lifting of Relief Valve RV-1-1105A.Relief Valve Reset. Further Info to Be Provided in AO 50-254/75-20 ML20084S2371975-08-0808 August 1975 AO 50-265/75-28:on 750729,RHR Svc Water Pump 2A Fell Below Required Flow Level & Pump Pressure Limit.Caused by Accumulation of Debris Lodged in Pump Suction & Impeller. Debris Was Removed ML20084S2261975-08-0808 August 1975 AO 50-265/75-27:on 750729,during HPCI Monthly Surveillance Operation Only Able to Attain Pump Flow Below Tech Spec Limit.Caused by Improper Pinning of Pilot Valve Lever Arm. Lever Arm Adjusted ML20084S2541975-08-0505 August 1975 Telecopy Ao:On 750805,reactor High Pressure Scram Switch PS-1-263-55A Was Still Valved Out from Previous Month Surveillance.Switch Was Calibr & Valved in Svc.Further Info to Be Provided in AO 50-254/75-19 ML20084S2591975-08-0404 August 1975 AO 50-265/75-26:on 750725,oxygen Level of Unit 2 Suppression Chamber Exceeded Tech Spec Limit.Caused by Insufficient Nitrogen Available to Inert Primary Containment Due to Leaking Flange.Gasket in Nitrogen Line Replaced ML20084S3311975-08-0101 August 1975 AO 50-254/75-18:on 750724,pressure Switch PS-1-1622B Tripped at Value Exceeding Tech Spec.Caused by Instrument Drift.Pressure Switch Recalibr ML20084S3751975-07-31031 July 1975 AO 50-254/75-17:on 750721,traversing Incore Probe Machine Three Ball Valve Failed to Close When Detector Was Withdrawn to in-shield Position.Caused by Failure of Spring to Close Ball Valve Completely.New Valve Installed ML20084S2321975-07-31031 July 1975 Telecopy Ao:On 750731,4 of 16 HPCI Area High Temp Switches Tripped at Values in Excess of Tech Spec Limits.Switches Calibr.Further Info to Be Provided in AO 50-265/75-29 ML20084S3181975-07-31031 July 1975 AO 50-265/75-25:on 750721,two Hydraulic Snubbers Found to Have Empty Oil Reservoirs.Caused by Several Oil Leaks for One Snubber.Failure of Second Snubber Unknown.One Snubber Fitting Tightened & Other Snubber Replaced ML20084S2421975-07-30030 July 1975 Telecopy Ao:On 750729,RHR Sys Svc Water Pump 2A Failed to Meet Tech Specs Required Flow Rate.Work Request 2794-75 Immediately Issued for Investigation & Repair.Further Info to Be Provded in AO 50-265/75-28 ML20084S2461975-07-29029 July 1975 Telecopy Ao:On 750729,HPCI Sys Could Not Obtain Tech Spec Required Flow Rate.Cause Unknown.Eccs Testing Begun as Investigation.Further Info to Be Provided in AO 50-265/75-27 ML20084S6641975-07-29029 July 1975 AO 50-265/75-24:on 750720,crack Found on Reactor Feedwater Sys Flushing Line 2-3206B-4-C.Caused by Stress Point Due to Improper Blending of Fillet Weld.New Section of Pipe Welded ML20084S3361975-07-28028 July 1975 Telecopy Ao:On 750724,pressure Switch 1-1622B Found to Trip at Value Exceeding Tech Specs Limit.Switch Was Immediately Recalibr.Further Info to Be Provided in AO 50-254/75-18 ML20084S2641975-07-25025 July 1975 Telecopy Ao:On 750725,during Completion of Inerting,Primary Containment Oxygen Concentration Was Not within Tech Spec Limits.Further Info to Be Provided in AO 50-265/75-26 ML20084S6931975-07-25025 July 1975 AO 50-265/75-23:on 750718,high Drywell Pressure Switch 2-1001-89B Failed to Operate.Caused by Dirt & Scale Plugging Pressure Pulsation Damper.Damper Cleaned ML20084S3901975-07-25025 July 1975 AO 50-254/75-16:on 750717,unsampled Laundry Water Added to Floor Drain Sample Tank River.Caused by Operator Error. Radwaste Foreman Must Verify Valve Checkoff List Prior to Discharging to River ML20084S7131975-07-24024 July 1975 AO 50-265/75-22:on 750716,two of Four High Drywell Pressure Switches Exceeded Tech Specs Limit.Caused by Instrument drift.PS-2-1001-88B & C Calibr to Trip at 1.90 Psi ML20084S6261975-07-22022 July 1975 Telecopy Ao:On 750721,traversing Incore Probe (TIP) 3 Ball Valve Failed to Close.Shift Foreman Went to TIP Cubicle & Tapped Valve,Causing Valve to Close.Further Info to Be Provided in AO 50-254/75-17 ML20084S3261975-07-22022 July 1975 Telecopy Ao:On 750721,one Grinnell & One Bergen-Paterson Snubber Found Defective.Work Request Issued for Repair. Further Info to Be Provided in AO 50-265/75-25 ML20084S6791975-07-21021 July 1975 Telecopy Ao:On 750720,water Discovered in MSIV Room.Caused by Crack on Feedwater Flush Line B.Preparations Currently Being Made for Repair of Cracked Line ML20084S6161975-07-18018 July 1975 Telecopy Ao:Laundry Drain Sample Tank Level Dropped & Floor Drain Sample Tank a Level Rose.Caused by Not Verifying Closing of Laundry Tank Discharge Valve.Discharge Immediately Stopped ML20084S6981975-07-18018 July 1975 Telecopy Ao:On 750718,pressure Switch 2-1001-893 Failed to Operate at Any Pressure.Work Request 2640-75 Initiated to Investigate & Correct Problem 1976-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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April 21, 1975 0'X t -s Y 97 j
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J. Keppler, Regional Director Directorate of Regulatory Operations Region til
- U. S. NUCLEAR REGULATORY COMMISS1011 799 RooseveIt Road .
Gicn Ellyn, IL 60137
REFERENCE:
Quad-Cities Nuc1 car Power Station, Unit 2 Docket No. 50-265, DPR-30 ~
Appendix A, Sections 1.0.A.4, 6.6.B.1.2.
Dear Hr. Keppler:
The purpose of this letter'Is to provide you with notification of an Abnormal Occurrence as required by Technical Specification 6.6.B.I.a. within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the occurrence.
At 8:00 p.m. on April 18, 1975, during the emergency core cooling system simu-lated automatic initiation surveillance test, the high pressure coolant in.lec-tion system turbine stop valve failed to open upon receipt of the int tlation signal. The stop valve did not open because the auxiliary tube oil pump failed to remain running, thus insufficient oil flow was supplied to open the valve.
The auxiliary lube oil pump sta,rted, but stopped again due to a failure of the scal-in circuit. Work Request 1385-75 was issued to investigate and make re-
. pairs as necessary.
This occurrence was discussed by telephone with Mr. Feierabend of your office on April 21, 1975 Further information will be provided by Abnormai Occurrence Report A0 50-265/75-14 which will be submitted within 10 days of the date of this occurrence.
Very truly yours, COMMOUWEALTil EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION
/! W . .
N. J. Kalivianakis Station Superintendent NJK:SRH/dkp .
cc: Directorate of Lic:nsing )
J. S. Abel ,
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April 2c, 1975 Mr. John F. O' Leary. Di recto r Directorate of Licensing Regulation U. S. Nuclear Pegulatory Co mission Washington, D. C. 20545 Re f e ren ce : Quad-Ci ti es Nuclear Powe r S ta ti on Occket No. 50-265, OPR-30 .
Appendix A, Sections 1.0.A.4, 6.6.B.l.a
Dear Mr. O' Leary:
Enclosed please find Abnorr al Occurrence Report No. 50-265/75-14 for Quad-Cities Nuclear Power Station. This occurrence was previously reported to Region Ill, Directorate of Regulatory Operations by telephone on April 21, 1975 and to you and Region Ill, Di rectorate of Regulatory Operations by telecopy on April 21, 1975 This report is submitted to you in accordance with the requi rements of Tech-nical Specification 6.6.8.1.a.
Very truly yours, COMMONWEALTH EDIS0'4 COMPANY '
QUAD-CITIES NUCLEAR POWER STATION s- '~! . /..
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N. J. Kalivianakis Station Superintendent NJK/S RH/lk cc: Region lil, Directorate of Regulatory Operations J. S. Abel
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L REPORT NUMBER: A0-50-265/75-14 REPORT DATE: April 28. 1975 OCCURRENCE DATE: April 18, 1975 FACILITY:
Quad-Ci ties Nuclear Power Station Cordova, Illinois 61242 IDENTI FICATION OF OCCURRENCE:
Failure of Uni t 2 High Pressure Coolant injection (HPCI) system control valve to open during the Emergency Core Cooling System (ECCS) simulated automatic actuation test. ,
CONDITIONS PRIOR TO OCCURRENCE:
Uni t 2 was in the refuel mode at zero poser. An ECCS simulated automatic actuation test was being performed at the time of the occurrence.
DESCRIPTION OF OCCURRENCE:
During the ECCS testing on April 18, 1975 at 8:00 p.m., the HPCI system failed to start. It was noted by the operator that the HPCI auxiliary oil pump was cycling on and off and the emergency pump started. The aux-liiary oil pump supplied both lubrication for the HPCI turbine and hydr'au-lic pressure to open the turbine steam stop valve. The emergency tube oil pump supplies only lubrication for bearings.
The operator manually started the auxiliary oil pump and the HPCI system started successfully.
DESIGNATION OF APPARENT CAUSE:
. The auxiliary oil pump starts automatically on a loss of coolant accident initiation signal when the control switch is in the auto posi tion. The auxiliary oil pump supplies both the high pressure hydraulic system and a lower pressure hydraulic control system. A portion of the control system oil is also used to supply the bearing lubrication header.
The emergency oil pump is used to supply the bearing lubrication header only in the event the shaf t driven and/or the auxiliary oil pumps become unavail-able. The signal required to auto start the emergency oil pump is normal
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O A0 50-265/75-14 April 28,1975 l
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pressure on the high pressure header and low pressure on the bearing lub-rication neader. ,
i i During an auto initiation of the high pressure coolant injection system the auxiliary oil purp auto starts and runs until the shaft driven pumps
- are capable of supplying the required hydraulic pressure at which time the auxiliary oil pump will auto trip. .
t Due to the pressure switch settings however, the emergency oil pump would sense nornal pressure on the high pressure hydraulic system while it was .
still sensing low pressure on the bearing lubrication header and would there- l fore auto start. As soon as the emergency oil punp started, the pressure would increase on the hydraulic control systen header which would auto trip i the auxiliary oil pump. The energency oil pump cannot supply the control ,
system header so the auxiliary oil pump would again auto start on a low pressure signal. During this cycling, there was not enough control oil pressure available to open the stop valve,.
I ANALYSIS OF OCCURRENCE:
Had an actual initiation signal for the HPCI systen been received during plant operation, the operator would have had to manually start the auxiliary lube oil pump in order to open the turbine stop valve. He would have re-cognized this when he saw the pump cycling. -
Wh'en such an initiation signal is received, the core spray'and residual heat j renoval (RHR) pumps also start but do not inject water into the core until the pressure is reduced. If the HPCI system is not started fast enough or the leak size is greater than its capacity, the automatic blowdown system
} will open the electric relief valves to reduce pressure and allow both core spray pumps and four RHR pumps to add water to the core. Therefore;. in spite of the HPCI sy. stem delayed start or failure to start, the core would have been adequately cooled to prevent any health h'azard to plant personnel or the public.
CORRECTIVE ACTION: .
The 'immediate action taken in response to this occurrence was to manually
~
start the HPCI auxiliary pump. Follow-up corrective action was to raise the auxiliary oil pump pressure switch set point to eliminate the automatic trip. During an automatic initiation signal the auxiliary oil pump will auto
- start and remain running until manually tripped.
FAILURE DATA:
This is the first such event to occur at Quad-Cities Station; therefore, there are no safety -implications based. on cumulative experience. !
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y v-m -m-- - em e ---- y .e , _, e-.e.