SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With

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Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With
ML20195H153
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 05/31/1999
From: Dimmette J, Hamilton L
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GL-97-02, GL-97-2, SVP-99-123, NUDOCS 9906160284
Download: ML20195H153 (11)


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', Quad Citics GenerJting St AtIOn s 22710 2(x4h Avenue North l Ostdova, II. 612 s 2-9740 Tel .umis4 224:

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SVP-99-123 1

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June 9,1999 U. S. Nuclear Regulatory Commission 1 ATTN: Document Control Desk Washington, D.C. 20555-0001 Quad Cities Nuclear Power Station, Units 1 and 2 {'

Facility Operating License Nos. DPR-29 and DPR-30 NRC Docket Nos. 50-254 and 50-265

Subject:

Monthly Operating Report ,

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In accordance with Generic Letter 97-02 and Technical Specifictition 6.9.5, I

'" Monthly Operating Reports," we are submitting the Monthly Op! rating Report for Quad Cities Nuclear Power Station, Units 1 and 2. This report covers the period

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May 1,1999, to May 31,1999.

Should you have any questions concerning this letter, please contact Mr. Wally Beck, Acting Regulatory Assurance Manager, at (309) 654-2241 extension 3100.

Resp ully,

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Joel P. Dimmette, Jr. I Site Vice President  !

Quad Cities Nuclear Power Station Attachment -

en cc: Regional Administrator- NRC Region lil NRC Senior Resident inspector - Quad Cities Nuclear Power Station

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9906160284 990531 PDR ADOCK 05000254 R PDR . . _

A Unicom company

pr ATTACHMENT QUAD CITIES NUCLEAR POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT COMMONWEALTH EDISON COMPANY l

AND MIDAMERICAN ENERGY COMPANY FACILITY OPERATING LICENSE NOS. DPR-29 AND DPR-30 i

NRC DOCKET NOS. 50-254 AND 50-265 1

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TABLE OF CONTENTS

1. - Introduction
11. Summary of Operating Experience

'A. Unit One

! B. Unit Two

.111. Operating Data Statistics A. Operating Data Report for May- Quad Cities Unit One B. Operating Data Report for May - Quad Cities Unit Two IV. . Unit Shutdowns A. Unit One 'hutdowns -

i B. Unit Twt Shutdowns V.- Amendments to Facility License or Technical Specifications 1

VI. Unique Reporting Requirements ,

1 A. Main Steam Relief Valve Operations j l

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l. INTRODUCTION-

. Qua'd Citie's Nuclear Power Station is composed of two Boiling Water Reactors and Steam Turbine / Generators, each with a Maximum Dependable Capacity of 769 MWe

- Net, located in Cordova. lilinois. The Station is jointly owned by Commonwealth Edison

-. Company and MidAmerican Energy Company. The Nuclear Steam' Supply Systems are G'eneral Electric Company Boiling Water Reactors." The Architect / Eng;neer was

- Sargent & Lundy, Incorporated, and the primary construction contractor was United Engineers &~ Constructors. The Mississippi River is the condenser cooling water source.

' The plant is subject to license numbers DPR-29 and DPR-30, issued October 1,1971, and March 21,1972, respectively; pursuant to Docket Numbers 50-254 and 50-265.

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The date of initial Reactor criticalities for Units One and Two, respectively were -

October 18,1971, and April 26,1972. Commercial generation of power began on February.18,1973 for Unit One and March 10,1973 for Unit Two.

This report was compiled by Lynne Hamilton and Debra Kelley, telephone number

. 309-654-2241, extensions 3114 and 2240, respectively.

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SUMMARY

OF OPERATING EXPERIENCE l

i A. Unit One  :

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' Quad Cities Unit One began the month of May with the reactor critical. The )

main generator was synchronized to the grid on May 1,~ 1999, at 6:05 a.m. On l May 21,1999, at 8:46 p.m., Unit 1 reactor auto-scrammed on Scram l Discharge Volume (SDV) hi-hi level. The reason for the scram was the  !

following: When the Reactor Wate'r Cleanup system was restarted, it caused '

one or more relief valves to lift at their setpoint of 1450 psig. The hot water from the relief valves flashed to steam in the lines going to the Reactor Building Equipment Drain Tank (RBEDT) and also flowed into the SDV drain lines connected to the RBEDT header lines. The put steam into the SDV, causing i the temperature sencing hi-hi level instruments to trip, which in turn caused the scram. On May 22,1999, startup activities commenced. On May 23,1999, at 5:41 a.m., Unit 1 went critical, and at 12:29 p.m., the generator was synchrontred to the grid. Unit One operated throughout the remainder of the month at full power with minor down power operations for routine maintenance and surveillance testing.

B.' Unit Two -

Quad Cities Unit Two began the month of May operating at full power, Unit ,

Two operated throughout the month at full power with minor down power ~ l operations for routine maintenance and surveillance testing.  ;

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111. OPERATING DATA STATISTICS A. Unit One Operating Data Report for May 1999 DOCKET NO.: 50-254 DATE: June 9,1999 COMPLETED BY: Lynne Hamilton TELEPHONE: (309) 654-2241 OPERATING STATUS 0000 050199

1. REPORTING PERIOD: 2400 053199 GROSS HOURS IN REPORTING PERIOD: 744
2. CURRENTLY AUTHORIZED POWER LEVEL (MWt): 2511 MAX > DEPEND > CAPACITY: 769 DESIGN ELECTRICAL RATING (MWe-NET): 789 THIS MONTH YEAR TO DATE CUMULATIVE
3. NUMBER OF HOURS REACTOR WAS CRITICAL 711.10 3108.60 179905.30
4. REACTOR RESERVE SHUTDOWN HOURS 0.00 0.00 3421.90
5. HOURS GENERATOR ON LINE 698.20 3073.20 174668.60
6. UNIT RESERVE SHUTDOWN HOURS 0.00 0.00 909.20
7. GROSS THERMAL ENERGY GENERATED (MWH) 1702734.00 7629966.00 383378460.60
8. GROSS ELECTRICAL ENERGY GENER'ATED (MWH) 555260.00 2493812.00 .124051155.00
9. NET ELECTRICAL ENERGY GENERATED (MWH) 528506.00 2377057.00 111674910.00 ,
10. REACTOR SERVICE FACTOR 95.58 85.80 75.63
11. REACTOR AVAILABILITY FACTOR 95.58 85.80 77.07
12. UNIT SERVICE FACTOR 93.84 84.82 73.43 l' 13. UNIT AVAILABILITY FACTOR 93.84 84.82 73.82
14. UNIT CAPACITY FACTOR (Using MDC) 92.37 85.32 61.05
15. UNIT CAPACITY FACTOR (Using Design Mwe) 90.03 83.16 59.51
16. UNIT FORCED OUTAGE RATE 0.00 0.00 6.97 5-TECllOPMRCJUNE99. DOC b

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IIL OPERATING DATA STATISTICS

B. Unit Two Operating Data Report for May 1999 DOCKET NO.: 50-265 DATE: June 9,1999 COMPLETED BY: Lynne Hamilton TELEPHONE: (309) 654-2241 OPERATING STATUS 0000 050199 1.- REPORTING PERIOD: 2400 053199 GROSS HOURS IN REPORTING PERIOD: 744
2. C!JRRENTLY AUTHORIZED POWER LEVEL (MWt): 2511 MAX > DEPEND > CAPACITY: 709 l

DESIGN ELECTRICAL RATING (MWe-NET): 789 THIS MONTH YEAR TO DATE CUMULATIVE

3. NUMBER OF HOURS REACTOR WAS CRITICAL 744.00 3424.80 173021.90
4. REACTOR RESERVE SHUTDOWN HOURS 0.00 0.00 2985.80
5. HOURS GENERATOR ON LINE 744.00 3400.30 168467.05
6. UNIT RESERVE SHUTDOWN HOURS 0.00 0.00 702.90 7, GROSS THERMAL ENERGY GENERATED (MWH) 1861517.52 8481749.28 369321832.14
8. GROSS ELECTRICAL ENERGY GENERATED (MWH) 603000.00 2749764.00 118498894.00
9. NET ELECTRICAL ENERGY GENERATED (MWH) 580036.00 2646748.00 112413792.00
10. REACTOR SERVICE FACTOR 100.00 94.53 73.22
11. REACTOR AVAILABILITY FACTOR 100.00 94.53 74.49
12. UNIT SERVICE FACTOR 100.00 93.85 71.29
13. UNIT AVAILABILITY FACTOR 100.00 93.85 71.59
14. UNIT CAPACITY FACTOR (Using MDC) 101.38 95.00 61.86 l 15. UNIT CAPACITY FACTOR (Using Design Mwe) 98.81 92.59 60.29
16. UNIT FORCED OUTAGE RATE 0.00 0.00 10.77 l

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IV. UNIT SHUTDOWNS l

A. Unit One Shutdowns for May 1999 DOCKET NO.: 50-254- l DATE: ' June 9,1999 l COMPLETED BY: Lynne Hamilton TELEPHONE: (309) 654-2241 No. ' DATE TYPE DURATION REASO METHOD OF CORRECTIVE F OR (HOURS) N SHUTTING ACTIONS / COMMENTS S DOWN l REACTOR {

99-02 990521 F 39.7 H 3 01F47 -When the RWCu system j was restarted, relief valves lifted, 3 flashing steam in lines going to l RBEDT and SDV drain lines. This put steam into the SDV causing temperature sensing hi-hi level instruments to trip, causing the scram.

Legend:

(1) Reason A- Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training /Ucense Examination F- Administrative G - Operational Error (Explain)

H - Other (Explain)

(2) Method 1 - Manual 2 - Manual Trip / Scram 3 - Automatic Trip / Scram 4 - Continuation 5 - Other (Explain)

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IV. UNIT SHilTDOWNS B. Unit Two Shutdowns for May 1999 DOCKET NO.: 50-265

' DATE: June 9,1999 COMPLETED BY: Lynne Hamilton TELEPHONE: (309) 654-2241 No. DATE TYPE DURATION REASO METHOD OF CORRECTIVE F OR 8 (HOURS) N . SHUTTING ACTIONSICOMMENTS DOWN REACTOR None for the Month of May.

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Legend:

(1) Reason A - Equipment Failure (Explain) )

B - Maintenance or Test C- Refueling -

D- Regulatory Restriction t E - Operator Training /Ucense Examination l F - Administrative j G - Operational Error (Explain)

H - Other (Explain) .

C) Method )

' 1 - Manual )

2 - Manual Trip / Scram 3 - Automatic Trip / Scram 4 - Continuation .

5 - Other (Explain)

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1 V.. AMENDMENTS TO FACILITY LICENSE OR TECHNICAL SPECIFICATIONS There were no Amendments to the Facility License or Technical Specifications for the reporting period.

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.VI. UNIQUE REPORTING REQUIREMENTS The following items are included in this report based on the requirements set forth in

- Technical Specification 6.9.A.5.

A. Main Steam Relief Valve Ooerations There were no Relief Valve Operations during the reporting period.

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