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Category:CORRESPONDENCE-LETTERS
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action ML20217F6321999-10-0707 October 1999 Forwards Insp Repts 50-254/99-01 & 50-265/99-01 on 990721- 0908.No Violations 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20212K9421999-10-0505 October 1999 Informs That NRC Accepts 990513 Inservice Inspection Relief Request CR-31 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage ML20212J0451999-09-21021 September 1999 Forwards Safety Evaluation of Licensee USI A-46 Program at Quad Cities Nuclear Power Station,Units 1 & 2,established in Response to GL 87-02 Through 10CFR50.54(f) Ltr ML20212D8231999-09-20020 September 1999 Informs That Effectieve 991101,NRC Region III Will Be Conducting Safety System Design & Performance Capability Pilot Insp at Quad Cities Nuclear Power Station.Insp Will Be Performed IAW NRC Pilot Insp Procedure 71111-21 ML20212C6961999-09-15015 September 1999 Forwards Insp Repts 50-254/99-17 & 50-265/99-17 on 990823- 0827.No Violations Noted SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20211Q7961999-09-0909 September 1999 Forwards Correction to Administrative Error on Page 8 of NRC Insp Repts 50-254/99-16 & 50-265/99-16,transmitted by Ltr, ML20211Q6511999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Quad Cities Operator License Applicants During Wk of 000327.Validation of Exam Will Occur at Station During Wk of 000306 ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211F8251999-08-25025 August 1999 Forwards Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Insp Evaluated Effectiveness of Maint Rule Program & Review Periodic Evaluation Specifically Required for 10CFR50.65 ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20211D1491999-08-19019 August 1999 Forwards Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22.Staff Identified Major Discrepancy Re Accuracy of Data Submitted to NRC for Protected Area Security Equipment Performance SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl ML20210T9941999-08-13013 August 1999 Forwards Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716.Violations Noted ML20210R7451999-08-13013 August 1999 Forwards Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NRC Identified Several Issues Which Were Categorized as Being of Low Risk Significance.Two Issues Involved NCVs of Regulatory Requirements SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated ML20210R9541999-08-10010 August 1999 Informs That During 990804 Telcon Between J Bartlet & M Bielby,Arrangements Were Made for NRC to Insp License Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210M5461999-08-0606 August 1999 Discusses 990804 Telcon Between J Bartlet & M Bielby,Where Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210L8371999-08-0202 August 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety Related Motor-Operated Valves ML20210M4691999-07-30030 July 1999 Forwards Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One NCV Was Identified & Discussed in Encl Insp ML20210H4661999-07-29029 July 1999 Forwards Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Insp Consisted of Selective Examination of Procedures & Representative Records, Observations of Activities & Interviews with Personnel SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20209B2081999-06-29029 June 1999 Discusses Closure of Response to RAI Re GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rvid,Version 2 Issued as Result of Review of Responses.Info Should Be Reviewed & Comments Submitted by 990901 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 ML20196F7921999-06-24024 June 1999 Forwards Meeting Summary,Nrc Meeting Handout & Licensee Handout from 990608 Meeting ML20196E7131999-06-23023 June 1999 Forwards Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20196E4821999-06-21021 June 1999 Discusses 990617 Meeting by Region III Senior Reactor Analysts (SRA) in Cordova,Il to Meet with PRA Staff to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA Staff 05000254/LER-1999-002, Forwards LER 99-002-00 IAW 10CFR50.73(a)(2)(iv).Listed Commitments Contained in LER1999-06-18018 June 1999 Forwards LER 99-002-00 IAW 10CFR50.73(a)(2)(iv).Listed Commitments Contained in LER 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period 05000254/LER-1999-002, Forwards LER 99-002-00 IAW 10CFR50.73(a)(2)(iv).Listed Commitments Contained in LER1999-06-18018 June 1999 Forwards LER 99-002-00 IAW 10CFR50.73(a)(2)(iv).Listed Commitments Contained in LER SVP-99-125, Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl1999-06-15015 June 1999 Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl ML20195E3491999-06-0707 June 1999 Withdraws Util Requesting License Change for Plant Security Plan Rev.Licensee Will re-evaluate Situation & May Request Approval of Change in Future ML20207G1451999-06-0707 June 1999 Forwards Rev 45 to Comed Quad Cities Nuclear Power Station Security Plan.Rev Includes Changes Listed.Security Plan Is Withheld from Public Disclosure Per 10CFR73.21 ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs SVP-99-105, Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 9905291999-05-20020 May 1999 Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 990529 ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB SVP-99-111, Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions1999-05-17017 May 1999 Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions SVP-99-098, Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i)1999-05-17017 May 1999 Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i) SVP-99-099, Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval1999-05-13013 May 1999 Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval SVP-99-096, Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 19991999-05-12012 May 1999 Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 1999 05000254/LER-1999-001, Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions1999-05-12012 May 1999 Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape SVP-99-108, Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 9903301999-04-30030 April 1999 Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 990330 SVP-99-036, Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions1999-04-29029 April 1999 Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions SVP-99-088, Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B1999-04-29029 April 1999 Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B ML20205T1141999-04-22022 April 1999 Provides Comments from Technical Review of Draft Info Notice Re Unanticipated Reactor Water Draindown at Quad Cities Nuclear Power Station,Unit 2,ANO,Unit 2 & JAFNPP ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 SVP-99-065, Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License1999-04-14014 April 1999 Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License SVP-99-058, Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations1999-04-14014 April 1999 Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations SVP-99-063, Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval1999-04-0909 April 1999 Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval JAFP-99-0129, Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick1999-04-0909 April 1999 Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick SVP-99-057, Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re1999-04-0505 April 1999 Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re SVP-99-062, Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-03-31031 March 1999 Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period SVP-99-025, Transmits Remediation Plan for Plant Intergranular Stress Corrosion Cracking Susceptible Welds,Per GL 88-01.Encl Includes Util Assessment of Recirculation Suction Valve, 1-0202-4A1999-03-31031 March 1999 Transmits Remediation Plan for Plant Intergranular Stress Corrosion Cracking Susceptible Welds,Per GL 88-01.Encl Includes Util Assessment of Recirculation Suction Valve, 1-0202-4A 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20065D0511990-09-17017 September 1990 Forwards Objectives & Scope of 901205 Emergency Plan Exercise ML20064A7091990-09-14014 September 1990 Forwards Endorsement 133 to Nelia Policy NF-187 & Endorsement 116 to Maelu Policy MF-54 ML20059F4891990-09-0404 September 1990 Forwards Listing of Changes,Tests & Experiments Completed During Month of Aug 1990 for Plant ML20059B9721990-08-28028 August 1990 Forwards Reactor Head & Upper Shell Insp Plan,Per 900419 Meeting.Insp Plan Does Not Encompass Uppermost shell-to- Shell Weld Due to Technological Limitations ML20059F0311990-08-27027 August 1990 Provides Schedule for Completion of Installation of Mods to Plants Reactor Water Level Instrumentation,Per Generic Ltr 84-23.Penetrations Will Be Installed During Outage 13 for Dresden & During Outage 12 for Quad-Cities ML20059E9531990-08-27027 August 1990 Forwards Summary of Fabrication History for Upper Reactor Vessel,Per 900419 Technical Meeting.Summary Indicates That Fabrication Mismatches,Considered to Be Significant for Development of Insp Plan,Identified at head-to-flange Weld ML20059C7201990-08-23023 August 1990 Forwards Effluent & Waste Disposal Semiannual Rept,Jan-June 1990 Gaseous Effluents-Summation of All Releases & Rev 8 to Quad-Cities Station Process Control Program for Processing of Radioactive Wet Waste ML20058P3481990-08-0909 August 1990 Forwards Summary of Fuel Performance,End of Cycle 10,May 1990. No Leakage or Fuel Failure Noted ML20058M8221990-08-0707 August 1990 Forwards Response to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions ML20058M8041990-08-0606 August 1990 Advises That W/Completion of Operator Training Program,Plant SPDS Meets Requirements Delineated in NUREG-0737,Suppl 1 ML20058M8591990-08-0606 August 1990 Forwards Rept of Metallurgical Exam That Revealed No Evidence of Defects,Porosity or Slag in Weld Overlay. Rept Responds to IGSCC Insp Performed on Facility IGSCC Susceptible Piping ML20058M4101990-08-0101 August 1990 Forwards Listing of Changes,Tests & Experiments Completed During Month of Jul 1990 for Plant ML20058M8291990-07-31031 July 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issue Resolved W/Imposition of Requirements of Corrective Actions. Status of Implementation of Generic Safety Issues Encl ML20055J1631990-07-26026 July 1990 Forwards Reactor Containment Bldg Integrated Leak Rate Test Quad-Cities Nuclear Power Station Unit 2,900427-28, & Related Apps Describing Type a Test,Per 10CFR50,App J, Section V.B.1.Next Test Scheduled for Fall 1991 ML20055H7631990-07-25025 July 1990 Forwards Financial Info Re Decommissioning of Plants ML20055G6331990-07-18018 July 1990 Responds to Generic Ltr 89-06 Re SPDS to Meet Requirements of Suppl 1 to NUREG-0737.SPDS Lesson Plan Incorporated Into Initial License Class Training Program ML17202L2861990-07-0202 July 1990 Forwards Dresden II Upper Vessel Contract Variation Review, La Salle II Upper Vessel Fabrication Summary & Quad-Cities II Upper Vessel Fabrication Summary. ML20055D4341990-06-29029 June 1990 Forwards Comm Ed Rept on Evaluation of Cracking in Quad- Cities Unit 2 Reactor Head, Per Commitment Made at 900419 Meeting W/Nrr.Rept Concludes That Cracks Caused by Interdendritic Stress Corrosion Cracking Mechanism ML20055D4741990-06-29029 June 1990 Forwards Annual FSAR Update for Quad-Cities Station ML20055C8551990-06-15015 June 1990 Forwards Special Neutron Attenuation Test for High Density Spent Fuel Racks (Wet), Final Rept.Rept Provides Results of Neutron Radioassay Measurement Program Conducted During Fall,1989 Refueling Outage ML20043D7661990-06-0404 June 1990 Responds to J Lieberman 900501 Ltr Re Rl Dickherber. Confidence in Dickherber Performance in Future for Nonlicensed Duties Can Be Based Upon Demonstrated Record of Good Past Performance ML20043D7691990-06-0404 June 1990 Responds to 900501 Ltr Re Work Hours for Dickherber.During Outage,Dickherber Worked Extended Hours Traditionally Associated W/Refueling Activities ML20043G4251990-06-0202 June 1990 Forwards Listing of Changes,Tests & Experiments Completed During May 1990 ML20043D3201990-06-0101 June 1990 Forwards Rev 24 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043B6681990-05-22022 May 1990 Forwards Proposed Changes to SER Re Hot Shutdown Repairs in Event of Fire,Per 10CFR50,App R Section Iii.G Covering Spurious Operations & High Impedance Faults & Electrical Isolation Deficiency ML20043A4681990-05-10010 May 1990 Forwards Proposed Changes to 880721 SER Re App R Section Iii.G Exemption for Fire Zones 1.1.1.1S & 1.1.1.2,southern & Northern Torus Level in Unit 1 Reactor Bldg Column & Unit 1 Reactor Bldg Elevations 623 Ft & 647 Ft ML20042H0011990-05-0303 May 1990 Forwards Listing of Changes,Tests, & Experiments Completed During Apr 1990 ML20042G3501990-05-0202 May 1990 Responds to NRC 900404 Ltr Re Violations Noted in Insp Repts 50-254/90-02 & 50-265/90-02.Corrective Actions:Continuous Fire Watch Initiated & Training Conducted on Procedure Rev ML20042F1181990-05-0101 May 1990 Advises of Listed Value for Secondary Containment,Per NRC Request for Addl Info Re LER 50-254/87-025.Value Based on Info Contained in Plant FSAR 05000254/LER-1950-254, Advises of Listed Value for Secondary Containment,Per NRC Request for Addl Info Re LER 50-254/87-025.Value Based on Info Contained in Plant FSAR1990-05-0101 May 1990 Advises of Listed Value for Secondary Containment,Per NRC Request for Addl Info Re LER 50-254/87-025.Value Based on Info Contained in Plant FSAR ML20042F0691990-05-0101 May 1990 Responds to Generic Ltr 83-28,Item 4.5.3 Re Reactor Protection Sys on-line Functional Test Intervals.Endorses Two BWR Owners Group Topical Repts NEDC-30844 & NEDC-30851P Generic Evaluations ML20042F1221990-05-0101 May 1990 Forwards Preliminary Rept of IGSCC Insp Results.Flaw Indication Detected in Weld Overlay Matl of Weld 02J-S3 & Removed by Boat Sample & Std Weld Overlay Thickness Restored.Final Rept Will Be Forwarded within 30 Days ML20042E4491990-04-11011 April 1990 Forwards Request for Rev to Previous NRC Exemption Approval on 860625 Re Combustible Load Values ML20042F0351990-03-23023 March 1990 Forwards Part 3 of 1989 Operating Rept.W/O Rept ML19330D5161990-03-14014 March 1990 Advises That Revs to Inservice Testing Program & Implementation Procedures Will Be Completed by 900629,per Generic Ltr 89-04 ML20012C0721990-03-0808 March 1990 Comments on SALP Board Repts 50-254/89-01 & 50-265/89-01 for Oct 1988 to Nov 1989.Util Appreciates NRC Recognition of Overall Improvements in Areas of Operation & Emergency Preparedness & Good Performance in Area of Security ML20012B5921990-03-0202 March 1990 Forwards Listing of Changes,Tests & Experiments Computed During Month of Feb 1990 for Plant ML20006F3361990-02-0808 February 1990 Responds to NRC Ltr 900110 Ltr Re Violations Noted in Insp Repts 50-254/89-25 & 50-265/89-25.Corrective Actions:Safety Evaluations Submitted Via 900116 Ltr & Table of Content Will Be Completed for 1989 FSAR Update to Be Submitted by 900630 ML20012A9551990-02-0808 February 1990 Responds to Violations Noted in Insp Repts 50-254/89-26 & 50-265/89-26.Corrective Action:Procedure Qis 47-1 Revised to Include Requirement That Equalizing Valve Be Open During Isolation of Transmitter ML20011E7131990-02-0606 February 1990 Forwards Reactor Containment Bldg Integrated Leak Rate Test,Quad Cities Nuclear Power Station,Unit 1,891114-15. Next Type a Test Scheduled for Fall 1990 ML20006E1721990-02-0202 February 1990 Forwards Listing of Changes,Tests & Experiments Completed During Jan 1990,including Items Completed in 1989. Interlocks Installed on Refuel Bridge Fuel Handling Machine to Prevent Raising Hoist While Hoist Loaded ML20006C5071990-01-30030 January 1990 Identifies Schedular Change for Completion of Corrective Actions Associated W/Human Engineering Deficiencies 159,187 & 489 Re Escutcheon Plates for Control Switches Which Need Replacement.Plates Will Be Replaced During Outages ML20006C7401990-01-22022 January 1990 Advises of Receipt of Accreditation Renewal by INPO in Sept 1989 for Operator Requalification Training Program,Per Generic Ltr 87-07 Requirements & Informs That Programs Developed Using Systematic Approach to Training ML19354E8591990-01-16016 January 1990 Responds to NRC 891128 Ltr Re Violations Noted in Insp Repts 50-254/89-17 & 50-265/89-17.Corrective Actions:Procedure NSWP-E-01, Electrical Cable Installation Insp, Will Be Revised to Enhance Human Factor Aspect ML19354D8131990-01-11011 January 1990 Forwards Corrected App C to Monthly Operating Rept for Dec 1989 for Quad Cities Units 1 & 2 ML20005F6441990-01-0303 January 1990 Forwards Listing of Changes,Tests & Experiments Completed During Dec 1989.Summary of Safety Evaluations Being Reported in Compliance w/10CFR50.59 & 10CFR50.71(e) Also Encl ML20005E1691989-12-22022 December 1989 Forwards Rev 22 to Security Plan,Reflecting Administrative Changes in Mgt Structure at Facility.Rev Withheld (Ref 10CFR73.21) ML20043A5741989-12-21021 December 1989 Responds to NRC 891124 Ltr Re Violations Noted in Insp Repts 50-254/89-23 & 50-265/89-23.Corrective Actions:Compressed Gas Cylinder Bottles Secured W/Chain & Fire Marshall Will Increase Tours of Plant Re Transient Combustible Matl ML20005E1211989-12-18018 December 1989 Forwards Final Rept of Fall 1989 IGSCC Insp Plan,Discussing Items Such as Overlay Repair on Weld 02G-S4,mechanical Stress Improvement & Piping Mods ML19332G3401989-12-0808 December 1989 Forwards Response to Generic Ltr 89-21, Implementation Status of USI Requirements. Actions to Resolve USI A-9 Re ATWS Will Be Completed in June 1990 & USI A-42 Re Pipe Cracks in BWRs Will Be Completed in Dec 1990 1990-09-04
[Table view] |
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4 r) Colninonwealth tidison One First National Plaza. Chicago,12nois s
Address Reply to: Post Omce Box 767 Chicago, Illinoa 60690 - 0767 July 24, 1986 l
Mr. James G. Keppler Regional Administrator U.S. Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Subject: Quad Cities Station Units 1 and 2 Response to Inspection Report Nos.
50-254/86-006 and 50-265/86-006 NRC Docket Nos. 50-254 and 50-265 Reference: April 18, 1986 letter from C. J. paperiello to Cordell Reed.
Dear Mr. Keppler:
The referenced letter transmitted the subject Quad Cities Inspection Report which addressed Integrated and Local Leak Rate Testing. Although no non-compliances were idt;ntified during this inspection, the referenced letter requested we provid* a response addressing our program for correcting j
repetitive local leak rate teilures. Our response is provided in the attachment in the form of Revision 1 to Licensee Event Report 86-001. This report describes our corrective action efforts.
i If you have any questions regarding this response, please contact i
this office.
Very tru, yours, L
& V-
'A:
D. L. Farrar Director of Nuclear Licensing im Attachment cc: NRC Resident Inspector - Quad Cities 860724 1894K 8607310121 PDR ADOCK 05000254 PDR JUL 2 51986 G
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LICENSEE EVENT REFORT (LER)
Pacility Name (1)
Dicket Numbir (2)
Paon (3) lof l8 OUAO-CITIES. NUCLEAR POWER STATION. UNIT 1 0!510101of21514 1
0 Title (4) Leak Rate From All Valves and Penetrations on Unit One in Excess of Technical specification Limit Event Date (5)
LER Number (6)
Recort Date (7)
Other Facilities Involved (8)
///j Revision Month Day Year Facility Names'I Docket Numberfs)
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Number
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Number Ol 51 01 01 Of I l 011 016 816 816
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0 1 0 {1
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0 l 1 017 019 816 01510101Of I l THIs REPORT !s SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR fCheck one or more of the followino) fil) 20.402(b) 20.405(c) 50.73(a)(2)(tv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) 22.405(a)(1)(11) 50.36(c)(2) 50.73(a)(2)(v11)
Other (specify LEVEL
!O 20.405(a)(1)(tit) 50.73(al(2)(1) 50.73(a)(2)(viii)(A) in Abstract below (101 0
0
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20.405(a)(1)(iv)
_X_ 50.73(a)(2)(11) 50.73(a)(2)(viii)(B) and in Text)
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20.405(a)(1)(v) 50.73(a)(2)(111) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
Name TELEPHONE NUMBER AREA CODE Nicos P. Diarindakis. Technical Staff Enoineer Ert. 2158 1 10l 9 615141-l2121 COMPLETE ONE LINE FOR EACH COM T FAILURE DESCRIBED IN THIS REPORT (13)
CAusE
system COMP 0NEMT MANuFAC-REPORTABLE
CAusE
SYSTEM COMPONENT MANUFAC-REPORTABLE TURER TO NPRDi_
TURER TO NPROS X
JlM l P!E IN Cl3 11 10 Y
B
$ lJ l Ils IV Cl6 18 14 B
SIJ l IIS IV Cf6 18 14 X
C lE l Ils IV Cl6 18 14 SUPPLEMENTAL REPORT EXPECTED (141 Expected Month l Day 1 Year submission X lyes (If vesmc.gm_21ete EXPECTED SUBMISSJQN_DATE)
X l N0 l
l l l
ABSTRACT (Limtt to 1400 spaces.1.e. approsimately fif teen single-space typewritten lines) (16)
On January 6, 1986, while performing Local Leak Rate Testing, the measured combined leakage rate for all Valves and Penetrations, except Main Steam Isolation Valves, was found to leak in excess of 293.75 SCFH (.060 La) which is allowed by the plant Technical Specifications.
Unit One was-shutdown for the end of cycle eight refueling and maintenance outage.
This report documents the repairs made to valves and penetrations with unacceptable leak rates and the final results of the local Leak Rate Testing program.
This report is submitted to you in accordance with the requirements of 10 CFR 50.73 (a)(2)(li), which requires the reporting of any event or condition that resulted in the condition of the nuclear power plant, including its principle safety barrier, being seriously degraded.
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"'a*O Unit One 01510IoIo121514 816 01011 0 11 012 OF 0l8 COMPLETE ONE LINE FOR EACM COGdPONENT FAILURE DESCR18ED IN THIS REPORT 113)
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' FACILITY NU4 (1)
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Number Quad Cities Unit 1 0 15l0 10 l0 l 21 51 4 8l6 Ol0l1 0 l 1 013 0F 0!8 TEXT
PLANT AND SYSTEM IDENTIFICATION
General Electric - Bolling Hater Reactor - 2511 MHt rated core thermal power.
Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
IDENTIFICATION OF OCCURRENCE:
Leak rate froa all valves and penetrations in excess of Technical Specification limit.
Discovery Date:
1-6-86 Report Date:
7-9-86 This report was initiated by Deviation Report D-4-1-86-5 CONDITIONS PRIOR TO OCCURRENCE:
SHUTDOWN Mode (l) - Rx Power 0% - Unit Load 0 MWe SHUTDOWN Mode (l) - In this position, a reactor scram is initiated power to the control rod drives is removed and the reactor protection trip systems have been deenergized for 10 seconds prior to permissive for manual reset.
DESCRIPTION OF OCCURRENCE:
At 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />, on January 6, 1986, Unit One was shutdown for end of cycle eight refueling and maintenance outage. While performing refueling outage Local Leak Rate Testing, the measured combined leakage rate for all Penetrations and Valves, except Main Steam Isolation Valves, was found to leak in excess of 293.75 SCFH (0.60 La)-
The following valves required repairs or adjustments (RA's).
Note that some of the RA's were not due to excessive leakage, but were the result of preventative maintenance.
The valve leakage before and after the RA's and an explanation of the work performed is provided in Table 1.
For valves where the RA's were initiated due to local leak rate test (LLRT) results, notes are shown in the comment section with details provided in the corrective action section of this report.
This report is being submitted to comply with the requirements of 10 CFR 50.73(a)(2)(11), which requires reporting of any event or condition that resulted in the condition of the nuclear power plant, including its principle safety barrier, being seriously degraded.
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LICENSEE EVENT REPORT fLER) TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER f61 Pace (3)
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Number Quad Cities Unit 1 0l 5 10 l0 10l 21 51 4 816 0l0 l 1 0 l1 014 0F Ol8 TEXT APPARENT CAUSE OF OCCURRENCE:
The first step to a good corrective action or maintenance program is to determine why the valve in question leaked.
The answer to that question is not always obvious t: hen dealing with valves that are sometimes quite large or when the air leakages are small but require repair due to regulatory limitations. At Quad Cities, we believe that we have a good program for diagnosing valve problems and facilitating repairs through the use of Station Procedure QMP 800-18 and the checklist QMP 800-S15. When any safety related and/or primary containment isolation valve is disassembled, a Quality Control inspector performs a thorough inspection of the valve in order to determine the root cause of the valve leakage (or any other problems mandating the repair). An additional inspection is performed during re-assembly of the valve.
He believe that this method of diagnostics and control on these types of repairs meet or exceed any prevailing standard within the industry.
In addition, Quad Cities maintains on file the LLRT results for every primary containment isolation valve and penetration dating back to plant startup and trends those results.
The station's willingness to repair valves or penetrations that exhibit low, but equipment specific high or increasing leakages over past LLRT results, demonstrates a sincere effort to meet the requirements of 10 CFR 50, Appendix J.
Because of the stringent testing requirements of the above regulation anri problems encountered industry-wide in meeting those requirements, the corrective action portion of this report has been prepared to identify " chronic" problems experienced at Quad-Cities. Actions taken in the past and future plans are discussed.
The specific action taken this refuel outage on all valves with RA's due to LLRT leakage is given below in Table The note numbers can be referenced back to Table I to identify the valves.
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Number Quad Cittes Unit 1 01510 1010 1 21 Sl 4 8l6 0 1011 0 l 1 015 0F 018 TEXT
CORRECTIVE ACTION
The immediate action taken for many of the RA's is sufficient corrective action because the leakages involved were small and no pattern of chronic failure exists.
The items of special concern, however, are valves that have a history of excessive leakage and/or large leakage rates.
These problems are identified as follows:
1)
All feedwater check valves (220-58A, B; 220-62A, B).
2)
Drywell floor drain sump and equipment drain sump isolation valves (A0 2001-3, 4, 15, and 16).
3)
HPCI Steam Exhaust Check Valve (2301-45).
4)
Drywell Head (X-4).
5)
Drywell Purge Butterfly Valves (1601-23, 24, 60).
The above problems will be discussed in detail here concerning future corrective actions required to prevent further recurrence.
1)
ALL FEEDWATER CHECK VALVES (220-58A, B; 220-62A, B)
The failure of these valves to give good LLRT results is well documented at Quad Cities and at other stations throughout the industry.
While modifications have been performed to reduce the potential of valve leakage (e.g.
modifications to the disc / seat assembly seals and hold down clamps),
the primary problem continues to be that these valves are intended to isolate a high pressure water line and we are testing them with low pressure air.
The test method does not include a wav to firmly seat the disc prior to testing.
The testing does not simulate either normal operating or accident conditions that would act to seat these valves, and normally the feedwater lines would not act as a leakage path because they are water filled.
While other stations, with NRC approval, have attempted to use water ar.d/or water / air mixtures to seat the valves prior to tcsting with air, Quad Cities has not found this t-shnique to be effective.
The quantity of water that can be introduced into a 18-inch line through a 1-inch test tap does not seem to affect closure of the valve, and at times can be counter-productive by washing rust and dirt into the seat.
The water velocity that can be developed seems inadequate to either move the disc or keep the surface free of crud.
While the station continues in its efforts to develop a better maintenance program and test procedure for this valve, we believe that the problem is to a great extent generic with these particular valves.
Unfortunately, recent industry experience with a newly designed dual seat valve offered by Anchor Darling Corp. has not been totally successful as documented in NRC IE Bulletins.
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Quad Cities Unit 1 0l5 1 0 l 0 l 0 1 21 51 4 8 l6 O l0 11 0 11 Ol6 0F 018 TEXT The station has initiated an Action Item Request (AIR NO. 85-12) to Station Nuclear Engineering Department (SNED) to investigate this problem and determine a solution.
2)
ORYWELL DRAIN SUMP VALVES (A0 2001-3, 4, 15, 16)
In the past, these valves have had trouble passing local leak rate tests.
It was discovered that the position of these valves was the cause of these failures.
The original design had the valves installed in the inverted position and the air operators were positioned below the valves.
This affected the ability of the air operator to tightly seat the valve which adversely affected the ability of these valves to perform well during local leak rate test.
To correct this problem Modifications M-4-l(2e-83-7 (floor drains) and M-4-1(2)-83-19 (equipment drains) were performed to upright the valves and operators. Modification M-4-1-83-7 was performed this refueling outage.
This modification uprighted vavles A0-2001-3 and 4.
Inis corrective action should prevent recurrence of LLRT failure.
The failure of A0-2001-16 was due to gasket and packing degredation.
This is not considered chronic problem.
No further corrective action is required.
3)
HPCI STEAM EXHAUST VALVE (2301-45)
There is an existing AIR to SNED to investigate a replacement for this valve.
The station does not feel that the Mission Duo Check valve is the best choice for this application.
Further engineering will be performed to determine if a more suitable valve is available, or if modifications to the existing valves will make them more reliable.
4)
DRYWELL HEAD (X 4)
Quad Cities One has had repeated LLRT failures of the drywell head o-rings.
The drywell head o-rings were made by J-Bar Inc., compound No. 2405.
Nuclear Services Technical has recommended that 0-rings made by Garlock (#8364) be installed. Another Commonwealth Edison Station has been using the Garlock material and have had success with their drywell head local leak rate tests.
Garlock o-rings were installed per the recommendation by Nuclear Services Technical.
Also, special care was taken during re-installation of the drywell head to ensure proper alignment.
0393H l
LICENSEE EVENT REPORT (LER) T[XT CONTINUATION
'ACILITY NAME (1)
DOCKET CUMBER (2)
LER NUMBER (6) paae (3)
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Quad Cities Unit 1 0 l 5 10 l0 10l 21 SI 4 8 I6 010 l1 O l1 017 0F 018 TEXT 5)
DRYWELL PURGE BUTTERFLY VALVES As was stated in the previous section, these valves have experienced two previous LLRT failures.
The causes of the previous failures and of the most recent failures are not considered to be due to a chronic problem, however the station has noted and is concerned that the "as-left" leakage of these valves (over the past six years) has been increasing.
The valves listed below will be disassembled during the next refuel outage for seat inspection and repair or replacement as necessary:
A0 1601-23 A0 1601-24 A0 1601-60 ANALYSIS OF OCCURRENCE:
The consequence of this occurrence is that it was necessary to repair a number of containment isolation valves to bring the ccmbined measured leak rate below the Technical Specification limit prior to resuming power operaton.
Exceeding the Technical Specification limit does not pose any significant risks or hazards to public safety because the total leakage determined by Type B and C tests does not, in any way, represent a probable leakage from the containment under accident conditions.
There are a number of factors which prevent totaling Type 3 and C test results to obtain a probable containment leakage.
First, many of the Type C tests are performed by pressurizing the volume between isolation valves in series.
While the Local Leak Rate Test (LLRT) does give the total leakage for both valves, the maximum (torst case) leakage one would expect from the containments could occur when both valves leak equally.
Therefore, the probable containment leakage would be no more than half of the LLRT total for both valves, and, in fact, the leakage could be zero if all the LLRT measured leakage was through only one of the valves.
Second, a number of Type C tests are performed on valves in series with other individually tested isolation valves.
In this situation, the worst case probable containment leakage would be the minimum of the two LLRT results, not the total of the two.
Third, there are also cases where the test boundary for the Type C test consists of three or more isolation valves.
In this situation, if the LLRT result shows that only one valve repair is required, the LLRT result following the repair would be the torst possible leakge for any other valve on the boundary.
Thus, the "as left" LLRT result would also be the " worst case" leakage from the containment prior to the repair.
Fourth, Type B tests, which tests penetrations and double gasketed seals, test two sealing surfaces, one from the pressurized volume to the Primary Containment and another from the pressurized volume to the Secondary Containment.
in this case, the " worst case" leakage would be half of the LLRT result.
0393H
LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (3)
LER NUMBER f61 Pace f3)
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Nym_her Ouad cities Unit 1 015 10 l0 10 l 2l 51 4 8 l 6 O l0 l 1 0 l1 018 0F 018 TEXT The " worst case" total leakage path calculation as described is still not a true measure of expected leakge during accident conditions.
For example, a number of Type C tests are performed on systems which would, under most accident scenarios, be filled with water and pressurized (e.g. Reactor Feedwater and RHRS).
These valves, thile they may represent a substantial portion of the total measured leakge for Type B and C testing, would contribute nothing to a radiological release under most accident conditions.
In addition to Primary Containment, other engineering safeguards are designed to mitigate the consequences of a radiological release during accident conditions.
These systems are the Emergency Core Cooling System (ECCS), the Emergency Diesel Generators [EK], the Secondary Containment, the Standby Gas Testment System [BH],
and the Off-Gas [WF) " hold-up" piping and chimney.
FAILURE DATA:
Previous leak rate failures are documented in LERs 254/84-002 and 265/85-007.
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TABLE 1 LEAKAGE (SCFH)
DESCRIPTION
VALVE NO.
COMPONENT DESCRIPTION AS FOUND AS LEFT COMMENTS "B" Reactor Feedwater CV-220-58B Crane Tilting Disc CV 750.1 0.0 Note 1 Table 2 "B" Reactor Feedwater CV-220-62B Same as Above 1937.0 0.0 Note 2 Table 2 1
Table 2 j
Cleanup Suction MO-1201-2 6 inch Crane Gate Would Not Pressuirze 21.45(c)
Note 3 (783-UL)
Cleanup Suction M0-1201-5 Same as Above Would Not Pressuirze 21.45(c)
Note 3 Table 2 Drycell/ Torus Purge A0-1601-23 Pratt 18 inch Butterfly 207.0 (c) 63.0(c)
Note 4 Table 2 Exhaust (D 1200G) s Drywell/ Torus Purge A0-1601-60 Same as Above 207.0(c) 63.0(c)
Note 4 Table 2 Exhaust j
Drywell Floor Drain A0-2001-3 3 inch Crane Gate 75.13 9.0(c)
Note 5 Table 2 Sump (D1200G)
Drycell Floor Drain A0-2001-4 Same as Above 18.0 9.0(c)
Note 6 Table 2 Sump Drywell Equipment A0-2001-16 Same as Above Would Not Pressurize 0.9(c)
Note 7 Table 2 Drain Sump HPCl Steam Supply M0-2301-4 10 inch Crane Gate 151.9 (c) 22.46 (c)
Note 8 Table 2 (783-U)
IIPCI Steam Supply M0-2301-5 Same as Above 151.9 (c) 22.46 Note 8 Table 2 HPCI Steam Exhaust CV-2301-45 24 inch Mission Duo Check Would Not Pressurize 0.0 Note 9 Table 2 Oxygen Analyzer A0-8801D Blaw-Know 3/4 inch Globe 12.5 0.0 Note 10 Table 2 Valve TIP Ball Valve 733-1 General Pneumatics Corp 0.5 0.9 Retested After (608 KWJ06-3)
Preventative Maintenance i
ih80H
TABLE 1 (continu:d)
LEAKAGE (SCFH)
DESCRIPTION
VALVE NO.
COMPONENT DESCRIPTION AS FOUND AS LEFT CO M NTS l
TIP Ball Valve 733-2 Same as Above 0.0 0.1 Same as Above TIP Ball Valve 733-3 Same as Above 0.25 0.8 Same as Above TIP Ball Valve 733-4 Same as Above 0.0 0.9 Same as Above TIP Ball Valve 733-5 Same as Above 0.0 0.0 Same as Above ACAD System CV-2599-23A Hancock Swing Check 0.3 2.3 Retested After (1-5580W-1-XNC062)
Maintenance Not Due to Leakage Dry = ell Head X-4 Chicago Bridge and Iron Would Not Pressurize 0.0 Note 11 Table 2 Dry: ell Head X-4 Chicago Bridge and Iron 1.4 0.0 Retested After i
Preventative Maintenance NOTE:
"(c)" denotes the combined leakage of all the valves in the test boundary.
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1 0580H
TABLE 2 NOTE NO.
DISCUSSION 1
Work Request No. Q47066.
Repairs to feedwater check valve (CV-220-588) included installing new pins and new bushings.
The condition of the old pins and bushings were causing the valve to seat' improperly.
Leakage History:
Feedwater Check Valve'(CV-220-588) 12-31-70 2.49 SCFH 4-25-74 888.20 SCFH 6-25-74 2.99 SCFH 1-8-76 3026.0 SCFH 1-12-76 5.38 SCFH 3-8-76 13.44 SCFH 4-2-77 10.4 SCFH 1-20-79 4.4 SCFH 9-5-80 5.39 SCFH 9-8-82 Could not pressurize 12-3-82 24.64 SCFH 3-26-84 Could not pressurize 6-21-84 0.0 SCFH 1-14-86 750.1 SCFH 3-5-86 0.0 SCFH Conclusion:
The feedwater check valves are large, 18" check valves on the feedwater lines and have an erratic test history.
The main reason for this is that the valve does not seat when tested with 48 PSIG of air. All feedwater check valves are considered a chronic problem.
Reference the corrective action section of this report.
0581H
TABLE 2 (Continued)
NOTE NO.
DISCUSSION 2
Work Request No. Q47052. Some small pieces of scale and crud were discovered on the seating surface. Valve was cleaned and re-assembled.
Leakage History:
Feedwater Check Valve (CV-220-628) 12-31-70 5.63 SCFH 4-25-74 1332.00 SCFH 6-25-74 11.10 SCFH 1-10-76 3040.00 SCFH 2-4-76 14.46 SCFH 4-1-77 2.22 SCFH 1-20-79 2558 SCFH 1-26-79 4.4 SCFH 10-14-80 17.76 SCFH 09-08-82 104.5 SCFH 12-08-82 23.9 SCFH 3-26-84 563.8 SCFH 5-24-84 0.0 SCFH 1-13-86 1937.0 SCFH 2-14-86 0.0 SCFH Conclusions:
Same as for CV-220-588 0581H
i TABLE 2 (Continued)
NOTE NO.
DISCUSSION 3
Work Request No. Q47878.
The inspection of the cleanup suction (M0-1201-2) valve showed that the stellite on the disc had cracks.
The old stellite was machined off and new stellite was welded on.
Work Request No. Q46529. Valve 1201-5 was repacked due leakage visually observed during plant operation.
Leakage History: Volume Boundary M0-1201-2 and M0-1201-5 12-31-70 0.033 SCFH 7-14-74 9.10 SCFH 1-26-76 2.48 SCFH 4-5-77 5.75 SCFH 2-1-79 0.0 SCFH 10-31-80 5.75 SCFH 09-30-82 14.87 SCFH 12-08-82 1.8 SCFH 5.16-84 5.0 SCFH 1-28-86 Would Not Pressurize 3-15-86 21.45 SCFH Conclusions: The leakage history of these valves do not indicate a chronic problem with leakage.
No further action is required.
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.=
TABLE 2 (Continued)
NOTE NO.
DISCUSSION 4
Work Request No. 048234.
Repairs on A0-1601-60 consisted of an adjustment of the valve disc.
Work Request No. Q48235.
Repairs on A0-1601-23 consisted of an adjustment of the valve disc.
Drywell/ Torus Purge Exhaust Leakage History: Volume Boundary - A0-1601-23, 24, 60, 61, 62, 63 12-31-70 0.38 SCFH 4-30-73 5.50 SCFH 4-22-74 5.50 SCFH 1-5-76 5.40 SCFH 4-12-77 4.5 SCFH 2-16-79 45 SCFH 2-18-79 14.2 SCFH 11-2-80 9.0 SCFH 10-17-82 9.0 SCFH 3-23-84 81.0 SCFH 3-27-84 27.0 SCFH 2-19-86 207.0 SCFH 3-19-86 63.0 SCFH Conclusions: There has been one other LLRT failure due to valve disc alignment on these valves.
There has been one LLRT failure due to a failed packing.
These failures are not considered to be due to a chronic problem.
Reference the corrective action section of this repcrt for additional infomation.
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0581H
TABLE 2 (Continued)
NOTE NO.
DISCUSSION 5
Work Request No. Q47924. A0-2001-3 was disassembled and the valve disc and seats were lapped.
Drywell Floor Drain Sump Valves Leakage History: Volume Boundary - A0-2001-3, 4 12-31-70 0.497 SCFH 4-12-74 4.00 SCFH 1-5-76 8.85 SCFH 3-24-77 2.6 SCFH 1-30-79 26.0 SCFH 2-2-79 1.85 SCFH 9-23-80 0.65 SCFH 10-20-82 1.1 SCFH 3-17-83 0.0 SCFH 4-2-84 75.6 SCFH 7-20-84 0.3 SCFH 2-26-86 3-75.13 SCFH, 4 = 18.0 SCFH 3-21-86 9.00 SCFH After Mod
The leakage history of valves A0 2001-3, 4, 15 and 16 have shown some leakage problems in the past.
Reference the corrective action section of this report.
- Modification is addressed in corrective action section of this report.
'0581H
- - - ~
TABLE 2 (Continued)
NOTE NO.
DISCUSSION 6
Work Request No. Q48558. A0 2001-4 was disassembled and the valve disc was lapped.
Drywell Floor Drain Sump Valves Leakage History: Volume Boundary - A0-2001-3, 4 12-31-70 0.497 SCFH 4-12-74 4.00 SCFH 1-5-76 8.85 SCFH 3-24-77 2.6 SCFH 1-30-79 26.0 SCFH 2-2-79 1.85 SCFH 9-23-80 0.65 SCFH 10-20-82 1.1 SCFH 3-17-83 0.0 SCFH 4-2-84 75.6 SCF,.
7-20-84 0.3 SCFH 2-26-86 3 - 75.13 SCFH, 4 - 18.0 SCFH 3-21-86 9.00 SCFH After Mod
- Conclusion: The leakage history of valves A0 2001-3, 4, 15, and 16 have shown some leakage problems in the past.
Reference the corrective action section of this report.
- Modification is addressed in the corrective action section of this report.
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0581H
TABLE 2 (Continued) 4 NOTE NO.
DISCUSSION 7
Work Request No. Q48039. A0 2001-16 was disassembled and the stem packing and bonnet gasket were replaced.
Drywell Equipment Orain Sump Valves Leakage History: Volume Boundary A0 2001-15, 16 12-31-70 0.522 SCFH 5-3-74 1.34 SCFH 1-5-76 10.37 SCFH 3-24-77 4.65 SCFH 2-2-79 2.85 SCFH 9-23-80 4.75 SCFH 10-20-82 0.9 SCFH 4-10-84 16.2 SCFH 7-21-84 3.2 SCFH After Mod
> 60.0 SCFH 3-17-86 0.9 SCFH Conclusions: Stem packing and bonnet gasket failures are not' considered chronic problems with these valves.
Reference the corrective action sction of this report for corrective action that has already been taken on these valves.
- Modification is addressed in the corrective action section of this report.
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TABLE 2 (Continued)
NOTE NO.
DISCUSSION 8
Work Request No. Q44649. M0 23J1-4 was repacked.
Work Request No. Q48189. M0 2301-5 was repacked.
HPCI Steam Supply Valves Leakage History: Volume Boundary M0 2301-4, 5 12-31-70 0.15 SCFH 5-24-74 1.43 SCFH 1-15-76 4.03 SCFH 3-20-77 3.47 SCFH 1-19-79 0.0 SCFH 8-31-80 5.185 SCF:1 9-6-82 3.46 SCFH 3-7-84 1.2 SCFH 7-21-84 0.0 1-7-86 151.9 SCFH 3-17-86 22.46 SCFH Conclusions:
These valves do not have a chronic problem.
N6 further action is required.
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0581H l
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TABLE 2 (Continued)
NOTE NO.
DISCUSSION 9
Work Request No. Q46386 and Modification M-1-85-68.
This valve is a Mission Duo Check on the HPCI turbine exhaust.
The inspection on this Valve showed damage to the rubber seat.
The valve was new in July, 1984.
The valve.was replaced this outage with a very similar valve.
Leakage History:
12-31-70 0.83 SCFH 4-16-74 4.03 SCFH 1-4-76 84.42 SCFH 1-4-76 12.86 SCFH 3-22-77 16.3 SCFH 1-19-79 190.3 SCFH 2-5-79 0.0 SCFH 8-31-80 4.02 SCFH 09-07-82 Could Not Pressurize 12-07-72 0.80 SCFH 3-12-84 Unable to Pressurize 7-13-74 4.0 SCFH 1-9-86 Could Not Pressurize 3-14-86 0.0 SCFH Conclusions: The life expectancy of this vavle appears to be approximately 1 or 2 cycles.
Because of the severe damage found during valve inspections and problems encountered in the industry with these valves used for this application, this is considered a chronic problem.
Reference the corrective action section of this report.
0581H
TABLE 2 (Continued)
NOTE NO.
DISCUSSION 10 Work Request No. 48040. A0 88010 was repacked.
Leakage History: 02 Analyzer Valve A0 8801-0 6-27-84 0.095 SCFH 1-4-76 1.77 SCFH 3-31-77 1.1 SCFH 2-3-79 0.1 SCFH 9-9-80 0.4 SCFH 9-13-82 0.2 SCFH 3-14-84 1.5 SCFH 2-27-86 12.5 SCFH 3-19-86 0.0 SCFH Conclusions: This valve does not have a chronic problem.
No further action is required.
A 0581H
TABLE 2 (Continued)
NOTE NO.
DISCUSSION 11 Work Request No.
45207.
The drywell head 0-rings were replaced with a Garlock Material.
Inspection showed o-ring degredation and potential head flange mis-alignment.
Leakage History:
12-31-70 0.0 SCFH 7-15-74 4.73 SCFH 4-18-75 0.00 SCFH 1-3-76 0.00 SCFH 5-7-77 0.00 SCFH 1-18-79 30 SCFH 2-18-79 0.0 SCFH 12-17-80 0.0 SCFH 09-06-82 Could Not Pressuirze 12-15-82 0.0 SCFH 3-7-84 30 SCFH 7-23-84 0.0 SCFH 1-6-86 Could Not Pressurize 3-15-86 0.0 SCFH Conclusions: The leakage history of the drywell head shows repeated failures.
This is considered a chronic problem.
Reference the corrective action section of this report.
4 0581H we
r SHEET 7 EVENT SUXMARY REV.1 4/86 A"ND VR Number PGK Of-1-E4rQQS CAESE CODES Ldst generation Reactor trip NRC violation, level ___
Cost > $25,000 ESF actuation GSEP event, class _____
Hazard or Spill z
NRC reportable Tech Spec LCO Personnel injury X
LER Potential or future loss Component PSE Failure mode type Denartment i
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f Commonwealth Edison ouad Cities Nuclear Power Station 22710 206 Avenue Nonh Corcova. Illinois 61242 Telephome 309/65 & 2241 RLB-86-102 July 10, 1986 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555
Reference:
Quad Cities Nuclear Power Station Docket Number 50-254, DPR-29, Unit One Enclosed please find Licensee Event Report (LER)86-001, Revision 01, for Quad Cities Nuclear Power Station.
This report is submitted to you in accordance with the requirements of the Code of Federal Regulations, Title 10, Part 50.73 (a)(2)(11), which requires reporting of any event or condition that resulted in the condition of the nurlear power plant, including its principle safety barrier, being sericusly degraded.
The original Licensee Event Report (LER)86-001 stated that the Local Leak Rate Testing (LLRT) program had found leakage in excess of Technical Specification limits, but did not provide a complete summary pending completion of the testing program and corrective actions.
This report addresses all valves and penetrations that had repairs performed to reduce the leakage total to within the Technical Specification limit.
Respectfully, COMMONWEALTH EDISON COMPANY Quad Cities Nuclear Power Station bb R. L. Bax Station Manager RLB/MSK/dak Encl.
cc:
J. Hojnarowski A. Madison INP0 Records Center NRC Region III 0581H
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05000265/LER-1986-001, :on 860103,at 97% Power,Group I Isolation & Subsequent Reactor Scram Occurred.Caused by Air Hose Breaking Loose & Striking Instrument Rack Due to Failure of Hose Connection |
- on 860103,at 97% Power,Group I Isolation & Subsequent Reactor Scram Occurred.Caused by Air Hose Breaking Loose & Striking Instrument Rack Due to Failure of Hose Connection
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-001-02, :on 860106,during Shutdown,Discovered That Measured Combined Leakage Rate for All Penetrations & Valves Except MSIVs in Excess of 293.75 Scfh.Cause Undetermined. Corrective Action Delayed Until Rept Completed |
- on 860106,during Shutdown,Discovered That Measured Combined Leakage Rate for All Penetrations & Valves Except MSIVs in Excess of 293.75 Scfh.Cause Undetermined. Corrective Action Delayed Until Rept Completed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-001, Responds to NRC Re Violations Noted in Insp Repts 50-254/86-06 & 50-265/86-06.Corrective Actions:Response to Repetitive Local Leak Rate Failures Provided in Encl Rev 1 to LER 86-001 | Responds to NRC Re Violations Noted in Insp Repts 50-254/86-06 & 50-265/86-06.Corrective Actions:Response to Repetitive Local Leak Rate Failures Provided in Encl Rev 1 to LER 86-001 | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000254/LER-1986-002, :on 860107,during Shutdown,Discovered That Three MSIVs Leaked in Excess of 11.5 Scfh Limit.Cause Undetermined.Leaks Will Be Repaired Before Startup |
- on 860107,during Shutdown,Discovered That Three MSIVs Leaked in Excess of 11.5 Scfh Limit.Cause Undetermined.Leaks Will Be Repaired Before Startup
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-002-02, :on 860107,while Performing MSIV Local Leak Rate Tests During Shutdown for Refueling & Maint,Valves AO 1-203-2A,2B & 2C Found W/Excess Leakage.Caused by Equipment Failure.Repairs Performed |
- on 860107,while Performing MSIV Local Leak Rate Tests During Shutdown for Refueling & Maint,Valves AO 1-203-2A,2B & 2C Found W/Excess Leakage.Caused by Equipment Failure.Repairs Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-002-02, :on 860117,Dec 1985 Monthly Grab Sample of Reactor Bldg Vent Stack Gaseous Effluent for Tritium Analysis Not Obtained.Caused by Personnel Error.Personnel Instructed |
- on 860117,Dec 1985 Monthly Grab Sample of Reactor Bldg Vent Stack Gaseous Effluent for Tritium Analysis Not Obtained.Caused by Personnel Error.Personnel Instructed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-003, :on 860102,diesel Generator 1/2 Cooling Water Pump Discovered Inoperable Due to Removal of Circuit Breaker Control Power Fuses.Caused by Human Factors Design Error. Labeling Clarified |
- on 860102,diesel Generator 1/2 Cooling Water Pump Discovered Inoperable Due to Removal of Circuit Breaker Control Power Fuses.Caused by Human Factors Design Error. Labeling Clarified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-003-07, :on 860303,HPCI Sys Declared Inoperable.Caused by Error in Routing HPCI Gland Exhauster Drain Piping. Temporary Drain Line Installed & Mod Initiated to Replace Drain Line |
- on 860303,HPCI Sys Declared Inoperable.Caused by Error in Routing HPCI Gland Exhauster Drain Piping. Temporary Drain Line Installed & Mod Initiated to Replace Drain Line
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-004-06, :on 860314,HPCI Turbine Tripped Due to Turbine Exhaust Pressure Switch 2-2368A Failure.Caused by Corroded Seals in Pressure Switch Allowing Moisture in Casing.Switch Replaced |
- on 860314,HPCI Turbine Tripped Due to Turbine Exhaust Pressure Switch 2-2368A Failure.Caused by Corroded Seals in Pressure Switch Allowing Moisture in Casing.Switch Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-004, :on 860119,reactor Scram Occurred Due to Atws/Alternate Rod Insertion Sys Initiation.Caused by Deficiency in Procedure Used to Drain Vessel.Procedure Revised |
- on 860119,reactor Scram Occurred Due to Atws/Alternate Rod Insertion Sys Initiation.Caused by Deficiency in Procedure Used to Drain Vessel.Procedure Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000000/LER-1986-005-03, Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points | Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points | | 05000265/LER-1986-005-07, :on 860404,fuel Pool Radiation Monitor Spiked High Causing Reactor Bldg Ventilation Sys to Isolate & Standby Gas Treatment Sys to Start.Caused by Contaminated Trash on Refuel Floor.Trash Moved |
- on 860404,fuel Pool Radiation Monitor Spiked High Causing Reactor Bldg Ventilation Sys to Isolate & Standby Gas Treatment Sys to Start.Caused by Contaminated Trash on Refuel Floor.Trash Moved
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-005, :on 860118,fuel Pool Radiation Monitor 1B Spiked High,Isolating Reactor Bldg Vent Sys & Starting Standby Gas Treatment Sys.Caused by Electronic Interference. Signal Cable Will Be Rerouted |
- on 860118,fuel Pool Radiation Monitor 1B Spiked High,Isolating Reactor Bldg Vent Sys & Starting Standby Gas Treatment Sys.Caused by Electronic Interference. Signal Cable Will Be Rerouted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-006, :on 860122,reactor Bldg Ventilation Sys Isolation Occurred as Result of Spurious Trip of Reactor Bldg Ventilation Monitor 1B.Caused When Disconnected Signal Cable Resulted in Spike |
- on 860122,reactor Bldg Ventilation Sys Isolation Occurred as Result of Spurious Trip of Reactor Bldg Ventilation Monitor 1B.Caused When Disconnected Signal Cable Resulted in Spike
| | 05000265/LER-1986-006-07, :on 860414,fuel Pool Radiation Monitor 2A Tripped,Causing Isolation of Reactor Bldg Ventilation Sys & auto-initiation of Standby Gas Treatment Sys.Caused by Instrument Setpoint Drift |
- on 860414,fuel Pool Radiation Monitor 2A Tripped,Causing Isolation of Reactor Bldg Ventilation Sys & auto-initiation of Standby Gas Treatment Sys.Caused by Instrument Setpoint Drift
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-007, :on 860409,core Spray Room Cooler 2B Would Not Run in Either Manual or Automatic Mode.Caused by Pitting & Burning of Contacts on Motor Control Ctr Contactor.Failed Contactor Replaced |
- on 860409,core Spray Room Cooler 2B Would Not Run in Either Manual or Automatic Mode.Caused by Pitting & Burning of Contacts on Motor Control Ctr Contactor.Failed Contactor Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-007-06, :on 860409,discovered That Core Spray Room Cooler 2B Inoperable.Caused by Pitting & Burning of Contacts on Motor Control Ctr Contactor That Supplies Power to Room Cooler Motor.Contactor Replaced |
- on 860409,discovered That Core Spray Room Cooler 2B Inoperable.Caused by Pitting & Burning of Contacts on Motor Control Ctr Contactor That Supplies Power to Room Cooler Motor.Contactor Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-007-01, :on 860203 & 13,phase a Differential Current Relay on Bus 13-1 Tripped & Actuated Lockout Relay.Probably Caused by Spurious Actuation Due to Vibration.Mod Initiated to Replace Relays W/Relays Less Sensitive |
- on 860203 & 13,phase a Differential Current Relay on Bus 13-1 Tripped & Actuated Lockout Relay.Probably Caused by Spurious Actuation Due to Vibration.Mod Initiated to Replace Relays W/Relays Less Sensitive
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-007, Responds to NRC Re Violations Noted in Insp Repts 50-254/87-09 & 50-265/87-09 on 870407-09.Corrective Actions: LER 86-007-00 for Unit 2 Will Be Supplemented to Describe More Fully Root Cause,Investigation & Corrective Actions | Responds to NRC Re Violations Noted in Insp Repts 50-254/87-09 & 50-265/87-09 on 870407-09.Corrective Actions: LER 86-007-00 for Unit 2 Will Be Supplemented to Describe More Fully Root Cause,Investigation & Corrective Actions | | 05000254/LER-1986-008-04, :on 860325,1/2 Diesel Generator Received auto- Start Signal Resulting in Diesel Generator Running Unloaded. Caused by Relay Inadvertently Contacted During Maint. Corrective Actions Unnecessary |
- on 860325,1/2 Diesel Generator Received auto- Start Signal Resulting in Diesel Generator Running Unloaded. Caused by Relay Inadvertently Contacted During Maint. Corrective Actions Unnecessary
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-008-01, :on 860525,while Unit Operating in Run Mode, Core Spray Sys Room Cooler 2-5748A Discovered W/Frayed Belts & Core Spray Room Cooler 2A Declared Inoperable.Caused by Normal Wear of Belts.Belts Replaced |
- on 860525,while Unit Operating in Run Mode, Core Spray Sys Room Cooler 2-5748A Discovered W/Frayed Belts & Core Spray Room Cooler 2A Declared Inoperable.Caused by Normal Wear of Belts.Belts Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-008-07, :on 860525,core Spray 2A & 2B Room Coolers Declared Inoperable Due to Frayed Belts on Core Spray Sys Room Cooler 2-5748A & Diesel Generator Trip.Caused by Normal Belt Wear.Belts Replaced |
- on 860525,core Spray 2A & 2B Room Coolers Declared Inoperable Due to Frayed Belts on Core Spray Sys Room Cooler 2-5748A & Diesel Generator Trip.Caused by Normal Belt Wear.Belts Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-009-01, :on 860211,scram Occurred from Scram Discharge Instrument Vol High Level.Caused by Personnel Error Due to Inadequate Awareness of Sys Status.Crd Scram Valves Will Be Checked for Leakage During Startup |
- on 860211,scram Occurred from Scram Discharge Instrument Vol High Level.Caused by Personnel Error Due to Inadequate Awareness of Sys Status.Crd Scram Valves Will Be Checked for Leakage During Startup
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000265/LER-1986-009, :on 860626,drive Belts on Core Spray Room Cooler 2B Broke & Remaining Belt Came Off Pulleys.Caused by Normal Operational Wear.Belts Replaced.Verification of Belts Performed Daily |
- on 860626,drive Belts on Core Spray Room Cooler 2B Broke & Remaining Belt Came Off Pulleys.Caused by Normal Operational Wear.Belts Replaced.Verification of Belts Performed Daily
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000254/LER-1986-010, :on 860211,Group II & III Isolations Occurred, During Hfa Relay Replacement.Caused by Personnel Error.Work Packages for Future Hfa Relay Replacements Will Be Written to Prevent Recurrence |
- on 860211,Group II & III Isolations Occurred, During Hfa Relay Replacement.Caused by Personnel Error.Work Packages for Future Hfa Relay Replacements Will Be Written to Prevent Recurrence
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-010-07, :on 860627,RWCU Sys Isolated,Resulting in Closure of Valves MO-2-1201-2,-5 & -80 & clean-up Pump Trip. Caused by Short in HX Outlet Temp Switch & Personnel Error. Personnel Counseled |
- on 860627,RWCU Sys Isolated,Resulting in Closure of Valves MO-2-1201-2,-5 & -80 & clean-up Pump Trip. Caused by Short in HX Outlet Temp Switch & Personnel Error. Personnel Counseled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-011, :on 860214,discovered That Undervoltage Relay in Position AB on Bus 13-1 Tripped at 2,870 Volts Ac Below Limit.Caused by Instrument Setpoint Drift.Relay Recalibr |
- on 860214,discovered That Undervoltage Relay in Position AB on Bus 13-1 Tripped at 2,870 Volts Ac Below Limit.Caused by Instrument Setpoint Drift.Relay Recalibr
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-011-08, :on 860907,standby Liquid Control Sys Failed to Provide Flow to Test Tank While Performing Qos 1100-6.Caused by Disc on Loop Throttling Valve Separating from Valve Stem Due to Broken Tack Weld.Stem & Disk Replaced |
- on 860907,standby Liquid Control Sys Failed to Provide Flow to Test Tank While Performing Qos 1100-6.Caused by Disc on Loop Throttling Valve Separating from Valve Stem Due to Broken Tack Weld.Stem & Disk Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-012, :on 860221,standby Gas Treatment Sys a Started & Reactor Bldg Ventilation Sys Isolated.Caused by Disconnected Power Supplier for Fuel Pool & Reactor Bldg Ventilation Monitor 1B.Personnel Cautioned |
- on 860221,standby Gas Treatment Sys a Started & Reactor Bldg Ventilation Sys Isolated.Caused by Disconnected Power Supplier for Fuel Pool & Reactor Bldg Ventilation Monitor 1B.Personnel Cautioned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-012-08, :on 861006,during Full Power Instrument Maint, Reactor Water Level Transient Resulted in Reactor Scram. Caused by Personnel Error.Event Will Be Discussed W/Maint Dept Personnel |
- on 861006,during Full Power Instrument Maint, Reactor Water Level Transient Resulted in Reactor Scram. Caused by Personnel Error.Event Will Be Discussed W/Maint Dept Personnel
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000265/LER-1986-013, :on 861011,leakage of MSIV AO 2-203-2D in Excess of 11.5 Std Cubic Ft Per Hour Discovered.Caused by Normal Operational Wear.Valve Body Reseated.Pilot Seats Lapped.Stem & Piston Ring Replaced |
- on 861011,leakage of MSIV AO 2-203-2D in Excess of 11.5 Std Cubic Ft Per Hour Discovered.Caused by Normal Operational Wear.Valve Body Reseated.Pilot Seats Lapped.Stem & Piston Ring Replaced
| | 05000254/LER-1986-013, :on 860310,ATWS Trip Received.Caused by Valving Error by Instrument Mechanics Performing Test Due to Inadequate Communications Between Mechanics.Drain Valve Tags on Instrument Rack Will Be Replaced |
- on 860310,ATWS Trip Received.Caused by Valving Error by Instrument Mechanics Performing Test Due to Inadequate Communications Between Mechanics.Drain Valve Tags on Instrument Rack Will Be Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000265/LER-1986-014, :on 861012,while Performing Refuel Outage Local Leak Rate Testing,Measured Combined Leakage for Penetrations & Valves,Except Msivs,Found to Be in Excess of Tech Spec Limit.Caused by Wear or Design Deficiency |
- on 861012,while Performing Refuel Outage Local Leak Rate Testing,Measured Combined Leakage for Penetrations & Valves,Except Msivs,Found to Be in Excess of Tech Spec Limit.Caused by Wear or Design Deficiency
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000254/LER-1986-014, :on 860312,Nov 1985 Monthly Particulate Samples for Main Chimney & Reactor Bldg Vent Sys Lost & Science Applications Intl Corp (SAI) Could Not Locate Samples.Sai No Longer Offsite Lab |
- on 860312,Nov 1985 Monthly Particulate Samples for Main Chimney & Reactor Bldg Vent Sys Lost & Science Applications Intl Corp (SAI) Could Not Locate Samples.Sai No Longer Offsite Lab
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000265/LER-1986-015-08, :on 861013,leakage from Containment Exceeded 75% of La Required by Tech Spec 3.7.A.2.b.Caused by Reduced Resiliency of Silicon Rubber Mfg by J-Bar Silicon Corp. Silicon Rubber Replaced |
- on 861013,leakage from Containment Exceeded 75% of La Required by Tech Spec 3.7.A.2.b.Caused by Reduced Resiliency of Silicon Rubber Mfg by J-Bar Silicon Corp. Silicon Rubber Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-015, :on 860312,reactor Scrammed from Scram Discharge Vol Hi Level Signal & Reactor Protection Sys Bus Power Feed Transfer.Caused by Procedure Deficient in Cautioning Loss of Bypass Capability |
- on 860312,reactor Scrammed from Scram Discharge Vol Hi Level Signal & Reactor Protection Sys Bus Power Feed Transfer.Caused by Procedure Deficient in Cautioning Loss of Bypass Capability
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-016, :on 860317,following Core Spray Logic Functional Test Qms 700-5,diesel Generator auto-started & Ran Unloaded.Caused by Inadvertent Contact W/Sensitive Relays.Corrective Action Unnecessary |
- on 860317,following Core Spray Logic Functional Test Qms 700-5,diesel Generator auto-started & Ran Unloaded.Caused by Inadvertent Contact W/Sensitive Relays.Corrective Action Unnecessary
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000265/LER-1986-017-08, :on 861105,while Unit Shut Down for Refueling, Visual Insp Revealed Recirculation (AD) Weld Area W/Water Seeping from Small Crack.Caused by Igscc.Further Analysis Being Performed |
- on 861105,while Unit Shut Down for Refueling, Visual Insp Revealed Recirculation (AD) Weld Area W/Water Seeping from Small Crack.Caused by Igscc.Further Analysis Being Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-017, :on 860318,several ATWS Trips Occurred.Caused by Isolated Instrument Root Valves & Open Drywell Penetration X-49 & Instrument Lines Due to Personnel Error |
- on 860318,several ATWS Trips Occurred.Caused by Isolated Instrument Root Valves & Open Drywell Penetration X-49 & Instrument Lines Due to Personnel Error
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-018, :on 860320,reactor Protection Sys Channel B Tripped,Resulting in Full Scram.Caused by Spiking of Intermediate Range Monitors 15 & 18.Monitor 15 Cable Replaced & Monitor 18 Will Be Replaced |
- on 860320,reactor Protection Sys Channel B Tripped,Resulting in Full Scram.Caused by Spiking of Intermediate Range Monitors 15 & 18.Monitor 15 Cable Replaced & Monitor 18 Will Be Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-019, :on 860317,ATWS/alternate Rod Insertion Trip Occurred.Caused by Scaffolding,Erected to Install Fire Protection Mods,In Contact W/Instrument Sensing Lines. Scaffolding Rearranged |
- on 860317,ATWS/alternate Rod Insertion Trip Occurred.Caused by Scaffolding,Erected to Install Fire Protection Mods,In Contact W/Instrument Sensing Lines. Scaffolding Rearranged
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000254/LER-1986-020, :on 860328 & 0402,during Refueling Outage, Spurious Group I Isolation Signals Received.Caused by Instrument Rack Vibration Due to Personnel Error.Personnel Reminded to Take Precautions |
- on 860328 & 0402,during Refueling Outage, Spurious Group I Isolation Signals Received.Caused by Instrument Rack Vibration Due to Personnel Error.Personnel Reminded to Take Precautions
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-021, :on 860405,during Startup,Reactor Scram Occurred.Caused by Failure of Min Flow Feedwater Regulator Valve Due to Leakage Through Valve Seat.Valve Will Be Disassembled & Repaired |
- on 860405,during Startup,Reactor Scram Occurred.Caused by Failure of Min Flow Feedwater Regulator Valve Due to Leakage Through Valve Seat.Valve Will Be Disassembled & Repaired
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-022, :on 860501,containment Atmosphere Monitoring Sys Piping Lines Found Not Meeting NUREG-0661 Acceptance Criteria.Caused by Preservice Design Error.Action Item Record 4-85-10 Issued |
- on 860501,containment Atmosphere Monitoring Sys Piping Lines Found Not Meeting NUREG-0661 Acceptance Criteria.Caused by Preservice Design Error.Action Item Record 4-85-10 Issued
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-022-02, :on 860501,containment Atmosphere Monitoring Lines Exceeded Code Stress Requirements of NUREG-0661 for Mark I Containment Design.Caused by Inadequate Drawing Design Control for Listed Mods.Lines Modified |
- on 860501,containment Atmosphere Monitoring Lines Exceeded Code Stress Requirements of NUREG-0661 for Mark I Containment Design.Caused by Inadequate Drawing Design Control for Listed Mods.Lines Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000254/LER-1986-023, :on 860505,RCIC Sys Turbine Tripped Numerous Times on Mechanical Overspeed.Caused by Mechanical Overspeed Trip Linkage Out of Adjustment.Linkage Adjusted & Partly Machined |
- on 860505,RCIC Sys Turbine Tripped Numerous Times on Mechanical Overspeed.Caused by Mechanical Overspeed Trip Linkage Out of Adjustment.Linkage Adjusted & Partly Machined
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000254/LER-1986-024-03, :on 860811,RHR Svc Water Supports Exceeded Allowable Stress During Safe Shutdown Earthquake Loading. Caused by Inadequate Design Control.Rhr Svc Water Supports Modified |
- on 860811,RHR Svc Water Supports Exceeded Allowable Stress During Safe Shutdown Earthquake Loading. Caused by Inadequate Design Control.Rhr Svc Water Supports Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-025-03, :on 860827,certain Small Bore Torus Attached Piping Not within Allowable Operability Limits.Caused by Inadequate Design Review.Piping Support Hangers Will Be Modified |
- on 860827,certain Small Bore Torus Attached Piping Not within Allowable Operability Limits.Caused by Inadequate Design Review.Piping Support Hangers Will Be Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000254/LER-1986-025-01, :on 860827,small Bore Torus Attached Piping Not Meeting FSAR Requirements Discovered.Caused by Inadequate Design Review.Mod Issued to Correct Remaining Mark I Issues for Small Bore Piping |
- on 860827,small Bore Torus Attached Piping Not Meeting FSAR Requirements Discovered.Caused by Inadequate Design Review.Mod Issued to Correct Remaining Mark I Issues for Small Bore Piping
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000000/LER-1986-026, Advises That Two Addl Events Discovered Re Issues Identified in 861129 Inerting Event at Dresden Unit 2.LER 86-026-00 & LER 86-039-00 Re Events Encl.Guidance Re Application of Tech Spec Section 3.0.A & 3.0.3 Under Development.W | Advises That Two Addl Events Discovered Re Issues Identified in 861129 Inerting Event at Dresden Unit 2.LER 86-026-00 & LER 86-039-00 Re Events Encl.Guidance Re Application of Tech Spec Section 3.0.A & 3.0.3 Under Development.W/O Encl | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
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