|
---|
Category:Letter
MONTHYEAR05000265/LER-2024-002-01, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-10-30030 October 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure SVP-24-065, Offsite Dose Calculation Manual (ODCM) Section 12.2.2 Radioactive Gaseous Effluent Monitoring Instrumentation Report Main Chimney High Range Noble Gas Monitor2024-10-29029 October 2024 Offsite Dose Calculation Manual (ODCM) Section 12.2.2 Radioactive Gaseous Effluent Monitoring Instrumentation Report Main Chimney High Range Noble Gas Monitor IR 05000254/20240102024-10-28028 October 2024 Age Related Degradation Inspection Report 05000254/2024010 and 05000265/2024010 and Notice of Violation RS-24-080, Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in .2024-10-16016 October 2024 Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in . RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests SVP-24-059, Correction to Registration of Use of Casks to Store Spent Fuel2024-10-0404 October 2024 Correction to Registration of Use of Casks to Store Spent Fuel ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24247A1642024-09-30030 September 2024 Alternative Request RP-01 IR 05000254/20244022024-09-12012 September 2024 Material Control and Accounting Program Inspection Report 05000254/2024402 and 05000265/2024402 (Public) SVP-24-054, Deviation from BWR Vessel and Internals Project (BWRVIP) Guidelines - Inspection of Top Guide Rim Welds2024-09-11011 September 2024 Deviation from BWR Vessel and Internals Project (BWRVIP) Guidelines - Inspection of Top Guide Rim Welds ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000254/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Quad Cities Nuclear Power Station (Report 05000254/2024005; 05000265/2024005) RS-24-078, Alternative Request RV-08, Revision 1, Associated with Safety Relief Valve Testing Interval2024-08-20020 August 2024 Alternative Request RV-08, Revision 1, Associated with Safety Relief Valve Testing Interval ML24183A1082024-08-0808 August 2024 – Issuance of Amendment Nos. 302 and 298 Adoption of Tstf-505, Provide Risk Informed Extended Completion Times – RITSTF Initiative 4b SVP-24-049, Owners Activity Report Submittal Sixth 10-Year Interval 2024 Refueling Outage Activities2024-08-0707 August 2024 Owners Activity Report Submittal Sixth 10-Year Interval 2024 Refueling Outage Activities IR 05000254/20243012024-08-0101 August 2024 NRC Initial License Examination Report 05000254/2024301; 05000265/2024301 SVP-24-048, Registration of Use of Casks to Store Spent Fuel2024-07-31031 July 2024 Registration of Use of Casks to Store Spent Fuel 05000265/LER-2024-002, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-07-22022 July 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions SVP-24-041, Regulatory Commitment Change Summary Report2024-07-0505 July 2024 Regulatory Commitment Change Summary Report SVP-24-043, Registration of Use of Casks to Store Spent Fuel2024-07-0505 July 2024 Registration of Use of Casks to Store Spent Fuel ML24162A0982024-07-0303 July 2024 – Issuance of Amendment Nos. 301 and 297 Adoption of 10 CFR 50.69 Risk Informed Categorization and Treatment of Structures, Systems, and Components for Nuclear Power Reactors SVP-24-040, Registration of Use of Casks to Store Spent Fuel2024-06-25025 June 2024 Registration of Use of Casks to Store Spent Fuel RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations SVP-24-039, Ile Post Exam Package Letter2024-06-12012 June 2024 Ile Post Exam Package Letter RS-24-053, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed2024-06-0606 June 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed ML24110A0492024-05-28028 May 2024 Audit Report Related to the TSTF-505 and 10 CFR 50.59 Amendments ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 ML24142A3352024-05-21021 May 2024 Quad Cities—Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes ML24141A2102024-05-20020 May 2024 Operator Licensing Examination Approval - Quad Cities Nuclear Power Station, May 2024 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000254/20240012024-05-14014 May 2024 Integrated Inspection Report Nos. 05000254/2024001 and 05000265/2024001 SVP-24-034, Annual Radiological Environmental Operating Report2024-05-10010 May 2024 Annual Radiological Environmental Operating Report 05000265/LER-2024-001, Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing2024-05-10010 May 2024 Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing RS-24-042, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion2024-05-10010 May 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion RS-24-046, 10 CFR 50.46 Annual Report2024-05-0606 May 2024 10 CFR 50.46 Annual Report ML24109A0662024-05-0202 May 2024 – Relief Request I5R-26, Revision 0 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests SVP-24-028, Independent Spent Fuel Storage Installation Annual Radioactive Effluent Release Report2024-04-26026 April 2024 Independent Spent Fuel Storage Installation Annual Radioactive Effluent Release Report SVP-24-029, Radioactive Effluent Release Report for 20232024-04-26026 April 2024 Radioactive Effluent Release Report for 2023 ML24114A1712024-04-23023 April 2024 State of Illinois (IEMA-OHS) Comment Quad Cities HI-STORM Exemption Environmental Assessment IR 05000254/20245012024-04-0505 April 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000254/2024501 and 05000265/2024501 RS-24-032, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion2024-04-0505 April 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion SVP-24-024, Corrected Radioactive Effluent Release Report for 20222024-04-0505 April 2024 Corrected Radioactive Effluent Release Report for 2022 RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report SVP-24-023, Ile Outline Submittal Letter2024-03-29029 March 2024 Ile Outline Submittal Letter RS-24-019, Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Completion Times TSTF2024-03-19019 March 2024 Response to Request for Additional Information Related to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Completion Times TSTF ML23340A1552024-03-15015 March 2024 – Issuance of Amendment Nos. 299 and 295 Adoption of TSTF-564, Safety Limit MCPR RS-24-020, Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 for Quad Cities Nuclear Power Station - Holtec MPC-68MCBS2024-03-15015 March 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 for Quad Cities Nuclear Power Station - Holtec MPC-68MCBS SVP-24-018, Ile Proposed Exam Submittal Letter2024-03-13013 March 2024 Ile Proposed Exam Submittal Letter 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000265/LER-2024-002-01, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-10-30030 October 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure 05000265/LER-2024-002, Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure2024-07-22022 July 2024 Turbine Trip and Automatic Scram Due to Digital EHC Power Supply Intermittent Failure 05000265/LER-2024-001, Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing2024-05-10010 May 2024 Automatic Actuation of Reactor Protection System During Scram Discharge Volume Leak Rate Testing 05000265/LER-2023-001-01, Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level2023-11-30030 November 2023 Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level 05000265/LER-2023-001, Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level2023-10-10010 October 2023 Turbine Trip and Automatic Reactor Scram Due to High Moisture Separator Level SVP-22-072, Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level2022-12-30030 December 2022 Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level 05000265/LER-2022-002, Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level2022-09-0101 September 2022 Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level 05000254/LER-2022-003, Both Trains of Standby Gas Treatment Inoperable Due to Blockage in the Common Discharge Line2022-09-0101 September 2022 Both Trains of Standby Gas Treatment Inoperable Due to Blockage in the Common Discharge Line 05000254/LER-2022-002, Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue2022-07-0808 July 2022 Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue 05000265/LER-2022-001, Electromatic Relief Valve 3B Did Not Actuate Due to Incorrectly Oriented Plunger Well Plastic Guides2022-05-20020 May 2022 Electromatic Relief Valve 3B Did Not Actuate Due to Incorrectly Oriented Plunger Well Plastic Guides 05000254/LER-2022-001, Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction2022-01-26026 January 2022 Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction 05000254/LER-2017-0042018-01-0505 January 2018 Unit 1 HPCI Did Not Trip Due to Wear Debris in the Turbine Stop Valve Oil Resetting Solenoid, LER 17-004-00 For Quad Cities Nuclear Power Station, Unit 1 re: Unit 1 HPCI Did Not Trip Due to Wear Debris in the Turbine Stop Valve Oil Resetting Solenoid 05000254/LER-2017-0032017-11-17017 November 2017 Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue, LER 17-003-00 for Quad Cities, Unit 1, Regarding Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue 05000265/LER-2017-0012017-07-13013 July 2017 High Pressure Coolant Injection Minimum Flow Valve Failed to Open, LER 17-001-00 for Quad Cities, Unit 2, Regarding High Pressure Coolant Injection Minimum Flow Valve Failed to Open 05000254/LER-2017-0022017-05-26026 May 2017 Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded, LER 17-002-00 for Quad Cities, Unit 1, Regarding Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded 05000254/LER-2017-0012017-03-22022 March 2017 Secondary Containment Interlock Doors Opened Simultaneously, LER 17-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Interlock Doors Opened Simultaneously 05000265/LER-2016-0022016-06-24024 June 2016 High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak, LER 16-002-00 for Quad Cities Nuclear Power Station Unit 2 - RE: High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak 05000265/LER-2016-0012016-05-19019 May 2016 Main Steam Isolation Valve Local Leak Rate Tests Exceed Technical Specification Limits, LER 2016-001-00 for Quad Cities Nuclear Power Station, Unit 2 Regarding Main Steam Isolation Valve Local Leak Rate Tests Exceed Technical Specification Limits 05000254/LER-2016-0022016-03-14014 March 2016 Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Pump Rm), LER 16-002-00 for Quad Cities Units 1 and 2, Regarding Secondary Containment Different Pressure Momentarily Lost due to Air Failure (RWCU pump Rm) 05000254/LER-2016-0012016-03-10010 March 2016 Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm), LER 16-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm) 05000254/LER-2015-0102016-02-0505 February 2016 Loss of Control Room Emergency Ventilation System Due to Differential Pressure Switch Failure, LER 15-010-00 for Quad Cities, Unit 1, Regarding Loss of Control Room Emergency Ventilation System Due to Differential Pressure Switch Failure SVP-03-036, LER 03-S01-00, Security Event Report for Quad Cities, Unescorted Protected Area Access Granted Based on Falsified Information and Inadequate Screening Caused by a Failure of Administrative Controls.2003-03-0303 March 2003 LER 03-S01-00, Security Event Report for Quad Cities, Unescorted Protected Area Access Granted Based on Falsified Information and Inadequate Screening Caused by a Failure of Administrative Controls. ML17252B4771976-09-15015 September 1976 LER 76-059-00 for Dresden, Units 2 and 3 Re Review of Quad-Cities Unusual Event Letter Led to Discovery That Dresden'S Standby Gas Treatment System Deviated from Single Failure Criteria That Disabled the SBGT System ML18348A2401976-08-0606 August 1976 LER 1976-027-00, Reportable Occurrence of Control Rods for Quad-Cities, Unit 1 ML18348A2391976-08-0404 August 1976 LER 1976-026-00, Reportable Occurrence of Control Rods for Quad-Cities, Unit 1 2024-07-22
[Table view] |
LER-2022-001, Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction |
Event date: |
|
---|
Report date: |
|
---|
Reporting criterion: |
10 CFR 50.73(a)(2)(v), Loss of Safety Function |
---|
2542022001R00 - NRC Website |
|
text
Exelon Generation
SVP-22-004 10 CFR 50.73
January 26, 2022
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555
Quad Cities Nuclear Power Station, Unit 1 Renewed Facility Operating License No. DPR-29 NRC Docket No. 50-254
Subject: Licensee Event Report 254/2022-001-00 "High Pressure Coolant Injection System Inoperable due to Gland Seal System Malfunction"
Enclosed is Licensee Event Report 254/2022-001-00 "High Pressure Coolant Injection System Inoperable due to Gland Seal System Malfunction," for Quad Cities Nuclear Power Station, Unit 1.
This report is submitted in accordance with 10 CFR 50. 73(a)(2)(v)(D) for an event or condition that could have prevented the fulfillment of a safety system needed to mitigate the consequences of an accident.
There are no regulatory commitments contained in this letter.
Should you have any questions concerning this report, please contact Sherrie Grant at (309) 227-2800.
Respectfully,
Brian Wake Site Vice President Quad Cities Nuclear Power Station
cc: Regional Administrator-NRC Region Ill NRC Senior Resident Inspector - Quad Cities Nuclear Power Station
Abstract
On December 1, 2021, Unit 1 was at 100% power with a High Pressure Coolant Injection (HPCI) surveillance in progress. HPCI was declared inoperable at 1809 per the surveillance instructions. With HPCI running at rated speed, Main Control Room alarms were received for the HPCI Gland Exhauster at 1843. At 1847, Operators in the plant reported smoke and acrid odors from cubicles at a Motor Control Center (MCC) associated with Unit 1 HPCI and the Gland Exhauster. Operations aborted the surveillance and placed HPCI in Trip/Latch, and subsequently closed steam supply isolation valves to HPCI making it unavailable for automatic operation.
The causes of this event are the failure of a level switch in the HPCI Gland Seal Condenser (GSC) Hotwell and a failed thermal overload for the HPCI Gland Exhauster motor. Immediate corrective actions were to electrically isolate the faulted Gland Exhauster and to restore the system to a normal standby line up. Subsequent actions included replacement of the level switch and thermal overload.
This report is being submitted in accordance with 10 CFR 50.73(a)(2)(v)(D) for an event or condition that could have prevented the fulfillment of a safety system needed to mitigate the consequences of an accident.
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power
Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
EVENT IDENTIFICATION
High Pressure Coolant Injection System Inoperable due to Gland Seal System Malfunction
CONDITION PRIOR TO EVENT
Unit: 1 Event Date: December 1, 2021 Event Time: 1847 CST
Reactor Mode: 1 Mode Name: Run Power Level: 100%
No structures, systems or components were inoperable at the start of this event that contributed to the event.
A. DESCRIPTION OF EVENT
On December 1, 2021, Unit 1 was operating at 100% power. Unit 1 High Pressure Coolant Injection (HPCl)[BJ] quarterly operability testing was in progress and had progressed to the point where Unit 1 HPCI was declared INOPERABLE at 1809.
At 1843, the Main Control Room (MCR) received a HPCI MOTOR OVERLOAD alarm, indicating a motor overload condition for the Unit 1 HPCI Gland Exhauster. At 1847, Operators in the plant reported smoke and acrid odor coming from multiple cubicles at 250VDC MCC [EJ] 1A. (This Motor Control Center (MCC) is the power supply for the Unit 1 HPCI Gland Exhauster.) Concurrently, Operators in the Unit 1 HPCI Room reported acrid odor and smoke coming from the vicinity of the Unit 1 HPCI Front Standard.
Unit 1 operators aborted the surveillance, and the Unit Supervisor directed Unit 1 HPCI taken to 'Trip/Latch' at 1847 hours0.0214 days <br />0.513 hours <br />0.00305 weeks <br />7.027835e-4 months <br />. By placing Unit 1 HPCI in 'Trip/Latch', the system was in a condition that could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident; therefore, this condition is reportable per 10 CFR 50.72(b)(3)(v)(D). An Event Notification Sheet (ENS) #55619 was transmitted to the NRC at 2358.
Steam supply to HPCI was also isolated at 1853. The Gland Exhauster was electrically isolated, supply steam was reestablished and the HPCI stand-by lineup was completed by 2110. HPCI was declared operable at 2110. HPCI was unavailable for automatic initiation for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 27 minutes.
The Unit 1 Reactor Core Isolation Cooling (RCIC) system and the Unit 1 Automatic Depressurization System (ADS) remained Operable throughout the event. There was no impact on the health and safety of the public or plant personal.
B. CAUSE OF EVENT
The cause of the event was attributed to two equipment malfunctions: a failed level switch in the Unit 1 HPCI Gland Seal Condenser Hotwell, and a failed thermal overload for the Unit 1 HPCI Gland Exhauster motor.
The high-level limit switch in the Gland Seal Condenser (GSC) Hotwell suffered age-related degradation which resulted in a failure of the Unit 1 HPCI GSC Condensate pump to actuate on high level. As water level increased in the Unit 1 HPCI GSC, water eventually impinged on the Unit 1 HPCI Gland Exhauster and overloaded the associated motor. Under these high current conditions, the Unit 1 Gland Exhauster's motor (located in the Unit 1 HPCI Room) and the associated motor overloads (located in a cubicle at 250VDC MCC 1A) underwent thermal events that generated a significant quantity of smoke and acrid odor.
Continued operation of the Unit 1 HPCI Turbine under these conditions could have presented an industrial safety hazard to plant personnel in the vicinity of the Turbine or the MCC 1A. This hazard was eliminated by tripping Unit 1 HPCI Turbine and preventing a subsequent initiation while personnel were in the immediate vicinity.
C. SAFETY ANALYSIS
System Design
The HPCI system is designed to ensure that adequate core cooling takes place for all break sizes less than those for which Low Pressure Coolant Injection (LPCI) or Core Spray systems can adequately protect the core without assistance from other engineered safety features. Based on previous analysis the HPCI system's safety-related mission time is 10-minutes.
The purpose of the HPCI GSC sub-system is to draw away non-condensable gases and condensate from the HPCI turbine rotor and valve seals during initial start-up and to keep steam from being leaked into the HPCI room from the turbine shaft seals. Per previous system assessment, the HPCI turbine can run without a GSC. However, if the GSC were not in operation while the turbine is running, a small amount of steam could leak from the turbine shaft seals into the HPCI room and increase the HPCI room temperature.
Safety Impact
The safety significance of this event is minimal. At the time of the event, Unit 1 was at full power in a normal electric plant lineup with all other means of Reactor Coolant Injection available. Prior to the faults seen with the Unit 1 HPCI GSC sub-system, the Unit 1 HPCI Turbine had already demonstrated
the ability to meet pressure and flow requirements to perform its required safety-related function within the required time. In the event of a line break less than those requiring LPCI or Core Spray, Unit 1 HPCI would have been able to generate adequate pressure and flow with manual operator action in the Main Control Room. Automatic initiation of HPCI would not have been possible during this event (i.e.,
during the time Unit 1 HPCI was in "Trip/Latch"). The only impact present was to workers in the immediate vicinity of leaking steam or smoke.
This event is considered a Safety System Functional Failure per NEI 99-02, Revision 7.
D. CORRECTIVE ACTIONS
Immediate:
- 1. Operations electrically isolated the faulted HPCI Gland Exhauster.
- 2. Operations restored Unit 1 HPCI to OPERABLE by placing the system in a normal standby lineup at 2110 on 12/1/2021.
Follow up:
- 1. Replace the faulted level switch for the Unit 1 HPCI Gland Seal Condenser Condensate Pump.
(Complete)
- 2. Replace the faulted motor overloads for the Unit 1 HPCI Gland Exhauster. (Complete)
E. PREVIOUS OCCURENCES
The station events database, LERs and INPO Industry Reporting Information System (IRIS) were reviewed for similar events at Quad Cities Nuclear Power Station. This event was caused by equipment failures causing operations to isolate the HPCI system. No previous occurrences were identified.
F. COMPONENT FAILURE DATA
Level Switch Manufacturer: Magnetrol Nomenclature: Tuffy Level Switch Model/Part Number: 039-5000-400
Thermal Overload Relay Manufacturer: Eaton I QualTech NP Nomenclature: Coil, Overload Model/Part Number: H1029
|
---|
|
|
| | Reporting criterion |
---|
05000265/LER-2022-001, Electromatic Relief Valve 3B Did Not Actuate Due to Incorrectly Oriented Plunger Well Plastic Guides | Electromatic Relief Valve 3B Did Not Actuate Due to Incorrectly Oriented Plunger Well Plastic Guides | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2022-001, Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction | Regarding High Pressure Coolant Injection System Inoperable Due to Gland Seal System Malfunction | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000265/LER-2022-002, Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level | Manual Scram Due to Feedwater Regulator Valve Failure Decreasing Reactor Water Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000254/LER-2022-002, Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue | Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000254/LER-2022-003, Both Trains of Standby Gas Treatment Inoperable Due to Blockage in the Common Discharge Line | Both Trains of Standby Gas Treatment Inoperable Due to Blockage in the Common Discharge Line | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
|