ML20084G505

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Responds to Re Items of Noncompliance.Development of Util Preventive & Corrective Maint Procedures Underway
ML20084G505
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 07/12/1971
From: Ayers T, Brian Lee
COMMONWEALTH EDISON CO.
To: Low L
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20084G486 List:
References
13635, NUDOCS 8304220048
Download: ML20084G505 (4)


Text

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9 o i Commonwealth Edison Company QNE FIRST NATIONAL PLAZA

PO57 OFFICS BOX 767

  • C N B C A G O, ILLINOl$ 60690 July 12, 1971 l

Mr. Lawrence D. Low, Director (,#

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Division of Compliance U. S. Atomic Energy Commission

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Washington, D.C. 20545 '

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Dear Mr. Low:

The purpose of this letter is to present our responses to the items of noncompliance with regulatory requirements which were enclosed with your letter of June 21, 1971. Our responses for the individual itema listed in your enclosure are as follows:

1.a. Commonwealth Edison has relied upon procedures in vendor manuals for maintenar.ce of reactor instrumentation and electrical systems. 'd e are presently preparing our own prevent-ative and corrective maintenance procedures which will incorporate references to the latest vendor manuals. We expect these proce-dures to be completed by November 1, 1971.

1.b. An out-of-service procedure for the high pressure coolant injection system (contained in Chapter 21, Book 2, Procedure 2300 I) was approved by the Station Review Board on October 13, 1970, and signed by the Station Superintendent.

This procedure was subsequently revised and approved by the Station Review Board along with other operating procedures on November 2, 1970 and April 13, 1971.

2.a. The installation of the main steam isolation valve air supply filters was presented to the Station Review Board on I December 18, 1970 by representatives of station management who had reviewed the proposed installation and evaluated its safety s consequences. A written safety evaluation was not prepared for the filter installation because the Station Review Board did not consider the installation to be a change to the main steam isola-tion valve system as described in the PSAR.

2.b. The modification to the electromatic relief valves was presented to the Station Review Board-on October 5, 1970 after an evaluation by the station management. The purpose of this modification was primarily a material change to increase l ,o the performance reliability of the electromatic relief valves.

Therefore, no written safety evaluation was prepared.

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Mr. Lawrence D. Low July 12, 1971 2.a.&b. To preclude the possibility of future plant modification without a written and approved safety evaluation in accordance with 10 CPR 50 59, the Station Review Board has instituted a procedure covering the evaluations of such modifi-cations.

3 The daily surveillance sheets being used by the station required recording of the magnitude and location of the highest LPRM chamber. This is the normal method used to check peak heat flux as stated in the Technical Specification Basis Paragraph 4.1.B.

The daily surveillance sheet did not specify an allowable limit.

The daily surveillance sheets were revised to include the magnitude at which the station operator is required to actify the shift engineer.

4 The inoperability of the main steam isolatien valves during the period of October 27 to November h, 1970 was reviewed by the Nuclear Review Board at its meeting on November 4, 1970.

The NhB decision and reccmmendation were reported to Mr. T. G. Ayers, President of Commonwealth Ediecn, in the minutes of that meeting.

Therefore, we believe the activity identified in this item was conducted in accordance with the Dresden Unit 2 Operating License.

Te assure that future items of non-compliance undergo NRB review and reccamendation, all future AEC Forn-592's will be assigned an action item number and will be put on the list of action items. These items will be reviewed expeditiously and reported in writing as required. This new procedure will be initiated as of this date.

5 The reactor core flux asymmetry condition was noted as i result of LPRM calibrations during April and May 1970.

Tne item was discussed by Commonwealth Edison station management and General Electric site management. A program was instituted to pursue the cause of the possible asymmetries and to determine their magnitude. Reactor power and linear heat flux were deter-mined directly from instrumentation and variation in power represented by core asymmetries are taken into account. Operating limits on MCHFR and linear heat generation were never exceeded.

The reactor was shutdown June 5 to August 4, 1970. Previous indications were tbat some LPRM assemblies had low sensitivity and were not providing reliable information. During the shutdown period, select LPRM assemblies were replaced. Selection of the locations in which to replace the monitors was based on maximizing the information to be gained about the possible power asymmetry l indications.

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O uommonwealth Edison Compay Q Mr. Lawrence D. Low July 12, 1971 A procedure was presented at the SRB meeting No. 40 on August 1, 1970 which was designed to investigate core asymmetries by pulling " local" criticals in various areas of the core. This procedure was approved at SRB meeting No. 41 on August 3, 1970.

This review by the SRB occurred prior to the startup of the unit.

Meanwhile, the situation was being studied in detail by the General Electric Company and possible mechanisms for the power asymmetry were investigated. General Electric concluded that the cost likely mechanism was due to inlet water temperature asymme-tries. The SRB again reviewed the problem at its September 11, 1970 meeting and approved a special test to demonstrate core asymmetry effects due to inlet temperature variations.

A special report No. 6, dated March 17, 1971, was sent to the AEC by Commonwealth Edison, followed by a supplemental report No. 6 dated May 13, 1971. As stated in the report, there is not (and never has been) a s af e ty problem involved with the core asymmetry for the following reasons:

Reactor power and linear heat flux are determined directly frcm instrumentation and therefore variations in power represented by core asymmetries are takan into account.,

The calculated MCHFR will always be less than tne actual MCHFR and thus the calculations are in the conservative ,

direction and ensure adequate margins for all calculated transients and postulated accidents. ,

Dresden 3 has undergone a feedwater aparger modification in an attempt to correct the inlet temperature variations. The Dresden 2 feedwater sparger may be modified if the results of the Dresden 3 feedwater modification show positive results. ,

6. The dated and initialed check lists prepared by members of the Station Technical Staff indicate functional tests of the generator load rejection scram sensor were performed on September 29, October 28, and November 7 in accordance with l operating license DPR-19 We have been unable to locate all the l operator's surveillance sheets for tests between August 5 and December 4, 1970.

I 7 Methods and procedures used during the required in-service inspecti)ns were approved by non-destructive testing experts from Commonwealth Edison's Operating Analysis Department. Mr. E. C.

Bailey of Commonwealth Edison was consulted both as to the findings and the action being taken throughout the examination program.

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s-  ! n baommonwealth Edison Compalf Mr. Lawrence D. Low - 4- July 12, 1971 Several linear and dot type surface indications were'found on various safe ends. Repairs were made by minimal grinding to remove the indications. The indication on Nozzle N-19A (core spray) also appeared to be merely a surface indication, but required extensive grinding before it was removed. The indications on the core spray nozzle safe end were so small and so few they would not have required removal to meet the applicable Code requirements. Their appearance did not indicate they were caused by corrosion. A repair procedure was wri+. ten to conform to Section III and Section XI of the ASME Boiler and Pressure Vessel Codes, which detailed methods to be employed, tests to be performed and witnesses to approve of the repair program. At the time that the inspection and repairs were made, Edison General Office management decided this repair should be classified as required maintenance to be reported in the Station Semi-Annual Report. Because of the AEC's concern over furnace sensitized safe ends, Commonwealth Edison will inform Region III Compliance in accordance with Paragraph }

6.6.A.3 whenever a repair requires removal of more than one-third 1 /;' 9 of the wall thickness. ,_j

8. Procedures now in effect require taat operation, maintenance, repair, refueling and plant modifications be reviewed, cocumented and adecuately tested. We recognize the need for addi-tional preceduree to be completely responsive to Appendix B " . We are currently developing a Ccmmonwealth Edison Compsny Qu ali ty Assurance Manual and the supporting procedures for each Station.

This Manual is intended to meet the requirements of Appendix "B",

10 CFR Dart 50. We expect the Manual to be completed by September 15, 1971 ana the supporting procedures by November 1, 1971.

Eecause of our growing commitment to nuclear generation, we have been reevaluating our management organization. In J anuary 1971, Mr. N. A. Kershaw was appointed Superintendent Nuclear and Fossil Systems, for our Production Department. One of his major respon-sibilities is the surveillance of our operations to assure compliance with licenses. In May 1971, Mr. E. J. Hemzy was named our Quality Assurance Administrator and reports directly to Mr. L. P. Lischer, our Engineering Vice President. He formerly reported to our Superintendent of Station Construction. On Friday, July 1, Mr. Ward, Chairman of Commonwealth Edison, and Mr. Ayers, President, met with Dr. Mann, Dr. Morris and Mr. Giambusso of the AEC to discuss our management organization. We are committed to meet with them again to discuss a review we have undertaken.

Very truly yours,

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%ncr\ 1 Byrpn Lee, Jr.

- /, ) A sistant to th President

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Approved:

Thomas G. Ayers President