|
---|
Category:INSPECTION REPORT
MONTHYEARIR 05000458/19990121999-10-19019 October 1999 Insp Rept 50-458/99-12 on 990822-1002.Non-cited Violations Noted.Major Areas Inspected:Operations,Engineering, Maintenance & Plant Support IR 05000458/19990101999-09-15015 September 1999 Insp Rept 50-458/99-10 on 990830-0903.No Violations Noted. Major Areas Inspected:Licensed Operators Requalification Program IR 05000458/19990081999-09-0808 September 1999 Insp Rept 50-458/99-08 on 990711-0821.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000458/19990111999-08-17017 August 1999 Insp Rept 50-458/99-11 on 990719-23.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000458/19990091999-08-16016 August 1999 Replacement Pages 9-18 for Insp Rept 50-458/99-09 Issued on 990730 ML20210N1901999-08-0404 August 1999 Insp Rept 50-458/99-07 on 990530-0710.One Violation of NRC Requirements Occurred & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee,Operations,Maint,Engineering & Plant Support ML20210K1471999-07-30030 July 1999 Insp Rept 50-458/99-09 on 990510-28 with in-office Insp Until 990701.Noncited Violations Identified.Major Areas Inspected:Review of Licensee Actions Re Testing & Cleaning of Auxiliary Bldg Unit Coolers ML20196L0551999-07-0606 July 1999 Revised Pages 4 of Report Details Section & 2 of Rept Attachment for Insp Rept 50-458/99-03.Corrections Made to Tracking Numbers Assigned to Seven Noncited Violations & to SRO Location During Refueling Activities IR 05000458/19990041999-06-30030 June 1999 Insp Rept 50-458/99-04 on 990412-16 & 28-29.Five Violations Occurred & Being Treated as Noncited Violations.Major Areas Inspected:Portions of Radiation Protection Program,Including Exposure Controls & Radiation Technical & Worker Practices IR 05000458/19990051999-06-18018 June 1999 Insp Rept 50-458/99-05 on 990418-0529.Nonccited Violations Noted.Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000458/19990031999-05-18018 May 1999 Insp Rept 50-458/99-03 on 990307-0417.Noncited Violations Noted.Major Areas Inspected:Operation,Maintenance, Engineering & Plant Support IR 05000458/19990061999-05-15015 May 1999 Insp Rept 50-458/99-06 on 990419-23.No Violations Noted. Major Areas Inspected:Inservice Exam Program Plan & Schedule,Implementation of Program Plan for Facility & Maint & Engineering Followup Review of Previous Insp Findings ML20205A4601999-03-26026 March 1999 Insp Rept 50-458/98-10 on 990222-26.Violations Noted.Major Areas Inspected:Radiation Work Permit Program Implementation from Oct 1997 to Feb 1999 & Problem Identification & Resolution Program as Applied to Program Deficiencies IR 05000458/19990021999-03-26026 March 1999 Insp Rept 50-458/99-02 on 990124-0306.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000458/19990011999-01-25025 January 1999 Insp Rept 50-458/99-01 on 990104-08.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Alarm Stations,Communications,Access Control of Personnel,Packages,Vehicles & Assessment Aids IR 05000458/19980201999-01-0707 January 1999 Insp Rept 50-458/98-20 on 981101-1212.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980161998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress ML20198N9311998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress IR 05000458/19980181998-11-30030 November 1998 Insp Rept 50-458/98-18 on 980920-1031.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20196G5161998-11-25025 November 1998 Insp Rept 50-458/98-10 Has Been Canceled.No Insp Rept Will Be Issued IR 05000458/19980191998-11-20020 November 1998 Insp Rept 50-458/98-19 on 981019-23.No Violations Noted. Major Areas Inspected:Operations IR 05000458/19980131998-10-27027 October 1998 Insp Rept 50-458/98-13 on 980608-12,22-26 & 0824-28.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations,Maint & Engineering IR 05000458/19980141998-10-21021 October 1998 Insp Rept 50-458/98-14 on 980928-1002.No Violations Noted. Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000458/19980171998-10-0505 October 1998 Insp Rept 50-458/98-17 on 980809-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980151998-08-28028 August 1998 Insp Rept 50-458/98-15 on 980628-0808.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19980121998-07-29029 July 1998 Insp Rept 50-458/98-12 on 980517-0627.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980071998-06-0808 June 1998 Insp Rept 50-458/98-07 on 980518-21.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring Programs IR 05000458/19980081998-06-0505 June 1998 Insp Rept 50-458/98-08 on 980405-0516.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980111998-06-0404 June 1998 Insp Rept 50-458/98-11 on 980518-21.No Violations Noted. Major Areas Inspected:Maint IR 05000458/19980061998-05-19019 May 1998 Insp Rept 50-458/98-06 on 980427-0501.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radioactive Effluent Waste Mgt Program IR 05000458/19980091998-04-30030 April 1998 Informs That Insp Rept 50-458/98-09 Has Been Canceled ML20217A4801998-04-17017 April 1998 Insp Rept 50-458/98-05 on 980222-0404.Violations Noted. Major Areas Inspected:Operations,Main,Engineering & Plant Support ML20217B4951998-03-24024 March 1998 Insp Rept 50-458/98-03 on 980223-26.Violations Noted.Major Areas Inspected:Review of Radiation Protection Program Activities IR 05000458/19972011998-03-20020 March 1998 Fire Protection Insp Rept 50-458/97-201 on 970615-20, 0629-0703,0819,980120 & 0305.No Violations Noted.Major Areas Inspected:Comprehensive Evaluation of Fire Protection Program & Post Fire Safe Shutdown Capability IR 05000458/19980041998-03-19019 March 1998 Insp Rept 50-458/98-04 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203L8831998-03-0404 March 1998 Insp Rept 50-458/98-01 on 980210-13.No Violations Noted. Major Areas Inspected:Licensee Performance & Capabilities During Fullscale,Biennial Exercise of Emergency Plan & Implementation Procedures ML20202B9401998-02-0606 February 1998 Insp Rept 50-458/97-19 on 971130-980110.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000458/19970201998-02-0505 February 1998 Insp Rept 50-458/97-20 on 971008-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000458/19980021998-02-0202 February 1998 Insp Rept 50-458/98-02 on 980112-16.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program, Including Access Authorization,Alarm Stations,Communication, Access Control of Personnel & Security Event Logs IR 05000458/19970181998-01-0606 January 1998 Insp Rept 50-458/97-18 on 971208-12.No Violations Noted. Major Areas Inspected:Maint & Engineering IR 05000458/19970121997-12-29029 December 1997 Insp Rept 50-458/97-12 on 971203-12.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program Following Guidelines in Insp Procedure 71001 ML20197G6191997-12-24024 December 1997 Insp Rept 50-458/97-17 on 971012-1129.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19970151997-11-17017 November 1997 Insp Rept 50-458/97-15 on 970922-1017.Violations Noted: Inadequate Procedrual Controls for Bus Restoration Contributed to Loss of Shutdown Cooling for 17 Min & Failure to Maintain Adequate Procedures IR 05000458/19970141997-11-14014 November 1997 Insp Rept 50-458/97-14 on 970831-1011.Violation Noted. Major Areas Inspected:Operation,Maint,Enginerring & Plant Support IR 05000458/19970161997-10-28028 October 1997 Insp Rept 50-458/97-16 on 970929-1003.No Violations Noted. Major Areas Inspected:Operations & Maint IR 05000458/19970131997-09-26026 September 1997 Insp Rept 50-458/97-13 on 970720-0830.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19970031997-09-10010 September 1997 Insp Rept 50-458/97-03 on 970804-08.Violations Noted.Major Areas Inspected:Implementation of Solid Radwaste Mgt & Radwaste & Matls Transportation Programs IR 05000458/19973011997-08-20020 August 1997 Insp Rept 50-458/97-301 on 970728-0801.No Violations Noted. Major Areas Inspected:Operations Examiners Evaluated Competency of Two Senior Reactor Operator & Three Reactor Operator License Applicants for Issuance of Licenses IR 05000458/19970101997-08-0606 August 1997 Insp Rept 50-458/97-10 on 970608-0719.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20149H1441997-07-21021 July 1997 Partially Withheld Insp Rept 50-458/97-11 on 970623-27.Major Areas Inspected:Specific Areas of Physical Security Program Including Review of Records & Repts,Testing & Maint,Vital Area Barriers & Detection Aids & Alarm Stations 1999-09-08
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000458/19990121999-10-19019 October 1999 Insp Rept 50-458/99-12 on 990822-1002.Non-cited Violations Noted.Major Areas Inspected:Operations,Engineering, Maintenance & Plant Support IR 05000458/19990101999-09-15015 September 1999 Insp Rept 50-458/99-10 on 990830-0903.No Violations Noted. Major Areas Inspected:Licensed Operators Requalification Program IR 05000458/19990081999-09-0808 September 1999 Insp Rept 50-458/99-08 on 990711-0821.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000458/19990111999-08-17017 August 1999 Insp Rept 50-458/99-11 on 990719-23.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000458/19990091999-08-16016 August 1999 Replacement Pages 9-18 for Insp Rept 50-458/99-09 Issued on 990730 ML20210N1901999-08-0404 August 1999 Insp Rept 50-458/99-07 on 990530-0710.One Violation of NRC Requirements Occurred & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee,Operations,Maint,Engineering & Plant Support ML20210K1471999-07-30030 July 1999 Insp Rept 50-458/99-09 on 990510-28 with in-office Insp Until 990701.Noncited Violations Identified.Major Areas Inspected:Review of Licensee Actions Re Testing & Cleaning of Auxiliary Bldg Unit Coolers ML20196L0551999-07-0606 July 1999 Revised Pages 4 of Report Details Section & 2 of Rept Attachment for Insp Rept 50-458/99-03.Corrections Made to Tracking Numbers Assigned to Seven Noncited Violations & to SRO Location During Refueling Activities IR 05000458/19990041999-06-30030 June 1999 Insp Rept 50-458/99-04 on 990412-16 & 28-29.Five Violations Occurred & Being Treated as Noncited Violations.Major Areas Inspected:Portions of Radiation Protection Program,Including Exposure Controls & Radiation Technical & Worker Practices IR 05000458/19990051999-06-18018 June 1999 Insp Rept 50-458/99-05 on 990418-0529.Nonccited Violations Noted.Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000458/19990031999-05-18018 May 1999 Insp Rept 50-458/99-03 on 990307-0417.Noncited Violations Noted.Major Areas Inspected:Operation,Maintenance, Engineering & Plant Support IR 05000458/19990061999-05-15015 May 1999 Insp Rept 50-458/99-06 on 990419-23.No Violations Noted. Major Areas Inspected:Inservice Exam Program Plan & Schedule,Implementation of Program Plan for Facility & Maint & Engineering Followup Review of Previous Insp Findings ML20205A4601999-03-26026 March 1999 Insp Rept 50-458/98-10 on 990222-26.Violations Noted.Major Areas Inspected:Radiation Work Permit Program Implementation from Oct 1997 to Feb 1999 & Problem Identification & Resolution Program as Applied to Program Deficiencies IR 05000458/19990021999-03-26026 March 1999 Insp Rept 50-458/99-02 on 990124-0306.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000458/19990011999-01-25025 January 1999 Insp Rept 50-458/99-01 on 990104-08.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Alarm Stations,Communications,Access Control of Personnel,Packages,Vehicles & Assessment Aids IR 05000458/19980201999-01-0707 January 1999 Insp Rept 50-458/98-20 on 981101-1212.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980161998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress ML20198N9311998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress IR 05000458/19980181998-11-30030 November 1998 Insp Rept 50-458/98-18 on 980920-1031.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20196G5161998-11-25025 November 1998 Insp Rept 50-458/98-10 Has Been Canceled.No Insp Rept Will Be Issued IR 05000458/19980191998-11-20020 November 1998 Insp Rept 50-458/98-19 on 981019-23.No Violations Noted. Major Areas Inspected:Operations IR 05000458/19980131998-10-27027 October 1998 Insp Rept 50-458/98-13 on 980608-12,22-26 & 0824-28.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations,Maint & Engineering IR 05000458/19980141998-10-21021 October 1998 Insp Rept 50-458/98-14 on 980928-1002.No Violations Noted. Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000458/19980171998-10-0505 October 1998 Insp Rept 50-458/98-17 on 980809-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980151998-08-28028 August 1998 Insp Rept 50-458/98-15 on 980628-0808.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19980121998-07-29029 July 1998 Insp Rept 50-458/98-12 on 980517-0627.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980071998-06-0808 June 1998 Insp Rept 50-458/98-07 on 980518-21.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring Programs IR 05000458/19980081998-06-0505 June 1998 Insp Rept 50-458/98-08 on 980405-0516.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980111998-06-0404 June 1998 Insp Rept 50-458/98-11 on 980518-21.No Violations Noted. Major Areas Inspected:Maint IR 05000458/19980061998-05-19019 May 1998 Insp Rept 50-458/98-06 on 980427-0501.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radioactive Effluent Waste Mgt Program IR 05000458/19980091998-04-30030 April 1998 Informs That Insp Rept 50-458/98-09 Has Been Canceled ML20217A4801998-04-17017 April 1998 Insp Rept 50-458/98-05 on 980222-0404.Violations Noted. Major Areas Inspected:Operations,Main,Engineering & Plant Support ML20217B4951998-03-24024 March 1998 Insp Rept 50-458/98-03 on 980223-26.Violations Noted.Major Areas Inspected:Review of Radiation Protection Program Activities IR 05000458/19972011998-03-20020 March 1998 Fire Protection Insp Rept 50-458/97-201 on 970615-20, 0629-0703,0819,980120 & 0305.No Violations Noted.Major Areas Inspected:Comprehensive Evaluation of Fire Protection Program & Post Fire Safe Shutdown Capability IR 05000458/19980041998-03-19019 March 1998 Insp Rept 50-458/98-04 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203L8831998-03-0404 March 1998 Insp Rept 50-458/98-01 on 980210-13.No Violations Noted. Major Areas Inspected:Licensee Performance & Capabilities During Fullscale,Biennial Exercise of Emergency Plan & Implementation Procedures ML20202B9401998-02-0606 February 1998 Insp Rept 50-458/97-19 on 971130-980110.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000458/19970201998-02-0505 February 1998 Insp Rept 50-458/97-20 on 971008-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000458/19980021998-02-0202 February 1998 Insp Rept 50-458/98-02 on 980112-16.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program, Including Access Authorization,Alarm Stations,Communication, Access Control of Personnel & Security Event Logs IR 05000458/19970181998-01-0606 January 1998 Insp Rept 50-458/97-18 on 971208-12.No Violations Noted. Major Areas Inspected:Maint & Engineering IR 05000458/19970121997-12-29029 December 1997 Insp Rept 50-458/97-12 on 971203-12.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program Following Guidelines in Insp Procedure 71001 ML20197G6191997-12-24024 December 1997 Insp Rept 50-458/97-17 on 971012-1129.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19970151997-11-17017 November 1997 Insp Rept 50-458/97-15 on 970922-1017.Violations Noted: Inadequate Procedrual Controls for Bus Restoration Contributed to Loss of Shutdown Cooling for 17 Min & Failure to Maintain Adequate Procedures IR 05000458/19970141997-11-14014 November 1997 Insp Rept 50-458/97-14 on 970831-1011.Violation Noted. Major Areas Inspected:Operation,Maint,Enginerring & Plant Support IR 05000458/19970161997-10-28028 October 1997 Insp Rept 50-458/97-16 on 970929-1003.No Violations Noted. Major Areas Inspected:Operations & Maint IR 05000458/19970131997-09-26026 September 1997 Insp Rept 50-458/97-13 on 970720-0830.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19970031997-09-10010 September 1997 Insp Rept 50-458/97-03 on 970804-08.Violations Noted.Major Areas Inspected:Implementation of Solid Radwaste Mgt & Radwaste & Matls Transportation Programs IR 05000458/19973011997-08-20020 August 1997 Insp Rept 50-458/97-301 on 970728-0801.No Violations Noted. Major Areas Inspected:Operations Examiners Evaluated Competency of Two Senior Reactor Operator & Three Reactor Operator License Applicants for Issuance of Licenses IR 05000458/19970101997-08-0606 August 1997 Insp Rept 50-458/97-10 on 970608-0719.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20149H1441997-07-21021 July 1997 Partially Withheld Insp Rept 50-458/97-11 on 970623-27.Major Areas Inspected:Specific Areas of Physical Security Program Including Review of Records & Repts,Testing & Maint,Vital Area Barriers & Detection Aids & Alarm Stations 1999-09-08
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000458/19990121999-10-19019 October 1999 Insp Rept 50-458/99-12 on 990822-1002.Non-cited Violations Noted.Major Areas Inspected:Operations,Engineering, Maintenance & Plant Support IR 05000458/19990101999-09-15015 September 1999 Insp Rept 50-458/99-10 on 990830-0903.No Violations Noted. Major Areas Inspected:Licensed Operators Requalification Program IR 05000458/19990081999-09-0808 September 1999 Insp Rept 50-458/99-08 on 990711-0821.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000458/19990111999-08-17017 August 1999 Insp Rept 50-458/99-11 on 990719-23.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000458/19990091999-08-16016 August 1999 Replacement Pages 9-18 for Insp Rept 50-458/99-09 Issued on 990730 ML20210N1901999-08-0404 August 1999 Insp Rept 50-458/99-07 on 990530-0710.One Violation of NRC Requirements Occurred & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee,Operations,Maint,Engineering & Plant Support ML20210K1471999-07-30030 July 1999 Insp Rept 50-458/99-09 on 990510-28 with in-office Insp Until 990701.Noncited Violations Identified.Major Areas Inspected:Review of Licensee Actions Re Testing & Cleaning of Auxiliary Bldg Unit Coolers ML20196L0551999-07-0606 July 1999 Revised Pages 4 of Report Details Section & 2 of Rept Attachment for Insp Rept 50-458/99-03.Corrections Made to Tracking Numbers Assigned to Seven Noncited Violations & to SRO Location During Refueling Activities IR 05000458/19990041999-06-30030 June 1999 Insp Rept 50-458/99-04 on 990412-16 & 28-29.Five Violations Occurred & Being Treated as Noncited Violations.Major Areas Inspected:Portions of Radiation Protection Program,Including Exposure Controls & Radiation Technical & Worker Practices IR 05000458/19990051999-06-18018 June 1999 Insp Rept 50-458/99-05 on 990418-0529.Nonccited Violations Noted.Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000458/19990031999-05-18018 May 1999 Insp Rept 50-458/99-03 on 990307-0417.Noncited Violations Noted.Major Areas Inspected:Operation,Maintenance, Engineering & Plant Support IR 05000458/19990061999-05-15015 May 1999 Insp Rept 50-458/99-06 on 990419-23.No Violations Noted. Major Areas Inspected:Inservice Exam Program Plan & Schedule,Implementation of Program Plan for Facility & Maint & Engineering Followup Review of Previous Insp Findings ML20205A4601999-03-26026 March 1999 Insp Rept 50-458/98-10 on 990222-26.Violations Noted.Major Areas Inspected:Radiation Work Permit Program Implementation from Oct 1997 to Feb 1999 & Problem Identification & Resolution Program as Applied to Program Deficiencies IR 05000458/19990021999-03-26026 March 1999 Insp Rept 50-458/99-02 on 990124-0306.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000458/19990011999-01-25025 January 1999 Insp Rept 50-458/99-01 on 990104-08.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Alarm Stations,Communications,Access Control of Personnel,Packages,Vehicles & Assessment Aids IR 05000458/19980201999-01-0707 January 1999 Insp Rept 50-458/98-20 on 981101-1212.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980161998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress ML20198N9311998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress IR 05000458/19980181998-11-30030 November 1998 Insp Rept 50-458/98-18 on 980920-1031.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20196G5161998-11-25025 November 1998 Insp Rept 50-458/98-10 Has Been Canceled.No Insp Rept Will Be Issued IR 05000458/19980191998-11-20020 November 1998 Insp Rept 50-458/98-19 on 981019-23.No Violations Noted. Major Areas Inspected:Operations IR 05000458/19980131998-10-27027 October 1998 Insp Rept 50-458/98-13 on 980608-12,22-26 & 0824-28.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations,Maint & Engineering IR 05000458/19980141998-10-21021 October 1998 Insp Rept 50-458/98-14 on 980928-1002.No Violations Noted. Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000458/19980171998-10-0505 October 1998 Insp Rept 50-458/98-17 on 980809-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980151998-08-28028 August 1998 Insp Rept 50-458/98-15 on 980628-0808.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19980121998-07-29029 July 1998 Insp Rept 50-458/98-12 on 980517-0627.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980071998-06-0808 June 1998 Insp Rept 50-458/98-07 on 980518-21.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring Programs IR 05000458/19980081998-06-0505 June 1998 Insp Rept 50-458/98-08 on 980405-0516.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980111998-06-0404 June 1998 Insp Rept 50-458/98-11 on 980518-21.No Violations Noted. Major Areas Inspected:Maint IR 05000458/19980061998-05-19019 May 1998 Insp Rept 50-458/98-06 on 980427-0501.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radioactive Effluent Waste Mgt Program IR 05000458/19980091998-04-30030 April 1998 Informs That Insp Rept 50-458/98-09 Has Been Canceled ML20217A4801998-04-17017 April 1998 Insp Rept 50-458/98-05 on 980222-0404.Violations Noted. Major Areas Inspected:Operations,Main,Engineering & Plant Support ML20217B4951998-03-24024 March 1998 Insp Rept 50-458/98-03 on 980223-26.Violations Noted.Major Areas Inspected:Review of Radiation Protection Program Activities IR 05000458/19972011998-03-20020 March 1998 Fire Protection Insp Rept 50-458/97-201 on 970615-20, 0629-0703,0819,980120 & 0305.No Violations Noted.Major Areas Inspected:Comprehensive Evaluation of Fire Protection Program & Post Fire Safe Shutdown Capability IR 05000458/19980041998-03-19019 March 1998 Insp Rept 50-458/98-04 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203L8831998-03-0404 March 1998 Insp Rept 50-458/98-01 on 980210-13.No Violations Noted. Major Areas Inspected:Licensee Performance & Capabilities During Fullscale,Biennial Exercise of Emergency Plan & Implementation Procedures ML20202B9401998-02-0606 February 1998 Insp Rept 50-458/97-19 on 971130-980110.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000458/19970201998-02-0505 February 1998 Insp Rept 50-458/97-20 on 971008-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000458/19980021998-02-0202 February 1998 Insp Rept 50-458/98-02 on 980112-16.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program, Including Access Authorization,Alarm Stations,Communication, Access Control of Personnel & Security Event Logs IR 05000458/19970181998-01-0606 January 1998 Insp Rept 50-458/97-18 on 971208-12.No Violations Noted. Major Areas Inspected:Maint & Engineering IR 05000458/19970121997-12-29029 December 1997 Insp Rept 50-458/97-12 on 971203-12.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program Following Guidelines in Insp Procedure 71001 ML20197G6191997-12-24024 December 1997 Insp Rept 50-458/97-17 on 971012-1129.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19970151997-11-17017 November 1997 Insp Rept 50-458/97-15 on 970922-1017.Violations Noted: Inadequate Procedrual Controls for Bus Restoration Contributed to Loss of Shutdown Cooling for 17 Min & Failure to Maintain Adequate Procedures IR 05000458/19970141997-11-14014 November 1997 Insp Rept 50-458/97-14 on 970831-1011.Violation Noted. Major Areas Inspected:Operation,Maint,Enginerring & Plant Support IR 05000458/19970161997-10-28028 October 1997 Insp Rept 50-458/97-16 on 970929-1003.No Violations Noted. Major Areas Inspected:Operations & Maint IR 05000458/19970131997-09-26026 September 1997 Insp Rept 50-458/97-13 on 970720-0830.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000458/19970031997-09-10010 September 1997 Insp Rept 50-458/97-03 on 970804-08.Violations Noted.Major Areas Inspected:Implementation of Solid Radwaste Mgt & Radwaste & Matls Transportation Programs IR 05000458/19973011997-08-20020 August 1997 Insp Rept 50-458/97-301 on 970728-0801.No Violations Noted. Major Areas Inspected:Operations Examiners Evaluated Competency of Two Senior Reactor Operator & Three Reactor Operator License Applicants for Issuance of Licenses IR 05000458/19970101997-08-0606 August 1997 Insp Rept 50-458/97-10 on 970608-0719.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20149H1441997-07-21021 July 1997 Partially Withheld Insp Rept 50-458/97-11 on 970623-27.Major Areas Inspected:Specific Areas of Physical Security Program Including Review of Records & Repts,Testing & Maint,Vital Area Barriers & Detection Aids & Alarm Stations 1999-09-08
[Table view] Category:UTILITY
MONTHYEARIR 05000458/19900311990-11-19019 November 1990 Insp Rept 50-458/90-31 on 901105-09.No Violations or Deviations Noted.Major Areas Inspected:Verification of Isolation Component Exemptions IR 05000458/19900251990-11-0707 November 1990 Insp Rept 50-458/90-25 on 900924-28 & 1015-19.Noncited Violation Identified.Major Areas Inspected:Quality Verification Function Including Condition Rept Program, Internal Audit Program IR 05000458/19900281990-10-17017 October 1990 Insp Rept 50-458/90-28 on 901009-12.No Violations or Deviations Noted.Major Areas Inspected:Installation & Testing of Mods & Installation of Heat Shrinkable Insulation Tubing ML20058A5461990-10-17017 October 1990 Insp Rept 50-458/90-23 on 900910-14.No Violations or Deviations Noted.Major Areas Inspected:Engineering Evaluation in Response to NRC Bulletin 88-004,action of Previously Identified Items & Review of Root Cause Analysis IR 05000458/19900221990-09-27027 September 1990 Insp Rept 50-458/90-22 on 900827-31.No Violations or Deviations Noted.Major Areas Inspected:Licensee Liquid & Gaseous Radwaste Mgt Program ML20059D6471990-08-28028 August 1990 Insp Rept 50-458/90-15 on 900611-15.No Violations or Deviations Noted.Major Areas Inspected:Operational Status of Emergency Preparedness Program,Including Followup to Previous Insp Findings & Equipment IR 05000458/19900201990-08-21021 August 1990 Insp Rept 50-458/90-20 on 900723-26.No Violations or Deviations Noted.Major Areas Inspected:Training & Qualification Effectiveness IR 05000458/19902001990-07-26026 July 1990 Electrical Distribution Sys Functional Insp Rept 50-458/90-200 on 900521-0622.No Violations Noted.Major Areas Inspected:Design & Implementation of Plant Electrical Distribution Sys & Adequacy of Engineering Support IR 05000458/19900171990-07-19019 July 1990 Advises That Insp 50-458/90-17 Canceled,Therefore,No Insp Rept Will Be Issued IR 05000458/19900141990-06-19019 June 1990 Insp Rept 50-458/90-14 on 900521-22.One self-identified Violation Noted.Major Areas Inspected:Licensee Occupational Radiation Protection Program Including High Radiation Area Controls IR 05000458/19890331989-09-21021 September 1989 Insp Rept 50-458/89-33 on 890801-31.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Test Observation,Ler Followup & Followup on 10CFR21 Repts IR 05000458/19890311989-08-29029 August 1989 Insp Rept 50-458/89-31 on 890701-31.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Test Observation,Esf Walkdown & Emergency Preparedness Drill IR 05000458/19890301989-08-17017 August 1989 Insp Rept 50-458/89-30 on 890619-23.Violations Noted.Major Areas Inspected:Physical Security Program IR 05000458/19890191989-08-10010 August 1989 Advises That Insp 50-458/89-19 Cancelled & No Insp Rept Will Be Issued for Rept Number IR 05000458/19890321989-07-31031 July 1989 Insp Rept 50-458/89-32 on 890717-21.No Violations or Deviations Noted.Major Areas Inspected:Surveillance Testing Program & Plant Instrumentation Calibr Program.Lists of Surveillance Test Performance & Loop Calibr Repts Encl IR 05000458/19890281989-07-27027 July 1989 Insp Rept 50-458/89-28 on 890601-30.Violations Noted.Major Areas Inspected:Plant Events,Operational Safety Verification,Maint & Surveillance Test Observation & Licensee Action on Previous Insp Findings IR 05000458/19890251989-07-27027 July 1989 Insp Rept 50-458/89-25 on 890710-14.No Violations or Deviations Noted.Major Areas Inspected:Startup Testing. Conservative Error in Util Procedure for Manual Calculations of Core Thermal Power Identified IR 05000458/19890291989-07-14014 July 1989 Insp Rept 50-458/89-29 on 890619-23.No Violations or Deviations Noted.Major Areas Inspected:Corrective Actions IR 05000458/19890271989-07-12012 July 1989 Insp Rept 50-458/89-27 on 890605-09 & 19-23.Violations Noted.Major Areas Inspected:Self Assessment Capabilities IR 05000458/19890241989-06-26026 June 1989 Insp Rept 50-458/89-24 on 890501-31.Violations Noted.Major Areas Inspected:Plant Events,Operational Safety Verification & Maint & Surveillance Test Observation IR 05000458/19890221989-06-20020 June 1989 Insp Rept 50-458/89-22 on 890525-27.No Violations or Deviations Noted.Major Areas Inspected:Containment Integrated Leak Rate Test & Review of Results of Local Leak Rate Test IR 05000458/19890261989-06-14014 June 1989 Insp Rept 50-458/89-26 on 890515-19.No Violations Noted. Major Areas Inspected:Action on Previously Indentified Insp Findings,Inservice Insp Data Review & Corrective Actions IR 05000458/19890011989-06-0707 June 1989 Insp Rept 50-458/89-01 on 890501-05.No Violations Noted. Major Areas Inspected:Facility Mods & Nonlicensed Staff Training ML20244C3561989-06-0505 June 1989 Insp Rept 50-458/89-18 on 890501-05 & 15-19.Violations Noted.Major Areas Inspected:Inservice Testing Program for Pumps & Valves,Welding Activities Associated W/Repairs to Svc Water Sys & Activities Re Instrument Air Sys Insp IR 05000458/19890231989-05-25025 May 1989 Insp Repts 50-458/89-23 on 890501-05.No Violations or Deviations Noted.Major Areas Inspected:Programs for Station Design Changes & Mods for Installation of Raychem Electrical Splices IR 05000458/19890111989-05-24024 May 1989 Insp Rept 50-458/89-11 on 890315-0430.Violations Noted.Major Areas Inspected:Plant Events,Operational Safety Verification,Maint & Surveillance Test Observation,Refueling Activities & Licensee Action on Previous Findings IR 05000458/19890171989-05-16016 May 1989 Insp Rept 50-458/89-17 on 890409-19.Violations Noted.Major Areas Inspected:Radiation Protection Program,Including Planning & Preparation for in-reactor Pressure Vessel Repair of Feed Water Spargers IR 05000458/19890131989-05-15015 May 1989 Advises That Insp Rept 50-458/89-13 Cancelled.No Rept Will Be Issued for Rept Number ML20244D4511989-05-15015 May 1989 Partially Withheld Insp Rept 50-458/89-15 on 890402-06 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Physical Security Program,Including Mgt Support,Security Program Plans & Audits & Protected & Vital Area Access IR 05000458/19890211989-05-10010 May 1989 Insp Rept 50-458/89-21 on 890424-28.No Violations or Deviations Noted.Major Areas Inspected:Surveillance Test Observation & Followup on Operating Events IR 05000458/19890101989-05-0909 May 1989 Insp Rept 50-458/89-10 on 890327-0406.No Violations or Deviations Noted.Major Areas Inspected:Review of Inservice Insp,Welding & Associated Documents & Procedures.Mod to RHR Sys Also Reviewed IR 05000458/19890141989-04-20020 April 1989 Insp Rept 50-458/89-14 on 890403-07.No Violations or Deviations Noted.Major Areas Inspected:Testing of Pipe Supports & Restraint Sys ML20244B6001989-04-0606 April 1989 Insp Rept 50-458/89-12 on 890327-31.Violation Noted.Major Areas Inspected:Welding Activities.Welding Program Well Defined & Includes Monitoring by Qc.Weakness in Welder Qualification Program Noted IR 05000458/19890071989-04-0505 April 1989 Insp Rept 50-458/89-07 on 890201-0314.No Violations or Deviations Noted.Major Areas Inspected:Plant Events, Emergency Preparedness Exercise,Operational Safety Verification & Surveillance Test Observation IR 05000458/19890091989-03-30030 March 1989 Insp Rept 50-458/89-09 on 890301-03.No Violations or Deviations Noted.Major Areas Inspected:Licensee Performance & Capabilities During Annual Exercise of Emergency Plan & Procedures IR 05000458/19890081989-03-10010 March 1989 Insp Rept 50-458/89-08 on 890213-17.No Violations or Deviations Noted.Major Areas Inspected:Calibr Program, Emergency Diesel Fuel Oil Program Into QA Program & Receipt, Storage & Handling of Diesel Generator Fuel Oil IR 05000458/19890061989-03-0808 March 1989 Insp Rept 50-458/89-06 on 890206-10.No Violations or Deviations Noted.Major Areas Inspected:Inservice Testing Program for Pumps & Valves IR 05000458/19890051989-02-24024 February 1989 Insp Rept 50-458/89-05 on 890101-31.No Violations Noted. Major Areas Inspected:Operational Safety Verification, Radiological Protection,Security,Surveillance Test Observation & Maint Observation IR 05000458/19890031989-02-23023 February 1989 Informs That Insp 50-458/89-03 Cancelled.No Insp Rept Will Be Issued for Subj Rept Number IR 05000458/19880291989-01-31031 January 1989 Partially Withheld Insp Rept 50-458/88-29 on 881212-16 (Ref 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Physical Security Program Included Mgt Support, Security Program Plans,Audits & Records & Repts IR 05000458/19880191988-10-14014 October 1988 Insp Rept 50-458/88-19 on 880801-0917.Violation Noted.Major Areas Inspected:Surveillance & Maint Observation,Safety Sys Walkdown,Operational Safety Verification,Radiological Protection Observation & Security ML20155G8291988-10-0303 October 1988 Insp Rept 50-458/88-21 on 880912-15.No Violations or Deviations Noted.Major Areas Inspected:Emergency Preparedness Program ML20155E2471988-09-27027 September 1988 Insp Rept 50-458/88-22 on 880829-0915.Violations Noted.Major Areas Inspected:Fuel Bldg Ventilation Charcoal Filtration Sys IR 05000458/19880201988-09-14014 September 1988 Insp Rept 50-458/88-20 on 880822-25.No Violations Noted. Details Withheld (Ref 10CFR73.21) ML20153E4051988-08-30030 August 1988 Insp Rept 50-458/88-18 on 880808-12.Violations Noted.Major Areas Inspected:Surveillance Procedures & Records IR 05000458/19880181988-08-30030 August 1988 Insp Rept 50-458/88-18 on 880808-12.Violations Noted.Major Areas Inspected:Surveillance Procedures & Records ML20151Z8021988-08-22022 August 1988 Partially Withheld Insp Rept 50-458/88-14 on 880613-17 (Ref 10CFR73.21).Violation Noted.Major Areas Inspected:Lers, Allegations,Security Procedures,Mgt Effectivenss,Security Program Audits & Records & Repts IR 05000458/19880171988-08-12012 August 1988 Insp Rept 50-458/88-17 on 880701-31.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on NRC Bulletin 88-005,surveillance Test & Maint Observation, Operational Safety Verification & Security IR 05000458/19880161988-07-27027 July 1988 Insp Rept 50-458/88-16 on 880620-24.No Violations or Deviations Noted.Major Areas Inspected:Liquid & Gaseous Effluent Release Program & Allegations Re Training & Qualifications of Supervisory Personnel ML20151G0971988-07-15015 July 1988 Insp Rept 50-458/88-13 on 880501-0630.Violation Noted.Major Areas Inspected:Previous Insp Findings,Nrc Bulletins 88-001 & 88-007,NRC Info Notices,Surveillance Test Observation, Maint Observation & Safety Sys Walkdown 1990-09-27
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000458/19990121999-10-19019 October 1999 Insp Rept 50-458/99-12 on 990822-1002.Non-cited Violations Noted.Major Areas Inspected:Operations,Engineering, Maintenance & Plant Support ML20212L9771999-10-0505 October 1999 Notice of Violation from Insp on 990710.Violation Noted:From 990224-0325,River Bend Station Operated in Mode I Without Three Operable EDGs IR 05000458/19990101999-09-15015 September 1999 Insp Rept 50-458/99-10 on 990830-0903.No Violations Noted. Major Areas Inspected:Licensed Operators Requalification Program IR 05000458/19990081999-09-0808 September 1999 Insp Rept 50-458/99-08 on 990711-0821.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000458/19990111999-08-17017 August 1999 Insp Rept 50-458/99-11 on 990719-23.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000458/19990091999-08-16016 August 1999 Replacement Pages 9-18 for Insp Rept 50-458/99-09 Issued on 990730 ML20210N1901999-08-0404 August 1999 Insp Rept 50-458/99-07 on 990530-0710.One Violation of NRC Requirements Occurred & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee,Operations,Maint,Engineering & Plant Support ML20210K1471999-07-30030 July 1999 Insp Rept 50-458/99-09 on 990510-28 with in-office Insp Until 990701.Noncited Violations Identified.Major Areas Inspected:Review of Licensee Actions Re Testing & Cleaning of Auxiliary Bldg Unit Coolers ML20196L0551999-07-0606 July 1999 Revised Pages 4 of Report Details Section & 2 of Rept Attachment for Insp Rept 50-458/99-03.Corrections Made to Tracking Numbers Assigned to Seven Noncited Violations & to SRO Location During Refueling Activities IR 05000458/19990041999-06-30030 June 1999 Insp Rept 50-458/99-04 on 990412-16 & 28-29.Five Violations Occurred & Being Treated as Noncited Violations.Major Areas Inspected:Portions of Radiation Protection Program,Including Exposure Controls & Radiation Technical & Worker Practices IR 05000458/19990051999-06-18018 June 1999 Insp Rept 50-458/99-05 on 990418-0529.Nonccited Violations Noted.Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000458/19990031999-05-18018 May 1999 Insp Rept 50-458/99-03 on 990307-0417.Noncited Violations Noted.Major Areas Inspected:Operation,Maintenance, Engineering & Plant Support IR 05000458/19990061999-05-15015 May 1999 Insp Rept 50-458/99-06 on 990419-23.No Violations Noted. Major Areas Inspected:Inservice Exam Program Plan & Schedule,Implementation of Program Plan for Facility & Maint & Engineering Followup Review of Previous Insp Findings ML20205A4601999-03-26026 March 1999 Insp Rept 50-458/98-10 on 990222-26.Violations Noted.Major Areas Inspected:Radiation Work Permit Program Implementation from Oct 1997 to Feb 1999 & Problem Identification & Resolution Program as Applied to Program Deficiencies IR 05000458/19990021999-03-26026 March 1999 Insp Rept 50-458/99-02 on 990124-0306.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20205A4131999-03-23023 March 1999 NRC Operator Licensing Exam Rept 50-458/99-301 (Including Completed & Graded Tests) for Tests Administered on 990222- 0303.All 14 Applicants Passed Exams ML20203A5351999-01-27027 January 1999 EN-99-005:on 990201,notice of Proposed Imposition of Civil Penalty in Amount of $55,000 Issued to Licensee.Action Based on Two Severity Level III Violations Involving Design Deficiency,Caused Uncertainty as to Ability of Div I & II IR 05000458/19990011999-01-25025 January 1999 Insp Rept 50-458/99-01 on 990104-08.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Alarm Stations,Communications,Access Control of Personnel,Packages,Vehicles & Assessment Aids IR 05000458/19980201999-01-0707 January 1999 Insp Rept 50-458/98-20 on 981101-1212.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199E2111999-01-0707 January 1999 Notice of Violation from Insp on 981101-1212.Violation Noted:On 971022,radiation Protection Technicians Released One Container with Two Items Contaminated Above Limits Specified in Procedure RSP-0213 ML20199A2161999-01-0505 January 1999 Notice of Violation from Investigation Conducted on 971231. Violation Noted:On 971015,A Wells,Employee on Entergy Operations,Inc,Submitted to NRC Info Known to Be Inaccurate in Some Respect Matl to NRC ML20198T0691999-01-0505 January 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:Info Was Provided to Senior Resident Inspector That Was Not Complete & Accurate in All Matl Respects Re 971010 of RWP 97-0002 ML20203A6601999-01-0505 January 1999 EN-99-001:on 990105,notice of Proposed Imposition of Civil Penalty in Amount of $55,000 Issued to Licensee.Action Based on Severity Level III Violation Involving Superintendent of Radiation Control at Licensee River Bend Station Facility ML20198N9311998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress IR 05000458/19980161998-12-29029 December 1998 Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress ML20198N9151998-12-29029 December 1998 Notice of Violation from Insp on 980720-0807.Violation Noted:On 980724,licensee Made Change to Facility as Described in Safety Analysis Rept,Which Created Unreviewed Safety Question,Without Prior Commission Approval IR 05000458/19980991998-12-22022 December 1998 SALP Rept 50-458/98-99 Canceled.Process Suspended for Two Yrs.No Insp Rept Will Be Issued for Number IR 05000458/19980181998-11-30030 November 1998 Insp Rept 50-458/98-18 on 980920-1031.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20196G5161998-11-25025 November 1998 Insp Rept 50-458/98-10 Has Been Canceled.No Insp Rept Will Be Issued IR 05000458/19980191998-11-20020 November 1998 Insp Rept 50-458/98-19 on 981019-23.No Violations Noted. Major Areas Inspected:Operations IR 05000458/19980131998-10-27027 October 1998 Insp Rept 50-458/98-13 on 980608-12,22-26 & 0824-28.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations,Maint & Engineering IR 05000458/19980141998-10-21021 October 1998 Insp Rept 50-458/98-14 on 980928-1002.No Violations Noted. Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000458/19980171998-10-0505 October 1998 Insp Rept 50-458/98-17 on 980809-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980151998-08-28028 August 1998 Insp Rept 50-458/98-15 on 980628-0808.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20154L7021998-08-17017 August 1998 Corrected Notice of Violation from Insp Completed on 980218. Corrected NOV Sent to Make Consistent with Ltr Sent on 980722 & to Make Clear That No Response Required ML20236V2081998-07-29029 July 1998 Notice of Violation from Insp on 980517-0627.Violation Noted:On 980601,while Accomplishing Clearance Order 98-0583, Operator Did Not Follow Sequence Shown on Clearance Order While Positioning Components IR 05000458/19980121998-07-29029 July 1998 Insp Rept 50-458/98-12 on 980517-0627.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20154M5531998-07-22022 July 1998 Notice of Violation from Investigation Completed on 980323. Violation Noted:On 970908,WJ Ginn,Employee of Contractor to Entergy Operations,Inc,Deliberately Submitted Info to Licensee That Was Incomplete & Inaccurate ML20154L7351998-07-22022 July 1998 Notice of Violation from Investigation Completed on 980218. Violation Noted:On 970711,DL Brown Employee of Contractor to Util Deliberatly Submitted Info to Licensee That Brown Knew Incomplete & Inaccurate on Security Questionnaire IR 05000458/19980071998-06-0808 June 1998 Insp Rept 50-458/98-07 on 980518-21.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring Programs IR 05000458/19980081998-06-0505 June 1998 Insp Rept 50-458/98-08 on 980405-0516.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000458/19980111998-06-0404 June 1998 Insp Rept 50-458/98-11 on 980518-21.No Violations Noted. Major Areas Inspected:Maint IR 05000458/19980061998-05-19019 May 1998 Insp Rept 50-458/98-06 on 980427-0501.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radioactive Effluent Waste Mgt Program IR 05000458/19980091998-04-30030 April 1998 Informs That Insp Rept 50-458/98-09 Has Been Canceled ML20217A4461998-04-17017 April 1998 Notice of Violation from Insp on 980222-0404.Violation Noted:Established Measures Did Not Assure That Deviation from Environ Design Criteria Was Controlled ML20217A4801998-04-17017 April 1998 Insp Rept 50-458/98-05 on 980222-0404.Violations Noted. Major Areas Inspected:Operations,Main,Engineering & Plant Support PNO-IV-98-016, on 980413,operators at River Bend Station Initiated Normal Reactor Shutdown.Plant Shutdown Deemed Necessary After Operators Identified Main Generator Hydrogen Seal Oil Leak at Main Generator Casing1998-04-14014 April 1998 PNO-IV-98-016:on 980413,operators at River Bend Station Initiated Normal Reactor Shutdown.Plant Shutdown Deemed Necessary After Operators Identified Main Generator Hydrogen Seal Oil Leak at Main Generator Casing ML20217B4701998-03-24024 March 1998 Notice of Violation from Insp on 980223-26.Violation Noted: Licensee Not Maintained Records of Reviews of Radiation Protection Program Content & Implementation ML20217B4951998-03-24024 March 1998 Insp Rept 50-458/98-03 on 980223-26.Violations Noted.Major Areas Inspected:Review of Radiation Protection Program Activities IR 05000458/19972011998-03-20020 March 1998 Fire Protection Insp Rept 50-458/97-201 on 970615-20, 0629-0703,0819,980120 & 0305.No Violations Noted.Major Areas Inspected:Comprehensive Evaluation of Fire Protection Program & Post Fire Safe Shutdown Capability 1999-09-08
[Table view] |
Text
'
.
APPENDIX C U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
NRC Inspection Report: 50-458/85-51 CP: CPPR-145 Docket: 50-458 Licensee: Gulf States Utilities (GSU)
P. O. Box 2951 Beaumont, Texas 77704 Facility Name: River Bend Station (RBS)
Inspection At: River Bend Station, St. Francisville, Louisiana Inspection Conducted: June 16 through August 15, 1985 Inspector - ._ . 42*(# //2O 7 8 85 rlain, Se(ior Resident Inspector Date
. f. Qia (pdrs.1, ,3,4,5,5',7,8,9,and15)
f+c 47-r- sh/tc Date W. R. Bennett, Reactor Inspector (pars. 1, 2, 10, and 11)
/_ & W 9f/8'
Date
' ,~ Reactor Inspecto (pa .{arbu 1, , 12, and 14)
bh/l 9//8/85 W. M. KcNbill, Reactor Inspector Dtite /
(pars.Iand13)
h h G
.I-
_- - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ .
-
.,
-2-Yn J. E. Bess, Reactor Inspector /
j&l ~
YW fY Eate '
(pars. I and 9)
W3M H. F. Bundy, Reactor 4Wspector MWrs Date (pars. l' and 2)
/
Approved: , . /?42 e f/d/8b
"
, chief,tProject Section A, Date J./P. (daud IReactor ojects Branch Inspection Summary Inspection Conducted June 16 through August 15, 1985 (Report 50-458/85-51)
Areas Inspected: Routine, unannounced inspection of licensee action on previous inspection findings, site tours, fuel transfer operations witness, preoperational test program implementation, initial fuel loading procedure review, River Bend Unit 2 site restoration work implementation, pipe supports anti restraints system testing, allegation follow up, maintenance procedures review, preoperational test results evaluation, high energy / moderate energy line break system review, reactor vessel and internals record review, licensee identified construction deficiency review, and facility review committee (FRC)
system operability review. The inspection involved 325 inspector-hours onsite by six inspector Results: Within the areas inspected, one violation was issued in the area of fuel transfer operations witness (failure to follow an administrative procedure, paragraph '4)' and one deviation was identified in the area of
.
.
preoperational test results evaluation (failure to meet FSAR test commitment, l paragraph 11).
T
.
.
e-2-Details
., Persons Contacted
,
'
Principal Licensee Employees K. Arnstedt, Quality Assurance (QA) Engineer
- H. Cahill, Jr. , Senior Vice President,~ River Bend Nuclear Group
- T. F. Crouse, QA Manager P. J. Dautel,' Licensing Staff Assistant
, C.:Deddens, Vice President, River Bend Nuclear Group
- D. R. Derbonne, Supervisor, Startup and Test
- S. L.-Driscoll, Supervisor, Radiological Engineering
,
S. Finnegan, Control Operating Foreman
.P. E. Freehill, Superintendent, Startup and Test
.
- D. R. Gipson, Assistant Plant Manager, Operations P. D. Graham, Assistant Plant Manager, Services R. W. Helmick, Director, Projects
- B. E. Hey, Licensing Engineer K. C. Hodges, Supervisor, Quality Systems
-
D.~ Jernigan, Engineer, Startup and Test
- G. R. Kimmell, Supervisor, Operations QA
- V. King, Supervisor, Plant Services
- A. D. Kowalczuk, Assistant Plant Manager, Maintenance
- T. L. Plunkett, Plant Manager J. G. Propson, Electrical Supervisor, Nuclear Plant Engineering S. R. Radebaugh, Assistant Superintendent, Startup & Test S. F. Sawa, Control Superintendent, Startup & Test
- J. E. Spivey, QA Engineer R. B. Stafford, Director, Quality Services K. E. Suhrke, Manager Project Planning & Coordination L. Sutton, QA Engineer
- P. F. Tomlinson, Director, Operations QA R. West, Supervisor, Startup and Test Stone and Webster D. P. Barry, Superintendent of Engineering F. W. Finger, III, Project Manager, Preliminary Test Organization (PTO)
P. H. Griffin, Site Advisory Manager
- B. R. Hall, Assistant Superintendent, Field Quality Control (FQC)
R. L. Spence, Superintendent, FQC General Electric S. Garg, Principal Engineer
F-
.
.
L
.
I-3-The NRC senior resident inspector (SRI) also interviewed additional licensee, Stone and Webster (S&W), and other contractor persor.nel during the inspection perio * Denotes those persons that attended the exit interview conducted on August 22, 198 NRC inspector, W. B. Jones, also attended the exit intervie . Licensee Action on Previous Inspection Findings (Closed) Open Item (458/8408-01): Determine if and how the diesel generator loading restrictions of calculation 12210-E-122 are implemented in plant' operating procedure Calculation 12210-E-122 was superseded by calculation 12210-E-192,
" Standby Diesel Generator Loading Calculation." Revision 1 to calculation E-192 was issued on August 7, 1985, to determine the maximum continuous loads to be supplied by the Division I and II standby diesel generators (EG1A and EG1B) during a loss of coolant accident (LOCA) concurrent with a loss of offsite power (LOP) and assuming a single failure of Division I, II or III. diesel generator Three load profile curves were generated and all three require operator action to drop certain loads 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after LOCA initiation prior to the adding of certain~ manually initiated load The SRI reviewed Abnormal Operating Procedure A0P-0004, " Loss of Offsite Power," Revision 2, to determine that the diesel generator loading restrictions of calculation E-192 were implemente All of the load restrictions from the load profile curves were implemented by A0P-000 This item is close (Closed) Unresolved Item (458/8408-04): Review of licensee program for tracking of commitments to the NR This item remained open for the SRI to evaluate the GSU method of identifying commitments that require closure prior to fuel 1 ca Many commitments made to the NRC include a committed date for completion and the committed date becomes the internal action completion date for tracking purposes. For items with no committed completion date, GSU nuclear licensing makes the determination whether the item requires closure prior to fuel loa The SRI reviewed the list of items that GSU nuclear licensing has determined can be completed after fuel load and no concerns were identifie This item is close , (Closed) Open Item (458/8415-01): Development of a. qualification matrix for project engineering and nuclear plant engineering personne .
.
-4-The SRI was provided copies of the qualification matrixes for selected project engineering and nuclear plant engineering personnel and back up documentation for completed training. The qualification matrixes included education,. experience, and training requirements. All
.
records reviewed were in orde This item is close (Closed) Open item (458/8424-02): Concern with the seismic adequacy of plastic tie wire supports used in combination with ~ spade type terminations in the control roo General Electric letter GSS-4676 dated June 13, 1985, confirms that the seismic testing of control room and other panels utilizing the spade lug with plastic tie wrap supports has been verified for seismic adequacy. The letter refers to design record file A00-579 for qualification documentatio This item is closed, (Closed) Violation (458/8512-02): Control of temporary alteration Corrective action included auditing of all temporary alterations and
. assigning dedicated personnel to control entries to the temporary alteration log and to verify correct installation and/or removal of temporary alterations. The NRC inspector verified the implementation of these corrective action This item is close (Closed) Open Item (458/8513-02): Issuance and approval of procedures for scheduling preventive maintenanc The NRC inspector reviewed procedures for scheduling' preventive maintenance and discussed the system with licensee personnel. The preventive maintenance system is considered adequate at this tim This item is close (Closed) Open Item (458/8522-02): Requirement for notification of quality control (QC) prior to the start of safety-related maintenance wor Administrative Procedure ADM-0028, " Maintenance Work Request,"
Revision 4, now states that "Q.C. shall be notified prior to performing safety-related "Q" maintenance and maintenance on the Radwaste, Radiation Monitoring and Fire Protection Systems."
This item is closed.
u- _
~
-
J
.
,
+1-5- (Closed) Open Item (458/8522-03): A program has not yet been established for reviewing completed corrective maintenance records to assess the adequacy of the preventative maintenance program, to identify repetitive failures of parts and components, and to identify design deficiencie Administrative Procedure ADM-0048, " Performance Monitoring and Trend Analysis. Program," Revision 0, was issued on July 29, 1985, to establish "the program for monitoring plant, system or component performance and trending data as necessary to identify losses in MWe output, optimize plant performance and meet various performance monitoring and trending commitments." This monitoring includes such things as performance evaluations of power system efficiencies, vibration monitoring, and monitoring of failures of specific plant component This. item is close (Closed) Open Item (458/8522-04): Licensee has not established a definition of acceptable locking devices for valves and circuit breaker Administrative Procedure ADM-0020, " Plant' Key Control," Revision 1, establishes definitions of acceptable locking devices for valves and circuit breakers. These include a chain and padlock for locked valves, a padlock or other key locked restraining device for locked
' breakers and wired for sealed valve This item is close (Closed) Open Item (458/8522-05): The procedure which provides for
. tabulating performance data for motor operated valves was still in draft for Procedure CMP-1253, "Limitorque Motor Operated Valves'," Revision 2, was issued on July 25,-1985. Appendix A of this procedure provides a tabulation of motor operated valve data which includes torque to open and close valves, torque switch type, motor size, motor voltage,. full load amps, locked rotor amps, and valve stroke tim ,
This item is~ close (Closed) Open Item (458/8522-06): Procedure CMP-1026 is currently being revised to provide for tabulation of data pertinent to elec- -
trical breaker overload relays, heater size, breaker size, and. trip setting.
a____-___= _ _ _ . _ -
r
.
.
-6-f
,
'
Procedure CMP-1026, " Corrective Maintenance of MCC Starters,"
Revision 2, was issued on July 25, 198 Appendix A of this procedure provides a tabulation of data for electrical breakers which
' includes overload relay NEMA size, heater size, breaker size, and breaker trip settin This item is close . (Closed) Open Item (458/8522-08): GSU has not identified which motor operated valves have operators with nonlocking gears or brake assemblie GSU conducted a review of all motor operated valves at River Bend and determined that they all have self-locking gears and none of the valves have brake assemblie This item is clcse (Closed) Open Item (458/8522-09): Establishing a master schedule for preventive maintenanc The NRC inspector determined that a master schedule for preventative maintenance is being utilized at this tim This item is close (Closed) Open Item (458/8522-11): Cleanness classifications of plent systems have not been establishe This item involved a failure to establish cleanliness grades for all systems and inclusion of these grades in ADM-0018. This was accom-plished in ADM-0018, Revision 1. However, the NRC inspector ident-ified several apparent discrepancies in the program for the cleanin of fluid systems and associated components as follows:
.
Section 4.2 of ADM-0018 states that the mechanical maintenance supervisor assigns cleanness grades. Section 5.1.1 of GM-0062, Revision 0, states that the general maintenance supervisor or designee assigns cleanness grade There appears to be a potential conflict of interest in either instance in that an individual who may be responsible for cleaning has been author-ized to establish acceptance criteri Also, it appears that assignment of cleanness grades should be an engineering functio . Grades of cleanness are defined in procedures ADM-0018, MSP-0013, and GMP-006 These definitions are not identica .
I im .
'
.
-7-
. ANSI N45.2.1-1973 requires that cleanness inspection personnel be qualified per ..NSI N45.2.6. Procedure GMP-0062 is not clear on who.should sign for inspections and what qualifications the inspectors should hav Open item 8522-11 is closed with the resolution of the above noted discrepancies considered an open item. (458/8551-03) (Closed) Open Item (458/8522-13): Surveillance testing and calibra-tion control program'does not yet include the inservice testing /inspec
,
tion requirements of 10 CFR Part 50.55(a).
There are two major testing / inspection programs scheduled to be in place at River Bend. One is the surveillance test procedure (STP)
program and the other is the in service inspection (ISI) progra The STP program deals with the functional performance and operability of systems and components required by technical specifications and the ISI program deals with nondestructive examination of components and pump and valve testing required by 10 CFR Part 50.55(a). ISI activities are generally covered by ISI procedures, however, 'there are some activities required by the ISI plan that are covered by STPs. These activities would include visual inspections, functional testing of' mechanical snubbers, and inspections of certain pumps and valves. In these instances, performance of the activities would be tracked in both the ISI and STP programs. As noted previously, a master schedule for surveillance testing / calibration has been established, but the River Bend 10 year ISI plan has not been submitted to the NRC. Per discussions with NRC licensing, the SRI was informed that the submittal of the ISI plan will be made.a low power testing license condition for River Ben Since the submittal of the ISI plan will be tracked as a license condition, this open item is closed, (Closed) Open Item (458/8522-31): Responsibility for reporting design changes and modifications to the NRC has not been establishe CFR Part 50.59 requires an annual report to the NRC of changes to the facility as described in the safety analysis report, River Bend Administrative Procedure ADM-0010, " Station Reporting Requirements",
identifies the requirement for an annual written report per 10 CFR Part 50.59(b) to be submitted to NRC Region IV and the Director of Inspection and Enforcemen This item is close (Closed) Open Item (458/8523-01): "Q list" was not inclusive and the procedures for control and use of the "Q list" were not approve ,_ ._ -. . . _ _
. _ _ _ ___
_
-
-8-
'
The following nuclear plant engineering (NUPE) procedures for control and.use of the "Q list" have been approved and issued:
. NUPE AA-64, Revision 0, " River Bend Station Instructions and Requirements for Use of th_e~ River Bend Q-List"
. NUPE-AA-63, Revision 0, " Control and Maintenance of the River Bend Q-List" The procedures state that all River Bend project personnel are responsible for using the Q-list to determine whether a system',
structure, component or an activity relating to a system, structure, or component is safety-related. Activities which may be safety-related, and therefore shall include use of the Q-list to determine such,' include designing, purchasing, fabricating, handling, shipping, storing, cleaning, erecting, installing, inspecting, testing, operating, maintaining, repairing, refueling, and modifyin Revision 0 of the Q-list has been issued and the list is still not all inclusiv However, Q-list users are required to contact NUPE.if a desired mark number is not located in the Q-list to determine whether the component is safety-related or no This item is close (Closed) Violation (458/8523-02): Preoperational test procedure-1-PT-210 was approved for performance without the procedure being stamped to establish notification points for operations quality assuranc The test procedure was immediately stamped to establish notification points for operations quality assurance. Although the procedure was not stamped, project quality test group personnel were notified and were present during the conduct of testing. Also, in order to prevent recurrence of this violation, startup and test personnel-received special training on the requirements of test instruction-(TI) -8, " Conduct of Testin This item is close (Closed) Violation (458/8523-03): The procedure used for the conduct of the HVAC systems duct leakage testing at River Bend did not require the use of a temperature indicating device and no temperature monitoring was conducted during leak testing performanc S&W mechanical test procedure 1.MPGEN.003, "HVAC Pressure and Leak i Test Procedure for ANSI 509/510 Ductwork," was written to include the '
requirement for use of a " temperature indicating device accurate and l
'
-
r-
.
.
.
.-9-i readable to + or - 0.5 F. All previously tested safety-related ductwork is being retested utilizing the new procedure. This 100%
retest of safety-related ductwork is being monitored by the SRI as an NRC open item (458/8523-05).
This item is close (Closed) Violation (458/8523-04): The gas meter used for HVAC duct
' air leakage testing at River Bend was not calibrated in the range of us All safety-related ductwork is being retested utilizing mechanical test procedure 1.MPGEN.003, "HVAC Pressure and Leak Test Procedure for ANSI 509/510 Ductwork," which uses the pressure decay method for
- determining the leakage rate instead of the gas meter method. . This 100% retest of safety-related ductwork is being monitored by the SRI as an NRC open item (458/8523-05).
This item is close .
' Site Tours The SRI toured areas of the site during the inspection period to gain
,
knowledge of the plant and to observe general job practices. The site tours conducted-included special tours on separate occasions with Mr. R. P. Denise (NRC Region IV Division Director) and Mr. R. D. Martin
_(NRC Region IV Regional' Administrator). The SRI also made several tours ,
of.the-containment and toured the suppression pool while it was drained for cleaning. During the tours it was noted that a number of tags remain on system components (e.g.,' jurisdictional tags', hanger as built tags, caution tags', etc.). The SRI discussed this with licensee management and action has been initiated to remove all tags that are no longer required for the operational phase activitie The removal of unnecessary equipment tagging will be an open item (458/8551-04).
No violations or deviations were identified in this area of inspectio . Fuel Transfer Operations Witness The SRI witnessed portions of the new fuel transfer from the spent fu'el pit to the containment refueling floor storage area. The licensee trans-ferred 200 fuel bundles through the inclined fuel transfer system in preparation for fuel loading of the reactor. During the witness of the fuel transfer operation, the SRI reviewed procedural documentation for TCN 85-1131 to procedure FHP-0005, " Fuel Transfer Tube Operations," which was required for conduct of fuel transfer operation It was noted by the SRI that the TCN was not stamped "TCN SHIFT SUPERVISOR APPROVED COPY"
f:
i
.
,
-10-in red ink and the fuel transfer evolution was being conducted even though the TCN was not followed exactly , which is in violation of administrative procedure ADM-003, " Development, Control and Use of Procedures,"
Revision 6. This failure to follow an administrative procedure was identified as a violation (458/8551-01). The licensee took immediate action to halt fuel transfer operations and to correct the procedural deficiencies identified. No other problems were identified with the fuel transfer operatio . Preoperational Test Program Implementation This area of inspection was conducted to assure that current design documents were being.used by test personnel for test development and conduct and to review the control of design change packages. The licensee startup program requires that all preoperational test procedure reference revisions be identified at the time of procedure development and that the latest revision be noted and checked for test impact at the time of test performance. This revision check is then administratively performed again during the review of test result The SRI checked 30 document references for the reactor protection system preoperational test and the correct revisions were verified at the time of test performanc The review of design change control packages revealed that in addition to the design requirements for review, approval and control of engineering and design coordination reports (E&DCR), the licensee has established a method of assembling design modification packages (DMP) to assure that all required actions are implemente No violations or deviations were identified in this area of inspectio : Initial Fuel Loading Procedure Review The SRI reviewed procedure 1-ST-3, " Fuel Loading," Revision 0. Several concerns and questions were generated as a. result.of this review primarily relating to the general prerequisites of the procedur All of the concerns and questions were discussed with the responsible startup and test personnel, and it was noted during these discussions that Major Change Request (MCR) No. 1 to the procedure had been issued and some of the concerns were already addressed by MCR-1. Subsequent to the discus-sions, MRC-2 to the procedure was issued to address the remaining concerns and questions of the SRI. MCR-1 and 2 addressed such concerns as:
. Composition of fuel handling crew
. Clarification of prerequisites for radiation monitoring and nuclear instrumentation
. Prerequisite for inspection of fuel
,
.
-
.
,
-11-
. Prerequisite for containment status
. Prerequisite for reactor pressure vessel status
. Prerequisite for cleanliness requirements
. Addressed moderator temperature monitoring
. Addressed action for unexpected neutron flux or detector response behavior
. Referenced procedure for lowering of SRM setpoints The SRI believes that the initial Fuel Loading Procedure 1-ST-3, Revision 0, as amended by MCR 1 and 2, is consistent with licensee commitments, regulatory requirements, and applicable codes and standard No violations or deviations were identified in this area of inspectio . River Bend Unit 2 Site Restoration Work Implementation A Board Order dated November 20, 1984, states, "That applicants' request to withdraw without prejudice the application to operate River Bend Station Unit 2 is granted, and the proceeding is terminated as to Unit 2, subject to.NRC. Staff approval of the implementation of site restoration work described in applicants' June 1984 Report on Termination of Construc-
-tion."
NRC Region IV will monitor GSU implementation of the Unit 2 site restora-tion work and will notify the NRC Office of Nuclear Reactor Regulation, Division of Licensing, upon completion of the verificatio NRC Region IV will track this activity as an open item (458/8551-05). Pipe Supports and Restraints System Testing This area of inspection was conducted to review the licensee programs pertaining to the examination and testing of safety-related pipe support and restraint systems. The SRI review of this area revealed that two '
separate programs exist at River Bend, one for the General Electric.(GE)
scope of supply and one for the S&W scope of supply. A review of these programs. revealed that they both covered the following elements: Examination of piping support systems at various temperatures to detect interference to thermal expansio Setting and calibration of snubbers, restraints, and vibration arrestors at predetermined temperature E ,
l
.
t-12- Examination of pipe support and restraint systems during transient l testing to ascertain that pipe motion and vibration are within design limit l Conduct af vibration tests, including resolution of high vibratio Displacement measurements at ambient and operating temperatur It was noted during this review that the GE program contained limits for expected minimum and maximum pipe movement and the S&W program only contained limits for expected maximum pipe movement. This was discussed by the SRI with responsible personnel, and the S&W program was modified to include expected minimum and maximum pipe movemen Any pipe movements that. exceed the expected minimum or maximum limits must be evaluated by GE or S&W engineerin .No violations or deviations were identified in this area of inspectio . Allegation Follow Up (Closed) Allegation: The NRC inspector reviewed and conducted a followup inspection on the concerns of an allegation made to GSU which could have an impact on plant safety. The following is a summary of this activity:
Allegation: The alleger stated that the "as wired" signal / ground circuit configuration of Rosemount trip units located in the control room PGCC panels does not comply with the Rosemount Instrument Manual Instruction in that~ signal common is not electrically isolated from chassis commo Signal common and earth common are tied together through a common earth groun This condition is causing spurious tripping of trip units when an adjacent unit is withdrawn from or inserted into a card fil Followup In'spection: The NRC inspector interviewed responsible personnel and reviewed available_ data to ascertain if a problem or problems existed which may have_an impact on plant safety. The NRC inspector reviewed the Rosemount Instrument Manual and examined the signal circuits in the Rosemount instrument panels. There were no discrepancies identifie However, after talking to several S&W, Gulf States Utilities (GSU), and GE personnel; it was noted that a conflict had been identified between a GE drawing for grounding and the "as installed" conditions. The conflict appeared to be that the GE drawing required the instrumentation ground to be isolated. The "as installed" configuration showed the instrument ground bus, the signal common bus, and the chassis ground bus to be connected to the floor section instrument ground bu The disposition of this conflict involved revising the GE drawing to reflect the "as installed" conditions of the panels. The NRC inspector reviewed GE Field
> Deviation Disposition Request (FDDR) No. LDI-3128, Revision 0, which was issued to evaluate and resolve this conflict. The NRC inspector also
_.
.
-13-reviewed. documentation relating to instrument calibration problems. The problem according to the PGCC engineering groups resulted from grounding busses being overloaded. A total of 42 FDDRs were issued to break up the
-
busses, install larger wiring, and correct various cases of improper connection The NRC inspector randomly selected FDDRs to verify work completion and no discrepancies were identifie In' addition to the grounding problem, the NRC inspector inspected the alleger's concerns pertaining to the spurious trip The NRC inspector reviewed the following documentation for the Rosemount Trip / Calibration System:
. Instruction Manual - Trip / Calibration System Model 510 DV
. Elementary Wiring Diagram - Low Pressure Core Spray System
. Functional Block Diagram - Master Trip Unit The situation was also discussed with responsible GSU and GE personne GSU conducted a number of bench tests of the Rosemount trip units with various grounding arrangements in order to evaluate the spurious trip proble As a result of these tests, it was determined that the Rosemount trip units may produce random false trips and false alarms anytime one of these units is pulled (unplugged) from service. Isolation of the signal common did not appear to correct the problem. It should be noted that the false trips occur in trip units of a single channel which alone would not cause any plant trip, equipment trip or safety actuatio The NRC inspector reviewed the GE position (FDDR No. LDI-3178).which indicates that this problem appears to be an inherent design characteristic of the'
Rosemount trip units and is not caused by improper signal / ground circuit
. configuration. GSU action that is ongoing for this problem includes short term action to establish administrative controls for corrective / preventive maintenance of the Rosemount trips units ~which requires. installing the calibration read out assembly or removing a card from a card fil Maintenance procedures will be revised to identify trip units that may be affected during maintenance and to require the technician to notify the
~
nuclear control operator prior to start of the maintenanc A long term solution is being pursued through ongoing engineering evaluatio Conclusion: Based o_n the above, the alleger's concerns with the grounding / bus problem was substantiated, but GSU was working ~to resolve the problem. The PGCC grounding problems have now been resolved and verified as not being the cause of the spurious trip The spurious- trip problem does exist, but it is not considered a safety problem due to the following:
. Once a trip unit is initially calibrated and tested it is not frequently remove . . - - - .
~
.
-14-
. Spurious trips occur in single channels only and single safety channels do not cause any plant trips, equipment trips or safety actuatio . Administrative controls are being implemented to provide technician and operator awareness of the potential for spurious trips and alarms
,
during the conduct of maintenance.
i
'
Therefore, this allegation is closed, but the NRC inspector will monitor the implementation of the administrative controls and monitor the engineering evaluation for a long term solution to the spurious trip problem. This will be tracked as an open item (458/8551-06).
10. Maintenance Procedures ,
The objective of this portion of the inspection was to confirm that the plant maintenance procedures are prepared to adequately control maintenance of safety-related systems within applicable regulatory requirements.
>
The NRC inspector reviewed the following procedures:
Procedure Title Revision Date f GMP-0077 Gasket Replacement and 0 1/16/85 Maintenance of Gasketed Surfaces TCn85-691 5/31/85 GMP-0081 Valve Maintenance 0 2//04/85 Program CMP-1001 Corrective Maintenance 1 7/07/85 of Potential Transformers CMP-1030 Battery Cell Jumpering 2 5/04/85 and Replacement TCN 85-088 5/09/85 CMP-1031 Activation and Initial 1 4/15/85 Charging of Dry-Charged Stationary Batterie CMP-1074 Corrective Maintenance of 1 7/06/85 RHR Pump Motors CMP-1245 Corrective Maintenance of 0 3/29/85 Emergency Diesel TCN 85-317 5/27/85
.
Generators
!
. . . - - - . - - . , - . - - - - . - . - - - - . - . . - _ . . . . - , .. -
- - - , . . - , , - -
.
,
-15-CMP-9107 Emergency Diesel Starting 2 6/26/85
~ Air Compressor, Disassembly, Inspection, Rework, and Reassembl CMP _-9144 - Main Steam Relief. Valve 2 6/26/85 Disassembly,. Inspection, Rework, and Reassembl CMP-9033 C11-0001 Hydraulic Control 2 6/25/85 Unit Component Removal, Dis-assembly, Inspection, Rework, Reassembly, and Inspectio MCP-4066 Calibration of Rosemount 1 3/28/85
.
Model 1151 Transmitter
'
-
MSP-0003 . Preventive Maintenance 2 5/01/85 Program MSP-007 Maintenance Planning 1 6/07/85
!and Scheduling The NRC inspector found several typographical errors in the maintenance U
procedures and notified the licensee of these error The maintenance
>
, _ procedures were found to be adequate for the desired maintenance. .The_NRC inspector, utilizing the procedure review and interviews with maintenance personnel, determined that the preventive maintenance system is in the process of being established and is working at this tim No violations or deviations were identified in this portion of the inspectio +
1 Preoperational Test Results Evaluation The objective of this portion of the inspection was to assure that the licensee is performing an adequate evaluation of test results and to ascertain-that the licensee had adequately tested the remote shutdown system with results as follows: The NRC inspector reviewed completed Preoperational Test Procedure 1-PT-210, " Integrated Emergency Core Cooling System and Loss of Offsite Power." Review determined that the test did not ensure that the RHR system would realign and inject to the reactor vessel from the test mode as committed to in the River Bend FSAR. This is an apparent deviation (458/8551-02). Subsequent discussion with startup-and test personnel revealed that the realignment and injection from the. test mode was not performed because of possible RHR pump'run ou The NRC' inspector questioned if this was a concern during an actual loss of coolant accident and if this was addressed in the accident analysis. This is considered an open item (458/8551-07).
, - -
.
.
.
-16- The NRC inspector reviewed the licensee's preoperational test results documented in procedure 1-PT-200, " Remote Shutdown System," (RSS),
and in the RSS portions of procedures 1-PT-202, " Automatic Depressur-ization System," and 1-PT-552, " Containment Monitoring System." It was determined that the RSS appeared to have been tested in accordance with the. requirements of-the licensee's startup manual (SUM), that the acceptance criteria had been met, and that test exceptions had been properly _dispositioned and closed with the following exception:
. Test Exception - 21 and the corresponding acceptance criteria, step 10.9, were still outstanding. The problem is that an interlock between two motor operated valves in the residual heat removal (RHR) system mandatory flow path to the pressure vessel, does not exist when control of these valves is trans-ferred to the RSS panel. The valves are 1E1Z*M0VF0278 (278) and IE12*MOVF0428 (428). The interlock is designed to prevent over pressurization of the RHR system during routine surveillance
'
cycling of these valves by preventing the manual opening of either valve if the other valve is not fully shu The NRC inspector considered.this to be an open item (458/8551-08)
pending NRC review of the disposition and closure of this T . High Energy / Moderate Energy Line Break System Review The purpose of this area of inspection was to verify that the hardware associated with the design modification package (DMP-4) based on the high energy line break (HELB) detection and mitigation and the moderate energy line break (MELB) detection and mitigation had been installed and teste The NRC inspector reviewed a sample of the completed work documents and generic test data and visually inspected several temperature sensors and level sensors in'the plant (comparing them to the documents reviewed). It was concluded that DMP-4 appeared to have been properly implemented. The NRC inspector also determined that the special situation test (SST-53) for DMP-4 had been completed but was still undergoing licensee revie . Completion of the licensee review of SST-53 test results will remain as an open item (458/8551-09).
~
No violations or deviations were identified in this area of inspectio . Reactor Vessel and Internals Record Review The objectives of this inspection were'to review a sample of reactor vessel and internals records and determine whether (a) the licensee system forfpreparing, reviewing, and maintaining records is functioning properly; (b) the selected records reflect work accomplishment consistent with NRC requirements and SAR commitments; and'(c) the records indicate any potentially generic problems, management control inadequacies,'or other weakness that could have safety significanc ,
, -- - - - - - , - - - - - -,,.,n,p = - - , . , - , , , - - , - . ~ - . .
.-
,
-17-The sample established for the inspection included steam separators, steam dryers, shroud,- jet pumps, control rod drive (CRD) housings, in-core housings, core plate and top guide in addition to the reactor vessel (RV).
The material certifications and receipt inspection of these components were reviewed. The records found on file were a~ GE product quality certification, ASME code reports, deviation report, certified material test reports (CMTRs) and NDE reports of welds. A number of errors were identified in these records. GE certification No.2645 was found to have an erroneous serial number (2007) for an in-core housing. A revised certification, No.10868, was issued by GE to correct these errors. The Sun Shipbuilding and Dry Dock Company data packages were found to have some errors. The shroud package did not have penetrant test (PT) reports for long seams L1 through L3 of the top flange rings (piece No. 5) although r6diographic test (RT) reports were on file for the same welds. The top guide package had a report on the repair of cubicle side walls. It documented that two heats of weld metal had been used (12051 and 16004C);
although the package had a CMTR for heat No. 16004C, it did not have a CMTR for heat No. 12051. Also in the same package were RT reports for long seams LS1 through LS8, but PT reports for only six seams for the water seal ring. The steam dryer had only a product quality certification and no additional data (e.g., CMTRs). It was noted that there was no product quality certification on file for the steam separator (non-code part) nor were there code forms, CMTRs, etc. for the CRD housing (code parts). CRD housing records are reportedly on file at GE, Wilmington, North Carolin The installation and inspection of installation records were reviewe These records were inspection reports of the RV and internals alignment, bolting, cleanliness, rigging and etc. It was noted that the RV was received with much of the internals installed (e.g., core plate, top guide, jet pumps CRD, and in-core housings. Storage records of the RV were reviewed to verify proper storage of the RV. In this regard the equipment storage history cards, maintenance check records and warm air system check logs were reviewed. It was noted that logs of the tempera-ture checks covered a time period from June 1981 to August 1983, however, the filter checks went on to June 1984 with a break in these filter records from January 1984 to April 1984. The RV was subsequently installed and inspected. This inspection indicated that the RV had been properly stored. In regard to the record problems identified above, open item (458/8551-10) was issued. The errors above are being followed by GSU Q The NRC shall review in a later inspection GSU review of NSSS records supplied by GE and the NSSS records to assure that no significant problems exist in these record . Licensee Identified Construction Deficiency Review This area of inspection was conducted to review action taken on the following licensee identified construction deficienc , -
,...-
-18-(Closed) Construction Deficiency Report DR-295: '" GE AKD-6 480 V Switchgear".
F
. Initial NRC notification date: March 27, 198 . Final - report: GSU letter RBG-21680 of July 24, 198 The corrective action for this reportable deficiency was to inspect the charging mechanisms. on the 28 breakers in question and-to correct any problems foun Part of this corrective action was to functionally test the breakers after repairs were made. A review of rework documentation by the NRC inspector revealed that all 28 breakers had been inspected, repaired, and tested as require . This item is close . Facility Review Committee (FRC) System Operability Review-This area of inspection was conducted to determine how the licensee was evaluating any remaining system related open items to determine the potential effect on system operability. The licensee has established a program for. the FRC to review outstanding system open items and to identify any~ items that potentially effect system operability. These FRC identified system operability items then require resolution prior to declaring the-system operabl The SRI reviewed several systems that had received the FRC: operability review and the program for system operability review is commendable. The potential sources of system open items (e.g., master punch _ list, nonconformance reports, engineering and design coordination reports, etc.) are being reviewed and any work items and/or paper items
,
- that could~effect system operability are being identified for resolutio I
'No violations or deviations were identified in this area of inspectio . Exit Interview t -
An exit interview was conducted on August 22, 1985, with licensee '
representatives (identified in paragraph 1). During this
~
interview, the SRI reviewed the scope and findings of the inspectio ,
A gs v- eme- e- - - -g-e,,i-,,we,y 9 -* v- w -e-we-- r---yy,y.--, - - . , , , ,,-,y-g.94 -,- ,...y-,iry,+v-e.-+-eg9-+e --w-,e-9 9 m +.yS- . - , - me<-