ML20198N931

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Insp Rept 50-458/98-16 on 980730-0807.Violations Noted. Major Areas Inspected:Engineering & Fire Protection.Also Reviewed,Status of Various Programs Which Were Planned or in Progress
ML20198N931
Person / Time
Site: River Bend Entergy icon.png
Issue date: 12/29/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20198N889 List:
References
50-458-98-16, NUDOCS 9901060254
Download: ML20198N931 (55)


See also: IR 05000458/1998016

Text

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-458

License No.:

NPF-47

Report No.:

50-458/98-16

Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station

Location:

St. Francisville, LA

Dates:

July 20 through August 7,1998

Inspectors:

M. Runyan, Reactor Inspector, Engineering Branch

P. Goldberg, Reactor inspector, Engineering Branch

R. Bywater, Reactor inspector, Engineering Branch

P. Qualls, Fire Piotection Engineer

D. Wigginton, Project Manager

R. Fretz, Project Manager

Accompanying

T. Tinkel, Consultant

Personnel:

R. Cooney, Consultant

Acproved By:

T. Stetka, Acting Chief, Engineering Branch

Division of Reactor Safety

ATTACHMENT:

Supplemental Information

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9901060254 981229

PDR

ADOCK 05000458

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TABLE OF CONTENTS

EX ECUTIVE SU M MARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

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Report Details . . . . . . . . . . . . . . . . . . . . . . . .

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111. Engin e e rin g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

E1

Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

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E1.1

Standby Gas Treatment System . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

E1.2 4.16 kV Electrical Distribution System . .

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E1.3 High Pressure Core Spray System . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

E1.4 Condition Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

E1.5 Temporary Alterations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

E2

Engineering Support of Facilities and Equipment . . . .

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E2.1

Evalcation of 10 CFR 50.59 Safety Evaluation Program . . . . . . . . . . 14

E4

Engineering Staff Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . 16

E4.1

General Engineering Experience and Competence . . . . . . . . . . . . . 16

E8

Miscellaneous Engineering Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

E8.1

(Closed) Inspection Followup Item 50-458/9621-01: Entergy Operations,

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Inc., Resolution of Quality Assurance Program Required for Resource

S ha rin g . . . . . . . . . . . . . . . . . . . . . . . . . .

... ....... 17

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E8.2 (Closed) Inspection Followup item 50-458/9622-01: Adequacy of Molded

Case Circuit Breaker Trip Setpoints . . . . . . . . . . . . . . . . . . . . . . . . 17

E8.3 (Closed) Inspection Followup Item 50-458/9627-02: NRR to Review

Near-Buoyant Objects . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ..... 18

E8.5 (Closed) Licensee Event Reoort 97-007: Cracked Screw Assembly

Swivel Pads on Emergencj Diesel Generators Could Have Prevented

Fulfillment of Safety Function . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

E8.6

Engineering Backlog .

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E8.7

System Engineering . .

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E8.8

USAR Review Program . . . . . . . . . . . . . . . . . . . . . . . .

....... 21

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E8.9 Year 2000 Computer issue . . . . . . . . . . . . . . . . . .

.... 22

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IV. Plant Support . . . . . . . . . . . . . . . . . . . . . . .

.... 23

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F8

Miscellaneous Fire Protection Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

F8.1

(Closed) Unresolved Item 50-4J8/97201-01: Smoke detector application,

placement, and installation in fire area C-24 does not meet requirements

of License Condition 2.C.10 .

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F8.2

(Closed) Unresolved item 50-458/97201-02: Failure to include fire

protection check valves in a functional testing program . . . . . . . . . . . 23

F8.3

(Closed) Unresolved item 50-458/97201-03: Lack of engineering

evaluations to establish the fire-rating or fire-resistant capabilities of fire-

rated boundaries. . . . . . . . . . . . . . . . . . .

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F8.4

(Closed) Unresolved item 50-458/97201-04: Outdated equipment and

failure to assign personnel to the fire brigade who have normal plant

duties that do not conflict with their response to a plant fire. . . . . . 26

F8.5

(Closed) Unresolved Item 50-458/9720105: Failure to perform an

adequate operability assessment and provide appropriate compensatory

measures for conditions affecting the functionality of post-fire safe-

shutdown capability. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

F8.6

(Closed) Unresolved item 50-458/97201-06: Failure to perform an

adequate post-fire safe. shutdown analysis that meets the licensee

commitment to Sections Ill.L.1, Ill.L.2, and Ill.L.7 of Appendix R to

10 CFR Fad 50 . . .

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F8.7

(Closad) Unresolved nam 50-458/97201-07: Deficiency in the design of

the reactor overpressure protection system, under certain postulated

conditions, could lead to inadvertent actuation of 16 SRVs resulting in an

un-analyzed plant transient . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

F8.8

Othe r FPFi lssues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

F8.8.2 Control of Combustible Materials . . . . . . . . . . . . . . . . . . . . . . . . . . . .33

V. Manag e m ent M e e ting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A

XI

Exit Me etin g Sum mary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

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EXECUTIVE SUMMARY

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River Bend Station

NRC Inspection Report 50-458/98-16

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t uring the period of July 20 through August 7,1998, an engineering and fire protection

inspection was conducted onsite. The safety system engineering inspection was performed on

the standby gas treatment system, the 4.16 kV electrical distribution system and the high

prestare core spray system. in addition, a followup inspection of previous inspection findings

was conducted in engineering arc. ; ire protection. The team also reviewed the status of various

programs which were planned or in progress.

Overall, the team determined that engineering activities were generally effectively implemented.

This determination was based on calculations, modifications, and condition reports that

exhibited sound engineering practices.

Enaineerina

The quality of recent design calculations showed improvement over earlier design

calculations, in that they contained more detail and were sufficient to facilitate an

independent review of the design. The older calculations were found to be adequate

after consultations with licensee engineers (Section E1.1.2).

The team concluded that the 4.16 kV electrical distribution system was well designed

and its design basis was well documented. The methodology used in updating older

calculations was a strength (Section E1.2.2).

No discrepancies were identified for the surveillance testing of the 4.16 kV electrical

distribution system. The time delay relay settings for loss of power instrumentation

surveillances were ir. correctly listed in the Updated Safety Analysis Report; however,

these settings were correctly stated in the Technical Specifications and in the

associated surveillance procedures (Section E1.2.3).

A problem was observed in the relief valve setpoint program, in that data sheets, with

values often differing from the design cold set pressure, had been used in one case to

set a relief valve, resulting in an improper setting. The licensee quickly recognized the

error, which did not introduce a safety concern, and corrected it (Section E1.4).

The team observed that two failures of the high pressure core spray system discharge

relief valve had occurred within the past four years. The licensee was still in the process

of determining the root cause (Section E1.4).

The temporary alteration program was effectively implemented. However, in response

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to NRC questions, the licensee determined that containment temperature had, on one

occasion. dropped to 60 degrees Fahrenheit compared to an assumed design minimum

temperature of 70 degrees Fahrenheit. The licensee initiated a condition report to

resolve the implications of this discrepancy (Section E1.5).

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Overall, the 10 CFR 50.59 program was found to be satisfactory. However, the failure

to identify as an unreviewed safety question an increase in the calculated doses for a

loss of coolant accident as reported in the updated safety analysis report was identified

as a violation of 10 CFR 50.59. Specifically, the exclusion area thyroid dose increased

from 32.8 to 37.8 rem, and the low population zone thyroid dose increased from 50.3 to

115.1 rem (Section E2.1).

The team concept developed in system engineering was effective because the

assignment of several individuals to each system increased the overall level of expertise

and provided more flexibility in supporting operations (Section E8.7).

Plant Support

The failure to provide a procedure for using standby service water for fire protection was

identified as a noncited violation (Section F8.2).

The condition where a postulated fire could have potentially caused all 16 safety relief

valves to open due to a fire-induced circuit failure was identified as a violation for failure

to implement the provisions of the fire protection program as required by Operating

License Condition 2.C.10. However, the licensee identified the violation and committed

to perforrn a modification to correct the condition during the April 1999 refueling outage.

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in accordance with Section Vll.B.6 of the NRC's Enforcement Policy, the NRC exercised

discretion and did not propose a civil penalty nor issue a violation in this case (Section

F8.6).

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Report Details

Summary of Plant Status

The unit operated at full power during the onsite portion of the inspection.

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E1

Conduct of Engineering

E1,1

Standby Gas Treatment System

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'E1.1.1 System Descriotion

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Mechanical

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in the post-accident mode following a design basis accident (DBA), standby gas

treatment system (SGTS) fans draw down and maintain a negative pressure in the

containment annulus and auxiliary building. The technical specifications (TS) require

the SGTS to draw down the annulus to a negative pressure of at least 0.5 inches water

glass (wg) within 18.5 seconds of system initiation and to draw down the auxiliary

building to a negative pressure of at least 0.25 inches wg in 13.5 seconds. Air removed

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from these areas is processed through the SGTS filter train before it is discharged to the

atmosphere. The filter train processes potentially contaminated air from the annulus

and auxiliary building following a DBA to limit thyroid and whole body dose to within the

limit 1 of 10 CFR Part 100 at the site boundary (exclusion area boundary) and

low! population zone outer boundary. Following initial draw down, the SGTS is designed

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to maintain a negative pressure of less than 0.5 inches wg in the annulus and less than

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O.25 inches wg in the auxiliary building continuously for 100 days.

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Electrica;

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The major components of this system receive electric power from 480 volt standby

buses 1EJS*LDC 1 A&2A (Red Train) and 1EJS*LDC 1B&2B (Blue Train). These 480

voit buses are in turn fed from 4.16 kV standby buses ENS-SWG 1 A&1B respectively,

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which are provided off site power via 230 kV-4.16 kV Reserve Station Service

Transformers RTX-XSR 1C&1D. The 4.16 kV buses may also be provided with power

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by emergency diesel generators (EDGs) 1EGS-EG1 A & 18 when power is not available

from the grid.

The air-operated fan and filter inlet and outlet dampers are operated by 125 volt de

solenoid valves. On a loss of de power, the dampers fail open. Red train solenoids are

supplied power by de bus EMB-SWG01 A and blue train solenoids are supplied power by

de Bus EMB-SWG01B.

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The 480 volt fans and the filter heater circuit breakers have solid state tripping devices,

which operate on overcurrent. The breakers are also tripped by load shed signals.

The fans are started automatically by load sequencer signals, by Radiation

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Monitor RMR-RE103, and by loss of air flow from the opposite-train fan.

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E1.1.2 Desian Review

a.

Insoection Scoce (93809)

Mechanical

The team exam'ned portions of various documents that discussed the safety and

design basis of the SGTS. These documents included the Updated Safety Analysis

Report (USAR), TS, the system requirements documents, calculations, drawings, and

condition reports (CRs). Additionally, discussions of various related topics were

conducted with licensee engineeru.

Electrical

The team reviewed one-line diagrams to assure that redundant components were fed

from separate buses and reviewed one calculation involving the fan flowswitches.

b.

Observations and Findinas - Mechanical

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USAR Fidelity

The team's review of the USAR identified a few examples of incorrect information in

the SGTS sections. USAR Section 6.2.3.2.1, stated that the SGTS fan receives

power from the EDG within 38 seconds after the design basis accident (DBA) (i.e.,

30 seconds plus 8 seconds for the fan to attain rated speed). A review of other

documentation (e.g., Calculations ES-194-3," Auxiliary building pressure following a

loss-of-coolant accident (LOCA)," Revision 3, and G13.10.2.7*23, " Shield building

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annulus following a LOCA," Revision 1) and discussions with engineering personnel

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confirmed that the 38-second value was incorrect. The correct value was 48 seconds,

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The incorrect 38-second value also appeared in Table 6.2-34 and Figure 6.2-61b.

USAR Section 6.2.3.3, discussed the positive pressure period (PPP) for the annulus and

auxiliary building. The PPP is the time following a DBA that the pressure is more

positive than -0.25 inches wg. The USAR stated that the PPP for the auxiliary building

was 111 seconds. A review of other documentation and discussions with engineering

personnel confirmed that the 111-second value was incorrect. The team noted that the

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associated procedures were not affected by this USAR discrepancy.

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The licensee had already identified these errors during their ongoing USAR

programmatic review, but the USAR had not yet been updated at the time of this

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inspection. The team determined that the errors did not result in a safety concern. The

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licensee was also aware of some additional SGTS USAR errors, and License Change

Notice (LCN) 15.06-006 was in process to correct them. The failure to update the

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USAR was considered to be a violation of 10 CFR Part 50.71(e). This failure constitutes

a violation of minor significance and is not subject te formal enforcement action.

Calculations

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The team found that certain older River Rend Station (RBS) calculations for SGTS

lacked sufficient explanation and detail in some areas to permit an independent review

without obtaining additional information.

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The team reviewed Calculation BV45.22-1," Fan External Total Pressure Fans

1GTS*FN1 A & FN1B Annulus and Auxiliary Building Exhaust, Accident Mode,"

Revision O. This calculation was designated safety-related. The pressure drop

calculation for node 4 to 5 used an input value of 2.269 inches wg based on

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Calculation BV45.20-1, " Fan External Total Pressure 1GTS*FN1 A & FN1B

Containment /Drywell Purge Exhaust, Normal Operation Mode lil," Revision 1. A cross

check of Calculation BV45.20-1 did not reveal how the 2.269 inch water value was

determined. When presented with this observation, the licensee informed the team that

after performing their own review, they determined that the result of this portion of the

calculation was correct as stated. The team verified that the calculation was correct.

However, the licensee agreed that the calculation lacked sufficient detail to readily

understand how the 2.269 inches wg value was derived in this portion of the calculation.

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The licensee stated that this information would be added to Calculation BV45.22-1.

The team reviewed Calculation PB-251,"To Determine the In-Leakage and Amount of

Exhaust Air Required To Maintain A Negative Pressure of 1/4 in. W.G. in the Aux. Bldg,"

Revision 0. This was a safety-related calculation. The team noted that the calculation

was overly conservative in determining the time to achieve negative pressure in the

auxiliary building. This resulted in an oversized fan being specified. The licensee agreed

with the team's observation that the oversized SGTS fan would create a larger negative

pressure condition in the auxiliary building than otherwise required by the design. While

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the team noted that plant operation and testing confirmed this observation and that this

condition did not represent a safety concern, the team also noted that the higher

negative pressure caused door passage problems. The team considered this problem

to be a burden for site personnel The effect of this condition on plant operations is

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further discussed in Section E8.2 of NRC Inspection Report 50-498/9805.

The team reviewed Calculation G13.18.2.1*079-00," Evaluation of Standby Gas

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Treatment System Drawdown Data," Revision 0. This was a recently prepared

safety-related calculation that was representative of the quality of calculations currently

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being prepared by the licensee. This calculation was considered to be well written and

exemplified the team's general impression that the technical quality of calculations was

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improving.

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Observations and Findinas - Electrical

The team reviewed Calculation IA-GTS*1,"Setpoint Calculation 1GTS*FS 24A & B,"

i'ievision 4, which was the safety-related setpoint calculation for the flowswitches that

monitor airflow from Fans 1GTS*FN 1 A&18. No discrepancies were identified in this

review.

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Conclusions

Some portions of the USAR contained incorrect information in the sections affecting the

SGTS. The licensee had previously identified these errors and was in the process of

correcting them. Some older SGTS calculations lacked sufficient detail to permit a

meaningful independent review, without obtaining clarification from licensee personnel.

The quality of more recent calculations showed improvement over earlier calculations.

E1.1.3 Surveillance Testina

a.

Inspection Scope (93809)

The team examined portions of selected documents that discussed surveillance test

requirements for the SGTS. Primarily, these documents were the TS and condition

reports (CRs) that addressed issues related to SGTS surveillance test results. Selected

requirements found in the evaluation of the CRs were compared to corresponding TS

requirements for consistency.

b.

Observations and Findinas

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No areas of concern were identified during this review.

c.

Conclusions

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The team concluded that the surveillance testing program with respect to the SGTS was

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satisfactory.

E1.1.4 Desian Modifications

a.

Insoection Scope (93809)

The team reviewed four engineering requests (ERs) that documented plant

modifications affecting the SGTS. In add un to the documentation for the particular

modification, other documentation contained or referenced in the ER documentation

packages were selectively reviewed. These documents included 10 CFR 50.59

screenings and evaluations, calculations, and LCNs.

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b.

Observations and Findinas

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No areas of concern were identified during this review.

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Conclusions

The team determined that the plant modification program with respect to the SGTS was

satisfactory.

E1.2 4.16 kV Electrical Distribution System

E1.2.1 System Descriotion

The standby power system, which supplied Class 1E safety-related motors and

4.16 kV/480 volt load centers, was arranged in three divisions. These divisions were

designated Train A (Red), Train B (Blue), and Train C (Orange).

Train A was supplied power from the 230 kV grid by preferred Station Service

Transformer 1RTX-XSR1C, whereas Train B was supplied from the 230 kV grid via

preferred Station Service Transformer 1RTX-XSR1D. Train C was supplied power from

1NNS-SWG1C, which in turn was supplied by either 1NNS-SWG1 A or 1NNS-SWG1B.

Those switchgear sections were supplied from the 230 kV grid by either Station Service

Transformer 1RTX-XSR IC or 1D. Each of the divisions was also provided with an

emergency diesel generator (EDG).

E1.2.2 Desian Review

a.

Inspection ScoDe (93809)

The team reviewed System Design Criteria Document SDC-302 ENS," Safety Related

4.16 kV Electrical Distribution System Design Criteria," Revision 0, seven design basis

calculations, seven CRs, two ERs, four one-line diagrams, the USAR, and seven

surveillance test procedures (STPs). The team assessed technical adequacy,

consistency, and completeness of the system. The team also conducted a walkdown of

the 4.16 kV switchgear.

b.

Observations and Findinas

The team determined that the system design criteria document was satisfactory in

scope and accuracy. The criteria clearly described the safety function of the Class 1E

standby buses. The criteria also addressed the supply of nonsafety-related plant

auxiliaries that require a reliable power supply and were therefore fed from the safety-

related buses.

Most of the calculations reviewed by the team were performed originally by an

architect / engineer. The licensee was in the process of updating most of these

calculations. The newly revised calculations were observed to be of considerably better

quality than the originals. The team considered the licensee's ongoing efforts to update

the existing electrical calculations to be a strength.

No discrepancies were identified during the system walkdown.

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c.

Conclusions

The team concluded that the 4.16 kV electrical distribution system was well designed

and documented. The methodology used in updating older calculations was a strength.

E1.2.3 Surveillance Testing

a.

Inspection Scope (93809)

The team reviewed Procedure STP-302-1601, " ENS-SWG1 A/B Loss of Voltage

Channel Calibration and Logic System Functional Test," and the resultant data from

procedure performance.

b.

Observations and Findinas

The tearn observed that the surveillance test results for STP-302-1601 were satisfactory

for the last three times it was performed.

The team identified discrepancies associated with time delay relay settings in the

loss-of-power instrumentation surveillance tests listed in TS Table 3.3.8.1-1. There

were inconsistencies among the values in this table and those reported in the USAR and

the STPs. USAR Section 8.3.1.1.3.9 lated the second time delay associated with

degraded voltage for Divisions 1 and E as 50 seconds, whereas TS Table 3.3.8.1-1

listed this time as 60 seconds. The same 'ISAR Section listed the time delay

associated with Loss of Voltage for Division 3 es 2 seconds while item 2.b of the TS

Table 3.3.8.1-1 listed this time as 3 seconds. The USAR Section listed the first time

delay associated with Division 3 degraded voltage as 10 seconds whereas item 2.e of

the same TS table listed it as 3 seconds.

The licensee responded to the team's observation with documentation that indicated

that the values in the USAR were in error and that the TS and surveillance procedures

were correct. The team agreed with the licensee's response and noted that since the

TS and the surveillance test procedures were correct, the error had not affected the

validity of past surveillance tests. In response to the team's finding, the licensee

initiated CR 98-1004, which identified the discrepant condition and recommended that

the USAR be revised to agree with the TS. This failure to correct the USAR error was a

violation of 10 CFR 50.71(e). This failure constitutes a violation of minor significance

and is not subject to formal enforcement action. In addition, since the licensee's review

of the USAR was in progress and, because additional reviews by the licensee in this

USAR section were pending, the team considered it likely that this inconsistency would

have been discovered and corrected independently by the licensee.

c.

Conclusions

in a limited sample, the team did not identify any discrepancies in surveillance testing of

the 4.16 kV electrical distribution system. Some USAR discrepancies, which were not

safety significant, were identified during this review.

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E1.2.4 Desian Modifications

a.

Insoection Scoce (93809)

The team reviewed Modification Requests 86-0595 and 86-1119.

b.

Observations and Findinas

Modification Requests 86-0595 and 86-1119 involved changing time delay relay settings

used in EDG starting circuits. The modification requests were complete and included

satisfactory safety evaluations.

c.

Conclusions

Based on review of the selected modification requests, the team concluded that these

modifications of the 4.16 kV electrical distribution system were satisfactory.

E1.3 Hiah Pressure Core Sorav System

E1.3.1 System Description

Mechanical

The high pressure core spray (HPCS) system is one of the four subsystems that

comprise the emergency core cooling system (ECCS) that cools the reactor following a

loss of coolant accident (LOCA). If the break is small, the HPCS system is designed to

maintain coolant inventory as well as vessel level while the reactor coolant system is still

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pressurized. If the water levelis not maintained by the HPCS system, the automatic

depressurization system (ADS), low pressure coolant injection (LPCI) system, and/or the

low pressure core spray (LPCS) systems are automatically initiated.

The HPCS system consists of a pump, discharge piping fill pump, injection valve, spray

sparger head, other system piping and valves, suppression pool suction strainer, system

instrumentation and controls, and electrical switchgear and power supplies. The system

is designed to operate from normal offsite auxiliary power or from an emergency diesel

generator (EDG) if offsite power is not available.

The HPCS system cerves as a backup to the reactor core isolation cooling (RCIC)

system to maintain the reactor water level in the event the reactor becomes isolated

from the main condenser during operation and feedwater flow is lost.

Electrical

The HPCS pump motor receives electric power from Division 3,4.16 kV standby bus

E22*S004. The motor-operated valves that are part of the HPCS system are supplied

power from standby MCC 1E22*S002, which is fed from the Division 3,4.16 kV bus via

4.16 kV /480 volt transformer 1E22*S003. Although not part of the HPCS system, the

standby service water (SSW) pump motor (SWP-P2C) is also supplied power from bus

E22*S004. The normal supply to E22*S004 is from 1NNS-SWG10, which in turn is

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supplied by either 1NNS-SWG1 A or SWG18. Both of these buses are supplied from

the 230 kV grid via preferred station service transformers 1RTS-XSR1C or XSR1D.

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When the normal supply to E22*S004 is lost, the EDG supplies power to the system.

125 volt dc power is provided to the diesel generator and to E22*S004 from battery

1 E22*S0018AT via 125 volt de bus 1 E22*PNLS001.

E1.3.2 Deslan Review

a.

Insoection Scoce (93809)

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The team examined portions of various documents that discussed the safety and design

basis of HPCS. These documents included the USAR, TS, system requirements

documents, calculations, drawings, and test reports. Additionally, discussions on

various ietated topics were conducted with engineering personnel.

b.

Observations and Findinas

USAR Fidelity

The review of the USAR identified one example of incorrect information in the HPCS

sections. Table 6.3-1 stated that at 30 seconds following the start of a DBA LOCA, the

HPCS injection valve is open and the pump is delivering design flow, completing HPCS

startup. Based on a review of other portions of the USAR and discussions with the

licensee, the 30 second value was determined to be incorrect. The correct value was 27

seconds. Upon additional review, the licensee determined that this was an

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administrative error and that the 30 second value should have been removed with other

changes addressed by LCN 06.03-030 dated December 12,1997. This failure to

correct the USAR was a violation of 10 CFR 50.71(e). This failure constitutes a violation

of minor significance and is not subject to formal enforcement action. The licensee

initiated CR-98-1001 to document the incorrect 30 second value in Table 6.3-1 and

indicated that an LCN to change the USAR would follow. The EDG loading calculations

were not affected by this error.

Calculations

The team reviewed Calculation G13.18.2.2*031-0," Net Positive Suction Head (NPSH)

Available for ECCS Pumps for Suction from the Suppression Pool Under Accident

Conditions,* Revision 0. This calculation supported analysis of a recent major design

modification that installed new design ECCS suction strainers in the suppression pool.

The team determined that this calculatic? was satisfactory.

System Desian Criteria

The team reviewed the HPCS system design criteria. One example was found where

the information was inconsistent with the USAR. Section 3.3.1 of the system design

criteria addressed the HPCS pump and stated that the minimum required net positive

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suction head (NPSH) for the pump was 2 feet at a reference location 36 inches above

the pump mounting base plate. A review of the manufacturer's test report T-36631-1,

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"HPCS 15 Stage Pump Performance Curve (Byron Jackson)," June 29,1977, indicated

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that the NPSH required was 1 foot, referenced to 3 feet c.bove the mounting flange.

USAR Table 6.3-13 likewise stated that the HPCS NPSH required was 1 ft at 3 ft above

the mounting flange. The licensee stated that this portion of the system design criterion

was covered by an open item listed in the back of the system design criteria that

indicated that an update was required because of the ECCS suction strainer

modification (i.e., the error was scheduled to be corrected). Because this error did not

affect the analytical design of the plant, the team noted that the discrepancy did not

constitute a safety concern.

Setooint Calculations

>

The team reviewed Calculations 1 A-E22*04, "Setpoint Calculation HPCS Condensate

Storage Tank Low Level," Revision 2, and 1 A-E22'05, "Setpoint Calculation

1E22*ESN655C & G," Revision 4. The methodology used in both setpoint calculations

was in accordance with applicable standards. The team did not observe any

assumptions that were not acceptable and considered these calculations to be

satisfactory,

c.

Conclusions

One portion of the USAR contained incorrect information in the sections affecting

HPCS. One example was found in the HPCS system design criteria where information

was inconsistent with respect to the USAR. Three calculations supporting the HPCS

design were observed to be satisfactory.

E1.3.3 Surveillance Testina

a.

Inspection Scope (93809)

The team examined portions of selected documents that discussed surveillance test

requirements for the HPCS system. These documents included the TS, surveillance

test procedures (STPs), and related CRs.

b.

Observations and Findinas

The team examined selected requirements in the STPs were compared to

corresponding requirements to assure consistency. In addition, selected test results

were reviewed to compare for consistency with the corresponding procedure and to

confirm that the results were within acceptance limits. No areas of concern were

identified during this review.

c.

Conclusions

The team determined that the surveillance testing program with respect to the HPCS

system was satisfactory.

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E1.3.4 Desian Modifications

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a.

Insoection Scope (93809)

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The team reviewed three engineering requests (ERs) describing plant modifications that

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affected the HPCS system.

' b.

Observations and Findinas

No areas of concern were identified during this review. The team determined that the

plant modification program with respect to the HPCS system was satisfactory.

c.

Conclusions

The team determined that the plant modification program with respect to the HPCS

system was satisfactory.

E1.4 Condition Reports

a.

Insoection Scoce (37550)

The team reviewed Procedure RBNT-030, " Initiation and Processing of Condition

Reports," Revision 12. In addition, the team reviewed 46 CRs associated with the

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' SGTS, the HPCS system, and the 4.16 kV electrical distribution system. The team

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discussed the CR process and some of the CRs with licensee personnel.

b.

Observations and Findinas

The team determined that the CR process provided a single process for documenting

the evaluation and resolution of problems, concerns, activities, and conditions that could

adversely affect or have the potential to adversely affect the safe operation of the plant.

As an overall observation, the team found that the licensee was using the CR program

successfully, in most cases, corrective actions were complete and well documented.

The team reviewed CR 97-1881, dated October 20,1997, and CR 97-2131, dated

December 18,1997. The first CR, CR 97-1881, stated that the set pressure of the

HPCS diesel generator starting air relief valves was set too low and reset them from

250 to 270 psig by means of Maintenance Action item Number 313888. The licensee

concluded that the setpoint was incorrect because the valve data sheet listed the

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setpoint as 270 psig. The inservice test procedure correctly listed the spring set

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pressure as 250 psig. At the time, the licensee erroneously assumed that the setpoint

value in the inservice test procedure was not correct. The second CR, CR 97-2131,

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documented that the relief valves were incorrectly set at 270 psig. The licensee initially

concluded that the maintenance personnel incorrectly read the setpoint data sheet.

However, subsequent to this finding, the licensee realized that the new set pressure

was incorrect and promptly installed valves with a setpoint of 250 psig. The team

reviewed a number of safety and relief valve data sheets for setpoints and compared

these values with the spring set pressure listed in Procedure STP-000-6606,"Section XI

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Safety and Relief Valve Testing," Revision 6. The procedure defined the cold differential

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test pressure as the inlet static pressure used for bench testing the valve. This set

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pressure was adjusted for back pressure and temperature. The team noted that the

valve data sheets contained only the process setpoint, not the cold differential test

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pressure. Out of 31 data sheets reviewed, the team found 13 examples where the

setpoint on the data sheet was different from the cold differential test pressure listed in

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the test procedure. These disparities ware not unexpected because of the differences in

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how the values are derived, but the team noted that, based on the differences noted, the

invalid use of data sheets could result in an incorrect pressure being set in the field.

The team determined that the pressure relief valve set pressure program had a

weakness since, at least in this one case, the valve data sheets were improperly used

for determining spring setpoints. For valves within the ASME Section XI inservice

Testing Program, the surveillance test procedure was required to be used for setting

pressures in the field and the data sheets were for information only. Therefore, this

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problem did not appear to involve a safety concern, and the improper use of the data

sheets appeared to be isolated. However, the licensee agreed that further actions were

needed to correct the noted inconsistencies. The licensee's resolution of relief valve

setpoints was identified as an inspection followup item. (50-458/9816-01)

The team reviewed CR 96-1585, dated August 31,1997, which documented an

electrical spike on the reactor building annulus ventilation radiation monitor, which

caused a ventilation system isolation and autostart of SGTS Train A. The licensee

concluded that the spike was probably due to an electrical noise spike in the detector

circuitry. There were two radiation monitors and the SGTS would start if one of them

alarmed. Since 1995, there had been shc inadvertent starts of the SGTS caused by

false alarms of a radiation monitor. The underlying cause of the problem was an

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actuation logic (one out of two) that did not preclude system actuation from a single

faulty detector. The team identified this situation as an observation but noted that the

inadvertent actuations did not present a safety concern.

The team reviewed CR 97-0804, dated May 29,1997, which documented the failure of

the HPCS pump discharge relief valve. The licensee discovered that the bellows in the

relief valve was broken, which allowed water to exit the weep hole in the valve bonnet.

The licensee performed a root cause inspection and came to a preliminary conclusion

that the bellows failed due to chloride stress corrosion cracking. The licensee consulted

the valve manufacturer who stated that the only bellows failures they had seen were

cause:I by valve cycling, which fatigued the bellows. The vendor stated that they had

not seen a beliows failure due to chloride stress corrosion cracking. During reviews

prompted by NRC questions during the inspection, the licensee determined that the

bellows in the same valve had failed in 1994. The 1994 failure was only documented as

a work request, not as a CR. As a result, the licensee had been unaware that the

bellows failure in 1997 was a repeat failure. The team was concerned that the use of

work requests could preclude the identification of repeat occurrences. Since CR

97-0804 was not yet closed, the licensee initiated another action to discuss the bellows

failure with the system engineer to determine if, during quarterly surveillance testing of

the HPCS pump, the relief valve cycled or chattered. The team noted that the failure of

the bellows would cause the opening pressure of the relief valve to be higher than

intended and, therefore, result in a higher pump discharge pressure. The team

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concluded that even with this postulated pressure increase, the increase would not

damage the system and that the system would still be operable. Review of the

licensee's determination of the root cause of the relief valve failure and the licensee's

review to investigate the possible misuse of the work request system in 1994 was

identified as an inspection followup item (50-458/9816-02).

c.

Conclusions

in most cases, engineering actions in response to CRs were satisfactory. Several

problems involving the relief valve setpoint program and a relief valve failure were noted

and brought to the licensee's attention.

E1.5 Temocrary Alterations

a.

Inspection Scope (93809)

The team reviewed the licensee's temporary alteration program and discussed some of

the safety-related temporary alterations with appropriate licensee personnel, in addition,

the team reviewed Procedure ADM-0031," Temporary Alterations," Revision 8A.

b.

Observations and Findinas

The team noted that the procedure defined a temporary alteration as any temporary

change that did not conform to approved drawings or other design documentation or

changed the design function of the equipment. The procedure specified that a

temporary alteration could not remain open beyond the operating cycle in which it was

installed unless an extension was obtained in accordance with the procedure.

Of the 11 existing temporary alterations,2 were installed in 1995,2 in 1996,3 in 1997,

and 4 in 1998. Two of the eleven temporary alterations were designated as

safety-related.

Temporary Alteration Number 96-025," Removal of Standby Liquid Control System Heat

Trace Capability and Annunciator Function," dated September 12,1996, removed an

annunciator in the control room that was intermittently clarming and considered a

nuisance and also removed power to all standby liquid control system heat trace circuits.

The licensee stated that a pending modification to the plant would eliminate the standby

liquid control system suction line heat trace controls and annunciation in the future.

The team reviewed the safety evaluation for the temporary alteration. When the system

was required to be operable in Modes 1 and 2, the sodium pentaborate se Jtion

temperature was required to be greater than 45 degrees Fahrenheit. The team noted

that with the improved Technical Specifications, the standby liquid control system was

no longer required to be operable in Mode 4 with a control rod withdrawn. The safety

evaluation stated that the ambient containment temperature was adequate to maintain

the solution above the precipitation temperature. In addition,if the ambient containment

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temperature decreased such that the solution temperature approached the 45 degrees

Fahrenheit limit, the tank heaters were available to provide solution heating. The

licensee concluded that because the heat tracing had no function in maintaining the

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system operable or supporting the system response to an accident, there was no effect

on operation of the system with the heat tracing disabled.

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The team questioned if consideration was given to a reactor stanup during winter with a

cold containment temperature and asked to see the minimum recorded containmcat

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temperature. During review of this question, the licensee initiated CR 98-0991 after they

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determined that the environmental design criterion's minimum containment ambient

temperature was 70 degrees Fahrenheit, whereas the minimum recorded containment

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temperature was 60 degrees Fahrenheit. The 60 degrees Fahrenheit temperature was

recorded during an unplanned outage in January and February 1996. The licensee

performed a preliminary review of the qualified equipment in containment. The licensee

found that the equipment reviewed were generally unaffected by temperature values

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below 70 degrees Fahrenheit. Most equipment could be shown to be operable at

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temperatures of approximately 40 degrees Fahrenheit. As noted above, the sodium

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pentaborate solution in the standby liquid control system required a minimum

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temperature of 45 degrees Fahrenheit. The team was satisfied that the standby liquid

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control system had not been adversely affected by this low temperature condition.

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In the CR, the licensee recommended that the basis for the minimum containment

temperature of 70 degrees Fahrenheit be evaluated and revised as necessary. The

licensee also recommended that procedures should be strengthened to provide

guidance to monitor containment temperature and to take actions to maintain

temperatures during cold weather shutdowns. This issue was identified as an inspection

followup item (50-458/9816-03) pending review of the licensee's actions to determine

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whether the 60-degree temperature excursion caused a safety concern, and whether

the 70-degree temperature limit should be reduced to accommodate future anticipated

low temperatures in containment.

Based on the low number of existing temporary alterations and quality of the

documentation, the team determined that the licensee was managing the temporary

alteration program in a satisfactory manner.

c.

Conclusions

The licensee was managing the temporary alteration program in a satisfactory manner.

A question concerning the minimum containment temperature was identified for future

followup.

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E2

Engineering Support of Facilities and Equipment

E2.1

Evaluation of 10 CFR 50.59 Safety Evaluation Prooram

a.

Inspection Scope (37001)

The team reviewed the licensee's 10 CFR 50.59 Safety Evaluation Program in

accordance with Inspection Procedure 37001. This included a review of procedures and

controls, training and qualifications of personnel performing evaluations, and completed

safety evaluations.

b.

Observations and Findinas

Procedures and Controls

The procedure governing the process for conducting 10 CFR 50.59 safety evaluations

was RBNP-057,"10 CFR 50.59 License Basis Reviews and Environmental Evaluations,"

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Revision 7. It implementeo the guidelines recommended in NSAC-125, " Guidelines for

10 CFR 50.59 Safety Evaluations," June 1989, as revised by Nuclear Energy Institute

(NEI) document NEl 96-07, "10 CFR 59 License Basis Reviews and Environmental

Evaluations," dated June 30,1998, Revision 7, to determine whether a proposed

change, test or experiment involved a change to technical specifications or an

unreviewed safety question (USO). Procedure RBNP-057 assigned responsibilities for

individuals allowed to prepare, review, and approve formal safety evaluations as well as

performing 10 CFR 50.59 applicability screenings.

The team reviewed the classifications of procedures identified by the licensee in

Procedure RBNP-057, as requiring screening and/or a 10 CFR 50.59 evaluation prior to

implementing procedure changes. A review of applicable procedures determined that

the licensee's classifications were appropriate.

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The team identified a potential concern with program procer.'ures during review of a

10 CFR 50.59 safety evaluation screening performed for Teroporary Alteration 97-018.

This temporary alteration modified the internals of the control rod drive system flow

control valves, C11-FCVD012A/B. These valves supply seal injection / purge water to the

reactor recirculation pump seals. The temporary alteration was implemented during a

recent outage without a 50.59 evaluation.

The team was concerned that the 10 CFR 50.59 screening did not properly determine

whether a safety evaluation was required. A review of the USAR description by the

team for the recirculation pump seals did not reveal any description of the seal

injection / purge water system. Therefore, since this information was not described in the

USAR, the temporary alteration package screening determination that a 10 CFR 50.59

safety evaluation was not required, was appropriate.

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Trainino and Qualifications

The team reviewed training outlines and materials for the initial and requalification

programs for personnel responsible to prepare and approve 10 CFR 50.59 safety

evaluations. The training materials noted the disagreements between the NRC and the

licensee regarding the definition of " increases in the consequences," as discussed later

in this section of the report.

Imolementation

The team reviewed 18 safety evaluations identified on the most recent Summary Report

of 10 CFR 50.59 changes. For each item, the team reviewed documentation of the

proposed change, the USAR review (including scope of USAR documents reviewed),

technical specification (TS) screening, and appropriateness of the safety evaluation's

conclusions. The team determined that each of these safety evaluations was

catisfactory.

As discussed above, the fusee recently adopted procedure changes, which

implemented NEl 96-07 guidance. All safety evaluations approved by the Facility

Review Committee after this procedure change went into effect (seven evaluations)

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were reviewed in order to determine whether an inappropriate use of an " increase in

consequences" was made.

Safety Evaluation (SEN) 98-0033, " Revise LOCA Calculations," evaluated an LON,

which changed LOCA dose calculation results in USAR Table 15.6-7. The LCN was

prompted from (1) a revision of the positive pressure period (PPP) in response to NRC

Information Notice (IN) 88-76, (2) correction to inaccuracies in the suppression pool

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water volume, (3) addition of a liquid leakage term in response to IN 91-56, and (4)

enhancement of engineered safety features liquid leakage. As a result, exclusion area

thyroid dose increased from 32.8 to 37.8 rem, and low population zone thyroid dose

increased from 50.3 to 115.1 rem. In the 10 CFR 50.59 safety evaluation

documentation, the licensee stated that, " . . . the dose consequences remain below the

regulatory limits of 10 CFR Part 100 and 10 CFR Part 50, Appendix A, General Design

Criterion (GDC) 19 as approved per NUREG-0989 and License Amendment 98." The

licensee's position was that, in the safety evaluation report (SER) for License

Amendment 98, " . . . the NRC's acceptance criteria for the removal of PVLCS are 10 CFR Part 100 and GDC 19, not the specific values calculated by either the NRC or

RBS." This statement conflicted with the NRC's publicly-stated position on increases in

consequences. The team determined that the licensee did not appropriately follow the

current 10 CFR 50.59 rule and should have declared the dose increase to be a

unreviewed safety question (USQ).

The team identified that the licensee's use of NEl guidance for " increases in

consequences"; specifically, the guidance on implied approval of 10 CFR Part 100

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limits, was contrary to NRC requirement because increases in consequences involve a

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USO when established licensee analysis values as reviewed by the NRC are exceeded.

10 CFR 50.59(a)(1) states, in part, that a holder of a license authorizing operation of a

production or utilization facility may make changes in the facility as described in the

safety analysis report without prior Commission approval unless the proposed change

involves an unreviewed safety question.

10 CFR 50.59(a)(2) states, in part, that a change shall be deemed to involve an

unreviewed safety question if the probably of occurrence or the consequences of an

accident previously analyzed in the safety analysis report may be increased.

The implementation of the USAR change as addressed by SEN 98-0033 increased the

consequences of a loss of coolant accident because the calculated doses were

increased. This was considered to be an unreviewed safety question. The failure to

obtain Commission approval prior to creating an unreviewed safety question by

changing the facility as described in the USAR was identified as a violation

(50-458/9816-04).

However, the team also noted that the low population zone thyroid dose increase was a

result of overly conservative assumptions and calculations in response to IN 91-56. The

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IN directly applied to a potential flow path from the safety injection system to the

refueling water storage tanks and the licensee made a number of conservative

assumptions in order to create an analogous flow path from the residual heat removal

(RHR) system to the condensate storage tank. In addition, the licensee did not credit

the standby gas treatment system in their dose calculations. The team also noted that

no regulatory dose limits were exceeded as the result of this USAR change. As noted in

Section XI of this report, the licensee disagreed that this issue constitued a violation of

NRC requirements.

c.

Conclusions

Overall, the 10 CFR 50.59 program was found to be satisfactory. Safety evaluation

documentation was thorough and provided appropriate justification for the conclusions.

in one case, the licensee inappropriately concluded that a USAR change did not involve

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an unreviewed safety question. This was identified as a violation of 10 CFR 50.59.

E4

Engineering Staff Knowledge and Performance

E4.1

General Enaineerina Experience and Competence

a.

Inspection Scoce (37550)

The team interacted with a large number of engineering and licensing staff personnel

during the inspection.

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Observations and Findinas

Based on this inspection effort, the team determined that engineering personnel were

experienced and possessed good technical and plant knowledge. Personnel knowledge

included a good understanding of the engineering processes and organizational

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interfaces involved in controlling, maintaining, and supporting the operating plant.

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Conclusions

Based on the results of this inspection, the team concluded that engineers possessed

good experience levels and competence in completing their assigned tasks.

E8

Miscellaneous Engineering issues (92903)

E8.1

(Closed) Inspection Followuo item 50-458/9621-01: Entergy Operations, Inc.,

Resolution of Quality Assurance Program Required for Resource Sharing

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Backaround

This item was opened to track licensee action on a licensee-identified issue involving the

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lack of clear quality guidelines controlling the procurement of services from one Entergy

site by another Entergy site. The licensee generally used standard procurement

proceaures for this process but often bypassed these controls. This was a concern

because the quality assurance programs varied from site to site.

Inspection Followup

.

To address this concern, Entergy developed Corporate Policy PL-126," Site

Providing Services to Other Sites," Revision 0, dated January 25,1997. Each

Entergy site was to revise their site procedures to be consistent with the corporate

,

policy. Procedure RBNP-093," Control of Shared Services," Revision 0, was developed

)

to implement the corporate policy and was placed into effect on June 22,1998.

Based on a review of Corporate Policy PL-126 and Procedure RBNP-093, which

appeared appropriate for the situation and internally consistent, the team concluded that

the licensee had adequately addressed this issue.

E8.2 (Closed) Inspection Followuo item 50-458/9622-01: Adequacy of Molded Case Circuit

Breaker Trip Setpoints

Backaround

Valve E51-MOVF064, RCIC turbine outboard isolation valve, failed to close because its

supply breaker tripped in response to an instantaneous reversal from an open to a close

demand signal. The licensee's original investigation did not include a review for generic

implications, in response to the NRC concern, the licensee reopened their review to

identify any generic concerns.

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As a separate concern, the NRC noted that the licensee's molded case circuit breakers

were set to trip at a maximum of 11 times the fullload current rather than the value of

1.73 times the locked-rotor current, as recommended by the Electric Power Research

Institute (EPRI). This was a concern because some high speed motors can have

locked-rotor currents approximately 10 times the full load current. Consequently, a

current of 11 times the full load current could be as low as 1.1 times locked-rotor current

for these motors.

The safety concern for both issues discussed above was that inadvertent breaker trips

could preclude the capability to remotely operate essential motor-operated valves.

Inspection Followup

The licensee issued CR 96-1110A to investigate the NRC concerns. The outcome of a

study of the locked-rotor and full load current for all safety-related high speed (>3400

rpm) motors was that 14 molded case circuit breakers were either adjusted or the trip

coils were replaced.

As a secondary corrective action, the licensee identified an additional 48 molded case

circuit breakers that had instantaneous trip coil settings that were less than 150 percent

of the measured inrush current. Of these,14 breakers had been adjusted with the

remainder to be completed by the end of 1999.

The licensee was confident that once the scheduled breaker adjustments are complete,

all of the breakers would have settings greater than the EPRI recommended 1.73 times

the locked-rotor current.

The licensee identified 19 motor-operated valves that could be susceptible to circuit

breaker trips during reversals in direction of travel. In each case, the ramifications of

this phenomenon were shown to be minimal because of administrative controls, such as

limiting conditions for operation being in effect, operators stationed locally, or other

administrative controls. The trip of Valve E51-MOVF064 occurred during a refueling

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outage under a limiting condition for operation.

The team determined that the licensee had acceptably addressed the concerns

regarding molded case circuit breaker settings, pending additional operating experience

that may, potentially, necessitate additional actions. The team determined that the

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licensee had not violated any plant procedures within this scenario of events.

E8.3 (Closed) inspection Followuo item 50-458/9627-02: NRR to Review Near-Buoyant

Objects

Backaround

The NRC identified a concern that objects of specific gravity slightly greater than water

(near-buoyant) could be carried by a tornado into the SSW cooling tower and be carried

into the suction of the SSW pumps. This matter was referred to the NRC program office

for further review.

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Inspection Followuo

The NRC program office determined that licensees do not have to specifically address

the effect of near-buoyant debris to meet design mquirements of cooling water supplies

unless a significant source of such material exists in the vicinity and is capable of

becoming airborne due to a tornado. The team determined that a source of

near-buoyant materials, r,uch as paper, grasses, hardhats, etc., were not present in

sufficient quantities near the plant site. Even if these materials were carrieo into the

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cooling tower, the team noted that the licensee would have some tims (a matter of days)

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to clear the debris to ensure adequate long-term cooling.

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E8,5

(Closed) Licensee Event Report 97-007: Cracked Screw Assembly Swivel Pads on

Emergency Diesel Generators Could Have Prevented Fulfillment of Safety Function

Backaround

The licensee issued CR 97-1647, " Swivel Pads on Cylinders 1 and 2 of the Div 11 Diesel

Generator have Cracks," on September 28,1997. The licensee discovered that six

valve adjusting screw assembly swivel pads (VASASPs) on the Division i emergency

diesel generator (EDG) and four VASASPs on the Division 11 EDG were cracked. The

VASASPs work in conjunction with the valve adjusting screw assemblies, which are

threaded screws that allow a fine adjustment of the valve clearances on the EDG. A

failure in this system could cause a loss of EDG function. Although the VASASPs were

cracked, they were functional and could have supported continued EDG operation.

However, as a conservative measure, the licensee declared both EDGs inoperable. The

plant was in Mode 5 at this time and the licensee entered the appropriate limiting

condition for operation. Within 4 days, all VASASPs, whether cracked or not, on both

EDGs had been replaced, and both EDGs were declared operable.

Inspection Followuo

The team reviewed the licensee event report and CR 97-1647. In the root cause

determination, the licensee, in consultation with the manufacturer, determined that the

cracks resulted from three conditions: (1) the material lot used to manufacture the

VASASPs was incorrect and had lower toughness than desired for the application, (2)

the swaging of the VASASPs socket over the ball of the valve adjusting screw

assemblies was performed to an excessive degree during the manufacturing process,

and (3) the ball on the valve adjusting screw assembly of at least one of the cracked

assemblies had an edge that helped to precipitate the crack. The licensee inspected

the replacement units before they were installed and determined that none of them were

affected by any of the above three conditions. This determination was supported by

discussions with the manufacturer, who shted that the swaging process had been

revised to prevent excessive swaging and that the materials used in the manufacturing

process were of sufficient toughness.

The licensee addressed the generic aspects of this event by considering two

possibilities: (1) that other components procured from the same manufacturer had

similar material and processing deficiencies, and (2) that the manufacturer had supplied

other nuclear utilities with defective VASASPs. With regard the first issue, the licensee

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reviewed the vendor's quality assurance program and reviewed the material history of

components supplied the manufacturer. Based on this information, the licensee

concluded that, absent information to the contrary, it was reasonable to consider the

EDGs operable pending discovery of any additional defects. With regard to the second

issue, the licensee determined that only one other nuclear plant used VASASPs of this

type, and that plant had not installed any VASASPs processed from the defective

material lot. The manufacturer processed a report in accordance with 10 CFR Part 21

to notify the industry of the problem.

The team determined that the licensee had adequately addressed the defects

discovered in the VASASPs. Corrective actions were comprehensive and appeared

sufficient to preclude rer-rence of the event.

E8.6 Enaineerina Backloa

a.

Insoection Scope (37550)

The team reviewed the licensee's engineering backlog and the manner in which it was

being trended and tracked. In addition, the team discussed the backlog with appropriate

licensee personnel.

b.

Observations and Findinas

The engineering backlog had a downward trend since January 1997. For design

engineering, the total engineering workload decreased from approximately 1900 items in

January 1997 to approximate!y 1000 in June 1998. The design engineering backlog

consisted of ERs, open modifications, open CR actions, and other miscellaneous items.

The system engineering backlog also had a slightly downward trend since January

1997, with a reduction from 170 to 149 items.

The number of open temporary modifications had a downward trend since 1992, at

which time there were 73 open temporary modifications. At the time of this inspection,

only 11 remained open. The licensee's goal of maintaining the number of temporary

alterations less than or equal to 15 had been met since 1996.

c.

Conclusions

The team concluded that the engineering backlog was declining and was being

managed effectively by the licensee.

E8.7 System Enaineerina

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a.

Insoection Scope (37550)

The tearn discussed the status of the system engineering department with applicable

department managers. In addition, the team interviewed some of the system engineers.

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b.

Observations and Findinos

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The system engineering department consisted of approximately 22 to 24 engineers, with

each system engineer responsible for three to five systems. The system engineering

manager stated that the number of system engineers had remained steady for the past

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few years, in October 1997, the licensee initiated a team concept for the system

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engineers where three or four engineers shared a number of primary systems.

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Eventually, each member of the system engineering team would become an erjert on

all of the systems within the team's responsibility. The system engineers who were

interviewed believed that the team concept was good since it allowed for peer review of

each other's work. The team considered the team concept to be a strength,

c.'

Conclusions

System engineering appeared to have adequate staffing and was stable. The team

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concluded that the system engineering team concept was a strength.

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E8.8

USAR Review Procram

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a.

inspection Scope (37550)

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The team reviewed the licensee's program for reviewing the USAR. The review was

focused on portions of the effort that affected the SGTS and the HPCS system.

b.

Observations and Findings

The USAR review effort was described in "USAR Review Procedure," Revision 3, dated

May 7,1998. Section 1.2 of this procedure stated that the objective of this review was

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to improve USAR accuracy through a reasonableness review and to identify the areas of

the USAR that require a more detailed evaluation. The review process relied on the

personal experience and knowledge of the designated reviewer and on the review of

pertinent documents. The designated reviewers were assumed knowledgeable in the

aubject matter and could exercise their judgment in using the procedure. A line-by-line

compliance to the guideline was therefore not necessary as long as the review objective

was met and the review was appropriately documented. The review therefore was not

intended to verify and validate full accuracy of the USAR text. However, during the

review, areas of the USAR requiring a detailed examination were to be identified for

future action.

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For the purpose of the review, the USAR was divided into 151 parts. At the time of the

inspection,18 of the 151 parts had been reviewed and approved as part of the Phasa 1

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" reasonableness" review. The remaining parts were in various stages of completion.

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Nonc of the USAR sections for the plant systems selected for the team's review had

been completed (i.e., SGTS and HPCS). However, portions of these sections were in

various states of completion. At the request of the team, the licensee provided the

partially completed packages for review.

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To obtain some insight into the nature and quality of the review process, the team

selected the package for the mechanical review of USAR Section 6.3," Emergency Core

Cooling Systems," for an in-depth evaluation. The licensee reviewer found that the

information in the section was appropriate for the subject matter and that the section

reasonably reflected the plant design and operating conditions. Some references to

other USAR sections, figures, tables, and external documents were found to be

incorrect and some editorial errors were identified. There were no obvious technical

inaccuracies or areas of technical concern to the reviewer. The team concurred with the

reviewer's assessment of this section.

c.

Conclusions

The ongoing USAR review effort appeared to be satisfactory; although, the team noted

that the review was not a line-by-line verification.

E8.9 Year 2000 Computer issue

a.

Inspection Scoce (37550)

The team reviewed the licensee's plans for ensuring the continued operability of digital

equipment in the year 2000.

b.

Observations and Findinas

The team reviewed " Year 2000 Desktop Guide," Revision 0, dated July 28,1998, which

established the licensee's plan to ensure that plant systems and components influenced

by digital circuitry will continue to operate safely and efficiently following January 1,

2000. The guide also identified additional dates that could result in computer difficulties.

The licensee employed 11 full-time contractors along with in-house participation to

address this issue. All work on critical systems was scheduled to be completed by

January 1,1999, with continued work on important systems to be completed in July

1999. At the time of the inspection, this activity was approximately two weeks behind

schedule, but, based on the resources available, the licensee did not believe that

meeting the deadlines would be a problem or that excessive use of overtime work would

be needed.

The team observed that the licensee's program was comprehensive and that strong

management support was evident.

c,

Conclusions

The licensee's program to address the Year 2000 computer problem appeared to be

satisfactory.

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IV. Plant Support

F8

Miscellaneous Fire Protection issues (92904)

The team reviewed the following items that were identified during the NRC's Fire

Protection Functional Inspection (FPFI) and documented in NRC Inspection

Report 50-458/97-201. The team also reviewed the licensee's June 30,1998, response

to the FPFI report.

F8.1

(Closed) Unresolved item 50-458/97201-01: Smoke detector application, placement,

and installation in fire area C-24 does not meet requirements of License

Condition 2.C.10.

Backaround

The FPFI team reviewed the placement of smoke detectors in Fire Area C-24. The

FPFI team observed that the smoke detectors were not installed in the pockets between

the ceiling beams. The licensee performed Calculation G13.18.12.2-127," Evaluation of

Smoke Detector Installation in Fire Area C-24 As Compared to NFPA-72E-1978,"

Revision 0, to address the FPFI concern. The calculation concluded that the fire

detectors were installed in accordance with the Code of Record and the licensing basis.

Inspection Followuo

The licensee's evaluation stated that the detectors were installed in accordance with the

National Fire Protection Association (NFPA) Code of Record, NFPA-72E-1978, for the

plant fire detection system. The team reviewed Calculation G13.18.12.2-127,

Revision 0, the Code of Record, and the installed configuration of the detection system

in Fire Area C-24. The team verified that the licensee's conclusion was correct and that

the system was installed in accordance with requirements.

F8.2

(Closed) Unresolv9.0 item 50-458/97201-02: Failure to include fire protection check

valves in a functional testing program.

Backaround

As described in Section 9.5.1.2.2.0," Seismic Design Requirements," of the USAR, a

Seismic Category I water supply is provided from the standby service water (SSW)

system to the seismically designed fire protection standpipe system to provide water for

hose stations serving equipment required for safe plant shutdown following a safe

shutdown earthquake. A seismically-qualified check valve is located in the normal fire

protection water supply piping upstream of each of the three SSW system cross

connections. These hose station supply header check valves are designed to prevent

diversion of SSW system flow through a break in the nonseismically qualified fire

protection water supply piping when the SSW system is being used as the fiie protection

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water supply. The NRC identified that the licensee did not have procedures for testing

these check valves. The subject valves were: Valve FPW-319," auxiliary and reactor

building fire protection header to hose racks inlet check valve"; Valve FPW-V395, " fuel

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building fire protection header hose racks header check valve"; and FPW-V820, " control

building fire protection header hose racks inlet check valve."

inspection Followup

The licensee's FPFI report response stated that the subject valves were tested in

accordance with the requirements of the Technical Requirements Manual (TRM) and

that the setject valves were verified to open in accordance with the TRM-required

Procedure, STP-251-3702, every 3 years. The team reviewed Procedure

STP-251-3702, " Fire Hose Station Water Flow Test and Hose Hydro inspection,"

Revision 7. The team noted that this procedure implemented the requirements of

surveillance requirement TSR 3.7.9.4.4 by partially opening each hose station valve to

verify that the valves were operable and that there was no flow blockage. This test

involved cracking open the hose rack angle valve to allow 2 to 3 gallons of water to flow.

The team concluded that performing this test at each hose station resulted in only a

partial stroke of the hose station supply header check valves. There was no test to

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verify that the check valves had closed.

The licensee's FPFI report response identified that the subject check valves were

reviewed in an engineering analysis, which recommended that they could be screened

from additional testing. The team reviewed Engineering Document No.1961C," River

Bend Station Check Valve Program Development," Revision 0. The check valve

analysis and prioritization that were performed as part of this evaluation concluded that

the subject valves were * Priority 5/ low usage," and recommended that the valves be

inspected every five plant operating cycles. The licensee used the recommendation of

this study, combined with the good historical performance and maintenance history of

these and similar valves, to conclude that no additional testing or inspections were

necessary. The team did not have a concern with the technical adequacy of this

conclusion.

The team reviewed Procedure STP-251-3502," Fire Protection Water Valve Cycle

Test," Revision 9, and verified that the manual isolation valves immediately upstream

of the hose station supply header check valves were included in the test. These

seismically-qualified, normally open, manual isolation valves were required to be

cycled through at least one complete cycle of full travel every 12 months.

Procedure STP-251-3502 accomplished this requirement. These valves provided

additional assurance that if the SSW system was required for fire protection water

system supply following a safe shutdown earthquake, a break in the nonseismically

qualified portion of the fire protection system could be isolated.

The team asked the licensee for a copy of the procedure that would be used to place

the SSW system in service as a source of fire protection water if necessary following a

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safe shutdown earthquake. The team was informed that there was no procedure for

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accomplishing this task and were provided with a copy of CR 98-0214, dated

February 26,1998, that also identified that there were no procedures to implement this

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function. The CR identified a corrective action for Plant Engineering to develop a scope

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and outline of operating instructions to place the SSW system in service to supply water

to the fire protection system in the event of a loss of the fire protection water supply.

This corrective action had a due date for completion of August 26,1998. The CR

identified another corrective action for Operations to develop a procedure using the

outline developed by Plant Engineering. This corrective action had a due date for

completion of June 30,1999.

The team was concerned that this due date may not be appropriate and that operators

may not be knowledgeable of the capability or have the necessary training for placing

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the SSW system in service in the event of a loss of fire protection water supply before

the procedure is written. The licensee provided the team with a copy of System Training

Manual Lesson Plan RBS-1-STM-GPST-A0118.00," Service Water Systems." This

lesson plan identified that operators were taught that the SSW system was capable of

providing a backup source of water to the fire protection system by means of opening

the manually-operated cross-connect valves. The licr;nsee also provided the team wi'h

a copy of Emergency Operating Procedure EOP-0005," Injection lato RPV with Fire

System," Revision 11, which identified procedural steps for using the fire protection

water supply system to inject into the reactor via the SSW system cross-connect valves.

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Based on the existence of this procedure and operator training regarding capability of

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the SSW system as a backup supply of water for the fire protection system, the team

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concluded that there was no safety issue, which would require immediate action to

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implement the corrective actions identified in the CR. The team did note, however, that

the SSW system lesson plan provided operators with incorrect training. The training

stated that check valves in the SSW system piping prevented fire protection system

water from entering the SSW system. These check valves had been previously

removed to allow a means of injecting water into the reactor per EOP-0005. The

licensee acknowledged the team's observation and initiated actions to correct the

training.

Technical Specification 5.4.1.d required that written procedures shall be established,

implemented, and maintained covering fire protection program implementation. The

failure to have written procedures for using the SSW system as a source of water to the

fire protection system, as described in the fire protection program, was a violation of

Technical Specification 5.4.1.d. This nonrepetitive, licensee-identified failure, which is

scheduled for correction by the licensee, is being treated as a noncited violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy (50-458/9816-05).

F8.3

(Closed) Unresolved item 50-458/97201-03: Lack of engineering evaluations to

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establish the fire-rating or fire-resistant capabilities of fire-rated boundaries.

Backaround

The FPFI team identified that the licensee did not have acceptance criteria for the

clearance around a fire door that was in accordance with the requirements of National

Fire Protection Association (NFPA) 80. The team reviewed the licensce's evaluation of

fire door clearance acceptance criteria.

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Inspection Fo.suo

The licensee provided copies of a fire door test conducted October 22,1986, by the

door manufacturer for the type of doors used at the station. The test demonstrated that

the door successfully passed a 3-hour fire endurance test. Therefore, the team

concluded that the licensee adequately demonstrated that the installed fire door

configuration would pass a 3-hour fire test.

F8.4

(Closed) Unresolved Item 50-458/97201-04: Outdated equipment and failure to assign

personnel to the fire brigade who have normal plant duties that do not conflict with their

response to a plant fire.

Backaround

The FPFI team identnied that the licensee's fire brigade personnel protection equipment

was outdated by current technology. The FPFI team also identified that the licensee

was not implementing the fire brigade staffing in accordance with a document, which

was referenced by the SER. The team reviewed the licensee's response to these two

fire brigade issues.

Insoection Followup

The licensee reviewed the FPFI team observation concerning the quality of the

personnel protection equipment for the fire brigade. At the time of this inspection, the

licensee had on order or had received state-of-the art fire protection equipment for fire

brigade members.

The facility operating license requires that the licensee implement the approved fire

protection program as approved in the USAR, the safety evaluation report (SER) dated

May 1984, and Supplement 3 to the SER dated August 1985. Section 9.5.1.3 of the

SER stated that the licensee committed to implement the NRC supplemental guidance

provided in " Nuclear Plant Fire Protection Functional Responsibilities, Administrative

Controls and Quality Assurance," dated August 29,1977. This letter stated that the

responsibilities of the fire brigade members, under normal plant conditions, should not

conflict with their responsibilities during a fire emergency. The licensee determined that

the statement in the SER (concerning the subject commitment) was in error because

they had never made the referenced commitment in any licensing submittals. The

licensee stated that they would send a letter to the NRC to document and correct the

error. The team reviewed the licensee's current fire brigade staffing requirements in the

approved fire protection program and noted that the licensee complied with the

requirements identified in 10 CFR Part 50, Appendix R. The team reviewed licensee fire

brigade drill response time records for the 18 months preceding this inspection and

noted that the fire brigade responded in a timely manner during these drills.

The team concluded that the licensee was taking actions to ensure that fire brigade

personnel had state-of-the art personnel protection equipment. The team also

concluded that the fire brigade members could respond to a fire in a prompt manner.

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F8.5

(Closed) Unresolved item 50-458/97201-05: Failure to perform an adequate operability

assessment and provide appropriate compensatory measures for conditions affecting

the functionality of post-fire safe-shutdown capability.

Backaround

The FPFI team identified that the licensee had removed an installed Thermo-Lag fire

barrier, rendering the barrier inoperable, while maintaining only an hourly fire watch

patrol. The FPFI team was concerned that since the barrier had been completely

removed, the compensatory measures that the licensee implemented were less than

adequate.

Inspection Followuo

The team observed that the licerdee's fire protection program required that an hourly

fire watch patrol be implemented when a missing or degraded fire barrier was identified.

The team found that the licensee implemented the requirements of the fire protection

program. However, during interviews with licensee personnel, they indicated that they

understood the concern expressed by the FPFI team that additional fire protection

enhancements may be warranted for planned impairments of significant portions of a

fire protection system. The licensee's position was that additional fire protection

enhancements could have been considered for this impairment but that the

requirements of the fire protection program were not violated in this case. The team

agreed with the licensee's conclusion that the use of an hourly fire watch patrol was

consistent with regulatory requirements. The team concluded that although the licensee

should have considered the implementation of additional fire protection features t".

compensate for the removed Thermo-Lag barrier, no violation occurred.

F8.6

LClosed) Unresolved item 50-458/97201-06: Failure to perform an adequate post-fire

safe-shutdown analysis that meets the licensee commitment to Sections lil.L.1, Ill.L.2,

and Ill.L.7 of Appendix R to 10 CFR Part 50.

Backaround

The FPFI team questioned whether the licensee performed an adequate post-fire safe

shutdown analysis. Specifically, a postulated fire in certain areas of the plant could

potentially cause all 16 safety relief valves (SRVs) to simultaneously open. The licensee

had identified this issue in 1996 but had determined that it was not credible and that

further consideration of the issue was not within the scope of its fire protection program

requirements.

Inspection Followun

Operating License NPF- 47, Condition 2.C.10, required that the licensee shall comply

with the requirements of the fire protection program as specified in Attachment 4 to the

license. Attachment 4 required that the licensee implement and maintain in effect all

provisions of the approved fire protection program as described in the Final Safety

Analysis Report for the facility through Amendment 22 and as approved in the SER,

dated May 1984, and SER Supplement 3, dated August 1985.

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The SER Supplement 3, page 9-13, stated that the fire protection program was in

conformance with the guidelines of Branch Technical Position CMEB 9.5-1and

10 CFR Part 50, Appendix R, Section Ill.G. The United States Courts have held that for

fire areas where alternative or dedicated shutdown is chosen, then 10 CFR Part 50,

Appendix R, Section Ill.L must apply. Therefore, the team concluded that the

requirements of 10 CFR Part 50, Appendix R, Section s Ill.G and Ill.L were applicable

as referenced to License Condition 2.C.10.

Each of the 16 SRVs was provided with a Division I and a Division 11 solenoid.

Energization of either solenoid caused its associated SRV to open. Four Rosemount

pressure transmitters were located in the reactor building and converted a reactor

pressure input signal into a de output signal. Two of the transmitters were used for the

Division l SRV solenoids and the other two were used for the Division ll SRV solenoids.

A high pressure condition detected by both pressure transmitters for either division

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satisfied the controllooic to energize their associated set of solenoids and open all

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16 SRVs.

The two twisted pairs of pressure transmitter signal conductors for each division were

contained in a common multi-conductor cable from the containment penetration to the

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trip unit in the main control room. If one of the wires in a pair were too short to the other

wire of the same pair, a high RCS pressure signal would be received by the SRV

pressure logic trip unit. If the other pair in the same cable were to short together, a

second high-RCS pressure signal would be received by the SRV pressure logic trip unit,

which would satisfy the trip logic to open the SRVs. The fault current caused by these

circuits was too low to cause the circuit protective fuses to open. Therefore, fire

damage to either of two multi-conductor cables (Division I or Division 11) could cause the

trip logic to be satisfied and result in the spurious opening of all 16 SRVs. Opening all

SRVs when the reactor is at full power would result in a blowdown to the suppression

pool and a rapid reactor pressure vessel depressurization.

in 1996, the licensee identified the potential that fire-induced circuit failures within a

single multi-conductor cable could result in spurious high-pressure signals that would

cause all of the SRVs to open. In Engineering Report (ER) 96-0672, dated November

18,1996, the licensee stated its position that only one fire-induced spurious operation

need be assumed during the fire event requiring alternate shutdown except in the case

of hi/lo pressure interfaces. Specifically, the licensee took the position that since it

would take two shorts to occur in either single multi-conductor cable of concern, and that

these conditions need not be assumed to occur concurrently, the single multi-conductor

cable was an acceptable condition. The licensee based its position on its interpretation

of the response to Question 5.3.10 in Generic Letter (GL) 86-10. " Implementation of Fire

Protection Requirements," April 24,1986. No modifications were performed or planned

to correct the condition.

Question 5.3.10 of GL 86-10, " Design Basis Piant Transients," states, "What plant

transients should be considered in the design of the alternative or dedicated shutdown

systems?" The response states,"Per the criteria of Section Ill.L of Appendix R, a loss

of offsite power shall be assumed for a fire in any fire area concurrent with the following

assumptions: (a) the safe shutdown capability should not be adversely affected by any

one spurious actuation or signal resulting from a fire in any plant area; (b) the safe

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shutdown capability should not be adversely affected by a fire in any plant area, which

results in the loss of all automatic functions (signals, logic) from the circuits located in

the area in conjunction with one worst case spurious actuation or signal resulting from

the fire; and (c) the safe shutdown capability should not be adversely affected by a fire

in any plant area, which results in spurious actuation of the redundant valves in any one

high-low pressure interface line.

The team considered that the licensee's conclusions regarding this issue were in error.

The licensee's interpretation that only one circuit failure (one twisted pair of wires

shorting together) needed to be considered did not meet the NRC's implementation

guidance in the GL 86-10 response to Question 5.3.1. This question," Circuit Failure

Modes," states, "What circuit failure modes must be considered in identifying circuits

associated by spurious actuation?" The response states,"Section s !ll.G.2 end Ill.L.7 of

Appendix R define the circuit failure modes as hot shorts, open circuits, and shorts to

ground. For consideration of spurious actuations, all possible functional failure states

must be evaluated, that is, the component could be energized or de-energized by one or

more of the above failure modes. Therefore, valves could fail open or closed; pumps

could fail running or not running; electrical distribution breakers could fail open or

closed. For three-phase AC circuits, the probability of getting a hot short on all three

phases in the proper sequence to cause spurious operation of a motor is considered

sufficiently low as to not require evaluation except for any cases involving Hi/Lo

pressure interfaces. For ungrounded de circuits, it it can be shown that only two hot

shorts of the proper polarity without grounding could cause spurious operation, no

further evaluation is necessag except for any cases involving Hi/Lo pressure

interfaces." Since the SRVs were not Hi/Lo pressure interfaces and the SRV circuitry

did not meet either of the exceptions discussed in the answer to Question 5.3.1,

evaluation of the SRV circuitry was required.

Section Ill.G.2 of Appendix R specified that where cables or equipment including

associated nonsafety circuits that could prevent the operation or cause the maloperation

due to hot shorts, open circuits, or shorts to ground of redundant trains of systems

necessary to achieve and maintain hot shutdown conditions were located within the

same fire area outside primary containment, that they be provided with fire protection

features necessary to ensure that they remain free of fire damage in accordance with

Appendix R, Section s Ill.G.2.a b, or c.

Appendix R, Section Ill.G.3, specified that alternative or dedicated shutdown capability

is required where the protection of systems whose function is required for hot shutdown

does not satisfy the requirement of Appendix R, Section Ill.G.2.

For a fire in the main control room, the system credited in the fire hazards analysis for

alternative shutdown reactor pressure vessel level control was the steam-driven reactor

core isolation cooling (RCIC) system. However, if all of the SRVs were to spuriously

open due to shorts of the SRV pressure transmitter conductors, the rapid

depressurization would eliminate the steam pressure required to drive the RCIC system

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turbine. Therefore, because fire-induced short circuits of the SRV pressure transmitter

conductors (located in the same fire area) could prevent the operation of the RCIC

system, which was required to achieve and maintain hot shutdown conditions, the

licensee was not in conformance with Appendix R, Section Ill.G.2. If a licensee does

not comply with Appendix R, Section Ill.G.2, then the licensee is required to provide

alternative or dedicated shutdown capability per the requirement of Appendix R,

Section Ill.G.3.

The normal emergency core cooling system (ECCS) and reactor feedwater systems

were not electrically isolated from the effects of a main control room fire. Therefore,

their availability to perform an RCS makeup function cannot be assured (e.g., there is

potential for a main control room fire to damage ECCS initiation logic, cause spurious

closing of ECCS flowpath valves, or cause spurious ECCS pump shutdowns).

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Using the GL 86-10 guidance, should a postulated control room fire occur that required

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evacuation, a reactor trip must be initiated as the operators leave to go to the remote .

shutdown panel. If th,e SRVs were to spuriously open, a rapid RCS depressurization

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would occur. As a result of this depressurization, the RCIC system would be

unavailable. The "A" train of the RHR system was protected from the effects of a fire,

but it would be in a suppression pool cooling mode lineup for decay heat removal rather

than low pressure coolant injection (LPCI). An operator at the remote shutdown panel

would have to manually realign the system from the suppression pool cooling mode of

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operation to the LPCI mode of operation.

10 CFR Part 50, Appendix R, Section Ill.L, required, in part, that the alternative

shutdown capability shall be able to maintain reactor coolant inventory and that it be

capable of maintaining the reactor coolant level above the top of the core. The licensee

performed an analysis of this event, which concluded that if the operator initiated

injection using the RHR system within 10 minutes after event initiation, the ECCS

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acceptance criteria of 10 CFR 50.46 were not exceeded but reactor coolant level would

not be maintained above the top of the core. Therefore, an alternative or dedicated

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shutdown capability was not provided in accordance with Appendix R, Section Ill.G.3

that met the performance goals of Appendix R, Section Ill.L. This was a violation of

License Condition 2.C.10.

The NRC had a meeting with the licensee to discuss this issue at on August 19,1997.

At this meeting, the licensee reaffirmed the position that considering multiple circuit

failures was outside the scope of Appendix R and the Generic Letter 86-10

implemenMon guidance. The licensee also presented information at the meeting that

concluded that this event was of very low probability and was not risk significant

in its response to the FPFI report, dated June 30,1998, the licensee committed to

implement a modification to mitigate the effects of any hypothetical SRV cable short

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during the April 1999 refueling outage. However, the licensee reiterated its position that

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its present configuration was in compliance with the fire protection program licensing

basis.

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d

!

The NRC had a meeting with the licensee on July 29,1998. At that meeting, the

licensee described conceptually a modification that would bypass the short circuit signal

l

and eliminate the spurious SRV actuation concern. The licensee reiterated its

commitment to install the modification during the April 1999 refueling outage.

The team noted that the licensee had proceduralized operator actions and had

conducted operator training to mitigate the post-fire SRV actuation event as described

above. Also, the team noted that although a refueling outage had already occurred

since the time of the FPFI inspection when a modification could have been performed,

'

the licensee had committed to perform a modification within a reasonable time after the

i

issuance of the FPFI report.

)

In accordance with Section Vll.B.6 of the NRC Enforcement Policy, the NRC exercised

its enforcement discretion to not propose a civil penalty and to not issue a violation in

this case. Discretion was warranted because: (1) the apparent widespread

misunderstanding of the requirements, (2) the fact it was licensee identified, (3) the low

risk significance, (4) the fact that the licensee took compensatory actions, and (5) the

]

l

licensee commitment to implement a modification during the next refueling outage that

'

will correct the condition.

F8.7

(Closed) Unresolved item 50-458/97201-07: Deficiency in the design of the reactor

overpressure protection system, under certain postulated conditions, could lead to

inadvertent actuation of 16 SRVs resulting in an un-analyzed plant transient.

Backarourt_d

,

'

The FPFI team questioned whether the design of the safety relief valve (SRV) actuation

I

circuitry complied with the requirements of general design criteria (GDC) 23 of

l

10 CFR Part 50, Appendix A. GDC 23 requires, in part, that the protection system be

designed to fail in a safe condition if a postulated adverse environment (such as a fire) is

experienced. The FPFI team was concerned that the protection system was not

designed to fail in a safe condition as exemplified by a postulated fire causing two

conductor-to-conductor shorts in a reactor pressure vessel pressure transmitter cable

'

and simultaneous opening of all 16 SRVs. The postulated transient had not been

j

reviewed in the safety analysis report.

Inspection Followup

The team reviewed the design of the SRV overpressure logic, the reactor protection

l

system, and the engineered safety features to determine whether the SRV overpressure

logic circuitry was within the scope of GDC 23.

The team reviewed USAR Section 3.1,"Conformance with NRC General Design

Criteria," Section 7.2, " Reactor Protection (Trip) System," and Section 7.3, " Engineered

Safety Features." USAR Figure 7.2-1, Sheet 3, identified that the four reactor vessel

1

,

31

_ _

_ _ _ _ _ _ _ _ _ . _ . _ . _ _ . . - . _ _ _ _ _ _ . _ _ . . _ _

_ _.. _ _

.

4

pressure transmitters that provided input to the reactor protection system were

B21-PTN078A, B21 PTN078B, B21-PTN078C, and B21-PTN078D. The pressure

transmitters that provided input to the SRV overpressure logic were B21-PTN068A,

B21-PTN0688, B21-PTN068E, and B21-PTN068F. Therefore, the SRV overpressure

. logic circuitry was not part of the reactor protection system addressed by GDC 23.

The GDC discussion in USAR Section 3.1 also referenced USAR Section 7.3. The

applicable discussion therein concerned the automatic depressurization system (ADS).

The team reviewed Section 7.3, and noted that although Section 7.3 included a

i

description of the SRV overpressure logic circuitry in Figure 7.3-2, Sheets 6 and 6A,

l

which used the affected pressure transmitters, ADS actuation did not require reactor

.

pressure as an input. Therefore, the SRV ov9rpressure logic circuitry was not

l

necessary for ADS actuation and not part of the protection system addressed by

GDC 23.

'

Based on the above review, the team concluded that the SRV overpressure logic

circuitry was not part of the protection system as identified in GDC 23.

F8.8

Other FPFI issues

The team reviewed the following additional FPFI issues that were identified as " Program

Weaknesses" in the FPFI inspection Report.

F8.8.1 Fire Suporession System in Fire Area C-4

a.

Insoection Scope

The FPFI team observed that the licensee had installed six side wall sprinkler heads to

provide automatic suppression in Fire Area C-4. The FPFI report noted that the heads

were not installed in accordance with the applicable NFPA Code and that no Code

deviation evaluation had been performed. The team reviewed licensee Calculation

G13.18.12.2-126," Justification for Deviations From NFPA 13-1983 For Suppression

System AS 6C in Fire Area C-4," Revision 0. The team also conducted a visual

inspection of Fire Area C-4.

b.

Observations and Findinas

The licensee completed Calculation G13.18.12.2-126 after the FPFI and the calculation

confirmed that the side wall sprinkler installation deviated from the requirements of

NFPA Code 13-1983. However, the calculation concluded that the deviation was not

safety significant. The team visually inspected Fire Area C-4 and noted that

combustible materialloading in the fire area was extremely low. The team also noted

that there were additional upright sprinkler heads instalied, in accordance with NFPA

Codes, throughout the fire area. Therefore, the team concluded that the as-built fire

suppression system was acceptable.

i

!

32

l

_ _ _ _ _ _

.

.

With regard to the generic aspects of this issue, the licensee informed the team that it

performed walkdowns of each fire area and did not identify any areas where the fire

suppression or detection system was inadequate. Additionally, the licensee planned to

perform a rigorous fire protection system design basis reconstitution effort, including

Code reconciliation. Deviations identified would be appropriately evaluated.

Operating License NPF-47, Condition 2.C.10, specified that the licensee shall comply

with the requirements of the approved fire protection program. The fire protection

program stated that the sprinkler systems were designed using the guidance of

NFPA 13; however, no deviation from the NFPA Code was described in the program.

Generic Letter 86-10 informed licensees' that deviations from the Code should be

identified and justified. This failure constituted a violation of minor significance and was

not subject to formal enforcement action.

c.

Conclusions

The team concluded that the licensee's evaluation was adequate to demonstrate that

full NFPA Code compliance was not needed for the side wall sprinkler heads in Fire

Area C-4 after this deviation was identified by the FPFI team. The failure to have

identified and justified this deviation from the NFPA Code was determined to be a

violation of minor significance.

F8.8.2 Control of Combustible Materials

a.

Inspection Scope

The FPFI team identified that Procedure FPP-0040, " Control of Transient

Combustibles," Revision 7, may not provide adequate control of transient combustible

materials in the plant. The team reviewed Procedure FPP-0040, visually inspected

housekeeping in various plant areas, and interviewed licensee personnel responsible for

the program.

b.

Observations and Findinas

The team observed that Procedure FPP-0040 did not explicitly contain each statement

contained in the NRC guidance concerning control of transient combustible materials.

The team observed that personnel were allowed to leave some small amount of

materials at the job site that had work in progress without formal review by the fire

protection staff. Tir team observed, however, that there was no excessive amount of

transient materials in the plant. The team noted that each small amount of materials left

in the plant had a " Work in Progress" sign in the area, which was dated and had a

responsible organization listed. The team did not observe any " Work in Progress" signs,

which had been left in place for an excessive amount of time. Interviews with

responsible plant personnel demonstrated that the staff had a high awareness of the

issue and could quickly identify and remove any excessive combustible materials that

might accumulate in the plant.

33

..

.

.

.

.

.

. _ _ _ _ _ _ _ _ _ -

. _ - . . - .._

..___m._

. . _ . _ . _ . . _ . _ . _ . _ - . . _ _ _ . _ . _ _ _ _ . _ . _ . . _ . _ . _ . _ . _

.

c.

Conclusions

l

The team concluded that the licensee was effectively controlling the use of transient

l

combustible materials.

1

V. Manaaement Meetinas

XI

Exit Meeting Summary

l

The team presented the preliminary inspection results in a debriefing to members of

l

licensee management on August 7,1998. The licensee acknowledged the findings

presented, but disagreed with two of the proposed violations discussed during the

meeting. The licensee did not agree that the issue stated in Section E2.1 of this report

constituted a violation of 10 CFR 50.59. In this matter, the licensee stated that they

l

were implementing the guidance of the Nuclear Energy Institute that was disseminated

j

l

industry-wide. The team explained that, since the NRC does not fully endorse this

guidance, utilities that use it are vulnerable to enforcement action. The licensee also did

not agree with a violation of failure to protect against the effects of a control room fire as

described in Section F8.6 of this report. In this case, the licensee believed that it was in

compliance with the regulations, and that guidance in Generic Letter 86-10 specifically

exempted the subject wiring configuration. As stated in the report, this violation was not

j

issued on the basis of an exercise of enforcement discretion.

1

Following additionalin-office review, the team presented the inspection results to

members of licensee management via telephone on October 15,1998.

.

The licensee was asked whether any materials examined during the inspection should

l

be considered proprietary. The licensee stated that some information reviewed by the

team was proprietary. This information was returned and was not discussed in the

report.

1

i

34

- .

. -

.-- -

--

-

- - - .

1

'

-

a

.

i

e

,

,

i

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

.

-

!

R. Azzerello, Manager, Electrical and instrumentation and Control Engineering .

_V. Bacanskas, Lead Engineer, Fire Protection

,

R. Brian, Manager, Mechanical Design Engineering .

R. Buell, Manager, Project Management

3

P. Campbell, Technical Assistant

D. Dormady, Manager, Plant Engineering

B. Ellis, Fire Protection Engineer

'

J. Fowler, Quality Programs Manager

. T. Hoffman, Supervisor, Engineering

R. Kerar, Fire Protection Engineer

R. King, Director,' Nuclear Safety and Regulatory Affairs

D.' Lorfing, Licensing Supervisor

S. Martin, Supervisor, Design Engineering

J. McGaha, Executive Vice President

D. Mims, General Manager-

1 W. O'Malley, Manager, Operations

D. Pace, Director, Engineering

B. Thumm, Licensing Engineer -

NRC

N. Garrett, Resident inspector -

INSPECDON PROCEDURES USED

1

92903'

Followup-Engineering

93809

Safety System Engineering Inspection

92904

Followup Plant Support

37550

Engineering

4

'

37001

10 CFR 50.59 Evaluations

1

_

_

- ___ __

_

_. _.

- _ _ _ . _ _ _ . _ . _

,

!

REMS OPENED. CLOSED. AND DISCUSSED

i

Opened

,

50-458/9816-01

IFl

Problems with Pressure Relief Valve Set Pressure

Program (Section E1.4).

50-458/9816-02

IFl

Root Cause of Relief Valve Failure (Section E1.4).

50-458/9816-03

IFl

Containment Temperature issues (Section E1.5).

50-458/9816-04

VIO

Failure to Consider an increase in Dose Consequences

to be an Unreviewed Safety Question (Section E2.1).

j

50-458/9816-05

NCV

Lack of Procedure to Use Service Water for Fire

Protection (Section F8.2).

Closed

'

50-458/97-007

LER

Cracked screw assembly swivel pads on emergency

diesel generators could have prevented fulfillment of

safety function (Section E8 5).

50-458/9621-01

IFl

Entergy Operations, Inc., resolution of quality assurance

,

,

program required for resource sharing (Section E8.1).

50-458/9622-01

IFl

Adequacy of molded case circuit breaker trip setpoints

(Section E8.2).

l

50-458/9627-02

IFl

NRR to review near-buoyant objects (Section E8.3).

j

50-458/97201-01

URI

Smoke detector application, placement, and installation

in fire area C-24 (Section F8.1).

!

50-458/97201-02

URI

Failure to include fire protection check valves in a

functional test program (Section F8.2).

50-458/97201-03

URI

Lack of engineering evaluation to establish fire

rating / fire resistance capabilities of fire-rated boundaries

(Section F8.3).

50-458/97201-04

URI

Failure to assign other people to fire brigade

(Section F8.4).

50-458/97201-05

URI

Failure to perform adequate operability assessment

(Section F8.5).

50-458/97201-06

URI

Failure to perform adequate post fire safe shutdown

analysis (Section F8.6).

50-458/97201-07

URI

Deficiency in design of reactor overpressure protection

system (Section F8.7).

50-458/9816-05

NCV

Lack of procedure to use service water for fire protection

(Section F8.2).

2

.

-

,

LIST OF ACRONYMS USED

)

ADS'

automatic depressurization system

cfm

cubic feet per minute

CR

condition report

CST

condensate storage tank

DBA

design basis accident

ECCS

emergency core cooling system

EDG

emergency diesel generator

i

EPRI

Electric Power Research Institute

ER

engineering request

FPFI

fire protection fu'nctionalinspection

)

GDC

general design criterion

GL

generic letter

j

HEPA

high-efficiency particulate air

HPCS

high pressure core spray

4

IN

NRC Information Notice

LCN

license change notice

l

LER

licensee event report

LOCA

loss-of-coolant accident

[

LPCI

low pressure coolant injection

LPCS

low pressure core spray

NEl

Nuclear Energy Institute

NFPA

National Fire Protection Association

NPSH

net positive suction head

NRC

Nuclear Regulatory Commission

PPP

positive pressure period

RBS

River Bend Station

- RCIC

reactor core isolation cooling

3

._.

_.

__

_ _ _ __

. . _

. . - _ . _ _ . _

. _ . . . _ _ . ._..

. _ . . . . . . . _

1...w.

la

i

l

~RHR

residual heat removal

i

t

L

SEN-

safety evaluation (10 CFR 50.59)

SER

safety evaluation report .

SGTS.

standby gas treatment system

l

SSW

standby service water

STP

surveillance test procedure

TP.

temporary test procedure

.TRM -

Technical Requirements Manual

TS--

. Tec'inical Specifications

USAR

Updated Safety Analysis Report

'

USO.

unreviewed safety question

VASASP

valve adjusting screw assembly swivel pad

wg

water glass

)

i

-

I

t

>

4

l

l

.

--,

,,-

..

.

- _ . -

. . .

-

._-

.-

._

_

o -

!

l

.

LIST OF DOCUMENTS REVIEWED

l

l

Procedures

I

NUMBER

DESCRIPTION

REVISION

i

ENG-3-037

Engineering Request

Revision 2

Process

l

RBNP-030

Initiation and Processing of

Revision 12

l

Condition Reports

!

J

EDP-AA-20

Engineering Calculations

Revision 12

RBNP-088

USAR Maintenance

Revision 0

'

l

No Number

USAR Review

Revision 3

l

l

STP 203-6305

HPCS Quarterly Pump and

Revision 7

'

l

Valve Operability Test

STP-203-6805

HPCS Cold Shutdown Valve

Revision 4

Operability Test

l

STP-302-1601

ENS-SWG1 A/B Loss of

Revision 0

Voltage Channel Calibration

and Logic System Functional

Test

PL-126

Site Providing Services to

Revision 0

Other Sites

RBNP-093

Control of Shared Services

Revision 0

ENG 3-006

Modification Design

Revision 16

Guidance

I

ENG 3-033

Modification Design Control

Revision 4

,

'

Plan

ADM-0031

Temporary Alterations

Revision 8A

RBNP-030

Initiation and Processing of

Revision 12

Condition Reports

RBNP-057

10 CFR 50.59 License Basis

Revision 7

!

!

Reviews and Envirc.unental

l

Evaluations

i

l

STP-000-6606

Section XI Safety and Relief

Revision 6

Valve Testing

5

l

_ _ _ _ _ _ _ _ _ _ _ _

O

e

STP-251-3702

Fire Hose Station Water

Revision 7

l

Flow Test and Hose Hydro

inspection

STP-251-3502

Fire Protection Water Valve

Revision 9

Cycle Test

EOP-0005, Enclosure 7

Injection into RPV with Fire

Revision 11

System

SOP-0042

Standby Service Water

Revision 16B

System Operating Procedure

SOP-0037

Fire Protection Water

Revision 16

System Operating Procedure

Enaineerina Reauests and Temporary Alterations

NUMBER-

DESCRIPTION

REVISION /DATE

ER 97-0147

ECCS Suction Strainer

-

Modification

ER 97-0277

Correct ESK-6GTS02

6/3/97

ER 97 0324

HPCS Design Basis

6/5/97

Information

ER 98-0166

SGTS Modification

4/19/98

ER 98-0230

SGTS Modification

-

ER 98-0233

SGTS Evaluation

6/17/98

ER 96-0017

Status of Normal / Preferred

1/16/96

Transfer

ER 96-0602

CSH PS235 & 249 Setpoint

8/22/96

Change

ER 97-0293

Modify Control Circuit of

6/10/97

E22*S004-ACB01

ER 98-0430

SRV Control Circuit

7/28/98

Modification

ER 96-0072

Spurious High RPV Signal

11/18/96

Initiation of SRVs

TA 96-13

Install enhanced option 1 A

10/10/97

flow control trip reference

card in APRM B

'

6

e

. _ _ _ _ _ _ _ - .

_ - . .

. . _ .

_ _ .

. _ .

. . . .

. . _ . _

..

_ - _ _ _

_ _ _ _ . - _

-

1

.' '

. .

TA 96-025

Disable SLC suction piping

9/01/96

'

heat trace and alarm

Condition Reports (CRs)

l

L

NUMBER

DESCRIPTION

REVISION /DATE

!-

CR 96-1137

CST Level for Vortex -

-

L

Prevention Allowance

}

CR 96-1511 ~

SGTS Fan GTS*FN1 A

6/7/96

Rotating Backwards

l

CR 97-0526A(CR-97-2154)

SGTS Surveillance Test -

-

l

Validity

o

l

l

CR 97-0800 '

SGTS USAR Changes

-

CR 97-0808

Low Vacuum in Annulus

-

l'

(Ventilation)

..

,

(

-.CR 98-0430

SGTS High Air Flow

-

.

t

..

CR 98-0437

SGTS High Air Flow

4/17/98

CR 98-0795

Div i and ll D/G Control Air

)

-

'

I

CR 98-0913

USAR Review Updates for

-

Section 6.3

'

CR 98-0924

High Vacuum Reading in

7/21/98

Auxiliary Building

- CR 98-1001

USAR Table 6.3-1 Error

-

CR 97-1494

STP-302-1602 Timer 62-6

9/17/97

j

CR 97- 0122

Circulating Water Pump

2/4/97

l

Motor Heater Removal

J

CR 97-1322

ENS SWG 18 ACB 29 Gnd

9/4/97

Overcurrent Relay

<

CR 94-1032

.52S contacts on 4.16 kV

8/18/94

,.

Switchgear

. CR 97-0793

Spring Charging Motor

5/28/97

Control Cicuit

CR 96-1516.

E22*S001 Battery Service

8/19/96

Test

7

, .

l:

,

,

-

.-_

-

.

_ _ _

_

._m

_ _ . _ _ _ _

_ .

..

..

_.

.Q.

'

a

CR 96-0562

HPCS Pump Motor Breaker

6/27/95

i

CR 97-1067

HPCS Breaker trip when

7/22/97

started

l

CR 97-0795

incorrect Calcula:!on used

5/26/97

SPDS EGF ESX15

l ~

CR 97-1079

. Allowable Values in TR

7/24/97

3.8.4.7~

'

!~

CR 97-0942

E22-LTN 054 C&G incorrect

5/17/96

!-

head correction

!

CR 96-1380

HPCS Diesel Alarm

7/21/96

!

l

CR 96-1459

HPCS 125V dc Distribution

8/7/96

System

'

CR 96-1516

Div 3 Volt Profile inrush I not

8/19/96

'

included

CR 97-2010

E22 MOV FO12 failed to

11/11/97

open

,

J

CR 96-1283

GTS-FNI A appeared to have

7/28/96

secured on its own

i

- CR 98-0632

GTS-FLT1 A heater failed to

5/21/98

energize as required by

i

procedures

L

CR 97-1157

Grease sjung from motor

8/6/97

'

bearings on both standby gas

treatment fan motors

97-1988

Auxiliary building supply fan

11/6/97

l

did not trip on low flow as

expected

CR 98-0230

High negative prassure in the

3/3/98

auxiiiary building and annulus

with standby gas treatment -

,

running

1

,

l

CR 98-0296

Difficulty opening aux building 3/19/98

doors with standby gas

,

running

8

E

!

.

.

_

..

O

CR 98-0415

Questions asked about the

4/15/98

impact of auxiliary building

access with both trains of

standby gas running -

CR 98-0430

Lineup of standby gas to limit

4/6/98

the off site dose limits

CR 96-1320

STP does not test the

7/16/96

pressure drop across the

profilters as required by TS

CR 98-0591

Incorrect acceptance criteria

5/17/98

was adopted for the high

pressure core spray pump

room cooler

CR 97-1690

10CFR21 notification for

9/30/97

defects and noncompliance

concerns for the EMD air start

motors

i

CR 98-0708

The current plant

6/8/98

l

configuration does not -

correspond to that described

in the SAR with respect to the

reserve volume of water in

the CST

CR 96-1593

Discrepancy in the minimum

10/3/96

temperature in the HPCS

diesel generator room

CR 97-1420

Piece of plastic gasket found

9/15/97

in service water side of heat

exchanger

CR 95-0581

Failure to grease the core

7/13/95

spray DSL turbo lube oil

pump during performance of

PM

CR 96-1581

Discrepancy between FSAR

9/12/96

and calculated maximum

temperature for HPCS pump

room

CR 96-1313

Battery performance

7/15/96

L-

discharge test was terminated

'

prior to meeting the

procedure conditions

9

-

.. ..

.. .. ..

..

.

.

.

.

..

.

.

_ - _ _ -

.

CR 98-0109

Heater cable was spared

2/1/98

without a 50.59 evaluation

CR 96-1137

Condensate storage tank

6/20/96

technical specification

minimum level requirement

may not ensure that 1254k

gallons of makeup water is

available

CR 95-0717

Discrepancies between

7/17/95

USAR figures and other

drawings

CR 98-0846

Two pieces of grey colored

8/23/95

/

cement were discovered on

top of the breaker when it

was removed from the cubicle

CR 97-0606

While running HPCS purnp it

4/30/97

was observed that the

minimum flow valve

functioned sluggishly

CR 97-2010A

HPCS minimum flow valve

1/22/98

demonstrated erratic

operation

CR 97-2100

HPCS minimum flow valve

11/11/97

failed to auto open

CR 97-0804

HPCS discharge relief valve

5/29/97

found with ruptured bellows

CR 98-0991

Actual containment

8/5/98

temperature was lower than

the minimum containment

temperature specified in the

Environmental Design Criteria

CR 96-1585

Standby gas system initiated

8/31/96

due to spike to radiation

monitor

.CR 97-0792

Radiation monitor went into

5/28/97

alarm and started standby

1

gas fan

^

CR 961584

Radiation monitor spiked and

8/31/96

,

started standby gas fan

j

10

1

>

-.

- . .. .

.

. _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _

_ _ _ _ _

. _

. _ .

_ . . _

.

.. ._

-

_

. _ _

._

-4

L

I

l

i.

CR 98-0216

Annulus high pressure alarms 2/27/98

!

were received

CR 97-1881

The relief valves for the diesel 10/20/97

l

starting air system were reset

to a higher set pressure

CR 97-2131

The relief valves for the diesel 12/18/97

l

starting air system were set

back to the original set

,

pressure

l

l

CR 961379

Relief valve for the

10/30/96

l

condensate pump motor air

.

l

cooler is set higher than

j

i

required

CR 96-1994

Relief valve on the

11/21/96

,

i

condensate emergency

i

makeup hotwelllevel control

l

valve bypass line is set higher

'

than required

CR 96-1571

Setpoints for the main steam

8/29/96

moisture separator reheater

pressure relief valves are not

l

In accordance with those

i

required by plant design

documentation

!

'

CR 97-2008

Relief valve was replaced

11/11/97

tiecause the valve set

pressure was 30 psi too high

CR 96-1082

46 discrepancies were

6/13/96

discovered between the

setpoints required by the

plant safety and relief valve

data sheets and the setpoints

etched on the valve data

plates

i

CR 92-0603

There is a question as to

8/21/02

what the actual pressure

setting is for the HPCS air

start system air dryer

discharge lines

l'

i

11

1

I

l

_

. _ _

..

.

..

~

..

..

.._

- . .

.

l

'

!

I

CR 98-0998 -

Open cable tray floor

8/6/98

i

penetrations without

!

guardrails in cable chase

'

room on 116' elevation

.

CR 98-0803

Fire detection, suppression,

6/25/98

and barrier issues

i

CR 97-0991

Po?'v d multiple shorts in

7/2/97

"

e

reactor > .ssure vessel

pressure transmitters causing

j

all 16 SRVs to open

l

-

CR 98-0214

No procedure to provide SSW 2/26/98

to fire protection hose

stations

'

Calculations

'

NUMBER

DESCRIPTION

REVISION

l

BV45,191

Fan External Total Pressure

Revision 1

l

i

Fans 1HVR-FN7A & FN78

Auxiliary Building Exhaust

System Normal Operation

1

Modes I,11, & Ill

BV45.20-1

Fan External Total Pressure

Revision 1

1GTS*FN1 A & FN1B

Containment /Drywell Purge

Exhaust, Normal Operation

Mode 111

BV45.22-1

Fan External Total Pressure

Revision 1

Fans 1GTS*FN1 A& FN1B

Annulus and Auxiliary

Building Exhaust, Accident

Mode

ES-151

Net Free Air Volume of the

Revision 0

Auxi!!ary Bldg

ES-193-4

Shield Bldg Annuius

Revision 4

Following a LOCA

l

ES-193-5

Shield Bldg Annulus

Revision 5

Following a LOCA

'

i

i

ES-194-3

Auxiliary Building Pressure

Revision 3

i

Following LOCA

'

12

i

l

l

l

!

B

4-

s.

i'

G13.18.14.1 *027-0

. Evaluation of Post-LOCA

Revision 0

Auxiliary Building Positive

> .

. Pressure Period in Support

l

of CR-98-0437

G13.18.2.1*079 00

Evaluation of SGTS -

Revision 0

I

Drawdown Data

G13.18.2.2'031-0

NPSH Available for ECCS

Revision 0

1.

Pumps for Suction from the

Suppression Pool Under

' Accident Conditions-

G13.18.2.7*23

Shield Building Annulus

Revision 1

Folicwing a LOCA (Note:

This calculation supersedes

ES-193-5)

'

_ To Determine the in-Leakage Revision 0

PB-251

and Amount of Exhaust Air

Required to Maintain a

Negative Pressure of 0.25 in

wg in Auxiliary Building

E129

Load Study 13.8 & 4.16 kV

Revision 4c

System

s

E130

Sizing Ground Resistors

Revision 3

4.16 kV System

E131

Station Service Short Circuit

Revision 1 & 8 addendum

Analysis

E132

Voltage Profile

Revision 3 & 9 addendum

1

E167

5 kV Cable Sizing

Revision 2 addendum B

EOS-64

5 kV Cable Lie Extension

4/8/85

lA-GTS*1

Setpoint Calculation

Revision 4

1GTS*FS 24A & B

IA-E22*04

Setpoint Calculation HPCS

Revision 2 addendum 4

Condensate Storage Tank

i

Low Level

j

1

l lA-E22*05

Setpoint Calculation

Revision 4

1E22*ESN 655C & G

lA DFR#2

Setpoint Calculation HPCS

Revision 5

Floor Water Level

l

I

I

13

l

t

g

y

v

. , , -

-

r

e-

.

O

G13.18.12.0*03

Common Cause Failure 4 kV

6/28/90

Circuit Breakers

G13.18.3.1 *01

Sustained & Degraded

Revision 1

Voltage Setpoints Div 1&2

G13.18.12.2-126

Jastification for Deviations

Revision 0

From NFPA 13-1983 For

Suppression System AS-6C

in Fire Area C-4

G13.18.3.1 *02

Sustained & Degraded

Revision 2

Voltage Setpoints Div 3

Drawinas

NUMBER

DESCRIPTION

REVISION

PID-27-15A

Engineering P&l Diagram

Revision 1

System 257 5sandby Gas

Treatment

PID-27-04A

Engineering P&l Diagram

Revision 2

System 203 HPCS System

PID-9-10E

Engineering P&l Diagram

Revision 18

System 256 Service Water

-Standby

PID-15-1C

Engineering P&l Diagram

Revision 9

System 251 Fire Protection

Water & Engine Pump

EB-45C-11

Ventilation and Cooling Plan

Revision 11

EL 95'-9" Auxiliary Bldg

EE1A

Main One Line Diagram Key

Revision 19

Drawing

EE1K

4.16 kV One Line Diagram

Revision 17

1 ENS *SWG 1 A

EE1L

4.16 kV One Line Diagram

Revision 14

1 ENS *SWG 1B

I

EE1M

4.16 kV One Line Diagram

Revision 7

E22*S004

i

1EJS* LOC 1 A&2A

480 V One Line Diagram

Revision 10

Standby Bus

i

14

.

4

l

s;

,

o

1EJS* LOC 1B&2B

480 V One Line Diagram

Revision 9

' Standby Bus

Miscellaneous Documents

NUMBER

DESCRIPTION

REVISION

River Bend Station Updated

Revision 10

-

Safety Analysis Report

Operating License NPF-47

River Bend Station Operating Revision 101

,

and Appendix A

License and Technical

Specifications

SDC-203

HPCS System Design

Revision 0

Critena

j

l

SDC-302 ENS

Safety Related 4.16 kV

Revision 0

Electrical Distribution System

Design Criteria

SURD-P50

SGTS Evstem Description

Revision 0

and ReqJirements Document

Test Report

HPCS 15 Stage Pump

6/29/77

T-36631-1

Performance Curve (Byron

Jackson)

Year 2000 Desktop Guide

Revision 0

-

Entergy Operations, Inc.,

7/29/98

-

Fire Protection PEER Group

Position Paper Regarding -

Fire Brigades and OSHA

29 CFR 1910.134

1961C

River Bend Station Check

Revision 0

Valve Program Develooment

STM-GPST-A0118.00

Service Water Systems

-

Training Manual

i

e

i

15

l

'

l

l

k

. -

_

-_

_

_

_

.

-N

?

i

Safety Evaluations

Document Evaluated

Safety Evaluation (SEN)

LCN 04.06-032

97-0063

,

l

LCN 06.03-029

97-0071

!

LCN 07.03-151

96-0086

l

_ LCN 08.03.062

96-0026

LCN 08.03-069

97-0023

'

MR 95-0010 & LCN 09.03-219 REVS

96-0098

MR 96-0068 & FCN 1, LCN 09.03-231

97-0073

CR 95-0839 & LCN 09.05-108

96-0052

MR 96-0048 & LCN 10.04-160

97-0016

LAR 97-27

97-0072

LAR 97-03

97-0005

LAR 97-03 REV 1

97-0009

ER 97-0155

97-0038

l

ER 97-0294

97-0081

ER 97-0607

97-0087

CR 96-1644

97-0008

,

'

!

SOP-0018

97-0007

TP-97-0004

97-0084

Safety Evaluations

!

SEN

Document

Title

l

98-0027

ER 98-0380

Repair / Replacement of HVC System Damper Blade Seals

98-0028

ER 98-0321

Uprate Motor Data to Reflect Actual LRA Test Data

98-0029

ER 98-0136

Evaluation of Alternate HVK Chiller 1C Motor

98-0030

ER 98-0068

Replace Trend Recorders with Digital Recorders

08-0031

ER 98-0397

Repair /Rertacement of HVC System Damper Blade Seals

l

98-0032

ER 97-0040

BWR Stab' ity Enhanced Option 1 A

98-0033

LCN 15.06-006

Revise LOCA Calculations

1

l

i

!

l

16

l

l

,