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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P3791999-10-21021 October 1999 Forwards NRC Form 396 & NRC Form 398 for Renewal of Licenses SOP-20607-1 & SOP-20610-1.Without Encls ML20217N2521999-10-20020 October 1999 Provides Supplemental Info Re 990405 Containment Insp Program Requests for Relief RR-L-1 & RR-L-2,in Response to 991013 Telcon with NRC ML20217K7541999-10-15015 October 1999 Forwards Rev 1 to Unit 1,Cycle 9 & Unit 2 Cycle 7 Colrs,Iaw Requirements of TS 5.6.5.Figure 5, Axial Flux Difference Limits as Function of Percent of Rated Thermal Power for RAOC, Was Revised for Both Units ML20217G6751999-10-13013 October 1999 Requests Withholding of Proprietary Info Contained in Application for Amend to OLs to Implement Relaxations Allowed by WCAP-14333-P-A,rev 1 ML20217G1071999-10-0707 October 1999 Informs That on 990930,NRC Staff Completed mid-cycle PPR of Vogtle & Did Not Identify Any Areas in Which Performance Warranted More than Core Insp Program.Nrc Plans to Conduct Core Insps at Facility Over Next Six Months ML20216J9041999-10-0101 October 1999 Forwards Response to RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20216J9161999-10-0101 October 1999 Forwards Response to NRC 990723 RAI Re GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20217B0141999-10-0101 October 1999 Forwards Insp Repts 50-424/99-06 & 50-425/99-06 on 990725- 0904 at Vogtle Units 1 & 2 Reactor Facilities.Determined That One Violation Occurred & Being Treated as non-cited Violation ML20212E8751999-09-20020 September 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear Grade Activated Charcoal. Description of Methods Used to Comply with Std Along with Most Recent Test Results Encl ML20212E7481999-09-20020 September 1999 Requests Approval Per 10CFR50.55a to Use Alternative Method for Determining Qualified Life of Certain BOP Diaphragm Valves than That Specified in Code Case N-31.Proposed Alternative,Encl ML20212C2191999-09-16016 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, Which Is Current Need for NRC Operator Licensing Exams for Years 2000 Through 2003 of Plant Vogtle,Per Administrative Ltr 99-03 ML20211Q4801999-09-0101 September 1999 Informs That on 990812-13,Region II Hosted Training Managers Conference on Recent Changes to Operator Licensing Program. List of Attendees,Copy of Slide Presentations & List of Questions Received from Participants Encl ML20211J5291999-08-30030 August 1999 Forwards Snoc Copyright Notice Dtd 990825,re Production of Engineering Drawings Ref in VEGP UFSAR ML20211J5251999-08-30030 August 1999 Forwards Response to NRC 990727 RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20211J7381999-08-27027 August 1999 Informs That Licensee Vessel Data Is Different than NRC Database Based on Listed Info,Per 990722 Request to Review Rvid ML20211E9251999-08-23023 August 1999 Forwards fitness-for-duty Performance Data for Jan-June 1999,as Required by 10CFR26.71(d).Data Reflected in Rept Covers Employees at Vogtle Electric Generating Plant ML20210V0881999-08-16016 August 1999 Forwards Insp Repts 50-424/99-05 & 50-425/99-05 on 990620- 0724.No Violations Noted.Vogtle Facility Generally Characterized by safety-conscious Operations,Sound Engineering & Maintenance Practices ML20210Q4611999-08-0505 August 1999 Informs That NRC Plans to Administer Generic Fundamentals Exam Section of Written Operator Licensing Exam on 991006 for Vogtle.Requests Info Re Individuals Who Will Take Exam. Sample Registration Ltr Encl ML20210L2181999-08-0202 August 1999 Forwards NRC Form 396 & Form 398 for Renewal of Listed Licenses,Iaw 10CFR55.57.Without Encl ML20210N1191999-08-0202 August 1999 Discusses 990727 Telcon Between Rs Baldwin & R Brown Re Administration of Licensing Exam at Facility During Wk of 991213 ML20210G3351999-07-27027 July 1999 Forwards Second Request for Addl Info Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20210E0121999-07-23023 July 1999 Forwards Second Request for Addl Info Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20210D9341999-07-22022 July 1999 Discusses Closure of TACs MA0581 & MA0582,response to Requests for Info in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20210C8011999-07-21021 July 1999 Provides Response to NRC AL 99-02,which Requests That Addressees Submit Info Pertaining to Estimates of Number of Licensing Actions That Will Be Submitted for NRC Review for Upcoming Fy 2000 & 2001 ML20210E0431999-07-15015 July 1999 Forwards Insp Repts 50-424/99-04 & 50-425/99-04 on 990502- 0619.Two Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20209H3881999-07-14014 July 1999 Forwards Revs 1 & 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Unit 1 & 2 ML20209C4041999-07-0101 July 1999 Forwards Rev 29 to VEGP Units 1 & 2 Emergency Plan.Rev 29 Incorporates Design Change Associated with Consolidation of Er Facilities Computer & Protues Computer.Justifications for Changes & Insertion Instructions Are Encl ML20196H8081999-06-28028 June 1999 Discusses 990528 Meeting Re Results of Periodic PPR for Period of Feb 1997 to Jan 1999.List of Attendees Encl ML20212J2521999-06-21021 June 1999 Responds to NRC RAI Re Yr 2000 Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701 ML20196F9171999-06-21021 June 1999 Forwards Owner Rept for ISI for Vogtle Electric Generating Plant,Unit 1 Eighth Maint/Refueling Outage. Separate Submittal Will Not Be Made to NRC on SG Tubes Inspected During Subj Outage ML20195F8031999-06-11011 June 1999 Forwards Changes to VEGP Unit 1 Emergency Response Data Sys (ERDS) Data Point Library.Changes Were Completed on 990308 While Unit 1 Was SD for Refueling Outage ML20207E7421999-06-0303 June 1999 Refers to from NRC Which Issued Personnel Assignment Ltr to Inform of Lm Padovan Assignment as Project Manager for Farley Npp.Reissues Ltr with Effective Date Corrected to 990525 ML20207F6201999-06-0202 June 1999 Sixth Partial Response to FOIA Request for Documents.Records in App J Encl & Will Be Available in Pdr.App K Records Withheld in Part (Ref FOIA Exemptions 7) & App L Records Completely Withheld (Ref FOIA Exemption 7) ML20207D9861999-05-28028 May 1999 Informs That,Effective 990325,LM Padovan Was Assigned as Project Manager for Plant,Units 1 & 2 ML20207D2701999-05-19019 May 1999 Forwards Insp Repts 50-424/99-03 & 50-425/99-03 on 990321- 0501.One Violation of NRC Requirements Identified & Being Treated as non-cited Violation Consistent with App C of Enforcement Policy ML20206M5141999-05-11011 May 1999 Informs That NRC Ofc of Nuclear Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Rl Emch Section Chief for Vogtle. Reorganization Chart Encl ML20206U4061999-05-11011 May 1999 Confirms Telcon with J Bailey Re Mgt Meeting Scheduled for 990528 to Discuss Results of Periodic Plant Performance Review for Plan Nuclear Facility Fo Period of Feb 1997 - Jan 1999 05000424/LER-1998-006, Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Exi1999-05-10010 May 1999 Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Existed ML20206D6411999-04-29029 April 1999 Forwards Vogtle Electric Generating Plant Radiological Environ Operating Rept for 1998 & Vogtle Electric Generating Plant Units 1 & 2 1998 Annual Rept Annual Radioactive Effluent Release Rept ML20206D5881999-04-29029 April 1999 Forwards Rept Which Summarizes Effects of Changes & Errors in ECCS Evaluation Models on PCT for 1998,per Requirements of 10CFR50.46(a)(3)(ii).Rept Results Will Be Incorporated Into Next FSAR Update ML20206D6951999-04-28028 April 1999 Provides Update of Plans for VEGP MOV Periodic Verification Program Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20206C2241999-04-21021 April 1999 Forwards Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2.Page E2-2 Was Iandvertently Omitted from Previously Submitted Rept on 990413 ML20206A6371999-04-21021 April 1999 Forwards SE Authorizing Licensee Re Rev 9 to First 10-yr ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML20205Q3351999-04-15015 April 1999 Forwards Insp Repts 50-424/99-02 & 50-425/99-02 on 990214-0320.Three Violations Identified & Being Treated as Non-Cited Violations ML20205T2351999-04-0909 April 1999 Informs That on 990317,B Brown & Ho Christensen Confirmed Initial Operator Licensing Exam Scheduled for Y2K.Initial Exam Date Scheduled for Wk of 991213 for Approx 10 Candidates ML20205K7501999-04-0505 April 1999 Informs That Effective 990329,NRC Project Mgt Responsibility for Plant Has Been Transferred from Dh Jaffe to R Assa ML20209A3741999-04-0505 April 1999 Submits Several Requests for Relief for Plant from Code Requirements Pursuant to 10CFR50.55a(a)(3) & (g)(5)(iii).NRC Is Respectfully Requested to Approve Requests Prior to Jan 1,2000 ML20205H3481999-03-31031 March 1999 Forwards Georgia Power Co,Oglethorpe Power Corp,Municipal Electric Authority of Ga & City of Dalton,Ga Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81 ML20205F9091999-03-29029 March 1999 Submits Rept of Number of SG Tubes Plugged During Plant Eighth Maintenance/Refueling Outage (1R8).Inservice Insps Were Completed on SGs 1 & 4 on 990315.No Tubes Were Plugged ML20205G0761999-03-26026 March 1999 Provides Results of Individual Monitoring for 1998.Encl Media Contains All Info Required by Form NRC 5.Without Encl 1999-09-20
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217P3791999-10-21021 October 1999 Forwards NRC Form 396 & NRC Form 398 for Renewal of Licenses SOP-20607-1 & SOP-20610-1.Without Encls ML20217N2521999-10-20020 October 1999 Provides Supplemental Info Re 990405 Containment Insp Program Requests for Relief RR-L-1 & RR-L-2,in Response to 991013 Telcon with NRC ML20217K7541999-10-15015 October 1999 Forwards Rev 1 to Unit 1,Cycle 9 & Unit 2 Cycle 7 Colrs,Iaw Requirements of TS 5.6.5.Figure 5, Axial Flux Difference Limits as Function of Percent of Rated Thermal Power for RAOC, Was Revised for Both Units ML20217G6751999-10-13013 October 1999 Requests Withholding of Proprietary Info Contained in Application for Amend to OLs to Implement Relaxations Allowed by WCAP-14333-P-A,rev 1 ML20216J9161999-10-0101 October 1999 Forwards Response to NRC 990723 RAI Re GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20216J9041999-10-0101 October 1999 Forwards Response to RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20212E7481999-09-20020 September 1999 Requests Approval Per 10CFR50.55a to Use Alternative Method for Determining Qualified Life of Certain BOP Diaphragm Valves than That Specified in Code Case N-31.Proposed Alternative,Encl ML20212E8751999-09-20020 September 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear Grade Activated Charcoal. Description of Methods Used to Comply with Std Along with Most Recent Test Results Encl ML20212C2191999-09-16016 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, Which Is Current Need for NRC Operator Licensing Exams for Years 2000 Through 2003 of Plant Vogtle,Per Administrative Ltr 99-03 ML20211J5291999-08-30030 August 1999 Forwards Snoc Copyright Notice Dtd 990825,re Production of Engineering Drawings Ref in VEGP UFSAR ML20211J5251999-08-30030 August 1999 Forwards Response to NRC 990727 RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20211J7381999-08-27027 August 1999 Informs That Licensee Vessel Data Is Different than NRC Database Based on Listed Info,Per 990722 Request to Review Rvid ML20211E9251999-08-23023 August 1999 Forwards fitness-for-duty Performance Data for Jan-June 1999,as Required by 10CFR26.71(d).Data Reflected in Rept Covers Employees at Vogtle Electric Generating Plant ML20210L2181999-08-0202 August 1999 Forwards NRC Form 396 & Form 398 for Renewal of Listed Licenses,Iaw 10CFR55.57.Without Encl ML20210C8011999-07-21021 July 1999 Provides Response to NRC AL 99-02,which Requests That Addressees Submit Info Pertaining to Estimates of Number of Licensing Actions That Will Be Submitted for NRC Review for Upcoming Fy 2000 & 2001 ML20209H3881999-07-14014 July 1999 Forwards Revs 1 & 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Unit 1 & 2 ML20209C4041999-07-0101 July 1999 Forwards Rev 29 to VEGP Units 1 & 2 Emergency Plan.Rev 29 Incorporates Design Change Associated with Consolidation of Er Facilities Computer & Protues Computer.Justifications for Changes & Insertion Instructions Are Encl ML20196F9171999-06-21021 June 1999 Forwards Owner Rept for ISI for Vogtle Electric Generating Plant,Unit 1 Eighth Maint/Refueling Outage. Separate Submittal Will Not Be Made to NRC on SG Tubes Inspected During Subj Outage ML20212J2521999-06-21021 June 1999 Responds to NRC RAI Re Yr 2000 Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701 ML20195F8031999-06-11011 June 1999 Forwards Changes to VEGP Unit 1 Emergency Response Data Sys (ERDS) Data Point Library.Changes Were Completed on 990308 While Unit 1 Was SD for Refueling Outage 05000424/LER-1998-006, Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Exi1999-05-10010 May 1999 Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Existed ML20206D5881999-04-29029 April 1999 Forwards Rept Which Summarizes Effects of Changes & Errors in ECCS Evaluation Models on PCT for 1998,per Requirements of 10CFR50.46(a)(3)(ii).Rept Results Will Be Incorporated Into Next FSAR Update ML20206D6411999-04-29029 April 1999 Forwards Vogtle Electric Generating Plant Radiological Environ Operating Rept for 1998 & Vogtle Electric Generating Plant Units 1 & 2 1998 Annual Rept Annual Radioactive Effluent Release Rept ML20206D6951999-04-28028 April 1999 Provides Update of Plans for VEGP MOV Periodic Verification Program Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20206C2241999-04-21021 April 1999 Forwards Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2.Page E2-2 Was Iandvertently Omitted from Previously Submitted Rept on 990413 ML20209A3741999-04-0505 April 1999 Submits Several Requests for Relief for Plant from Code Requirements Pursuant to 10CFR50.55a(a)(3) & (g)(5)(iii).NRC Is Respectfully Requested to Approve Requests Prior to Jan 1,2000 ML20205H3481999-03-31031 March 1999 Forwards Georgia Power Co,Oglethorpe Power Corp,Municipal Electric Authority of Ga & City of Dalton,Ga Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81 ML20205F9091999-03-29029 March 1999 Submits Rept of Number of SG Tubes Plugged During Plant Eighth Maintenance/Refueling Outage (1R8).Inservice Insps Were Completed on SGs 1 & 4 on 990315.No Tubes Were Plugged ML20205G0761999-03-26026 March 1999 Provides Results of Individual Monitoring for 1998.Encl Media Contains All Info Required by Form NRC 5.Without Encl ML20205H4051999-03-25025 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81,as Requested IAW 10CFR50.75(f)(1) ML20205H3891999-03-25025 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81,as Requested IAW 10CFR50.75(f)(1).Page 2 in Third Amend Power Sales Contract of Incoming Submittal Not Included ML20205A9441999-03-25025 March 1999 Forwards VEGP Unit 1 Cycle 9 Colr,Per TS 5.6.5.d ML20205H3811999-03-24024 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81,as Requested IAW 10CFR50.75(f)(1) ML20205H3621999-03-22022 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81, as Requested IAW 10CFR50.75(f)(1) ML20204G4361999-03-18018 March 1999 Forwards Summary Rept of Present Level & Source of on-site Property Damage Insurance Coverage for Vegp,Iaw Requirements of 10CFR50.54(w)(3) ML20204C0591999-03-17017 March 1999 Forwards Rev 0 to WCAP-15160, Evaluation of Pressurized Thermal Shock for Vegp,Unit 2 & Rev 0 to WCAP-15159, Analysis of Capsule X from Vegp,Unit 2 Reactor Vessel Radiation Surveillance Program ML20207K9551999-03-11011 March 1999 Forwards Response to Rai,Pertaining to Positive Alcohol Test of Licensed Operator.Encl Info Provided for NRC Use in Evaluation of Fitness for Duty Occurrence.Encl Withheld,Per 10CFR2.790(a)(6) ML20207L9721999-03-10010 March 1999 Forwards Rev 15 to EPIP 91104-C of Manual Set 6 of Vogtle Epips.Without Encl ML20207B0191999-02-25025 February 1999 Forwards Fitness for Duty Performance Data for six-month Reporting Period 980701-1231,IAW 10CFR26.71(d) 05000424/LER-1998-009, Forwards LER 98-009-00 Re Event in Which Improper Testing Method Resulted in Inadequate Surveillances on 9812291999-01-27027 January 1999 Forwards LER 98-009-00 Re Event in Which Improper Testing Method Resulted in Inadequate Surveillances on 981229 ML20199F7701999-01-13013 January 1999 Submits Revised Response to RAI Re Licensee 980713 Proposed Amend to Ts,Eliminating Periodic Response Time Testing Requirements on Selected Sensors & Protection Channels. Corrected Copy of Table,Encl ML20199F7981999-01-13013 January 1999 Forwards Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage. Change Bar in Margin of Affected Pages Denotes Changes to Rept ML20199G1381999-01-13013 January 1999 Forwards Copy of Permit Renewal Application Package for NPDES Permit Number GA0026786,per Section 3.2 of VP Environ Protection Plan 05000424/LER-1998-007, Forwards LER 98-007-00,re Inadequate Surveillances Due to Improperly Performed Response Time Testing,On 981215,IAW 10CFR50.731999-01-13013 January 1999 Forwards LER 98-007-00,re Inadequate Surveillances Due to Improperly Performed Response Time Testing,On 981215,IAW 10CFR50.73 ML20198F6131998-12-18018 December 1998 Forwards Revised Certification of Medical Exam Form for License SOP-21147.Licensee Being Treated for Hypertension. Util Requests That Individual License Be Amended to Reflect Change in Status ML20198L6631998-12-18018 December 1998 Forwards Amend 37 to Physical Security & Contingency Plan. Encl 1 Provides Description & Justification for Changes & Encl 2 Contains Actual Amend 37 Pages.Amend Withheld,Per 10CFR73.21 ML20198D9291998-12-16016 December 1998 Forwards Requested Info Re Request to Revise TSs Elimination of Periodic Pressure Sensor Response Time Tests & Elimination of Periodic Protection Channel Response Time Tests ML20198D9991998-12-16016 December 1998 Forwards Responses to 980916 RAI Re Response to GL 97-01, Degradation of Control Rod Drive Mechanism Nozzle & Other Vessel Closure Head Penetrations ML20198D8171998-12-14014 December 1998 Forwards NRC Form 396 & Form 398 for Renewal of License OP-20993.Without Encls ML20206N3051998-12-0808 December 1998 Submits RAI Re Replacement of Nuclear Instrument Sys Source & Intermediate Range Channels & post-accident Neutron Flux Monitoring Sys 1999-09-20
[Table view] Category:UTILITY TO NRC
MONTHYEARELV-02056, Forwards Operator Exam Schedule for Facility,Per Generic Ltr 90-07 Request,Including Number of Candidates to Be Examined During NRC Site Visits,Requalification Schedules & Number of Candidates to Participate in Generic Fundamentals Exam1990-09-0606 September 1990 Forwards Operator Exam Schedule for Facility,Per Generic Ltr 90-07 Request,Including Number of Candidates to Be Examined During NRC Site Visits,Requalification Schedules & Number of Candidates to Participate in Generic Fundamentals Exam ELV-01599, Discusses Mods to HED-1114 Re Plant Dcrdr,Per . Amber Monitor Light Covers Installed for Spare Pumps to Make Status of Pumps Readily Apparent to Operator1990-09-0404 September 1990 Discusses Mods to HED-1114 Re Plant Dcrdr,Per . Amber Monitor Light Covers Installed for Spare Pumps to Make Status of Pumps Readily Apparent to Operator ELV-02059, Clarifies 900409 Response to 900323 Confirmation of Action Ltr.Util Made 31 Successful Start Attempts for Diesel Generator (DG) 1A & 29 Successful Start Attempts for DG 1B1990-08-30030 August 1990 Clarifies 900409 Response to 900323 Confirmation of Action Ltr.Util Made 31 Successful Start Attempts for Diesel Generator (DG) 1A & 29 Successful Start Attempts for DG 1B ELV-01956, Forwards Listed Documents in Response to Request for Addl Info Re Settlement Monitoring Program,Per 900614 Request1990-08-30030 August 1990 Forwards Listed Documents in Response to Request for Addl Info Re Settlement Monitoring Program,Per 900614 Request ELV-02050, Responds to Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Administrative Procedures Controlling Verification & Validation of Emergency Operating Procedures Will Be Evaluated & Revised as Required1990-08-30030 August 1990 Responds to Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Administrative Procedures Controlling Verification & Validation of Emergency Operating Procedures Will Be Evaluated & Revised as Required ELV-02028, Forwards Fitness for Duty Performance Data for First Six Month Period,Per 10CFR26.71(d)1990-08-22022 August 1990 Forwards Fitness for Duty Performance Data for First Six Month Period,Per 10CFR26.71(d) ELV-02022, Forwards Revised LER Re Apparent Personnel Error Leading to Unsecured Safeguards Info.Ler Withheld1990-08-22022 August 1990 Forwards Revised LER Re Apparent Personnel Error Leading to Unsecured Safeguards Info.Ler Withheld ELV-02027, Forwards Rev 0 to Core Operating Limits Rept, for Cycle 3, Per Amends 32 & 12 to Licenses NPF-68 & NPF-79,respectively1990-08-20020 August 1990 Forwards Rev 0 to Core Operating Limits Rept, for Cycle 3, Per Amends 32 & 12 to Licenses NPF-68 & NPF-79,respectively ELV-01973, Submits Rept Re Results of Leakage Exams Conducted During Spring 1990 Refueling Outage,Per TMI Item III.D.1.1.None of Identified Leakage Considered Excessive.Work Orders Issued in Effort to Reduce Leakage to Level as Low Practical1990-08-14014 August 1990 Submits Rept Re Results of Leakage Exams Conducted During Spring 1990 Refueling Outage,Per TMI Item III.D.1.1.None of Identified Leakage Considered Excessive.Work Orders Issued in Effort to Reduce Leakage to Level as Low Practical ELV-01918, Responds to NRC 900612 Request for Comments & Suggestions on Draft risk-based Insp Guide.Util Conducting Individual Plant Exam & Will Withhold Comment on risk-based Insp Guide Until Completion1990-08-0303 August 1990 Responds to NRC 900612 Request for Comments & Suggestions on Draft risk-based Insp Guide.Util Conducting Individual Plant Exam & Will Withhold Comment on risk-based Insp Guide Until Completion ELV-01943, Responds to Violation & Proposed Imposition of Civil Penalty in Insp Repts 50-424/90-11 & 50-425/90-11.Corrective Action: Complete Audit of Contents of Safeguards Info Container Performed & Unassigned Safeguards Info Dispositioned1990-07-27027 July 1990 Responds to Violation & Proposed Imposition of Civil Penalty in Insp Repts 50-424/90-11 & 50-425/90-11.Corrective Action: Complete Audit of Contents of Safeguards Info Container Performed & Unassigned Safeguards Info Dispositioned ELV-01949, Forwards Info Re Status of Pen Branch Fault Investigation. Investigations Conducted So Far Still Indicate That Pen Branch Fault Not Capable1990-07-26026 July 1990 Forwards Info Re Status of Pen Branch Fault Investigation. Investigations Conducted So Far Still Indicate That Pen Branch Fault Not Capable ELV-01500, Forwards Nuclear Decommissioning Funding Plan for Plant.Info Provides Assurance That NRC Prescribed Min Funding Will Be Available to Decommission Facilities1990-07-25025 July 1990 Forwards Nuclear Decommissioning Funding Plan for Plant.Info Provides Assurance That NRC Prescribed Min Funding Will Be Available to Decommission Facilities ML20055H6441990-07-23023 July 1990 Submits Summary of Snubber Types & Sample Plans for Functional Testing to Be Performed During Sept 1990 Outage ML20044B0311990-07-13013 July 1990 Forwards Vogtle Electric Generating Plant Unit 1 Reactor Containment Bldg 1990 Integrated Leakage Rate Test Final Rept. ML20044B1541990-07-12012 July 1990 Responds to NRC 900612 Ltr Re Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Eop Step Deviation Documents to Be Upgraded,Adding More Justification & Temporary Change Issued to Correct EOP Deficiencies ELV-01867, Responds to Violations Noted in Insp Repts 50-424/90-10 & 50-425/90-10.Corrective Action:Level Indication Error Corrected After Discrepancy Discovered1990-07-12012 July 1990 Responds to Violations Noted in Insp Repts 50-424/90-10 & 50-425/90-10.Corrective Action:Level Indication Error Corrected After Discrepancy Discovered ML20055F1651990-07-0909 July 1990 Forwards Comments Re NUREG-1410 ELV-01858, Advises That Full Compliance W/Violation Will Not Be Achieved Until Nov 1990,when Evaluation of VP-2693 Complete1990-07-0606 July 1990 Advises That Full Compliance W/Violation Will Not Be Achieved Until Nov 1990,when Evaluation of VP-2693 Complete ML20044A8851990-07-0606 July 1990 Forwards Response to NRC Question on Steam Generator Level Instrumentation Setpoints,Per Revised Instrument Line Tap Locations.Tap Location Will Be Changed from Above Transition Cone to Below Transition Cone ELV-01834, Forwards Response & Comments to Regulatory Effectiveness Review Rept.Encl Withheld (Ref 10CFR73.21)1990-06-28028 June 1990 Forwards Response & Comments to Regulatory Effectiveness Review Rept.Encl Withheld (Ref 10CFR73.21) ML20044A2791990-06-25025 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Table Indicating Status of Each Generic Safety Issue Encl ML20043J0171990-06-22022 June 1990 Discusses Corrective Actions for Plant Site Area Emergency, Per 900514 Ltr.Jacket Water High Temp Switches Calibr for Diesel Generators,Using Revised Calibr Procedure ML20043H3061990-06-15015 June 1990 Forwards Rev 3 to ISI-P-014, Inservice Insp Program, for Review & Approval,Per Tech Spec 4.0.5 Re Surveillance Requirements.Rev Includes Withdrawal of Relief Requests RR-45,47,48 & 54 ML20043G2071990-06-12012 June 1990 Forwards Amend 18 to Physical Security & Contingency Plan. Amend Withheld (Ref 10CFR73.21) ML20043G1021990-06-0606 June 1990 Requests Temporary Waiver of Compliance from Requirements of Action Statement 27 of Tech Spec 3.3.2 for Period of 6 H When Two Operating Control Room Emergency Filtration Sys Trains Shut Down for Required Testing ML20043E6901990-06-0505 June 1990 Forwards Rev 12 to Emergency Plan & Detailed Description & Justification of Changes.W/O Rev ML20043G7651990-06-0505 June 1990 Forwards Rev 13 to Emergency Plan & Description & Justification of Changes ML20043B5991990-05-25025 May 1990 Forwards Scope & Objectives Re 1990 Annual Emergency Preparedness Exercise to Be Conducted on 900801 ML20043B5981990-05-24024 May 1990 Responds to Violations Noted in Insp Rept 50-424/90-05 on 900217-0330.Corrective Actions:Locked Valve Procedure Revised to Eliminate Utilization of Hold Tag on Valves Required by Tech Specs to Be Secured in Position ML20043B6291990-05-22022 May 1990 Forwards Rev 5 to ISI-P-008, Inservice Testing Program, Per Tech Specs 4.0.5 Re Surveillance Requirements & Generic Ltr 89-04 ML20043B6351990-05-22022 May 1990 Forwards Rev 2 to ISI-P-016, Inservice Testing Program, Per Generic Ltr 89-04, Guidance on Developing Acceptable Inservice Testing Programs. ML20042H0601990-05-14014 May 1990 Forwards Summary of Corrective Actions for 900320 Site Area Emergency Due to Loss of Offsite Power Concurrent W/Loss of Onsite Emergency Diesel Generator Capability.Truck Driver Disciplined for Lack of Attention ML20042G7301990-05-11011 May 1990 Forwards Revised Pages for May 1989,Jan & Mar 1990 Monthly Operating Repts for Vogtle Electric Generating Plant,Units 1 & 2.Revs Necessary Due to Errors Discovered in Ref Repts ML20042E2911990-04-18018 April 1990 Forwards Amend 17 to Security Plan.Amend Withheld (Ref 10CFR2.790) ML20042E7481990-04-0909 April 1990 Requests Approval to Return Facility to Mode 2 & Subsequent Power Operation,Per 900320 Event Re Loss of Offsite Power Concurrent W/Loss of Onsite Emergency Diesel Generator Capability ML20012E9001990-03-28028 March 1990 Provides Supplemental Response to Station Blackout Rule,Per NUMARC 900104 Request.Mods & Associated Procedure Changes Identified in Sections B & C W/Exception of Mods to Seals Will Be Completed 1 Yr from Acceptance of Analysis ML20012E8581990-03-28028 March 1990 Suppls Response to NRC Bulletin 88-010,Suppl 1 Re Traceability Reviews on Molded Case Circuit Breakers Installed in safety-related Applications.All Breakers Procured & Installed in Class 1E Equipment Reviewed ML20012E9761990-03-27027 March 1990 Requests Withdrawal of Inservice Insp Relief Requests RR-45, RR-47,RR-48 & Conditional Withdrawal of RR-54 Based on Reasons Discussed in Encl,Per 900206 Conference Call ML20012D8561990-03-22022 March 1990 Submits Special Rept 1-90-02 Re Number of Steam Generator Tubes Plugged During 1R2.One of Four Tubes Exceeded Plugging Limit & Required Plugging.Remaining Three Tubes Plugged as Precautionary Measure.No Defective Tubes Detected ML20012D6641990-03-22022 March 1990 Provides Followup Written Request for Waiver of Compliance to Make Tech Spec 3.04 Inapplicable to Tech Spec 3.8.1.2 to Permit Entry Into Mode 5 W/Operability of Diesel Generator a & Associated Load Sequencer Unverified ML20012D3681990-03-19019 March 1990 Forwards Proprietary & Nonproprietary Suppl 2 to WCAP-12218 & WCAP-12219, Supplementary Assessment of Leak-Before-Break for Pressurizer Surge Lines of Vogtle Units 1 & 2, Per 900226 Request.Proprietary Rept Withheld (Ref 10CFR2.790) ML20012D3401990-03-19019 March 1990 Submits Response to 891121 Request for Addl Info Re Settlement Monitoring Program.Current Surveying Procedures Used by Plant to Monitor Settlement of Major Structures Outlined in Procedure 84301-C.W/41 Oversize Drawings ML20012D6631990-03-15015 March 1990 Responds to Generic Ltr 89-19 Re Resolution of USI A-47 on Safety Implications of Control Sys in Lwrs.Overfill Protection Sys Sufficiently Separate from Control Portion of Main Feedwater Control Sys & Not Powered from Same Source ML20012C4681990-03-0606 March 1990 Provides Summary Rept of Property Damage Insurance Levels, Per 10CFR50.54(w)(1) ML20012B2891990-03-0606 March 1990 Forwards Plant Pipe Break Isometrics,Vols 1 & 2 & Advises That Encl Figures Have Been Revised to Be Consistent W/Pipe Analysis in Effect at Time That Unit 2 Received Ol,Including Revs Through 890930.W/309 Oversize Figures ML20012B2421990-03-0606 March 1990 Forwards Cycle 3 Radial Peaking Factor Limit Rept & Elevation Dependent Peaking Factor Vs Core Height Graph ML20011F5291990-02-26026 February 1990 Withdraws 881107 Proposed Amend to Tech Spec 3.8.1.1, Revising Action Requirements for Inoperable Diesel Generator to Clarify Acceptability of Air Roll Tests on Remaining Operable Diesel Generator ML20011F5261990-02-26026 February 1990 Forwards 1989 Annual Rept - Part 1. Part 2 Will Be Submitted by 900501 ML20011E8911990-02-12012 February 1990 Advises That Hh Butterworth No Longer Employed by Util 1990-09-06
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e Georgia Power Corspany
, . 333 Piedmont Avenue Atlanta, Georgia 30308 Teephone 404 5266526 Mamng Mdress:
Post Offce Bom 4545 Attanta, Georgia 30302 W. G. Heireton, lit mesouherrt edocarcsyseme
. Semor Vce PresMent Nxlow Opwatens y(,g7 ;
0051e X7GJ17-V600 i October 19, 1988 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 PLANT YOGTLE - UNIT 1 NRC DOCKET 50-424 OPERATING LICENSE NPF-68 i REPORT OF LOCA REANALYSIS l
Gentlemen: <
Georgia Power Company (GPC) in our letter VL-51 dated August 3 0, 1 1838, withdrew a request to revise the value of the Her.t Flux Hot Channel Factor FQ(z) found in Technical Specification 3.2.2. This withdrawal was ba',ed upon an analysis perfomed by Westinghouse Electric Corporation (Westinghouse) which demonstrated the acceptability of a value of 'F (z) of 2.30. A report ;
on the Westinghouse analysis and its conclusions s horeby provided as ,
Enclosure i for NRC review. .
1 Revisions to the FSAR are being evaluated in accordance with 10 CFR 50.59 -
and will be included in an upcoming FSAR amendment. Upon restart from the current refueling outage, the administrative limit for Fq(z) of 2.25 which was imposed pending completion of the Westinghouse analysis will be rescinded, and Plant Vogtle will return to operation with a value of FQ (z) of 2.30.
The analyses and conclusions discussed herein are equally valid for Plant Yogtle Unit 2.
'If you have questions regarding this information, please contact this office. ,
Sincerely, l
Y W. G. Hairston, III WEB /11h Enclosure C: (see next page) 8810250138 881019 "1 DR ADOCK 0%4 4 Aool
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Georgia Power d U. S. Nuclear Regulatory Comission October 19, 1988 Page Two c: Georgia Power Company Mr. P. D. Rice Mr. G. Bockhold, Jr.
GO-NORMS l
l U.'S; Nuclear Regulatory Comission
! Dr. J. N. Grace, Regional Administrator Mr. J. B. Hopkins, Licensing Project ?ianager, NRA (2 copies)
Mr. J. F. Rogge, Senior Resident Inspector - Operations, Vogtle l
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I ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RATE FOR V0GTLE UNIT 1 BACKGROUND As an indirect result of pre-operational testing at Vogtle Unit 2, it was determined that the Containment Spray System (CSS) maximum flow rate for Unit 1 was higher than was quoted in several sections of the FSAR. Further investigation by Westinghouse Fluid Systems indicated a minimum increase of 169 gpm. The following presents the summaries of safety evaluations performed to assess the effect of increased CSS flow rates on the LOCA-related anulyses performed by Westinghouse for Vogtle Unit 1.
BASES LARGE BREAK LOCA - FSAR CHAPTER 15.6.5
! The large break LOCA analysis which formed the licensing basis for Vogtle Unit 1 had very little marain to the 22000f peak clad temperature (PCT) limit specified in 10CFR 50.'46. The limiting case had a PCT of 21720F at an overall peaking factor (F of 2.30 for the 'imiting discharge coefficient :
i (CD ) of 0.6 (Reference 1)g), as computed using the 1981 version of the large break Westinghouse Evaluation Model (Reference 2). The effect of containment purging as reported in Chapter 6.2.1. 5 of the Vogtle FSAR (Reference 1) increases the PCT by 100F. A safety evaluation performed by Westinghouse which considers the effect of thimble tube modeling and chamfered fuel pellets resulted in an 80F increase in the PCT. Therefore, the overall PCT that served as the licensing basis was 21900F. An increase of 169 gpm in the containment spray system flow rate (from S400 to 6569 gpm) would have resulted in a PCT increase of approximately 250F based on conservative sensitivities. This would have resulted in an overall PCT of approximately 22150F which exceeded the 22000F PCT limit as specified in 10CFR 50.46. A Justification for Continued Operation (JCO) was submitted to the NRC and Vogtle Unit I was allowed to operate at a reduced Fg of 2.25.
In order to address the increased CSS flow rate and return to an Fo of 2.30, the idrge break LOCA was reanalyzed. The reanalysis was perfonned with the 1981 version of the large break Westinghouse Evaluation Model (Reference 2) ;
with modifications for thimble tube modeling Ps specified in Reference 3. The ;
analysis incorporated the following considerations:
- 1) increased containment spray flow from 6400 gpm to 6669 gpm
- 2) increased RCS pressure from 2280 psia to 2295 psia to account for instrument uncertainty (Veritrak issue resolution)
- 3) reduced fuel rod backfill pressure from 350 psia to 275 psia
- 4) chamfered fuel data (17x17 STD fuel) '
- 5) reduced accumulator L/D ratios from calculated to measured values E-1 ,
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. s ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RATE FOR V0GTLE UNIT 1
- 6) revised containment heat sink data
- 7) thimble tube modeling as required by WCAP-9561-P-A
- 8) reduced RHR flows
- 9) 5% steam generator tube plugging Items 2, 4, 7, and 8 have been addressed previously via a 10CFR 50.59 Safety Evaluation.
Analysis results show the limiting break continues to be the double ended cold leg guillotine (DECLG) with maximum safeguards safety injection flow and Cp=0.6 resulting in a PCT of 1995.80F for an FQ of 2.32. The increased PCT margin to the regulatory limit can be largely attributed to the benefit which accrues from the reduced fuel rod backfill pressure (Item 3 above). In the previous 1981 Model ECCS analysis, perfonned in 1983, the hot assembly average fuel rod burst at 105.1 seconds resulting in an assembly average blockage of 56.47, and a burst / blockage penalty of 2700F when compared to the unblocked rod temperature (according to NRC imposed burst / blockage models of NUREG-0630). Because of the reduced backfill pressure the average hot assembly rod did not burst and, therefore, did not incur the 2700F penalty.
This behavior is known as the cliff effect since a small change in plant parameters or model input may cause rod burst. This cliff effect is characteristic of the NUREG-0630 burst / blockage models.
In addition to reanalyzing the Co=0.6 maximum safeguards case, the C D=0.6 and 0.8 case for minimum safeguards were also reanalyzed. The results and FSAR changes for the reanalysis were provided to Georgia Power Company (GPC) in Reference 4. These results demonstrate compliance with the limits set forth in 10CFR 50.46 for the increased containment spay system flow rate for Vogtle Unit 1.
Of the changes to the large break LOCA analysis specified above (items 1 to 9), only increased containment spray flow had the potential to effect radiological consequences. Regulatory Guide 1.4 dictates a set of assumptions regarding core damage tnd containment leakage which defines a conservative and bounding case that ef fectively eliminates any effect that might be realistically expected from these changes. The exception, as stated, is containment spray flow which is used in detennining the rate of removal of airborne iodine from the containment. However, increased containment spray increases the iodine removal rate thereby decreasing the radiological consequences. Therefore, the reported values continue to be bounding with !
respect to increased containment spray flow.
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s ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RA 1 FOR V0GTLE UNIT 1 SMALL BREAX LOCA - FSAR CHAPTER 15.6.5 The current FSAR small break LOCA analysis for Vogtle Unit 1 was performed using the NRC approved Suall Break LOCA ECCS Evaluation Model (Reference 5),
which resulted in the most limiting PCT of 15370F for the 4 inch equivalent diameter brer.k at an FQ of 2.32 (Reference 1). A containment analysis is not performed as part of the small break LOCA analysis (unlike la*ge break LOCA), therefore, no modeling of the containment spray system is considered.
Consequently, an increase in the containment spray system flow rate will have no effect on the small break LOCA and the current results remain valid.
ROD EJECTION MASS AND ENERGY RELEASE FOR DOSE CALCULATION - FSAR CHAPTER 15.4.8.3 and TABLE 15.4.8-2 Similar to a small break LOCA, a rod ejection accident analysis is performed to provide primary ad secondary mass and energy releases for use in computing the radiological consequences of a rod ejection accident as per Regulatory Guide 1.77. This analysis is a long term transient perfomed specifically to determine primary RCS mass and energy releases thrcugh the upper head break and secondary mass and energy releases via the secondary code safety valves.
These mass and energy releases are then used to compute the radiological consequences of a rod ejection accident. As with small break LOCA, no modeling of the containment spray system is performed. Therefore, an increase in the CSS flow rate will have no effect on the computed mass and energy releases and the subsequent calculated doses remain valid.
CONTAINMENT INTEGRITY -
(SHORT AND LONG TERM MASS AND ENERGY RELEASES AND INADVERTENT CONTAINMENT SPRAY ACTUA"0N) FSAR CP TER 6.2 The containment integrity analyses are described in FSAR Chapter 6.2. This chapter considers, Subcompartment Pressure Transient Analyses, Short Term and Long Term Mass and Energy Release Analyses for Postulated Loss-of-Coolant Accidents (LOCA), Containment Response Analyses following a LOCA or Steamline Break Inside Containment, and Inadvertent Spray Actuation Analyses.
For subcompartment pressure transient and short tem mass and energy analyses, an increase in the containment spray flowrate would have no effect on the calculated results since, because of the short duration of the transient (< 3 seconds), containment spre actuation is not considered. The long tcne mass and energy release and containment response calculations following a LOCA or a steamline break inside containment do take credit for the containment spray system. However, a low spray flowrate is modeled to minimize heat removal in order to conservatively calculate peak containment pressure and temperature re sponses. An increase in the containment spray fiowrate would be a benefit to these above identified analyses. Therefore, the conclusions presented in the current Yogtle FSAR will remain valid.
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l ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RATE FOR V0GTLE UNIT 1 The Inadvertent Spray Actuation Analysis is documented in Section 6.2.1.1.3.3 of the Vogtle FSAR. The purpose of this analysis is to determine the minimum pressure inside containment to calculate the peak differential pressure across the containment shell. In the event of inadvertent spray, the containment will depressurize until the air temperature is approximately equal to the spray temperature or the operator takes action to terminate the spray.
A reanalysis was performed based upor. the revised containment spray flowrate.
Results indicate a reduced containment pressure of 12.3 psia at approximately 10 minutes into the transient. Thus, the peak differential pressure is 2.36 psi across the containment shell. The design differential pressure for Vogtle is 3.0 psi. Therefore, the results of this analysis are within design limits ,
and conform to the acceptance criteria of NUREG-0880, i
STEAM GENERATOR TUBE RUPTURE - FSAR CHAPTER 15.6.3 For a steam generator tube rupture (SGTR) accident, safety injection (SI) is actuated on a low pressurizer pressure signal shortly after reactor trip due to the decrease in reactor coolant inventory. For the SGTR analysis, it is assumed that the SI flow is delivered to the RCS until the operator actions are completed to tenninate SI. Since the containment spray system is not actuated for an SGTR, operation of the spray system is not modeled in the analysis. Therefore, it is concluded that the increase in the containment spray flow for Vogtle will not effect the SGTR analysis cu: rentiv .. the '
Vogtle FSAR and the revised SGTR analysis presented in WCAP-ll731 (Reference 6).
BLOWDOWN REACTOR VESSEL AND LOOP FORCES - FSAR CHAPTER 3.6.2 The blowdown hydraulic forcing functions resulting from a loss of coolant accident are considered in Section 3.6.2.2 (Analytical Methods to Define Forcing Functions and Response Model s) of Volume 8 of the Vogtle FSAR ,
(Reference 1). The increase in the CSS flow rate will have no effect on the LOCA blowdown hydraulic loads since the maximum loads are generated within the first few tenths of a second after break initiation. For this reason the .
containment, including the containment spray system, is not considered in the LOCA hydraulic forces modeling and thus the increase in the CSS flow rate will have no effect on the results of the LOCA hydraulic forces calculations.
POST LOCA LONG TERM CORE COOLING SUBCRITICALITY REQUIREMENT; WESTINGHOUSE LICENSING POSITION - FSAR CHAPTER 15.6.5 The Westinghouse licensing position for satisfying the requirements of 10CFR Part 50 Section 50.46 Paragraph (b) Item (5) "Long Term Cooling" is defined in E-4 I
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ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RATE FOR V0GTLE UNIT 1 WCAP-8339 (Reference 7, pp. 4-22). The Westinghouse commitment is that the reactor will remain shutdown by borated ECCS water residing in the sump ,
following a LOCA (Reference 8). Since credit for the control rods is not l taken for large break LOCA, the borated ECCS water provided by the i accumulators and the RWST must have a concentration that, when mixed with other sources of borated and non-borated water, will result in the reactor core remaining subcritical assuming all control rods out. An increase in the containment spray system flow rate will have no effect on those volumes and boron concentrations assumed for this calculation. Therefore, the current values are unaffected by the increase in CSS flow rate for Vogtle Unit 1.
HOT LEG SWITCH 0VER TO PREVENT POTENTIAL BORON PRECIPITATION - FSAR CHAPTER I
6.3.2.5.4 The hot leg reci rculation switchover time analysis has been performed to determine the time following a LOCA that hot leg recirculation should be initiated. During a LOCA the plant switches to cold leg recirculation after the RW5T switchover setpoint has beer reached. If the break is in the cold leg there is a concern that the cold let injection water will fail to establish flow through the cora. Safety injection entering the broken loop i
will spill out the break, while SI entering the intact cold legs will I ci rculate around the downcome and out the break. With no flow path established through the core, core decay heat will cause boiling. As steam is produced, the boron associated with the steam remains in the vessel, thereby increasing the boric acid concentration in the core. The boron concentration in the vesal will increase to the solubility limit of the boric acid solution and the boron precipitates, plating out on the fuel rods, and adversely affecting their heat transfer characteristics.
The hot leg recirculation switchover time analysis establishes the time at which hot leg recirculation must be initiated to prevent boron precipitation in the core. This time is dependent on power level, and the RCS, RWST, and accumulator water volumes, masses, and boron concentrations. An increase in the containment spray system flow rate will have no effect these parameters such that there will be no effect on the post-LOCA hot leg switchover time of 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />.
, CONCLUSIONS The effect of an increase in the containment spray system flow rate on the LOCA related FSAR analyses for Vogtle Unit 1 has been evaluated by Westinghouse. In all cases, this change did not result in exceeding any design or regulatory limit. Therefore, the increased containment t., ray system flow rate for Vogtle Unit 1 is acceptable from the standpoint of the FSAR accident analyses discussed in this evaluation. Table 1 'ummarizes the results of this checklist. These analyses and conclusions nf equally vaild for Plant Vogtle Unit 2.
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ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RATE FOR YOGTLE UNIT 1 REFERENCES
- 1. Yogtle Units 1 and 2 (GAE/GBE) FSAR - Updated 6/30/88 Amendment 36.
- 2. WCAP-9220-P-A (Proprietary), WCAP-9221 (Non-Proprietary), Eiche1dinger, i C., "Westinghouse FCCS Evaluation Model - 1981 Version", Revision 1, '
1 981.
- 3. WCAP-9561 -P-A Addendum 3, Revision 1 (Proprietary), Young, M.Y.,
"Addendum To: BART-A1: A Computer Code For The Best-Estimate Analysis Of Reflood Transients (Special Report: Thimble Modeling In Westinghouse ECCS Evaluation Model)", July,1986. .
4 NS-SAT-SAI-88-318, "Vogtle Units 1 and 2 (GAE/GB") Final Large Break LOCA Analysis Results", August 24, 1988.
- 5. WCAP-8970 (Proprietary) and WCAP-8971 (Non-Proprietary), "Westinghouse Emergency Core Cooling System Small Break October 1975 Model", April I
1977.
- 6. WCAP-11731 (Proprietary), Lewis, R. N. , Mendler, O. J. , Mi'ler, T. A. , f and Rubin, K., "LOFTTR2 Analysis for a Steam Generator Tube Rupture ,
Event for the Yogtle Electric Generating Plant Units 1 and 2", January 1988.
- 7. WCAP-8339 (Non-Proprietary), Bordelon, F. M., et. al. , "Westinghouse ECCS Evaluation Model - Summary", June 1974.
- 8. "Westinghouse Technical Bulletin NSID-TB-86-08, "Post-LOCA Long-Tenn Cooling: Boron Requirements", October 31, 1986.
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ENCLOSURE REPORT OF THE EVALUATION FOR INCREASED CSS FLOW RATE FOR YOGTLE UNIT 1 TABLE 1 TRANSIENT SUM 4ARY FSAR CHAPTER ACCIDENT DESCRIPTION EFFECT ON RESULTS :
15.6.5 Large Break LOCA Large Break LOCA reanalyzed.
Compliance with 10CFR 50.46b(1-3) maintained.
15.6.5 Small Break LOCA No ad'!erse effect on the FSAR peak cladding temperature calculations, maximum cladding oxidation or maximum hydrogen generation.
Compliance with 10CFR 50.46b(1-3) maintained.
15.4.8.3 Rod Ejection Accident No adverse effect on mass and .
energy releases. Compliance with !
10CFR 100,11 limits maintained.
6.2 Containment Integrity No adverse effect on short or long Short and Long Term term mass and energy releases.
Mass and Energy Release Compliance with current environ- i mental qualification limits main- I tained.
Inadvertent Spray Inadvertent spray actuation re-Actuation analyzed. Compliance with Tech Spec limit for minimum containment pressure maintained.
15.6.3 Steam Generator Tube No adverse effect on primary-to-Rupture secondary mass release. Compliance witn 10CFR 100.11 limits maintained.
3.6.2 Blowdown Reactor Yessel No adverse effect on the LOCA
, and Loop Forces hydraulic forcing functions.
15.6.5 Post-LOCA Long term No itdverse effect on the post-Core Cooling LOC), sump boron concentration.
Compliance with 10CFR 50.46b(5) maintained.
6.3.2.5.4 Hot Leg Switchover to No adverse effect on the post-Prevent Potential Boron LOCA hot leg switchover time.
Precipitation.
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