ML20044B154

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Responds to NRC 900612 Ltr Re Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Eop Step Deviation Documents to Be Upgraded,Adding More Justification & Temporary Change Issued to Correct EOP Deficiencies
ML20044B154
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 07/12/1990
From: Hairston W
GEORGIA POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
ELV-01879, ELV-1879, NUDOCS 9007170444
Download: ML20044B154 (5)


Text

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M G90fD's Power Comp;ny . , p", f s 333 Pedmont Avenue ... ' < i X '<

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Post Offee Box 1255 '

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                                                               - leiephone 205 868 SSB1 -                                                                                                           !

Q: - . L ' July 12, 1990 l'e soutten tkctnc systern

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                                                               ' W. G. Heireton, lil : .

Senior Vce President - i 1 Nuclear Operations , ELV-01879: n,, . . 474 ,, I( - t +r L* e, +

                    .                                   < Docket Nos.: 50-424                                                                                                   '

p 50-425 '

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LU.S. Nuclear Regulatory Commission. k .Wl ATTN: Document Control: Desk-a ?.i  : Washington,=D.C. ~ 20555.' l Gentlemen:c A ' V0GTLE ELECTRIC GENERATING PLANT. REPLY T0' INSPECTION REPORT

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          .. ,                                    ' qAs requested inINRC' letter. dated June l2, 1990, Georgia Power Company.(GPC)'

M submits the enclosed information:in response to the findings identified-in Inspection Report 50-424/90-08 and 50-425/90-08 which concerns the inspection

    &                                                      conducted .by Mr. L.' Lawyer, Mr. R. F. Aiello, Mr. ~ R.. Baldwin, Mr. :R. Schin,:and
 -                                                      ' Mr.- R. DL1Starkey of) the NRC: from May 7 1.8, 1990. In the enclosure,;

Ltranscription of,the findings: precede GPC's responses. :1:

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                                                         ' Please contact. this ~ office if you have any questions.                                                                           . 3 L

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                             ,                    .                                                                                 _ Si ncerely, .

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                                                                                                                                      . G. Hairston, Ill:                                           >
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Enclosure:

Findings 50-424;-425/90-08-01 through 11

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                                                                       =Georoia Power Comnany
                                                                           .Mr. C. K,LMcCoy-
Mr. G. Bockhold, Jr.

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                        ,                                                  :Mr.-R.-M. Odom
                                                                           'Mr. P. D. Rushton NORMS                                                                                                                 1

, V U.S. Nuclear Reaulatory Commission'

                                                                           .Mr. S.LD. Ebneter, Regional Administrator M'                                                     .Mr. T. A.-Reed, Licensing Project Manager, NRR M              >

Mr. B. R. Bonser, Senior. Resident Inspector, Vogtle a:q q , M 5

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ENCLOSURE' o V0G1LE ELECTRIC GENERATING PLANT - UNITS 1 & 2

                      ,                     RESPONSE TO NRC INSPECTION REPORT 50-424/90-08 AND 50-425/90                ;

IFI 424. 425/90-08 "EOP ES-3.2 missing:with no,10 CFR 50.59 ' safety evaluation,' paragraph.2" r 3

                                  ,Resnonse to IFl 424. 425/90-08-01:    Westinghouse has performed a review and            ;

advised that since the VEGP plant blowdown-(p system does not discharge to a storage-i tank or the liquid. waste processing system H

                                                                        'but.rather to eitherLthe waste water            sl retention basin which'is open to'the s                                                                      atmosphere or to-the condenser which is             3 the same discharge path as the steaming J

o method, the use of blowdown would not  ;

  • result in decreasing releases below-that '

which would be' expected by cooling-down using the' steaming method.- Thus a VEGP' specific procedure equivalent to-the ', Revision.1 ERG ES-3.2,' Post-SGTR Cooldown ~ Using Blowdown, would not ' accomplish the  ! original intention of that particular generic guideline which is.to minimize releases.  !

                                                                                                                          )'

The VEGP emergency operating procedures Pr (E0Ps) do'contain procedures based on the 1 ERG ES-3.1,. Post-SGTR Cooldown Using' . Backfill and ES-3.3, Post-SGTR Cooldown :i Using Steam Dump. The ES-3.1 procedure. ~j which is-based.on the guideline 1 provides- -J lL the operators.with: adequate. instructions j to. recover from a steam generator tube 1 , , rupture event.. This satisfies the 1 original:NRC concern-for~having a i procedure-to eliminate or minimize

                                                                                                                          ~

releases following' recovery' from a steam g generator tube rupture accident.. An' equivalent to the ERG,ES-3.2 guideline is j not necessary and therefore, no 10 CFR; R 50.59 safety evaluation is required.

                                                                                                                       -{
                                  -lFI 424.'425/90-08-02:
                "                                                         "EOP step deviation document deficiencies, '    )

paragraph 3"  : l_ Resnonse--to IFl 424. 425/90-08-02: .EOP step deviation documents will be ',.*. upgraded adding more justification where required.

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o. . ENCLOSURE (CONTINUED) y V0GTLE ELECTRIC GENERATING PLANT - UNITS 1 & 2 RESPONSE TO NRC INSPECTION REPORT 50-424/90-08 AND 50-425/90-08' 2 )

Appendix-B of this report will be. reviewed l for indications where operator confusion 4 or. misunderstanding could exist and-m , procedures will revised as required._ g Licensed operators will receive training

, on appropriate._ changes. ,

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 +'                                                                                          The above actions _ will be completed.by                 :l J.iy 1, 1991.,                                               '

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                                                  'JFI 424'. 425/90-08-03i                   "EOP technical deficiencies, paragraph 3"'

n Response to'Ifl 424.-425/90-08-03: The specific E0P technical deficiencies -

                                                                                           listed'in paragraph 3 have been: corrected                E!
 '.                                                                                          by issuance of a temporary change to                        )

procedures (TCP). Appendix B'will be " 1

                                                                                            .further reviewed and appropriate procedure                   !

changes will be made by July 1,1991. -

                                                    ~ IFl 424. 425/90-08-04:-                "EOP nomenclature differs from component
   ' A:                   4 labeling, paragrap.h 4

Response to IFI 424.~425/90-08-04: Appendix D will be r eviewed ~ and evaluated for nomenclature deviations and-procedures ij will bel corrected as required .byJJuly 1, i j 1991. 1 j JF1 424. 425/90-08-05: " Lack of detail in E0P's,- paragraph 4"

                                                                                                                                                      ~l' Resoonse to IFl 424. 425/90-08-05:       The examples listed in IFI 424, .                   ..

425/90-08-05 and the discrepancies noted in Appendix B will be evaluated and- :1 e procedures will be revised as required by ;j

                                                                                            ' July 1, 1991.

J: IFl 424. 425/90-08-06: "The S/G blowdown radiation monitor alarm a was set high, paragraph 4" , L , li' E-1-2 r  : I l' ' i, iI ) L i 6_. ______a_ - - - - - -

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              ,                                                             . ENCLOSURE (CONTINUED).

m . V0GTLE ELECTRIC GENERATING PLANT - UNITS 1 & 2 1 RESPONSE TO NRC INSPECTION REPORT 50-424/90-08 AND 50-425/90-08 4 y j Response to IF1 424. 425/90-08-06: The alarm-setpoint of the Steam Generator- d Blowdown Process Radiation Monitor, j' RE-0019, 'is being evaluated to determine the appropriate'setpoint to provide early a warning to-the operators of a steam ;j generator tube leak. This evaluation will 'H

      ,                                                                                  be completed and the appropriate procedure     1 4

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                                           ,                                            will be changed by August 31,-.1990.-

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                                       .IFI 424; 425/90-08-07::                          "EOP verification and validation              1 deficiencies, paragraph 4"                         ;
q Response to IFI 424. 425/90-08-07: The following revisions will be made to.
  • the E0P Writers. Guide: ,

o add action verbs and abbreviations! / o upgrade criteria for level of : detail.. I Also.the E0P Writers Guide will be-' - 1 evaluated and appropriate actions will' be

         ,                                                                               taken for the following. -                    g!

o more detailed verification checklist m o include E0P rules of usage a L o additional guidance to' ensure  : consistency o -addition of an index to make it more i user friendly-  : y 1 G The administrative procedures controlling: ,

                                                                                        .the-verification and validation of the          '

E0Ps will be evaluated and revised as required. The above actions will be completed by' c December 1, 1990. L'

i. , ,

IFI 424.'425/90-08-08: "EOP technical and human factors comments,

  • paric,' ph 4 and Appendix B"
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Response'to--IFI 424. 425/90-08-08: The E0P technical and human factor > l

             >                                                                           comments noted in Appendix ~B will be         j h

evaluated and the procedures willLbe revised as required by July'1,'1991. jl E-1-3 ,

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ENCLOSURE (CONTINUED) .

                                                           .V0GTLE ELECTRIC GENERATING PLANT - UNITS 1 & 2-RESPONSE TO NRC INSPECTION REPORT 50-424/90-08 AND 50-425/90-08 m                - IF1 424. 4'i5/90-08-09:                              "EOP Writers Guide comments, paragraph.4 and Appendix C" Resoonse to IFl 424. 425/90-08-09:                    The E0P Writers Guide comments in' Appendix C will be evaluated and procedures will be revised as required by July 1, 1991.

IFI 424, 42'/90-08-10: 5 "EOP nomenclature versus component labeling observations, paragraph 4 and Appendix D" Response to IFl 424. 425/90-08-10: The E0P nomenclature versus component labeling observations in Appendix D will be evaluated and procedures will be revised as required by July 1, 1991. _ IFl 424.-425/90-08-11: " Lack of E0P Users' Guide, paragraph 7" Response'to IFI 424. 425/90-08-11: An "E0P Users Guide" will be developed and-the lesson plans will be revised to

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include training on the E0P Users' Guide. This. guide will be used as a training handout to the lesson material. Improver .nts will be made in the lesson plans used in Licensed Operator training

on E0Ps.to correct the following deficiencies:'

o rules regarding entry. conditions o rules regarding action verbs including continuous action steps o . rules regarding cautions and notes o explanation of decision or logic

  > -                                                                                           structures included in major EOPs o use of response not obtained (RN0) column inclu' ding how/when to-exit The above actions will be completed by July 1,1991.

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