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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20084K4981976-10-0505 October 1976 Updates AOs 50-265/74-3,50-265/74-13,50-265/74-16 & 50-265/74-19 Re low-low Reactor Water Level Switch LIS-2-263-728 Failure.Surveillance Interval Changed to Monthly.Switch Installation Delayed Pending Analog Trip Sys ML20084S2291975-12-19019 December 1975 Supplementary Ao:Four Temp Switches Were Found to Trip at Values Exceeding Tech Specs Limits.Caused by Sensors Placed Too Closely to HPCI Turbine & Steam Piping.Different Temp Sensor Will Be Installed ML20084S5561975-11-19019 November 1975 Preliminary Ao:On 751109,traversing Incore Probe (TIP) Ball Valve 2 Failed to Close.Manual Attempts to Close Valve Failed.No Cause Stated.Addl Info Will Be Submitted in AO 50-265/75-45 ML20084S5851975-11-17017 November 1975 AO 50-265/75-44:on 751107,RCIC Turbine Tripped.Caused by Failure of Hydraulic Fluid servo-valve Actuator.Actuator Replaced & Overspeed Trip Mechanism Repaired ML20084S5731975-11-10010 November 1975 Preliminary Ao:On 751107,reactor Core Isolation Cooling (RCIC) Sys Turbine Tripped.Caused by Failure of Hydraulic Fluid servo-valve actuator.Servo-valve Actuator Will Be Replaced.Addl Info Will Be Submitted in AO 50-265/75-44 ML20084S5931975-10-30030 October 1975 Ao:On 751029,RHR Sys 2 Supply from Emergency Diesel & Core Spray Sys 2 Bus/Logic Power Failure Alarms Received.Caused by Switch 12 in Off Position.Switch Returned to on Position. Addl Info Will Be Submitted in AO 50-265/75-43 ML20084S6021975-10-28028 October 1975 AO 50-265/75-42:on 751018,differential Pressure Across B Train of Standby Gas Treatment Sys Exceeded Tech Spec Limit. Caused by Fouling of High Efficiency Prefilter.Filter Changed & Tested Satisfactorily ML20084S6191975-10-27027 October 1975 AO 50-265/75-41:on 751018,while Performing Monthly Diesel Generator Surveillance Test,Diesel Generator Reactive Power Meter in Control Room Pegged Full Scale.Megawatt Output Load Erratic.Operator Tripped Diesel.Caused by Equipment Failure ML20084S7771975-10-24024 October 1975 AO 50-265/75-38:on 751014,weld Exams Indicated Crack on B Loop of Rx Recirculation Discharge Bypass Line.Caused by Intergranular Stress Assisted Corrosion.Both Bypass Lines Will Be Removed ML20084S6471975-10-24024 October 1975 AO 50-265/75-40:on 751016,while Performing Routine Surveillance,Three High Drywell Pressure Scram Switches Found to Exceed Tech Spec Limit.Apparently Caused by Instrument Drift.Pressure Switches Recalibr & Tested ML20084S6741975-10-24024 October 1975 AO 50-265/75-39:on 751016,one Bergen-Patterson & Two Grinnell Hydraulic Snubbers Found W/Empty Oil Reservoirs. Apparently Caused by Equipment Failure.Snubbers Will Be Repaired or Replaced ML20084S6121975-10-20020 October 1975 Telecopy AO 50-265/75-42:on 751018,differential Pressure Across B Train Particulate Filters of Standby Gas Treatment Sys Exceeded Tech Specs.Caused by Smoke from Small Fire Created by Onsite Welders.Work Request Issued ML20084S2071975-10-20020 October 1975 Telecopy Ao:On 751020,radwaste Discharge Batch 3709 Discharged at Rate Which Exceeded Tech Spec Limit.Further Info to Be Provided in AO 50-254/75-22 ML20084S6291975-10-18018 October 1975 Telecopy AO 50-265/75-41:on 751017,during Monthly Surveillance Testing of Diesel Generator,Electrical Flash Burned Out Diode Rectifier Array of Generator Exicitation Circuitry.Output Breaker Tripped.Generator Inoperable ML20084S6561975-10-17017 October 1975 Telecopy AO 50-265/75-40:on 751016,during Routine Monthly Surveillance,Three High Drywell Pressure Switches Found to Exceed Tech Spec Limit.Cause Not Stated.Instruments Recalibr & Tested Satisfactorily ML20084S6831975-10-17017 October 1975 Telecopy AO 50-265/75-39:on 751016,two Grinnell & One Bergen-Patterson Hydraulic Snubbers Found Defective.Cause Not Stated.Work Request Issued for Repair ML20084S7821975-10-17017 October 1975 AO 50-265/75-37:on 751007,minor Leakage from B Feedwater Flush Line Observed.Caused by Equipment Failure.Flush Line Being Repaired ML20084S2181975-10-15015 October 1975 Telecopy Ao:On 751014,two High Drywell Pressure Scram Switches Found in Isolated Condition.Further Info to Be Provided in AO 50-254/75-21 ML20084S7681975-10-14014 October 1975 Telecopy Ao:On 751014,crack Indication Confirmed on B Loop in heat-affected Zone on Pipe Side of pipe-to-weldolet Weld. Repair Plans Incomplete.Addl Info Will Be Submitted in AO 50-265/75-38 ML20084S7851975-10-0707 October 1975 Telecopy Ao:On 751007,pipe Crack Found on Feedwater Flush Line 2-3206B-4-C at Main Feedwater Line 2-3204B-18-C.Minor Leakage Did Not Affect Reactor Inventory.Repairs Initiated. Addl Info Will Be Submitted in AO 50-265/75-37 ML20084S0391975-08-31031 August 1975 Telecopy Ao:On 750830,while Performing Monthly RCIC Operability Surveillance Test RCIC Would Not Reach Normal Conditions.Possibly Caused by Overspeed Mechanism.Required Testing of HPCI Sys Initiated ML20084R9871975-08-31031 August 1975 Telecopy of AO 50-265/75-36:on 750831,during Shutdown, Instability Was Experienced on Feedwater Control Sys Which Caused 3/4 Inch Drain Lines to Sever from Low Flow Feedwater Regulating Valve.No Radioactive Matl Released ML20084S0041975-08-31031 August 1975 Telecopy Ao:On 750830,while Testing Operability of HPCI Sys, Auxiliary Oil Pump Kept Tripping & HPCI Turbine Failed to Start.Orderly Shutdown Was Initiated.Further Info to Be Provided in AO 50-265/75-35 ML20084S0651975-08-25025 August 1975 Telecopy Ao:On 750825,oil Separator Overflowed Into Spray Canal Releasing Contaminated Water.Caused by Rainfall. Remaining Water in Oil Separator Being Discharged as Controlled Batch Release ML20084S0991975-08-25025 August 1975 Telecopy Ao:On 750824 Grinnel Snubber Had Empty Fluid Reservoir & Bergen-Paterson Snubber Had Leaking Accumulator. Replacement Parts Installed Prior to Reactor Startup on 750825.Further Info to Be Provided in AO 50-265/75-32 ML20084S1831975-08-18018 August 1975 Telecopy Ao:On 750817,following Maint Outage,Reducer of Low Flow Feedwater Regulating Valve 2-643 Severed Due to Vibration.Unit Manually Scrammed & Reactor Level Maintained W/Rcic Sys ML20084S2471975-08-15015 August 1975 AO 50-254/74-19:on 750805,reactor High Pressure Scram Switch 1-263-55A Was Isolated.Caused by Switch Left Isolated After Completion of Previous Month Testing.Establishment of Administrative Control Over Valves Initiated ML20084S2231975-08-13013 August 1975 Telecopy Ao:On 750812,ECCS Low Pressure Permissive Sensor PS-2-263-52A Discovered in Isolated condition.PS-2-263-52A Put Into Svc & All Switches Satisfactorily Functionally Tested.Further Info to Be Provided in AO 50-265/75-30 ML20084S2221975-08-11011 August 1975 Telecopy Ao:On 750809,standby Liquid Control Pump 1A Produced Flow Rate Below Tech Spec Limit.Caused by Premature Lifting of Relief Valve RV-1-1105A.Relief Valve Reset. Further Info to Be Provided in AO 50-254/75-20 ML20084S2371975-08-0808 August 1975 AO 50-265/75-28:on 750729,RHR Svc Water Pump 2A Fell Below Required Flow Level & Pump Pressure Limit.Caused by Accumulation of Debris Lodged in Pump Suction & Impeller. Debris Was Removed ML20084S2261975-08-0808 August 1975 AO 50-265/75-27:on 750729,during HPCI Monthly Surveillance Operation Only Able to Attain Pump Flow Below Tech Spec Limit.Caused by Improper Pinning of Pilot Valve Lever Arm. Lever Arm Adjusted ML20084S2541975-08-0505 August 1975 Telecopy Ao:On 750805,reactor High Pressure Scram Switch PS-1-263-55A Was Still Valved Out from Previous Month Surveillance.Switch Was Calibr & Valved in Svc.Further Info to Be Provided in AO 50-254/75-19 ML20084S2591975-08-0404 August 1975 AO 50-265/75-26:on 750725,oxygen Level of Unit 2 Suppression Chamber Exceeded Tech Spec Limit.Caused by Insufficient Nitrogen Available to Inert Primary Containment Due to Leaking Flange.Gasket in Nitrogen Line Replaced ML20084S3311975-08-0101 August 1975 AO 50-254/75-18:on 750724,pressure Switch PS-1-1622B Tripped at Value Exceeding Tech Spec.Caused by Instrument Drift.Pressure Switch Recalibr ML20084S3751975-07-31031 July 1975 AO 50-254/75-17:on 750721,traversing Incore Probe Machine Three Ball Valve Failed to Close When Detector Was Withdrawn to in-shield Position.Caused by Failure of Spring to Close Ball Valve Completely.New Valve Installed ML20084S2321975-07-31031 July 1975 Telecopy Ao:On 750731,4 of 16 HPCI Area High Temp Switches Tripped at Values in Excess of Tech Spec Limits.Switches Calibr.Further Info to Be Provided in AO 50-265/75-29 ML20084S3181975-07-31031 July 1975 AO 50-265/75-25:on 750721,two Hydraulic Snubbers Found to Have Empty Oil Reservoirs.Caused by Several Oil Leaks for One Snubber.Failure of Second Snubber Unknown.One Snubber Fitting Tightened & Other Snubber Replaced ML20084S2421975-07-30030 July 1975 Telecopy Ao:On 750729,RHR Sys Svc Water Pump 2A Failed to Meet Tech Specs Required Flow Rate.Work Request 2794-75 Immediately Issued for Investigation & Repair.Further Info to Be Provded in AO 50-265/75-28 ML20084S2461975-07-29029 July 1975 Telecopy Ao:On 750729,HPCI Sys Could Not Obtain Tech Spec Required Flow Rate.Cause Unknown.Eccs Testing Begun as Investigation.Further Info to Be Provided in AO 50-265/75-27 ML20084S6641975-07-29029 July 1975 AO 50-265/75-24:on 750720,crack Found on Reactor Feedwater Sys Flushing Line 2-3206B-4-C.Caused by Stress Point Due to Improper Blending of Fillet Weld.New Section of Pipe Welded ML20084S3361975-07-28028 July 1975 Telecopy Ao:On 750724,pressure Switch 1-1622B Found to Trip at Value Exceeding Tech Specs Limit.Switch Was Immediately Recalibr.Further Info to Be Provided in AO 50-254/75-18 ML20084S2641975-07-25025 July 1975 Telecopy Ao:On 750725,during Completion of Inerting,Primary Containment Oxygen Concentration Was Not within Tech Spec Limits.Further Info to Be Provided in AO 50-265/75-26 ML20084S6931975-07-25025 July 1975 AO 50-265/75-23:on 750718,high Drywell Pressure Switch 2-1001-89B Failed to Operate.Caused by Dirt & Scale Plugging Pressure Pulsation Damper.Damper Cleaned ML20084S3901975-07-25025 July 1975 AO 50-254/75-16:on 750717,unsampled Laundry Water Added to Floor Drain Sample Tank River.Caused by Operator Error. Radwaste Foreman Must Verify Valve Checkoff List Prior to Discharging to River ML20084S7131975-07-24024 July 1975 AO 50-265/75-22:on 750716,two of Four High Drywell Pressure Switches Exceeded Tech Specs Limit.Caused by Instrument drift.PS-2-1001-88B & C Calibr to Trip at 1.90 Psi ML20084S6261975-07-22022 July 1975 Telecopy Ao:On 750721,traversing Incore Probe (TIP) 3 Ball Valve Failed to Close.Shift Foreman Went to TIP Cubicle & Tapped Valve,Causing Valve to Close.Further Info to Be Provided in AO 50-254/75-17 ML20084S3261975-07-22022 July 1975 Telecopy Ao:On 750721,one Grinnell & One Bergen-Paterson Snubber Found Defective.Work Request Issued for Repair. Further Info to Be Provided in AO 50-265/75-25 ML20084S6791975-07-21021 July 1975 Telecopy Ao:On 750720,water Discovered in MSIV Room.Caused by Crack on Feedwater Flush Line B.Preparations Currently Being Made for Repair of Cracked Line ML20084S6161975-07-18018 July 1975 Telecopy Ao:Laundry Drain Sample Tank Level Dropped & Floor Drain Sample Tank a Level Rose.Caused by Not Verifying Closing of Laundry Tank Discharge Valve.Discharge Immediately Stopped ML20084S6981975-07-18018 July 1975 Telecopy Ao:On 750718,pressure Switch 2-1001-893 Failed to Operate at Any Pressure.Work Request 2640-75 Initiated to Investigate & Correct Problem 1976-10-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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- . Comm :lth Edison e Quid-Cit uclear Power Station M Post Offic 216 g) op V
Cordova,!!!inois 61242 Telephone 309/654-2241 g C lI FAP-72-146 g f?h/f[ll'* L O s gT Q
July 24, 1972 7 Qq,8fg g 7 9-Ahh'N iY Mr. J. F. O' Leary 4 /. !b7 '
Director, Directorate of Licensing .
U. S. Atomic Energy Commission 4IM Washington, D. C. 20545 50-265
Dear Mr. O' Leary:
Ref: Quad-Cities Nuclear Power ~ Station Unit 2-DPR-30 Appendix A Sections 6.6.A.3 and 6.6.B.3 The purpose of thi,s letter is to inform you of the details regarding the fire.in two electrical cable trays in the Reactor Building at Quad-Cities Station Unit 2. This incident occurred on' July 16, 1972, at 1:30 a.m.
This letter was prepared by Messrs. B. H. Temple, N. J.
Kalvianakis, and W. C. Lui, members of a special committee appointed by Messrs. H. K. Hoyt (Superintendent of Generating Station - Nuclear) and F. A. Palmer (Superintendent, Quad-Cities Nuclear Power Station) to investigate the incident.
Description of Incident During startup testing on Unit 2 at. Quad-Cities Nuclear Power Station with the reactor operating at 80% thermal power, Reactor Water Recirculation Motor-Generator Set 2B tripped and the indicating lights for the following equipment were initially observed to be out:
Reactor Water Recirculation Suction Valve MO-2-202-4B Reactor Water Recirculation Discharge Valve MO-2-202-5B Reactor Water Recirculation Equilizer Bypass Valve MO 202-9B.
f>;/ Reactor Water Recirculation Discharge Bypass Valve MO 202-7B
.fh>;y_
Drywell Cooling Blower 2C, 2D, and 2E 4//
i
' Standby Liquid Control System
]
h2 Reactor thermal power dropped to 60% after the recirculation pump tripped. An operator was dispatched to investigate and attempt to reset the Reactor Water Recirculation System in preparation for restart of 2B Recirculation Motor-Generator Set t O '
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COPY SENT REGION
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Mr, 4. F . O' Le ary July 2 4, 19 72 while a second operator was dispatched to investigate the Standby Liquid Constrol System and replace the blown fuse.
It was discovered that none of theThe valves that had lost their voltage on their supply indicating lights could be reset.
- bus, Bus 28/29-5, was checked and found to be normal. One of the Station Operating Engineers was notified while a search for abnormal conditions in the station was in progress. At 3:30 a.m.
a 8 mall fire was discovered in the two electrical cable trays in the TIP (Traversing In-Core Probe) room in Unit 2. The fire appeared to have extinguished itself. No smoke was detected in the room when it was entered. fire Some remaining sparks were extinguished with a portable CO2 extinguisher.
Immediate Actions, When the source of'the trouble was discovered an orderly shut-down of the reactor was initiated. All The equipment affected by turbine-generator was the fire was taken out of service.
off the system at 5:37 a.m. and all rods were inserted by 9: 16 a.m.
Investigation An investigation was performed to determine the cause of the fire. Engineers from Commonwealth Edison's Station Electrical Engineering and Production Departments were on site to investigate and concurred with the corrective action recommended by General Electric. Investigation revealed the following:
- 1. Location The fire was located in the TIP room in the southwest quad-rant of the 595' elevation of the Reactor Building in cable pan sections 603T (top) and 603B (bottom) . The trays are 30" wide and 6" deeps The fire had confined itself to approx-imately 5 feet at the end of cable - tray sections 603T and 603B. The maj or burning was in the bottom cable ' tray , 603B.
The cable trays in this area are ladder type trays and run against the drywell at elevations 614'6" and 616' above the drywell penetrations which are at elevation 611'. The only cables affected were those going through penetration 100F.
. All of the electrical leads coming out of penetration 100F were led up into the bottom ladder tray and spliced onto the incoming cable after their jackets had been stripped back.
Nineteen of .the total of 24 damaged cables had been routed in the bottom cable tray. The remaining 5 cables had been-routed in the top cable tray and looped down through the ladder section for splicing to the . penetration leads in the lower ladder section directly above penetration 100F.
x s
o o .
Mr. J. F. O' Leary '
July 24, 1972
- 2. Location of Hottest Area of Fire The apparent hot spot of the fire was located approximately 3 feet from the end of the bottom pan and towards the front e edge of the pan. This was also the location of the majority of the conductor splices.
3 Area of Spread
~The fire had fairly well consumed all of~the insulation in the front half of the lower pan at the apparent fire center.
It had spread along the loosely stacked cables to the point where they all came together in a tight bundle (approximately 2 feet from.the fire center) to continue on along the pan.
The fire extinguished itself as soon as it reached this tightly packed bundle and at the top of the vertical run of -
the penetration leads where they dropped out of the ladder tray., One 2-conductor number 14 cable (25799) in the top j pan directly above the fire hot spot had its insulation burned off. Its conductors had burned through in two places as a result of electrical arcing on two of the rungs of the ladder section. Four reactor protection system cables were also routed through penetration 100F. As specified by design they-were in separate conduit and were completely unaffected by the i
l fire.
- 4. Cause of Fire Cable 22770, the 3 conductor 1/0 power feed for Drywell Cooling Blower 2D, was buried near the bottom of the apparent hottest
_ spot of the fire. After removal of the upper cables, it was observed that phase T3 (c) conductor was burned through at the end of the splice which had the penetration leads crimped into it. The cable was burned completely through with face pitting and fusion. This type of burn is typical of a high resistence joint failure. The 2 pieces of the conductor were completely separated and there was no apparent arcing to the other phases of the cables, to any of the surrounding wires, or the cable pan.
C Repair Procedure
- 1. The conductor bundles from the penetration were all opened and the individual conductors were cut back to good conductor and good insulation. This left approximately a three foot lead from the penetration.
- .. n - - , , . - .. . _ - _ _ _ _ _ - _ _ . _
. .5-0 O Mr. J . F . O ' Le ary July 2 4, 19 72
- 2. A new 12" x 12" wire tray was run from the original pan just inside the TIP room wall directly to the penetration.
A 45 elbow sloping down to the penetration was installed on the wire duct for the purpose of making the cable splices.
3 The cables in the bottom tray were rerouted into the new wire tray.
- 4. The cables in the upper pan were left there until they were rolled out for splicing.
5 The rerouted cables were then cut back to good conductor and good insulation and spliced to the penetration leads as per original procedures with the exception of the drywell cooling blower power feeds.
- 6. For the drywell ' cooling blower power feeds , the splices were accomplished as follows:
A. A standard 1/0 YS25 Burndy sleeve was crimped to the 1/0 cable with a Burndy MY29-3 indenting tool.
B. The seven #10 101 strand conductors from the pene-tration were inserted into the other end of the 1/0 connector sleeve.
C. Three solid #10 copper filler pins were then inserted into the connector sleeve with the #10 stranded con-ductors. This gave a total copper cross section of 102,800 circular mills verses 105,600 circular mills for 1/0 'c able. The connector was then indented using a MY29-3 indenting tool set on the 1/0 index. Several of the splices were made on a trial basis. They were then sectioned at the dents in the connector. The
= cross-section of"the 7 #10 101 strand conductors plus the 3 #10 filler pins were a homogeneous cross-section of copper. The #10 solid conductors were not visually identifiable in the cross-section. The entire splice was of very good quality.
- 7. The connectors were, then insulated with GE8380 tape and the splice completed with a Scotchcast 82-A2 splicing kit.
Corrective Action All remaining drywell cooling blower feeds for both Unit 1 and 2 were physically inspected for evidence of overheating at the splice.
i 7.?.
i -
.O O Mr . J . F. O ' Le ary July 24, 1972 1
No indications of over heating were discovered. Since the original splices were approximately 30,000 circular mills short on copper at the penetration end, all drywell cooling blower feeds will be respliced in the following sequence:
A. All feeds through penetration 100F in Unit 2 drywell.
B. All feeds through penetration 104B in Unit 2 drywell.
C. Unit #1 cables outside of the drywell as each drywell cooler can be taken out of service.
After completion of the cable repairs, tests were conducted to verify the correct operation of the affected system components.
All required tests were completed prior to startup. The unit was returned to service at 3:45 p.m. on July 22, 1972.
Conclusion ,
Investigation indicated that the fire originated from a bad splice in the C phase of the power feed for the 2D Drywell Cooler. Although there was little visible evidence of arcing, it is reasonable to assume that the initial arc from this cable contributed to the spread of the fire. It was apparent that the fire did not spread out of the main zone by radiation or conduction. All power cable protective devices functioned pro-perly and were instrumental in containing the spread of the fire.
Had the fire occurred in an area where both division I and II engineered safeguard system cables were present, the separation system used throughout the plant would have prevented spread of the fire from one division to the other. A complete list of cables damaged by the fire is attached.
Very truly yours ,
COMMONWEALTH EDISON COMPANY Quad-Cities 5 clear Power Station j$
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Superinte ent FAP/zm .
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.;.s O 9 l RE ACTOR WATER RECIRCULATION CABLE # EQUIPMENT NAME 22857 suction valve MO-2-202-4B Motor 22864 Discharge valve MO-2-202-5B Motor 22871 Discharge Bypass valve MO-2-202-7B Motor l 22883 Equilizer bypass valve MO-2-202-9B Motor 22859 Suction valve MO-2-202-4B Limit switches 22866 Discharge valve MO-2-202-5B Limit switches
~22 873 Discharge bypass valve MO-2-202-7B Limit switches 22885 Equilizer bypass valve MO-2-202-9B Limit switches 20592 Current Transformer at 2B pump motor 25779 _ Discharge valve MO-2-202-5B limit switches DRYWELL COOLING ,
22430 Blower 2C 22770 Blower 2D 22435 Blower 2E TIP (TRAVERSING IN-CORE PROBE) 25183 Channel #1 Indexing Mechanism 25185 Channel #2 Indexing Mechanism 25769 Channel #3 Indexing Mechanism 25771 Channel #4 Indexing Mechanism 25773 Channel #5 Indexing Mechanism STANDBY LIQUID CONTROL 26340 Shut-off valve 1101-1 position indication RESIDUAL HEAT REMOVAL 20687 Injection manual valve 1001-33B position indicationc 22573 Shutdown cooling isolation Valve 1001-50 limit switch.
PLANT EVACUATION 24240 Reactor Building S'iren - S-35 -
REACTOR VALVES AND EQUIPMENT 26336 Reactor head cooling drain valve _AO-2-220-47 26326 Reactor head seal instrument Shut-off valve A0-2-220-52 i- .
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