ML17347A386

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Special Rept:Fire Barrier Breached for Longer than 7 Days & Other Fire Protection Sys Impairments Noted.Caused by Extensive Alternate Shutdown Work Remaining to Be Completed. Plant Continues to Implement Compensatory Measures
ML17347A386
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/06/1987
From: Woody C
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-87-158, NUDOCS 8704130213
Download: ML17347A386 (11)


Text

REGULATORY ORMATION DISTRIBUTION SY (R IDS)

ACCESSION NBR: 8704130213 DOC. DATE,: 87/04/Ob NOTARIZED: NO DOCKET ¹

~" FACIL: 50-250 Turkey Point Plant> Unit 3i Florida Power and Ligh+ C 05000250 50-251, Turkey Point Planti Uni+ 4i Florida Power and Ligh+ C 05000251 AUTH. NAME AUTHOR AFFILIATION WOODYi C. O *Florida Power 5 Light Co.

RECIP. NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk )

SUBJECT:

Special rept: fire barrier breached for longer than 7 days 5 other fire protection sos impairments noted. Caused bg extensive alternate shutdown uork remaining to be completed Plant continues to implement compensatorg measures.

DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ENCL SI ZE:

TITLE: 50. 73 Licensee Event Report (LER)i Incident Rpt> etc..

NOTES:

RECIPIENT CO~I~8 RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 PD2-2 PD 1 1 Mc DONALD, D 1 1 INTERNAL: ACRS MI CHELSON 1 1 *CRS MOELLER 1 1 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TAPB 1 1 NRR/ADT 1 1 NRR/DEST/ADE 1 0 NRR/DEST/ADS 1 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 NRR/DEST/ ICSB i. 1

, NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 NRR/DEST/PSB 1 1 NRR/DEST/RSB 1 NRR/DEST/SQB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 NRR/DOEA/EAB 1 1 NRR/DREP/EPB 1 1 NRR/DREP/RAB 1 ILRB 1 NRR/PMAS/PTSB 1 1 02 1 RES SPEISi T 1 1 RQN2 FILE 01 1 EXTERNAL: EQSQ QROHiM 5 5 H ST LOBBY WARD LPDR 1 NRC PDR NSI C HARRIS, J 1 1 NSIC MAYSi Q TOTAL NUMBER OF COPIES REQUIRED: LTTR 41 ENCL 39

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3zrg.'PRIL 0('987 L I 58 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gent lemen:

Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-25 I Special Report - Breached Fire Barriers and Other Fire Protecton S stem Im airments In accordance with Technical Specification 6.9.3 the attached Special Report is provided for your information.

Should there be any questions on this information, please contact us.

Very truly yours, c'~.:-g C. O. Woody Group Vice President Nuc I ear Energy COW/SDF/gp Attachment cc: Dr. J. Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant g70qygQP ] 3 870406 PDR B

ADOCK 05000250 gjP SDF I /M4/I

SPECIAL REPORT APRIL 6, 1987 FIRE BARRIERS BREACHED FOR LONGER THAN SEVEN DAYS OTHER FIRE PROTECTION SYSTEM IMPAIRMENTS REQUIRING NRC NOTIFICATION

~Pnt ese:

Technical Specification (TS) 3.14.5.b requires the submission of a report to the NRC if a non-functional fire barrier penetration is not returned to functional status within 7 days. TS 3.14 states that certain other conditions also require NRC notification. In accordance with the above requirements, this special report is being generated in order to notify the NRC. This report will be updated on a 30 day basis until the Appendix R associated work is complete.

Event:

The plant has been and is continuing to implement numerous modifications, mainly in accordance with Appendix R Alternate Shutdown requirements.

The schedular exemptions for the Safe Shutdown modifications, which outlined the alternative compensatory measures to be taken when a barrier is breached, expired on September 30, 1986, and on October 1, 1986. Upon the expiration of the exemptions, the compensatory measures as described in Attachment 1 of our letter L-85-386 (dated October 11, 1985), are continuing to be in place until the Safe Shutdown modifications are complete. Breaches incurred during Alternate Shutdown modifications are governed by the Technical Specifications or the exemptions, as applicable. Impairments are also incurred as part of plant maintenance and during the implementation of plant modifications.

Cause and Corrective Actions:

The ma5or cause of the impairments is the Appendix R Alternate Shutdown work which remains to be completed. Due to the large volume of work being performed, the plant is reporting the impairments in this one report, rather than on a case-by-case basis. The impairments reported this month are either, open or closed at the present time, but were open in excess of the time period permitted without requiring NRC notification (see attached lists of impairments).

The plant continues to implement the compensatory measures as applicable.

0 1

ATTACHMENT FIRE PROTECTION SYSTEM IMPAIRMENTS CLOSED IN MARCH BUT WERE OPEN FOR LONGER THAN TECH SPEC LIMIT Breach or Impairment Open Closing Number Date Date 1015 Fire Detection Systems 02/23/87 03/15/87 1047 Fire Door 021-1 02/20/87 03/13/87 1051 Fire Doors 101-1 02/IO/87 03/08/87 87-0049 Fire Barriers No. 040E-EO I I 01/12/87 03/05/87 87-0077 Fire Barriers No. 019W-E060 01/26/87 03/17/87 87-0078 Fire Barries No. 019W-E059 01/26/87 03/05/87 87-0083 Fire Barriers No. 106N 02/05/87 03/14/87 87-0084 Fire Barriers No. 106N 01/29/87 03/14/87 87-0085 Fire Barriers No. 106N 02/02/87 03/14/87 87-0086 Fire Barriers No. 106N 02/04/87 03/14/87 87-0102 Structural Steel Fireproofing Member: W12X79 02/09/87 03/02/87 87-0105 Fire Barriers No. 055N 02/18/87 03/02/87 87-0106 Fire Barriers No. 055N 02/18/87 03/02/87 87-0107 Fire Barriers No. 055S-2 02/18/87 03/23/87 F)RE PROTECTION SYSTEM IMPAIRMENTS OPENED IN MARCH WHICH HAVE BEEN OPEN FOR LONGER THAN TECH SPEC LIMITS Breach or Impairment Open Number Descri tion Date 1052 Fire Detection Systems 03/13/87 1053 Thermo-Lag From 3B ICW PP 03/09/87 1057 Water Suppression Systems 03/17/87 1058 Alarm PT 27, 03/17/87 1061 Fire Water Supply System 03/26/87 1068 Fire Doors No. 070-3 03/23/87 SDF I /004/3

The following barriers were breached prior to March, l987, however they are being included in this report as they were not reported previously.

Breach or Impairment Open Closing Number Date Date I046 Structural Steel Co. 29.5 02/20/87 87-0056 Fire Barrier l06E-EOI7 OI/I3/87 02/I9/87 87-0068 Fire Barrier 070N-E024 OI/I9/87 OI/29/87 SOF I /004/4

April 6, 1987 DIG, IBUTION

~ Docket Fx..e w/o-encl,.

PAD2 Rdg. w/o encl.

D. Miller w/encl ..

D. McDonald w(encl..

DOCKET NO(S). 50-250pand 50-251 Mr. C. 0. Moody, Group Vice President'uclear Energy Department Florida Power and Light Company Post Officd Box 14000 Uuno Beach, Florida 33408

SUBJECT:

TURKEy POINT UNIT 3

,The following documents concerning our review of the subject facility are transmitted for your information.

Notice of Receipt of Application, dated Draft/Final Environmental Statement, dated Notice of Availability of 'Draft/Final Environmental Statement, dated Safety Evaluation Report, or Supplement No. dated Environmental Assessment and Finding of No Significant Impact, dated Q Notice of Consideration of Issuance of Facility Operating License or Amendment to Facility Operating License, dated Bi-Meekly Notice; Applications and Amendments to Operating Licenses Involving No Q Bgifi Exemption, dated II* d C id i .d d~f tl]

Construction Permit No. CPPR-Facility Operating License Order Extending Construction Completion Date, dated No., , Amendment No.

Amendment No.

dated dated Monthly Operating Report for transmitted by letter dated Annual/Semi-Annual Report-transmitted by letter dated Division of PMR Licensing-A Office of Nuclear Reactor Regulation

Enclosures:

As stated cc: See next page 0FF1CSP

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SURNAME)

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OAVE f> 4/ /87

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NRC FORM 318110/801 NRCM 0240 OFFICIAL RECORD COPY

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