IR 05000413/1988016

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Insp Repts 50-413/88-16 & 50-414/88-16 on 880418-22.No Violations or Deviations Noted.Major Areas Inspected:Review of Recently Completed post-refueling Startup Tests,Calibr of Nuclear Instruments & Core Power Distribution Monitoring
ML20153G463
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 05/02/1988
From: Burnett P, Jape F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20153G458 List:
References
50-413-88-16, 50-414-88-16, NUDOCS 8805110243
Download: ML20153G463 (9)


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Report Nos.: 50-413/88-16 and 50-414/88-16

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Licensee: Duke Power Company 422 South Church Street Charlotte, NC 28242 Docket Nos.: 50-413 and 50-414 License Nos.: NPF-35 and NPF-52 Facility Name: Catawba 1 and 2 Inspection Conducted: p1118-22,1988 Inspector: wmedv [J Y W T. BurlifR Date igned Approved by: . //Gk(. 6 2" F. Jape, Section Chief y/ Date Signed Engineering Branch Division of Reactor Safety SUMMARY Scope: This routine unannounced inspection addressed the areas of review of recently completed post refueling startup tests, calibration of nuclear instru-ments, core power distribution monitoring, and fcllowup of open item Results: No violations or deviations were identified.

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REPORT DETAILS 1. ' Persons Contacted '

Licensee Employees H. B. Barron, Operations Superintendent R. G. Blessing, Engineer, Reactor Group

  • S. W. Brown, Reactor Engineer
  • A. Cote', Licensing Specialist J. W. Cox, Training Manager S. L. Cox, Training Specialist
  • T. E. Crawford, Integrated Scheduling Superintendent C. L. Hartzell, Compliance Supervisor M. W. Hawes, Engineer, Reactor Group J. E. Burchfield, Engineer, Nuclear Engineering Services Other licensee personnel contacted included security force members, engineers and office personne Other Organization R. L. Wolfgang, Westinghouse NRC tiesident Inspectors
  • P. K. VanDoorn, Senior Resident Inspector
  • S. Lesser, Resident Inspector
  • Attended exit interview Exit Interview The inspection scope and findings were summarized on April 22, 1988, with those persons indicated in paragraph I above. The inspector described the areas inspected and discussed in detail the inspection find'igs. No dissenting comments were received from the license Proprietr's informa-tion was reviewed and discussed in the course of the inspecti n. but is not included in this repor . Licensee Action on Previous Enforcement Matters (0 pen) Violation 414/87-30-01: Use of incorrect values in the Z and S terms of Technical Specification equation 2.2-1 to determine the accept-ability of power range trip setpoints. In their response to the violation dated December 28, 1987, the licensee used correct and acceptable values

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of the Z and S terms, but their formulation of the R term used the percentage miscalibration value reduced by two percent RT They argued that a two percent error was already included in the Z term. The inspector stated that credit could not be taken for the error assigned to the power calorimetric calculation in the setpoint analysis; since that was based upon instrumental uncertainties and did not constitute an available safety margin. The licensee agreed to that restriction, but stated there was additional margin in the setpoint analysis that was appropriate to consider in the R term. They will provide an amended response to the violation by May 15, 198 (0 pen) Unresolved Item 414/86-30-01: Determine the need and establish the guidance for reverifying and documenting system status and test prerequi-sites for interrupted tests. A response to this issue is now scheduled for June 1, 1988. At the exit interview, licensee management agreed this item had remained open long enough, and appropriate policy would be issued by the stated dat . Unresolved Items No unresolved items were identifie . Unit 1 Post-Refueling Startup Tests (72700, 61702, 61705, 61708, 61710)

Initial criticality for Unit 1, Cycle 3 was achieved on December 29, 1987 in accordance with procedure PT/1/A/4150/19,1/M Approach to Criticalit Under this procedure, dilution of the NC system boron concentration was initiated at 277 gpm with all control and safety rods inserted while monitoring inverse multiplication by calculating and plotting the ICRR for every thousand gallons of dilution water. During dilution, the SRNI countrates doubled. The reduction in boron concentration was from 1831 to 1333 ppm (The target endpoint had been 1336 ppmB.) At that point, new baseline data for the inverse multiplication measurement calculations were obtained. Inverse multiplication was calculated and plotted periodically during rod withdrawa Good features of PT/1/A/1/4150/19 included turning off the spray flow to the VCT while in alternate dilute mode to prevent over dilution of that tank, and performing ten and three-observatior. Chi-Squared tests of the SRNIs periodically to assure their proper functionin Both SRNIs

"failed" the test at control bank C at 96 step Actually, the failure was probably the result of a non-constant source and an indicator of imminent criticalit Prior to pulling rods, OP/0/A/6100/06, Reactivity Balance, was perfonned and a critical position of 60 steps on control bank D was predicte The actual critical position was seven steps on control bank D. The re. activity difference in the positions was consistent with the difference between the predicted and measured AR0 C B determined later in the test progra . . = . - . _ -

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3 The balance of the startup testing program was performed under the guidance of PT/1/A/4150/21, Post Refueling Controlling Procedure for Criticality, Zero Power Physics, and Power Escalation Testing.

> Onscale overlap between the SRNIs and the IRNIs of more than one decade

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was confirme Two reactivity computers were used. One was designed and manufactured by Westinghouse and the other was an onsite fabrication based upon on IBM 9000 computer. For nominal reactivity insertions of 25 and 50 pcm, each computer in every case agreed within 4% of the value derived from period measurement and the inhour equatio The point of adding nuclear heat was determined by establishing a slow startup rate, 20,2DPM, and allowing flux to increase until heating was observed by an increase in average NC temperature accompanied by a change in the reactivity traces on the computers. The upper flux limit for zero s power physics tests was established one decade below the observed point

of adding heat. This testing limit was established to prevent doppler feedback effects from invalidating the precise reactivity measurements required for the isothermal temperature coefficient measurement, reference bank worth measurements and other zero power test The ARO C n was determined to be 1441.4 ppmB, which was in good agreement with the predicted value of 1411 i 50 ppmB. The boron endpoints for both .

4 AR0 and safety bank B inserted conditions were obtained using PT/1/A/

4150/1 Each endpoint was the average of four measurements, and each set showed good internal consistency. It was noted that the procedure has no provision for adjusting the results for differences between the actual and reference NC average temperatur PT/1/A/4150/12A, Isothermal Temperature Coefficient of Reactivity Measure-i ment, was performed at AR0. The resulting ITC and MTC were +1.33 and

+2.65 pcm/ F, respectively. The latter satisfied the Technical Specifica-tion 3.1.1.3 limit of 7 pcm/'F at powers less than 70% RTP. By perfonn-ance of PT/1/A/4150/20, Temporary Rod Withdrawal Limit Determination, the licensee confirmed that no withdrawal limits were necessary to satisfy the MTC specification at any power leve A good feature of PT/1/A/4150/12A was the requirement to have the tempera- .

ture changes exceed 4 F, which wa- satisfied. The procedure does allow

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control rod motion (step 6.4 and note after step 12.5) if it does not interfere with the interpretation of the test result PT/1/A/4150/11A, Control Rod Worth Measurement by Boron Dilution, was performed to determine the reactivity worth of the reference bank, in this case safety bank B, by boron dilution. That test used the reactivity computers to measure the reactivity added by periodic insertion of the

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4 1 bank during continuous dilution. The procedure requires a dilution rate of approximately 23 gpm to assure a reactivity insertion rate of less than 300 pcm/h Examination of the recorded reactivity traces indicated a maximum insertion rate of about 200 pcm/h Then by performance of PT/1/A/4150/11B, Control Rod Worth Measurement by Rod Swap, the worth of each other bank was determined by observing the critical position of safety bank 8 with that bank inserted. A correction was made to the remaining inserted worth of safety bank B to account for the presence of the test bank, which was not present when the reference bank worth was determined. All measured rod bank worths agreed with their predicted values within 15%. The total reactivity worths agreed within 3%, with the measured being higher than predicte No value of the differential baron worth was specifically derived from the endpoint measurements for comparison with the predicted value of -9.94 pcm/ppm However, a comparison of reference bank worth with that calculated from the measured change in gC and the predicted worth of the boron was in good agreemen Power escalation was begun on December 30, 1987, and 100% RTP was attained on January 6, 1988. Power distribution maps obtained at 30 and 50% RTP

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exhibited QPTRs in excess of 2%. By 80% RTP the tilts had reduced to less ,

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than 2% satisfying Technical Specification 3. Between 49 and 80% RTP, thirteen quarter core flux maps were obtained for use in the incore-excore nuclear instrument correlation, but only twelve were later used. PT/1/A/4600/05F, Post Refueling Incore and NIS Recal-ibration, was performed on January 3-4, 1988. Using the licensee's raw data, the inspector independently correlated full-power top and bottom chamber currents for N41 with the incore-measured axial offset. The calculations were performed using a least-squares spreadsheet and the microcomputer program SUPERCALC3 (release 2.1). The correlation coeffi-cients for the top and bottom chambers were 0.967 and 0.979 respectivel The licensee's corresponding values were 0.969 and, 6.983. Licensee values for other ch:mbers ranged from 0.969 too 0.986. To perform the analyses, chamber currents were first normalized to 100% RTP. Only four of the twelve sets of data were obtained at power in excess of ~0% RT The need for :onsiderable power normalization may account for the relatively poor fit of the data. A plot of the inspector's analysis is given in Attachment 2. The licensee stated the routine incycle periodic test to perform the incore-excore correlation was performed less than thirty days into the cycle to address their own concerns on the quality of fi Three days after reaching full power, NC flow as indicated by the elbow taps became marginal, and power was reduced to 97.5% RTP in accordance with Technical Specification Figure 3.2-3. Subsequently, a change in the specificatiun was approved by NRR to allow full power operation with flow as low as 387600 gp No violations or deviations were identifie * *

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5 Unit 2 Post-Refueling Startup Tests (72700, 61702, 61705, 61708, 61710)

Unit 2 startup test procedures performed between March 7 and March 30, 1988 were virtually identical to those used earlier in the Unit I startup and were performed by essentially the same personnel with some interchange in role The measured ARO MTC was 2.94 pcm/ F in acceptable agreement with the predicted value of 1.94 3 pcm/'F. The measured AR0 Cnwas 1349 ppmB, which was in good agreement with the predicted value of I370ppm The comparison between measured and predicted reference bank worths was equally as good at 1258 and 1279 pcm, respectively. The sum of the measured rod bank worths exceeded the predicted by four percen No power tilts were encountered during power escalation, and NC system flow exceeded the minimum requirement The incore-excore nuclear instrument correlation was based upon twelve quarter _ core flux maps obtained between 52 and 79% RTP. The correlation coefficients were fair at best, ranging from 0.974 to 0.98 Once power had stabilized at 97% RTP, the test was repeated using seven flux maps obtained at axial offsets ranging from +5.3 to -6.6% RTP. The correlation coefficients were much better, ranging from 0.992 to 0.999. The better fit is demonstrated in Attachment Qo violations or deviations were identifie . End of Life Moderator Temperature Coefficients (61708)

The measurement of the MTC within seven days of reducing NC Cn below 300 ppmB was reviewed for the last cycle for each unit. The pf'ocedures used were PT/1(2)/A/4150/12B, End of Life Moderature Temperature Coeffi-cient, which are essentially identica The basis of each test was to hold power constant while changing NC average temperature by first increasing and thei; decreasing Cg . No use is made of a reactivity computer, instead the boron change and calculated boron worth were used to measure reactivit The measured at-power MTCs were -24.6 and -16.8 pea /*F, respectively and satisfied Technical Specification 3.1.1. No violations or deviations were identifie Attachments:

1 List of Acronyms and Initialisms l First Incore-Excore Correlation Unit 1, Cycle 3 Second Incore-Excore Correlation Unit 2, Cycle 2

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Attachment 1 List of Acronyms and Initialisns 1/M --Inverse Multiplication AR0 - All Rods Out C - Boron Concentration in Reactor Coolant DhM - Decades Per Minute gpm - Gallons Per Minute ICRR - Inverse Count Rate Ratio IRNI - Intermediate Range Nuclear Instruments ITC - Isothermal Temperature Coefficient MTC - Moderator Temperature Coefficient NC - Nuclear (Reactor) Coulant (System)(Nonenclature Unique to this Licensee)

NRR - Office of Nuclear Reactor Regulation O Operating Procedure pcm - Percert M1111 rho (Unit of Reactivity)

- ppmB - Parts Per Million Boron -

PT - Periodic Test (Procedure)

QPTR - Quadrant Power Tilt Ratio RTP - Rated Thermal Power SRNI - Source Range Nuclear Instrument 4 VCT - Volume Control Tank

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