ML20128R095
ML20128R095 | |
Person / Time | |
---|---|
Site: | Catawba |
Issue date: | 10/07/1996 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20128Q953 | List: |
References | |
50-413-96-13, 50-414-96-13, NUDOCS 9610210290 | |
Download: ML20128R095 (31) | |
See also: IR 05000413/1996013
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U.S. NUCLEAR REGULATORY COMMISSION
- REGION II
1 Docket Nos: 50-413. 50-414
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- Report Nos.
- 50-413/96-13. 50-414/96-13
j Licensee: Duke Power Company l
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Facility: Catawba Nuclear Station. Units 1 and 2
! Location: 422 South Church Street
Charlotte. NC 28242
! Dates: July 28 - September 7. 1996
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Inspectors: R. J. Freudenberger. Senior Resident Inspector
a P. A. Balmain. Resident Inspector
J. L. Coley, Reactor Inspector. Region II
R. L. Franovich Resident Inspector
L. R. Moore. Reactor Ins)ector
S. B. Rudisail Project Engineer. Region II
- P. S. Tam. Project Manager. NRR
- H. L. Whitener. Reactor Inspector. Region II '
] M. N. Miller. Reactor Inspector Region II
f.
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Approved by: L. D. Wert. Acting Chief
- Reactor Projects Branch 1
4 Division of Reactor Projects
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Enclosure 2
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9610210290 961007 3
DR ADOCK 0500
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EXECUTIVE SUMMARY
, Catawba Nuclear Station. Units 1 & 2
NRC Inspection Report 50-413/96-13. 50-414/96-13
, This integrated inspection included aspects of licensee operations.
- maintenance, engineering. and plant support. The report covers a 6-week
period of resident ins]ection: in addition, it includes the results of
announced inspections ]y regional reactor safety and retctor projects
, inspectors and reviews by a licensing project manager. In addition, the
results of a maintenance inspection conducted by a regional reactor inspector
during the week of July 8. has been included in Sections M2.3 and M/.
Ooerations
, . Although a required 10 CFR 50.72 report was submitted late (Non-Cited
l Violation 50-414/96-13-01), communication conventions were consistently
utilized, a timely decision regarding the initiation of the shutdown was
made, and good command and control was exhibited during a forced Unit 2
shutdown. (Section 01.1)
. A procedure change to prewarm the Residual Heat Removal pump prior to
placing it in service resulted in the unanticipated binding of a manual
, isolation valve, which rendered the system inoperable (VIO 50-413.414/
96-13-02). (Section 01.2)
- . The licensee was proactive in determining the source of the water on the j
ground surface in the vicinity of Nuclear Service Water System piping. l
The delay of Unit 2 startup until the source was identified and repaired
demonstrated an appropriate focus on safe operation of the facility. ;
- (Section 01.3)
Maintenance
. The licensee's effort to determine root causes was thorough and adequate
to ensure appropriate classification of safety significant motor
failures. (Section M1.1)
. The decision to delay refueling until the 1A Residual Heat Removal Pump
could be returned to an operable status was considered to be indicative
of a conservative operational approach. The root cause evaluation of
the motor failure was of an appropriate scope. (Section M1.2)
. The actions to re] air damaged secondary contact blocks on the Unit 1
Reactor Trip Brea(ers (RTBs) and bypass RTBs were appropriate. Planned
corrective actions also were appropriate. (Section M1.3)
. The licensee was actively monitoring and evaluating equipment
reliability. Adverse trends were identified, and corrective actions
were initiated. Actions reviewed by the inspectors addressed the
concerns and were comprehensive in scope. (Section M2.1)
Enclosure 2
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Executive Summary 2
. The Maintenance self-assessment program was effective and well managed.
The program identified a high number of rework items which were the
result of poor work practices. (Sections M2.1 and M7.1)
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. An inadequate procedure caused unanticipated component actuations that l
interfered wit 1 the dilution flow for a liquid radioactive release. I
(Violation 50-413.414/96-13-02). (Section M3.1)
. The licensee identified a violation (non-cited) involving the
performance of Emergency Diesel Generator Head reassembly steps out of I
sequence (Non-Cited Violation 50-413/96-13-03). (Section M4.1) '
Enaineerina
. An example of a violation for inadequate design control was identified
in that Main Steam Isolation Valve (MSIV) solenoid valve nameplate
rating was less than the instrument air maximum pressure (Violation 50-
413.414/96-13-04). (Section El.2)
. Actions to determine the root cause of the B main feedwater pump trip
were timely and appropriate. Proposed corrective actions were adequate.
(Section E2.1)
. Several Unit 1 modifications were implemented during the outage to
resolve existing equipment problems and improve plant reliability. The
modifications demonstrated appropriate control of the design control
process at Catawba. The requirements of 50.59 were met for associated
safety evaluations that were reviewed. (Section E2.2)
. The erosion / corrosion program was effective in identifying main
feedwater pipe localized wall thinning. (Section E2.3)
. The 1995 revision of the Catawba UFSAR matched the provisions of 10 CFR
50.71 and was therefore in compliance with 10 CFR 50.71.(Section E3.1)
. Design input errors in Calculation 1223.04-00-0009 were not identified
by the licensee on two occasions: first during the independent review of
the calculation in November 1993, and again during the licensee's steam
supply station (SSS) pre-inspection self-assessment in June 1996
(Violation 50-413.414/96-13-04). (Section E4.1)
Plant Sucoort
. An unauthorized entry of an individual into the Radiation Control Area-
without appropriate dosimetry. training, or body burden analysis was
identified as a violation of Radiation Protection Directive No. II-1.
Radiation Area Access and Monitoring Devices (Violation 50-413,414/96-
13-06). Corrective actions for a previous occurrence were not effective
in preventing recurrence. (Section R1.1)
Enclosure 2
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Reoort Details
Summary of Plant Status
Unit 1 was in a refueling / steam generator replacement outage for the duration
of the inspection period.
Unit 2 was in a forced outage because of inoperability of both trains of the
Control Room Ventilation System between August 3 and 12. The unit operated at
or near 100% power throughout the remainder of the inspection period.
Review of UFSAR Commitments
A recent discovery of a licensee operating their facility in a manner contrary
to the Updated Final Safety Analysis Report (UFSAR) description signified the
need for a special focus review that compares plant practices, procedures,
and/or parameters to the UFSAR descriptions. While performing inspections
discussed in this report, the inspectors reviewed the applicable portions of
the UFSAR that related to the areas ins)ected. The inspectors verified that
the UFSAR wording was consistent with tie observed plant practices,
procedures, and/or parameters. No deficiencies were identified.
I. Operations
01 Conduct of Operations
01.1 Unit 2 Forced Shutdown
a. Insoection Scooe (71707)
On August 3.1996. Catawba Unit 2 entered Technical Specification 3.0.3
and was shut down when both trains of the Control Room Area Ventilation
system became inoperable. During the forced outage, the inspectors
observed control room activities, assessed equipment failures and
reviewed reporting requirements.
b. Observations and Findinas
Train B of the Control Room Area Ventilation system was out of service
for planned maintenance. The system's A Train pressurization fan motor
subsequently failed, and Technical Specifications (TS) required the unit
to shutdown /cooldown (see section M1.1 of this report). While the unit
was in Hot Shutdown (Mode 4) on August 4. a fan motor failure occurred ,
on Train A of the Auxiliary Building Ventilation System (see section
M1.1 of this report). This failure resulted in both trains of Auxiliary
Building Ventilation being inoperable because Train B was out of service
for )lanned filter testing. Subsequent problems encountered with
esta)lishing Residual Heat Removal flow on Train B (See section 01,2 of
this report) required the use of Train A of the Residual Heat Removal
system to take the unit to cold shutdown (Mode 5) at 12:58 p.m. on
August 4.
Enclosure 2
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The inspector observed control room activities during the forced
shutdown and noted that communication conventions were consistently
utilized. a timely decision regarding the initiation of the shutdown was
made, and good command and control was exhibited.
The licensee identified a missed 10 CFR 50.72 report regarding the
failure of the A Auxiliary Building Ventilation Filtered Exhaust Fan
Motor. Prior to the failure, the B train was removed from service for
filter testing and replacement. With both trains inoperable, a second
condition existed that required entry into TS 3.0.3. On-shift personnel l
considered re)orting of this second condition as having been
accomplished )y the previous report and did not make a second report
regarding this failure. This condition was later recognized as
reportable under 10 CFR 50.72(b)(2)(iii)(d) and a report was made. The ,
report did not meet its associated timeliness requirements. The
licensee initiated a Problem Investigation Process (PIP) Report for this i
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occurrence (PIP 0-C96-2058). Corrective actions included a " read and
sign" discussion of the occurrence for operations personnel and plans
for including performance and assessment of reportability determinations
in simulator training. This licensee-identified and corrected violation
is characterized as Non-Cited Violation 50-414/96-13-01: Failure to
Report Inoperability of Both Trains of Auxiliary Building Ventilation,
consistent with Section VII.B.1 of the NRC Enforcement Policy.
c. Conclusions
With the exce) tion of a late 10 CFR 50.72 report, operators perTarmed
well during tie forced shutdown in response to ventilation system
failures.
01.2 Residual Heat Removal Train B Inocerable Durina Unit 2 Forced Shutdown
a. Insoection Scooe (71707)
On August 4 during the forced shutdown when TS 3.0.3 was entered after
both trains of Control Room Ventilation were inoperable, control room
operators were attempting to place the B train of the Residual Heat
Removal (RHR) system in service. The 2B RHR heat exchanger inlet manual
isolation valve. 2ND-53, was closed by procedure and became wedged in
its seat. A stem to disc failure was incurred during attempts to open
the valve. As a result. B train of RHR was inoperable during the Unit 2
cooldown from Mode 4 to Mode 5. The inspector interviewed plant
personnel and reviewed procedures, system diagrams, and metallurgical
analysis report #2032. The inspector also reviewed the licensee's root
cause evaluation and associated recommendations.
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b. Observations and Findinas
i Operators attempted to place B train RHR in service'using
l OP/2/A/6200/04. Retype #13. Residual Heat Removal System. Enclosure 4.1.
Startup of the RHR System During Normal Plant Cooldown. A recent
! procedure change directed clerators to close valve 2ND-53 at step 2.6.29
and bypass flow around the leat exchanger. Flow was diverted through
the heat exchanger bypass line and into the letdown system so that the 1
2B residual heat removal pump and associated suction and discharge
piping could be slowly heated to within 50 F of reactor coolant system
temperature before the pump was placed in service. The procedure change
l was designed to prevent thermal deformation of the pum) casing and
subsequent casing leakage. The procedure introduced t1e potential for
thermally induced pressure locking of 2ND-53.
Step 2.6.46 of OP/2/A/6200/04 directed operators to open 2ND-53 to
establish flow through the heat exchanger and place B train RHR in
service. The valve could not be opened by normal use of a reach rod or
direct, unassisted manipulation of the handwheel. A valve wrench was
used to open the valve, and a stem to disc failure occurred but was not )
immediately recognized. As'a result, the B train of the residual heat i
removal system was inoperable during unit cooldown from Mode 4 to Mode 5 1
and remained inoperable from 10:00 a.m. on August 4. 1996, until 4:00
p.m. on August 7, 1996. The A train of RHR was placed in service so
that unit cooldown to Mode 5 could be achieved within the remaining time
allowed by TS.
Valve 2ND-53 is a manual double disc gate valve. and it is located near
(approximately 1.5 feet from) the heat exchanger bypass flowpath. The
licensee concluded that the most likely cause of the valve binding was
thermally induced pressure locking as RHR temperature increased.
The stem to disc failure occurred at a link that affixes the stem to the
disc. According to metallurgical analysis report #2032. Catawba Linkage
from 2ND-53, fracture of the 2ND-53 linkage was caused by a single
overstress event, most likely attributable to attempts by plant
personnel to free the stuck valve. No signs of pre-existing cracks or
other material problems that might have made the linkage susceptible to
premature failure were detected.
The inspector questioned the use of a valve wrench to open the valve and
determined that Operations Management Procedure 2-33 allows for the use
of a valve wrench if no more than normal force of a "large individual"
is applied. The inspector determined that the requirements of this
procedure were complied with.
, The inspector reviewed the change to OP/2/A/6200/04 for prewarming the
l pump before placing the system in service, including the 10 CFR Part
50.59 evaluation. The inspector concluded that the potential for
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pressure locking and thermal binding was evaluated during the 10 CFR
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Enclosure 2
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50.59 review process. However, the evaluation was narrow in scope
(limited to active valves) and the licensee concluded'that, since 2ND-
53 was a manual isolation valve. it would not be affected by these
phenomena.
The licensee did not recognize that 2ND-53 was broken until flow could
not be established through the heat exchanger, at which time the failure
of 2ND-53 was self-disclosing. Because the binding and subsequent
failure of valve 2ND-53 resulted in the inoperability of the B train of 1
RHR. only one train of RHR was operable during the Unit 2 forced
cooldown.
Incidentally, the inspector determined that the Unit 1 procedure for
prewarming the RHR pumps had been changed before the refueling / steam
generator replacement outage began. The change involved isolating the
letdown piping from the RHR system to prevent water hammer in the
letdown piping as RHR was placed in service and the RHR to letdown
piping was rapidly pressurized. The same procedure change had not been
made to Unit 2 procedures when the forced shutdown was initiated. The
inspector considered implementation of procedure changes that were not
unit specific on only one unit to be a poor practice. The licensee
revised operation department guidelines to require simultaneous
implementation of non-unit specific procedure changes in the future.
c. Conclusions
Procedure changes to OP/2/A/6200/04 were inadequate in that the
procedure established conditions which caused thermally induced pressure
locking of valve 2ND-53. The valve was damaged in attempts to open it,
thereby extending the time that the B-train of RHR was inoperable. This
issue is characterized as Example 1 of Violation 50-413.414/96-13-02:
Inadequate Procedures.
01.3 Nuclear Service Water System Pioe Leak in Yard
a. Insoection Scoce (40500 and 71707)
On August 8. licensee maintenance technicians identified water bubbling
up from the ground near the steam generator storage facility. The
licensee was aware that nuclear service water (RN) system piping was
buried in the general vicinity where the water was found and, concerned
that an RN pipe was leaking, excavated the piping. A hole was found on
the B train supply header, and a modification was implemented to repair
the 42-inch pipe. The inspector reviewed the modification package,
including the 10 CFR 50.59 evaluation, observed parts of the excavation.
attended a PORC meeting, and reviewed the compensacory actions that were
developed to ensure that, during the pipe repair, the seismic integrity
of the RN piping was maintained and tornado missile protection could be
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Enclosure 2
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reestablished within one hour of a tornado watch or warning
notification.
b. Observations and Findinas
l The leak emerged from an external pit initiated from corrosion. The pit
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was approximately two inches in diameter on the outer surface of the
pipe and roughly three-sixteenths of an inch in diameter on the inner
pipe surface. The hole was temporarily plugged. Minor modification
CNCE-8150 was developed to make 3ermanent code repairs to the defect and
other non-through wall pits in tie vicinity. The pits appeared to be
caused by localized damage to the protective coating while on the piping
during initial installation. While the source of the water was being
investigated and repaired. Unit 2 startup was delayed.
c. Conclusions
The inspector concluded that the licensee was proactive in determining
l the source of the water on the ground surface. Compensatory actions
i that were in effect during the pipe repair were appropriate. The delay
of Unit 2 startup until the source was identified and repaired
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demonstrated an appropriately conservative focus on safe operation of
the facility.
II. Maintenance
l M1 Conduct of Maintenance
M1.1 Follow-uo of Ventilation Motor Failures
a. Insoection Scooe (93702)
On August 3.1996. Unit 2 entered TS 3.0.3 due to both trains of the
l Control Room Ventilation system being inoperable. The B train of
Control Room Ventilation was inoperable due to Nuclear Service Water
system work in progress. The A train became inoperable when the filter
fan motor breaker trip)ed and would not reset. This resulted in both
l trains of ventilation 3eing inoperable; thereby requiring entry into TS
l 3.0.3. During the shutdown the auxiliary building ventilation exhaust
fan tripped on a ground fault. The inspector reviewed the failuru of
the ventilation system motors to determine if the failures were
l appropriately classified and adequate corrective actions completed or
l planned.
l b. Observations and Findinas
{ The inspector reviewed the failure of the Control Room Ventilation
System Fan Motor 1CRA-PFT-1. The failure of this motor was determined
- to be an electrical failure due to a ground fault on the T3 phase
winding. This failure was verified using a winding analysis test. The
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winding analysis test includes a winding resistance measurement. an
insulation resistance (megger) test, a Hi-pot test, a polarization index
test and a surge comparison test. The results of this test identified a
ground fault with the megger indicating failure at 400 volts and the
surge test. revealing a 92% mismatch between two of the three phases.
, Further analysis was performed by the motor manufacturer. Reliance
! Electric, which confirmed the licensee's results. This motor was
approximately 15 years old and had been in service since initial
i operation of the plant. A definitive root cause for the fault of the
motor was indeterminate, but age related failure was suspected. The
motor was replaced and the system returned to service prior to Unit !
- restart.
l Additionally, the inspector reviewed the failure of the Auxiliary
l Building Filtered Exhaust Fan Motor ABXF-2A Initial failure
l investigation revealed a phase to ground fault on all three phases.
This was determined by meggering. Bearing failure was suspected due to I
difficulty in rotation of the motor; however, after the motor was i
removed and taken to the shop for troubleshooting the cause of the i
rotation difficulty was determined to be melted copper from the damage
caused by the fault. The inspector observed this inspection by the
licensee and also reviewed the motor damage. The inspector concurred
with the licensee's assessment during this preliminary investigation. ,
The motor was subsequently shipped to a vendor troubleshooting and l
repair facility for further analysis.
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The inspector reviewed the licensee's root cause effort to determine -l
whether a common cause had initiated the failure of the two motors and
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possibly resulted in other motors being susceptible to failure. From
! this review the inspector determined that a common cause for these two
! motor failures had not been identified. The licensee's review for a
l common root cause was adequate to ensure that these two failures were
l random failures without a single initiating cause.
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c. Conclusions
! The inspector concluded that the licensee's effort to determine root
cause was thorough and adequate to enst ce appropriate classification of
the motor failures.
- M1.2 Followuo of Residual Heat Removal Motor Failure
a. Insoection Scot. (62703)
On August 31. the 1A Residual Heat Removal Pump tripped after
I approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of run time following installation. The ins)ector
! reviewed the operational impact and the root cause evaluation of t1e
failure.
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Enclosure 2
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b. Observations and Findinas
At the time of the failure. Unit 1 had no' fuel in the core and
preparations were underway to initiate refueling. Plant TS allow core
alterations with one operable Residual Heat Removal pump and the
refueling cavity filled. Based on questioning by o)erations personnel,
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the licensee chose to delay refueling until the 1A lesidual Heat- Removal
Pump could be returned to an operable status. The inspector considered
this decision to be reflective of a conservative operational approach.
Based on information provided by the licensee, the motor that failed had
been refurbished by Westinghouse in 1994. The refurbishment was l
primarily a mechanical refurbishment to correct an out of tolerance i
condition on the upper bearing housing and improve vibration of the j
motor. Electrical testing indicated that the motor was in good
condition. After storage in the contaminated warehouse on site at
Catawba, the motor was installed in July, 1996. Electrical testing
again indicated that the motor was in good condition at that time.
Shortly after functional testing, the motor failed while in service. '
Initial cause investigation during disassembly indicated the fault was
initiated by a turn-to-turn fault in the stator windings. The licensee
root cause analysis was not complete at the end of the report seriod. :
but poor storage conditions in the contaminated warehouse was seing
investigated as a possible cause.
c. Conclusions
The licensee's decision to delay refueling until the 1A Residual Heat
Removal Pump could be returned to an operable status was considered to
be reflective of a conservative operational approach. The cause
evaluation of the motor failure was of an appropriate scope.
M1.3 Reactor Trio Breaker Secondary Contact Blocks
a. Insoection Scoce (62703)
In June 1996, the licensee identified cracked secondary contact blocks
- on the reactor trip breakers (RTBs) and bypass RTBs at the McGuire and
Catawba Nuclear Stations. The issue is documented in NRC Ins)ection
Report 50-413.414/96-10. In this inspection report period, t1e
inspector reviewed work orders (W0s) to verify that all damaged
secondary contact blocks on the Unit 1 RTBs and bypass RTBs were
replaced with new blocks prior to unit restart from a refueling and
steam generator replacement outage. The inspector also reviewed the
procedure for handling RTBs and bypass RTBs. and reviewed the licensee's
root cause evaluation and proposed corrective actions.
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b. Observations and Findinas
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The inspector reviewed the task completion notes associated with W0s
96054700-01. 96010780-01. 96019781-01. and 96026725-01 and determined
- that the damaged RTB and bypass RTB secondary contact blocks were
l replaced with new blocks. The inspector also reviewed the root cause
l evaluation which indicated that mishandling was the most likely cause
i for the damage to the secondary contact blocks. Based on the facts
presented in the root cause, the inspector concluded that this root
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cause was the most likely. Proposed corrective actions include: (1)
revise the standard procedure for breaker maintenance during refueling l
outages. SI/0/A/2410/001. Westinghouse DS-416 Air Circuit Breakers l
Inspection and Maintenance, to include a torque limit for the secondary ;
contact block assembly mounting bolts: (2) to remove and inspect all l
secondary contact blocks on each breaker during each breaker PM: (3) add I
a caution statement to OP/0/A/6350/10. Operation of Station Breakers and l
Disconnects, to note the need for careful handling during breaker
movement to avoid damage to secondary contact blocks and other breakable
parts: and (4) provide two breaker hoists each dedicated to a unit.
versus the existing single shared hoist.
c. Conclusions
The inspector concluded that the licensee's actions to repair damaged
secondary contact blocks on the Unit 1 RTBs and bypass RTBs were
l appropriate. Planned corrective actions were also appropriate.
M1.4 Maintenance Observations
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a. Insoection Scooe (62700)
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l The inspectors observed and reviewed portions of various licensee
corrective and preventive maintenance activities to determine
implementation of administrative controls, plant procedures, work
instructions industry codes and standards. Technical Specifications and
regulatory requirceents. ;
The inspectors observed portions of the following work activities:
! * WO 96045006-01 Diesel Generator 1A: Pull 4 heads and pistons;
l measure and inspect liners and welds. Remove
j and replace 12 additional heads.
. WO 95053556-01 Component Cooling Water Pump 1A2 Corrective
Maintenance. ;
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b. Observations and Findinas
The inspectors observed that the licensee had implemented the pro mr
administrative controls in the performance of maintenance. For t1ose
- periods of maintenance observed
- cleanliness was maintained, tools were
properly calibrated, inventory control logs were maintained, exclusion
of foreign material was implemented, procedures were at the job and
followed, Quality Control personnel were closely following the work, and !
procedure sign off was performed by both the craft and Quality Control
personnel as steps were performed. Additionally, supervisory oversight
was evident and personnel performing the maintenance were knowledgeable i
in their assigned tasks. I
c. Conclusi ,
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The ins'.;ctors concluded that the licensee has developed and implemented l
adequate maintenance controls to assure reliability of equipment. j
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Eouioment Performance and Availability Monitorina
a. Insoection Scoce (62700) l
The inspectors reviewed plant records and procedures to evaluate the
licensee's activities to maintain equipment reliability. The licensee
monitors equipment performance and availability in several ways. Some
of these methods are: i
e Component Failure Analysis Reports (CFAR) using the Nuclear Plant
Reliability Data System (NPRDS) to compare Catawba performance
with industry averages for specific equipment.
- Failure Analysis Trending System (FATS) using the Work Management
System to obtain equipment maintenance history and maintenance
work order data for trending system / component performance.
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e Maintenance Assessments using maintenance rework items as a
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performance indicator to improve maintenance efficiency and
equipment reliability.
i e Self-Initiated Technical Audit (SITA) using a focused approach to
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highlight 3roblems in a specific area. In this case the Diesel
Generator Recovery Program.
( * Problem Investigation Process (PIP) Reports used to document
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identified plant problems, proposed corrective actions and problem
i resolutions.
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b. Observations and Findinos l
The inspectors reviewed portions of the above documents to evaluate the
l licensee's activities to monitor and maintain equipment reliability.
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The following was noted: l
- CFAR results reported July 1996 indicated that 24 Catawba
components were higher than the industry average. The licensee
reviews the failure history of each of these components for cause l
and corrective action.
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- The FATS quarterly report is the main method for establishing
i adverse equipment trends. In this report the equipment
performance was evaluated over the previous 18 months to detect
adverse trends and the previous 36 months to detect repeat
failures, In the first quarter of 1996, adverse trends were
I identified for pressure switches and battery chargers in the ;
electrical area and motors. HVAC chillers and diesel engines in 1
the mechanical area. The report provided a description of the i
problem problem significance, explanation of the trend,
corrective action. PIP to track corrective action. Modifications
if required, and the action plan. For instance, for the diesel
generator,19 specific actions were identified.
. Maintenance assessment of rework items was started in March 1995.
Assessment for 1995 has identified problems in several areas. Of
the 120 potential rework events assessed. 74 were confirmed as
rework events. Of the 74 events. 41 or 55% of the total were due
to )oor work practices. These included inadequate self-checking,
lacc of independent verification and skill based discrepancies.
l The assessment made detailed recommendations to improve these
! discrepancies and to focus management attention.
, The assessment also identified strengths in Steam Generator. HVAC.
l and Pipe Support maintenance where maintenance crews had
I recognized and corrected maintenance weaknesses.
The Problem Investigation Process was used to track corrective
actions.
l
- The Diesel Generator Recovery Program was initiated as a result of
l reliability and availability decrease in diesel performance. A
! SITA was performed to identify the problems and the recovery
l 3rogram developed to resolve the problems. Areas such as design
! 3 asis. Maintenance. Operation, and trending were addressed.
1
! . The inspector reviewed PIP 0-C96-0172. initiated for tracking the
i failure of Instrument Air Compressor D motor. The root cause was
! ioentified as a break down of insulation from loss of cooling due
,
to dirt and oil deposits. Thorough corrective action was taken.
Enclosure 2
__ _ . _ . . .__ __ _ ___. _ _ _ . _ - - . __ _ _ _ . -. . . . _
t
,
11
Actions included upgrading the insulation, check of insulation
every 18 months, internal inspection every 36 months, installation
]
of thermocouples and trending of temperature' data,
c. Conclusions ;
Based on review of portions of the above documents and discussions with
licensee personnel, the inspectors concluded that the licensee was
actively monitoring and evaluating equipment reliability. Adverse
trends were identified and corrective actions initiated. Those actions
reviewed by the inspectors addressed the concerns and were comprehensive
,
in scope.
3
M2.2 Safety-Related Carbon Filter Status
>
a. Insoection Scooe (61726)
"
The inspector reviewed the status of the Unit 1 and Unit 2 safety-
related carbon filters, including the Annulus. Auxiliary Building,
Control Room. Fuel Pool, and Containment Purge Ventilation Systems.
b. Observations and Findinas
On August 1, the 28 Auxiliary Building Ventilation carbon filter unit
failed a TS required bypass leakage surveillance test. After
troubleshooting for approximately three days the licensee re
carbon and surveillance testing was completed successfully. The placed the
'
inspector verified by reviewing methyl iodide penetration test results
that safety-related filters in both units met TS requirements. Carbon
filters such as the 2B auxiliary building unit which are operatad
continuously or have restrictive surveillance test acceptance criteria
have been replaced more often than intermittent duty filters.
Penetration test results showed consistent iodine adsorption ability
relati m to carbon age.
,
c. Conclusion
Sofety-related carbon filters were found to meet TS requirements for
methyl iodide penetration. The licensee was meeting carbon sampling
requirements.
M2.3 Observation of General Material Condition
a. Insoection Scoce (62703)
The inspector conducted a walkdown inspection of Unit 2 to examine
, general housekeeping conditions. In addition, the safe shutdown and
auxiliary shutdown rooms and panels were examined to determine their
material condition and identify any existing deficiencies. The main
transformers and switchyard were also included in the walkdown. Also.
Enclosure 2
. - - _ _
.- - - .- - - . . - - - . . - _ - - -
l
12
I
portions of on-going maintenance work and test activities were reviewed
i that included: (1) installation of optical isolators: (2) control room
area chiller test: and (3) air compressor motor alignment.
b. Observations and Findinas
The housekeeping observed was adequate. The maintenance de)artment was
recently assigned housekeeping responsibility in 1996. In Jnit 2. very
few leaks were identified. The valve stems for MOVs were lubricated and
in good condition. Not all the stems for manual valves and air operated ;
valves were up to the same standards as the MOVs. The switchyard's !
relay building and battery rooms were in good condition. The switchyard
disconnect switches were also in good condition as observed from the
ground.
M3 Maintenance Procedures and Documentation
M3.1 Nuclear Service Water System Valve Realianments Durina Liauid Waste
Release
a. Insoection Scooe (61726) 4
On August 13 during Auxiliary Shutdown Panel (ASP) 1B testing, valve
1RN-58B. Nuclear Service Water Loop B Return to Standby Nuclear Service
Water Pond Isolation Valve, and valve 1RN-8438 Nuclear Service Water to
Conventional Low Pressure' Service Water Isolation Valve. were
inadvertently realigned to establish a flowpath to the Standby Nuclear
Service Water Pond. A liquid radioactive waste release was initiated
after the valves had realigned to the pond, and since RN was diverted to
the pond, it was not available to carry the radwaste to the low pressure
servicc water system for discharge to Lake Wylie. The inspector
discussed the occurrence with 31 ant personnel'and reviewed procedures,
system diagrams, the Off-site Jose Calculation Manual and liquid
radiological release package #0336, and PIP 0-C96-2123.
b. Observations and Findinas
The licensee initiated a root cause investigation to determine why the
valves changed position during ASP 1B testing. The root cause
investigation revealed that procedure PT/1/A/4700/14. Retype #0.
Auxiliary Shutdown Panel 1B Functional Test Enclosure 13.9. Control
Room / Auto Closure of 1NI-65B and 1NI-888. was inadequate. Specifically,
- the preparer of the procedure failed to recognize that valve.
- 1RN-58B
,
and 1RN-843B would be affected by the simulation of control transfer
l from the control room to 1ASPB. As a result these valves were omitted
from step 12.3.1 of PT/1/A/4700/14. Step 12.3.1 of PT/1/A/4700/14
listed eight affects of the manipulation of three transfer relays and
, directed the performer to verify that the listed effects would not
adversely affect plant conditions. Since the effects on valves 1RN-58B
- and 1RN-843 were not listed, no such verification was made. As a
,
Enclosure 2
~ _ - . - - - . . .- .-. -- --
13
result. the valves repositioned during the test, isolating flow to a
portion of the Nuclear Service Water System that was in service to
support a liquid radioactive release.
l
l The inspector questioned the impact of the valve repositionings on the
liquid radioactive waste release and determined the following:
- The concentrations of radionuclides in the waste stream were such
that dilution flow was not required to comply with the limits
stated in 10 CFR 20. Appendix B. Table 2. Column 2.
- Since flow was isolated to the Nuclear Service Water System
discharge header to Lake Wylie. the liquid radioactive waste may
have collected in the header until the system alignment was
returned to normal. Had the radionuclide concentrations been
i higher, dilution flow requirement may not have been met. The
'
licensee plans to evaluate process controls to ensure that Nuclear
Service Water flow remains available throughout the duration of a
release.
c. Conclusions
The inspector concluded that procedure PT/1/A/4700/14. Auxiliary
l Shutdown Panel 1B Functional Test, was inadequate in that it did not
l specify all components which would be affected by the test. This
procedure inadequacy resulted in valve repositions in the Nuclear
'
Service Water System which isolated flow to a portion of the system
which was supporting a liquid radioactive release and is identified as
Example 2 of Violation 50-413.414/96-13-02: Inadequate Procedures.
l M4 Maintenance Staff Knowledge and Performance
M4.1 Emeraency Diesel Generator Head Reassembiv (62703)
During this inspection the licensee identified a failure to follow
3rocedure problem during reassembly of the diesel generator cylinder
leads per procedure MP/0/A/7400/009. Revision 10. 3/6/89. Diesel Engine
- Cylinder Head Removal And Replacement. MP/0/A/7400/009 is a " Reference
!
Use" procedure for which, by Nuclear System Directive (NSD) 704.
Technical Procedure Use and Adherer.ce. Revision No. 3. 9/21/95. the
steps must be followed in sequence unless a deviation is documented.
NSD 704, paragraph 704.6. states that .t is the intent that steps in
" Continuous Use" and " Reference Use" procedures be performed
sequentially where the procedure does not specify flexibility.
Out-of-secuence steps are acceptable only if a deviation is allowed by
the procecure or is made under the following conditions:
. The sequence deviation shall be reviewed by a knowledgeable
- supervisor.
4
Enclosure 2
l
l
- - - - . ._. .. - . - .. .
l l
'
i
1
14
. Out-0f-Sequence steps shall be reviewed and initialed by the
performer and a knowledgeable supervisor prior to performing the
steps. j
. The supervisor shall ensure that a clarifying explanation of why
the deviation was made is documented within the procedure or work
order.
. The supervisor determination should take into account the
i necessity for a procedure change.
l
! Steps 11.3.17 to 11.3.20 of MP/0/A/7400/009 deal with the installation I
l of the intake elbow for the airline from the cylinder head to the air l
l header intake manifold. The procedure specifically requires that the
elbow be installed and torqued to the cylinder head, the head installed.
- the elbow aligned to the intake manifold by moving the head, and then l
torque head holddown nuts.
'
i
l The licensee deviated from the secuence of the procedural ste)s by first
installing and torquing the cylincer head before installing t1e elbows i
on 4 cylinders. When this was discovered the condition was corrected by '
removing the cylinder heads and installing the elbow per procedure. !
l
The licensee stated that, although the machine could be reassembled !
either way, the purpose for this sequence of steps was to avoid the l
possibility of stressing the elbow while aligning it to a fixed head and l
intake manifold in a cramped space. l
Investigation showed that the su)ervisor had directed the technician to
install and torque the cylinder leads 3rior to installing the elbows on
the heads for four cylinders. The tec1nician and supervisor failed to
annotate the procedure steps and the supervisor did not make a
clarifying statement in the procedure as to why the deviation was
necessary.
The inspector reviewed the circumstances and determined that the
licensee had violated the requirements of NSD 704, paragraph 704.6 in
that the deviation was not properly documented. The situation was
identified by the licensee, was corrected immediately, and had minimal l
safety significance. This licensee-identified and corrected violation '
is being treatet as a Non-Cited Violation, consistent with Section
VII.B.1 of the NRC Enforcement Policy. This issue is identified as Non-
Cited Violation 50-413/96-13-03: Failure To Follow Procedure For
Deviation Of Step Sequence.
4
Enclosure 2
l
.
_ _ _ . _ _ _ ___ _. _ - _ _ _ .__ _ _ _ . _ _ _ _ .
I
15' I
i
M7 Quality Assurance in Maintenance Activities
l
M7.1 Imolementation of Self-Assessment Proarams
!
t
i a. Insoection Scoce (40500. 61726. and 62703)
!
The inspector reviewed the implementation of the new maintenance self-
assessment program and portions of the work reduction program initiated
in January 1996. The self-assessment program was reviewed in depth to
l determine the effectiveness of the licensee's controls in identifying.
l -resolving, and implementing corrective action in the maintenance area.
!
b. Observations and Findinos
Self-assessment was part of the licensee's Quality Assurance program and
is described in Section 17.3.3 of the Duke-1 -Topical Report. Corporate
procedure NSD-607. Revision 2. Self-Assessments, was the controlling
l administrative procedure. Procedure MMP 1.14. Revision 0. Maintenance
Self-Assessment Process Guideline, was approved February 29, 1996, for
implementing the program.
The program was comprised of two categories. The first requires
continuous assessment. The second requires assessment on an as-needed
basis. The as-needed includes control of vendors, chemical control,
pre-job briefings, staffing, and procedures used.
l The self-assessment corrective actions are managed in four ways:
(1) Key management issues are major concerns that have a maintenance
i manager assigned as a sponsor to oversee the corrective action:
(2) Focus issues are concerns su3ervisors (foreman) follow for job
! observations and briefings: (3) Rework issues occurring within 90 days
l are identified in the rework program; and (4) Small scope items that
have ownership under a certain individual or crew.
The first two quarter assessments identified several problem areas such
as: (1) Work Practices - adherence to following technical procedures:
(2) Communications - technical procedures have errors and administrative
directives are numerous, overlapping, confused, and sometimes hidden:
(3) Foreign Material Exclusion - housekeeping and foreign material
entering system: (4) Misposition devices continued to be a problem: and
l (5) Rework with pumps, valves, and heat exchangers.
'
The inspector reviewed 10 Problem Investigation Process (PIP) reports to
verify the licensee was implementing approariate and timely corrective
action for the problem areas identified a3ove. Overall, there were:
. (1) four key management issues: (2) two focus items: (3) 16 rework
- items: and (4) 43 small scope items addressed in the PIPS listed.
1
.
Enclosure 2
. - . -
- - - - = , - - - .-- _ ..
i l
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l
I
i
16
The license's work order (WO) reduction program has been effective. The
backlog of 1231 in January 1996, was reduced to 429. The backlog for
W0s over six months old has been reduced from 279 to 99 and the W0s over
'
one year have been reduced from 79 to 20 over the same time period in
1996.
c. Conclusion
The maintenance department has implemented an effective self-assessment
program that is detailed and well managed. Problems such as poor work )
3ractices, foreign material exclusion and configuration control have
3een identified and management has sup)orted im)lementing appropriate
corrective action. The work order bacciog has )een significantly
reduced during 1996.
,
III. Enaineerina
El Conduct of Engineering
E1.1 Review of Radioaraohs for Relief Reauest No. 95-01 (Weld No.1RHRB-W3)
a. Insoection Scooe (57090)
On August 22, 1996, the inspectors reviewed the licensee's radiographic
film for Weld No.1RHRB-W3. This review was-conduct because during the
licensee's ultrasonic examination of Unit I residual heat removal heat l
exchanger flange-to-shell circumferential Weld No.1RHRB-W3. two '
directional coverage as required by ASME Section XI. Appendix III and
Section V Article IV as modified by Code Case N-460, could not be
obtained,
b. Observations and Findinas
The causes of the scan limitation were part geometry and physical
barriers. Where possible, a combination of angles and wave modes were
used to maximize the coverage obtained. The weld and base metal at the
component inside surface was covered from at least one direction with a
minimum of one angle. The licensee provided NRC's Office of Nuclear
Reactor Regulation (NRR) an ISI Limitation Report that gave the layout
of Weld 1RHRB-W3. The layout showed flange geometry and bolting limited
ultrasonic scanning: thus precluding examination of approximately 78% of
the weld volume. The licensee proposed using radiography as an
alternate volumetric examination method. However, a modification to the
heat exchanger had to be completed to allow access to the ID surface for
source positioning and the qualification of an acceptable radiographic
technique. The radiographic examination was scheduled to be performed
in the first refueling outage of the Second 10-Year Interval (End of
Cycle 9). Although this examination would be performed after the close
of the first inspection interval. it would enhance the 22% Code-acquired
volumetric examination coverage achieved using ultrasonic techniques.
Enclosure 2
. -_
- . .. - - - - . .. . - . - .- .- - -
i I
l
17
NRR Safety Evaluation Report (SER) for Relief Request No. 95-01
concurred with the licensee's proposed alternative examination method.
NRR concluded that, based on the coverage obtained and the radiographic
examination scheduled during the first outage of the second inspection
interval, it was reasonable to conclude that degradation, if present,
would be detected. Thus, reasonable assurance of continued inservice
structural integrity would be provided.
The inspector's review of radiographic film for weld 1RHRB-W3 did not
reveal any unacceptable indications. The inspector also concluded that
the licensee had made the best attempt possible to examine the weld with
radiography. However, 100% volumetric coverage was also not obtained
with this method of examination. The licensee's " Limited Examination
Coverage Worksheet" for this method of examination revealed that out of
i the 258.75 square inches in the inspection volume, a total of 149.15
i
'
square inches (58%) were examined with radiography. The examination
limitation was due to component configuration, which resulted in a
l portion of the weld metal and 100% of the base metal on the flange side
of the weld not being recorded.
c. Conclusion
Based on the licensee's best attempt with a combination of one
directional ultrasonic examination of the weld and base material- 10. as
well as the additional radiographic examination coverage, the inspectors
,
concluded 'that it was reasonable to assume that significant degradation.
l if present, would be detected. Thus, reasonable assurance of continued
l
inservice structural integrity will be provided.
E1.2 Solenoid Valve Nameolate Ratina Less than Instrument Air Desian Pressure
a. Insoection Scoce (37551) 1
The inspector reviewed the u.ain steam isolation valve solenoid valve
application as it related to maximum instrument air system design
pressures.
b. Observations and Findinas
During testing and troubleshooting of main steam isolation valve
actuators discussed in Section E8.3, the licensee identified that the
cause of a previous MSIV stroke time failure was associated with a
malfunctioning solenoid exhaust valve. When an MSIV closure signal is
generated, these solenoid valves function as pilot valves that operate
by spring force to vent pilot air when the solenoid is deenergized.
, This in turn repositions a shuttle valve that exhausts air from the MSIV
! actuator and allows the MSIV to close. During replacement of the
solenoid valves on the Unit 1 actuators, the licensee recognized that
internal springs in the replacement solenoid valves were larger than the
1 existing valves and concluded that the relatively low spring force
Enclosure 2
'
. .
. - . - . . - . - - .-. _-- - . - - - - .. - ._ ._. .
,
l
1
l
i
'
18
,
available in the existing solenoid valves may have contributed to the
'
previous stroke time failure.
Subsequent to this troubleshooting, the inspector compared the nameplate
pressure ratings for the solenoid valves to the maximum design pressure
of the instrument air system based on instrument air system relief valve
settings (Flow Diagram CN-1605-1.1). On August 22. the inspector
identified that the nameplate rating of the solenoid valves (100 psi)
was less than the relief setpoints for main air receiver tanks located
at the discharge of the main air compressors (115 psi). The inspector
informed the licensee of this discrepancy and questioned whether normal
o)erating pressures of the instrument air exceeded the design rating of
t1e solenoid valve and if provisions existed for control room operators
to detect an increase in instrument air pressure resulting from a
malfunction of the instrument air system. At the time of identification
this concern only pplied to Unit 2 since Unit 1 was shutdown and the i
Unit 1 solenoid va ves had been refurbished. '
The licensee took actions to measure air pressures locally at the Unit 2
MSIVs and found air pressure at ap3roximately 91 psi. Normal instrument
air pressure at the discharge of t1e air compressors is approximately
100 psi. The 3ressure differential between the air compressors and
MSIVs is attri)uted to air system losses. The licensee also initiated
an increased surveillance of instrument air pressures because no high
pressure alarms were available in the control room. The licensee
performed additional bench testing of the old Unit 1 solenoid valves and
determined that the solenoid valves would function properly above 115
psi with the exception of the solenoid valve assumed to have caused the
1SM-1 stroke time failure. The licensee also obtained vendor
concurrence to operate the valves with air pressures up to 120 psi.
c. Conclusion
The licensee's initial and subsequent actions were adequate to resolve
an NRC identified discrepancy where the nameplate design rating of the
MSIV solenoid valves was less than the maximum design pressure of the
instrument air system. This discrepancy is significant because it
resulted in the unrecognized potential to degrade the ability of the
main steam isolation valves to close in the event of an instrument air
system malfunction. This issue is identified as Example 1 of Violation
50-413.414/96-13-04: Inadequate Design Controls (Selection of MSIV
Solenoid Valves.)
l
,
l Enclosure 2
l
l
_ . .- __ _
. -_ ___ _ _ _ _ - - - - . - . - _ - _ _ . . _ _. __ ___ _ _ _ -
l
19
E2 Engineering Support of Facilities and Equipment
E2.1 Main Feedwater Pumo B Trio Durina Unit 2 Startuo
a. Insoection Scooe (37551)
On August 10, during the Unit 2 restart from a forced shutdown, the 2B
main feedwater pump tripped on high discharge pressure while operators
were attempting to place it in service. A Failure Investigation Process
(FIP) team was formed to determine why the pump tripped. The inspector
observed the initial meeting of the FIP team, discussed the issue with
engineering personnel, and reviewed instrument details and Problem
Investigation Process (PIP) report 2-C96-2110.
b. Observations and Findinas
Several indication anomalies associated with the pump trip were noted
during the aump startup and trip. Specifically, control room operators
indicated tlat they did not receive an annunciator for high pump
discharge pressure prior to the pump trip, nor did the control room
indication for pump discharge pressure reach the high discharge pressure
setpoint of 1385 psig. As a result, there was some confusion over the
validity of the pump trip.
According to data obtained from the Operator Aid Computer (0AC), the 2B
Main Feedwater pump discharge pressure closely approached and probably l
reached the pump discharge pressure high setpoint. This indicated that
'
the trip was valid. To explain the anomalies observed by the control
room operators, the licensee began to explore the pump discharge
pressure instruments. The inspector reviewed drawing number CN-1499-
CF1. Revision 8, Instrument Detail for Feedwater Pump Discharge Pressure
and discussed the drawing with engineering personnel to understand how
the indication and control instruments functioned.
Three pum) discharge pressure switches perform a pump trip function on 2
out of 3 ligh discharge pressure signals. Two of these pressure
switches sense process fluid directly. As such, these switches provide
an instantaneous res)onse to changes in pump discharge pressure. The
third pressure switc1 is operated by a pneumatic transmitter. This
pressure switch is not as responsive to changes in pump discharge
pressure. In addition, the same pneumatic transmitter provides the
signal to indicate pump discharge pressure on the control board and to
the high pump discharge pressure annunciator. The OAC data was
transmitted from an electronic transmitter which directly sensed process
fluid.
The B Main Feedwater pump apparently tripped when a short duration
i pressure spike was sensed by the pressure switches which monitor the
! process fluid directly, thereby satisfying the 2 out of 3 trip logic.
! The OAC data were valid, but process limitations introduced a lag in the
i
- Enclosure 2
i
l
, - -. . - - - -. - - . -. - - - - . . --- .
20
transmission of the pump discharge pressure information to the control ,
board gauge and annunciator. As a result, the control indications were j
l
consistent with the conditions in the plant and the pump trip was valid. 4
The FIP team concluded that a combination of factors caused the B Main
Feedwater aump discharge pressure to reach the Jump trip setpoint.
l Steam for iain Feedwater pump operation while t1e associated unit is
offline is typically provided from the other unit. Since Unit 1 was in
l a refueling / steam generator replacement outage, steam was provided by an
,
auxiliary boiler. The FIP team concluded that the combination of
l supplying auxiliary steam from a single auxiliary boiler and relatively
rapid increases in pump speed demand by the control room operator caused ;
the speed to overshoot, causing the high discharge pressure. 1
The FIP has recommended that two auxiliary boilers be used to supply
steam to the main feedwater pum) turbines in future unit start-ups
occurring when both units are slut down An extended time for steam
piping and turbine chest warming was also proposed. Operator monitoring
of steam pressure at the low pressure steam admission valve to the main
feedwater pump turbine during pump starts was identified as an
additional potential corrective action.
c. Conclusions
'
The inspector concluded that the licensee's actions to determine the
root cause of the 28 main feedwater pump trip, and evaluate the
l indication anomalies observed by the operators were timely and
,
appropriate. Proposed corrective actions addressed the apparent cause
l
identi fied.
E2.2 Enaineerina Sucoort of Facilities and Eauioment - Modifications
a. Insoection Scooe (37550)
The inspector reviewed several Nuclear Station Modifications (NSMs)
implemented during the current Unit 1 outage. The modification review
included verification that design control requirements of Regulatory
l Guided 1.64 and ANSI N45.2.11-1974. Quality Assurance Requirements for
i the Design of Nuclear Power Plants, and licensee procedures were
implemented. Elements of the design process reviewed included post
!
modification testing, procurement, procedure revision, training, 50.59
safety evaluation, and field verification of plant hardware changes as
applicable. The following NSMs were reviewed:
- CN-11360. Diesel Generator Battery Charger Replacement
! * CN-11375. Upgrade Allowable Temperature for Some Auxiliary
- Feedwater (CA) System Piping
i
-
Rian 8%Ws f CA System F w pt miz t n nd Run-out
Enclosure 2
. _ _ . ,_ __
.- .- - -- - - . .. .. -
i
f
21
. CN-11372, Revise Run-out Setpoints for Component Cooling (KC)
l System Single Pump Operation
b. Observations and Findinas
The following modifications were implemented to resolve long-standing ,
i
equipment problems at Catawba:
l
. The DG battery chargers were replaced (CN-11360) to resolve a
reliability concern with the previous chargers related to the
impact of ambient temperatures on charger performance. The
purchase specification recuired vender testing to verify the new
chargers were not impactec by the anticipated DG room ambient
temperature transients.
. Piping supports for portions of the Auxiliary Feedwater system
were modified (CN-11375) to allow increasing the piping allowable
temperature.
. The Auxiliary Feedwater flow optimization and run-out protection '
circuit deletion (CN-11371) was to com3ensate for the changed
Auxiliary Feedwater operating system claracteristics associated
with the new steam generators.
. Future run-out protection was to be provided by mechanical stops
on the Auxiliary Feedwater pump flow control valves.
. The Component Cooling water pump run-out setpoint change (CN-
11372) was to permit single pump operation of the Component
Cooling system for normal plant conditions. Singic pump operation
would allow the pumps to operate at an optimum condition with
reduced vibration ar.J impeller wear.
Post modification testing performed and scheduled was adequate to verify
equipment and system function following the modifications. Appropriate
procedures were revised and adequate training was scheduled or completed
for the",e modifications. The licensee's 50.59 safety evaluations were
detailed and adequately justified the conclusions. An outstariding issue
from a previous NRC inspection remains open related to the 50.59
evaluation for the Auxiliary Feedwater piping temperature upgrade.
Procurement documentation demonstrated that the appropriate quality
level material was used for installed equipment and materials. Field
verification for the Auxiliary Feedwater piping supports and the DG
chargers demonstrated that equipment installation was consistent with
,
the Nuclear Station Modification requirements.
l
c. Conclusion
l Several Unit 1 modifications were implemented during the outage to
resolve existing equipment problems and improve plant reliability. The
l Enclosure 2
l
l
. . ~ . - -.
- . - _. . .. - . - --
'
i
I
22 ;
modifications demonstrated appropriate control of the design control l
process at Catawba. For the safety evaluations reviewed. the !
requirements of 50.59 were met.
E2.3 Main Feedwater Pioino Erosion / Corrosion 1
a. Insoection Scoce (37551) l
During the Unit 1 Steam Generator Replacement Outage, the licensee
identified erosion / corrosion of a localized area in the main feedwater
piping between the check valves and isolation valves in the doghouses.
The licensee requested approval of ASME Code Case N-480 to allow for
planned replacement of some of the affected piping during the next
refueling outage. The inspector reviewed the erosion / corrosion
inspection data and PIP 0-C96-1963.
b. Observations and Findinas l
With the approval of the ASME Code Case N-480. the licensee performed
evaluations to support operation until the next refueling outage for two
of the four feedwater lines on Unit 1. One line was degraded to the
point that a repair was performed and the remaining line was acceptable
"as is." During the forced outage on Unit 2 erosion / corrosion
inspections of similar locations were performed with acceptable results.
NRC approval to implement ASME Code Case N-480 was required prior to ,
restart of Unit 1. This approval was received in a letter dated i
September 9. 1996,
c. Conclusions
The inspector concluded that the erosion / corrosion program was effective
in identifying this issue and an appropriate decision was made to
inspect Unit 2 for similar conditions at the first available
opportunity.
E3 Engineering Procedures and Documentation
E3.1 1995 Revision to the Uodated Final Safety Analysis Reoort
By letter dated May 28. 1996, the licensee submitted the 1995 revision
to the Updated Final Safety Analysis Report (UFSAR) in accordance with
10 CFR 50.71. This regulation requires that this submittal shall
contain all the changes necessary to reflect information and analyses
submitted to the Commission by the licensee or arepared by the licensee
pursuant to Connission requirement since the su3 mission of the original
FSAR or, as appropriate. the last updated FSAR.
l
!
f Enclosure 2
l
l
l
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[- 23
a. InsDection ScoDe
10 CFR 50.71 provides that the updated FSAR shall be revised to include
- the effects of
- "All changes made in the facility or procedures as described in
the FSAR."
e " Safety evaluations performed by the licensee either in support of
requested license amendments. . . ." - Since this category clearly
involves NRC staff approval of licensing basis changes, other
changes that the staff approved (e.g., topical reports, reliefs to
ASME Code sections, exemptions, etc.) but were not conveyed as
amendments are also implied.
"
....or in support of conclusions that changes did not involve an
unreviewed safety question" - These are evaluations performed by
the licensee in accordance with the provisions of 10 CFR 50.59.
. "All analyses of new safety issues performed by or on behalf of
the licensee at Commission request" - Examples include licensee
actions as a result of generic letters, bulletins, etc.
b. Observations and Findinas
The inspector reviewed the 1995 revision of the Catawba UFSAR in-office
and met with licensee personnel on-site. The purpose of the review was
to confirm if the changes made in the 1995 revision comply with the
provisions of 10 CFR 50.71. The inspector reviewed the changed pages to
confirm that all changes'were appropriately addressed by licensing
actions. 10 CFR 50.59 reports, or regional inspection activities.
The inspector traced the changes in the 1995 revision of the UFSAR to
documents in the official NRC records such as amendments to the
operating license, staff letters transmitting safety evaluations, annual
10 CFR 50.59 reports submitted by the licensee, inspection reports, or
licensee letters. The inspector confirmed that the 1995 revision does
not constitute a source of initial communication (to NRR) of these
changes.
The inspector noted that some UFSAR changes made under 10 CFR 50.59
appeared to have not been reported in the periodic update submitted
immediately after the changes were made. Examples include CN-50422. CN-
50431. CE-3604. CE-3605, and CE-60212. The licensee should review the
circumstances involved and determine the cause of the delayed update.
The inspector noted that the licensee had performed the required
analyses in accordance with 10 CFR 50.59 and concluded that the
apparently late reporting of some changes was not a violation of
regulatory requirements.
I
Enclosure 2
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The inspector noted that UFSAR Section 13.1 regarding the licensee's
nuclear organization, had been revised. The licensee had not performed
an evaluation in accordance with 10 CFR 50.59. or sought prior staff- l
a) proval. The inspector reviewed the changes and determined that the j
clanges do not reduce the organizational resources committed to r/ lear i
safety and are therefore acceptable. In an August 20, 1996, meeting, j
the licensee stated that it planned to institute an internal procedure
to ensure that such changes receive sufficient evaluation in the future.
c. Conclusion
The inspector concluded that the 1995 revision of the Catawba UFSAR
matched the provisions of 10 CFR 50.71. and is therefore in compliance
with 10 CFR 50.71.
E4 Enaineerina Staff Knowledae and Performance
E4.1 Standby Shutdown System (SSS) Ooerability
a. Insoection Scooe (92903)
The inspector reviewed the licensee's activity to resolve a recently ,
identified issue related to the operability of the SSS. )
1
b. Observations and Findinas
During an inspection of the SSS on July 8-12. 1996, (NRC Inspection
Report 50-413.414/96-10) an NRC inspector noted non-conservative
assumptions / design inputs in calculation CNC 1223.04-00-0009, Standby i
Make-up Pump (SMUP) Sizing, dated November 1,1993. Discussions with !
the licensee indicated these incorrect assumptions did not impact the
calculation conclusion that the SMUP was operable for the required
72-hour period of an SSS' event. Further review by the licensee after
the inspection determined that the design input errors did impact the
calculation conclusion, resulting in an operability concern for both
Units 1 and 2 SSS. Problem Investigation Process Report (PIP) 0-C-96-
1824 was initiated by the licensee on July 18, 1996, to address this
issue.
The calculation included the following errors:
- Incorrect determination of Spent Fuel Pool (SFP) Inventory: boil
off not included
. Incorrect pump speed
. Incorrect SFP (cycle specific) temperature
Enclosure 2
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- Design minimum pump flow rather than actual flow used for SFP
inventory reduction
The significant error was the temperature value used for the SFP which
provided the water source for SMUP to the reactor coolant pump seals.
The temperature was derived from a heat up rate based on pool loading of
spent fuel that was specific to a past cycle on Unit 2. -This
temperature value would not be appropriate for any other pool loading.
A calculation revision in November 1993 reviewed the SMUP suction
pulsation danpener based on these past cycle conditions and concluded
that the dampener (and SMUP) was operable for the required 72-hour
period. The dampener's function is to assure adequate net positive
suction head (NPSH) for SMUP operation. The licensee's recent
evaluation initiated by PIP 0-C-96-1824. determined that the dampener
(and SMUP) operability could not be assured near the end of the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> ,
period.
At the time that the operability concern was identified. Unit 2 was at
power and Unit 1 was in an extended outage for steam generator
replacement. The licensee determined that the Unit 2 SSS was operable
but degraded and Unit 1 SSS was inoperable. Unit 1 SSS was not required
to be operable until entering mode 3.
The Unit 2 SSS degraded operability determination was based on analysis
and imposition of more limiting SFP temperature requirements. The
analysis was provided by Calculations CNC 1201.30-00-0019, Catawba Unit
2 SFP Decay Heat and Temperature Calcuiction for PIP 0-C96-1824, dated
July 24. 1996, and CNC 1223.04-00-0069, Unit 2 Cycle 8 SMUP NPSH l
Requirements for PIP 0-C96-1824. dated July 24. 1996. The SFP decay
heat calculation determined that with an initial SFP temperature of
125 F and the current Unit 2 SFP load, the SFP temperature would be
aaproximately 181 F. 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> after the initiation of an SSS event. The i
SiUP NPSH calculation determined that at 181 F, adequate NPSH was
available to the SMUP, assuming the suction dampener was inoperable.
The licensee established controls to assure that the SFP temperature was
maintained less than 125 F. The SFP temperature alarm was reset to
115 F (included a 9 F instrument error) and increased operations
surveillance for SFP temperature monitoring. The normal summer
temperature range of the SFP was 100-105 F. The inspector reviewed the
calculations and verified the correct design input values were used.
The above actions were immediate corrective actions to establish Unit 2
SSS operability for the current fuel cycle. Long-term corrective
actions were being evaluated and will include resolution of the Unit 1
SSS operability prior to restart of the unit.
c. Conclusion
The licensee's immediate corrective actions were adequate to resolve
present operability concerns on Unit 2. The licensee failed to identify
Enclosure 2
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1 the design input errors in Calculation 1223.04-00-0009 on two occasions:
i first during the independent review of the calculation in November 1993,
and again during the licensee's SSS pre-inspection self-assessment in
- June 1996. This issue is identified as Example 2 of Violation 50-
413.414/96-13-04. Inadequate Design Controls (Standby Shutdown System
Make-up Pump Sizing Calculation.)
E8 Hiscellaneous Engineering Issues
E8.1 Safety-Related Loaic Circuits Testina Discreoancy
-
a. Insoection Scooe (37551)
The inspector reviewed the licensee's response to their finding that the
.
'
testing of the degraded voltage and undervoltage logic on the DG load
sequencer had been insufficient. The licensee's finding was in response
to the review of safety-related logic circuits required by Generic
Letter (GL) 96-01. " Testing of Safety-Related Logic Circuits."
b. Observations and Findinas
During the review of the safety-related logic circuits required by GL 96-01, the licensee discovered that part of the logic circuits for the
degraded voltage and undervoltage relays for the emergency diesel
generator load sequencer logic circuits were not being tested
completely. This logic is a 2 out of 3 logic circuit. Portions of the
logic circuit were not verified during surveillance testing in that not
all possible combinations of logic were tested. This resulted in
portions of circuitry not being verified operable during each
surveillance cycle. The licensee documented this issue in PIP 0-C96-
2015.
Both Units 1 and 2 were affected by this testing deficiency: however,
both Units were shutdown at the time of discovery. The licensee's
corrective action was prepration and completion of revised testing
which would satisfy the testing requirements for the logic circuitry.
Procedure IP/2/A/4971/075A Logic Testing for Degraded Bus and Load
Sequencer Voltage Circuits was completed to satisfy the testing
requirements. The inspector reviewed this test procedure and found that
it adequately resolved the testing concern. The licensee planned to
complete this testing for both Units 1 and 2 prior to restart.
c. Conclusions
Licensee identification of this test deficiency met the intent of
Generic Letter 96-01 and corrective actions were appropriate.
Enclosure 2
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E8.2 Temocrary Station Modification Audit Proaram (92903) l
(Closed) Violation 50-413.414/94-30-01. Inadequate Corrective Action for
Temporary Station Modification (TSM) Program Deficiency. This item 1
addressed the licensee's failure to correct a TSH program deficiency '
related to periodic audits of active TSMs. The licensee identified that
several monthly audits required by procedure were not performed. After i
the completion of the corrective actions, an NRC inspector reviewed the l
TSM program and identified approximately 30 active TSMs which were not l
included in the previous audit. This demonstrated that the licensee's
original corrective actions were not adequate. The licensee's
corrective action for the violation was to revise the TSM audit process
to. incorporate increased management oversight and increase guidance for
the audit process. The inspector reviewed the June 1996 quarterly TSM
audit and verified that all active TSMs were included. The inspector
concluded that the licensee adequately resolved the TSM program
deficiency related to periodic audits. 1
E8.3 Main Steam Isolation Valve 1SM-1 Reoortability Evaluation (92903) I
(Closed) Unresolved Item 50-413/96-02-05. Review of MSIV 1SM-1
Reportability Evaluation and In-Plant Review of PIP Initiation
Performance. During this inspection aeriod the licensee completed the
Reportability Evaluation and troubleslooting for the stroke time failure
of Main Steam Isolation Valve 1SM-1 (refer to PIP 1-C96-0751). Results
of testing performed during the current 1E0C9 refueling outage
determined that the cause of the stroke time failure was due to an
intermittently malfunctioning B-train exhaust solenoid valve. Based on
the test results, the licensee plans to submit an LER. The inspector ,
reviewed the results of the licensee's in-plant review of PIP initiation i
during test activities (Report No. SA-96-41(CN) (SRG). PIP 0-C96-1759).
The licensee's audit consisted of the review of approximately 150
completed test procedures and other records. The review concluded that
PIPS are being initiated to assess systems / components that do not meet
test acceptance criteria. The review recommended enhancements to NSD
208. Problem Investigation Process, to clarify references for PIP
initiation. The inspector concluded from this review that the failure
to initiate PIPS in response to test failures is not a programmatic
concern.
IV. Plant SuoDort
R1 Radiological Protectior.' and Chemistry Controls
R1.1 Individual Escorted into Radiation Control Area
a. Insoection Scooe (71750)
On July 19. 1996, a contractor employee escorted his spouse into the
Radiation Control Area during a plant tour. A radiation protection
Enclosure 2
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technician in u)per containment questioned their need to enter that area
and requested tlat they leave. While exiting the Radiation Control Area
a second radiation protection technician questioned the absence of l
appropriate dosimetry and recognized the unauthorized access. Problem
Investigation Process (PIP) Report 1-C96-1837 was initiated to address
the issue. A root cause analysis was performed by the licensee because
station management recognized the similarity of this occurrence to an '
issue in October 1995. The inspector reviewed the PIP and its l
associated root cause, discussed the issue with the contractor employee. '
and reviewed the circumstances of the previous occurrence documented in
NRC Inspection Report 50-413.414/95-22.
b. Observations and Findinas
While in the Radiation Controlled Area, the individuals remained
together, did not enter any high radiation areas, and had one electronic
dosimeter which was operating. The electronic dosimeter registered no
exposure during the entry.
1
The inspector noted that the previous occurrence was characterized as a !
non-cited violation (NCV 50-413,414/95-22-03) since it was identified by i
the licensee, was apparently an isolated case, and appropriate
'
corrective actions were initiated.
The recent issue was also identified by the licensee and appropriate
actions were taken by radiation protection personnel to question,
identify, and document the occurrence. Appropriate sensitivity to the
issue was demonstrated by the performance of a root cause evaluation
which identified expanded proposed corrective actions.
Conclusioilg
'
c.
The unauthorized entry of an individual into the Radiation Control Area
without appro]riate dosimetry, training, or body burden analysis is a i
violation of Radiation Protection Directive No. II-1, Radiation Area
Access and Monitoring Devices. Since corrective actions for a previous.
similar occurrence were not effective in preventing recurrence, this
issue is identified as Violation 50-413.414/96-13-05: Repeat Radiation
Control Area Entry Without Dosimetry.
1
V. Manaaement Meetinas
X1 Exit Meeting Summary
The inspectors ] resented the inspection results to members of licensee l
management at tie conclusion of the inspection on September 16, 1996. The ,
licensee acknowledged the findings presented. No proprietary information was
identified. l
Enclosure 2
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PARTIAL LIST OF PERSONS CONTACTED
- Licensee
!
Bhatnager. A. Operations Superintendent
Coy. S. Radiation Protection Manager ,
Eller. R., Licensing Specialist i
Forbes, J. , Engineering Manager .
Funderburk. W. , Work Control. Superintendent j
Hallman.-W., Project Director. SGRP
Harrall. T.. IAE Maintenance Superintendent
Kelly..C... Maintenance Manager
Kimball. D.. Safety Review Group Manager
Kitlan, M., Regulatory Compliance Manager
Lowery J., Compliance Specialist
McCollum. W. Catawba Site Vice-President
Nicholson. K., Compliance Specialist
Parker. R., Manager. Inage
Patrick, M. , Safety Assurance Manager
Peterson G., Station Manager
Propst. R., Chemistry Manager
Rogers. D., Mechanical Maintenance Manager
Rose. I., Manager. Workforce Processing
Self. T. , Maintenance Supervisor
Tower. D.. Compliance Engineer
i
Enclosure 2
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{
INSPECTION PROCEDURES USED
IP 37550: Engineering
IP 37551: Onsite Engineering
IP 40500: Effectiveness-of Problem Identification and Prevention
IP 57090: NDE Procedure Radiographic Exam. Procedure Review
IP 61726: Surveillance Observation
IP 62700: Maintenance Program Implementation
IP 62703: Maintenance Observation
IP 71707: Plant Operations
IP 71750: Plant Support Activities
IP 92903: Followu) - Engineering
IP 93702: Onsite Response to Events
ITEMS OPENED, CLOSED. AND DISCUSSED
Onened
l
50-414/96-13-01 NCV: Failure to Report Inoperability of Both
Trains of Auxiliary Building Ventilation (Section
01.1).
50-413, 414/96-13-02 VIO: Inadequate Procedures (Sections 01.2. M3.1).
50-413/96-13-03 NCV: Failure To Follow Procedure For Deviation of -
Step Sequence (Section M4.1). -
50-413.414/96-13-04 VIO: Inadequate Design Controls for (1) Standby j
Shutdown System Make-up Pump Sizing Calculation, and 1
(2) Selection of MSIV Solenoid Valves (Sections E4.1 l
and E1.2). ;
'
50-413.414/96-13-05 VIO: Repeat Radiation Control Area Entry Without
Dosimetry (Section R1.1). ,
Closed
i
50-413.414/94-30-01 VIO: Inadequate Corrective Action for Temporary ;
Station Modification Program Deficiency (Section
E8.2). 3
50-413/96-02-05 URI: Review of MSIV 1SM-1 Reportability
Evaluation and In-Plant Review of PIP Initiation
Performance (Section E8.3).
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Enclosure 2 !
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i
LIST OF ACRONYMS USED
1
ANSI - American Nuclear Standard Institute
- ASME - American Society of Mechanical Engineers
Auxiliary Shutdown Panel
-
ASP -
CA -
Auxiliary Feedwater System
CFAR -
Component Failure Analysis Report
CFR -
Code of Federal Regulations
CNS -
Catawba Nuclear Station i
CR -
Control Room
DG -
Diesel Generator
DPC -
Duke Pts:er Company
EOC -
End of Cyck
- F -
degrees Fahrenheit
FATS - Failure Analysis Trending System
GL -
Generic Letter
HVAC - Heating. Ventilation, and Air Conditioning
IAE -
Instrument and Electrical
ID -
ID Inner Diameter i
IFI -
Inspector Followup Item
IR -
Inspection Report
KC -
Component Cooling
LER -
Licensee Event Report
MOV -
Motor Operated Valve
MSIV - Main Steam Isolation Valve
, NDE -
l NPRDS - Nuclear Plant Reliability Data System
'
NPSH - Net Positive Suction Head
NSD -
Nuclear System Directive
i
NSM -
Nuclear Station Modification
'
OOS -
Out-of-Service
l PIP -
Problem Investigation Process
PM -
Preventive Maintenance
l PORC - Plant Operations Review Committee
i
RG -- Regulatory Guide
l
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RHR -
RN -
Nuclear Service Water System
RTB -
Reactor Trip Breaker
SFP -
Spent Fuel Pool
SGRP - Steam Generator Replacement Project
SITA - Self-Initiated Technical Audit
l SMUP -
Standby Make-up Pump
'
SSS -
Standby Shutdown System
TSM -
Tem)orary Station Modification
TS -
Tec1nical Specifications
UFSAR - Updated Final Safety Analysis Report
URI -
Unresolved Item
VC/YC - Control Room Ventilation and Chilled Water Systems
VIO -
Violation
WO -
Work Order
Enclosure 2
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