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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:NRC TO U.S. CONGRESS
MONTHYEARML20236G5871987-07-30030 July 1987 Responds to 870617 Request for Info Re GE Reed Rept on LER Sys.No Issues Raised in Reed Rept Support Need to Curtail Operation of GE BWRs ML20215F2291986-12-16016 December 1986 Responds to Re Constituent Concerns.Concerns Carefully Considered & Given Thorough Response Consistent W/ Commission Regulations & Adequate Protection of Public Health & Safety NUREG-1068, Responds to Constituent Inquiry Re Nuclear Reactor Containment Sys Designed by G.E.Probability of Severe Reactor Accidents Quite Low.Third Party Liability Insurance Provided Under Price-Anderson Legislation.W/O Stated Encls1986-08-26026 August 1986 Responds to Constituent Inquiry Re Nuclear Reactor Containment Sys Designed by G.E.Probability of Severe Reactor Accidents Quite Low.Third Party Liability Insurance Provided Under Price-Anderson Legislation.W/O Stated Encls ML20138R1581985-12-18018 December 1985 Responds to R Digiacomo 851023 Inquiry Re Recent Issuance of Facility OL & Effect on Costs of Electricity & on Water Conditions in Schuylkill River.No Significant Impact on Water Use or Conditions Expected ML20137U2691985-11-26026 November 1985 Submits Results of Investigation of Constituent R Dobson ,Per 851029 Request.Region I Combined Insp Repts 50-352/85-30 & 50-353/85-07 Re Water Spill Incident Encl ML20132B8341985-07-18018 July 1985 Forwards Quarterly Status Rept for Second Quarter CY85. Licensing Delay for Limerick 1 Projected to Be 5 Months. Delay Cannot Be Quantified for Shoreham Due to Litigation. Full Power OL Issued for Palo Verde 1 on 850601 ML20140H6701985-06-0303 June 1985 Forwards Press Release 85-78 Re NRC Proposed Fine Against Util for Alleged Violations of Requirements Concerning Unplanned Occupational Radiation Exposures & Failure to Control Contractor Work Forces ML20126B1491980-02-0707 February 1980 Forwards NRC 800130 Response to M Seidts Re Size of Facility Low Population Zone ML20125B6621979-10-12012 October 1979 Responds to Re Fr Romano 790723 Concern About Blasting at Rock Quarry Near Facilities.Request Being Treated Per 10CFR2.206.Effects of Blasting at Nearby Quarry Must Be Carefully Evaluated ML20235F1361971-12-15015 December 1971 Forwards Notice of Hearing to Be Held on Util Application Re Plant.Div of Reactor Licensing Safety Evaluation & Rept to ACRS Also Encl.W/O Encls 1987-07-30
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20206Q5871999-05-14014 May 1999 Advises That Info Contained in ,Which Submitted Revised Procedures for Plant EP Response Procedures Will Be Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R3031999-05-11011 May 1999 Informs That on 990407,NRC Administered GFE Section of Written Operator Licensing Exam to Employees of Facility. Forwards Copies of Both Forms of Exam,Including Answer Keys & Grading Results of Facility ML20206N1111999-05-0707 May 1999 Forwards Insp Repts 50-352/99-02 & 50-353/99-02 on 990302-0412.Three Violations of NRC Requirements Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20206H2651999-05-0606 May 1999 Informs That on 990112 Licensee Submitted to NRC Core Shroud Insp Plan for Plant,Unit 2,in Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Boiling Water Reactors ML20206G5131999-05-0303 May 1999 Approves Change of Completion Date for Implementation of Thermo-Lag Fire Barrier Corrective Actions at Plant from End of April 1999 Limerick Unit 2 RFO to 990930 ML20206H8301999-04-30030 April 1999 Forwards Exam Repts 50-352/99-301 & 50-353/99-301 on 990312-19 (Administration) & 22-26 (Grading).Four of Five RO Applicants & Three of Four SRO Applicants Passed All Portions of Exams ML20206E6951999-04-30030 April 1999 Advises That Plant,Unit 2 Cycle 6 Safety Limit Mcpr, ,contained in PECO Energy Co 990311 Application & 990204 Affidavit Will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20206F4221999-04-27027 April 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990312 & 990315-19 at Facility.Completed ES-501-2,power Plant Licensing Exam Results Summary & Summary of Overall Exam Results Encl.Without Encl ML20205N2291999-04-0909 April 1999 Discusses Limerick Generating Station Plant Performance Review Conducted for Period April 1998 Through 990115 & Informs of NRC Planned Insp Effort Resulting from Review. Historial Listing of Plant Issues,Encl IR 05000352/19980091999-03-30030 March 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-09 & 50-353/98-09 Issued on 990106.Actions Will Be Examined During Future Insp of Licensed Program ML20205C2711999-03-26026 March 1999 Forwards Insp Repts 50-352/99-01 & 50-353/99-01 on 990112-0301.One Violation Noted & Being Treated as Non-Cited Violation.Staff Conduct of Activities During Insp Generally Characterized by Safe & Conservative Decision Making ML20205G7651999-03-22022 March 1999 Forwards RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs, for Plant, Units 1 & 2.Response Requested within 90 Days of Receipt of Ltr ML20204G9721999-03-11011 March 1999 Informs of Completion of Review of Changes Proposed by PECO Energy Co to Lgs,Units 1 & 2,EALs.Proposed EALs Incorporate Guidance in NUMARC/NESP-007,Rev 2.Forwards Safety Evaluation Supporting Proposed Changes ML20204H8171999-03-10010 March 1999 Discusses Request That NEDC-32645P, Limerick Generating Station,Units 1 & 2,SRV Setpoint Tolerance Relaxation Licensing Rept, Rev 2,dtd Dec 1998,be Withheld from Public Disclosure.Determined Info Proprietary & Will Be Withheld ML20207J0611999-03-0808 March 1999 Provides Authorization to Administer Initial Written Exams to Listed Applicants on 990312.NRC Region I Operator Licensing Staff Will Administer Operating Tests on 990315-19 at Limerick Generating Station ML20203G6721999-02-17017 February 1999 Second Partial Response to FOIA Request for Documents. Records in App D Encl & Being Made Available in Pdr.App E Records Being Withheld in Part (Ref FOIA Exemption 5) & App F Records Completely Withheld (Ref FOIA Exemptions 6 & 7) ML20203B9001999-02-0808 February 1999 First Partial Response to FOIA Request for Documents. Forwards Documents Listed in App a Already Available in PDR, Documents in App B Released in Entirety & Documents in App C Being Withheld in Part (Ref Exemption 6) ML20202J0261999-02-0303 February 1999 Informs of Completion of Licensing Action for NRC Bulletin 96-03, Potential Plugging of Emergency Core Cooling Suction Strainers by Debris in Boiling-Water Reactors ML20203A6111999-01-22022 January 1999 Confirms 990115 Conversation Between Mj Williams & P Orphanos Re Arrangements Made for Administration of Licensing Exam at Limerrick Generating Station & Peach Bottom Atomic Power Station During Week of 990705 ML20199F9251999-01-11011 January 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-05 & 50-353/98-05 ML20199C6501999-01-0606 January 1999 Forwards Insp Repts 50-352/98-09 & 50-353/98-09 on 981018- 1130 & Notice of Violation.Violation of Concern Because Technicians Exercised Poor Judgement & Deviated from Procedure in Attempt to Resolve Problem Without Mgt ML20198H4951998-12-18018 December 1998 Forwards Results of Audit of Licensee Year 2000 Program for Limerick Generating Station,Units 1 & 2 ML20198A3721998-12-10010 December 1998 Forwards Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20198B1751998-12-0808 December 1998 Advises of Planned Insp Effort Resulting from Limerick mid-year Insp Resource Planning Meeting Held on 981110. Historical Listing of Plant Issues & Details of Insp Plan for Next Six Months Encl IR 05000352/19980081998-11-23023 November 1998 Discusses licensee-identified Issue Involving Potential for Bypass of Suppression Pool as Documented in Insp Repts 50-352/98-08 & 50-353/98-08.NOV Will Not Be Issued & Civil Penalty Will Not Be Proposed ML20196C3311998-11-23023 November 1998 Forwards Insp Repts 50-352/98-08 & 50-353/98-08 on 980901-1017.No Violation Identified.Security Program Insp Identified That Security Program Effectively Protects Public Health & Safety ML20195D1491998-11-13013 November 1998 Forwards RAI Re on-going Review of IPEEE Submittal Dtd 951014.Understands That Licensee Will Inform NRC in Writing, by 981130,on How Question Re Effects of New Probable Max Precipitation at Plant,Units 2 & 3 Will Be Addressed IR 05000352/19980061998-10-15015 October 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-06 & 50-353/98-06 on 980826.Finds C/As for Violation Involving Failure to Select Performance Measures to Be Acceptable ML20154F8191998-10-0101 October 1998 Forwards Notice of Withdrawal of 960503 & Suppl Application for Amend to Fols.Amend Would Have Modified Facility TSs Pertaining to Rev to Frequency of Testing Stand Gas Treatment Sys & Reactor Encl Recirculation Sys ML20154A3461998-09-25025 September 1998 Forwards Insp Repts 50-352/98-07 & 50-353/98-07 on 980707-0831.No Violations Noted.Weaknesses Noted with Reactor Engineering Support to Rod Pattern Adjustment ML20153G4291998-09-24024 September 1998 Forwards Request for Addl Info Re Licensee Revised Emergency Action Level Guidelines for Limerick Generating Station, Units 1 & 2 & Peach Bottom Atomic Power Station,Units 2 & 3. Response Requested within 30 Days of Receipt of Ltr ML20153D0151998-09-21021 September 1998 Informs of Completion of Licensing Action for GL 92-08, Thermo-Lag 330-1 Fire Barriers, for Plant, Units 1 & 2 ML20151X2421998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-04 & 50-353/98-04 on 980805 ML20151W9601998-09-10010 September 1998 Informs That as Part of NRC PRA Implementation Plan, Commission Has Assigned Two Senior Reactor Analysts (Sras) to Each Regional Ofc.T Shedlosky & J Trapp Were Selected as SRAs for Region I ML20237D5421998-08-26026 August 1998 Ack Receipt of & Fee for $55,000 in Payment for Civil Penalty Proposed by NRC in .C/As Will Be Examined During Future Insps 1999-09-09
[Table view] |
See also: IR 05000352/1985030
Text
_- .
,
' '
, 9 311
/ UNITED STATES
E ^t NUCLEAR REGULATORY COMMISSION
$ ,E WASHINGTON, D. C. 20555
NOV 2 61985
k ..... #
I
The Honorable Richard Schulze
United States House of Representatives
Washington, D.C. 20515
Dear Congressman Schulle:
This refers to your letter to Mr. C. Kammerer, Nuclear Regulatory Commission
(NRC),datedOctober 29, 1985, which included a letter from a Mr. R. Dobson,
Jr., to yourself, dated October 14, 1985. In your letter you requested that
the NRC- review the concerns raised by Mr. Dobson and provide you a report of
our findings. The NRC Region I office was assigned the responsibility to
investigate Mr. Dobson's concerns. Results of that investigation follow.
Prior to receiving your letter, NRC Region I conducted an inspection to deter-
mine the circumstances surrounding the water spill incident, referred to in Mr.
! Dobson's letter, which occurred at Limerick Generating Station, Unit 1, on
August 1,1985. At the request of the NRC Senior Resident Inspector at Limerick,
a Regional specialist inspector was sent to Limerick on August 6,1985 to review
this incident. It was determined that the cause of the water spill was a 3/4-inch
open vent valve on drain piping from the Unit I liquid radwaste system's Equipment
Drain Collection Tank. Details of this inspection were included as a matter of
routine in the monthly NRC Senior Resident Inspector's report, NRC Region I
Combined Inspection Report No. 50-352/85-30; 50-353/85-07 (Enclosure 1).
NRC Region I concluded that this incident was of minimal safety significance
i
and did not constitute a basis that would require the licensee to shut down the
reactor if indeed it had been operating. Furthermore, NRC Region I determined
that this incident was not reportable, that is, it did not meet the notification
criteria of any Emergency Class nor any non-Errergency event category as defined
by the Code of Federal Regulations Title 10, Parts 50.72 and 50.73. However,
the licensee did make a " courtesy call" to the NRC Region I office on August 2
,'
1985 to provide initial notification of the water spill. Dissemination of this
information by Philadelphia Electric Company to the NRC is considered beyond
that required by the Code of Federal Regulations.
InregardtoMr. Dobson'sconcernoverPhiladelphiaElectricCompany's(PEco)
ability to safely operate Limerick, Unit 1, we have evaluated and co'ntinue to
review PEco's performance as an operating licensee. Since granting PECo an
operating license on October 26, 1984, wehavenotidentifiedanyincident(s)
which could be conceived as a basis for concluding thit PEco cannot safely
operate Limerick, Unit 1. On the contrary, in this specific incident PEco's
actions to contain the contaminated water, isolate the source of the leak, ;
investigate additional potential sources and extent of' contamination, process '
the contaminated water and decontaminate the sumps, review generic implications,
I
G512090252 851126
DR ADOCKODOOg2
__ _ _ _ _ __ ___ _ __ . . _ _ _ _ _ - _ . _ . . _ _ _ _ _ _ _ _ -
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The Honorable Richard Schulze 2
and implement corrective and preventive actions were determined by NRC Region I to
be timely, thorough and appropriate.
Regarding Mr. Dobson's concern that the plant was allowed to continue operation
while contaminated water had not yet been cleaned up, we have determined that
Limerick Unit I was shutdown at the time. However, had Unit I been operating,
the licensee would not have been required to shut down the reactor as no license
condition was exceeded, no regulation was violated, and nothing of safety
significance was involved. The spilled water, which contained very low levels
of contamination, was collected from the sumps and processed through the
radwaste system. All water had been transferred to the radwaste system by the
end of August 2, 1985. All sumps were then decontaminated. Although not required,
the licensee posted the areas as Radiation Areas in order to minimize possible
spreading of contamination. (See Enclosure 1 for further details.)
In regard to Mr. Dobson's concern over metal particles in the reactor coolant
which would pick up and transfer excessive radiation to the cooling system and
possibly the environment the only " particles" that could be construed as such
are normally-occurring metal corrosion products in the reactor coolant. These
are continuously removed by filtration and ion exchange systems in order to
maintain the purity of the reactor coolant.
Whenever there are piping interfaces (for example, in a heat exchanger) involving
the reactor coolant system and a secondary system whose discharge is to the
environment, there exists the potential for leakage between the systems and
into the environment. However, various design features have been built into
Limerick, as well as all nuclear power plants, such that the potential for
leakage into the environment is minimal and within regulatory requirements.
These features include 1) secondary system isolation capability (both automatic
and manual), 2) maintenance of a differential pressure such that leakage will
be from the secondary system into the reactor coolant, 3) continuous-reading
radiation monitors on the secondary system discharge lines which can annunciate
- alarms and initiate automatic actions and 4) leak testing of the reactor coolant
pressure boundary to ensure a leak-tight system. These examples are not all-
inclusive, and the specific design details can vary from plant to plant.
However, the purpose of each remains the same -- to prevent the radioactive
reactor coolant from reaching the environment.
Regarding Mr. Dobson's final concern, the NRC has been mandated the responsibi-
lity for protecting the radiological health and safety of the public and the
environment, and assuring nuclear industry conformance to regulatory requirements.
To accomplish this goal, we engage in major inspection efforts on a daily basis
by assigning Resident Inspectors to each nuclear site and supplementing that
effort with Regional Inspectors.
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- The Honorable Richard Schulze 4
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. Any finding resulting from an inspection is evaluated in the context of the
NRC enforcement policy (Ccoa of Federal Regulations, Title 10, Part 2, Appendix
C). This enforcement policy authorizes the NRC to issue notices of violations,
. civil penalties, and orders to. those licensees who do not achieve the necessary
,
attention to detail-and the high standard of ccmpliance which the NRC expects.
l However, each enforcement action is dependent on the circumstances of the case.
- The NRC has taken such enforcement action in the past and will continue to do
i so when necessary and within the bounds of our lawful authority.
!
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I trust you will find this report sufficient for answering the concerns of
your constituent.
Sincerely,
i
, y (Sinned) T. A, Rehm
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William J. Dircks
Executive Director
for Operations
! Enclosure:
NRC Region I Combined Inspection Report No. 50-352/85-30;
, 50-353/85-07, excerpt
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RI:DRP DRP DRSS DRP REG ATTNY DEP RA
j Gallo/jc Collins T. Martin Starostecki Gutierrez Allan
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Distribution
EDO 1156
E00 Reading File
SECY 85-932
Docket No. 50-352
Public Document Room
Local Public Document Room
Commonwealth of Pennsylvania
W. Dircks
J. Roe
T. Rehm
V. Stello
C.-Kammerer
J. Taylor
H. Denton
G. Cunningham
T. Murley
J. Allan
R. Starostecki
S. Collins
R. Gallo
E. Kelly
K. Abraham
P. Lohaus
J. Gutierrez
T. Martin
R. Bores
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UNITE 3 STATES
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C'UCLEAR RE!ULATORY COMMISSION '
[ REGION I
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mine or caussia.esansvi.vansa e4ee
Docket Nos. 50-352--- - --- OCT 211985
50-353
Philadelphia Electric Company
ATTN: Mr. Shields L. Daltroff
Vice President
Electric Production
2301 Market Street
Philadelphia, Pennsylvania 19101
Gentlemen:
-
Subject: Combined Inspection 50-352/85-30; 50-353/85-07
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This1refers
July to the22,
- September rout'ne
1985 resident safety inspection by Mr. E. M. Kelly on .
Pennsylvania. at the Limerick Generating Station, Limerick,
The inspection consisted of document reviews, interviews, and
observation
Leitch of your of staff.
activities, and the results have been discussed with Mr. G. M.
No violations of NRC requirements were identified and no response is require .
In accordance with 10 CFR 2.790(a), a copy of this letter and the enclosures
will be placed in the Public Document Room. -
Your cooperation is appreciated.
Sincerely,
muel .C ns, Chief
Projects Branch No. 2
Division of Reactor
Projects
Enclosure: NRC Region I Combined Report 50-352/85-30; 50-353/85-07
cc w/ encl:
V. S. Boyer, Senior Vice President, Nuclear Power John
S. Kemper, Vicq President, Engineering and Research
G. Leitch, Station Superintendent
Troy B. Conner, Jr. , Esquire
Eugene J. Bradley, Esquire, Assistant General Counsel
Limerick Hearing Service List
Public Document Room (POR)
Local Public Document Roo'm (LPOR) -
Nuclear Safety Information Center (flSIC)
NRC Resident Inspector
Commonwealth of Pennsylvania
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U. S. NUCLEAR REGULATORY COMISSION
REGION I
Report Nos. 85-30; 85-07
Docket Nos. 50-352; 50-353
License Nos. NPF-39; CPPR-107 Priority -- Category C;A
Licensee: Philadelphia Electric Company -
2301 Market Street
Philadelphia, Pennsylvania 19101
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Facility Nane: Limerick Generating Station, Unit 1 & 2
Inspection Conducted: July 1 - September 22, 1985
Inspectors: E. M. Kelly, Senior Resident Inspector
J. E. Beall, Project Engineer
R. J. Bores, Technical Assistant
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D. J. Florek, Lead Reactor Engineer
T. 8. Silko, Reactor Engineer
Reviewed by: Am
J. E. Beall, Project Engi'neir }Oh14 BT
datt
Approved by:
R. M. Gallo,~ Chief, (7
dats
Reactor Projects Section 2A
ORP ,
Inspection Summary: Combined Inspection Report for Inspection
Conducted July 1 - September 22, 1985 (Report Nos. 50-352/85-30;
50-353/85-07)
Areas Inspected: Routine and backshift inspections by the resident inspector
and region-based inspectors of: activities associated with issuance of the
full power operating license on August 8, 1985 and subsequent power ascension;
followup on outstanding items and license conditions; plant tours; observation
of startup testing and review of test procedures and results, maintenance and
surveillance observations, and review of periodic reports. Also addressed are
events that occurred dur,ing the reporting period which include: corrective
action for cable tray penetration fire seal voids, contaminated water spill on
August
11.
1, a RWCU resin spill on Sept' ember 7, and a reactor scram on September
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Result: Three unresolved items were identified associated with: the potential
third offsite 33 kV power source (Detail 2.3); overtime guidelines for shift
personnel (Detail 3.4.3); and drywell temperature control (Detail 7.0). No
violations were identified.
This inspection involved 274 hours0.00317 days <br />0.0761 hours <br />4.530423e-4 weeks <br />1.04257e-4 months <br /> of onsite inspection by the Senior Resident
Inspector, the Limerick Project Engineer and other region-based inspectors.
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The inspector observed both tests at the remote shutdown panel. The
inspector monitored the pre-test briefings, operator communications,
adherence to approved test procedures, and plant response to the
imposed transients. Additional details are provided in Inspection
Report No. 50-352/85-37.
No violations were identified.
5.4 Loss' of Offsite Power Test
,
The licensee successfully completed the loss of offsite power test
(STP 31.1) on September 16, 1985. The test was initiated from about
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20% power and the unit scrammed about one minute later on low reactor
water level. The level drop was caused by the loss of power to the
~ condensate pumps which tripped the feed pumps on low suction pressure
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and caused a loss of feedwater flow to the reactor. All four unit
diesel generators automatically started and powered vital loads as
designed. HPCI initiated automatically 23 minutes into the test as
reactor level continued to decrease. As level began to increase.
HPCI was manually secured to prevent excessive reactor vessel cooldown,
and the smaller RCIC turbine pump was manually started and used to
restore level. The test was terminated as planned after 30 minutes
with the reactor shutdown, vital loaos on the diesels, and vessel
{ 1evel being controlled by RCIC.
The licensee had conducted extensive preparation for this test,
including several hours of scenarios run on the site simulator with
those shif t and test personnel taking part in the test. The scenarios
were not limited to the expected course of events, but included
sequences of events containing failures of key components such as one
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or more diesels failing to auto start. The inspector monitored the
i pre-test briefings in the Control Room and noted that they were
thorough and of high quality. The briefings were interdisciplinary
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in nature, included potential "what-if" scenario variants, and clearly
outlined the announcements which would be made to abort the test
prematurely and the major restorative actions. The importance of
good communications was stressed, and exhibited, throughout the test.
Additional details are provided in Inspection Report 50-352/85-37.
No violations were identified.
6.0 Event Followup
6.1 Contaminated Water Leak into Unit 2
l 6.1.1 Description'of Event
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On August 1, 1985, at about 10:00 p.m., a security guard
reported to Itcensee management the accumulation of water
in a pit (Unit 2 Pipe Tunnel and Access Room) near the Unit
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2 offgas holdup piping. The water level in the pit rose
from about 1/2 inch to about 18 inches on August 2. Health
physics personnel analyzed this water and found low levels
of radioactive contamination. Approximately 4 E-6 micro-
curies /cc of CO-58, and lesser levels of Co-60 and Cr-51 in
some samples were found in water sampled from the Unit 2
Pipe Tunnel and Access Room, the location where the water
accumulation was first noted. The highest concentrations
were about 4% of the 10 CFR 20, Appendix B limits for
unrestricted areas.
The licensee's investigation identified the source of the
,
water as an open 3/4 inch manual vent valve on drain piping
from the Unit 1 liquid radwaste system Equipment Drain
Collection Tank. Liquid waste was being transferred from
_ the Equipment Drain Collection Tank to the larger Equipment
Drain Surge Tank to provide additional available tank
capacity in the former. With the 3/4 inch manual vent
valve V-2104 open, liquid was apparently siphoned from the
Unit 1 Equipment Drain Surge Tank (through the piping) to
the Unit 2 Pipe Tunnel and Access Room. The source was
identified and isolated on August 2, 1985. Confirmation
that the open valve and the Equipment Drain Surge T,ank were
the cause of the leakage was based on:
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the Itcensee's review of drawings;
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cessation of leakage after valve isolation;
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activity concentrations of comparable levels, and
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a slight downward trending in the Equipment Drain
Surge Tank level after the completion of the transfer
from the* Equipment Drain Collection Tank.
6.1.2 Clean-up Activities
The licensee initiated timely actions to identify and
isolate the source of the leakage, to sample all Unit 2
sumps (several others were found to contain low levels of
contamination), and to begin the processing of the water
(estimated at 10 to 20,000 gallons) through the radwaste
processing system. The contamination in the other sumps
was traced to either pumping from the Unit 2 Pipe Tunnel
and Access Room or gravity flow from that area. No other -
sources were identified.
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All Unit 2 sump water had been transferred to the radwaste
system by the end of August 2, 1985. The sump walls and
floors were monitored for contamination. The highest level
of contamination was about 5000 dpa per 100 square centimeters
in the Pipe Tunnel and Access Room. Most of the other
sumps were about 300 dpm per 100 square centimeters. Since
these are normally " Clean" sumps, all were being decontami-
nated. Although the contamination levels were low, the
licensee posted the areas as Radioactivity Areas to
minimize possible spreading of contamination.
. The licensee's sampling program included all Unit 2 sumps,
the settling pond (last hold-up point on site before
discharge) and a low point in the discharge hose from the
Unit 2 Reactor Enclosure Floor Drain Sump. This sump has
an automatic level control and therefore would automatically
pump to the settling pond when the level rose past the trip
point. No detectable activity was found in water samples
taken from the discharge hose, nor from the settling pond.
This would indicate that no contaminated water had been
discharged to the settling pond. The licensee lifted the
pump electrical leadslof the Unit 2 Reactor Enclosure Floor
Drain Sump to assure no discharge of slightly contaminated
water from the sump could recur without appropriate
processing.
6.1.3 Corrective / Preventive Activities
The licensee closed, locked and tagged valve V-2104, although
it was not determined how or when this valve had been opened.
Numerous previous waste water transfers from the Unit 1
Equipment Drain Collection Tank to the Equipment Drain
Surge Tank had taken place with no identified leakage.
Routine surveillance of all noncontaminated sumps and
systems in response to IE Bulletin 80-10 was conducted as
recently as July 18, 1985. No contamination had been found
previously. The licensee indicated that V-2104 may have
been overlooked in the valve lineup procedures because it
was thought to be a Unit I valve, yet it does have a Unit 2
coding on the P & ID. Consequently, it was apparently
omitted from the surveillance procedures from both units.
Valve V 2104 was incorporated into the valve lineup checkoff
list on August 6 and also 16corporated in the monthly
surveillance procedure. In addition, the licensee has
directed that, in the future, all Unit 2 sumps will be
, sampled and analyzed prior to transfer to Unit I for
l . appropriate processing. Finally, the licensee has initiated
a third independent review of all the Unit 1/ Unit 2 inter-
faces in radwaste piping; this had been underway by the ,
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Limerick Radwaste Coordinator, and was scheduled for
completion by August 8, 1985. Two previous reviews of
these interfaces had been conducted of this area; one by
Bechtel and the other by PEco.
6.1.4 Summary
PECo Upset Report UR-012 dated. August 2, 1985 was reviewed.
The inspector noted that the actual radiological consequences
of this event were insignificant, although the potential
for more serious concerns existed. The licensee's actions
to (1) contain the contaminated water, (2) isolate the
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source of the leak, (3) investigate additional sources and
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the extent of contamination, (4) process the contaminated
water and decontaminate the sumps, (5) review generic
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implications and (6) implement corrective and preventive
actions were timely, thorough and appropriate. The inspector
had no further questions.
No violations were identified.
6.2 Contaminated Spill at 'Jnit 1 Reactor Building, Elevation 313
On September 7, 1985, the licensee experienced a spill of a highly
contaminated resin water mixture at elevation 313 of the Unit 1
Reactor Building. The spill was caused by the failure of a RWCU
demineralizer vent valve to close while valving the system on line.
An area about 20 feet by 30 feet was contaminated to levels of about
800,000 dpm per 100 square centimeters; no personnel contamination
occurred,
The inspector reviewed tNe radiological protection measures imple-
mented by the licensee to cleanup the spill while limiting the poten-
tial for airborne contamination and personnel exposure. The initial
steps by the licensee included tenting off the corridor surrounding
the spill, frequent air sampling and use of respirators by cleanup
personnel. The inspector reviewed the radiation work permit (RWP) .
and verified that the personnel involved in survey and cleanup activ-
ities were following RWP requirements. The Ifcensee's approach was
consistently conservative with respect to radiation protection measures
from the discovery of the spill until the corridor area was released
for general access. Additional review of this incident is provided
in Inspection Report 50-352/85-28.
.
No violations were identified.
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o NUCLEAR REGULATORY COMMISSION
i ; j WASHINGTON D. C. 205$5
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- FROM
- DUE: 11/90/85 EDO CONTROL: 001156
i DOC DT: 10/29/85
i REP. DICK SCHULZE FINAL REPLY:
i'
TO:
CARLTON KAMMERER
i FOR SIGNATURE OF: ** GRFEN ** SECY NO: 85-932
EXECUTIVE DIRECTOR
DESC: ROUTING.
i I
/ ENCLOSES LETTER FROM ROBERT G. DOBSON RE INCIDENT DENTON
AT LIMERICK PLAN ON 8/1/85 TAYLOR
> OCUNNINGHAM
j DATE: 11/05/85
j ASSIGNED TO: RI CONTACT: MURLEY
i
l SPECIAL INSTRUCTIONS OR REMARKS: '
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Rep Dick Schulze
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CORRESPONDENCE CONTROL TICKET
,
SdCYNUMBER: 85-932 LOGGING DATE "
0FFICE OF THE SECRETARY
ACTION OFFICE: E00
AUTHOR:
- Rep Dick Schulze--Const Ref
AFFILIATION: Robert Dobson
LETTER DATE: 10/29/85 FILE CODE inAR-s timerick
ADDRESSEE: OCA
SUBJECT:
August 1st incident at the Lirnerick plant
ACTION:
Direct Reply... Suspense: Nov 14
DISTRIBUTION: OCA to Ack
SPECIAL HANDLING: None
SIGNATURE DATE: FOR THE COPMISSION
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