ML20195C950

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Forwards Transparencies & Matrices Presented at 860521 Meeting at Region III Re Mod Installation Insp
ML20195C950
Person / Time
Site: Dresden Constellation icon.png
Issue date: 05/23/1986
From: Farrar D
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
1711K, NUDOCS 8606020034
Download: ML20195C950 (46)


Text

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A ~N Commonwealth Edison bh6 0- o ) One first National Plaza, Chicago, Ilknoes O A.1 dress Reply to: Post Office Box 767 Chicago, liknois 60690 PR10311Y RQiHING May 23, 1986 Eirst SymL.

Ik kT fi t+ / //P T SSZ v ud Lima S. QL-c- A -

Mr. James G. Keppler fiL %

Regional Administrator U.S. Nuclear Regulatory Commission Region III

~199 Roosevelt Road Glen Ellyn, IL 60137

Subject:

Dresden Station Unit 3 Modification Installation Inspection RC Docket Nos. 50-249 9 ear Mt. Keppler:

Per your request, enclosed please fihd copies of information presented at the May 21, 1986 meeting at Region III offices regarding the subject inspection findings. Attachment I contains copies of the transparencies utilized in our presentation. Attachment 2 contains copies of the matrices we developed during our detailed review of the individual inspection findingr:7 We will contact you at c later date to arrange a meeting at Dresden Station during which we will present the results of our ongoing investigations and proposed long term corrective actions, If you wish to further discuss the enclosed information, please contact this office.

Very tr 'ly yours, A_ :_ ~ - ,

D. L. Farrar Director of Nuclear Licetising la

' Enclosures cc: J. M. Taylor - IAE j

J. A. ZWolinski - NRR R. A. Gilbert - NRR Resident Inspector - Dresden 1711K 8606020034 G60523 PDR ADOCK 00000s!49 7 O}I G PDR $N ,,11s.fst

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o ATTTODENT 1 TRANSPARENCIES FROM MAY 21, 1986 CECO /NRC MEETING 1711K

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NRC Presentation - 5/21/85

1. Assessment of-NRC Findings C. Reed A. Process - Interdisciplinary Review "

B. Findings - Safety Significance J. Abel C. Grease Issue D. 50.59 Issue "

, 2. Identified Weaknesses D. Scott

3. Corrective Actions "

4

4. Actions At Other Stations D. Galle S. Summary C. Reed l

9 J

A f

Interdisciplinary Review Assembled Large Interdisciplinary Review Team Experienced Personel Many Backgrounds Reviewed All 100+ NRC Concerns Constructed Matrix Evaluated Accuracy, Safety Significan.ce

& Corrective Actions

. . _ . ._. _ _ . _ _ _ _ _ . _ . - - . _ E- --

Interdisciplinary Review FINDINGS 1, 22 Packages Reviewed - 20 Modifications & 2 Work Requests

2. Summary of Findings

-Improper Installation ,

-Improper Changes to Design (Field Change Reviews & Documentation)

-Inadequate Procedures and Instructions

-Inadequate Quality Assurance and Control - Indicated by Other Findings 1

Interdisciplinary Review FINDINGS

3. Examples of Findings

-Improper Installation Cable Splices -

Instrument Rack Weld

-Improper Change to Design Torus Vaccuum Breaker Environmentally Qualified Solenoid Valve Orientation

-Inadequate Procedures & Instructions Torus Vaccum Breaker Air Hose Connections and Electrical Splices

-Inadequate Quality Assurance and Quality Control Inspection of Electric Splices Prior to Placing in the Junc* ion Box 2

Interdisciplinary Review Safety Significance Evaluations

1. No Immediate Safety Concerns

.;, -Units in Cold Shutdown

-No Significant Deficiencies Identified on Operable Systems

2. Several Items Potentially Safety Significant If Undetected and Uncorrected ,

-Recirc Pipe Replacement Interference Removal Outside Scope of Work Packages

-Electrical Splices (RAYCHEM)

-Wiring Connected to Wrong Terminals 3

Interdisciplinary Review Lubrication of Pratt Valve Seats

-NRC Confirmatory Action Letter (April 13, 1983)

Implement Program to Ensure that

. Foreign Materials are not Applied to Valve Seating Surfaces

-Commonwealth Edison Response (April 22, 1983)

Restriction on Use of Lubricants on Valve Seating Surfaces Will Be In Accord With Valve Vendor Recommendations

-Henry Pratt Company Recommendations (November 1984)

" Steps Should Be Taken To See That The Valves Are Cleaned With A Solvent Instead Of An Abrasive And Lightly Lubricated With Silicone Based Grease..."

-WR 39291/2 Did Not Cause The Valves To Be Opened 4

Interdisciplinary Review 10CFR 50,59 Reviews

-Field Changes to Modification Designs Require Design Review

-Changes to Design Details Do Not Require A 10CFR 50,59 Safety Evaluation Per 3-2.

"At Operating Plant Sites Only Minor Desigh Changes Will Be Processed By FCR. Major Changes Shall Be Processed As Revised Modification Per QP 3-51"

-Example Missed Weld On Instrument Rack Structural Change Will Receive Documented Design Review Without A New Safety Evaluation 5

Identified Weaknesses I. Improper Installation A. Instructions Need Improvement B. Failure to Follow Instructions

c. Attitude - Allow Change w/o Adequate Documentation '

D. Humon Error II. Adherence to Design Change Control A. FCR System Perceived to be Too Complex B. Training Needs Improvement C. Attitude - Allow Change w/o Adequate Documentation D. Accountability Needs Enhancement III. Procedures / Instructions A. Insufficient Detail B. Lack of Acceptance Criteria C. Instructions Not Transmittea.

to Worker IV. QA/QC Overview A. QC INSPECTIONS /QA PROGRAM AUDITS NEED ADDITIONAL DETAIL ,

B. QC INSPECTIONS /QA PROGRAM AUDITS NEED ADDITIONAL COMPREHENSIVENESS

Corrective Actions

1. Review All Unit 3 S/R Modification Packages Installed This Outage By Sta. Maint. & SSC.

(Correct / Eval. Safety Significance Of Any Ident. Deficiencies)

2. Review 5 Unit 3 S/R Design Changes Installed By Contractors (Correct / Eval. Safety Significance Of Any Ident. Deficiencies)
3. Inspect 50% of Station' RAYCHEM Splices (Sample Will Include All D2 Drywell Splices)
4. Walkdown CB&I Interference Scope Boundaries
5. Discuss Design Change Problems and Expectations With All Involved Station Employees
6. Ensure Sufficient Corp. Engineering Onsite to Handle Design Change Requests
7. Increase Tech. Staff Involvement In Design Change Package
8. Resolve All Specific Deficiencies Identified By The Safety System Outage Modification Installation Inspection Team E

ACTIONS TAKEN AT OTHER OPERATING STATIONS l (QC/Z/LS/BY)

O MAY 19, 1986 NUCLEAR STATION'S DIVISION MEM0 INSPECT (10) RAY-CHEM SPLICES

+ MINIMUM BEND RADIUS

+ LENGTH

+ FIBER GLASS BRAID REVIEW (5) MOD PACKAGES (STATION, SUB-STA., CONST.,

CONTRACTOR) FOR INSTALLATION CHANGES W/0 ADEQUATE DESIGN APPROVAL REVIEW (5) MOD PACKAGES (STATION, SUB-STA. CONST.,

CONTRACTOR) FOR POST INSTALLATION VERIFICATION

+ CABLE TERMINATION WITH DESIGN DRAWINGS

+ USE OF SPECIFIED MATERIALS

+ FABo' CATION IAW DESIGN EVALUATE SUB-STATION CONSTRUCTION WORK INSTRUCTIONS AND PROCEDURES FOR COMPLETENESS o QUALIFIERS IMPRECISE INSTRUCTIONS QUICK SNAPSHOT CALIBRATION OF REVIEWERS RESULTS PRELIMINARY 9

SUMMARY

OF PRFIIMINARY RESULTS (AS OF 4:00 P.M. ON 5/20)

OTHER STATIONS REVIEW (QC/Z/LS/BY)

CONTROL OF POST ADEQUACY RAY-CHEM SPLICE INSTALLATION INSTALLATION OF SUB-STA.

INSPECTION CHANGES VERIFICATION PROC.

QUAD (11) INSP. (5) MODS - ALL OK (5) MODS - ALL OK YES ALL OK (EXCEPT POLARITY (NOT EQ HOWEVER) REVERSED ON TIMER COIL, FUNCTIONALLY OK)

ZION (6) BUTT SPLICES INSP. (5) MODS - ALL OK (5) MODS - ALL OK YES ALL OK (16) END SPLICES INSP.

(16) SHORT (8) BRAIDING EXTENDS UNDER TUBE LSCS (12) INSP. (3) MODS - ALL OK (3) MODS - ALL OK NO ALL OK (PLUS 1985 REVIEW) (PLUS 1985 REVIEW)

BYRON (20) INSP. (8) MODS - ALL OK (8) M0DS - ALL OK N/A ALL OK 1

Summary Conducting general review of modification program at all our stations .

Long term correctice actions identified within 30 days.

Will make incrovements in:

Accountability Training COMPREHENSIVENESS AND DETAIL IN QC INSPECTIONS /QA OVERVIEW LEVEL OF DETAIL IN SSC PROCEDURES 9

Attachment 2 INSPECTION FINDINGS EVALUATION MATRIX The following pages summarize the results of the detailed evaluation of the inspection findings performed by our interdisciplinary task force prior to and subsequent to the May 21, 1986 meeting at Region III. For each modification package reviewed during the inspection, the task force addressed each deficiency as characterized by the inspection team throughout the inspection and at the interim debriefing on May 7, 1986.

The review addressed whether CECO. agrees with each finding as described by the inspectors, the safety significance of each finding, and short term and long teen corrective actions. The descriptions below provide additional background on the meaning of each column heading as intended by the task force participants.

NRC Issue - This column reflects the specific findings or deficiencies identified by the inspection team for each modification. The description of each deficiency represents the findings as characterized by the inspection teen members and communicated to our staff.

CECO. Agreement - This column indicates whether Commonwealth Edison agrees with each deficiency as characterized by the inspection team. In some cases, agreement is indicated on the basis that we concur that a deficiency exists with regard to the specific finding although we may not agree with the manner in which it was characterized. These conclusions represent the collective opinion of the inter-disciplinary task force based on discussions with plant personnel involved in the inspections and a review of the documentation associated with each mod package.

Safety Significance - This column represents the actual immediate safety significance of each individual finding in the judgement of the task force members. These conclusions are based on the accuracy of the findings as described by the inspection team, consideration of subsequent testing or documentation reviews that had not yet been performed and engineering evaluations of discrepancies. Note that this column reflects our perception of the immediate safety significance on an item-by-item basis and is not intended to reflect a collective review of the findings.

1329b l

l

Cp. erective Actions - The short term corrective actions reflect actions currently completed or in progress to resolve specific deficiencies. Long term corrective actions are indicated for some items. In many cases, identification of long term actions has been deferred pending completion of our task force investigations.

NRC Concern - This column reflects the more general areas of concern into which we believe the individual findings would be grouped by the inspection team.

1329b

M12-3-84-27 End M12-3-84-23 *

(INSTALL 3-1601-50A & B SOLEMOID VALVES)

SAFETY CORRECTIVE ACTION .

NRC ISSUE Ceco AGREEMENT SIGNIFICANCE SHORT TERM LONG ' TERM NRC CONCERN A) Station Traveler says install Yes None (vendor Change Unit 2 -

Inadequate solenoid vertically, however, allows to be Mod Package Procedure solenoid is horizontal, horizontal) New MMP for Unit 3 B) Westec E.Q. checklist was for Yes None (final QA/ Jerify correct - Inadequate different valves QC documentation catalog # and Procedure review would revise check-find error) List C) Serial d's for solenoids not Yes None (final QA/ Red tags placed -

Lack of QA/QC the same as red tags in QC documentation in proper Review packages. Suspect red tags review would packages were reversed in packages. find error)

NRC asked us to verify this.

D) Schematic air line detail is Yes None(test would Correct -

Inadequate wrong. have found Drawings Procedure problem)

Inadequate Design Change E) Operational test does not Yes None (would have Revise Mod -

Inadequate include a stroke time (just says been required be- Package Test Procedure open or closed) fore startup)

Does not like second part of DOS and DIS test that verifies valve before unit s ta r t-up would open on loss of air. Does not believe step is explicit enough to verify proper operation F) Critical Drwg is wrong for M-25 Yes None - M-25 was DCR submitted -

Inadequate

& H-356. correct for M-356 Design Control

M12-3-84-27 AND M12-3-84-28 ,

(INSTALL 3-1601-50A & B SOLENOID VALVES) -

SAFETY CORRECTIVE ACTION -

NRC ISSUE CECO ACREEMENT SIGNIFICANCE SHORT TERM LONC TERM NRC CONCERN i

G) HMP States no existing drawing Yes None - M-25 was DCR submitted - Inadequate Design is affected by Mod. However, correct for M-356 Control P&lD's are a ffected.

H) Poor workmanship on air tubing No None - reinspec- - -

Improper installation to the 3-1601-20B valve. tion indicates no air flow "" #9"' " 0^

restriction I) U-2 solenoids installed correctly Yes None - installa- Correct Task Force Improper however, package did not reflect tion within drawings Recommenda- Installation

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changes in packages. vendor tions tolerances

, M12-2/3-85-34 t *~ j[}3 (PROVIDE A FLANCED PORTHOLE BETWEEN UTIT 2 6.3 RX ELDC FOR DECON HOSES)

SAFETY CORRECTIVE ACTION .

NRC ISSUE CECO AGREEMENT SIGNIFICANCE SHORT TERM LONG TERM NRC CONCERN A) Questioned that this Hod should No None- Not secon- -

Inadequate be safety related. dary cont. bound- Design Change ary and proper review by SNED B) Mod package lacks details. No None - details - -

Inadequate Procedure (e.g. no weld sizes, grout spec, were included pipe size, etc.)

C) S&L technical evaluation in Yes None - based on Engineering -

Inadequate package only discusses a 4" engineering Evaluation Design Change diameter core bore in wall. evaluation However, a 5" core bore was installed.

Exact location on wall where hole is installed is different than where referenced in pack-age.

D) No explicit veld direction Yes None - not Repair Weld -

Inadequate Procedure given (sketch says 3/8" weld, structural or however 1/8" welds used). pressure boundary Inadequate QA/QC I"" I'*"*"'

weld E) S&L asks to mention a REBAR HIT, Yes None - hits Document liits, -

Inadequate Procedure however, no mention of Rebar in within engineer- Engineering package. ing guidelines Evaluation F) Safety Evaluation made to Yes None - based on New Safety -

Inadequate 50.59 approve 4" holes not 5" holes. engineering and Evaluation, Review safety evalua- Engineering tions Evaluation

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RPR INTERFERENCES M12-3-85-17 SAFETY CORRECTIVE ACTION -

NPC ISSUE CECO AGREEMENT SIGNIFICANCE SHORT TERM LONC TERM NRC CONCERN A) 2 piping runs did not match No None - piping Complete -

Improper Instal-CB&I/Impell sketch drawings matches drawings verification lation

  1. 181 and #187 on piping run B) No spring hanger setting on Yes None - final QC/ Received -

Inadequate Procedure Drwg #181. QA documentation hanger review would find setting error C) Observation; cut in a frame Yes None (planned - - -

needs repaired. to repair)

D) Slope conditions on drains Yes Potential 1. Evaluate -

Inadequate Design not defined technical Change significance 2.Walkdown

& evaluate lines E) CB&1 sketches must be approved Yes None - sketches - -

Inadequate Procedure before being used. (Our comment are approved was that Impell does approve the sketches).

F) CB&I worked outside their scope. Yes Potential 1. Audit of -

Improper Instal-work within lation packages

2. Umbrella walkdown &

commitments 3.Fix specific items

M12-3-85-SO-D/C COOLINC WATER PUMP-SUCTLON PRESSURE CAUCES .

SAFETY CORRECTIVE ACTION NRC ISSUE Ceco ACREEMENT SIGNIFICANCE SHORT TERN IANG TERN NRC CONCERN A) A bronze valve was mentioned Yes None - S & L DR written Task Force Inadequate Design in package, however, a brass permits either Recommenda- Control valve was actually used. No type valve tions documentation was changed in package to reflect this.

B) A Seismic Evaluation for the No None - (documented Will complete -

Inadequate Design addition of this piping was through 50.59) seismic eval. Control not addressed.

C) Package states a rising stem Yes None , DR written -

Inadequate Design valve to be used however, a Control non-rising stem valve was actually used. Not documented.

D) A 2-2 \" socket was used to No (addressed in None - -

Inadequate fit up on an 8" pipe. No men- general welding Procedure tion of grinding was included procedure)

, in package.

E) NRC found the pressure gauge Yes (due to None Walked line -

isolation valve open, however surv.) and found when we visited the plant, found valve in the valve closed. proper positior

LEAD SillELDING REVIEWS , .

SAFETY CORRECTIVE ACTION ~

NRC ISSUE CECO AGREEMENT SIGNIFICANCE S110RT TERM LDNC TERM NRC CONCERN 1.

Lack of lead installation procedure Yes None -

Revice DAP Inadequate Design doezn't ensure analysis is valid. 12-12 Control

2. Write DTS Nerd a 50.59 analysis for each No None - Procedure - -

Inadequate Design istallation is reviewed per Control 50.59 I

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M12-3-83-29 (MODIFY LPCI CONTROL ROOM SUCTION VALVES 3-1501-5A, B C & D)

  • SAFETY CORRECTIVE ACTION .

NRC ISSUE CECO ACREEMENT SIGNIFICANCE SHORT TERM LONC TERM NRC CONCERN

1) Modification approval sheet Yes None - FSAR Revise Mod Revise DAP Inadequate and SNED Mod letter do not agree design require- approval 5-1 Design Change for T.S. and FSAR categories. ments met sheet

M12-3-84-9 (ANTI-HAMME3ING PREVENTION ON C.S. 1402-25A & B VALVES)

  • SAFETY CORRECTIVE ACTION .

NRC ISSUE CECO AGREEMENT SIGNIFICANCE SHORT TERM LONG TERM NBC CONCERN

1) Need a drawing change to a Yes None - !!od Submit DCR Task Force Inadequate cable tab. Installed Recommenda- Design Changes correctly tions
2) MOV 3-1402-25B incorrect cable Yes None (Cable I.D. Correct field Improper ID # for a wire in the field. problem not part label installation of modification
3) MOV 3-1402-25A splices exceed Yes ' None- No actual 1. Straightened Task Force Improper the minimium bend radius. damage splice Recommenda- installation tions
2. Ray Chem Inadequate Procedures Inspection ,

Program Inadequate QA/QC h

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M12-3-85-26 (RPR Elsctrical 1 terforcrcco)

  • SAFETY CORRECTIVE ACTION -

MRC ISSUE CECO AGREEMENT SIGNIFICANCE SHORT TERM IANG TERM NRC CONCERN J

1) ECTP does not have acceptance Yes None - equipment -

ECTP's to be Inadequate Procedure criteria for motors. meets design revised requirements

2) 2 wires were found terminated Yes None - equipment Fix termina- -

Inadequate Design j on the same terminal connection operable. tions Changes in the MOV 3-1501-228.

3) Annaconda T.W. wire was found No None - not E.Q. - -

Inadequate Design being used internally in the because of short Changes Mov 1001-58. oper, time

4) In C.E. Package 042 field cable No None - - -

76902 not striped to NRC sat'is fac t ion. (NRC comment)

5) In C.E. Package, a T/C ground Yes None - T/C still Improve Improper installation wire end crimped over insulation operable installation

, per NRC. per this Mod Inadequate QA/QC involvement

6) In C.E. Package, a concrete ex- No None - minimum Verify -

Improper installation pansion anchor extended too far embedment embedment out of embedment by NRC view- verified to be Inadequate QA/QC point. correct involvement

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M12-3-83-38 & 39 (Trcnealttcr Repiteemert fcr EVLIS Mod)

  • SAFETY CORRECTIVE ACTION
  • NRC ISSUE CECO AGREEMENT SIGNIFICANCE SliORT TERM LONC TERM NRC CONCERN
1) liardware okay by Pope. N/A - - -
2) 50.59 generic checklist problem Yes None - intent of , QA Manual - ' Inadequate Design in Q.A. Manual. ,

50.59 met L revised Contr01

3) Mod approval form and SNED Yes None - FSAR Revise Mod Revise DAP Inadequate letter does not agree. design require- approval 5-1 Design change ment met sheet Change DAP 5-1
4) A) DAP 5-1 Form 5-lD (Fire Yes None - no fire Form Signed Task Force Inadequate Protection Checklist) not protection Recommenda- Procedures signed before start of work. concerns associa- tions ted with this MOD B) Need Form 5-ID re-written Yes None - same as 4A . DAP Form to be to provide blanks for user revised to sign-off.

Hl2-3-03-30 (MODIFY C.S. CONTROL ROOH SUCTION VALVES 3-1402-3 A G 'd)

SAFETY CORRECTIVE AC'f1W NRC ISSUE Ceco ACTEGENT SIGNIFICANCE SilORT TERM l 1.ONC TERM NRC CONCERN

1. Mod approval sheet and CNED Yes None - FSAR design Eevise Mod Revise DAP 5-1 Inadequate Mod letter do not agree, require:nents net approval sheet Design Change
2. Wires landed incorrectly - Yes None- Testing Wiring Task Force Improper traveler and drwg's correct, how- would have found corrected Recommenda- Inetallation ever, mistake by workman in the probleme tions Inadequate Q W field functional test and Q.C. .I"' I'*"*"E release had not been completed yet
3. An FCR should have been Yes None - does not Issued FCR -

Inadequate incorporated for this job. (No af fect Hod , Design Change crange-bik cable)

4. ERC believes this Hod should No None - based on Engineering -

Lack of 50.59 be reflected in the FSAR. engineering evaluation ,

Review evaluation e

M12-3-84-27 & 28 (INSTALL S0 3-M01-50A E4 0 VALVES)

SAFETY CORPJltCTIVE ACTION -

NRC ISSUE CECO ACREEMENT SIGNIFICANCR 'S!! ORT TERM IENG nEM NRC CONCP.RN

1. A) E.Q. splices over braided Yes None (Raychem to Re-spliced Task Force Improper dastallation jacket. discuss Monday) Recommenda-tions Inadequate QA/QC B) Conductor showing through Yes Potential Conducto r Task Force ' Improper ins t allation splice. . respliced Recommenda-Inadequate Procedure tions Inadequate QA/QC C) Marks on splice from codulet. No None - splice intact D) Exceeded Ray Chem minimum Yes Potential Conductor Task Force bend radius. respliced Recommenda-tions O N

_. HI2-3-84-38 (SEISMIC SUPPORT 2208-5 & 6 RACKS) -

SAFETY CORRECTIVE ACTION ,

NRC ISSUE CECO AGREEMENT SIGNIFICANCE SIIORT TERM LONC TERN NRC CONCERN

1. FCR 042-17 written to change No None - change - -

Inadequate Design configuration due to inter- reviewed per QA Changes fe rences. Does SNED review Manual and should a new 50.59 be written?

2. M-3620 Sheet 3 of 3 from A/E No None - M-3620 - -

Inadequate transmittal referenced for Sheet 3 does not Procedures Unit 2 but not for Unit 3 apply to Unit 3

3. M-3620 Sheet 2 of 3 says use Yes None - engineering NCR started to Task Force Improper ASTM-36 tubing, however not evaluation correct draw- Recommenda- installation possible. ing and mod tions letter Inadequate Design Changes Inadequate QA/QC involvement
4. On 2203-8 rack, a weld was Yes None - engineering Weld installed Task Force Improper installation missing. evaluation Recommenda-tions Inadequate QA/QC involvement

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H12-3-84-49 & 50 (E.Q. East and West LPCI Room Cooler Motors) .

CECO SAFETY CORRECTIVE ACTION NRC NRC I^ SUE ACREEMENT SIGNIFICANCE SHORT TERM LONG TERP CONCERN

1) Hotor mounting in question; Yes None - engineering Engineering -

Inadequate Design nn detail in package. evaluation evaluation Changes

2) Ray Chem in-line tubing for Yes None- Tag lost but - -

Inadequate QA/QC uotor leads had no material part is listed on doc. involvement c rts in package. Review checklist with Q.A. Inspector said he rcviewed certs to verify proper size. No red tags crn be found.

3) MMP seems to indicate all 3 No None - Necessary - -

Inadequate Design leads should be repaired. work accomplished Changes However, intent was only to do damaged lead.

4) Fcr the East Room Cooler M12-3-84-50 A) One belt found off/other Yes None - redundant Belt -

Improper inatallat ion belt okay. belts reinstalled Inadequate QA/QC involvement B) NRC says we need matched No None- Surveillance belts.

Inadequate Design would catch this Changes C) Poor operation practice No None- Not required -

N/A noted-coolers not taken per Tech. Spec.

00S for belt problem.

Observation.

M12-3-84-49 & 50 (E.Q. East End West LPCI Room Coolcr Motcro) ,

CECO SAFETY CORRECTIVE ACTION NRC NRC ISSUE ACREEMENT SIGNIFICANCE SHORT TERM LONG TERM CONCERN

4) Continued-D) Flexible conduit not No None - not a design Red tag re- -

Improper installa t ion replaced. requirement in the moved from Inadequate QA/QC Mod package E) Connection for conduit Yes None- Conduit cennot - -

Imprope r installat ion loose not per Traveler come off I dequate QA/QC involvement F) Per Westinghouse Manual. No None - engineering Engineering Improper installation Raychem not okay for evaluation evaluation splicing but should have Inadequate OA/QC g y,3, ,,,

used 3M Scotch Tape.

C) Splice kit installed on No None - eugineering Engineering -

Improper installation glass braided tubing not evaluation evaluation per 2nd MMP. nadequate QA/QC involvement II) Q.C. verification did not No None - FB1P instal'la- - -

Inadequate QA/QC follow MMP. tion was properly involvement QC verified I) For both M12-3-84-49&50

1. Q.C. inspector not No None - The 2 QC - -

Inadequate QA/QC aualified per ANSI Inspectors meet ANSI involvement 45.2.6 45.2.6 requirements 2 Not all Q.C. trained Yes None- QC inspector - -

Inadequate QA/QC ca Raychem splices qualified per ANSI involvement 45.2.6 requirement

M12-3-84-49 & 50 (E.Q. East cnd We2t LPCI Room Cool;r Mot rc) ,

'CE E ~ SAFETY CORRECTIVE ACTION NRC NRC ISSUE ACREEMF.NT SICHIFICANCE SHORT TERM LONC TERM CONCERN

4) Continued-J) NRC does not like how Yes None - No evidence of Memo issued -

Inadequate Procedures Attachment "B" are/was any T.S. violations to Operating filled out. Station Memo okay for T.S. but not sufficient for caution 6tstement.

Found error in T.S.

sections on 49 pkg.

K) Form 5-lD not properly Yes None - No fire Form signed Revise Inadequate Procedures signed. Protection concerns DAP 5-1 associated with this Mod L) Static Seismic Analysis No None - Engineering Engineering -

Inadequate Design not correct. evaluation Evaluation Changes M) No hold points for E.Q. Yes None - Splices -

Task Force Inadequate Procedures splices for motor lead installed adequately Recommenda-repair splices I adequate QA/QC tions involvement N) No acceptance criteria Yes None- Exceeds IEEE -

ECTP's to be Inadequate Procedures for Megger. Results, etc. Standard revised in Traveler.

O) No Polarization Test Yes None- Not applicable Engineering ECTF's to be Inadequate Procedures in Traveler as required for small motors Eval ua tion revised for E.Q.

P) Bolted cannection splice Yes None - Splice sealing Opened -

Improper Installation over wire braid area unaffected splice -

found no problems

M12-3-84-8 (HGA 11 RELAY)

SAFETT CORRECTIVE ACTION NRC ISSUE CECO ACREEMENT SIGNIFICANCE SHORT TERM LONC TERM NRC CONCERN

1) Construction test signed off Yes None - Test Const. Test -

Improper installation by maintenance man in two spots completed Corrected

, j where only one spot should have satisfactorily been signed. involvement

2) Finding on wiring connection No None- M12-3-82-27 Correct -

Improper installation being wrong so that if M12-3 has steps to put construction 27 was completed would disable wire in proper test (new MMP) Inadequate Design e HCA 11 relay. place Change Inadequate QA/QC involvement

3) Traveler step signed off for Yes None - Construc- Correct -

Improper installation item 2 above but not correctly ~

tion test would Traveler (new completed. catch MMP)

Inadequate Design Change Inadequate QA/QC involvement

4) Referenced copies of drawings in Yes None - Not used Remove sketch -

Improper installation

- panels not all changed properly as a design - Revise MMP as signed off in traveler document Inadequate QA/QC involvement

5) Inadequate Design Change Yes None- Corrected DCR submitted Task Force Inadequate Design Control - 12E3757D had error in field. Recommenda- Change but no FCR written. tions G) Unapproved notes on drawings No None - Notes were Document Task Force Inadequate Procedures to help workmen do the job / aids to clarify approval of' Recommenda-rotes should be on MMP. drawing notes (new tions MMP)

Ml_2-3-84-8 (HCA 11 RELAY)

SAFETY CORRECTIVE ACTION NRC ISSUE Ceco AGREEMENT SIGNIFICANCE SHORT TERM LONG TERM NRC CONCERN

7) Not all applicable drawings in No None - Instruc- - -

Inadequate Design package and NRC feels job should tions and drawingt Change have been re-drawn showing as- Provided informa-built conditions. Traveler does tion needed for not list all drawings. installation Inadequate Procedures

8) Traveler does not give explicit No None - See item 6 Document Task Force Inadequate Procedures details. approval of Recommenda-notes (new tions IDIP)
9) Potential non-compliance for No None - Drawing -

Inadequate Design oo DAP 2-7 Attachment "A" for 12E2758C Rev. Y Change drawing 12E-2758C Rev. Y. does not exist 9

6

M12-3-83-40 (EVLIS AND TESTING MOD)

SAFETY CORRECTIVE ACTION NRC ISSUE CECO ACREEMENT SIGNIFICANCE SHORT TERM LONC TERM NRC CONCERN

1) 50.59 problem as stated in Yes None - Intent of QA Manual Inadequate Design M12-3-83-38 and 39. 50.59 met revised Control
2) Step 10 of Traveler dated 2-6-85 Yes None - No signifi- -

Generate new Inadequate Procedures ctates all work to be completed cant installation procedures by approved SSC procedures. de ficiencies However, SSC has no procedures except for Ray for all evolutions. Chem splices e.g., cable pull procedure which measures tension Install cable tray Run raceways and termination etc.

3) In 3-2202-73 A & B have NSR yes None - installa- ECN to be -

Inadequate rnd SR cables not 6" separation tion not finished issued Design Changes yer

4) Per 12E-2103A, Rev. E Note 5 Yes None - Requirement NCR issued - Inadequate Procedures cays record pull tension of not necessary (on cable cable. SSC does not have a based on installa- pulls)

. procedure to do this nor was it tion methods documented.

5) Stickers on conduits too far Yes None - Cable Install more -

rpart greater than 15 feet. identification stickers Improper installation maintained Inadequate QA/QC involvement

6) Supports greater than 42" from Yes None - Engineering NCR issued -

Improper installation conduit bends. evaluation Inadequate Design Changes Inadequate QA/QC involvement

M12-3-83-40 (RVLIS AND TESTING MOD)

SAFETY CORRECTIVE ACTION NRC ISSUE CECO ACREEMENT !iIGNIFICANCE SHORT TERM LONG TERM NRC CONCERN

7) Improper grounding from conduit Yes None- Personnel Ground clamps Task Force Improper installation to cable trays. safety issue to be in- Recommenda-stalled tions Inadequate QA/QC invo'rement
8) In panel 3-2352 and 3-2389 A & B Yes None- Not in Change fit- Task Force Improper ins tallation cplices did not conform to service tings and Re commenda-vendor requirements. Vendor Inadequate Procedures resplice tions requirements found in 83-40 Inadequate QA/QC but not in 83-38. Raychem involvement (plice approximately 3" long not 6" as required.
9) DFPP 4175-1 Rev. O does not reflect T.S. 3.12.4 and procedure in package. However, DFPP 4175-1 Rev 1 does reflect T.S.

A) Concerned that temporary No None - Engineering Engineering -

Inadequate Design firestop using Kaowool is evaluation evaluation Control not adequate.

' B) This should be a temporary No None - Proce- - -

mod using a 50.59 review. durally controlled

10) No Q.C. hold points for E.Q. Yes Not in service QC hold pts Task Force Improper installation cplices as required by DAP 15-1. yet on splice Recommenda-NRC feels this is a general Inadequate QA/QC rework tions involvement problem with SSC work.

M12-3-83-16 (MSL RAD MONITORS)

SAFETY CORRECTIVE ACTION NRC ISSUE CECO AGREEMENT SIGNIFICANCE SHORT TERM LONG TERM NRC CONCERN

1) T.S. reference in DAP 15-1 Yes None - Applicable Correct Att. -

Inadequate Attachment "B" is incorrect. Tech Spec not "B", Memo to Procedures ,

required at this Operating time

2) DAP 5-1 Form 5-ID not filled out Yes None - No fire DAP form being -

Inadequate Procedures protection revised concerns associa-ted with this Mod

3) Installation test needs to be No None - ANSI N45. Check ANSI -

Inadequate Procedures initialed not checked per ANSI 2.3 does not standard ctandards. require each step to be initialed

4) NRC asked to see seismic qual. NA - - -

documents.

5) Needs acceptance criteria for test.

A) MSL Mon. No None - GE func- - -

Inadequate Procedures tional test required by Spec T-3315 R) Recorder Yes None - Not in Revise Test -

Inadequate Procedures service

6) No reference in mod installation Yes None - Surv. to Procedure - Inadequate Procedures test for proper "Q" setpoint & be performed being written trips and settings. before S/U for "Q"

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CENERAL PROBLEMS SAFETT CORRECTIVE ACTION

  • NRC ISSUE Ceco ACREEMENT SIGNIFICANCE SHORT TERM LONG TREM NRC CONCERN A) In 903-33 & 32, \" dia. spare Yes None - Workmanship Remove cable -

Improper installation cable needs to be removed or secured and labeled. -

D) No 00S tags on this cable No None - Not within - -

mentioned above. 00S scope C) 903-32, no covers on trays Yes None WR written to -

(Panduit) replace covers D) Paper combustibles in 903-32. Yes None Paper -

removed E) 14 safety related fuses removed Yes None OOS tag to be -

but only a few had 00S tags placed on connected to fuses. Other fuses - memo DOS tags just on bottom of panel issued to Operating Dept F) Terminal block broken in 903-33. Yes None- Just cracked WR written to -

Work request written to repair repair terminal block C) Bad splice in 903-33 panel. Yes None WR written to -

replace cable- no splice

E12-2-84-14 -

(nuTT 7 ccCW PihP VAlH_T canI RR BRUFIPC M VALVRE)

SAFETY CORRRCTIVE ACTION NRC ISSUE CECO ACREEMENT SIGNIFICANCE SHOET TERM IANG TERM NRC CONCERN A) A/E drawing reflects as-built Yes None - Engineering Engineering Task Force Inadequate Design casembly after Mod was installed evaluation evaluation and Recommenda- Change Cooler l's were backwards on drawings three of the dimensions were not correctly shown on as-built drawing.

B) No direction in package was Yes None (valve in- - -

Inadequate Civen for proper orientation of stalled properly) Procedure valve in pipe.

C) Operating procedures should Yes None - Engineering Engineering -

Inadequate address perferred flow direc- evaluation evaluation Procedure tion e

WORK REQUESTS ON 3-1601-50A & C VALVES /1601-20A & 20B -

SAFETY CORRECTIVE ACTION NRC ISSUE CECO AGREEMENT SIGNIFICANCE SHORT TERM LONC TERM NRC CONCERN A) Bolt problem not correctly Yes None - Proper DR written Task Force Inadequate documented in package. Used bolt was Recommenda- Design Change

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correct bolt however, not installed tions properly documented. Inadequate

. Procedure O) Weld was different than stated Yes None - Weld does Finish Task Force Improper Installation on weld MAP- not affect safety Weld Recommenda-function of valve tions C) Work request states to apply No None - CAL - -

Inadequate cilicone grease to seats. NRC not violated Procedure concerned this is the same issue as the MSIV grease issue.

D) NRC feels this work request No None - Classified - -

Inadequate Design chould be a Mod. in accordance Control with QA Manual E) Cidn't stake all bolts as W.R. Yes None - Document Task Force Inadequate cLates. Staking was not Impractical Change in Recommenda- Design Change practical, however not Package tions documented.

F) W.R. needs a 11-7A or 11-5A No None - Proper - -

Inadequate for bolts. bolt was Procedure installed C) No sign-off for system No None - (package - -

Inadequate cleanliness. had not been QA/QC closed out & Involvement valve not opened)

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