ML20009C056

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Forwards Updated LER 81-005/03X-L.Deviation Rept Encl
ML20009C056
Person / Time
Site: Dresden Constellation icon.png
Issue date: 06/16/1981
From: Scott D
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009C057 List:
References
81-409, NUDOCS 8107200226
Download: ML20009C056 (2)


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[ 7N Commonrxith Edison Dr dm hucleu Poyssr Station

[h7/ c jf Morris, filinois 60450 Telephone 815/942-2920

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  • y June 16, 1981 'a d f

-DJS LTR #81-409

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James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III \/M/ ,N . ,]I] IQ' U.S. Nuclear Regulatary Commission 799 Roosevelt Road Glen Ellyn, IL 60137 i.

Reportable Occurrence Report #81-05/03X-1, Docket #050-237 is being submitted to your office in accordance with Dresden Nuclear Power Station Technical Specification 6.6.B.2. (b), conditions leading to operation in a degraded mode permitted by a limiting condition for operation. The reason for the revision is to update the cause de-scription and corrective actions taken and future action portions of the Licensee Event Report.

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D. . Scott Station Superintendent Dresden Nuclear Power Station DJS/lg f Enclosure cc: Director of Inspection & Enforcement I Director of Management Information & Program Control

! U.S. NRC, Document Mgt. Branch File /NRC Jhs

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@1 4M 8107200226 810616 l' gDRADOCK 05000237

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DEVIAT10N REPORT

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Revision #1  !

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Commonwealth Etiisan su UNIT YEAR NO.

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, 17 Il T l TLE O F CEVIATICN CCCU RRED l-17 91 1100 Failure of 2-1601-23 Valve to Pass LLRT am we SYSTEM AFFECTED PLANT CON 0iTIONS TESTING 1600 Pressure Suppression L_J uccEShutdown zwp e w- i 0 . tcAotuwe 0 YES NO ,

CESCRIPTICN CF iVENT During LLRT of Drywell and torus vent, 2-1601-23 valve failed to hold pressure. Leak Rate i

determined to be 1715.55 SCFH DESCRIPTION CF CAUSE Unknown at this time OTHER APPLICABLE INFORMATION Reactor in cold shutdown Primary Containment not required.

! EOUlPMENT C YES OR NO. 'WR NO.

FAlt,URE N/A Dll279 K. R. Zirwas 1_17_gi i (NO PART 2 ) OPERATING ENGINEERS CCMMENTS  ;

The measured leakage exceeded the limit for a single isolation valve (29 38 SCFH. T.S. 4.7.A).

_  ? leakage was determined to be through the 2-1601-23 valve toward the drvwell. - 1 TYPE OF CEVI ATION EVENT OF POTENTI AL l SAFE *Y- )

TECH SPEC l NCN-REPORTABLE ANNUAL RELATED l REPORTABLE OCCURRENCE PUBLIC INTEREST v!OLATION OCCURRENCE REPCRTING WR ISCUED i f ;4 ggy 10CFR21 YES YES y

~ l X l 30 C AY NO NO hTICN __,

l RE?ORTABLE CCCUPRENCE ACTICN ITEM NO. P9CMPT CN-SI TE NOTI FI CATICN NUMBER l R. M. Ragan 1/22/81 1200 Xti5 81-05/03X-1 Tl RE CATE ME TI TLE CATE TIME l

24-HOUR NRC NOTI FI CATION I RCMPT OFF-SI TE NOTI FICATION

'PH N/A F. A. Palmer 1/22/81 1:33 REG ON lli OATE lME TI TLE DATE TIME TGM N/A REGIGN III a CCL CATE TIME Tl TLE CATE TIME RESPCNSI SLE COM' ANY O FFI CER INF0P9ED OF 10 CFR 21 "Nor-icNs 2NO wrio occ0=* 'O Not

  • T I TL E CATE 'W REvi Ew AND COMPLETED . John W. Wuici,a 1/20/81 CP E R AT I NG iNG I N t-H CATE ACCE?TANCE SY STATICN REVfEW

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RESOLUTI ON APDPOVEC ANO eet for signatures AUTHORI ZED FOR CI STRI BUTI ON d69 '" / d/ F.

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