05000237/LER-1981-005-03, During Local Leak Rate Testing,Measured Leakage of Single Isolation Valve Exceeded Tech Specs.Caused by Normal Deterioration of Valve Seat. Valve Replaced

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During Local Leak Rate Testing,Measured Leakage of Single Isolation Valve Exceeded Tech Specs.Caused by Normal Deterioration of Valve Seat. Valve Replaced
ML20009C065
Person / Time
Site: Dresden Constellation icon.png
Issue date: 06/15/1981
From: Zirwas K
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009C057 List:
References
LER-81-005-03X, LER-81-5-3X, NUDOCS 8107200232
Download: ML20009C065 (2)


LER-1981-005, During Local Leak Rate Testing,Measured Leakage of Single Isolation Valve Exceeded Tech Specs.Caused by Normal Deterioration of Valve Seat. Valve Replaced
Event date:
Report date:
2371981005R03 - NRC Website

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U. S. NUCLEA3 ff EGULATO3Y COMMISSION A

ORT hed ous Report LICENSEE EVENT REPORT Date - 01/29/81 CONTROL SLOCK: l l

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REPORT DATE do EVENT CESCRIPTION AND PROBA8LE CONSEQUENCES to I 2 I I uring local leak rate testing of con ainment tent line, the measured leakage was D

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) 13l l1715.55 SCFH which exceeds Tech. Spec. 4.7.A for single iso'_ation (29.38 SCFH).

3,,; l Investigation showed leakage through A0-2-1601-23.

No leakage was detected through g jany other valve. The safety significance was minimal since all leakage was con-g

) is I Itained in the venC line. Similar Events:

50-249/80-07. Health and safety of the l7l{pblic was not affected.

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CAuSE DESCRIPTION AND CCRRECTIVE ACTICNS The g ; valve was replaced and local '.eas Rtc tested satisfactorily. No further action yrequired.

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PART I l TITLE OF EVENT OCCURRED 1-17-81 1100 Failure of 2-1601-23 Valve to Pass LLRT DATE T lite REASON FOR SUPPLEMEffTAL REPORT Update Cause Description and Corrective Actions.

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