ML17342A949

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Special Rept:On 860930 & 1001,schedular Exemptions for Safe Shutdown Mods Expired Resulting in Fire Protection Impairments.Caused by Number of Mods Being Performed. Compensatory Measures Described in 851011 Ltr in Place
ML17342A949
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 10/06/1987
From: Woody C
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
L-87-403, NUDOCS 8710130247
Download: ML17342A949 (7)


Text

REGULATORY IFORMATION DISTRIBUTION SY M (RIDB>ACCESSION NOR: 8710130247 DOC.DATE: 87/10/06 NOTARIZED:

NO DOCKET 0 FACIL: 50-250 Turkey Point Planti Unit 3i Florida Poeer and Light C 05000250 50-251 Turkey Point Planti Unit 4i Florida Poeer and Light C 05000251 AUTH.NAME AUTHOR AFFILIATION WOODY'.O.Fl or id a Poeer 5 Li g h t Co.REC IP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)BUH JECT: Special rept: on 860930 5 100ii schedular exemptions for safe shutdown mods expired resulting in fire protection impairments.

Caused bg number of.mods being perFormed.

Compensatorg measures described in 851011 ltr in place.DISTRIBUTION CODE'006D COPIEB RECEIVED: LTR l ENCL~SIZE: TITLE: OR/Licensing Submittal:

Fire Protection NOTES: REC IP IENT, ID CODE/NAME PD2-2 LA McDONALDe D INTERNAL'RM/DAF/LFMB NRR/DEBT/*DS OGC/HDB2 EXTERNAL'PDR NBIC COPIES LTTR ENCL 1 0 1 1 1 0 1 1 1 0 1 1 1 1 REC IP IENT ID CODE/NAME PD2-2 PD NRR WERMEILi J NRR EST/PSB 01 NRC PDR COPIEB LTTR ENCL 5 5 1 0 1 1 1 1 1 1 TOTAL NUMBER OF COP IEB REQUIRED: LTTR i&ENCL 12 tI I I t I}'g IWQ W~I g wt!ll Wf 4"'f r,tt~}I>>X}I It II Q I NWI C.~1 j}}lt'C', W~I'L gott)II W Il'k II I I WP I I I$tt I, It W h}c W s~',I t ISW'E II$Ii It W}'tt}I'I}1 C'>>,}$I l.it.W P.O.BO 000, JUNO BEACH, FL 33408.0420 ~Ng~OCTOBER 0 6 1SST L-87-403 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.205S5 Gent I em en: Re: Turkey Point Units 3 and 4 Docket Nos.50-2SO and 50-25 I Special Report-Breached Fire Barriers and Other Fire Protection S stem Im airments In accordance with Technical Specification 6.9.3 the attached Special Report is provided for your information. Should there be any questions on this information, please contact us.Very truly yours, C.O.Wo Group President Nucl ear Energy COW/TCG/gp Attachment cc: Dr.J.Nelson Grace, Regional Administrator, Region ll, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8710'0247 87100b,'PDR ADOCK 05000250 8 PDRg SDF I/004/I an FPL Group company ~o 4~~I r'II if H f V4 Ih h I 4 H HH fr 4'lH R~R I'I I II~II~~~4 4 4 SPECIAL REPORT OCTOBER 6, 1987 FIRE PROTECTION SYSTEM IMPAIRMENTS REQUIRING NRC NOTIFICATION ~Pur ese: Technical Specification (TS)3.14.5.b requires the submission of a report to the NRC if a non-functional fire barrier penetration is not returned to functional status within 7 days.TS 3.14 states that certain other conditions also require NRC notification. In accordance with the above requirements, this special report is being generated in order to notify the NRC.This report will be updated on a 30 day basis.Event: The plant has been and is continuing to implement modifications in accordance with Appendix R Alternate Shutdown requirements and other unrelated requirements. The schedular exemptions for the Safe Shutdown modifications, which outlined the alternative compensatory measures to be taken when a barrier is breached, expired on September 30, 1986, and on October 1, 1986.Upon the expiration of the exemptions, the compensatory measures as described in Attachment 1 of our letter L-85-386 (dated October 11, 1985), are continuing to be in place until the Safe Shutdown modifications are complete.Impairments incurred during Alternate Shutdown modifications are governed by the Technical Specifications or the exemptions, as applicable. Other impairments are governed strictly by the Technical Specifications. Cause and Corrective Actions: The major cause of the impairments is performed. Due to the volume of work reporting the impairments in this one basis.The impairments reported this present time, but were open in excess requiring NRC notification. the number of modifications being being performed, the plant is report, rather than on a case-by-case month are either open or closed at the of the time period permitted without This report includes impairments which were: e 1)opened prior to October and 2)stayed open for longer than the time permitted by the Technical Specifications, and 3)are either still open or were closed prior to October.The plant continues to implement the compensatory measures as applicable.

FIRE PROTECTION SYSTEM IMPAIRMENTS OPENED SINCE AUGUST REPORT WHICH HAVE BEEN OPEN FOR LONGER THAN TECH SPEC LIMITS Imp/i Description Open Closed 87-0330 87-0331 87-0332 87-0328 Raceway Protection 09/15/87 Penetration Seal 98K-E001 09/22/87 Penetration Seal 098N-E035 09/23/87 Fire Barrier 72-S 09/01/87 09/14/87 FIRE PROTECTION SYSTEM IMPAIRMENTS CLOSED SINCE AUGUST REPORT BUT WERE OPEN FOR LONGER THAN TECH SPEC LIMITS Impd 1004 1176 1146 87-0308 87-0327 87-0323 Description Penetration Seal Zone 39 Water Suppression System.Fire Door 106.2 Raceway Protection Penetration Seal'106F-3-69 Penetration Seal 097F-E014 Open 10/17/86 08/09/87 07/24/87 06/30/87 07/31/87 07/30/87 Closed 09/30/87 09/19/87 08/11/87 09/03/87 09/04/87 09/04/87 The following impairment was incurred prior to August 1987, however they are being included in this report as they were not reported previously. Impd Description Open Closed 1173 Fire Detection System 08/24/87}}