ML20148E909: Difference between revisions

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DUKE POWER GOMPANY                                      !
P.O. HOX 03180 CIIARLOTTE, N.O. 28242 HALU. TUCKER                                                                rzternoxz mm rareinant                                                            (yo4) a73 45a:
WLT. LEAR rBOOLTTION February 29, 1988
        .U.S. Nuclear Regulatory Commission Document Control Desk                                '
Washington, D.C. 20555                                                                      ,
 
==Subject:==
Catawba Nuclear Station, Unit 2 Docket No. 50-414 Special Report Gentlemen:
Pursuant to Technical Specification 3/4.8.1.1.3 and 6.9.2, please find attached a Special Report concerning Diesel Generator 2B invalid failures which took place on January 15, 1988. Submittal of this report was delayed pursuant to my January 4, 1988 letter.
Very truly yours, 0      '
                    .c4 k.- kor              x Hal'B. Tucker JGT/41/j gc Attachment xc:      Dr. J. Nelson Grace, Regional Administrator U.S. Nuclear Regulatory Commission Regien II 101 Marietta St., NW, Suite 2900 Atlanta, Georgia 30323 Mr. P.K. Van Doorn NRC Resident Inspector Catawba Nuclear Station p~
                                                                                              \
                                                                                                  )
8803280027 880229 PDR        ADOCK 05000414 S                      DCD
 
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      'A SPECIAL REPORT CATAWBA NUCLEAR STATION, UNIT 2 DIESEL GENERATOR 2B INVALID FAILURES ON JANUARY 15, 1988 DUE TO TRASH AND MOISTURE AFFECTING THE LUBE OIL PRESSURE SENSORS Three Invalid Failures of Diesel Generator (D/G) 2B occurred on January 15, 1988, while Unit 2 was in Mode 6, Refueling. There have been 3 Valid Failures within the last 100 Valid Starts of D/G 2B and one in the last 20 Valid Starts.      Consequently, the current testing interval is 31 days, which is in accordance with Technical Specifications Surveillance 4.8.1.1.2.            There have been 3 Valid Failures within the last 100 Valid Starts on Unit 2 D/Gs.
While troubleshooting a Valid Failure which occurred on the same day (see Special Report dated February 29, 1988), D/G 2B tripped af ter starting and operating for approximately 80 seconds.          Annunciators indicating a lube oil problem were received.
The cause of the problem was found to be trash and moisture in 2 out of the 3 sensors for D/G 2B Lube Oil Pressure. The sensors were cleaned and recal-ibrated. The D/G periodic test was later satisfactorily completed.
D/G 2B had been previously removed from service af ter the Unit entered the current refueling outoge.        D/G 2A was operable throughout the period in which these Invalid Failures occurred on D/G 2B. The necessary corrective mainte-nance was performed within 35 hours.
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Revision as of 17:20, 21 July 2020

Special Rept:On 880115,three Invalid Failures of Diesel Generator 2B Occurred.Caused by Trash & Moisture in 2 Out of 3 Sensors for Lube Oil Pressure.Sensors Cleaned & Recalibr & Diesel Generator Periodic Test Later Completed
ML20148E909
Person / Time
Site: Catawba Duke Energy icon.png
Issue date: 02/29/1988
From: Tucker H
DUKE POWER CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
NUDOCS 8803280027
Download: ML20148E909 (2)


Text

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DUKE POWER GOMPANY  !

P.O. HOX 03180 CIIARLOTTE, N.O. 28242 HALU. TUCKER rzternoxz mm rareinant (yo4) a73 45a:

WLT. LEAR rBOOLTTION February 29, 1988

.U.S. Nuclear Regulatory Commission Document Control Desk '

Washington, D.C. 20555 ,

Subject:

Catawba Nuclear Station, Unit 2 Docket No. 50-414 Special Report Gentlemen:

Pursuant to Technical Specification 3/4.8.1.1.3 and 6.9.2, please find attached a Special Report concerning Diesel Generator 2B invalid failures which took place on January 15, 1988. Submittal of this report was delayed pursuant to my January 4, 1988 letter.

Very truly yours, 0 '

.c4 k.- kor x Hal'B. Tucker JGT/41/j gc Attachment xc: Dr. J. Nelson Grace, Regional Administrator U.S. Nuclear Regulatory Commission Regien II 101 Marietta St., NW, Suite 2900 Atlanta, Georgia 30323 Mr. P.K. Van Doorn NRC Resident Inspector Catawba Nuclear Station p~

\

)

8803280027 880229 PDR ADOCK 05000414 S DCD

o

.4 -i

'A SPECIAL REPORT CATAWBA NUCLEAR STATION, UNIT 2 DIESEL GENERATOR 2B INVALID FAILURES ON JANUARY 15, 1988 DUE TO TRASH AND MOISTURE AFFECTING THE LUBE OIL PRESSURE SENSORS Three Invalid Failures of Diesel Generator (D/G) 2B occurred on January 15, 1988, while Unit 2 was in Mode 6, Refueling. There have been 3 Valid Failures within the last 100 Valid Starts of D/G 2B and one in the last 20 Valid Starts. Consequently, the current testing interval is 31 days, which is in accordance with Technical Specifications Surveillance 4.8.1.1.2. There have been 3 Valid Failures within the last 100 Valid Starts on Unit 2 D/Gs.

While troubleshooting a Valid Failure which occurred on the same day (see Special Report dated February 29, 1988), D/G 2B tripped af ter starting and operating for approximately 80 seconds. Annunciators indicating a lube oil problem were received.

The cause of the problem was found to be trash and moisture in 2 out of the 3 sensors for D/G 2B Lube Oil Pressure. The sensors were cleaned and recal-ibrated. The D/G periodic test was later satisfactorily completed.

D/G 2B had been previously removed from service af ter the Unit entered the current refueling outoge. D/G 2A was operable throughout the period in which these Invalid Failures occurred on D/G 2B. The necessary corrective mainte-nance was performed within 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br />.

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