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{{Adams | |||
| number = ML20204G368 | |||
| issue date = 03/04/1987 | |||
| title = Insp Repts 50-321/87-02 & 50-366/87-02 on 870124-0220. Violation Noted:Failure to Adequately Test Mode Changing Air Sys Operation in Containment Isolation Sys | |||
| author name = Holmesray P, Nejfelt G, Ruland W | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000321, 05000366 | |||
| license number = | |||
| contact person = | |||
| case reference number = TASK-2.K.3.18, TASK-TM | |||
| document report number = 50-321-87-02, 50-321-87-2, 50-366-87-02, 50-366-87-2, IEIN-87-008, IEIN-87-8, NUDOCS 8703260385 | |||
| package number = ML20204G126 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 10 | |||
}} | |||
See also: [[see also::IR 05000321/1987002]] | |||
=Text= | |||
{{#Wiki_filter:m | |||
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UNITED STATES | |||
NUCLEAR REGULATORY COMMISSION | |||
[*' , REGION 88 | |||
< 0 101 MARIETTA STREET, N.W. | |||
$ Tf ATLANT A. GEORGI A 30323 | |||
*- | |||
..... | |||
) | |||
Report Nos.: 50-321/87-02 and 50-366/87-02 | |||
Licensee: Georgia Power Company | |||
P. O. Box 4545 | |||
Atlanta, GA 30302 | |||
Docket Nos.: 50-321 and.50-366 License Nos.: DPR-57 and NPF-5 | |||
Facility Name: Hatch 1 and 2 | |||
Inspection Conducted: January 24 - February 20, 1987 | |||
Inspectors: Md / | |||
Peter nior Resident Inspector | |||
~ | |||
R Dit'e 'S'igned | |||
/ % rez | |||
William Ruland, Senior Resident Inspector | |||
8l4/82 | |||
Dite Si~ned | |||
g | |||
(Brunsw /. _ | |||
2dZm re | |||
George M. Nejfelt, Resident Inspector | |||
sMm | |||
Date Signed | |||
O | |||
~ | |||
~ | |||
Approved by: , | |||
Floyd S. Caritrell, SFdtgn' ief Date 'S4gned | |||
Division of Reactor' Pro] ts | |||
SUMMARY | |||
This routine inspection was conducted at' the- site in the areas of | |||
~ | |||
Scope: | |||
Operational Safety Verification, Maintenance Observation, Plant Modification, | |||
Surveillance Testing Observation, Engineering Safety Feature (ESF) System | |||
Walkdown, Reportable Occurrences, On Site Followup of Eve'nts, Emergency | |||
Planning, Three Mile Island (TMI) Item Update, and Limitorque Motor Operators. | |||
Results: One violation, 50-321/87-02-01, was identified as a failure to | |||
adequately test the mode changing operation of air systems used for containment | |||
isolation systems (paragraph 7). | |||
87032%k | |||
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REPORT DETAILS | |||
1. Persons Contacted | |||
Licensee Employees | |||
J.T. Beckham, Jr. , Vice President, Plant Hatch | |||
*H.C. Nix, Plant Manager | |||
D. Read, Plant Support Manager | |||
*H.L. Sumner, Operations Manager | |||
. *P.E. Fornel, Maintenance Manager | |||
*T.R. Powers, Engineering Manager | |||
R.W. Zavadoski, Health Physics and Chemistry Manager | |||
C. Coggin, General Support Manager | |||
*M.H. Googe, Outages and Planning Manager | |||
*0.M. Fraser, Site Quality Assurance (QA) Manager (Acting) | |||
*C.T. Moore, Training and Emergency Preparedness Manager | |||
*S.B. Tipps, Nuclear Safety and Licensing Manager | |||
*A. Vest, Procedure Upgrade Program (PUP) Manager | |||
*R. Dedrickson, Assistant to Vice President, Plant Hatch | |||
Other licensee employees contacted included technicians, operators, | |||
mechanics, securit.v force members and office personnel. | |||
NRC management on site during inspection period: | |||
L.A. Reyes, Director, DRP, on February 13, 1987 | |||
F.S. Cantrell, Chief, Project Section 28, DRP, on January 26-27, 1987; | |||
and on February 13, 1987 | |||
* Attended exit interview | |||
2. Exit Interview (30703) | |||
The inspection scope and findings were summarized on February 20, 1987, | |||
with those persons indicated in paragraph 1 above. The licensee did not | |||
identify as proprietary any of the material provided to or reviewed by the | |||
inspectors during this inspection. The licensee acknowledged the findings | |||
and took no exception. | |||
(0 pen) Violation 50-321/87-02-01. Failure to provide surveillance | |||
procedures. (Paragraph 7). | |||
(0 pen) Unresolved Item 50-366/87-02-02. Design control modification | |||
problems. (Paragraph 4.a.). | |||
(0 pen) Unresolved Item 50-321, 366/87-02-03. Method to ensure qualified | |||
personnel are available to fill emergency organization positions. | |||
(Paragraph 4b). | |||
n | |||
. | |||
2 | |||
(0 pen) Inspector Followup Item 50-321/87-02-04. Nondestructive testing of | |||
piping and detemination of chemical contaminates. (Paragraph 5). | |||
.3. Licensee Action on Previous Enforcement Matters (92702) | |||
No action on previous enforcement matters was taken. | |||
4. Unresolved Items * | |||
Two unresolved items (URIs) were identified during this report period. | |||
These URIs were: | |||
a. Design Control Modification Items - Two concerns were identified. | |||
The first concern involved the development of Unit-2 design control | |||
request (DCR) 84-201 for upgrading the automatic depressurization | |||
system (ADS) to satisfy the commitment for Three Mile Island (TMI) | |||
item II.K.3.18. It appeared to the inspector that this DCR package | |||
on site was closed, when in fact, an interim modification was in | |||
place. This interim modification involved a push button which was | |||
installed in lieu of the required key lock switch to provide for | |||
inhibition of the ADS without a high drywell pressure. The second | |||
item concerned the inconsistency between a Unit-2 elementary wiring | |||
drawing (H-27979) for the remote shutdown panel and its "as built | |||
notice" (ABN 2-77-55) for items not affected by the drawing change. | |||
Specific examples were: | |||
(1) indicated motor control center (MCC) for valve 2E11-F009 was | |||
2R24-S011 on drawing H-27979, Revision 7; and was 2R27-SO96 in | |||
ABN 2-77-55, Revision 0; | |||
(2) the nomenclature for E11-F009 was called the inboard suction | |||
isolation valve on drawing H-27979, Revision 7, and was called | |||
the outboard suction isolation valve in ABN 2-77-55, Revision 0. | |||
(3) the practice of referencing "not applicable" ABNs on the | |||
microfiche cards maintained in the document control center | |||
(DCC). Neither ABN 81-92 for drawing H-27979, Revision 7, nor | |||
ABN 83-134 for drawing H-16276, Revision 17, changed the- | |||
drawings for which they were listed. | |||
These design control modification questions are considered as URI | |||
50-366/87-02-02. | |||
. b. Emergency Position Matrix - The inspector questioned whether the | |||
licensee had made adequate plans to provide qualified personnel for | |||
the emergency organization. It was noted that only two individuals | |||
were qualified as Technical Support Center (TSC) Manager as indicated | |||
by a Moore to Reddick memo dated January 27, 1987. No emergency | |||
position matrix which reflected the recent reorganization could be | |||
provided to the inspector. When asked, the licensee responded that | |||
no method existed to ensure that at least one qualified person was | |||
always available to fill each position in the emergency organization. | |||
*An Unresolved Item is a matter about which more information is required to | |||
determine whether it is acceptable or may involve a v,iolation or deviation. | |||
p- -, | |||
. | |||
. | |||
3 | |||
The ' licensee had already identified the problem with insufficient | |||
, numbers of qualified personnel in their 1987 Emergency Procedure (EP) | |||
Training Quality Improvement Program. The licensee stated that the | |||
emergency matrix was under _ revision. This item is unresolved pending | |||
further inspector review. This is URI 50-321,366/87-02-03: Method | |||
To Ensure Qualified Personnel Available To Fill Emergency. | |||
Organization Positions. | |||
5. ' Operational Safety Verification (71707) | |||
The inspectors kept themselves informed on a daily basis of the overall | |||
plant status and any significant safety matters related to plant | |||
operations. Daily discussions were held with plant management and various | |||
members of the plant operating staff. The inspectors made frequent visits | |||
to the control room. Observations included instrument readings, setpoints | |||
and recordings, status of operating systems, tags and clearances on | |||
equipment, controls and switches, annunciator alarms, adherence to | |||
limiting conditions for operation, temporary alterations in effect, daily | |||
journals and data sheet entries, control room manning, and access | |||
controls. This inspection activity included numerous informal discussions | |||
with operators and their supervisors. Weekly , when on site, selected | |||
Engineering Safety Feature (ESF) systems were confirmed operable. The | |||
confirmation was made by verifying the following: accessible valve flow | |||
path alignment, power supply breaker and fuse status, instrumentation, | |||
major component leakage, lubrication, cooling, and general condition. | |||
General plant tours were conducted on at least a biweekly basis. Portions | |||
of the control building, turbine building, reactor building, and outside | |||
areas were visited. Observations included safety related tagout | |||
verifications, shift turnover, sampling program, housekeeping and general | |||
plant conditions, fire protection equipment, control of activities in | |||
progress, radiation protection controls, physical security, problem | |||
identification systems, and containment isolation. | |||
During a plant tour on February 6,1987 on the 130' elevation of reactor | |||
building Unit-1, the inspector noticed a white foreign material on control | |||
rod drive system stainless steel piping and copper tubing. The licensee | |||
was contacted and asked to determine the chemical composition of the. | |||
material and to determine its source. The material source was the reactor | |||
water clean up (RWCU) system heat exchanger room. The material flowed | |||
around a floor drain hub, which was not grouted in, then dripped off the | |||
floor drain elbow just below the 158 elevation onto the control rod drive | |||
(CRD) piping'below. Analysis showed that the material contained high | |||
concentrations of chlorides and sulfides. The licensee cleaned the fouled | |||
piping and stopped the leak around the drain hub. Additional action such | |||
as nondestructive testing of the piping and determination of the source of | |||
the chemical contaminates is on going and will be inspector followup item | |||
(IFI) 50-321/87-02-04. | |||
In the area of housekeeping a number of discrepancies were observed by the | |||
inspectors particular in the Unit-2 Northwest Diagonal (e.g., emergency | |||
lighting on stairwell inoperable, equipment drain clogged, Gai-tronic loud | |||
speaker plugged with paper, temporary funnel under leaking valve clogged, | |||
, | |||
. | |||
9 | |||
4 | |||
potentially contaminated clothing was left behind a panel, radiation | |||
warning signs were not stored properly; and tools, trash, and a small dead | |||
bird were left in area). These housekeeping items were reported to the | |||
licensee as they were found for corrective action. | |||
In the course of the monthly activities, the Resident Inspectors included | |||
a review of the licensee's physical security program. The performance of | |||
various shifts of the security force was observed in the conduct of daily | |||
activities to include: protected and vital access controls, searching of | |||
personnel, packages and vehicles, badge issuance and retrieval, escorting | |||
of visitors, patrols and compensatory posts. | |||
No violations or deviations were identified. | |||
6. Maintenance Observation (62703) | |||
During the report period, the inspectors observed selected maintenance | |||
activities. The observations included a review of the work documents for | |||
adequacy, adherence to procedure, proper tagouts, adherence to technical | |||
specifications, radiological controls, observation of all or part of the | |||
actual work and/or retesting in progress, specified retest requirements, | |||
and adherence to the appropriate quality controls. | |||
On January 28, 1987, the inspector noted that the hydraulic hoses from | |||
each diesel generator control panel to gauges on another panel were hard | |||
and inflexible. These hoses may be the hoses originally installed for the | |||
diesel generators, since no record of replacing these hose was able to be | |||
found by the licensee. At the exit interview the licensee stated that | |||
preventive maintenance for these hydraulic hoses will be performed on a 5 | |||
year interval to ensure the hydraulic hose integrity. The hydraulic hoses | |||
questioned by the inspector have been scheduled for replacement. | |||
During this reporting period, several instances of poor maintenance | |||
cleanup practices were observed. The particular items were discussed with | |||
and have been corrected by the licensee. | |||
No violations or deviations were identified. | |||
7. Surveillance Testing Observations (61726) | |||
i | |||
' | |||
The inspectors observed the performance of selected surveillances. The | |||
observation included a review of the procedure for technical adequacy, | |||
conformance to Technical Specifications, verification of test instrument | |||
calibration, observation of all or part of the actual surveillances, | |||
removal from service and return to service of the system or components | |||
affected, and review of the data for acceptability based upon the | |||
acceptance criteria. | |||
During the inspection period, it was found by the inspector that no | |||
procedures were established to verify the activated devices for the | |||
following cases: | |||
I | |||
- | |||
7 . | |||
' | |||
. | |||
5 | |||
a. Non-interruptable Service Air: The automatic actuation of valves | |||
(e.g. , IP52-F875, -F876, -F877, and -F878) needed for the transfer of | |||
non-interruptable service air from the plant instrument air system to | |||
the nitrogen. inerting system, upon loss of instrument air, was not | |||
verified. The non-interruptable service air supplied a number of | |||
primary containment isolation valves specified in TS Table 3.7-1 | |||
(e.g., IP33-F002, -F003, -F011, and -F014) . Also, the pressure | |||
switches associated with this transfer (e.g., IPIS-N018, -N019, | |||
-N021, and -N022) were tested on a 5 year surveillance frequency by | |||
"non-safety related" surveillance procedure 57CP-P52-001-1, | |||
Revision 0. Drawings used in this finding were: H-11667, | |||
Revision 1; H-16251, Revision 14; and H-15239, Revision 14. | |||
b. Drywell Pneumatic System: The integrated operation of the | |||
drywell pneumatic system was not tested, although portions of this | |||
system (e.g., flow transmitter by procedure 57CP-CAL-011-1S, | |||
Revision 2) were tested. There was no verification of the automatic | |||
actuation of the drywell pneumatic system isolation valves (e.g., | |||
IP70-F004, -F005, -F066, and -F067) in the event of a continuous high | |||
flow for greater than 10 minutes indicating a drywell pneumatic | |||
downstream header rupture. Drawings used in this finding were: | |||
H-16286, Revision 18; and H-16299, Revision 0. | |||
The safety significance of these items in terms of functions lost to | |||
isolate primary system valves was negligible, because of the redundancy of | |||
the containment isolation valves affected. However, this finding emphasized | |||
that safety related equipment subsystems are needed to be tested | |||
periodically to prove designed equipment operability. These items are | |||
considered as a violation, 50-321/87-02-01. | |||
8. ESF System Walkdown (71710) | |||
The inspectors routinely conducted partial walkdowns of ESF systems. Valve | |||
and breaker / switch lineups and equipment conditions were randomly verified | |||
both locally and in the control room to ensure that lineups were in | |||
accordance with operability requirements and that equipment material | |||
conditions were satisfactory. The Unit-2 reactor core isolation cooling | |||
(RCIC) system was walked down in detail on February 12-13, 1987. The | |||
following Unit-2 remote shutdown panel, 2C82-P001, procedural | |||
discrepancies were found by the inspector in the validated procedure | |||
l | |||
upgrade program (PUP) procedure 3450-E51-001-2S, Revision 4: | |||
a. Breaker No. 2C82-523 for the test bypass valve, 2E51-F007, was found | |||
in the " NORMAL" position. The lineup procedure for the remote | |||
shutdown panel, 34S0-E51-001-2S, Revision 4, Attachment 2, list the | |||
position of this breaker in the "CLOSE" position. | |||
It was determined that the procedure was incorrect, because this | |||
switch is spring returned to the " NORMAL" position from the "CLOSE" | |||
position. | |||
: | |||
! | |||
t | |||
,- - - . - - - , - -- -.- | |||
, | |||
' | |||
, | |||
e | |||
. | |||
. | |||
6' , | |||
. b. The RCIC turbine flow controller, was found.j"n " MANUAL" .and set at | |||
-; O gpm. Procedure 34SO-E51-001-2S,. Revision 4, Step 7.1.5.6, required- | |||
that this flow controller be confirmed in "AUT0" with the flow rate | |||
- | |||
set at 400 gpm. Also, RCIC system electrical lineup check'off sheet | |||
in Attachment 2 of this procedure 34S0-E51-001-2S did not specify-the- | |||
positioning of the flow controller, 2C82-R001. ' | |||
' | |||
' | |||
The' Shift Supervisor, upon notification' by th'e inspector, hadL the- | |||
~ | |||
RCIC remote shutdown flow controller. repositioned to "AUT0" and set | |||
at 400.gpm. | |||
The problem described does not make RCIC inoperable. The - safety - | |||
significance of this RCIC flow controller set at zero flow rate and | |||
in manual was negligible. Also, procedure 34S0-E51-001-25, > , | |||
Revision 4, .was currently being considered to change the wording of* ' | |||
Step 7.1.5.6 from " confirm" to " confirm or place" the RCIC flow - | |||
controller. . | |||
. | |||
These two . items are particularly noteworthy, because they represented | |||
procedural discrepancies not identified in the PUP validation process. | |||
The housekeeping inside the . locked area of the remote shutdown panel was | |||
f very poor. The area was not cleaned up after work was done in this space. | |||
- | |||
Also, a pair of head phone were plugged in and thrown on the floor. I | |||
, | |||
j Within the areas inspected, no violations or deviations were identified. | |||
. | |||
f 9. Reportable Occurrences (90712 & 92700) - | |||
Newly issued -Licensee Event Reports (LERs) were reviewed for potential ~ | |||
f- generic impact, to detect trends, and to determine whether corrective s | |||
actions appeared appropriate. Events, which were reported immediately. | |||
' | |||
3., | |||
~ | |||
p were also reviewed as they occurred to determine that Technical ~ | |||
~ | |||
Specifications were being met and the public health and safety were of p,l | |||
1- | |||
- | |||
- | |||
utmost consideration. .J | |||
! | |||
! .10. Onsite Followup of Events (93702) 7 , | |||
On January 27/28, 1987 the failure of the Unit 2 "B" Condensate Transfer f h | |||
; Pump (CTP) resulted in the loss of about 92,000 gallons of Condensate y | |||
L Storage Tank (CST) water. The spill was to the CTP enclosure then out | |||
. | |||
" | |||
.through conduit to the control and turbine buildings. The conduit was not J | |||
leak tight so a small amount of CST water leaked from the conduit iicTtN- | |||
' | |||
, | |||
ground in the vicinity of the CST. The exact amount of water that went C | |||
C | |||
from the CST to the buildings and through drains to cadwaste is | |||
; indeterminate since other sources of in leakage to radwaste occurred | |||
. | |||
simultaneously. Radiological surveys indicated that no significant ,_ 3 | |||
contamination of the ground or the buildings occurred as a result of the J | |||
l - | |||
' | |||
event. | |||
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s ' ' "5equanc'e of events (A11' times are Central Standard Time (CST): | |||
, | |||
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'0 ate Time ' Event ' - | |||
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1/27/87' d430 CSTc level from Main Control Room (MCR) reading | |||
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35.0 ft. | |||
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2 1735 s x Outside rounds Plant Equipment Operator (PEO) found no i | |||
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1 | |||
(excessi'cewaterinCSTorCTPenclosures. CST level | |||
35.7 ft jyslocal indication. | |||
, | |||
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1745 From plots of CST level made after the event, it.is- | |||
probable that the CTP failure occurred at this time,. - | |||
v, | |||
' | |||
, 2100 Radwaste reports to MCR excessive leakage into Control ' | |||
' | |||
Buildir,g floor drain sumps. Shift Supervisor (51) out | |||
Nq of the MCR to investigate. i > | |||
4 2130 SS back in MCR but did not find cause of leakage. h | |||
:g Shift personnel continue to look for leakage., | |||
y y v q s. t | |||
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\?230 | |||
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CSTidfft.,29.5ft(MCR). | |||
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3 li.'28/87 0030 Water; found comNtg out of a drain hub in the conderi.e'r | |||
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bay.l , is | |||
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s0ido, "B" OFI tri pud.,/ ' | |||
i, | |||
' | |||
0105h Shift Supervisors find water near condensate booster | |||
; | |||
,k< $ pumps and in westf cable way. They investigated the | |||
s | |||
', EN n CST atee a.H found water on the asphalt near the CST | |||
*encidjdd, bpproximately ocht f at of water in the | |||
' | |||
Jg ;* 'g | |||
- | |||
e CTP enUoyure and approximately two feet of water in | |||
the CST enclosure. | |||
l' y ; - | |||
h* c 'Y 0115 Commenceq a' fort to close "B" CTF suction valve. ' | |||
d \( Bufidirig kric Grounds contacted 'to build a sandbag dike | |||
Q'<Y ' | |||
. | |||
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to cop +Al HP/ Lab contacted and | |||
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Maintenilide/p spill.I&dcontacted. m | |||
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,'N'!0120 - Site Vice President, Managers and 'datch Duty Officer p | |||
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jotified. | |||
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enclosure being * drained to r'3dwasti through manual , | |||
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3 vahts. .., .. a | |||
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- | |||
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0200 Mwint(t.rp*,e requested to sets up Tymp f rom' CTP to CST I | |||
, | |||
* enclosm* and from Unit-2 Turbine Building to Unit-1 | |||
' | |||
,,' 7' ' , | |||
/g TurbineBuilding"\eysipmentdrainuumps,. | |||
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i, 1123Q CST level 24.3 ft (local). CTPVS"1 suction valve | |||
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closed. Temporar9 pumps transferriag water. from CTP q | |||
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.M o CST enclosures. , | |||
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~ 0250 'NRC Senior-Resident Inspector (SRI) notified. - | |||
, | |||
, | |||
0336 CST enclosure drain' to radwaste stopped - by closing | |||
manual valve. Leak path identified as through' the | |||
gland seal of "B" CTP. | |||
0400 NRC SRI on site.in response'to the, event. | |||
' | |||
.].. | |||
0530' . Temporary pumps transferring water from Unit 2 to | |||
Unit 1 Turbine Butiding equipment drain suinps. | |||
0545 Leakage into turbine buildin'g west cable way reported ' | |||
,- stopped. '~ ' | |||
p | |||
n ' | |||
i . | |||
0600 Unit-1 condensate transfer system cross connected' to. | |||
Unit-2 condensate transfer system. This provided | |||
backwash wat'er for demineralizers in Unit-2 radwaste | |||
syst.em. ' | |||
0630 CST level 23.0. ft . (MCR). The continued drop in CST | |||
l level after "B" CTP was isolated was due to normal | |||
. makeup to Unit-2 .without addition to the CST from | |||
radwasteft , | |||
The licensee took prompt corrective actions to mitigate the effects of '' | |||
this event; and no release to the environment resulted. , | |||
Noviolationordeviationwasidentiffted. j : | |||
, . | |||
- | |||
a . | |||
11. Visit byJBrunswick Senior Resident' Inspector | |||
The inspector familiaihzed himself with the site _ for emergency purposes, | |||
:obtained a badge for unescorted access, toured the emergency response | |||
facilities and major plant > areas. TheMnsoector' reviewed the licensee's | |||
. current emergency plan,/ the emergency - clas'41fication . procedure,' | |||
73EP-EIP-001-0S, and the emergency operating prc,cedure flow charts. The | |||
review was limited to a brief faintliarization with the documents. | |||
* ' ' | |||
! | |||
r; | |||
, , . | |||
No violations or deviations were identified; t' . - | |||
- | |||
> | |||
' | |||
12. | |||
' ? | |||
, | |||
. | |||
ThreeMileIsland(TMI)]ItemII.K.3.18 | |||
,, s- | |||
The inspector , reviewed TMI item II.K.3.18, concerning the automatic | |||
' | |||
depressurization system (ADS) logic, which was considered close'd by the | |||
site licensing-' staff. # However, this THI Jtem was not completedgand an | |||
interim modification was performed - installation of a push button rather | |||
than a key switch to provide manual inhibition of ADS without a jhigh ' | |||
drywell pressure signal present. | |||
~ | |||
r Documentation concerning II.K.3.18 prior to 1984 was summarized in IE | |||
<, Inspection Reports. 50-321/83-27 and 50-366/83-29, cparagraph 11. | |||
;- Subsequent correspondences were: | |||
. | |||
i .'. , | |||
. | |||
W + | |||
%[ r N | |||
g *W | |||
' | |||
< T == -a- | |||
9tTk e -- 8" v -'Iv*---'T * * ' ' W * | |||
? ---'*--T-'-4'-PW"U--*NT w----'-A'-t'M'-"m-W--"7-**dW 9'-FT- 74St-25-W W-1 8k W We '' W+T*D'''+T---"' | |||
Pr ' ,, | |||
% | |||
4l | |||
* | |||
.* | |||
'f. | |||
j. 3' 9 | |||
Date'' . Originator | |||
y | |||
" | |||
3:,, | |||
' | |||
03-15-85, GPC Partial implementation request push button | |||
rather than a key switch to be installed for | |||
?" the ADS manual inhibit, because of | |||
anticipated transient without scram (ATWS) | |||
L | |||
, | |||
.- considerations. | |||
02-28-86 GPC ADS modification completed for both units | |||
' | |||
with the exception of the manual inhibit | |||
switch. GPC committed to install the manual | |||
' | |||
inhibit key switch during the Spring 1987 | |||
Unit-1 and the Spring 1988 Unit-2 refueling | |||
. | |||
outages. | |||
* ' | |||
13. Limitorque DC~ Motor Operators | |||
^ | |||
IE Information Not' ice No. 87-08 addressed the potential degradation of | |||
motor leads in Limitorque DC motor operators that were fitted with | |||
. | |||
Nomex-Kapton insulated leads and manufacture _d between December 1984 and | |||
December 1985. The licensee has identified three Limitorque motor | |||
- operators with' the Nomex-Kapton insulated leads (e.g. ,1E41-F001, -F011, | |||
; and'2E41-F011). However, only one valve,1F41-F001, used the insulated | |||
leads ' manufactured in the specified 12 n.v .1 period. As a result, - a | |||
" Justification for' Continued Operation" (JCO) was done for 1E41-F001, the | |||
steam supply valve to the high pressure coolant injection (HPCI) turbine. | |||
The JC0 concluded that no additional action was required by the licensee, | |||
because IE41-F001 is not a primary containment isolation valve and no. | |||
credi.t is taken for the operation of this valve in the event of a High | |||
Energy Line Break (HELB) in the HPCI room. | |||
= | |||
t | |||
l % | |||
# 4 | |||
4 | |||
h | |||
I | |||
,V' | |||
y . ,,- . , ,. ,. w - - - | |||
w i y | |||
}} |
Latest revision as of 05:17, 20 December 2021
ML20204G368 | |
Person / Time | |
---|---|
Site: | Hatch |
Issue date: | 03/04/1987 |
From: | Holmesray P, Nejfelt G, Ruland W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20204G126 | List: |
References | |
TASK-2.K.3.18, TASK-TM 50-321-87-02, 50-321-87-2, 50-366-87-02, 50-366-87-2, IEIN-87-008, IEIN-87-8, NUDOCS 8703260385 | |
Download: ML20204G368 (10) | |
See also: IR 05000321/1987002
Text
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'
UNITED STATES
NUCLEAR REGULATORY COMMISSION
[*' , REGION 88
< 0 101 MARIETTA STREET, N.W.
$ Tf ATLANT A. GEORGI A 30323
- -
.....
)
Report Nos.: 50-321/87-02 and 50-366/87-02
Licensee: Georgia Power Company
P. O. Box 4545
Atlanta, GA 30302
Docket Nos.: 50-321 and.50-366 License Nos.: DPR-57 and NPF-5
Facility Name: Hatch 1 and 2
Inspection Conducted: January 24 - February 20, 1987
Inspectors: Md /
Peter nior Resident Inspector
~
R Dit'e 'S'igned
/ % rez
William Ruland, Senior Resident Inspector
8l4/82
Dite Si~ned
g
(Brunsw /. _
2dZm re
George M. Nejfelt, Resident Inspector
sMm
Date Signed
O
~
~
Approved by: ,
Floyd S. Caritrell, SFdtgn' ief Date 'S4gned
Division of Reactor' Pro] ts
SUMMARY
This routine inspection was conducted at' the- site in the areas of
~
Scope:
Operational Safety Verification, Maintenance Observation, Plant Modification,
Surveillance Testing Observation, Engineering Safety Feature (ESF) System
Walkdown, Reportable Occurrences, On Site Followup of Eve'nts, Emergency
Planning, Three Mile Island (TMI) Item Update, and Limitorque Motor Operators.
Results: One violation, 50-321/87-02-01, was identified as a failure to
adequately test the mode changing operation of air systems used for containment
isolation systems (paragraph 7).
87032%k
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REPORT DETAILS
1. Persons Contacted
Licensee Employees
J.T. Beckham, Jr. , Vice President, Plant Hatch
- H.C. Nix, Plant Manager
D. Read, Plant Support Manager
- H.L. Sumner, Operations Manager
. *P.E. Fornel, Maintenance Manager
- T.R. Powers, Engineering Manager
R.W. Zavadoski, Health Physics and Chemistry Manager
C. Coggin, General Support Manager
- M.H. Googe, Outages and Planning Manager
- 0.M. Fraser, Site Quality Assurance (QA) Manager (Acting)
- C.T. Moore, Training and Emergency Preparedness Manager
- S.B. Tipps, Nuclear Safety and Licensing Manager
- A. Vest, Procedure Upgrade Program (PUP) Manager
- R. Dedrickson, Assistant to Vice President, Plant Hatch
Other licensee employees contacted included technicians, operators,
mechanics, securit.v force members and office personnel.
NRC management on site during inspection period:
L.A. Reyes, Director, DRP, on February 13, 1987
F.S. Cantrell, Chief, Project Section 28, DRP, on January 26-27, 1987;
and on February 13, 1987
- Attended exit interview
2. Exit Interview (30703)
The inspection scope and findings were summarized on February 20, 1987,
with those persons indicated in paragraph 1 above. The licensee did not
identify as proprietary any of the material provided to or reviewed by the
inspectors during this inspection. The licensee acknowledged the findings
and took no exception.
(0 pen) Violation 50-321/87-02-01. Failure to provide surveillance
procedures. (Paragraph 7).
(0 pen) Unresolved Item 50-366/87-02-02. Design control modification
problems. (Paragraph 4.a.).
(0 pen) Unresolved Item 50-321, 366/87-02-03. Method to ensure qualified
personnel are available to fill emergency organization positions.
(Paragraph 4b).
n
.
2
(0 pen) Inspector Followup Item 50-321/87-02-04. Nondestructive testing of
piping and detemination of chemical contaminates. (Paragraph 5).
.3. Licensee Action on Previous Enforcement Matters (92702)
No action on previous enforcement matters was taken.
4. Unresolved Items *
Two unresolved items (URIs) were identified during this report period.
These URIs were:
a. Design Control Modification Items - Two concerns were identified.
The first concern involved the development of Unit-2 design control
request (DCR)84-201 for upgrading the automatic depressurization
system (ADS) to satisfy the commitment for Three Mile Island (TMI)
item II.K.3.18. It appeared to the inspector that this DCR package
on site was closed, when in fact, an interim modification was in
place. This interim modification involved a push button which was
installed in lieu of the required key lock switch to provide for
inhibition of the ADS without a high drywell pressure. The second
item concerned the inconsistency between a Unit-2 elementary wiring
drawing (H-27979) for the remote shutdown panel and its "as built
notice" (ABN 2-77-55) for items not affected by the drawing change.
Specific examples were:
(1) indicated motor control center (MCC) for valve 2E11-F009 was
2R24-S011 on drawing H-27979, Revision 7; and was 2R27-SO96 in
ABN 2-77-55, Revision 0;
(2) the nomenclature for E11-F009 was called the inboard suction
isolation valve on drawing H-27979, Revision 7, and was called
the outboard suction isolation valve in ABN 2-77-55, Revision 0.
(3) the practice of referencing "not applicable" ABNs on the
microfiche cards maintained in the document control center
(DCC). Neither ABN 81-92 for drawing H-27979, Revision 7, nor
ABN 83-134 for drawing H-16276, Revision 17, changed the-
drawings for which they were listed.
These design control modification questions are considered as URI
50-366/87-02-02.
. b. Emergency Position Matrix - The inspector questioned whether the
licensee had made adequate plans to provide qualified personnel for
the emergency organization. It was noted that only two individuals
were qualified as Technical Support Center (TSC) Manager as indicated
by a Moore to Reddick memo dated January 27, 1987. No emergency
position matrix which reflected the recent reorganization could be
provided to the inspector. When asked, the licensee responded that
no method existed to ensure that at least one qualified person was
always available to fill each position in the emergency organization.
- An Unresolved Item is a matter about which more information is required to
determine whether it is acceptable or may involve a v,iolation or deviation.
p- -,
.
.
3
The ' licensee had already identified the problem with insufficient
, numbers of qualified personnel in their 1987 Emergency Procedure (EP)
Training Quality Improvement Program. The licensee stated that the
emergency matrix was under _ revision. This item is unresolved pending
further inspector review. This is URI 50-321,366/87-02-03: Method
To Ensure Qualified Personnel Available To Fill Emergency.
Organization Positions.
5. ' Operational Safety Verification (71707)
The inspectors kept themselves informed on a daily basis of the overall
plant status and any significant safety matters related to plant
operations. Daily discussions were held with plant management and various
members of the plant operating staff. The inspectors made frequent visits
to the control room. Observations included instrument readings, setpoints
and recordings, status of operating systems, tags and clearances on
equipment, controls and switches, annunciator alarms, adherence to
limiting conditions for operation, temporary alterations in effect, daily
journals and data sheet entries, control room manning, and access
controls. This inspection activity included numerous informal discussions
with operators and their supervisors. Weekly , when on site, selected
Engineering Safety Feature (ESF) systems were confirmed operable. The
confirmation was made by verifying the following: accessible valve flow
path alignment, power supply breaker and fuse status, instrumentation,
major component leakage, lubrication, cooling, and general condition.
General plant tours were conducted on at least a biweekly basis. Portions
of the control building, turbine building, reactor building, and outside
areas were visited. Observations included safety related tagout
verifications, shift turnover, sampling program, housekeeping and general
plant conditions, fire protection equipment, control of activities in
progress, radiation protection controls, physical security, problem
identification systems, and containment isolation.
During a plant tour on February 6,1987 on the 130' elevation of reactor
building Unit-1, the inspector noticed a white foreign material on control
rod drive system stainless steel piping and copper tubing. The licensee
was contacted and asked to determine the chemical composition of the.
material and to determine its source. The material source was the reactor
water clean up (RWCU) system heat exchanger room. The material flowed
around a floor drain hub, which was not grouted in, then dripped off the
floor drain elbow just below the 158 elevation onto the control rod drive
(CRD) piping'below. Analysis showed that the material contained high
concentrations of chlorides and sulfides. The licensee cleaned the fouled
piping and stopped the leak around the drain hub. Additional action such
as nondestructive testing of the piping and determination of the source of
the chemical contaminates is on going and will be inspector followup item
(IFI) 50-321/87-02-04.
In the area of housekeeping a number of discrepancies were observed by the
inspectors particular in the Unit-2 Northwest Diagonal (e.g., emergency
lighting on stairwell inoperable, equipment drain clogged, Gai-tronic loud
speaker plugged with paper, temporary funnel under leaking valve clogged,
,
.
9
4
potentially contaminated clothing was left behind a panel, radiation
warning signs were not stored properly; and tools, trash, and a small dead
bird were left in area). These housekeeping items were reported to the
licensee as they were found for corrective action.
In the course of the monthly activities, the Resident Inspectors included
a review of the licensee's physical security program. The performance of
various shifts of the security force was observed in the conduct of daily
activities to include: protected and vital access controls, searching of
personnel, packages and vehicles, badge issuance and retrieval, escorting
of visitors, patrols and compensatory posts.
No violations or deviations were identified.
6. Maintenance Observation (62703)
During the report period, the inspectors observed selected maintenance
activities. The observations included a review of the work documents for
adequacy, adherence to procedure, proper tagouts, adherence to technical
specifications, radiological controls, observation of all or part of the
actual work and/or retesting in progress, specified retest requirements,
and adherence to the appropriate quality controls.
On January 28, 1987, the inspector noted that the hydraulic hoses from
each diesel generator control panel to gauges on another panel were hard
and inflexible. These hoses may be the hoses originally installed for the
diesel generators, since no record of replacing these hose was able to be
found by the licensee. At the exit interview the licensee stated that
preventive maintenance for these hydraulic hoses will be performed on a 5
year interval to ensure the hydraulic hose integrity. The hydraulic hoses
questioned by the inspector have been scheduled for replacement.
During this reporting period, several instances of poor maintenance
cleanup practices were observed. The particular items were discussed with
and have been corrected by the licensee.
No violations or deviations were identified.
7. Surveillance Testing Observations (61726)
i
'
The inspectors observed the performance of selected surveillances. The
observation included a review of the procedure for technical adequacy,
conformance to Technical Specifications, verification of test instrument
calibration, observation of all or part of the actual surveillances,
removal from service and return to service of the system or components
affected, and review of the data for acceptability based upon the
acceptance criteria.
During the inspection period, it was found by the inspector that no
procedures were established to verify the activated devices for the
following cases:
I
-
7 .
'
.
5
a. Non-interruptable Service Air: The automatic actuation of valves
(e.g. , IP52-F875, -F876, -F877, and -F878) needed for the transfer of
non-interruptable service air from the plant instrument air system to
the nitrogen. inerting system, upon loss of instrument air, was not
verified. The non-interruptable service air supplied a number of
primary containment isolation valves specified in TS Table 3.7-1
(e.g., IP33-F002, -F003, -F011, and -F014) . Also, the pressure
switches associated with this transfer (e.g., IPIS-N018, -N019,
-N021, and -N022) were tested on a 5 year surveillance frequency by
"non-safety related" surveillance procedure 57CP-P52-001-1,
Revision 0. Drawings used in this finding were: H-11667,
Revision 1; H-16251, Revision 14; and H-15239, Revision 14.
b. Drywell Pneumatic System: The integrated operation of the
drywell pneumatic system was not tested, although portions of this
system (e.g., flow transmitter by procedure 57CP-CAL-011-1S,
Revision 2) were tested. There was no verification of the automatic
actuation of the drywell pneumatic system isolation valves (e.g.,
IP70-F004, -F005, -F066, and -F067) in the event of a continuous high
flow for greater than 10 minutes indicating a drywell pneumatic
downstream header rupture. Drawings used in this finding were:
H-16286, Revision 18; and H-16299, Revision 0.
The safety significance of these items in terms of functions lost to
isolate primary system valves was negligible, because of the redundancy of
the containment isolation valves affected. However, this finding emphasized
that safety related equipment subsystems are needed to be tested
periodically to prove designed equipment operability. These items are
considered as a violation, 50-321/87-02-01.
8. ESF System Walkdown (71710)
The inspectors routinely conducted partial walkdowns of ESF systems. Valve
and breaker / switch lineups and equipment conditions were randomly verified
both locally and in the control room to ensure that lineups were in
accordance with operability requirements and that equipment material
conditions were satisfactory. The Unit-2 reactor core isolation cooling
(RCIC) system was walked down in detail on February 12-13, 1987. The
following Unit-2 remote shutdown panel, 2C82-P001, procedural
discrepancies were found by the inspector in the validated procedure
l
upgrade program (PUP) procedure 3450-E51-001-2S, Revision 4:
a. Breaker No. 2C82-523 for the test bypass valve, 2E51-F007, was found
in the " NORMAL" position. The lineup procedure for the remote
shutdown panel, 34S0-E51-001-2S, Revision 4, Attachment 2, list the
position of this breaker in the "CLOSE" position.
It was determined that the procedure was incorrect, because this
switch is spring returned to the " NORMAL" position from the "CLOSE"
position.
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,
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6' ,
. b. The RCIC turbine flow controller, was found.j"n " MANUAL" .and set at
-; O gpm. Procedure 34SO-E51-001-2S,. Revision 4, Step 7.1.5.6, required-
that this flow controller be confirmed in "AUT0" with the flow rate
-
set at 400 gpm. Also, RCIC system electrical lineup check'off sheet
in Attachment 2 of this procedure 34S0-E51-001-2S did not specify-the-
positioning of the flow controller, 2C82-R001. '
'
'
The' Shift Supervisor, upon notification' by th'e inspector, hadL the-
~
RCIC remote shutdown flow controller. repositioned to "AUT0" and set
at 400.gpm.
The problem described does not make RCIC inoperable. The - safety -
significance of this RCIC flow controller set at zero flow rate and
in manual was negligible. Also, procedure 34S0-E51-001-25, > ,
Revision 4, .was currently being considered to change the wording of* '
Step 7.1.5.6 from " confirm" to " confirm or place" the RCIC flow -
controller. .
.
These two . items are particularly noteworthy, because they represented
procedural discrepancies not identified in the PUP validation process.
The housekeeping inside the . locked area of the remote shutdown panel was
f very poor. The area was not cleaned up after work was done in this space.
-
Also, a pair of head phone were plugged in and thrown on the floor. I
,
j Within the areas inspected, no violations or deviations were identified.
.
f 9. Reportable Occurrences (90712 & 92700) -
Newly issued -Licensee Event Reports (LERs) were reviewed for potential ~
f- generic impact, to detect trends, and to determine whether corrective s
actions appeared appropriate. Events, which were reported immediately.
'
3.,
~
p were also reviewed as they occurred to determine that Technical ~
~
Specifications were being met and the public health and safety were of p,l
1-
-
-
utmost consideration. .J
!
! .10. Onsite Followup of Events (93702) 7 ,
On January 27/28, 1987 the failure of the Unit 2 "B" Condensate Transfer f h
- Pump (CTP) resulted in the loss of about 92,000 gallons of Condensate y
L Storage Tank (CST) water. The spill was to the CTP enclosure then out
.
"
.through conduit to the control and turbine buildings. The conduit was not J
leak tight so a small amount of CST water leaked from the conduit iicTtN-
'
,
ground in the vicinity of the CST. The exact amount of water that went C
C
from the CST to the buildings and through drains to cadwaste is
- indeterminate since other sources of in leakage to radwaste occurred
.
simultaneously. Radiological surveys indicated that no significant ,_ 3
contamination of the ground or the buildings occurred as a result of the J
l -
'
event.
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s ' ' "5equanc'e of events (A11' times are Central Standard Time (CST):
,
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1/27/87' d430 CSTc level from Main Control Room (MCR) reading
, ,
35.0 ft.
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2 1735 s x Outside rounds Plant Equipment Operator (PEO) found no i
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(excessi'cewaterinCSTorCTPenclosures. CST level
35.7 ft jyslocal indication.
,
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1745 From plots of CST level made after the event, it.is-
probable that the CTP failure occurred at this time,. -
v,
'
, 2100 Radwaste reports to MCR excessive leakage into Control '
'
Buildir,g floor drain sumps. Shift Supervisor (51) out
Nq of the MCR to investigate. i >
4 2130 SS back in MCR but did not find cause of leakage. h
- g Shift personnel continue to look for leakage.,
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CSTidfft.,29.5ft(MCR).
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3 li.'28/87 0030 Water; found comNtg out of a drain hub in the conderi.e'r
' ad
bay.l , is
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0105h Shift Supervisors find water near condensate booster
,k< $ pumps and in westf cable way. They investigated the
s
', EN n CST atee a.H found water on the asphalt near the CST
- encidjdd, bpproximately ocht f at of water in the
'
Jg ;* 'g
-
e CTP enUoyure and approximately two feet of water in
the CST enclosure.
l' y ; -
h* c 'Y 0115 Commenceq a' fort to close "B" CTF suction valve. '
d \( Bufidirig kric Grounds contacted 'to build a sandbag dike
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to cop +Al HP/ Lab contacted and
'
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Maintenilide/p spill.I&dcontacted. m
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,'N'!0120 - Site Vice President, Managers and 'datch Duty Officer p
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jotified.
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enclosure being * drained to r'3dwasti through manual ,
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0200 Mwint(t.rp*,e requested to sets up Tymp f rom' CTP to CST I
,
- enclosm* and from Unit-2 Turbine Building to Unit-1
'
,,' 7' ' ,
/g TurbineBuilding"\eysipmentdrainuumps,.
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i, 1123Q CST level 24.3 ft (local). CTPVS"1 suction valve
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closed. Temporar9 pumps transferriag water. from CTP q
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~ 0250 'NRC Senior-Resident Inspector (SRI) notified. -
,
,
0336 CST enclosure drain' to radwaste stopped - by closing
manual valve. Leak path identified as through' the
gland seal of "B" CTP.
0400 NRC SRI on site.in response'to the, event.
'
.]..
0530' . Temporary pumps transferring water from Unit 2 to
Unit 1 Turbine Butiding equipment drain suinps.
0545 Leakage into turbine buildin'g west cable way reported '
,- stopped. '~ '
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i .
0600 Unit-1 condensate transfer system cross connected' to.
Unit-2 condensate transfer system. This provided
backwash wat'er for demineralizers in Unit-2 radwaste
syst.em. '
0630 CST level 23.0. ft . (MCR). The continued drop in CST
l level after "B" CTP was isolated was due to normal
. makeup to Unit-2 .without addition to the CST from
radwasteft ,
The licensee took prompt corrective actions to mitigate the effects of
this event; and no release to the environment resulted. ,
Noviolationordeviationwasidentiffted. j :
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11. Visit byJBrunswick Senior Resident' Inspector
The inspector familiaihzed himself with the site _ for emergency purposes,
- obtained a badge for unescorted access, toured the emergency response
facilities and major plant > areas. TheMnsoector' reviewed the licensee's
. current emergency plan,/ the emergency - clas'41fication . procedure,'
73EP-EIP-001-0S, and the emergency operating prc,cedure flow charts. The
review was limited to a brief faintliarization with the documents.
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No violations or deviations were identified; t' . -
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12.
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ThreeMileIsland(TMI)]ItemII.K.3.18
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The inspector , reviewed TMI item II.K.3.18, concerning the automatic
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depressurization system (ADS) logic, which was considered close'd by the
site licensing-' staff. # However, this THI Jtem was not completedgand an
interim modification was performed - installation of a push button rather
than a key switch to provide manual inhibition of ADS without a jhigh '
drywell pressure signal present.
~
r Documentation concerning II.K.3.18 prior to 1984 was summarized in IE
<, Inspection Reports. 50-321/83-27 and 50-366/83-29, cparagraph 11.
- - Subsequent correspondences were
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Date . Originator
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03-15-85, GPC Partial implementation request push button
rather than a key switch to be installed for
?" the ADS manual inhibit, because of
anticipated transient without scram (ATWS)
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.- considerations.
02-28-86 GPC ADS modification completed for both units
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with the exception of the manual inhibit
switch. GPC committed to install the manual
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inhibit key switch during the Spring 1987
Unit-1 and the Spring 1988 Unit-2 refueling
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outages.
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13. Limitorque DC~ Motor Operators
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IE Information Not' ice No. 87-08 addressed the potential degradation of
motor leads in Limitorque DC motor operators that were fitted with
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Nomex-Kapton insulated leads and manufacture _d between December 1984 and
December 1985. The licensee has identified three Limitorque motor
- operators with' the Nomex-Kapton insulated leads (e.g. ,1E41-F001, -F011,
leads ' manufactured in the specified 12 n.v .1 period. As a result, - a
" Justification for' Continued Operation" (JCO) was done for 1E41-F001, the
steam supply valve to the high pressure coolant injection (HPCI) turbine.
The JC0 concluded that no additional action was required by the licensee,
because IE41-F001 is not a primary containment isolation valve and no.
credi.t is taken for the operation of this valve in the event of a High
Energy Line Break (HELB) in the HPCI room.
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