ML17345A638: Difference between revisions

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| issue date = 04/21/1989
| issue date = 04/21/1989
| title = Special Rept:On 890322,condenser Air Ejector High Range Noble Gas Monitor Removed from Svc in Order to Performed Maint & Became Inoperable for Greater than 7 Days.Monitor Scheduled to Be Returned to Svc Prior to Restart of Unit
| title = Special Rept:On 890322,condenser Air Ejector High Range Noble Gas Monitor Removed from Svc in Order to Performed Maint & Became Inoperable for Greater than 7 Days.Monitor Scheduled to Be Returned to Svc Prior to Restart of Unit
| author name = CONWAY W F
| author name = Conway W
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:gCCEMP>TED DfLRIBUTTON DEMONST4110%
{{#Wiki_filter:gCCEMP>TED             DfLRIBUTTON             DEMONST4110%             SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8904260303 DOC.DATE: 89/04/21 NOTARIZED:
ACCESSION NBR:8904260303           DOC.DATE:   89/04/21   NOTARIZED: NO         DOCKET FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH. NAME           AUTHOR AFFILIATION CONWAY,W.F.         Florida Power & Light Co.
NO DOCKET FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
RECIP.NAME           RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Special rept re condenser air ejector high range noble gas monitor inoperable for greater than 7 days.DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME PD2-2 LA EDISON,G COPIES LTTR ENCL 1 1 1 1 RECIPIEN1 ID CODE/NAME PD2-2 PD COPIES LTTR ENCL 1 1 INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB DEDRO NRR/DEST/ADE 8H NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR DRIS/SXB 9A 02~R B EXTERNAL: EG&G WILLIAMS,S L ST LOBBY WARD NRC PDR NSXC MURPHY,G.A 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 1 1 1 1 1 1 1 1 1 1 1 1 1 1''1'1 4 1 1 1 ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP IRM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RPB 10 NUDOCS-A'BSTRACT RES/DSIR/EIB RGN2 FILE 01 FORD BLDG HOY I A LPDR NSIC MAYS,G 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1'2 1 1 1 1 1 1 1 1'1 1 1 R I NOTE IO ALL"RIDS" RECIPIENT.
Special rept re condenser air ejector high range noble gas monitor inoperable for greater than 7 days.
PLEASE HELP US'IO REDUCE WAS'!CORZACI'IHE DXXRKMl'OÃIRDL DESK, ROOM Pl-37 (EXT.20079)M EIZKQCQZ RÃ3R KQK FKR DISTEKBUTXON LISTS FOR DOCUMENI'S YOU DON'T NEED!h D D S TOTAL NUMBER OF COPIES REQUIRED: LTTR 44 ENCL 43 P.O.Box14000, Juno Beach, Fl 33408-0420.I'we y~APRIL 2 1 I989 L-89-161 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR                 ENCL     SIZE:
Re: Turkey Point Unit 3 Docket No.50-250 Special Report-Condenser Air Ejector High Range Noble Gas Monitor Ino erable for Greater than Seven Da s In accordance with Technical Specification 6.9.3 the attached Special Report is provided for your information.
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
Should there by any questions on this information, please contact US~Very truly yours, W.F.Co y Senior Vice President-Nuclear WFC/JRH/cm Attachment cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 85'04260303 Sr/0421 PDR ADOCK 0 000250 PDC an FPL Group company SPECIAL REPORT CONMNSER AIR EJECTOR HIGH RANGE NOBLE GAS MONITOR Puru os e Technical Specification 3.5, Table 3.5-5, item 13.c requires that if the condenser air ejector high range noble gas monitor is inoperable for greater than 7 days, FPL shall prepare and submit a special report to the Commission pursuant to Technical Specification 6.9.3 within 30 days following the event, outlining the action taken, the cause of the inoperability, and the plans and schedule for restoring the system to operable status'vent and Action Taken On March 22, 1989, at approximately 1115, the'Unit 3 condenser air ejector high range noble gas monitor was removed from service in order to perform preventive maintenance and channel calibrations as required by the Technical Specifications
NOTES:
.At that time, the Chemistry Department initiated the preplanned alternate method of monitoring, as required by the Technical Specifications.
RECIPIENT           COPIES              RECIPIEN1        COPIES ID   CODE/NAME         LTTR ENCL        ID  CODE/NAME    LTTR ENCL PD2-2 LA                   1     1     PD2-2 PD             1    1 EDISON,G                  1     1 INTERNAL: ACRS MICHELSON             1      1    ACRS MOELLER          2    2 ACRS WYLIE                 1      1    AEOD/DOA              1    1 AEOD/DSP/TPAB             1      1    AEOD/ROAB/DSP        2    2 DEDRO                     1      1    IRM/DCTS/DAB          1    1 NRR/DEST/ADE 8H           1      1    NRR/DEST/ADS    7E    1    0 NRR/DEST/CEB 8H            1      1    NRR/DEST/ESB    8D    1    1 NRR/DEST/ICSB 7            1      1    NRR/DEST/MEB    9H    1     1 NRR/DEST/MTB 9H            1      1    NRR/DEST/PSB    8D   1    1 NRR/DEST/RSB 8E            1      1    NRR/DEST/SGB    8D   1    1 NRR/DLPQ/HFB 10            1      1    NRR/DLPQ/QAB   10   1    1' NRR/DOEA/EAB 11            1  '' 11'  NRR/DREP/RPB   10         2 NRR DRIS/SXB 9A            1            NUDOCS-A'BSTRACT     1    1 02~      1            RES/DSIR/EIB         1    1 R      B          1      1    RGN2     FILE 01     1    1 EXTERNAL: EG&G WILLIAMS,S            4      4    FORD BLDG HOY I A     1     1 L ST LOBBY WARD            1       1   LPDR                        1         R NRC PDR                    1       1   NSIC MAYS,G          1     1 NSXC MURPHY,G.A            1       1                                           I h
On March 29, Unit 3 was shutdown, and therefore, the preplanned alternate method of monitoring was discontinued when the condenser air ejector was removed from service.Cause of the Ino erabilit The Unit 3 condenser air ejector.high.range noble gas monitor was removed from service in order to perform preventive maintenance and channel calibrations as required by the Technical Specifications.
D D
Schedule for Return of E ai ment The Unit 3 condenser air ejector high range noble gas monitor is scheduled to be returned to operable status prior to restart of Unit 3.}}
NOTE IO ALL "RIDS" RECIPIENT.
S PLEASE HELP US 'IO REDUCE WAS'! CORZACI'IHE DXXRKMl'OÃIRDLDESK, ROOM Pl-37 (EXT. 20079) M EIZKQCQZ RÃ3R KQK FKR DISTEKBUTXON LISTS FOR DOCUMENI'S YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED: LTTR             44   ENCL   43
 
P.O. Box14000, Juno Beach, Fl 33408-0420
            .I 'we y ~
APRIL 2     1 I989 L-89-161 U. S. Nuclear Regulatory Commission Attn:     Document Control Desk Washington, D. C.                 20555 Gentlemen:
Re:   Turkey Point Unit 3 Docket No. 50-250 Special Report Condenser Air Ejector High Range Noble Gas Monitor Ino erable for Greater than Seven Da s In accordance with Technical Specification 6.9.3 the attached Special Report is provided for your information.
Should there by any questions on this information, please contact US ~
Very   truly           yours, W. F. Co             y Senior Vice President               Nuclear WFC/JRH/cm Attachment cc:   Stewart D. Ebneter, Regional Administrator, Region II,                 USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 85'04260303 Sr/0421 PDR   ADOCK 0 000250 PDC an FPL Group company
 
SPECIAL REPORT CONMNSER AIR EJECTOR HIGH RANGE NOBLE GAS MONITOR Puru os e Technical Specification 3.5, Table 3.5-5, item 13.c requires that     if the condenser air ejector high range noble gas monitor is inoperable for greater than 7 days, FPL shall prepare and submit a special report to the Commission pursuant to Technical Specification 6.9.3 within 30 days following the event, outlining the action taken, the cause of the inoperability, and the plans and schedule for restoring the system to operable status'vent and Action Taken On March 22, 1989, at approximately 1115, the 'Unit 3 condenser air ejector high range noble gas monitor was removed from service in order to perform preventive maintenance and channel calibrations as required by the Technical Specifications .
At that time, the Chemistry Department initiated the preplanned alternate method of monitoring, as required by the Technical Specifications. On March 29, Unit 3 was shutdown, and therefore, the preplanned alternate method of monitoring was discontinued when the condenser air ejector was removed from service.
Cause   of the Ino erabilit The   Unit 3 condenser air ejector. high .range noble gas monitor was removed from service in order to perform preventive maintenance and channel calibrations as required by the Technical Specifications.
Schedule   for Return of E ai ment The   Unit 3 condenser air ejector high range noble gas monitor is scheduled to be returned to operable status prior to restart of Unit 3.}}

Latest revision as of 22:31, 3 February 2020

Special Rept:On 890322,condenser Air Ejector High Range Noble Gas Monitor Removed from Svc in Order to Performed Maint & Became Inoperable for Greater than 7 Days.Monitor Scheduled to Be Returned to Svc Prior to Restart of Unit
ML17345A638
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 04/21/1989
From: Conway W
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-89-161, NUDOCS 8904260303
Download: ML17345A638 (3)


Text

gCCEMP>TED DfLRIBUTTON DEMONST4110% SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8904260303 DOC.DATE: 89/04/21 NOTARIZED: NO DOCKET FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH. NAME AUTHOR AFFILIATION CONWAY,W.F. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Special rept re condenser air ejector high range noble gas monitor inoperable for greater than 7 days.

DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIEN1 COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2-2 PD 1 1 EDISON,G 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/ADE 8H 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/QAB 10 1 1' NRR/DOEA/EAB 11 1 11' NRR/DREP/RPB 10 2 NRR DRIS/SXB 9A 1 NUDOCS-A'BSTRACT 1 1 02~ 1 RES/DSIR/EIB 1 1 R B 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY I A 1 1 L ST LOBBY WARD 1 1 LPDR 1 R NRC PDR 1 1 NSIC MAYS,G 1 1 NSXC MURPHY,G.A 1 1 I h

D D

NOTE IO ALL "RIDS" RECIPIENT.

S PLEASE HELP US 'IO REDUCE WAS'! CORZACI'IHE DXXRKMl'OÃIRDLDESK, ROOM Pl-37 (EXT. 20079) M EIZKQCQZ RÃ3R KQK FKR DISTEKBUTXON LISTS FOR DOCUMENI'S YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 44 ENCL 43

P.O. Box14000, Juno Beach, Fl 33408-0420

.I 'we y ~

APRIL 2 1 I989 L-89-161 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

Re: Turkey Point Unit 3 Docket No. 50-250 Special Report Condenser Air Ejector High Range Noble Gas Monitor Ino erable for Greater than Seven Da s In accordance with Technical Specification 6.9.3 the attached Special Report is provided for your information.

Should there by any questions on this information, please contact US ~

Very truly yours, W. F. Co y Senior Vice President Nuclear WFC/JRH/cm Attachment cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 85'04260303 Sr/0421 PDR ADOCK 0 000250 PDC an FPL Group company

SPECIAL REPORT CONMNSER AIR EJECTOR HIGH RANGE NOBLE GAS MONITOR Puru os e Technical Specification 3.5, Table 3.5-5, item 13.c requires that if the condenser air ejector high range noble gas monitor is inoperable for greater than 7 days, FPL shall prepare and submit a special report to the Commission pursuant to Technical Specification 6.9.3 within 30 days following the event, outlining the action taken, the cause of the inoperability, and the plans and schedule for restoring the system to operable status'vent and Action Taken On March 22, 1989, at approximately 1115, the 'Unit 3 condenser air ejector high range noble gas monitor was removed from service in order to perform preventive maintenance and channel calibrations as required by the Technical Specifications .

At that time, the Chemistry Department initiated the preplanned alternate method of monitoring, as required by the Technical Specifications. On March 29, Unit 3 was shutdown, and therefore, the preplanned alternate method of monitoring was discontinued when the condenser air ejector was removed from service.

Cause of the Ino erabilit The Unit 3 condenser air ejector. high .range noble gas monitor was removed from service in order to perform preventive maintenance and channel calibrations as required by the Technical Specifications.

Schedule for Return of E ai ment The Unit 3 condenser air ejector high range noble gas monitor is scheduled to be returned to operable status prior to restart of Unit 3.