PNO-II-85-056, on 850517,reactor Tripped.Caused by Loss of Offsite Power Due to Fire Disabling 500-kV Line Near Util Substation.Unusual Event Declared.All Safety Sys Functioned Normally.Power Restored
ML20128A601 | |
Person / Time | |
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Site: | Turkey Point |
Issue date: | 05/17/1985 |
From: | Brownlee V, Dick G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
References | |
PNO-II-85-056, PNO-II-85-56, NUDOCS 8505240271 | |
Download: ML20128A601 (1) | |
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Category:PRELIMINARY NOTIFICATION OF EVENT OR OCCURRENCE (PNO
MONTHYEARPNO-II-93-052, on 930930,plant Commenced Unit Shutdown from 100% Power Due to RCS Leakage Through Pressurizer Manway Flange.Unit Currently in Mode 3 at Normal Operating Temp & Pressure1993-10-0101 October 1993
[Table view]PNO-II-93-052:on 930930,plant Commenced Unit Shutdown from 100% Power Due to RCS Leakage Through Pressurizer Manway Flange.Unit Currently in Mode 3 at Normal Operating Temp & Pressure PNO-II-93-040, on 930825,two Contractor Painters Struck by Lightning While Working on Turbine Deck in man-basket Approx 50-70 Ft Above Ground.No Damage Identified to Facility.State of Fl Notified1993-08-25025 August 1993 PNO-II-93-040:on 930825,two Contractor Painters Struck by Lightning While Working on Turbine Deck in man-basket Approx 50-70 Ft Above Ground.No Damage Identified to Facility.State of Fl Notified PNO-II-93-025, on 930610,controlled Shutdown from 100% Power to Mode 5 to Repair Secondary Steam Leak Began.Licensee Planning to Complete Repairs & Return Unit on Line as Early as 9306131993-06-10010 June 1993 PNO-II-93-025:on 930610,controlled Shutdown from 100% Power to Mode 5 to Repair Secondary Steam Leak Began.Licensee Planning to Complete Repairs & Return Unit on Line as Early as 930613 PNO-II-92-055C, on 920824,Hurricane Andrew Passed Directly Over Turkey Point Nuclear Plant W/Wind Reported as High as 140 Mph & Gusts Up to 152 Mph as Measure Before Meterological Equipment Disabled1992-09-0303 September 1992 PNO-II-92-055C:on 920824,Hurricane Andrew Passed Directly Over Turkey Point Nuclear Plant W/Wind Reported as High as 140 Mph & Gusts Up to 152 Mph as Measure Before Meterological Equipment Disabled PNO-II-92-055B, on 920830,offsite Power Was Restored to Four Safety Buses Following Loss of Offsite Power to Both Units on 920824,due to Hurricane Andrew1992-08-31031 August 1992 PNO-II-92-055B:on 920830,offsite Power Was Restored to Four Safety Buses Following Loss of Offsite Power to Both Units on 920824,due to Hurricane Andrew PNO-II-92-055A, on 920824,declaration Was Issued Declaring South Florida Disaster Area as Result of effe25X,per Governor L Chiles Request1992-08-27027 August 1992 PNO-II-92-055A:on 920824,declaration Was Issued Declaring South Florida Disaster Area as Result of effe25X,per Governor L Chiles Request PNO-II-92-055, on 920824,Turkey Point,Unit 3 & 4 Were Shutdown & in Mode 4 W/Hurricane Procedures in Effect.Units 3 & 4 Diesel Generator Manned.State of Fl,Fema,Doe & EPA Notified1992-08-24024 August 1992 PNO-II-92-055:on 920824,Turkey Point,Unit 3 & 4 Were Shutdown & in Mode 4 W/Hurricane Procedures in Effect.Units 3 & 4 Diesel Generator Manned.State of Fl,Fema,Doe & EPA Notified PNO-II-90-039, on 900723,const Worker Fell & Was Injured & Subsequently Transported by Helicopter to Local Hosp.Extent of Injuries Unknown.Injury Occurred Outside Protected Area at New Maint Bldg Under Const1990-07-23023 July 1990 PNO-II-90-039:on 900723,const Worker Fell & Was Injured & Subsequently Transported by Helicopter to Local Hosp.Extent of Injuries Unknown.Injury Occurred Outside Protected Area at New Maint Bldg Under Const PNO-II-88-030A, on 880517,during Police Interview,Security Officer at Turkey Point Admitted That Story Told Last Week of Exchanging Shots W/Three Unidentified Persons During Early Morning Hours of 880506 Near Plant False1988-05-17017 May 1988 PNO-II-88-030A:on 880517,during Police Interview,Security Officer at Turkey Point Admitted That Story Told Last Week of Exchanging Shots W/Three Unidentified Persons During Early Morning Hours of 880506 Near Plant False PNO-II-88-027, on 880415,ENERCON Svc,Inc Completed Independent Mgt Appraisal of Plant Nuclear Operations Per NRC Order EA 87-85.Licensee Issued News W/Appraisal on 880418 & Currently Reviewing Appraisal.State of Fl Informed1988-04-19019 April 1988 PNO-II-88-027:on 880415,ENERCON Svc,Inc Completed Independent Mgt Appraisal of Plant Nuclear Operations Per NRC Order EA 87-85.Licensee Issued News W/Appraisal on 880418 & Currently Reviewing Appraisal.State of Fl Informed PNO-II-88-005, on 880113,manual Reactor Trip Initiated Per off-normal Procedure.Caused by Loss of Power to Movable Gripper Coils.Unit Will Remain Down for Approx 10 Days Due to Pinhole Leak in Canopy Seal for Rod D-81988-01-15015 January 1988 PNO-II-88-005:on 880113,manual Reactor Trip Initiated Per off-normal Procedure.Caused by Loss of Power to Movable Gripper Coils.Unit Will Remain Down for Approx 10 Days Due to Pinhole Leak in Canopy Seal for Rod D-8 PNO-II-87-075, on 871021 & 25,voiding Noted in Vessel Head Regions.Caused by Mispositioned Manual Valve in Nitrogen Vent Line.Investigation Continuing1987-10-28028 October 1987 PNO-II-87-075:on 871021 & 25,voiding Noted in Vessel Head Regions.Caused by Mispositioned Manual Valve in Nitrogen Vent Line.Investigation Continuing PNO-II-87-074, on 870929,24 H Control Room Coverage Initiated by NRC in Response to Determination That Licensee Violated 10CFR50.54 by Allowing Nonlicensed Person to Manipulate Reactor Dilution Controls1987-10-26026 October 1987 PNO-II-87-074:on 870929,24 H Control Room Coverage Initiated by NRC in Response to Determination That Licensee Violated 10CFR50.54 by Allowing Nonlicensed Person to Manipulate Reactor Dilution Controls PNO-II-87-069, on 871012,Turkey Point Units 3 & 4 Declared NOUE Based on Potential for Hurricane Force Winds & Technical Support Ctr Activated for Mgt of Storm Preparation & Operations.St Lucie Also Made Severe Weather Preparations1987-10-13013 October 1987 PNO-II-87-069:on 871012,Turkey Point Units 3 & 4 Declared NOUE Based on Potential for Hurricane Force Winds & Technical Support Ctr Activated for Mgt of Storm Preparation & Operations.St Lucie Also Made Severe Weather Preparations PNO-II-87-062, on 870926,nonlicensed Person Not in Training Status Allowed to Manipulate Reactor Dilution Controls in Control Room.Cause Not Stated.Licensed Personnel Had Prepared Sys Properly for Manipulation of Controls1987-09-29029 September 1987 PNO-II-87-062:on 870926,nonlicensed Person Not in Training Status Allowed to Manipulate Reactor Dilution Controls in Control Room.Cause Not Stated.Licensed Personnel Had Prepared Sys Properly for Manipulation of Controls IR 05000250/19870161987-05-19019 May 1987 PNO-II-87-030:updating PNO-II-87-019 & PNO-II-87-019A. Augmented Insp Team Repts 50-250/87-16 & 50-251/87-16 on Boric Acid Leakage & Buildup Problem Issued on 870515.Loss of Offsite Power Test Scheduled for 870520 PNO-II-87-024, on 870407,Region II Ofc Received Anonymous Telcon Alleging That 14 Members of Bechtel Corp Work Crew Involved in Onsite Drug Use.On 870408,region Received Addl Telcon Alleging Drug Use by 5 Other Bechtel Employees1987-04-0909 April 1987 PNO-II-87-024:on 870407,Region II Ofc Received Anonymous Telcon Alleging That 14 Members of Bechtel Corp Work Crew Involved in Onsite Drug Use.On 870408,region Received Addl Telcon Alleging Drug Use by 5 Other Bechtel Employees PNO-II-87-017, media Interest Developed Re Air Lock Problem Identified When Routine Surveillance Test Indicated Minor Pressure Leakage on Inside Door of Personnel Lock.Unit to Be Retested & Returned to Svc1987-03-24024 March 1987 PNO-II-87-017:media Interest Developed Re Air Lock Problem Identified When Routine Surveillance Test Indicated Minor Pressure Leakage on Inside Door of Personnel Lock.Unit to Be Retested & Returned to Svc PNO-II-87-019A, on 870322,NRC Informed That Insp & NDT of Reactor Head Closure Studs Indicated Exterior Corrosion & Evidence of Internal Thread Wasting.Reactor Head Will Be Removed for Insp1987-03-23023 March 1987 PNO-II-87-019A:on 870322,NRC Informed That Insp & NDT of Reactor Head Closure Studs Indicated Exterior Corrosion & Evidence of Internal Thread Wasting.Reactor Head Will Be Removed for Insp PNO-II-87-020, on 870319,facility Made Critical,For First Time Since 861209,feed Sys Pipe Rupture.Extensive Replacement of Feedwater Piping in Both Units Completed & Program for Periodic Insp of Sys Instituted1987-03-20020 March 1987 PNO-II-87-020:on 870319,facility Made Critical,For First Time Since 861209,feed Sys Pipe Rupture.Extensive Replacement of Feedwater Piping in Both Units Completed & Program for Periodic Insp of Sys Instituted PNO-II-86-003, on 860107,unscheduled Shutdown Lasted Longer than 48 H Due to Damaged Steam Supply Stop Check Valve in Each Auxiliary Feedwater Sys Train.Remaining Valves Being Inspected1986-01-0808 January 1986 PNO-II-86-003:on 860107,unscheduled Shutdown Lasted Longer than 48 H Due to Damaged Steam Supply Stop Check Valve in Each Auxiliary Feedwater Sys Train.Remaining Valves Being Inspected PNO-II-85-112, on 851123,Limitorque Valve Motors Inside & Outside Containment Bldg Inspected After Util Determined That Some Motors May Not Be Environmentally Qualified.Unit Will Be Restarted.Insp of Unit 3 Motors Planned1985-11-25025 November 1985 PNO-II-85-112:on 851123,Limitorque Valve Motors Inside & Outside Containment Bldg Inspected After Util Determined That Some Motors May Not Be Environmentally Qualified.Unit Will Be Restarted.Insp of Unit 3 Motors Planned PNO-II-85-110A, on 851122,Hurricane Kate Downgraded to Tropical Storm.No Adverse Effects Occurred to Licensed Facilities in Storm Path1985-11-22022 November 1985 PNO-II-85-110A:on 851122,Hurricane Kate Downgraded to Tropical Storm.No Adverse Effects Occurred to Licensed Facilities in Storm Path PNO-II-85-110, on 851119,Hurricane Kate Centered Slightly Inland Over North Central Cuba,About 150 Miles South of Key West,Fl.Diesel Generators at All Three Sites Operable.Turkey Point Declared Unusual Event on 8511181985-11-19019 November 1985 PNO-II-85-110:on 851119,Hurricane Kate Centered Slightly Inland Over North Central Cuba,About 150 Miles South of Key West,Fl.Diesel Generators at All Three Sites Operable.Turkey Point Declared Unusual Event on 851118 PNO-II-85-097, on 851021,notification Received That Reactor Will Be Shut Down for Approx 8-10 Days to Repair Boot Seal Between Condenser & Low Pressure Turbine.Region II Will Conduct Routine Followup1985-10-21021 October 1985 PNO-II-85-097:on 851021,notification Received That Reactor Will Be Shut Down for Approx 8-10 Days to Repair Boot Seal Between Condenser & Low Pressure Turbine.Region II Will Conduct Routine Followup PNO-II-85-070, utils Contacted to Confirm That Progress of Tropical Storm Bob Being Followed as Result of Natl Weather Svc Upgrading from Tropical Depression to Tropical Storm1985-07-23023 July 1985 PNO-II-85-070:utils Contacted to Confirm That Progress of Tropical Storm Bob Being Followed as Result of Natl Weather Svc Upgrading from Tropical Depression to Tropical Storm PNO-II-85-056, on 850517,reactor Tripped.Caused by Loss of Offsite Power Due to Fire Disabling 500-kV Line Near Util Substation.Unusual Event Declared.All Safety Sys Functioned Normally.Power Restored1985-05-17017 May 1985 PNO-II-85-056:on 850517,reactor Tripped.Caused by Loss of Offsite Power Due to Fire Disabling 500-kV Line Near Util Substation.Unusual Event Declared.All Safety Sys Functioned Normally.Power Restored PNO-II-84-069A, update to PNO-II-84-069,issued on 841010. Region II Continues to Monitor Hurricane Josephine,Centered Near Latitude 29.4 North & Longitude 72.5 West1984-10-11011 October 1984 PNO-II-84-069A:update to PNO-II-84-069,issued on 841010. Region II Continues to Monitor Hurricane Josephine,Centered Near Latitude 29.4 North & Longitude 72.5 West PNO-II-84-039, on 840625,10 Gpm Primary Coolant Leak Inside Containment Bldg Caused Slight Increase in Pressure & Containment Radiation Levels.Reactor Placed in Cold Shutdown for Corrective Maint on Root Valve1984-06-25025 June 1984 PNO-II-84-039:on 840625,10 Gpm Primary Coolant Leak Inside Containment Bldg Caused Slight Increase in Pressure & Containment Radiation Levels.Reactor Placed in Cold Shutdown for Corrective Maint on Root Valve PNO-II-83-081, on 831012,FPL Took Unit Out Svc Because of Failure of One of Two Rhrps.Determined Rhrp Failure on 831011 Was Due to Short Circuit Caused by Water in Terminal Box Which Houses Pump Motor Leads1983-10-12012 October 1983 PNO-II-83-081:on 831012,FPL Took Unit Out Svc Because of Failure of One of Two Rhrps.Determined Rhrp Failure on 831011 Was Due to Short Circuit Caused by Water in Terminal Box Which Houses Pump Motor Leads PNO-II-82-086, on 820721,while at 100% Power,Reactor Tripped When Reactor Coolant a Tripped.Caused by Momentary Undervoltage Condition on 4160-volt Bus Which Supplies Reactor Coolant Pump Electrical Power1982-07-21021 July 1982 PNO-II-82-086:on 820721,while at 100% Power,Reactor Tripped When Reactor Coolant a Tripped.Caused by Momentary Undervoltage Condition on 4160-volt Bus Which Supplies Reactor Coolant Pump Electrical Power PNO-II-82-077B, updating PNO-82-077A Issued 820713.Unit Remains Shut Down for Insp of Secondary Side of Steam Generators for Presence of Foreign Matl.Efforts Underway to Remove Objects from Generators A,B & C1982-07-20020 July 1982 PNO-II-82-077B,updating PNO-82-077A Issued 820713.Unit Remains Shut Down for Insp of Secondary Side of Steam Generators for Presence of Foreign Matl.Efforts Underway to Remove Objects from Generators A,B & C ML20055B5861982-07-13013 July 1982 Updated PNO-II-82-077A:on 820707,eddy Current Exam Revealed No Denting in Steam Generator Tubes.Check Valve Pin from Feedwater Regulating Valve Bypass Line Recovered from Secondary Side of Generator PNO-II-82-077, on 820707,controlled Shutdown from 100% Power Initiated After Tube Leaks Developed in Steam Generator B. Leakage Rate Remained Below Tech Specs.Insp & Repairs Planned During Cold Shutdown on 8207081982-07-0707 July 1982 PNO-II-82-077:on 820707,controlled Shutdown from 100% Power Initiated After Tube Leaks Developed in Steam Generator B. Leakage Rate Remained Below Tech Specs.Insp & Repairs Planned During Cold Shutdown on 820708 PNO-II-82-062, on 820603,two Inspectors Dispatched to Plant to Suppl Resident Staff in Monitoring Operations If Hurricane Hit Plant.Inspectors Equipped W/High Frequency Radio Unit for Communicating During Adverse Weather1982-06-0404 June 1982 PNO-II-82-062:on 820603,two Inspectors Dispatched to Plant to Suppl Resident Staff in Monitoring Operations If Hurricane Hit Plant.Inspectors Equipped W/High Frequency Radio Unit for Communicating During Adverse Weather ML20216J7021978-09-0606 September 1978 PNO-78-160:on 780905,3,300 Gallons of Water Overflowed Into Cask Washdown Area & Storm Drain Sys.Cause of Incident Was Failure of Operator to Secure SFP Recirculation Pump After Making Valve Lineup to Equalize Canal & SFP Levels ML20249A5391978-07-18018 July 1978 PNS-78-035:on 780718,cardboard Box Containing an Apparent Explosive Device Was Found in Hot Machine Shop on Ground Floor of Auxiliary Bldg.Licensee Prepared to Initiate Controlled Shutdown of Both Units as Precaution ML20248L0131978-02-14014 February 1978 PNO-78-031:on 780214,unit Shutdown Commenced at 1:00pm Due to Apparent SG Tube Leak of 20.8 Gallons Per Hour.Unit Will Be Placed in Cold Shutdown Condition,Portion of RCS Will Be Drained & SG Will Be Tested to Identify Leaky Tubes ML20151X5321977-06-28028 June 1977 PNO-77-116:on 770625,notified That 10 Addl SG Tube Explosive Plugs Missing from Cold Leg Side of 4B Sg.Licensee Conducted Preliminary Investigation of 7 of Tubes & Plugs Were Not Inside.Plans Being Formulated for More Extensive Search ML20151U6771977-05-16016 May 1977 PNO-77-085:on 770516,TPS Unit 3 Reactor Tripped When RPS Received Signal That 3C Pump Had Tripped.Low Grid Voltage Caused Fossil Units to Trip.Slp Unit 1 Also Affected by Voltage Loss.Power Restored to Sys Grid from Fossil Units ML20249A9041977-03-21021 March 1977 PNS-77-009:on 770322,FP&L Maint Employee at Plant Arrested for Possession of Arms,Explosives & Narcotics.Fp&L Representatives Withdrew Security Badge to Assure That Individual Is Not Permitted Entry Into Plant ML20249A8621977-03-0202 March 1977 PNS-77-006:on 770225,two News Reporters Decided to Check Guard Alertness at Plant Following Announcement That Security Measures Would Be Increased at Nuclear Facilities. Reporters Got in & Out of Areas Before Seeing Guard ML20236F3381976-08-13013 August 1976 PNS-76-040:on 760812,pretrial Hearing Involving R Otero in Us District,Court,Jacksonville,Fl Revealed That Informants Had Told FBI That Otero Tried in Oct 1975 to Get Explosives from anti-Castro Terrorist Group to Use at Plant ML20236F5541976-04-23023 April 1976 PNS-76-014:on 760423,Radio Station Wftl,Ft Lauderdale,Fl, Reported to Util That Message Received by Radio Station,That Hidden Devices Placed at Key Areas of Turkey Point & Port Everglades Generating Plants.No Unidentified Objects Found ML20249B2281976-03-15015 March 1976 PNO-76-041:during Wk of 760308,reporter Contacted Region Re Proposed Enlargement of Sf Storage Capacity at Plant Site & Previous Repts of Water Leakage from Sf Pits.Details of Leak Submitted ML20236F4401976-03-0808 March 1976 PNS-76-010:on 760309,message Found in Back Door of Miami Herald,Broward County Ofc Stating That Hidden Devices Had Been Placed at Key Areas of Turkey Point & Everglades Generating Plants.No Unidentified Objects Were Located ML20249B0801976-02-10010 February 1976 PNO-76-022:on 760208,unmarked Twin Engine Cessna Airplane, Out of Fuel Crash Landed Approx 300 Yards South of Turkey Point Plants.Pilot Reported to Be in Custody of Police ML20236U0151975-04-15015 April 1975 PN-75-010:on 750414,Region II Notified by Licensee That Unplanned Release of Radioactive Liquid Occurred on 750413. No Apparent Threat to Health & Safety of Public Resulted. About 7400 Gallons of Water from SFP Released 1993-08-25 Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS MONTHYEARIR 05000250/19970091997-09-26026 September 1997
[Table view]Partially Withheld Insp Repts 50-250/97-09 & 50-251/97-09 on 970825-26.No Violations Noted.Major Areas Inspected: Insp Conducted in Area of Plant Support by Regional Safeguards Specialists ML20149E5981997-03-20020 March 1997 Partially Deleted Investigation Rept 2-96-027 on 970320.No Noncompliance Noted.Major Areas Investigated:Allegation Re Discrimination Against I&C Technician for Raising Safety Concern Re Calibr of Test Equipment IR 05000250/19970021997-03-0707 March 1997 Partially Withheld Insp Repts 50-250/97-02 & 50-251/97-02 on 970203-07 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Plant Support ML20136E5151997-03-0707 March 1997 Partially Withheld NOV on 970203-07 (Ref 10CFR73.21). Violations Noted:Employee Denied Unescorted Access & Was Not Provided Opportunity for Review of Info on Which Denial of Access Authorization Was Based PNO-II-93-052, on 930930,plant Commenced Unit Shutdown from 100% Power Due to RCS Leakage Through Pressurizer Manway Flange.Unit Currently in Mode 3 at Normal Operating Temp & Pressure1993-10-0101 October 1993 PNO-II-93-052:on 930930,plant Commenced Unit Shutdown from 100% Power Due to RCS Leakage Through Pressurizer Manway Flange.Unit Currently in Mode 3 at Normal Operating Temp & Pressure PNO-II-93-040, on 930825,two Contractor Painters Struck by Lightning While Working on Turbine Deck in man-basket Approx 50-70 Ft Above Ground.No Damage Identified to Facility.State of Fl Notified1993-08-25025 August 1993 PNO-II-93-040:on 930825,two Contractor Painters Struck by Lightning While Working on Turbine Deck in man-basket Approx 50-70 Ft Above Ground.No Damage Identified to Facility.State of Fl Notified ML20056E6661993-08-12012 August 1993 Notice of Violation from Insp on 930712-16.Violations Noted: Work Procedure Used for Overhaul of 3B Charging Pump & Pull of Motor Lead Cables Inadequate to Assure Important Activities Satisfactorily Accomplished IR 05000250/19930201993-08-10010 August 1993 Insp Repts 50-250/93-20 & 50-251/93-20 on 930712-16. Violations Noted.Major Areas Inspected:Area of Electrical Maint PNO-II-93-025, on 930610,controlled Shutdown from 100% Power to Mode 5 to Repair Secondary Steam Leak Began.Licensee Planning to Complete Repairs & Return Unit on Line as Early as 9306131993-06-10010 June 1993 PNO-II-93-025:on 930610,controlled Shutdown from 100% Power to Mode 5 to Repair Secondary Steam Leak Began.Licensee Planning to Complete Repairs & Return Unit on Line as Early as 930613 IR 05000250/19920331992-12-23023 December 1992 Insp Repts 50-250/92-33 & 50-251/92-33 on 921130-1204.No Violations or Deviations Noted.Major Areas Inspected. Physical Barriers,Intrusion Detection Alarms,Communication & Training & Qualification Plan.Rept Partially Withheld PNO-II-92-055C, on 920824,Hurricane Andrew Passed Directly Over Turkey Point Nuclear Plant W/Wind Reported as High as 140 Mph & Gusts Up to 152 Mph as Measure Before Meterological Equipment Disabled1992-09-0303 September 1992 PNO-II-92-055C:on 920824,Hurricane Andrew Passed Directly Over Turkey Point Nuclear Plant W/Wind Reported as High as 140 Mph & Gusts Up to 152 Mph as Measure Before Meterological Equipment Disabled PNO-II-92-055B, on 920830,offsite Power Was Restored to Four Safety Buses Following Loss of Offsite Power to Both Units on 920824,due to Hurricane Andrew1992-08-31031 August 1992 PNO-II-92-055B:on 920830,offsite Power Was Restored to Four Safety Buses Following Loss of Offsite Power to Both Units on 920824,due to Hurricane Andrew PNO-II-92-055A, on 920824,declaration Was Issued Declaring South Florida Disaster Area as Result of effe25X,per Governor L Chiles Request1992-08-27027 August 1992 PNO-II-92-055A:on 920824,declaration Was Issued Declaring South Florida Disaster Area as Result of effe25X,per Governor L Chiles Request PNO-II-92-055, on 920824,Turkey Point,Unit 3 & 4 Were Shutdown & in Mode 4 W/Hurricane Procedures in Effect.Units 3 & 4 Diesel Generator Manned.State of Fl,Fema,Doe & EPA Notified1992-08-24024 August 1992 PNO-II-92-055:on 920824,Turkey Point,Unit 3 & 4 Were Shutdown & in Mode 4 W/Hurricane Procedures in Effect.Units 3 & 4 Diesel Generator Manned.State of Fl,Fema,Doe & EPA Notified IR 05000250/19910331991-08-29029 August 1991 Insp Repts 50-250/91-33 & 50-251/91-33 on 910819-23.No Violations Noted.Major Areas Inspected:Training & Surveillance Testing for Upgrade of Emergency Power Sys & Followup of Previously Identified Items ML20138F6711991-04-18018 April 1991 Notice of Violation from Insp on 910225-0301.Violation Noted:On 910225-26,licensee Failed to Follow Procedures for Labeling Resin Liners Having Contact Dose Rates Exceeding 1.5 Mrem/Hr Which Were Maintained in Storage Area IR 05000250/19910081991-04-18018 April 1991 Insp Repts 50-250/91-08 & 50-251/91-08 on 910225-0301. Violations Noted.Major Areas Inspected:Outage HP Acs, Employee Training & Qualifications,Personnel Exposure Monitoring & Assessments & Radioactive Matl IR 05000250/19910101991-04-12012 April 1991 Insp Repts 50-250/91-10 & 50-251/91-10 on 910304-08 & 18-22. No Violations Noted.Major Areas Inspected:Procedures,Work Activities & Quality Records Pertaining to Erection of Structural Steel in New Diesel Generator Bldg IR 05000250/19910061991-02-25025 February 1991 Partially Withheld Insp Repts 50-250/91-06 & 50-251/91-06 on 910128-0201.No Violations or Deviations Noted.Major Areas Inspected:Mgt Support,Protected Area Physical Barriers, Status of Security Upgrade Program & Packages & Vehicles ML20059N3511990-09-21021 September 1990 Notice of Violation from Insp on 900804-31.Violation Noted: Administrative Policies Not Established to Control Changes to Master Instrument Calibr Data Sheet for Component Cooling Water Pump Automatic Start Pressure Switch PNO-II-90-039, on 900723,const Worker Fell & Was Injured & Subsequently Transported by Helicopter to Local Hosp.Extent of Injuries Unknown.Injury Occurred Outside Protected Area at New Maint Bldg Under Const1990-07-23023 July 1990 PNO-II-90-039:on 900723,const Worker Fell & Was Injured & Subsequently Transported by Helicopter to Local Hosp.Extent of Injuries Unknown.Injury Occurred Outside Protected Area at New Maint Bldg Under Const IR 05000250/19890421989-09-21021 September 1989 Partially Withheld Insp Repts 50-250/89-42 & 50-251/89-42 on 890828-0901 (Ref 10CFR2.790(d) & 73.21).No Violations or Deviations Noted.Major Areas Inspected:Security Plan & Implementing Procedures & Security Organization IR 05000250/19890331989-08-0909 August 1989 Partially Withheld Insp Repts 50-250/89-33 & 50-251/89-33 on 890717-21 (Ref 10CFR2.790(d) & 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Mgt Effectiveness, Physical Barriers,Assessment Aids & Personnel Training IR 05000250/19890301989-07-27027 July 1989 Partially Withheld Insp Repts 50-250/89-30 & 50-251/89-30 on 890614-16 (Ref 10CFR2.790(d) & 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Access Control of Personnel,Packages,Vehicles & Alarm Stations IR 05000250/19890211989-06-0101 June 1989 Partially Withheld Insp Repts 50-250/89-21 & 50-251/89-21 on 890424-28 (Ref 10CFR2.790 & 73.21).Violations Noted.Major Areas Inspected:Mgt Support & Security Program Plans & Protected & Vital Area Physical Barriers IR 05000250/19890031989-03-0808 March 1989 Insp Repts 50-250/89-03 & 50-251/89-03 on 890206-10. Violations Noted.Major Areas Inspected:Access Control to Protected Vital Areas,Records & Repts,Compensatory Measures & Protection of Safeguards Info ML20235U2121989-02-24024 February 1989 Notice of Violation from Insp on 890117-20.Violation Noted: Licensee Failed to Promptly Classify Event Involving Unit 3 RCS Leakage Greater than 50 Gpm & to Make Timely Notification to State of Fl & NRC IR 05000250/19880151988-11-18018 November 1988 Corrected Pages to SALP Repts 50-250/88-15 & 50-251/88-15 for June 1987 - June 1988 PNO-II-88-030A, on 880517,during Police Interview,Security Officer at Turkey Point Admitted That Story Told Last Week of Exchanging Shots W/Three Unidentified Persons During Early Morning Hours of 880506 Near Plant False1988-05-17017 May 1988 PNO-II-88-030A:on 880517,during Police Interview,Security Officer at Turkey Point Admitted That Story Told Last Week of Exchanging Shots W/Three Unidentified Persons During Early Morning Hours of 880506 Near Plant False PNO-II-88-027, on 880415,ENERCON Svc,Inc Completed Independent Mgt Appraisal of Plant Nuclear Operations Per NRC Order EA 87-85.Licensee Issued News W/Appraisal on 880418 & Currently Reviewing Appraisal.State of Fl Informed1988-04-19019 April 1988 PNO-II-88-027:on 880415,ENERCON Svc,Inc Completed Independent Mgt Appraisal of Plant Nuclear Operations Per NRC Order EA 87-85.Licensee Issued News W/Appraisal on 880418 & Currently Reviewing Appraisal.State of Fl Informed ML20196B8921988-02-0808 February 1988 EN-88-008:on 880211,notice of Proposed Imposition of Civil Penalty in Amount of $150,000 Issued to Licensee.Action Based on Two Severity Level III Violations Involving Multiple Failures to Maintain Positive Access Control PNO-II-88-005, on 880113,manual Reactor Trip Initiated Per off-normal Procedure.Caused by Loss of Power to Movable Gripper Coils.Unit Will Remain Down for Approx 10 Days Due to Pinhole Leak in Canopy Seal for Rod D-81988-01-15015 January 1988 PNO-II-88-005:on 880113,manual Reactor Trip Initiated Per off-normal Procedure.Caused by Loss of Power to Movable Gripper Coils.Unit Will Remain Down for Approx 10 Days Due to Pinhole Leak in Canopy Seal for Rod D-8 ML20236J9531987-11-0505 November 1987 EN-87-060A:on 871105,order Imposing Civil Penalty in Amount of $75,000 Issued to Licensee Based on Two Violations Re Access Control & Search.Nrc Concluded That Violation Did Occur Following Review of Util 870826 Response PNO-II-87-075, on 871021 & 25,voiding Noted in Vessel Head Regions.Caused by Mispositioned Manual Valve in Nitrogen Vent Line.Investigation Continuing1987-10-28028 October 1987 PNO-II-87-075:on 871021 & 25,voiding Noted in Vessel Head Regions.Caused by Mispositioned Manual Valve in Nitrogen Vent Line.Investigation Continuing PNO-II-87-074, on 870929,24 H Control Room Coverage Initiated by NRC in Response to Determination That Licensee Violated 10CFR50.54 by Allowing Nonlicensed Person to Manipulate Reactor Dilution Controls1987-10-26026 October 1987 PNO-II-87-074:on 870929,24 H Control Room Coverage Initiated by NRC in Response to Determination That Licensee Violated 10CFR50.54 by Allowing Nonlicensed Person to Manipulate Reactor Dilution Controls ML20236A1511987-10-15015 October 1987 EN-87-086:on 871019,order & Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $225,000 Will Be Issued Based on Loss of Emergency Boration Flow Paths & Failure of Personnel to Follow Procedures PNO-II-87-069, on 871012,Turkey Point Units 3 & 4 Declared NOUE Based on Potential for Hurricane Force Winds & Technical Support Ctr Activated for Mgt of Storm Preparation & Operations.St Lucie Also Made Severe Weather Preparations1987-10-13013 October 1987 PNO-II-87-069:on 871012,Turkey Point Units 3 & 4 Declared NOUE Based on Potential for Hurricane Force Winds & Technical Support Ctr Activated for Mgt of Storm Preparation & Operations.St Lucie Also Made Severe Weather Preparations PNO-II-87-062, on 870926,nonlicensed Person Not in Training Status Allowed to Manipulate Reactor Dilution Controls in Control Room.Cause Not Stated.Licensed Personnel Had Prepared Sys Properly for Manipulation of Controls1987-09-29029 September 1987 PNO-II-87-062:on 870926,nonlicensed Person Not in Training Status Allowed to Manipulate Reactor Dilution Controls in Control Room.Cause Not Stated.Licensed Personnel Had Prepared Sys Properly for Manipulation of Controls ML20236D7571987-07-23023 July 1987 EN-87-060:on 870728,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000 Will Be Issued.Action Based on Violations Re Failure to Maintain Positive Access Control Over Personnel & Equipment ML20236D4291987-07-16016 July 1987 EN-87-057:on 870721,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $100,000 Will Be Issued Based on Licensee Failure to Take Prompt Corrective Action for Reactor Coolant Leak IR 05000250/19870161987-05-19019 May 1987 PNO-II-87-030:updating PNO-II-87-019 & PNO-II-87-019A. Augmented Insp Team Repts 50-250/87-16 & 50-251/87-16 on Boric Acid Leakage & Buildup Problem Issued on 870515.Loss of Offsite Power Test Scheduled for 870520 ML20213A7261987-04-16016 April 1987 EN-87-032:on or About 870421,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000 Will Be Issued for Licenses.Action Based on Violations of Physical Security Plan Involving Sleeping Guard & Unescorted Visitor PNO-II-87-024, on 870407,Region II Ofc Received Anonymous Telcon Alleging That 14 Members of Bechtel Corp Work Crew Involved in Onsite Drug Use.On 870408,region Received Addl Telcon Alleging Drug Use by 5 Other Bechtel Employees1987-04-0909 April 1987 PNO-II-87-024:on 870407,Region II Ofc Received Anonymous Telcon Alleging That 14 Members of Bechtel Corp Work Crew Involved in Onsite Drug Use.On 870408,region Received Addl Telcon Alleging Drug Use by 5 Other Bechtel Employees PNO-II-87-017, media Interest Developed Re Air Lock Problem Identified When Routine Surveillance Test Indicated Minor Pressure Leakage on Inside Door of Personnel Lock.Unit to Be Retested & Returned to Svc1987-03-24024 March 1987 PNO-II-87-017:media Interest Developed Re Air Lock Problem Identified When Routine Surveillance Test Indicated Minor Pressure Leakage on Inside Door of Personnel Lock.Unit to Be Retested & Returned to Svc PNO-II-87-019A, on 870322,NRC Informed That Insp & NDT of Reactor Head Closure Studs Indicated Exterior Corrosion & Evidence of Internal Thread Wasting.Reactor Head Will Be Removed for Insp1987-03-23023 March 1987 PNO-II-87-019A:on 870322,NRC Informed That Insp & NDT of Reactor Head Closure Studs Indicated Exterior Corrosion & Evidence of Internal Thread Wasting.Reactor Head Will Be Removed for Insp PNO-II-87-020, on 870319,facility Made Critical,For First Time Since 861209,feed Sys Pipe Rupture.Extensive Replacement of Feedwater Piping in Both Units Completed & Program for Periodic Insp of Sys Instituted1987-03-20020 March 1987 PNO-II-87-020:on 870319,facility Made Critical,For First Time Since 861209,feed Sys Pipe Rupture.Extensive Replacement of Feedwater Piping in Both Units Completed & Program for Periodic Insp of Sys Instituted IR 05000250/19870111987-03-20020 March 1987 Partially Withheld Enforcement Conference Repts 50-250/87-11 & 50-251/87-11 on 870223 (Ref 10CFR2.790 & 73.21).Repts Address Followup Insp on 870303-04.Violations Noted:Failure to Provide Positive Control of Visitors ML20207T7141987-03-11011 March 1987 Notice of Violation from Insp on 870112-0209 IR 05000250/19870061987-03-0505 March 1987 Insp Repts 50-250/87-06 & 50-251/87-06 on 870112-0209. Violations Noted:Failure to Correct Conditions Adverse to Quality & Failure to Establish & Implement Adequate Procedures ML20207T4441987-02-20020 February 1987 Accelerated Requalification Exam Rept 50-250/OL-86-05 on 861215-17.Exam Results:Three of Eight Senior Reactor Operators Passed.Exam Questions & Answer Key & Util Comments Encl 1997-09-26 |
m s
May 17, 1985
' PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PNO-II-85-56 This preliminary notification. constitutes EARLY notice _of events of POSSIBLE safety or public. interest significance. The information is as initially. received without verifi-Ecation or evaluation,;and is basically all that is known by the Region II staff on this data.
- FACILITY
- 1 Florida Power and Light Company- Licensee Emergency Classification:
Turkey Point Units 3 and 4 X Notification of Unusual Event Docket Nos. 50-250 and 50-251 Alert
- Homestead, Florida Site Area Emergency General Emergency Not Applicable
SUBJECT:
-LOSS'0F 0FF-SITE POWER AND 'SDESPREAD POWER OUTAGE Turkey Point Unit 4, which was operating' at 100 percent power, tripped at 11:40 a.m. (EDT)
. today because of. a loss of off-site power. The power loss was caused by a fire which (disabled a 500-KV transmission line near Florida Power and Light's (FPL) Andytown
- substation .in. central Florida. The loss of this substation caused a cascading power loss.
. cffect which interrupted electricity service to about 1.5 million customers from Palm Beach
< s::uth through' the Miami area, affecting the off-site. power supply to Turkey _ Point. Unit 3 is shutdown for refueling. The power interruption also tripped oil-fired Turkey Point Units 1 and 2.
FPL'd'eclared'an unusual event at noon and terminated it at.2:07 p.m. All safety systems,-
- including the. emergency diesel generators, functioned as required.
Off-site power was restored to Turkey Point Unit 4 by approximately 1:55 p.m. and to Unit 3 ~
by 2:30 p.m. as. power was being generally restored to the south Florida area.
Media interest has occurred. Both FPL and NRC have responded to inquiries.
.Thi-State of. Florida has been informed.
~FPLTinformed the'NRC headquarters duty officer of this incident by telephone at 12:18 p.m.-
"today.-
Ctntact: G. Pick, 842-3187 V. Brownlee, 242-5583 DISTRIBUTION-MNBB MAIL:
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,Com. Asselstine MPA AE0D Applicable State -
Comm.-Bernthal ELD
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Licensee: T,56 (ReactorLicensees) i Applicable Resident Site 3,. 6]
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