ML20129A987

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Monthly Operating Repts for Sept 1996 for Peach Bottom Unit 2 & 3
ML20129A987
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 09/30/1996
From: Hydrick L, Warner M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9610220298
Download: ML20129A987 (14)


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PECO NUCLEAR e= =< c-1848 Lay Road A UNtrl#PECO ENrkcy Delta. PA 17314 9032 i 717 456 7o14 t

October 7,1996 U.S. Nuclear Regulatory Ccaudssion Document Control Desk Washington, D.C. 20555 Dor,ket Nos. 50-277 and 50-278

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Enc'esbd is the monthly operating report for Peach Bottom Units 2 and 3 for the month of September 1996 forwarded pursuant to Technical Specification 5.6.4 under the guidance of Regulatory Guide 10.1, Revision 4.

Sincerely, Nk Mark E. Wamer -

Director, Site Engineering i Peach Bottom Atomic Power Station  !

d6N MEW /JGH:lph Enclosures i B.W. Gorman, Public Service Electric & Gas cc:

W.P. Domsife, Commonwealth of Pennsylvania R.I. McLean, State of Maryland T.T. Martin, Administrator, Region I, USNRC W.L. Schmidt, USNRC, Senior Resident inspector i H.C, Schwemm, Atlantic Electric  !

A.F Kirby,Ill, Delmarva Power & Light l INPO Records Center T. N. Mitchell, PECO Nuclear, Vice President, Peach Bottom Atomic Power Station l 220104 9610220298 960930 DR ADOCK0500g7 p'

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ccn 96-14079 i

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PEACH COTTOM ATOMIC POWER STATION i NRC MONTHLY OPERATIONS

SUMMARY

l SEPTEMBER 1996 I

UNIT 2  :

Unit 2 began the month of September at 53% power. Prior to 2R11 Refueling Outage the average power for the month was 50.24%. The majority of the Megawatt losses prior to 2R11 were a result ,

of the Unit coastdown. In addition, there were minimallosses due to leaking valves. On 9/13/96 l the Unit came off-line to commence the Refueling Outage.  !

Unit 2 net generation for September was 147,646 MWH. I i

, UNIT 3 I l

Unit 3 began the month of September at 100% power. Unit 3 Mega.vatt losses included a load drop for condenser water box cleaning on 9/11/96. The Unit remained at 100% power for the rest

, of the month.

Unit 3 net generation for September was 795,554 MWH.

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Attachment to Monthly Operating Report for September 1996 UNIT 2 REFUELING INFORMATION

1. Name of facility:

Peach Bottom Unit 2

2. Scheduled date for next refueling shutdown:

Reload 11 began September 13,1996.

3. Scheduled date for restart following refueling:

Restart following refueling forecast for October 4,1996.

4. Will refueling or resumption of operation therefore require a technical specification change or other ,

license amendment?

Yes.

If answer is yes, what, in general, will these be?

1,10CFR50 Appendix J, Option B

2. Increase MCPR Value
5. Scheduled date(s) for submitting proposed licensing action and supporting information:

Items 1 and 2 have been submitted for review and approval. NRC approval has been received.

6. Important licensing considerations associated with refueling, e g., new or drfferent fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:

GE-13 Fuel Product Line will be utilized requiring a Tech Spec amendment.

7. The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:

(a) Core- 764 Fuel Assemblies (b) Fuel Pool- 2720 Fuel Assemblies,52 Fuel Rods

Docket No. 50-277 Attachment to Monthly Operating Report for September 1996 Page 2. ,

I UNIT 2 REFUELING INFORMATION (Continued)

8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 3819 fuel assemblies.  :

9. The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present capacity: ,

September 2002 without full core omoad capability.

September 1998 with full core omoad capibility.

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Dockit No. 50-278 Attachment to Monthly Operating Report for September 1996 ilNIT 3 REFUELING INFORMATION

1. Name of facility:

Peach Bottom Unit 3

2. Scheduled date for next refueling shutdown:

Reload 11 scheduled for September 12,1997

3. Scheduled date for restart following refueling Restart following refueling scheduled for October 11,1997
4. Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?

N/A If answer is yes, what, in general, will these be?

5. Scheduled date(s) for submitting proposed licensing action and supporting information:
6. Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, j new operating procedures:

N/A l

7. The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:

(a) Core - 764 Fuel Assemblies (b) Fuel Pool - 2485 Fuel Assemblies,16 Fuel Rods

8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:  !

The spent fuel pool storage capacity has been relicensed for 3819 fuel assemblies.

Dock".t No. 50-278 Attachment to Monthly Operating Report for September 1996 Page 2 ,

UNIT 3 REFUELING INFORMATION (Continued)

9. Tlw projected date of the last refueling that can be discharged to the spent fuel pool assuming the present capacity:- ,

September 2003 without full core offload capability.

September 1999 with full core offload capability.

AVERAGE DAILY POWER LEVEL '.

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DOCKET NO 50 - 277 ,

UNIT PEACH BOTTOM UN!T2 DATE ' OCTOSER 8,1996 .

COMPANY PECO ENENGY COMPANY L P. HYDRfCK BUSINESS SERVICES SITE SUPPORT DIVISION PEACH BOTTOM ATOteC POWER STATION TELEPHONE - (717) 456-4383 MONTH SEPTEMBER,1996 DAY AVERAGE DAILY POWER LEVEL DAY- AVERAGE DAILY POWER LEVEL (MWE-NET) . (MWE-NET) 1 507 17 0 2 503 18 0 3 499 19 0 4 494 20 0 5 495 21 0 6 400 22 0 7 486 23 - 0 8 486 24 0' 9 406 25 0 10 490 26 0 11 478 27 0 12 479 28 0 13 361 29 0 14 0 30 0 15 0 16 0

AVERAGE DAILY POWER LEVEL '.

DOCKET NO 50-275 '

UNIT PEACH BOTTOM UNIT 3 DATE OCTOBER 8,1996 .

COMPANY PECO ENERGY COMPANY L P. HYDRICK BUSINESS SERVICES SITE SUPPORT DMSION PEACH BOTTOM ATOMIC POFJ1 STATION TELEPHONE (717)4564383 MONTH SEPTEMBER,1996 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-NET) (MWE-NET) 1 1097 17 1114 2 1097 18 1113 3 1097 '19 1119 4 1093 20 1107 5 1097 21 1114 6 1097 22 1120 7 1097 23 1117 8 1101 24 1116 9 1097 25 1112 10 1089 26 1116 11 1037 27 1116 12 1102 28 1115 13 1110 29 1118 14 1107 30 1110 15 1109 16 1110

r OPERATING DATA REPORT .

DOCKET NO. 50 -277 . ,

DATE OCTOBER 8,1996 COMPLETED BY PECO ENERGY COMPANY L P. HYDRICK BUSINESS SERVICES SITE SUPPORT DIVISION PEACH BOTTOM ATOMIC POWER STATION TELEPHONE (717)456 4383 OPERATING STATUS

1. UNIT NAME _ _ _ , _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _P_EACH BOTT_OM_ UNIT ;

NOTES:

2. REPORTING PERIOD: , _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _SEPTEMB E_Rit_996,
3. UCENSED THERMAL POWER (MWT). _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _3458
4. HAMEPLATE RATING (GROSS MWE): __ _ _ __ _ __ __ __ _ _ _ __ _ __ _ __ _ _ _ _ __1_221 S. DESIGN ELECTRICAL RATING (NET MWE): __________________________11_19
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): __________________ ,__1159
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): ,______________________1_093
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THROUGH 7 ) SINCE LAST REPORT, GIVE REASONS:
9. POWER LEVELTO WHICH RESTRICTED,IF ANY(NET MWE).
10. REASONS FOR RESTRICTIONS,IF ANY:

THIS MONTH YR-TO-DATE CUMULATIVE

11. HOURS IN REPORTING PERIOD 720 6,575 194.975
12. NUMBER OF HOURS REACTOR WAS CRITICAL 310 0 6,165.0 128,760.5
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 00 00
14. HOURS GENERATOR ON-LINE 310.0 6,165.0 124,766.2
15. UNIT RESERVE SHUTDOWN HOURS 00 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MNH) 542,076 17,727,278 375,303,321
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 160,700 ~ 5,729,100 123,268,890
18. NET ELECTRICAL ENERGY GENERATED (MWH) 147,646 5,521,107 118.327,003 PAGE 1 OF 2

t OPERATING DATA REPORT (CONTINUED)

  • DOCKET NO_ . 50 -277 DATE OCTOBER 8,1996 THIS MONTH YR-TO-DATE CUMULATIVE
19. UNIT SERVICE FACTOR ' 43.1 % 93.8 % 64.0 %
20. UNIT AVAILABILITY FACTOR - 43.1 % 938% 64.0 % ~
21. UNIT CAPACITY FACTOR (USING MDC NET) 18.8 % 76.8 % 57.4 %
22. UNIT CAPACITY FACTOR (USING DER NET) 18.3 % 75.0 % 56.6 %
23. UNIT FORCED OUTAGE RATE .0 % .0 % 11.7 %
24. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE. DATE AND DURATION OF EACH):

Refueling culage began 9f13/96 -

25. IF SHUTDOWN AT THE END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP. 1004/96
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATIONS): FORECAST ~ ACHIEVED INITIAL CRITICALITY 09/16f73 INITIAL ELECTRICITY 02/18/74 COMMERCIAL OPERATION 07 2 /74

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OPERATING DATA REPORT '

DOCKET NO. ' 50-278 ,

DATE OCTOBER 8,1996 COMPLETED BY PECO ENERGY COMPANY ,

L P. HYDRICK BUSINESS SERVICES .

SITE SUPPORT DIVISION PEACH BOTTOM ATOMIC POWER STATION .

TELEPHONE (717)456-4383 OPERATINA TATUS

1. UNIT NAME: _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _P_EACH BOTTO_M_U NIT 3 NOTES:
2. REPORTING PERIOD: _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ , , _ _ _ _ _ _ _ _ _ _ _ _ _SEPTEMB E_R 1_996 1
3. LICENSED THERMAL POWER (MWT). _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _3458 4 NAMEPLATE RATING (GROSS MWE): __ ,____ ,___________ ______,, ,___1221,
5. DESIGN ELECTRICAL RATING (NET MWE): __________ ,_______________11_19
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): ,____________________1159,
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): _____________________,_1_093, 8 IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THROUGH 7 ) SINCE LAST REPORT, GIVE REASONS:
9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE): i i

10 REASONS FOR RESTRICTIONS,IF ANY'.

THIS MONTH YR-TO-DATE CUMULATIVE t

11. HOURS IN REPORTING PERIOD 720 6,575 190.871 i
12. NUMBER OF HOURS REACTOR WAS CRITICAL 720.0 6,486.1 127,773.3
13. REACTOR RESERVE SHUTDOWN HOURS 00 0.0 0.0
14. HOURS GENERATOR ON-LINE 720.0 6,418.0 124,226.2 I
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MWH) 2,482,785 21,742,287 371,428,745
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 821,100 7,178,000 121,797,432
18. NET ELECTRICAL ENERGY GENERATED (MWH) 795.554 6,971,718 116,985.570 PAGE 10F 2

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A OPERATING DATA REPORT (CONTINUED)

DOCKET NO. 50 - 278 DATE OCTOBER 8,1996

  • THIS MONTH YR-TO-DATE CUMULATIVE
19. UNIT SERVICE FACTOR 100.0 % 97.6 % - 85.1 %
20. UNIT AVAILABOUTY FACTOR 100.0 % 97.6 % 85.1 % -
21. UNIT CAPACITY FACTOR (USING MDC NET) 101.1 % 97.0 % 59.0 %  !
22. UNIT CAPACITY FACTOR (USING DER NET) 98 7 % 94.8 % 57.3 % <
23. UNIT FORCED OUTAGE RATE .0 % 2.4 % 10.6 % -

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24. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH): ,
25. IF SHUTDOWN AT THE END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

.26. UNITS IN TEST STATUS (PRIOR TO Cole 4ERCIAL OPERATIONS): FORECAST ACHIEVED INITIAL CRITICALITY 0807/74 IAITIAL ELECTRICITY 0901/74 i COlm4ERCIAL OPERATION -12/23/74

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__._.u..m. _ _ _ . o__ . _ . ._______m.__,__.__m. . _ -_..m_ . _ _ _ - . _ _-__ _ _ _ _ _ _ . _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _s c . ,, _ m h.~. , , i- ,--vv+- +% - - - , . .

UNIT SHUTDOWNS AND POWER REDUCTIONS '-

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- DOCKET NO.' 50-277

  • UNIT NAE PEACH BOTTOM UNIT 2
  • DATE OCTOBER B.1996 COMPLETED BY PECO ENERGY COMPANY L P. HYDRICK BUSINESS SERVICES SITE SUPPORT DMSM)N PEACH BOTTOM ATOMIC POWER STATION REPORT MONTH SEPTEMBER,1996 TELEPHONE (717)456-4383 METHOD OF LICENSEE SYSTEM COMPONENT CAUSE AND CORRECTIVE -

TYPE DURATION REASON SHUTTING DOWN EVENT CODE CODE ACTION TO NO. DATE (1) (HOURS) (2) REACTOR (3) REPORT # (4) (5) PREVENT RECURRENCE 18 960913 S 410_0 C 2 ZZ 777777 Refuehng Outage-2R11 TOTAL. HOURS 410.0 T

l (1) (2) (3) (4)

F-FORCED REASON METHOD EXHIBIT G -INSTRUCTIONS S-SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 -MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2-MANUAL SCRAM ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER)

D - REGULATORY RESTRICTION 4- OTHER (EXPLAIN) FILE (NUREG4161)

E - OPERATOR TRAINING + LICENSE EXAMINATION

F- ADMINISTRATIVE (5)

G - OPERATIONAL ERROR (EXPLAIN) EXHIBIT I-SAME SOURCE H - OTHER (EXPLAIN) i

_ _ _ _ . _ _ _ = _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____ ., . . . . . . . . . - _ _ . - - .._

UNIT SHUTDOWNS AND POWER REDUCTIONS *o DOCKET NO. 50-278 *

- UN!T NAME PEACH BOTTOM UNIT 3 DATE OCTOBER 8,1996 - .

, COMPLETED BY PECO ENERGY COMPANY L P. HYDRICK BUSINESS SERVICES SITE SUPPORT DMSION PEACH BOTTOM ATOMIC POWER STATION REPORT MONTH SEPTEMBER,1996 . TELEPHONE ' (717) 456-4383 METHOD OF LICENSEE SYSTEM COMPONENT CAUSE AND CORRECTIVE TYPE DURATION REASON SHUTTING DOWN EVENT CODE CODE' ACTION TO NO. DATE- (1) (HOURS) (2) REACTOR (3) REPORTS (4) (5) PREVENT RECURRENCE 20 960910 S 5.0 B 4 HC XXXXXX Condenser Walerta Cleenmg Reackr not shit down TOTAL HOURS 5.0 l

l (1) (2) (3) (4) l F-FORCED REASON METHOD EXHIBIT G-INSTRUCTIONS S- SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARAFA OF DATA B - MAINTENANCE OR TEST 2 -MANUAL SCRAM ENTRY SHEET S FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPCRT (LER)

D - REGULATORY RESTRICTION 4 -OTHER (EXPLAIN) FILE (NUREG-0161)

E - OPERATOR TRAINING + LICENSE EXAMINATION F - ADMINISTRATIVE (5)

, G- OPERATIONAL ERROR (EXPLAIN) EXHIBIT I- SAME SOURCE H - OTHER (EXPLAIN)

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