ML112240223

From kanterella
Jump to navigation Jump to search
IR 05000482-11-003 & Notice of Violation, on 04/1/2011 6/30/2011, Wolf Creek Generating Station, Integrated Resident Report, Adverse Weather Protection, Equipment Alignments, Inservice Inspection Activities, Post Maintenance Testing, Event
ML112240223
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 08/12/2011
From: Geoffrey Miller
NRC/RGN-IV/DRP/RPB-B
To: Matthew Sunseri
Wolf Creek
References
EA-11-149 IR-11-003
Download: ML112240223 (103)


See also: IR 05000482/2011003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

August 12, 2011

EA-11-149

Matthew Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Subject: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION

REPORT AND NOTICE OF VIOLATION 05000482/2011003

Dear Mr. Sunseri:

On June 30, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Wolf Creek Generating Station. The enclosed integrated inspection report documents the

inspection findings, which were discussed on July 13, 2011, with Mr. Stephen Hedges, Site Vice

President, and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, one violation is cited in the enclosed Notice of Violation

(Notice) and the circumstances surrounding this violation are described in detail in the enclosed

report. The violation involved the failure to implement procedures for opening of main steam

isolation valves without causing safety system actuations (EA-11-149). Although determined to

be of very low safety significance (Green), this violation is being cited in the Notice because

Wolf Creek failed to restore compliance within a reasonable time after the violation was

identified in NRC Inspection Report 05000482/2010004, per Section 2.3.2 of the NRC

Enforcement Policy. The current Enforcement Policy is included on the NRC's Web site at

http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.

Please note you are required to respond to this letter and should follow the instructions specified

in the enclosed Notice. If you have additional information that you believe the NRC should

consider, you may provide it in your response to the Notice. The NRC will use your response, in

part, to determine whether further enforcement action is necessary to ensure compliance with

regulatory requirements.

This report also documents nine additional NRC-identified and self-revealing issues that were

evaluated under the risk significance determination process as having very low safety

Wolf Creek Nuclear Operating Corporation -2-

EA-11-149

significance (Green). The NRC determined that violations are associated with eight of these

issues. Additionally, two licensee-identified violations, which were determined to be of very low

safety significance, are listed in this report. However, because of the very low safety

significance and because they were entered into your corrective action program, the NRC is

treating these findings as noncited violations, consistent with Section 2.3.2 of the NRC

Enforcement Policy.

If you contest the violation or the significance of the noncited violations, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.

20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission,

Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the

NRC Resident Inspector at the facility. In addition, if you disagree with the cross-cutting aspect

assigned to any finding in this report, you should provide a response within 30 days of the date

of this inspection report, with the basis for your disagreement, to the Regional Administrator,

Region IV, and the NRC Resident Inspector at the facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response, if you choose to provide one for cases where a response is not

required, will be made available electronically for public inspection in the NRC Public Document

Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not

include any personal privacy or proprietary, information so that it can be made available to the

Public without redaction.

Sincerely,

/RA/

Geoffrey B. Miller, Chief

Project Branch B

Division of Reactor Projects

Docket No. 50-482

License No. NPF-42

Enclosure:

NRC Inspection Report and Notice of Violation 05000482/2011003

w/Attachment: Supplemental Information

cc w/Enclosure:

Distribution via Listserv

Electronic distribution by RIV:

Wolf Creek Nuclear Operating Corporation -3-

EA-11-149

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Art.Howell@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

DRP Deputy Director (Jeff.Clark@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

Acting DRS Director (Robert.Calwell@nrc.gov)

DRS Deputy Director (Tom.Blount@nrc.gov)

Senior Resident Inspector (Chris.Long@nrc.gov)

Resident Inspector (Charles.Peabody@nrc.gov)

WC Administrative Assistant (Shirley.Allen@nrc.gov)

Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Senior Project Engineer, DRP/B (Leonard.Willoughby@nrc.gov)

Project Engineer, DRP/B (Nestor.Makris@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Randy.Hall@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROPreports

RIV/ETA/OEDO (John.McHale@nrc.gov)

DRS/TSB STA (Dale.Powers@nrc.gov)

R:\_REACTORS\_WC\2011\WC2011003-RP-CML

ADAMS: No Yes SUNSI Review Complete Reviewer Initials: RWD

Publicly Available Non-Sensitive

Non-publicly Available Sensitive

SRI:DRP/B RI:DRP/B C:DRS/EB1 C:DRS/EB2 DRS/PSB1

CLong CPeabody TFarnholtz NOKeefe MHay

/E-GBM/ /E-GBM/ /RA/ /JMateychick for/ /JLarson for/

8/12/2011 8/2/2011 8/9/2011 8/9/2011 8/10/2011

C:DRS/OB C:DRS/TSB DRS/PSB2 RIV:ACES GMiller

MHaire DPowers GWerner RKellar

/RA/ /RA/ /RA/ /RA/ /RA/

8/10/2011 8/10/2011 8/9/2011 8/11/2011 8/12/2011

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

NOTICE OF VIOLATION

Wolf Creek Nuclear Operating Corporation Docket: 50-482

Wolf Creek Generating Station License No: NPF-42

EA-11-149

During an NRC inspection conducted March 19 through June 30, 2011 a violation of an NRC

requirement was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

Technical Specification 5.4.1.a requires that procedures be established,

implemented, and maintained covering the activities described in Regulatory

Guide 1.33, Revision 2, Appendix A. Regulatory Guide 1.33, Revision 2,

Appendix A, Section 3.i requires procedures for the startup, operation and shutdown

of the main steam system. Wolf Creek Procedure SYS AB-120, Main Steam and

Steam Dump Startup and Operation, Revision 27, implements these requirements

for the main steam system.

Contrary to the above, from March 5, 2010, to March 19, 2011, Wolf Creek

Procedure SYS AB-120 had not been maintained to cover activities for the startup,

operation and shutdown of the main steam system. Specifically,

Procedure SYS AB-120, Revision 27, contained inadequate steps necessary to open

a main steam isolation valve without causing a safety injection signal.

This violation is associated with a Green Significance Determination Process finding

(EA-11-149).

Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Corporation is

required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the

Regional Administrator, Region IV, and a copy to the NRC Senior Resident Inspector at the

facility that is the subject of this Notice of Violation (Notice), within 30 days of the date of the

letter transmitting this Notice. This reply should be clearly marked as a "Reply to Notice of

Violation EA-11-149," and should include for each violation (1) the reason for the violation, or, if

contested, the basis for disputing the violation or severity level, (2) the corrective steps that

have been taken and the results achieved, (3) the corrective steps that will be taken to avoid

further violations, and (4) the date when full compliance will be achieved. Your response may

reference or include previous docketed correspondence, if the correspondence adequately

addresses the required response. If an adequate reply is not received within the time specified

in this Notice, an Order or a Demand for Information may be issued as to why the license should

not be modified, suspended, or revoked, or why such other action as may be proper should not

be taken. Where good cause is shown, consideration will be given to extending the response

time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

-1- Enclosure

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information. If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 12th day of August 2011.

-2- Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000482

License: NPF-42

Report: 05000482/2011003

Licensee: Wolf Creek Nuclear Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane NE

Burlington, Kansas

Dates: April 1 to June 30, 2011

Inspectors: C. Long, Senior Resident Inspector

C. Peabody, Resident Inspector

D. Reinert, Acting Resident Inspector

J. Drake, Senior Reactor Inspector

A. Fairbanks, Reactor Inspector

G. Guerra, CHP, Emergency Preparedness Inspector

G. Pick, Senior Reactor Inspector

D. Strickland, Operations Engineer

Approved By: G. Miller, Chief, Project Branch B

Division of Reactor Projects

-3- Enclosure

SUMMARY OF FINDINGS

IR 05000482/2011003, 4/1 - 6/30/2011; Wolf Creek Generating Station, Integrated Resident

Report, Adverse Weather Protection, Equipment Alignments, Inservice Inspection Activities,

Postmaintenance Testing, Event Follow-up, and Other Activities.

The report covered a 3-month period of inspection by resident inspectors and announced

baseline inspections by region-based inspectors. One Green cited violation, eight Green

noncited violations, and one finding of significance were identified. The significance of most

findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined

using Inspection Manual Chapter 0310, Components Within the Cross-Cutting Areas.

Findings for which the significance determination process does not apply may be Green or be

assigned a severity level after NRC management review. The NRC's program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a noncited violation of Technical

Specification 5.4.1.a, Administrative Procedures, for having no procedure to

address onsite debris impacting plant equipment during severe weather. The

inspectors walked down external areas of the plant on June 1 and June 9, 2011,

prior to the onset of predicted severe thunderstorms and tornadoes. The

inspectors found loose debris each time and brought it to the attention of the

licensee who secured the materials. The inspectors walked down the

transformer yard and tank yard during a thunderstorm on June 16 and found

loose debris such as plywood, trash, wood planks, and fiberglass planks. The

inspectors brought this to the attention of Wolf Creek and the materials were

removed or secured. Wolf Creek initiated several condition reports but they only

addressed immediate cleanup. Wolf Creek procedures had no steps for securing

potential wind-driven projectiles prior to severe weather. After June 16, Wolf

Creek wrote Condition Report 40573 which started a weekly maintenance activity

to remove loose materials and added procedure steps to have operations walk

down external areas prior to severe weather.

This finding was more than minor because it impacted the protection against

external factors attribute of the Initiating Events Cornerstone, and it affected the

cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. The inspectors evaluated this finding using Inspection Manual

Chapter 0609.04, and determined that it was of very low safety significance

(Green) for June 16, 2011, because it did not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment would be unavailable

since the reactor was shutdown. Inspectors used Manual Chapter 0609

Appendix G, Checklist 4 for the other occurrences because Wolf Creek was in

-4- Enclosure

Modes 4 or 5. The finding again screened to Green because it did not increase

the likelihood of a loss of inventory, did not cause the loss of reactor coolant

system instrumentation, did not degrade the ability of the licensee to terminate a

leak path or add inventory when needed, or degrade the ability to recover

residual heat removal if it was lost. This finding has a cross-cutting aspect in the

area of problem identification and resolution, specifically the corrective action

program attribute because licensees short-term corrective actions failed to

ensure debris was secured or removed prior to severe weather

P.1(d)(Section 1R01).

  • Green. The inspectors documented a self-revealing noncited violation of 10 CFR

Part 50, Appendix B, Criterion IX, Control of Special Processes. Specifically, in

October 2009, welders failed to ensure the fillet weld between the train B

charging header and the half coupling used to attach two vent valves met the

specified weld requirements. This weld failed in January 2011, rendering the

train B charging system inoperable. The licensees extent of condition review

identified 12 vent line welds which did not meet ASME code weld size

requirements and/or procedural requirements for 2:1 weld taper configuration.

Additionally, quality assurance inspectors failed to identify that the 2:1 taper weld

requirements specified by procedure, and ASME minimum weld size

requirements, were not met in multiple vent line welds. The weld was repaired

and built up to the correct 2:1 aspect ratio. This issue was entered into the

licensees corrective action program as Condition Reports 32648, 33686, 33689,

and 36438.

The finding was more than minor because it was associated with the equipment

performance attribute of the Initiating Events Cornerstone and adversely affected

the cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during power operations. The

inspectors performed a Phase 1 screening in accordance with Inspection Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,

and determined that the finding was of very low safety significance (Green)

because the issue did not result in exceeding the technical specification limit for

identified reactor coolant system leakage or affect other mitigating systems

resulting in a total loss of their safety function. This finding had a cross-cutting

aspect in the area of human performance, resources, because the licensee failed

to ensure that personnel, specifically welders and quality assurance inspectors,

were adequately trained in the procedural requirements and methods for

measuring weld dimensions to assure nuclear safety H.2(b)(Section 1R08).

  • Green. The inspectors identified a noncited violation of 10 CFR Part 50 involving

the failure of the licensee to ensure that weld preparation was protected from

deleterious contamination in that drawers (located in the hot tool room)

containing files, grinding wheels, flapper wheels, and cutting wheels, used for the

purpose of weld preparation, contained a mixture of both stainless steel tools and

carbon steel tools. The failure to separate tools used for stainless steel weld

preparation from tools used for carbon steel preparation could result in the

-5- Enclosure

contamination of stainless steel welds by carbon steel and affect the material

integrity and corrosion resistance. The licensee immediately removed the tools

and replaced them with new tools stored separately for use on specific types of

metal. This issue was entered into the licensees corrective action program as

Condition Report 36444.

The finding was more than minor because it was associated with the equipment

performance attribute of the Initiating Events Cornerstone and adversely affected

the cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during power operations, and if left

uncorrected the finding would become a more significant safety concern. The

inspectors performed a Phase 1 screening in accordance with Inspection Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,

and determined that the finding was of very low safety significance (Green)

because the issue did not result in exceeding the technical specification limit for

identified reactor coolant system leakage or affect other mitigating systems

resulting in a total loss of their safety function. This finding had a cross-cutting

aspect in the area of human performance, resources, because the licensee did

not provide complete, accurate, and up-to-date procedures for the preparation of

stainless steel and carbon steel welds H.2(c)(Section 1R08).

Appendix B, Criterion III, Design Control, involving the failure of the licensee to

review the suitability of installing brass fittings and leaving test fittings on

pressure, differential pressure, and flow transmitter equalizing block valve drain

ports instead of the design specified stainless steel manifold plugs. During a

boric acid walkdown, the inspectors identified that drain ports on the equalizing

block of two separate reactor coolant system flow transmitters had brass fittings

installed instead of the design specified stainless steel fittings. In response to

inspector concerns about the brass fittings, the licensee subsequently discovered

that a design configuration nonconformance existed by leaving the test fittings on

the drain port during plant operation. Licensee Drawing J-17D22 specifies that

manifold plugs be installed in the drain ports during plant operation. The licensee

immediately replaced the brass caps with stainless steel fittings. This issue was

entered into the licensees corrective action program as Condition Report 36439.

The finding was more than minor because it was associated with the design

control attribute of the Initiating Events Cornerstone and adversely affected the

cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during power operations. The

inspectors performed a Phase 1 screening in accordance with Inspection

Manual 0609.04, Phase 1 - Initial Screening and Characterization of Findings,

and determined that the finding was of very low safety significance (Green)

because the issue would not result in exceeding the technical specification limit

for identified reactor coolant system leakage or affect other mitigating systems

resulting in a total loss of their safety function. The inspectors also determined

that the finding had a cross-cutting aspect in the area of human performance,

resources, because the licensee did not provide adequate training of personnel

-6- Enclosure

so that the inappropriately installed fittings could be identified during system

walkdowns H.2(b)(Section 1R08).

  • Green. The inspectors identified a cited violation of Technical

Specification 5.4.1.a, Administrative Procedures, involving Wolf Creeks failure

to correct Procedure SYS AB-120 for main steam isolation valve operation.

Specifically, between March 3, 2010, and March 19, 2011, Wolf Creek

experienced repeat cases of safety-system actuations due to

Procedure SYS AB-120 containing inadequate steps to establish conditions

necessary to open a main steam isolation valve. Corrective actions were

previously limited to steam header pressures below 300 psi. Wolf Creek

commenced a root cause evaluation of the March 19, 2011, safety injection

under Condition Report 34964. Due to Wolf Creeks failure to restore compliance

from previous NCV 05000482/2010004-01 within a reasonable time after the

violation was identified, this violation is being cited as a Notice of Violation

consistent with the Enforcement Policy.

Failure to correct deficiencies in Procedure SYS AB-120 for steam pressures

above 300 psi was a performance deficiency. The inspectors determined that

this finding was more than minor because it impacted the equipment

performance attribute for the Initiating Events Cornerstone, and it affected the

cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Specifically, this issue relates to the configuration control attribute for

shut down equipment alignment. The inspectors evaluated the significance of

this finding using Inspection Manual Chapter 0609.04. Assuming worst case

degradation, the finding resulted in exceeding the technical specification limit for

reactor coolant system leakage due to the pressurizer power-operated relief

valve cycling. Therefore, the inspectors screened the finding to a Phase 2 review

by the senior reactor analyst. The senior reactor analyst used the Wolf Creek

SPAR model and concluded that the incremental core damage probability

was 3.7E-7 (Green). The inspectors found that the cause of the finding has a

cross-cutting aspect in the area of problem identification and resolution

associated with the corrective action program. Specifically, several evaluations

failed to have an adequate extent of condition review and did not find that

procedures were inadequate for opening a main steam isolation valve above

300 psi P.1(c)(Section 4OA3.1).

  • Green. The inspectors reviewed a self-revealing noncited violation of Technical

Specification 5.4.1.a, Administrative Procedures, for failure to follow procedural

requirements to maintain reactor coolant system pressure below 350 psig.

Control room operators increased charging flow at too great a rate with the

reactor coolant system water-solid which caused the pressurizer power-operated

relief valve to cycle three times over several minutes until adjustments to letdown

could be made to reduce reactor coolant system pressure. Also, the letdown

pressure controller was left in manual when automatic control would have

lessened the pressure increase. Wolf Creek wrote Condition Report 35244 to

-7- Enclosure

correct the deficiency by changing several procedures for water-solid plant

operations.

The failure to maintain pressure below the power-operated relief valve setpoint

was a performance deficiency. The performance deficiency was more than

minor because it impacted the Initiating Events Cornerstone objective of

configuration control to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. The significance of the finding was determined using Inspection

Manual Chapter 0609, Significance Determination Process, Appendix G,

Checklist 2, and determined to be of very low safety significance (Green),

because it did not cause the loss of mitigating capability of core heat removal,

inventory control, power availability, containment control, or reactivity control.

Additionally, the finding also did not cause any low temperature overpressure

technical specifications to be exceeded. The inspectors found that the cause of

the finding had a cross-cutting aspect in the area of human performance.

Specifically, operators had to rely on skill of the craft when procedures should

have supplied more instruction for manipulating charging and letdown with a

water-solid plant H.2.c](Section 4OA3.2).

  • Green. The inspectors reviewed a self-revealing noncited violation of License

Condition 2.C.5 for failure to implement adequate fire watches which affected

both trains of vital ac and dc switchgear. The inadequate fire watches occurred

during an actual fire which negated the Halon system discharge because internal

fire doors were not shut, as required, by the fire watch. The inspectors found

problems with fire impairments and watches from 2008 that had not been

corrected. Subsequent to the fire, Wolf Creek again briefed and trained its

personnel on the requirements for fire watches. This issue is captured in the

corrective action program as Condition Report 36719.

Failure to implement adequate fire impairments such that the fire watches

ensured the success of the Halon system was a performance deficiency. The

performance deficiency was more than minor because it impacted the Initiating

Events Cornerstone and its objective to limit the likelihood of those events that

upset plant stability and challenge critical safety functions during shutdown as

well as power operations. Specifically, the protection against external factors

attribute was impacted by the fire impairment. To determine significance, the

inspectors used Inspection Manual Chapter 0609.04 to screen the finding to

Inspection Manual Chapter 0609, Appendix F, because the fire protection

defense-in-depth strategies involving automatic suppression, fire barriers, and

administrative controls were degraded. The senior reactor analyst conducted a

Phase 3 review of this finding and concluded that the incremental core damage

frequency was 1.6E-8 per year, or very low safety significance (Green). The

inspectors found that the cause of the finding had a cross-cutting aspect in the

area of problem identification and resolution. Specifically, corrective actions from

ineffective fire watches in 2008 did not prevent recurrence of the inadequate fire

watch on April 5, 2011 P.1.d](Section 4OA3.3).

-8- Enclosure

Cornerstone: Mitigating Systems

  • Green. The inspectors reviewed a self-revealing noncited violation of Technical

Specification 5.4.1a, Administrative Procedures, for a loss of component

cooling water train B inventory caused by inadequate clearance order

verification. Valve HBV110 was stuck in position and was partially open. When

the clearance order was implemented, the operators concluded the valve was

already closed. Subsequently, the valve created a leakage path which exceeded

the surge tank makeup flow capacity and required manual isolation by the control

room operators to protect safety-related components. Wolf Creek has taken

corrective actions to include communication of expected as-found equipment

positions in pre-job briefings and the clearance order template. This issue is

captured in the corrective action program as Condition Reports 34505

and 40219.

Failure to properly establish clearance order boundary isolation was a

performance deficiency. The performance deficiency is more than minor

because it is associated with the equipment performance and human

performance attributes of the Mitigating Systems Cornerstone and impacted the

cornerstone objective of ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using Inspection Manual Chapter 0609.04, the finding was determined to be of

very low safety significance because the finding did not result in the loss of

operability or functionality of the component cooling water train or screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating

event or screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. The inspectors found that the finding had a cross-cutting

aspect of work practices in the area of human performance associated with the

communication of human error prevention techniques, such as holding pre-job

briefings, self- and peer-checking, and proper documentation of activities

H.4(a)(Section 1R04).

  • Green. The inspectors identified a finding involving the failure to follow the

requirements of Procedure AP 16E-002, Post Maintenance Testing

Development, for the startup feedwater pump. On November 4-6, 2010, Wolf

Creek workers disassembled the startup feedwater pump for numerous

preventive and corrective activities including removing the rotating element. On

November 17, 2010, Wolf Creek conducted surveillance Procedure STN AE-007,

Startup Main Feedwater Pump Operational Test, following reassembly. The

only acceptance criteria listed in this procedure is that the motor-driven feedwater

pump starts from the control room with no local operator action. The inspectors

found this contrary to Procedure AP 16E-002, which requires acceptance criteria

for a pump flow capacity test, vibration, bearing and lubrication temperatures,

motor current, external leakage, and lubrication level be found satisfactory. This

issue is captured in the corrective action program as Condition Report 39494.

Wolf Creek issued a new work package to conduct a single-point pump capacity

test and complete the required postmaintenance testing. Wolf Creek found,

pending final review, that initial calculations show that the pump design is

-9- Enclosure

capable of enough flow to provide a heat sink in emergency operating

procedures.

Failure to follow Procedure AP 16E-002 for developing test criteria for plant

equipment after the completion of maintenance activities is a performance

deficiency. The finding is more than minor because it is associated with the

Mitigating Systems Cornerstone attribute of equipment performance and it

adversely affects the cornerstone objective of ensuring the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609.04, the inspectors

determined that the finding had very low safety significance (Green) because it

did not result in a loss of system safety function, an actual loss of safety function

of a single train for greater than its technical specification allowed outage time, or

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The inspectors determined that the finding had a cross-cutting

aspect in the area of problem identification and resolution. Specifically, Wolf

Creek created a testing procedure in response to a root cause evaluation, but did

not consider acceptance criteria to ensure that the pump performs acceptably

P.1(d)(Section 1R19).

Appendix B, Criterion III, Design Control, for the failure to translate the design

basis into instructions, procedures, and drawings. The inspectors found that the

licensee failed to assess whether vortexing occurred in the containment spray

additive tank in the event of a design-basis accident. Wolf Creek entered this

issue in the corrective action program as Condition Report 38715.

Failure to implement design control measures to analyze whether containment

spray piping remained full of water was a performance deficiency. This finding

was more than minor because it affected the design control attribute of the

Mitigating Systems Cornerstone objective to ensure the availability, reliability,

and capability of the containment spray system to respond to initiating events

and prevent undesirable consequences. Specifically, the inspectors had

reasonable doubt on the capability of the containment spray system to properly

inject because of vortexing in the containment spray additive tank. The

inspectors performed the significance determination using Inspection Manual

Chapter 0609.04. The finding was determined to be of very low safety

significance (Green) because it was a design or qualification deficiency

confirmed not to result in loss of operability or functionality. Although the failure

to have this calculation had existed since original construction, the inspectors

determined this finding reflected current performance since the licensee was

required to evaluate likelihood of tanks allowing gas intrusion into the emergency

core cooling systems in response to Generic Letter 2008-01, Managing Gas

Accumulation in Emergency Core Cooling, Decay Heat Removal, and

Containment Spray Systems. Consequently, this finding had problem

identification and resolution cross-cutting aspects associated with the corrective

action program in that the licensee did not thoroughly evaluate the potential for

gas intrusion from all possible tanks P.1(c)(Section 4OA5).

- 10 - Enclosure

B. Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

condition report numbers are listed in Section 4OA7.

- 11 - Enclosure

REPORT DETAILS

Summary of Plant Status

Wolf Creek began the quarter shut down for Refueling Outage 18. Wolf Creek restarted on

June 22, 2011. Reactor operators manually tripped the reactor from 82 percent power on

June 26 due to a trip of main feedwater pump B. Wolf Creek restarted on June 29 and ended

the quarter holding at 55 percent power to complete troubleshooting and repairs on main

feedwater pump B.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Summer Readiness for Offsite and Alternate-ac Power

a. Inspection Scope

The inspectors performed a review of preparations for summer weather for selected

systems, including conditions that could lead to loss-of-offsite power and conditions that

could result from high temperatures. The inspectors reviewed the procedures and

communications protocols between the transmission system operator and the plant to

verify that the appropriate information was being exchanged when issues arose that

could affect the offsite power reliability. Examples of aspects considered in the

inspectors review included:

  • The coordination between the transmission system operator and the control

room personnel during off-normal or emergency events

  • The explanations for the events
  • The estimates of when the offsite power system would be returned to a normal

state

  • The notifications from the transmission system operator to the plant when the

offsite power system was returned to normal

During the inspection, the inspectors focused on plant-specific design features and the

procedures used by plant personnel to mitigate or respond to adverse weather

conditions. Additionally, the inspectors reviewed the Updated Safety Analysis

Report (USAR) and performance requirements for selected systems, and verified that

operator actions were appropriate per station procedures. Specific documents reviewed

during this inspection are listed in the attachment. The inspectors also reviewed

corrective action documents to verify that the licensee was identifying adverse weather

issues at an appropriate threshold and entering them into their corrective action

- 12 - Enclosure

program. These activities constitute completion of one readiness for summer weather

affect on offsite and alternate ac power sample as defined in Inspection

Procedure 71111.01-05.

b. Findings

No findings were identified.

.2 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

When thunderstorms, tornados, and high winds were forecast in the site vicinity on

June 1, 9, and 16, 2011, the inspectors reviewed the plant preparations for the expected

weather conditions. On June 1, 9, and 16, the inspectors walked down the offsite power

system, refueling water storage tank, and reactor makeup water storage tank because

their safety functions could be affected by high wind-generated missiles or a loss of

offsite power. The inspectors evaluated these preparations against the site procedures

and determined that actions by the plant staff were adequate. During the inspection, the

inspectors focused on plant-specific design features and the station procedures used to

respond to specified adverse weather conditions. The inspectors also toured outdoor

areas of the plant to look for any loose debris that could become a wind-driven projectile.

The inspectors evaluated operator staffing and accessibility of instrumentation and

controls for systems required to operate the plant. Additionally, the inspectors reviewed

the USAR and performance requirements for the selected systems and verified that

operator actions were appropriate per station procedures. The inspectors also reviewed

a sample of corrective action documents to verify that the licensee-identified adverse

weather issues at an appropriate threshold and entered them into the corrective action

program. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of two readiness for impending adverse weather

condition samples as defined in Inspection Procedure 71111.01-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.4.1.a for having no procedure to address onsite debris impacting plant

equipment during severe weather.

Description. On June 1, 2011, a severe thunderstorm watch was announced by the

national weather service. The inspectors walked down the transformer yard at 6 p.m.,

with the storms forecast to arrive later that night. The inspectors found numerous pieces

of unsecured plywood and 2x4 and 2x8 planks. The inspectors brought this to the

licensees attention, and Wolf Creek personnel secured the materials. The inspectors

reviewed station Procedure AI 14-006, Severe Weather, Revision 9A. The procedure

directed public address system announcements for national weather service severe

weather declarations and instructions on personnel sheltering, but included no steps on

- 13 - Enclosure

equipment protection from onsite debris. The inspectors reviewed

Procedure OFN SG-003, Natural Events, Revision 20A, but it did not direct entry until a

tornado is sighted or a tornado warning is issued.

The national weather service issued a tornado warning for the site area on June 9, at

3:20 p.m. The inspectors walked down the transformer yard at 5 p.m. The inspectors

again found unsecured debris in the transformer and tank areas. The inspectors

reported the debris to the control room and outage control center who sent personnel to

secure the material. On June 10, a severe thunderstorm watch was issued at 5 p.m.,

and the inspectors walked down the transformer and tank yards at 6 p.m. to verify the

corrective action from the previous day had been implemented for the pending storms.

The inspectors found that some material was removed or secured, but also found

numerous unsecured sections of scaffolding, wood, palettes, diamond plate, and debris.

The inspectors discussed this with the outage control center. Condition Report 40351

was written with immediate actions to secure the loose materials. The extent of

condition description included any area where inclement weather has the potential of

creating airborne objects that could challenge plant equipment. On June 16, the

inspectors walked down the transformer yard and tank areas during a thunderstorm.

The inspectors found numerous unsecured pieces and stacks of wood and other debris

that could impact plant equipment if winds were more severe. Wolf Creek responded by

securing or removing the debris and writing Condition Report 40573 which implemented

a weekly preventive maintenance activity to clean up outside areas and changed

Procedure AI 14-006 to perform walkdowns of outside areas prior to severe weather.

The inspectors found previously written condition reports on lack of adverse weather

preparations for outdoor areas prior to the inspection.

Analysis. Failure to remove potential wind-driven debris from the transformer and tank

areas before severe weather is a performance deficiency. This finding was more than

minor because it impacted the protection against external factors attribute of the

Initiating Events Cornerstone, and it affected the cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. The inspectors evaluated this finding

using Inspection Manual Chapter 0609.04, and determined that it was of very low safety

significance (Green) for June 16 because it did not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment would be unavailable since the

reactor was shutdown. Inspectors used Manual Chapter 0609, Appendix G, Checklist 4,

for the other occurrences because Wolf Creek was in Modes 4 or 5. The finding again

screened to Green because it did not increase the likelihood of a loss of inventory, did

not cause the loss of reactor coolant system instrumentation, did not degrade the ability

of the licensee to terminate a leak path or add inventory when needed, or degrade the

ability to recover residual heat removal if it was lost. This finding has a cross-cutting

aspect in the area of problem identification and resolution, specifically the corrective

action program attribute because licensee short-term corrective actions failed to ensure

debris was secured or removed prior to severe weather P.1(d).

Enforcement. Technical Specification 5.4.1.a requires, in part, that written procedures

shall be established, implemented, and maintained covering the procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory

- 14 - Enclosure

Guide 1.33, Appendix A, Section 6.w, requires, in part, written procedures for acts of

nature (e.g., tornado, flood, dam failure, earthquakes). Contrary to the above, prior to

June 16, 2011, Wolf Creek had not established written procedures for acts of nature

associated with tornados. Specifically, there were no procedural directions that

addressed how the licensee was to protect from wind-driven projectiles, associated with

tornados, in the protected area. Because this violation was of very low safety

significance and was entered into the licensee's corrective action program as Condition

Report 40573, this violation is being treated as a noncited violation, consistent with

Section 2.3.2 of the NRC Enforcement Policy: NCV 05000485/2011003-01, No

Procedure for Debris in Transformer and Tank Yards Prior to Severe Weather.

1R04 Equipment Alignments (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed a partial system walkdown of the following risk-significant

system:

  • March 8, 2011, Component cooling water

The inspectors selected this system based on its risk significance relative to the Reactor

Safety Cornerstone at the time it was inspected. The inspectors attempted to identify

any discrepancies that could affect the function of the system, and, therefore, potentially

increase risk. The inspectors reviewed applicable operating procedures, system

diagrams, USAR, technical specification requirements, administrative technical

specifications, outstanding work orders, condition reports, and the impact of ongoing

work activities on redundant trains of equipment in order to identify conditions that could

have rendered the systems incapable of performing their intended functions. The

inspectors also inspected accessible portions of the system to verify system components

and support equipment were aligned correctly and operable. The inspectors examined

the material condition of the components and observed operating parameters of

equipment to verify that there were no obvious deficiencies. The inspectors also verified

that the licensee had properly identified and resolved equipment alignment problems

that could cause initiating events or impact the capability of mitigating systems or

barriers and entered them into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of one partial system walkdown sample as defined

in Inspection Procedure 71111.04-05.

b. Findings

Introduction. The inspectors reviewed a self-revealing Green noncited violation of

Technical Specification 5.4.1a, Administrative Procedures, for an inadequate clearance

order verification which caused a loss of component cooling water B inventory.

- 15 - Enclosure

Description. On March 8, 2011, Wolf Creek was preparing to implement Temporary

Modification Order (TMO) 10-017-EG-00 to install temporary equipment to cool the

radwaste system heat loads. These preparations included hanging clearance

order D-HB-N-029 which required station operators to verify closed manual

valves EGV0079 and HBV0110 and open and uncap the associated piping header hose

connection valves HBV0088 and HBV0111. Until TMO 10-017 is implemented,

component cooling water must be periodically aligned to the radwaste building to cool its

associated nonsafety-related heat loads. This nonsafety component cooling water

function adds seismic vulnerabilities that render the aligned train inoperable

(NCV 05000482/2010007-01). At 9:30 a.m., station operators attempted to move

valve HBV0110 in the closed direction and found that the valve would not turn. The

operators compared the stem position relative to that of an identical model valve. The

operators successfully manipulated travel of valve EGV0079 in the previous step from

the fully open to fully closed position. This apparent position verification was made using

the naked eye, and was the basis for assuming that the valve was firmly on its seat and

signed the clearance order verifications accordingly.

At 2:37 p.m., the control room operators performed a planned routine alignment of

component cooling water train B to radwaste. This action immediately resulted in a

200 gpm component cooling water leak through valve HBV0110 and out of the hose

connection piping penetrations. The rapidly decreasing component cooling water B

surge tank level caused an auto start of the demineralized water makeup to the

component cooling water B surge tank and simultaneously sent an alarm to the control

room operators. However, the demineralized water makeup capacity is only 60 gpm,

resulting in a component cooling water B inventory loss of 140 gpm and a decreasing

surge volume. Without prompt manual actions, the 5000 gallon component cooling

water train B surge tank volume would have been exhausted in 25 minutes, at which

point component cooling water train B would void and fail. For the duration of the leak,

component cooling water train B was unavailable because it was unable to meet its

accident mission time. Operators identified the cause and isolated the component

cooling water supply from the radwaste building. The leak was determined to be

approximately 500 gallons total, or 10 percent of the normal component cooling water

surge tank inventory.

The leak revealed that valve HBV0110 was not fully closed but was stuck in a throttled

position. Station operators were directed by the control room to attempt to move the

valve in the open direction, which they did with an approved torque assist device. When

the operators subsequently moved the valve in the closed direction, it moved beyond its

previous position and was properly seated. Later that evening, when component cooling

water was once again aligned to radwaste, no leakage occurred. Wolf Creek entered

the event into their corrective action as Condition Report 34505.

The inspectors reviewed the history for valve HBV0110. All four of the subject valves

had minimal manipulation since the waste evaporator package they were originally

associated with had been abandoned in place in the early 1990s. Also, periodic

maintenance to inspect and lubricate the valve internals has not been performed during

this time. The last position verification made on valve HBV0110 was conducted April 21,

2006, and indicated that the valve was throttled partially open. The valve was also listed

- 16 - Enclosure

on drawing M-12HB02 as normally throttled. The clearance order paperwork specified

to leave the valve 1.4 turns open upon removal of the clearance order.

The inspectors determined that the operators failed to meet the requirements of station

Procedure AP 21E-001, step 6.4.2.1, to properly position the equipment/components in

the sequence specified on the clearance order tag hang list, as well as step 6.4.3.1, the

independent verification of that component or equipment condition. The inspectors

interviews with operators and station management indicated that the cause of the

leakage was a lack of information communicated to the operators performing the tagout.

Wolf Creek tagout practices did not provide expected, as-found component positions for

taggers and verifiers in the clearance order tag Hang List nor is this information

communicated during pre-job briefings. Wolf Creek initiated Condition Report 40219

which directed oral communication of the expected initial component positions during

pre-job briefings and on the clearance order paperwork template.

Analysis. Failure to properly establish clearance order boundary isolation is a

performance deficiency. The performance deficiency is more than minor because it

impacted the equipment performance and human performance attributes of the

Mitigating Systems Cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609.04, the finding was determined

to be of very low safety significance (Green) because the finding is not a design or

qualification deficiency confirmed not to result in loss of operability or functionality; the

finding does not represent a loss of system safety function; the finding does not

represent actual loss of safety function of a single train for more than its technical

specification allowed outage time; the finding does not represent an actual loss of safety

function of one or more nontechnical specification trains of equipment designated as risk

significant per 10 CFR 50.65 for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and the finding does not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

The inspectors found that the finding had a cross-cutting aspect of work practices in the

area of human performance. The licensee communicates human error prevention

techniques, such as holding pre-job briefings, self- and peer-checking, and proper

documentation of activities. Specifically, Wolf Creek did not communicate the expected

as-found condition of valve HBV0110 to the taggers and verifiers of the clearance order

H.4(a).

Enforcement. Wolf Creek Technical Specification 5.4.1a requires that procedures be

established, implemented, and maintained covering the activities described in

Regulatory Guide 1.33, Revision 2, Appendix A. Regulatory Guide 1.33, Revision 2,

Appendix A, Section 1(c) requires, in part, procedures governing equipment control,

including locking and tagging. Licensee Procedure AP 21E-001 Clearance Orders,

steps 6.4.2.1 and 6.4.3.1, specifies that equipment and components be positioned and

verified in the sequence specified on the clearance order tag list. Contrary to the above,

on March 8, 2011, the licensee failed to ensure the component was positioned and

verified in the sequence specified on the clearance order tag list. Specifically, while

performing clearance order D-HB-N-029, valve HBV0110 was not properly positioned

and verified as specified on the clearance order tag list. These actions directly resulted

in a loss of component cooling water train availability. Because this finding is of very low

- 17 - Enclosure

safety significance and was entered into the licensee corrective action program as

Condition Reports 34505 and 40219, this violation is being treated as a noncited

violation in accordance with Section 2.3.2 of the Enforcement Policy:

NCV 05000482/2011003-02, Failure to Properly Establish Clearance Order Boundary

Isolation Resulting in Loss of Component Cooling Water Inventory.

.2 Complete Walkdown and System Walkdown Associated with Temporary

Instruction (TI) 2515/177

a. Inspection Scope

On April 27, 2011, the inspectors performed a complete system alignment inspection of

the containment spray system to verify the functional capability of the system. The

inspectors selected this system because it was considered both safety significant and

risk significant in the licensees probabilistic risk assessment. The inspectors inspected

the system to review mechanical and electrical equipment lineups, electrical power

availability, system pressure and temperature indications, as appropriate, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. The inspectors reviewed a sample of

past and outstanding work orders to determine whether any deficiencies significantly

affected the system function. In addition, the inspectors reviewed the corrective action

program database to ensure that system equipment-alignment problems were being

identified and appropriately resolved. Specific documents reviewed during this

inspection are listed in the attachment.

The inspectors conducted a walkdown of the containment spray system in sufficient

detail to reasonably assure the acceptability of the licensees walkdowns (TI 2515/177,

Section 04.02.d). The inspectors also verified that the information obtained during the

licensees walkdown was consistent with the items identified during the inspectors

independent walkdown (TI 2515/177, Section 04.02.c.3).

In addition, the inspectors verified that the licensee had isometric drawings that describe

the containment spray system configurations and had acceptably confirmed the

accuracy of the drawings (TI 2515/177, Section 04.02.a). The inspectors verified the

following related to the isometric drawings.

  • High point vents were identified
  • Other areas where gas can accumulate and potentially impact subject system

operability, such as at orifices in horizontal pipes, isolated branch lines, heat

exchangers, improperly sloped piping, and under closed valves were acceptably

referenced in documentation

  • Horizontal pipe centerline elevation deviations and pipe slopes in nominally

horizontal lines that exceed specified criteria were identified

  • All pipes and fittings were clearly shown

- 18 - Enclosure

  • The drawings were up-to-date with respect to recent hardware changes and that

any discrepancies between as-built configurations and the drawings were

documented and entered into the corrective action program for resolution

The inspectors verified that piping and instrumentation diagrams accurately described

the subject systems; that they were up-to-date with respect to recent hardware changes;

and any discrepancies between as-built configurations, the isometric drawings, and the

piping and instrumentation diagrams were documented and entered into the corrective

action program for resolution (TI 2515/177, Section 04.02.b).

Documents reviewed are listed in the attachment to this report.

These activities constitute completion of one complete system walkdown sample as

defined in Inspection Procedure 71111.04-05. Also, this inspection effort counts toward

the completion of TI 2515/177. See Section 4OA5 for additional information.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • March 19, 2011, Safety injection pump room A
  • March 19, 2011, Control room ventilation equipment room B
  • March 20, 2011, Auxiliary building 1988 pipe chase
  • April 6, 2011, Containment building

The inspectors reviewed these areas to assess if licensee personnel had implemented a

fire protection program that adequately controlled combustibles and ignition sources

within the plant; effectively maintained fire detection and suppression capability;

maintained passive fire protection features in good material condition; and had

implemented adequate compensatory measures for out of service, degraded or

inoperable fire protection equipment, systems, or features in accordance with the

licensees fire plan. The inspectors selected fire areas based on their overall

contribution to internal fire risk as documented in the plants Individual Plant Examination

of External Events with later additional insights, their potential to affect equipment that

could initiate or mitigate a plant transient, or their impact on the plants ability to respond

to a security event. Using the documents listed in the attachment, the inspectors verified

that fire hoses and extinguishers were in their designated locations and available for

- 19 - Enclosure

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees corrective action

program. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08)

.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control

(71111.08-02.01)

a. Inspection Scope

The inspection procedure required review of two or three types of nondestructive

examination activities and, if performed, one to three welds on the reactor coolant

system pressure boundary. It also required review of one or two examinations with

relevant indications (if any were found) that had been accepted by the licensee for

continued service.

The inspectors directly observed the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Pressurizer TBB03-CIRCUM-1-W Ultrasonic Examination

Pressurizer TBB03-SEAM-4W Ultrasonic Examination

Pressurizer TBB03-10-B-W Ultrasonic Examination

Pressurizer TBB03-10-C-W Ultrasonic Examination

Pressurizer TBB03-10-B-IR Ultrasonic Examination

Pressurizer TBB03-10-C-IR Ultrasonic Examination

Steam Generator EBB01A-SEAM-5-W Ultrasonic Examination

- 20 - Enclosure

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Steam Generator EBB01A-SEAM-8-W Ultrasonic Examination

RV Closure Head CH-STUD-19 through 36 Ultrasonic Examination

Studs and Nuts

Main Steam AB-01-R001 Visual Examination 3

Piping Support

Main Steam AB-01-R003 Visual Examination 3

Piping Support

Feedwater Piping AE05-R028 Visual Examination 3

Support

Feedwater Piping AE-04-R019 Visual Examination 3

Support

Feedwater Piping AE05-C001 Visual Examination 3

Support

Main Steam AB-01-R010 Magnetic Examination

Integral

Attachment

Feedwater AE-05-R028 Magnetic Examination

Integral

Attachment

During the review and observation of each examination, the inspectors verified that

activities were performed in accordance with ASME Boiler and Pressure Vessel Code

requirements and applicable procedures. Indications were compared with previous

examinations and dispositioned in accordance with ASME code and approved

procedures. The qualifications of all nondestructive examination technicians performing

the inspections were verified to be current.

Only the visual examination of AE05-R028, Piping Support, identified any relevant

indications. Repairs were made to AE05-R028 and it was reexamined and was

satisfactory. Wolf Creek personnel stated that no relevant indications were accepted by

the licensee for continued service.

- 21 - Enclosure

The inspectors directly observed a portion of the following welding activities:

SYSTEM WELD IDENTIFICATION WELD TYPE

Reactor Coolant 13BG22-W-33 Shield Metal Arc Welding

System

Reactor Coolant 13BG22-W-34 Shield Metal Arc Welding

System

The inspectors verified, by review, that the welding procedure specifications and the

welders had been properly qualified in accordance with ASME Code,Section IX,

requirements. The inspectors also verified through record review that essential variables

for the welding process were identified, recorded in the procedure qualification record,

and formed the bases for qualification of the welding procedure specifications. Specific

documents reviewed during this inspection are listed in the attachment.

b. Findings

.1 Failure to Ensure Fillet Weld Met Size Requirements on Train B Charging Header Vent

Line

Introduction. The inspectors documented a self-revealing Green noncited violation of

10 CFR Part 50, Appendix B, Criterion IX, Control of Special Processes, after the

licensee failed to ensure that that the fillet weld between the train B charging header and

the half-coupling used to attach two vent valves met 2:1 taper weld requirements. The

undersized weld subsequently resulted in a 300 drop-per-minute leak in January 2011.

Description. On January 3, 2011, the licensee identified a 300 drop-per-minute pinhole

leak at the weld joint between the train B charging header and/or the half coupling used

to attach vent valves BGV0845 and BGV0846. The licensee measured the subject weld

and concluded that the weld was undersized and the required 2:1 aspect ratio was not

obtained. The weld was performed in the October/November 2009 timeframe during the

installation of vent valves in the chemical and volume control system, the residual heat

removal system, and the high pressure coolant injection system. Also, quality assurance

inspectors inappropriately accepted the undersized weld.

Wolf Creeks extent-of-condition review concluded that 12 additional welds either did not

meet the procedurally required 2:1 aspect ratio or did not meet ASME minimum weld

size requirements. No other undersized welds developed leaks. After the leak was

identified, the train B charging system was declared inoperable and the weld was

repaired and built up to the correct 2:1 aspect ratio.

Wolf Creek performed a hardware failure analysis on the failed weld and concluded that

although the main characteristics of the weld fracture were consistent with stress

corrosion cracking, the crescent shape of the fracture indicated cyclic crack growth. The

licensee also concluded that the configuration of the vent line with no lateral support

- 22 - Enclosure

could have created a cantilever effect on the line and in combination with a notch

created by the lack of fusion in the weld root served as a stress concentrator. This issue

was entered into the licensees corrective action program as Condition Report 36438.

Analysis. Failure to meet ASME code weld size requirements is a performance

deficiency. The finding was more than minor because it was associated with the

equipment performance attribute of the Initiating Events Cornerstone. The finding

adversely affected the cornerstone objective to limit the likelihood of those events that

upset plant stability and challenge critical safety functions during power operations. The

inspectors performed a Phase 1 screening in accordance with Inspection Manual

Chapter 0609.04 and determined that the finding was of very low safety significance

(Green) because the issue did not result in exceeding the technical specification limit for

identified reactor coolant system leakage or affect other mitigating systems resulting in a

total loss of their safety function. This finding had a cross-cutting resources aspect in

the area of human performance, because the licensee failed to ensure that welders and

quality assurance inspectors were adequately trained in the procedural requirements

and methods for measuring weld dimensions to assure nuclear safety H.2(b).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion IX, Control of Special

Processes, requires in part, that measures be established to ensure that special

processes, including welding are controlled and accomplished by qualified personnel

using qualified procedures in accordance with applicable codes, standards,

specifications, criteria, and other special requirements. Contrary to the above, in

October 2009, the licensee failed to ensure that special processes, including welding,

were controlled and accomplished using qualified procedures. Specifically, welders

failed to ensure that the fillet weld between the train B charging header and the half-

coupling used to attach two vent valves met 2:1 taper weld requirements, which

subsequently resulted in a 300 drop-per-minute leak in January 2011. This issue was

entered into the licensees corrective action program as Condition Report 36438.

Because this finding was determined to be of very low safety significance and was

entered into the licenses corrective action program, this violation is being treated as a

noncited violation consistent with Section 2.3.2 of the NRC Enforcement Policy:

NCV 05000482/2011003-03, Failure to Assure Fillet Weld Met Size Requirements on

Train B Charging Header Vent Line.

.2 Failure to Ensure Separation of Stainless Steel and Carbon Steel Grinding and Cutting

Tools

Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.55a,

Codes and Standards, after the licensee failed to ensure that stainless steel and

carbon steel grinding wheels, flapper wheels, cutting wheels, and files were stored

separately and used only for the weld preparation of the designated steel.

Description. During inspection of the tool issue room in the radiologically controlled

area, the inspectors identified that tools designated for either stainless steel or carbon

steel weld preparation were not stored separately. The inspectors noted that although

stainless steel grinding wheels, flapper wheels, and cutting wheels were marked for

stainless steel use, they were stored with carbon steel grinding wheels, flapper wheels,

- 23 - Enclosure

and cutting wheels. Additionally, the inspectors identified that although stainless steel

files and carbon steel files were stored in separate drawers, there were files in the

stainless steel drawer that appeared to have been used on carbon steel, and there was

a file marked for use on stainless steel in the carbon steel drawer. There was also no

procedure or written guidance pertaining to proper storage and control of the equipment.

The failure to separate tools used for stainless steel weld preparation from tools used for

carbon steel preparation could result in the contamination of stainless steel welds by

carbon steel and affect the material integrity and corrosion resistance. The licensee

immediately removed the tools and replaced them with new tools stored separately for

use on specific types of metals. This issue was entered into the licensees corrective

action program as Condition Report 3644.

Analysis. Failure to protect stainless steel welds from deleterious contamination is a

performance deficiency. The finding was more than minor because it was associated

with the equipment performance attribute of the Initiating Events Cornerstone. The

finding adversely affected the cornerstone objective to limit the likelihood of those events

that upset plant stability and challenge critical safety functions during power operations

and if left uncorrected, the finding would become a more significant safety concern. The

inspectors performed a Phase 1 screening in accordance with Inspection Manual

Chapter 0609.04 and determined that the finding was of very low safety significance

(Green) because the issue did not result in exceeding the technical specification limit for

identified reactor coolant system leakage or affect other mitigating systems resulting in a

total loss of their safety function. This finding had a resources cross-cutting aspect in

the area of human performance, because the licensee did not provide adequate

procedures for the preparation of stainless steel and carbon steel welds H.2(c).

Enforcement. Title 10 CFR 50.55a, states in part, that Each operating license for a

boiling or pressurized water-cooled nuclear power facility is subject to the conditions in

paragraphs (f) and (g). Title 10 CFR 50.55a(g)(4), requires, in part, that components

classified as ASME Code Class 1, Class 2, and Class 3 meet the requirements set forth

in Section XI of the ASME Boiler and Pressure Vessel Code and Addenda.Section XI of

the ASME Code, Part IWA-4221(b)(2), states that When adding a new component to an

existing system, the Owner shall specify a Construction Code. The licensee specified

Section III of the subject code when adding a new component to an existing system.

Section III, Part NG4412, states that The work [weld preparation] shall be protected

from deleterious contamination. Contrary to the above, prior to June 2011, the licensee

did not ensure that weld preparation was protected from deleterious contamination.

Specifically, the licensee failed to ensure weld preparation was protected, in that tools

located in the hot tool room drawers containing files, grinding wheels, flapper wheels,

and cutting wheels that were used for the purpose of weld preparation, were found to

contain a mixture of both stainless steel tools and carbon steel tools. This issue was

entered into the licensees corrective action program as Condition Report 36444.

Because this finding was determined to be of very low safety significance and was

entered into the licensees corrective action program, this violation is being treated as a

noncited violation consistent with Section 2.3.2 of the NRC Enforcement Policy:

NCV 05000482/2011003-04, Failure to Assure Separation of Stainless Steel and

Carbon Steel Grinding and Cutting Equipment.

- 24 - Enclosure

.2 Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)

a. Inspection Scope

The inspectors witnessed portions of the licensees performance of the required visual

inspection (VT-2) of the reactor head and pressure-retaining components above the

reactor pressure vessel head in accordance with requirement of ASME Code

Case N-729-1 as mandated by 10 CFR 50.55a. Implementation required ASME

Code IWA-2212 VT-2 under the mirror insulation on top of the reactor head through

multiple access points. The inspectors reviewed the results of this inspection for

evidence of leaks or boron deposits at reactor pressure boundaries and related

insulation above the head. Specific documents reviewed during this inspection are listed

in the attachment.

These actions constitute completion of the requirements for Section 02.02 of Inspection

Procedure PI 71111.08.

b. Findings

No findings were identified.

.3 Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)

a. Inspection Scope

The inspectors evaluated the implementation of the licensees boric acid corrosion

control program for monitoring degradation of those systems that could be adversely

affected by boric acid corrosion. The inspectors reviewed the documentation associated

with the licensees boric acid corrosion control walkdown as specified in

Procedure STN PE-040D, RCS Pressure Boundary Integrity Walkdown, Revision 3,

and Procedure AP 16F-001, Boric Acid Corrosion Control Program, Revision 6A. The

inspectors also reviewed the visual records of the components and equipment. The

inspectors verified that the visual inspections emphasized locations where boric acid

leaks could cause degradation of safety-significant components. The inspectors also

verified that the engineering evaluations for those components where boric acid was

identified gave assurance that the ASME code wall thickness limits were properly

maintained. The inspectors confirmed that the corrective actions performed for evidence

of boric acid leaks were consistent with requirements of the ASME code. Specific

documents reviewed during this inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 71111.08-02.03.

b. Findings

Failure to Assure Configuration Control of Safety-Related Systems

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, involving the failure of the licensee to review

- 25 - Enclosure

the suitability of replacing the design specified stainless steel manifold plugs with test

fittings and brass caps on various flow transmitter equalizing block valve drain ports.

Description. During a boric acid walkdown, the inspectors identified that drain ports on

the equalizing block of two separate reactor coolant system flow transmitters had brass

fittings installed instead of stainless steel fittings. The inspectors brought this condition

to Wolf Creeks attention. The licensee determined that a design configuration

nonconformance existed in that licensee Drawing J-17D22 specified that stainless steel

manifold plugs be installed in the drain ports during plant operation. The licensee failed

to review the suitability of installing brass fittings and leaving test fittings on flow

transmitter equalizing block valve drain ports instead of the design specified stainless

steel manifold plugs. Wolf Creek immediately replaced the brass caps with stainless

steel fittings. This issue was entered into the licensees corrective action program as

Condition Report 36439.

Analysis. Plugging instrument lines with test fittings of a different material is a

performance deficiency. The finding was more than minor because it was associated

with the design control attribute of the Initiating Events Cornerstone. The finding

affected the cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during power operations. The inspectors

screened the finding per Inspection Manual Chapter 0609.04 and determined that the

finding was of very low safety significance (Green) because the issue would not result in

exceeding the technical specification limit for identified reactor coolant system leakage

or affect other mitigating systems resulting in a total loss of their safety function. The

inspectors also determined that the finding had a resources cross-cutting aspect in the

area of human performance, because the licensee did not provide adequate training of

personnel so that the inappropriately installed fittings could be identified during system

walkdowns H.2(b).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that measures be established for the selection and review of suitability of

application of materials, parts, equipment, and processes that are essential to the safety-

related functions of the structures, systems, and components. Contrary to the above,

the licensee failed to establish measures for the selection and review for suitability of

parts that are essential to the safety-related functions of systems and components.

Specifically, the licensee failed to review the suitability of replacing the design specified

stainless steel manifold plugs with brass caps and test fittings on various equalizing

block valve drain ports for pressure, differential pressure, and flow transmitters. This

issue was entered into the licensees corrective action program as Condition

Report 36439. Because this finding was determined to be of very low safety significance

and was entered into the licensees corrective action program, this violation is being

treated as a noncited violation consistent with Section 2.3.2 of the NRC Enforcement

Policy: NCV 05000482/2011003-05, Failure to Assure Configuration Control of Safety-

Related Systems.

- 26 - Enclosure

.4 Steam Generator Tube Inspection Activities (71111.08-02.04)

a. Inspection Scope

The inspection procedure specified an assessment of in situ screening criteria to assure

consistency between assumed nondestructive examination flaw sizing accuracy and

data from the EPRI examination technique specification sheets. The inspection

procedure also specified assessment of appropriateness of tubes selected for in situ

pressure testing, observation of in situ pressure testing, and review of in situ pressure

test results. No conditions were identified that warranted in situ pressure testing. The

steam generators are original construction steam generators.

The inspectors reviewed both the licensee site-validated and qualified acquisition and

analysis technique sheets used during this refueling outage and the qualifying EPRI

examination technique specification sheets to verify that the essential variables

regarding flaw sizing accuracy, tubing, equipment, technique, and analysis had been

identified and qualified through demonstration.

Wolf Creek completed steam generator eddy current inspections for Refueling

Outage 18 on April 12, 2011. In accordance with the EPRI steam generator examination

guidelines, bobbin coil inspections were expanded in steam generator B due to

inspection results associated with wear at anti-vibration bar locations that resulted in a

C-2 condition. In accordance with the EPRI guidelines, another 20 percent of the tubing

in steam generator B was inspected. No other scope expansions were required. In

accordance with Technical Specification 5.5.9.c, nine tubes in steam generator B, three

tubes in steam generator C, and three tubes in steam generator D were plugged based

on inspection results indicating they contained flaws with a depth equal to or exceeding

40 percent of the nominal tube wall thickness. The damage mechanism associated with

each of the pluggable indications was wear at anti-vibration bar locations. No tubes in

steam generator A required plugging. No new corrosion damage mechanisms were

identified.

The following secondary side maintenance and inspections were performed:

each steam generator was: steam generator A, 26 lbs; steam generator B,

34 lbs; steam generator C, 30 lbs; and steam generator D, 27.5 lbs.

  • Foreign object search and retrieval of all four steam generators to locate, identify,

and retrieve foreign objects present on the steam generator tube sheet. Foreign

object search and retrieval was also performed to inspect for any possible loose

parts identified during the eddy current program. Minor foreign objects were

identified and addressed within the corrective action program and plant

procedures. Visual examination and eddy current testing verified that no

degradation was associated with any tubes surrounding the foreign objects.

  • In-bundle inspection of steam generators B and C to inspect the condition of the

top of the tube sheet and to augment the foreign object search and retrieval

- 27 - Enclosure

effort. No anomalies were identified during these inspections and the information

will be used for trending and to plan future maintenance operations.

condition of the upper steam drum components with regard to damage of any

kind. Ultrasonic testing was also performed on locations susceptible to erosion

on the feeding in steam generators B and C. No anomalies were identified and

the information will be used for trending and to plan future maintenance.

Specific documents reviewed during this inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 71111.08-02.04.

b. Findings

No findings were identified.

.5 Identification and Resolution of Problems (71111.08-02.05)

a. Inspection Scope

The inspectors reviewed 99 condition reports which dealt with inservice inspection

activities and found the corrective actions for inservice inspection issues were

appropriate. The specific condition reports reviewed are listed in the documents

reviewed section. From this review the inspectors concluded that the licensee had an

appropriate threshold for entering inservice inspection issues into the corrective action

program and had procedures that direct a root cause evaluation when necessary. The

licensee also had an effective program for applying industry inservice inspection

operating experience. Specific documents reviewed during this inspection are listed in

the attachment.

These actions constitute completion of the requirements for Section 71111.08-02.05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Inspection Scope

On June 14, 2011, the inspectors observed a crew of licensed operators in the plants

simulator to verify that operator performance was adequate, evaluators were identifying

and documenting crew performance problems; and training was being conducted in

accordance with licensee procedures. The inspectors evaluated the following areas:

  • Licensed operator performance
  • Crews clarity and formality of communications

- 28 - Enclosure

  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Crews correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Crews ability to identify and implement appropriate technical specification

actions and emergency plan actions and notifications

  • Compliance with assumptions for manual action timing in Chapter 15 of the

USAR

The inspectors compared the crews performance in these areas to preestablished

operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed-operator requalification

program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant system:

  • Vital switchgear air conditioning units

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures

- 29 - Enclosure

  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of one quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

  • June 3, 2011, Component cooling water train A while train B was inoperable

The inspectors selected these activities based on potential risk significance relative to

the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

- 30 - Enclosure

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one maintenance risk assessment and

emergent work control inspection sample as defined in Inspection

Procedure 71111.13 05.

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • May 18, 2011, Source range NI-31 high counts after loss of cavity cooling

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available so that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and USAR to

the licensee personnels evaluations to determine whether the components or systems

were operable. Where compensatory measures were required to maintain operability,

the inspectors determined whether the measures in place would function as intended

and were properly controlled. The inspectors determined, where appropriate,

compliance with bounding limitations associated with the evaluations. Additionally, the

inspectors also reviewed a sampling of corrective action documents to verify that the

licensee was identifying and correcting any deficiencies associated with operability

evaluations. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of three operability evaluations inspection samples

as defined in Inspection Procedure 71111.15-04.

b. Findings

No findings were identified.

- 31 - Enclosure

1R18 Plant Modifications (71111.18)

.1 Temporary Modifications

a. Inspection Scope

To verify that the safety functions of important safety systems were not degraded, the

inspectors reviewed the temporary modification identified as TMO 10-017, component

cooling water modification to radioactive waste building.

The inspectors reviewed the temporary modification and the associated safety-

evaluation screening against the system design bases documentation, including the

USAR and the technical specifications, and verified that the modification did not

adversely affect the system operability/availability. The inspectors also verified that the

installation and restoration were consistent with the modification documents and that

configuration control was adequate. Additionally, the inspectors verified that the

temporary modification was identified on control room drawings, appropriate tags were

placed on the affected equipment, and licensee personnel evaluated the combined

effects on mitigating systems and the integrity of radiological barriers.

These activities constitute completion of one sample for temporary plant modifications as

defined in Inspection Procedure 71111.18-05.

b. Findings

No findings were identified.

.2 Permanent Modifications

a. Inspection Scope

The inspectors reviewed key parameters associated with energy needs, materials,

timing, heat removal, control signals, licensing basis, and failure modes for the

permanent modification identified as the source range gamma metrics equivalency to

Westinghouse detectors.

The inspectors verified that modification preparation, staging, and implementation did

not impair emergency/abnormal operating procedure actions, key safety functions, or

operator response to loss of key safety functions; systems, structures and components

performance characteristics still meet the design basis; the modification design

assumptions were appropriate; and licensee personnel identified and implemented

appropriate corrective actions associated with permanent plant modifications. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample for permanent plant modifications

as defined in Inspection Procedure 71111.18-05.

- 32 - Enclosure

b. Findings

No findings were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • November 17, 2010, Startup feedwater pump testing after rebuild
  • March 7, 2011, Feedwater regulating bypass valve controller setting adjustment
  • April 1, 2011, Solid state protection system train B after Westinghouse card

testing

  • May 17, 2011, Offsite power to engineered safety features transformer A after

replacement of Raychem splices

  • June 12, 2011, Component cooling water to thermal barrier heat exchangers

after flow balance Procedure SYS EG-205

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following:

  • The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

  • Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the USAR,

10 CFR Part 50 requirements, licensee procedures, and various NRC generic

communications to ensure that the test results adequately ensured that the equipment

met the licensing basis and design requirements. In addition, the inspectors reviewed

corrective action documents associated with postmaintenance tests to determine

whether the licensee was identifying problems and entering them in the corrective action

program and that the problems were being corrected commensurate with their

importance to safety. Specific documents reviewed during this inspection are listed in

the attachment.

- 33 - Enclosure

These activities constitute completion of six postmaintenance testing inspection samples

as defined in Inspection Procedure 71111.19-05.

b. Findings

Introduction. The inspectors identified a finding of very low safety significance (Green)

involving the failure to follow the requirements of Procedure AP 16E-002, Post

Maintenance Testing Development, for the startup feedwater pump.

Description. On November 4-6, 2010, Wolf Creek workers performed maintenance on

the startup feedwater pump to replace a leaking pump casing gasket. Workers

disassembled the pump per the vendor manual instructions and found a split casing

gasket and both mechanical seals darkened and cracked from overheating. The pump

was reassembled using new parts including bearings, O-rings, mechanical seals, and

casing gasket. The service water cooling lines were also replaced. Wolf Creek

Procedure AP 16E-002, Post Maintenance Testing Development, states that it provides

guidelines to develop test criteria for plant equipment after the completion of

maintenance activities. The procedure also ensures proper testing is implemented to

prove components, systems, and sub-systems perform as designed after the completion

of maintenance activities. Furthermore, Procedure AP 16E-002, Revision 9C, step 6.2

and attachments, requires that when a pump is disassembled or replaced, the

postmaintenance testing includes a pump-flow capacity test be conducted to determine

the capability of the pump to produce the required flow rates within the range of

differential pressure limits. Also, it requires that vibration, bearing, and lubrication

temperatures, motor current, external leakage, and lubrication level are satisfactory.

The inspectors reviewed root cause corrective action 25817-02-14 which created

Procedure STN AE-007 to test the pump with no local actions and ensure a minimum

recirculation flow of 60,000 pounds per hour for pump protection. The inspectors did not

find a discussion of adequate flow. On November 17, 2010, Wolf Creek conducted

surveillance Procedure STN AE-007, Startup Main Feedwater Pump Operational Test,

following the pump reassembly. The only acceptance criteria listed in this procedure

was that the motor-driven feedwater pump started from the control room with no local

operator action. The test contained no acceptance criteria to ensure that after the

completion of maintenance activities, the pump could produce the required flow rates for

either low power or emergency operations.

The purpose of the motor-driven startup feedwater pump is to provide heated feedwater

to the steam generators during plant startup and shutdown operations. The startup

feedwater pump is a horizontal, multi-stage, centrifugal pump with a rated maximum flow

rate of 260,000 pounds per hour. Maximum flow through the startup feedwater pump

suction lines is limited to 230,000 pounds per hour to prevent excessive tube vibration in

the steam generator blowdown regenerative heat exchanger. According to Wolf Creek

training materials, Form APF 30E-004-01, Revision 2, Main Feedwater System, the

required steam generator flow rate during plant startup is 200,000 pounds per hour.

This is based on the maximum steam generator blowdown rate, the heat lost to ambient

surroundings from all main steam lines, and the maximum heatup rate of all main steam

lines and the turbine stop valve heat. The startup feed pump is also used in Emergency

- 34 - Enclosure

Management Guideline FR-H1, Response to Loss of Secondary Heat Sink, step 17, to

feed the steam generator until the steam generator level is restored to greater than the

minimum level for ensuring an adequate heat sink. The success criteria in emergency

operating procedures for feedwater is based on 270,000 pounds per hour for auxiliary

feedwater or greater than 6 percent narrow range steam generator level. The

emergency operating procedure setpoint document requires 250,000 pounds per hour

from each motor-driven auxiliary feedwater pump.

This issue is captured in Condition Report 39494. Wolf Creek issued a new work

package to conduct a single-point pump capacity test and complete the required

postmaintenance testing in accordance with Procedure AP 16E-002. Wolf Creek also

found that there was not a technical basis for the blowdown heat exchanger vibrations

which previously limited the allowable flow through the pump to approximately

200,000 pounds per hour. Wolf Creek initial calculations, pending final review, show that

the pump would be capable of enough flow to provide a heat sink.

Analysis. The failure to follow Procedure AP 16E-002 for developing test criteria for

plant equipment after the completion of maintenance activities is a performance

deficiency. The finding is more than minor because it is associated with the Mitigating

Systems Cornerstone attribute of equipment performance and it adversely affects the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Using Inspection

Manual Chapter 0609.04, the inspectors determined that the finding had very low safety

significance (Green) because it did not result in a loss of system safety function, an

actual loss of safety function of a single train for greater than its technical specification

allowed outage time, or screen as potentially risk significant due to a seismic, flooding,

or severe weather initiating event. The inspectors determined that the finding had a

cross-cutting aspect in the area of problem identification and resolution. Specifically,

Wolf Creek created a testing procedure in response to a root cause evaluation, but did

not consider acceptance criteria to ensure that the pump performs acceptably P.1(d).

Enforcement. Enforcement action does not apply because the performance deficiency

did not involve a violation of regulatory requirements. This finding is of very low safety

significance and the issue was entered into the licensee's corrective action program as

Condition Report 39494: FIN 05000482/2011003-06, Inadequate Acceptance Criteria

for Postmaintenance Testing of the Startup Feedwater Pump.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the refueling

outage, conducted from March 19 through June 22, 2011, and June 26-29, 2011, to

confirm that licensee personnel had appropriately considered risk, industry experience,

and previous site-specific problems. The inspectors determined that the plan ensured

sufficient defense in depth. During the refueling outage, the inspectors observed

portions of the shutdown and cooldown processes and monitored licensee controls over

the outage activities listed below.

- 35 - Enclosure

  • Configuration management maintains defense in depth, commensurate with the

outage safety plan, and in compliance with technical specifications.

  • Clearance activities were properly tagged and equipment configured to safely

support work.

  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error.

  • Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities.

  • Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system.

alternative means for inventory addition, and controls to prevent inventory loss.

  • Controls over activities that could affect reactivity.

specifications.

  • Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage.

  • Startup and power ascension, tracking of startup prerequisites, walkdown of

containment to verify that debris removal, and reactor physics testing.

  • Licensee identification and resolution of problems related to refueling outage

activities.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage sample and one forced

outage inspection sample as defined in Inspection Procedure 71111.20-05.

b. Findings

No findings were identified.

- 36 - Enclosure

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and technical

specifications to ensure that the surveillance activities listed below demonstrated that the

systems, structures, and/or components tested were capable of performing their

intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the significant surveillance test attributes were adequate to address the

following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method supported operability or functionality
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for restoring systems,

structures, and components not meeting acceptance criteria were correct

  • Reference setting data

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing. The following

surveillance testing was observed:

  • September 8, 2010, Main steam valve AB-V85 inservice valve test

- 37 - Enclosure

  • April 26, 2011, Filling, venting, and void surveillance of safety injection
  • May 13, 2011, Tan-delta testing of offsite power underground cables
  • May 14, 2011, STS PE-018, Containment integrated leak rate test
  • May 18, 2011, Containment isolation valve EJHV8811B inservice test

train B

  • June 15, 2011, STS IC-615A, Safety injection signal slave relay test

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of eight surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

No findings were identified.

.2 Surveillance Testing Associated with TI 2515/177, Managing Gas Accumulation in

Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems

a. Inspection Scope

When reviewing the April 26, 2011, filling, venting, and void surveillance of safety

injection and the May 24, 2011, filling, venting, and void surveillance of residual heat

removal train B surveillances listed above in Section 1R22.1, the inspectors verified that

the procedures were acceptable for (1) testing with shutdown operation, maintenance,

and subject system modifications; (2) void determination and elimination methods; and

(3) post-event evaluation.

The inspectors reviewed the procedures used for conducting surveillance tests and the

determination of void volumes to ensure that the acceptance criteria were satisfied and

would be reasonably assured to remain satisfied until the next scheduled surveillance test

(TI 2515/177, Section 04.03.a). Also, the inspectors reviewed procedures used for filling

and venting following conditions which may have introduced voids into the subject

systems to verify that the procedures acceptably addressed testing for such voids and

provided acceptable processes for their reduction or elimination (TI 2515/177,

Section 04.03.b). Specifically, the inspectors verified that:

- 38 - Enclosure

  • Gas intrusion prevention, refill, venting, monitoring, trending, evaluation, and void

correction activities were acceptably controlled by approved operating

procedures (TI 2515/177, Section 04.03.c.1)

  • Procedures ensured the system did not contain voids that may jeopardize

operability (TI 2515/177, Section 04.03.c.2)

  • Procedures established that void criteria were satisfied and will be reasonably

ensured to be satisfied until the next scheduled void surveillance (TI 2515/177,

Section 04.03.c.3)

  • The licensee entered changes into the corrective action program as needed to

ensure acceptable response to issues. In addition, the inspectors confirmed that

a clear schedule for completion is included for corrective action program entries

that have not been completed (TI 2515/177, Section 04.03.c.5)

  • Procedures included independent verification that critical steps were completed

(TI 2515/177, Section 04.03.c.6)

The inspectors verified the following with respect to surveillance and void detection:

  • Specified surveillance frequency was consistent with technical specification

requirements (TI 2515/177, Section 04.03.d.1)

  • Surveillance frequencies were stated or, when conducted more often than

required by technical specifications, the process for their determination was

described (TI 2515/177, Section 04.03.d.2)

  • Surveillance methods were acceptably established to achieve the needed

accuracy (TI 2515/177, Section 04.03.d.3)

  • Surveillance procedures included up-to-date acceptance criteria (TI 2515/177,

Section 04.03.d.4)

  • Procedures included effective follow-up actions when acceptance criteria are

exceeded or when trending indicates that criteria may be approached before the

next scheduled surveillance (TI 2515/177, Section 04.03.d.5)

  • Measured void volume uncertainty was considered when comparing test data to

acceptance criteria (TI 2515/177, Section 04.03.d.6)

  • Venting procedures and practices utilized criteria such as adequate venting

durations and observing a steady stream of water (TI 2515/177,

Section 04.03.d.7)

- 39 - Enclosure

  • An effective sequencing of void removal steps was followed to ensure that gas

does not move into previously filled system volumes (TI 2515/177,

Section 04.03.d.8)

  • Qualitative void assessment methods included expectations that the void will be

significantly less than allowed by acceptance criteria (TI 2515/177,

Section 04.03.d.9)

  • Venting results were trended periodically to confirm that the systems are

sufficiently full of water and that the venting frequencies are adequate. The

inspectors also verified that records on the quantity of gas at each location are

maintained and trended as a means of pre-emptively identifying degrading gas

accumulations (TI 2515/177, Section 04.03.d.10)

  • Surveillances were conducted at any location where a void may form, including

high points, dead legs, and locations under closed valves in vertical pipes

(TI 2515/177, Section 04.03.d.11)

  • The licensee ensured that systems were not preconditioned by other procedures

that may cause a system to be filled, such as by testing, prior to the void

surveillance (TI 2515/177, Section 04.03.d.12)

  • Procedures included gas sampling for unexpected void increases if the source of

the void is unknown and sampling is needed to assist in determining the source

(TI 2515/177, Section 04.03.d.13)

The inspectors verified the following with respect to filling and venting:

  • Revisions to fill and vent procedures to address new vents or different venting

sequences were acceptably accomplished (TI 2515/177, Section 04.03.e.1)

  • Fill and vent procedures provided instructions to modify restoration guidance to

address changes in maintenance work scope or to reflect different boundaries

from those assumed in the procedure (TI 2515/177, Section 04.03.e.2)

The inspectors verified the following with respect to void control:

  • Void removal methods were acceptably addressed by approved procedures

(TI 2515/177, Section 04.03.f.1)

of damage following a gas-related event in which pump acceptance criteria was

exceeded (TI 2515/177, Section 04.03.f.2)

Documents reviewed are listed in the attachment to this report.

This inspection effort counts towards the completion of TI 2515/177. See Section 4OA5

for additional information.

- 40 - Enclosure

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspector performed an in-office review of the Wolf Creek APF 06-002-01,

Emergency Action Levels, Revision 15A. This revision made two administrative

changes to EAL-6, Loss of Electrical Power/Assessment Capability. The change

included replacing the abbreviation D/Gs with the capitalized and bolded wording

DIESEL GENERATORS, and capitalizing and bolding the wording NB

TRANSFORMERS.

This revision was compared to its previous revision, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in

10 CFR 50.47(b) to determine if the revision adequately implemented the requirements

of 10 CFR 50.54(q). This review was not documented in a safety evaluation report and

did not constitute approval of licensee-generated changes; therefore, this revision is

subject to future inspection.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.04-05.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the

licensee for the 1st Quarter 2011 performance indicators for any obvious inconsistencies

prior to its public release in accordance with Inspection Manual Chapter 0608,

Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

- 41 - Enclosure

b. Findings

No findings were identified.

.1 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific

activity performance indicator for the period from the 2nd Quarter 2010 through the 1st

Quarter 2011. The inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6

to determine the accuracy of the performance indicator data reported during those

periods. The inspectors reviewed the licensees reactor coolant system chemistry

samples, technical specification requirements, issue reports, event reports, and NRC

integrated inspection reports for the period of April 1, 2010, through March 31, 2011, to

validate the accuracy of the submittals. The inspectors also reviewed the licensees

condition report database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this indicator and none were

identified. In addition to record reviews, the inspectors observed a chemistry technician

obtain and analyze a reactor coolant system sample. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one reactor coolant system specific activity

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.2 Reactor Coolant System Leakage (BI02)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage

performance indicator for the period from the 2nd Quarter 2010 through the

1st Quarter 2011. The inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6

to determine the accuracy of the performance indicator data reported during those

periods. The inspectors reviewed the licensees operator logs, reactor coolant system

leakage tracking data, issue reports, event reports, and NRC integrated inspection

reports for the period of April 1, 2010, through March 31, 2011, to validate the accuracy

of the submittals. The inspectors also reviewed the licensees condition report database

to determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Specific documents

reviewed are described in the attachment to this report.

These activities constitute completion of one reactor coolant system leakage sample as

defined in Inspection Procedure 71151-05.

- 42 - Enclosure

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of various baseline inspections discussed in previous sections, the inspectors

reviewed issues to verify that they were being entered into the Wolf Creek corrective

action program at an appropriate threshold. The inspectors verified the program to be

addressing issues in a timely manner as well as identifying and correcting adverse

trends. The inspectors reviewed attributes that included:

  • Complete and accurate identification of the problem
  • Timely correction, commensurate with the safety significance
  • Evaluation and disposition of performance issues, generic implications, common

causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews

  • Classification, prioritization, focus, and timeliness of corrective actions.

Minor issues entered into the licensees corrective action program because of the

inspectors observations are included in the attached list of documents reviewed.

These reviews for the identification and resolution of problems did not constitute any

additional inspection samples. They were considered a part of the inspections

performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

The inspectors performed a daily screening of items entered into the licensees

corrective action program through review of the Wolf Creeks daily corrective action

documents.

- 43 - Enclosure

The inspectors performed these daily reviews as part of their plant status monitoring

activities and did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the Wolf Creek corrective action program and

associated documents to identify trends that could represent a more significant safety

issue. The inspectors focused their review on repetitive equipment issues, but also

considered the results of daily corrective action item screenings, licensee trending

efforts, and licensee human performance results. The inspectors considered the

6-month period of January through June 2011 although some examples expanded

beyond those dates where necessary.

The inspectors also reviewed issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and maintenance rule assessments.

The inspectors compared and contrasted their results with the conclusions reached in

the Wolf Creek corrective action program trending reports.

The inspectors reviewed corrective actions for problem identification and resolution and

human performance cross-cutting themes.

These activities constitute completion of a one semi-annual trend inspection sample as

defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

.4 Selected Issue Follow-up Inspection

a. Inspection Scope

During a review of Wolf Creek corrective action program items, the inspectors noted a

condition report documenting over drilling of stud holes on a feedwater regulating valve

body. The inspectors reviewed vendor manuals and station procedures for drilling and

installing Heilicoil inserts. The inspectors reviewed vendor calculations for the strength

of the joint. The inspectors interviewed engineers regarding the procedure and

determined that work performed was consistent with vendor instructions.

- 44 - Enclosure

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

4OA3 Event Follow-up (71153)

.1 March 19, 2011, Safety Injection

a. Inspection Scope

On March 19, 2011, with the reactor in hot standby, the inspectors responded to the

control room when Wolf Creek received a safety injection signal for a rapid steamline

pressure decrease. The inspectors reviewed control room logs and plant computer data.

The inspectors interviewed control room operators about the conditions leading up to the

event as well as the plant response. The inspectors reviewed plant operating practices

regarding methods of feedwater heating, main steam procedures, and emergency

operating procedures. From interviews with several members of the operating crew and

plant data before and after the event, the inspectors independently reviewed the

sequence of events:

  • The crew assumed the watch in Mode 1 and reduced reactor power to Mode 3

for Refueling Outage 18.

  • On March 18, 2011, SYS AE-200, Feedwater Preheating During Plant Startup

and Shutdown, Revision 29, was entered for the plant shutdown.

  • At midnight, the turbine was tripped in accordance with procedure.
  • At 12:07 a.m., feedwater temperature and steam flows begin oscillating. Over

the next hour, feedwater temperature and steam flows oscillated. It was later

determined that the oscillations were due to manual control of FB-PIC 300

combined with solenoid valve air leakage. This action was not peer-checked and

control room supervision was not made aware. PIC-300 controls valve FB-17A

which admits steam to the high pressure feedwater heaters. This is a large

steam demand. The heaters had several temperature swings. This was not

identified until after the safety injection.

  • At 12:37 a.m., March 19, the reactor entered Mode 2.
  • At 12:54 a.m., March 19, the reactor entered Mode 3.
  • At 1:00 a.m., letdown automatically isolated at 17 percent pressurizer level due to

a cooldown in progress.

- 45 - Enclosure

  • At 1:01 a.m., reactor coolant temperature could not be maintained, operators

shut the main steam isolation valves to stop the cool down. Reactor coolant

system temperature subsequently recovered to 560°F. Main feedwater pump A

turbine was subsequently tripped from the control room.

temperature decreases.

steam from the main steam header. Steam line temperature decreases.

Procedure SYS AB-120. This procedure is intended for use in Mode 4 with a

maximum steam line pressure of 300 psi. Steam line pressure was

approximately 1000 psi. Precaution 4.5 and step 6.14.2 require that main steam

isolation valve differential pressure be less than 20 psi to open a main steam

isolation valve. Senior reactor operators and management oversight mark these

steps as not applicable.

pressure rate on steam line C triggered an automatic safety injection signal.

  • Operators entered EMG E-0, Response to Reactor Trip or Safety Injection.
  • The pressurizer power-operated relief valve began cycling due to the pressure

increase from the high head centrifugal charging pumps adding inventory to the

reactor coolant system.

  • At 4:11 a.m., the safety injection signal was reset and Technical

Specification 3.0.3 was entered for both trains of emergency core cooling system

inoperable because automatic safety injection signal was blocked.

  • At 4:12 a.m., high pressure injection was terminated when the boron injection

tank valves were shut.

  • At 4:18 a.m., pressurizer power-operated relief valve stops cycling and closes.
  • At 4:23 a.m., Wolf Creek transitioned to Procedure EMG ES-03, Safety Injection

Termination.

established to reduce pressurizer level from a high of 88 percent.

  • At 5:20 a.m., Wolf Creek completed Procedure EMG ES-03 and transitioned to

Procedure OFN EM-024 Safety Injection Recovery.

- 46 - Enclosure

  • At 5:54 a.m., Wolf Creek notified the headquarters operations officer of the event

by making event notification 46685 per 10 CFR 50.72(b)(2)(iv)(A) which is a

4-hour report for emergency core cooling system discharge into the reactor

coolant system.

  • At 6:39 a.m., both reactor trip breakers were closed using SYS SF-120 and

Technical Specification 3.0.3 was exited.

information regarding safety system actuation and loss of an accident mitigation

safety system after the inspectors identified that these 8-hour reporting

requirements may also apply to this event. Condition report 34995 was written

for the potentially missed reports.

plant using the atmospheric relief valves to a temperature where the residual

heat removal system could be placed in service.

b. Findings

Introduction. A Green self-revealing cited violation of Technical Specification 5.4.1.a,

Administrative Procedures, was reviewed involving the failure to correct a previous

violation for an inadequate main steam system procedure. Specifically,

Procedure SYS AB-120 was not corrected to establish appropriate conditions to open a

main steam isolation valve. The inadequate procedure resulted in a safety injection.

Description. The inspectors reviewed a March 5, 2010, event involving excessive steam

generator level swell and feedwater isolation following opening of a main feedwater

isolation valve described in Condition Report 23938 and noncited violation

NCV 05000482/2010004-01. Wolf Creek determined the cause of the March 5, 2010,

P-14 feedwater isolation was an inadequate means of determining the pressure

difference across the main steam isolation valves using control room pressure

indicators. Procedure SYS AB-120, Main Steam and Steam Dump Startup and

Operation, Revision 24, used an acceptance criterion of less than 25 psi differential

pressure to allow opening of a main steam isolation valve. The procedure directed the

operators to determine valve differential pressure using control room indicators before

opening the main steam isolation valves. The control room instruments have ranges

from 0 to 1300 psi or greater with a 25 psi scale and are accurate to within plus or minus

25 to 38 psi. The inspectors concluded the apparent cause evaluation in Condition

Report 23938 appropriately determined that instrument uncertainty equal to or greater

than the procedures acceptance criteria was not reasonable. Subsequently, Wolf Creek

revised Procedure SYS AB-120 to direct operators to determine differential pressure

using locally installed instruments in lieu of the control room pressure indicators, but this

change was only implemented for steam line pressures below 300 psi. Additional

changes were made to several procedures which reduced the allowable steam

generator level band when opening a main steam isolation valve.

Procedure SYS AB-120 revisions did not address steam pressures above 300 psi nor

- 47 - Enclosure

were its precautions and limitations updated to reflect main control board instrumentation

accuracy.

On March 19, 2011, Wolf Creek was in Mode 3 shutting down for a refueling outage.

The steam header pressure was 1000 psi. At 1:01 a.m., operators shut all main steam

isolation valves due to an excessive cooldown. Several hours later, the operators began

to open the valves using Procedure SYS AB-120. A tighter acceptance criterion of

20 psi differential pressure was specified in the procedure before opening a main steam

isolation valve. Wolf Creek operators did not use local instruments as specified by the

procedure. Instead they used control room instruments to determine main steam line

pressures on both side of the main steam isolation valves without considering that the

instrument uncertainty exceeded the range of acceptance criteria. While the control

room pressure and temperature instruments indicated that the differential pressure was

acceptable, actual differential pressure was about 200 psi. When main steam isolation

valve C was opened, a safety injection signal occurred.

The inspectors reviewed corrective actions for Procedure SYS AB-120 and found

several missed opportunities to correct the deficiency. On October 18, 2010, Condition

Report 29168 was written stating Guidance for opening MSIVs not good above 35 psi

steam press, as its problem description. Wolf Creek reviewed Condition Report 30453

which responded to noncited violation NCV 05000482/2010004-01 and appropriately

concluded that the evaluation was flawed for two reasons. First, Condition Report 30453

failed to incorporate the instrument uncertainty issue previously identified in Condition

Report 29168 into the precautions and limitations of Procedure SYS AB-120. Second,

Condition Report 30453 failed to address the full range of anticipated plant conditions

which may require opening a main steam isolation valve, specifically steam pressures

above 300 psi. The inspectors concluded the failure to implement comprehensive

corrective actions to address the March 5, 2010, event directly contributed to the

March 19, 2011, inadvertent safety injection event and constituted a failure to restore

compliance for noncited violation NCV 05000482/2010004-01.

The inspectors reviewed the safety impact of the safety injection transient on Wolf

Creek. Actual safety impacts included a waterhammer on the main steam lines. This

caused a partial failure of main steam isolation valve actuator to bonnet gaskets. The

pressurizer power-operated relief valve 455 cycled seven times. Main feedwater was

lost when the feedwater isolation valves received a close signal from the safety injection.

Emergency core cooling system injection check valve BB8948C experienced body-to-

bonnet gasket leakage. The pressurizer started at 17 percent level and filled to

88 percent level until letdown was reestablished. Inadvertent safety injection has the

potential to challenge the pressurizer safety valves and escalate to a loss of coolant

accident if not terminated.

Analysis. The failure to correct deficiencies in Procedure SYS AB-120 for steam

pressures above 300 psi was a performance deficiency. The inspectors determined that

this finding was more than minor because it impacted the equipment performance

attribute for the Initiating Events Cornerstone and it affected the cornerstone objective to

limit the likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Specifically, this issue relates to

- 48 - Enclosure

the configuration control attribute for shutdown equipment alignment. The inspectors

evaluated the significance of this finding using Inspection Manual Chapter 0609.04.

Assuming worst case degradation, the finding resulted in exceeding the technical

specification limit for reactor coolant system leakage due to the pressurizer power-

operated relief valve cycling. Therefore, the inspectors screened the finding to a

Phase 2 review by the senior reactor analyst. The senior reactor analyst used the Wolf

Creek SPAR Model and concluded that the incremental core damage probability

was 3.7E-7, Green. The inspectors found that the cause of the finding has a cross-

cutting aspect in the area of problem identification and resolution associated with the

corrective action program. Specifically, several evaluations failed to include an adequate

extent of condition review that identified that the procedures were inadequate for

opening a main steam isolation valve at system pressures above 300 psi P.1(c).

Enforcement. Technical Specification 5.4.1.a requires that procedures be

established, implemented, and maintained covering the activities described in

Regulatory Guide 1.33, Revision 2, Appendix A. Regulatory Guide 1.33, Revision 2,

Appendix A, Section 3.i, requires procedures for the startup, operation, and

shutdown for the main steam system. Wolf Creek Procedure SYS AB-120, Main

Steam and Steam Dump Startup and Operation, Revision 27, implements these

requirements for the main steam system. Contrary to the above, from March 5,

2010, to March 19, 2011, Wolf Creek Procedure SYS AB-120 had not been

maintained to cover activities for the startup, operation and shutdown of the main

steam system. Specifically, Procedure SYS AB-120, Revision 27, contained

inadequate steps necessary to open a main steam isolation valve without causing a

safety injection signal.This issue and the corrective actions are being tracked by the

licensee in Condition Report 34964. Due to the licensees failure to restore

compliance from previous NCV 05000482/2010004-01 within a reasonable time after

the violation was identified, this violation is being cited as a Notice of Violation

consistent with Section 2.3.2 of the Enforcement Policy: VIO 05000482/2011003-07,

Failure to Correct Procedure for Opening Main Steam Isolation Valves

(EA-11-149).

.2 March 21, 2011, Low Temperature Overpressure System Actuation.

a. Inspection Scope

On March 21, 2011, Wolf Creek was shutdown for a refueling outage. While cleaning

the reactor coolant system, operators failed to maintain reactor coolant system pressure

below 350 psi. When charging was increased for the clean-up, the low temperature

overpressure setpoint was exceeded causing pressurizer power-operated relief

valve 455 to lift three times. The inspectors interviewed reactor operators, reviewed

control room logs, procedures, pressure and temperature limits report, License

Amendment 130, and plant computer data.

- 49 - Enclosure

b. Findings

Introduction. The inspectors reviewed a self-revealing Green noncited violation of

Technical Specification 5.4.1.a, Procedures, for failure to maintain pressure below the

low pressure overpressure protection setpoint.

Description. On March 21, 2011, Wolf Creek was adjusting the chemical and volume

control system to inject hydrogen peroxide into the reactor coolant system to induce a

crud burst to reduce system radioactivity for the refueling outage. Letdown flow was at

approximately 63 gpm. The unit was in Mode 5 with the pressurizer solid and

maintaining reactor coolant system temperature at 160°F and 350 psig pending reactor

coolant system cleanup. The pressurizer is considered solid when it is water filled

because water is not compressible when compared with a gas bubble. Charging and

letdown were in the process of being increased in order to increase the rate of reactor

coolant system cleanup. At 2:52 p.m., power-operated relief valve 455A cycled three

times over the following 4 minutes when reactor coolant system pressure increased to its

lift setpoint of 415 psig. Reactor coolant system pressure control was subsequently

reestablished at 350 psig when letdown flow was increased to approximately 120 gpm.

During interviews, the operators stated that the charging header controller was adjusted

before letdown, and that it was sluggish at the low pressure. The procedure only stated

to maintain pressure and did not provide specific guidance. At the time, operators had a

band of 330-350 psig to maintain, and the operators stated that the normal charging

pump controller was sluggish at its reduced operating pressure. The operators stated

that the charging pump controller was increased three times and on the third time, a

large increase in charging was received.

The inspectors reviewed plant computer data and found that when charging header

pressure was initially increased without increasing letdown flow from the residual heat

removal system, the reactor coolant system pressure rapidly increased. As the 4 minute

event progressed, the normal charging pump controller was adjusted several times while

letdown was progressively increased. Charging header pressure and flow drove the

increases in reactor coolant system pressure. The three lifts of the power operated relief

valve were due to the changes in charging header pressure with a solid pressurizer.

The inspectors reviewed Procedures GEN 00-006 and SYS BG-120 and found that they

did not contain any precautions or limitations regarding the reactor coolant system

pressure response to a sluggish charging controller with a water-solid plant. There were

no instructions that letdown should have been increased first and to adjust charging

second, to match. Procedure GEN 00-006, step 6.44.8.3 only stated to maintain a

pressure band of 325-350 psig when adjusting charging flow. Although the procedures

had several steps to maximize letdown and charging for reactor coolant system clean-

up, there were no specific steps on how to perform this, and there were no continuous

action steps or precautionary steps to prevent over-pressurizing the reactor coolant

system.

The inspectors reviewed the Just in Time Training for the refueling outage and

identified that it contained guidance on raising letdown to 120 gpm and subsequently

taking the plant solid. It did not contain guidance or lessons on manipulating letdown

- 50 - Enclosure

with the plant solid. With the reactor coolant system pressure at the upper end of the

band specified in Procedure GEN 00-006, letdown would be appropriate to adjust first to

prevent the lifting of relief valves. If the reactor coolant system was solid at the lower

end of the pressure band specified in Procedure GEN 00-006, adjusting charging first

would be appropriate to avoid a decrease in reactor coolant system pressure that could

meet the reactor coolant pump trip criteria.

Analysis. Failure to maintain pressure below the power operated relief valve setpoint

was a performance deficiency. The performance deficiency was more than minor

because it impacted the Initiating Events Cornerstone objective of configuration control

to limit the likelihood of those events that upset plant stability and challenge critical

safety functions during shutdown as well as power operations. The significance of the

finding was determined using Inspection Manual Chapter 0609, Significance

Determination Process, Appendix G, Checklist 2, and determined to be of very low

safety significance (Green), because it did not cause the loss of mitigating capability of

core heat removal, inventory control, power availability, containment control, or reactivity

control. Additionally, the finding also did not cause any low temperature overpressure

technical specifications to be exceeded. The inspectors found that the cause of the

finding had a cross-cutting aspect in the area of human performance. Specifically,

operators had to rely on skill of the craft when procedures should have supplied more

instruction for manipulating charging and letdown with the pressurizer water solid H.2.c].

Enforcement. Wolf Creek Technical Specification 5.4.1.a, Procedures, requires, in

part, that written procedures shall be established, implemented and maintained for the

activities recommended in Regulatory Guide 1.33, Revision 2, Appendix A,

February 1978. Regulatory Guide 1.33, Revision 2, Appendix A, February 1978,

General Plant Operating Procedures, Section 2.j, requires procedures for hot standby

to cold shutdown. Procedure GEN 00-006, Hot Standby to Cold Shutdown,

Revision 76, implements this procedure. Procedure GEN 00-006, Step 6.44.8.3 required

the licensee to maintain a pressure band below 350 psig when manipulating charging

flow. Contrary to the above, on March 21, 2011, Wolf Creek did not implement

Procedure GEN 00-006, step 6.44.8.3, to maintain a pressure band below 350 psig

when manipulating charging flow. Because the finding is of very low safety significance

and has been entered into the licensees corrective action program as Condition

Report 35244, this violation is being treated as a noncited violation consistent with

Section 2.3.2 of the NRC Enforcement Policy: NCV 05000482/2011003-08, Failure to

Maintain Reactor Coolant System Pressure Below Relief Valve Setpoint.

.3 April 5, 2011, Vital Switchgear Room Fire

a. Inspection Scope

The inspectors responded to a fire in the switchgear rooms and to the control room. The

inspectors interviewed fire brigade leaders and the control room shift manager regarding

the fire alarms and the fire brigade response and examined the damage inside of

nonvital inverter PN009. The inspectors observed postfire actions to ventilate the area

to remove the smoke and Halon.

- 51 - Enclosure

b. Findings

Introduction. The inspectors reviewed a self-revealing Green noncited violation of

License Condition 2.C.5 for failure to implement adequate fire impairments which

affected both trains of vital ac and dc switchgear.

Description. On March 26, 2011, Wolf Creek implemented a breach authorization

requiring a continuous fire watch because the doors between vital ac and dc switchgear

rooms were propped open. These doors are 3-hour fire barriers. This was done to allow

the train B air conditioning unit and ventilation to provide cooling to the train A

switchgear in accordance with Procedure SYS GK-200, Inoperable Class IE A/C Unit.

With the train A air conditioning unit out of service, two sets of double doors were

propped open between vital ac switchgear trains A and B on the 2000 elevation of the

control building. On April 5, 2010, Wolf Creek completed preventive maintenance on

nonvital inverter PN009 which is located in the 2000 elevation train A vital switchgear

room. Wolf Creek was preparing to test nonvital inverter PN009 and reenergized it for

about 20 minutes. Two electricians were at the inverter cabinet in the train A vital

switchgear room when smoke began emanating from the top of the cabinet. The

electricians shut off the dc input and opened the ac output breakers on the lower door of

the cabinet. The Halon actuation alarm sounded indicating that Halon would discharge

into the room in 30 seconds. One electrician told the fire watch that it was necessary to

evacuate. The two electricians and the fire watch were egressing through the north

missile door when the Halon system discharged. The breached doors between ac

switchgear rooms were not shut. The fire brigade responded and removed an extension

cord and shut the doors between the vital ac switchgear rooms. The fire brigade found

only smoke and Halon in the rooms and no fire at PN009. Subsequent examination by

Wolf Creek and the vendor found that vendor errors in labeling the terminals caused an

excessive current in an adjacent transformer which caused the fire. Both transformers

were replaced. The vendor stated that no other damage occurred. Condition

Report 36719 was written on the inadequate fire watch response.

The inspectors interviewed the April 5 fire watch and found that he thought Halon was

going to discharge into both the trains A and B vital switchgear rooms. Thus, he would

have to egress through the north missile door and not to the train B switchgear room.

He understood his duty to shut the doors upon alarm, but indicated that he would not be

able to remove the extension cord, shut the doors, and exit within 30 seconds. The fire

watch stated that removing the extension cord and shutting the doors would likely take

3 to 4 minutes. The inspectors found that the Halon system was designed to discharge

into the switchgear room with the alarming smoke detectors. The fire watch also stated

that he left the room without shutting the doors because the electricians instructed him to

leave the room prior to the Halon actuation.

The inspectors found that the only written instructions for fire watches was the statement

on the fire impairment which said Per AP 10-104, section 6.1.9 (SYS GK-200), in case

of fire or Halon discharge, close doors 33011 & 33023 and exit area and notify control

room. Wolf Creek relies on training and reading of the fire impairment to understand

the compensatory action. The inspectors reviewed the design of the 1301 Halon system

and found that the system was sized to extinguish a fire in one switchgear room only.

- 52 - Enclosure

The inspectors found that with doors 33011 and 33023 (each a set of double doors)

open between vital switchgear rooms, the Halon system would not have been successful

at extinguishing a fire.

The inspectors reviewed written statements from the fire brigade, the fire watch, and the

electricians. The inspectors reviewed Procedure AP 10-107, Fire Protection Impairment

Control, and Procedure APF 10-104-01, Breach Authorization Permit, and found that

the requirements of the breach permit were not met because the fire watch failed to

close doors 33011 and 33023 during an actual fire. Procedure AP 10-104, step 5.62,

states, in part, that the boundary watch must be able to clear any cord or tool crossing a

breached barrier and to notify the control room if any condition in which a breached

barrier cannot be closed within the time requirements. The inspectors reviewed form

APF 10-104-01, breach authorization, for the 2000 and 2016 elevation switchgear

rooms and found no quantitative timing requirements for closing the doors. The

inspectors concluded that a 30-second acceptance criterion was critical because open

doors would prevent the Halon system from reaching the necessary concentration to

extinguish a fire. The inspectors found that the breach permit was not met because the

fire watch did not close the doors and that the breach permit was inadequate because it

did not contain timed acceptance criteria necessary to ensure the success of the Halon

system.

On April 12, 2011, the inspectors interviewed a different vital ac switchgear room fire

watch and found that the watch was also not clear on their duty to shut the doors

regardless of what other workers tell them to do. The fire watch did have correct

knowledge of the Halon system, the 30-second delay between the alarm and discharge,

and what room to egress to depending on the fire location. The inspectors shared this

with the outage control center.

On April 14, 2011, Wolf Creek inhibited the Halon systems for the rod-drive motor

generator set room, all vital dc switchgear rooms, and the vital ac switchgear rooms.

Wolf Creek judged it more important to ensure that the fire watches shut the fire doors

rather than have an ineffective automatic Halon system actuation. On April 13, 2011,

Wolf Creek initiated new training for all fire watches to ensure they had copies of the

breach permits. The inspectors interviewed fire watches on April 14, 2011, and found

that the watches had a complete and correct understanding of their duties.

The inspectors found that the inability to close these fire doors was identified in

Refueling Outage 16 in Condition Report 2008-1357. Actions included protective

equipment and training to remove cables crossing the open doors, but the inspectors

concluded that those corrective actions did not ensure proper fire watch actions on

April 5, 2011. Corrective actions included APF 10-104-06 to include Special

Requirements for Boundary Watch. Although a new section of the breach impairments

was created, it was typically not utilized when breaching vital switchgear doors.

As an extent of condition review, the inspectors reviewed previous fire impairments for

Procedure SYS GK-200 for open fire doors on the 2000 and 2016 control building

elevations. The inspectors found that Procedure SYS GK-200 had been implemented

- 53 - Enclosure

23 times over the prior year of operation representing approximately 36 days of

impairments for both trains of ac and dc switchgear and batteries.

Analysis. The failure to implement adequate fire watches that ensured the success of

the Halon system was considered a performance deficiency. The performance

deficiency was considered more than minor because it impacted the Initiating Events

Cornerstone and its objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Specifically, the fire area of the protection against external factors attribute

was impacted. The inspectors used Inspection Manual Chapter 0609.04 to screen the

finding to Inspection Manual Chapter 0609, Appendix F, because the fire protection

defense-in-depth strategies involving automatic suppression, fire barriers, administrative

controls were degraded. Because the subject finding was not clearly covered by the

approach used in Appendix F, the senior reactor analyst performed a Phase 3 analysis.

The doors were open for 36 days, so a 36-day exposure period (EXP) was used. The

analyst used generic values for the Fire Ignition Frequency (FI), Severity Factor (PSF)

and the probability of manual suppression before damage (PMS). The Fire Mitigation

Frequency (FM) was calculated as follows:

FM = FI * PSF * PMS * EXP

= 2.0 x 10-2/year * 0.1 * 0.1 * 36 days ÷ 365 days/year

= 1.97 x 10-5

The analyst assumed that if the fire grew to a point that it could spread to the opposite

train, it would actuate the opposite trains Halon system and cause an isolation of all

ventilation. However, there was no credible source of flammable materials that would

cause the growth of the fire into the opposite trains switchgear. Therefore, the analyst

quantified the conditional core damage probability (CCDP) for the failure of

Switchgear NB01 using the Standardized Plant Analysis Risk Model for Wolf Creek

Station, Revision 8.15. The resulting CCDP was 8.3 x 10-4. The final change in core

damage frequency (CDF) was calculated as follows:

CDF = FM * CCDP

= 1.97 x 10-5 * 8.3 x 10-4

= 1.6 x 10-8

Therefore, this finding was determined to be of very low safety significance (Green).

The inspectors found that the cause of the finding had a cross-cutting aspect in the area

of problem identification and resolution. Specifically, corrective actions from 2008

ineffective fire watches did not prevent recurrence of the April 5, 2011, inadequate fire

watch P.1.d].

Enforcement. License condition 2.C.(5) states, in part, that the licensee shall maintain in

effect all provisions of the approved fire protection program as described in the

- 54 - Enclosure

Standardized Nuclear Unit Power Plant System USAR for the facility through

Revision 17, the Wolf Creek site addendum through Revision 15, and as approved in the

safety evaluation report through Supplement 5, Amendments 191 and 193. AP 10-100,

fire protection program, states, in part, that AP 10-104, Breach Authorization, is part of

the fire protection program. Procedure AP 10-104, step 5.62, states, in part, that the

boundary watch must be able to clear any cord or tool crossing a breached barrier and

to notify the control room if any condition in which a breached barrier cannot be closed

within the time requirements. Procedure AP 10-104, steps 6.1.8 and 6.1.9, require, in

part, that a continuous fire watch shall be established for the vital switchgear rooms

because open doors will reduce Halon concentration and expose redundant trains to the

same fire. Contrary to the above, prior to April 14, 2011, the licensee failed to implement

and maintain in effect all provisions of the approved fire protection program. Specifically,

the licensee used an ineffective fire barrier breach permit system that did not ensure that

the Halon systems would effectively extinguish fires because the fire watches could not

clear any cord or tool crossing a breached barrier and did not notify the control room of a

condition in which a breached barrier could not be closed within the time requirements.

The licensee entered this issue into their corrective action program as Condition

Report 36719. Because this violation was of very low safety significance and it was

entered into the corrective action program, this violation is being treated as a noncited

violation, consistent with the NRC Enforcement Policy, Section 2.3.2:

NCV 05000482/2011003-09, Inadequate Fire Watch Defeats Halon Fire Suppression in

Vital Switchgear Rooms During Fire.

.4 (Closed) Licensee Event Report (LER) 2006-003-00, Indications Discovered on

Pressurizer during Preplanned Inservice Inspections

On October 11, 2006, during Refueling Outage 15, engineering personnel performing

preplanned inservice examination of the pressurizer nozzle to safe end dissimilar metal

welds identified five circumferential flaw indications. Three indications were located in

the surge nozzle dissimilar metal weld, one indication was in the safety nozzle C

dissimilar metal weld, and one indication was in the relief nozzle dissimilar metal weld.

The locations were all part of the reactor coolant system pressure boundary. There was

no evidence of reactor coolant system pressure boundary leakage. The most probable

mechanism responsible for the indications was primary water stress corrosion cracking.

Wolf Creek Generating Station was in Mode 5, cold shutdown. Weld overlay repairs of

the flaw indications were performed prior to the unit's return to power operations. The

inspectors reviewed LER 05000482/2006-003-00 to verify that the cause was identified

and that corrective actions were appropriate. This LER is closed.

.5 (Closed) Notice of Violation VIO 05000482/2010006-05, Failure to Correct NRC

Identified NCV Apparent Cause Evaluation Vice Root Cause Evaluation for Essential

Service Water

The violation involved the failure to perform an adequate cause evaluation and to take

corrective actions to preclude repetition for a significant condition adverse to quality.

Although determined to be of very low safety significance (Green), this violation was

cited in Notice of Violation 05000482/2010006-05 because not all of the criteria specified

in Section 2.3.2 of the NRC Enforcement Policy were satisfied (EA-10-160). Specifically,

- 55 - Enclosure

the Wolf Creek Generating Station failed to restore compliance within a reasonable time

for a previously NRC identified noncited violation as documented in NRC Inspection

Report 05000482/2009007-03. The inspectors reviewed the corrective actions

completed by the licensee and verified that the cause was identified and that corrective

actions were appropriate. This violation is closed.

4OA5 Other Activities

.1 (Closed) NRC TI 2515/177, Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems (NRC Generic Letter 2008-01)

a. Inspection Scope

As documented in Sections 1R04.1 and 1R22 of this report, the inspectors confirmed the

acceptability of the described actions for the high pressure safety injection system and

the containment spray system. This inspection effort counts towards the completion of

TI 2515/177 which is closed in this inspection report.

The inspectors evaluated whether the licensee maintained documents, installed system

hardware, and implemented actions with the information provided in their response to

NRC Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems. Specifically, the inspectors

verified that the licensee has implemented or was in the process of implementing the

commitments, modifications, and programmatically controlled actions described in the

response to Generic Letter 2008-01. The inspectors conducted their review in

accordance with TI 2515/177 and considered the site-specific supplemental information

provided by the Office of Nuclear Reactor Regulation (NRR) to the inspectors.

b. Inspection Documentation

The inspectors reviewed the licensing basis, design, testing, and corrective actions as

specified in the TI. The specific items reviewed and any resulting observations are

documented below.

Licensing Basis. The inspectors reviewed selected portions of licensing basis

documents to verify that they were consistent with the NRR assessment report and that

the licensee properly processed any required changes. The inspectors reviewed

selected portions of technical specifications, technical specification bases, and the

USAR. The inspectors also verified that applicable documents that described the plant

and plant operation, such as calculations, piping and instrumentation diagrams,

procedures, and corrective action program documents, addressed the areas of concern

and were changed, if needed, following plant changes. The inspectors confirmed that

the licensee performed surveillance tests at the frequency required by the technical

specifications. The inspectors verified that the licensee tracked their commitment to

evaluate and implement any changes that will be contained in the technical specification

task force traveler.

- 56 - Enclosure

Design. The inspectors reviewed selected design documents, performed system

walkdowns, and interviewed plant personnel to verify that the licensee addressed design

and operating characteristics. Specifically:

  • The inspectors verified that the licensee had identified the applicable gas

intrusion mechanisms for their plant.

  • The inspectors verified that the licensee had established void acceptance criteria

consistent with the void acceptance criteria identified by NRR. If NRR

acceptance criteria were not met, then the inspectors verified that the licensee

has justified the deviations. The inspectors also confirmed that the range of flow

conditions evaluated by the licensee was consistent with the full range of design

basis and expected flow rates for various break sizes and locations.

The inspectors noted that the licensee used the methods developed by

Westinghouse to estimate the suction voids emergency core cooling system

pumps. Westinghouse documented their review and test results

in WCAP-16631-NP, Testing and Evaluation of Gas Transport to the Suction of

ECCS Pumps. Wolf Creek used WCAP-16631-NP to show that GOTHIC can

acceptably predict quantitative void transport behavior. However, the inspectors

noted that test configuration and conditions differed from actual plant

configuration and conditions. These methods relied on industry testing

documented by Westinghouse and used the GOTHIC computer code to better

estimate the impacts resulting from voiding in the emergency core cooling

systems.

The licensee had received analyses for their facility based upon the simplified

equation developed by Westinghouse, which would more accurately estimate the

void sizes allowed on the suction of the emergency core cooling pumps without

affecting operability. In addition, the license had received a revised estimate of

water hammer effects developed by Fauske on the pump discharges for their

emergency core cooling systems. These analyses would replace the use of

GOTHIC. These analyses allow for a more realistic estimate of void sizes on

both the suction and discharge of the emergency core cooling system pumps.

The licensee had not accepted these analyses at the time of this inspection.

The inspectors discussed with NRR that the licensee had used these methods.

The ultimate acceptability of these methods required further evaluation by NRR

to: (1) better understand the acceptability of the application of the revised test

results contained in WCAP-16631-NP to void assessment analysis; (2) better

understand and evaluate the use of the simplified equation; and (3) assess

potential generic implications. The licensee documented these outstanding

issues in Condition Report 39943.

  • The inspectors selectively reviewed applicable documents, including calculations,

and engineering evaluations with respect to gas accumulation in the emergency

core cooling systems. Specifically, the inspectors verified that these documents

addressed venting requirements, aspects where pipes were normally void such

- 57 - Enclosure

as some spray piping inside containment, void control during maintenance

activities, and the effect of debris on strainers in containment emergency sumps

causing accumulation of gas under the upper elevation of strainers and the

impact on the required net positive suction head.

  • The inspectors conducted a walk down of selected regions of the emergency

core cooling systems in sufficient detail to assess the licensees walk downs.

The inspectors completed a full containment spray system alignment as

documented in Section 1R04. The inspectors also verified that the information

obtained during the licensees walkdown was consistent with the items identified

during the inspectors independent walk down.

  • The inspectors verified that piping and instrumentation diagrams and isometric

drawings that describe the residual heat removal and safety injection system

configurations. The review of the selected portions of isometric drawings

considered the following:

1. High point vents were identified.

2. High points without vents were recognizable.

3. Other areas where gas could accumulate and potentially impact

operability, such as at orifices in horizontal pipes, isolated branch lines,

heat exchangers, improperly sloped piping, and under closed valves,

were described in the drawings or in referenced documentation.

4. Horizontal pipe centerline elevation deviations and pipe slopes in

nominally horizontal lines that exceed specified criteria were identified.

5. All pipes and fittings were clearly shown.

6. The drawings were up to date with respect to recent hardware changes,

and that any discrepancies between as-built configurations and the

drawings were documented and entered into the corrective action

program for resolution.

  • The inspectors verified that the licensee had completed their walkdowns and

selectively verified that the licensee identified discrepant conditions in their

corrective action program and appropriately modified affected procedures and

training documents. The inspectors determined that the licensee appropriately

considered the differing gas intrusion mechanisms with one exception. The

inspectors noted that the licensee failed to analyze whether vortexing would

occur in their containment spray additive tank. The details of this issue are

described in Section 4OA5.1.e of this report.

Testing. The inspectors reviewed selected surveillance, postmodification test, and

postmaintenance test procedures and results implemented during power and shutdown

operations to verify that the licensee had approved and used procedures that addressed

- 58 - Enclosure

gas accumulation and/or intrusion into the subject systems. This review included the

verification of procedures used for conducting surveillances and determination of void

volumes to ensure that the licensee satisfied the established void criteria with

reasonable assurance until the next scheduled void surveillance. Also, the inspectors

reviewed procedures used for filling and venting following conditions that may have

introduced voids into the subject systems to verify that the procedures addressed testing

for such voids and provided processes for their reduction or elimination. The inspectors

observed the performance of the emergency core cooling system void surveillance as

documented in Section 1R22.

Corrective Actions: The inspectors reviewed selected actions from the 2011

assessment review and sampled other corrective action program documents to assess

how effectively the licensee addressed the issues in their corrective action program

associated with Generic Letter 2008-01. In addition, the inspectors verified that the

licensee implemented appropriate corrective actions for condition reports identified in the

9-month and supplemental responses. The inspectors determined that the licensee had

initiated a large number of corrective actions in response to previous events at their

facility. The inspectors determined that the licensee had effectively implemented the

actions required by Generic Letter 2008-01.

Based on this review, the inspectors concluded that reasonable assurance exists the

licensee will continue to implement the requirements of Generic Letter 2008-01 and will

complete all outstanding items. This TI is closed.

1. Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control for the failure to translate the design basis into

instructions, procedures, and drawings. The inspectors found that the licensee failed to

assess whether vortexing occurred in the containment spray additive tank during a

design-basis accident.

Description. The inspectors evaluated licensee activities related to evaluation of gas

intrusion into their emergency core cooling systems. The inspectors questioned whether

air entrainment in the containment spray system, as a result of vortexing in the

containment spray additive tank, affected the ability of the containment spray system to

remain full of water and meet the accident flow requirements. The licensee did not have

a calculation to determine whether vortexing would occur in their containment spray

additive tank at the required design flow rates. The licensee initiated Condition

Report 38715 to document this deficiency; initiated actions to calculate the effects of

vortexing in the containment spray additive tank during design basis flows; and

established a Mode 3 restraint related to completing the calculation to ensure that

containment spray would be operable as required.

The system used an eductor driven by discharge flow from both of the containment

spray pumps to draw sodium hydroxide from the single chemical additive tank during a

design-basis accident. Vacuum breakers allowed air into the tank as the liquid drained.

- 59 - Enclosure

Calculation EN M-024, Critical Submergence in Containment Spray Additive

Tank (TEN01) to Avoid Vortex, Revision 0, concluded that vortexing would not occur.

Analysis. Failure to implement design control measures to analyze whether containment

spray piping remained full of water was a performance deficiency. This finding was

more than minor because it affected the design control attribute of the Mitigating

Systems Cornerstone objective to ensure the availability, reliability, and capability of the

containment spray system to respond to initiating events and prevent undesirable

consequences. Specifically, the inspectors had reasonable doubt on the capability of

the containment spray system to properly inject because of vortexing in the containment

spray additive tank. The inspectors performed the significance determination using

Inspection Manual Chapter 0609.04. The finding was determined to be of very low

safety significance (Green) because it was a design or qualification deficiency confirmed

not to result in loss of operability or functionality. Although the failure to have this

calculation had existed since original construction, the inspectors determined this finding

reflected current performance since the licensee was required to evaluate likelihood of

tanks allowing gas intrusion into the emergency core cooling systems in response to

Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems. Consequently, this finding had

problem identification and resolution cross-cutting aspects associated with the corrective

action program in that the licensee did not evaluate thoroughly the potential for gas

intrusion from all possible tanks P.1(c).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

design control measures shall provide for verifying or checking the adequacy of design,

such as by the performance of design reviews, by the use of alternate or simplified

calculational methods, or by the performance of a suitable testing program, was

identified. Specifically, the design capability of the containment spray system requires

that the system be full of water in order to achieve and maintain the design rate of flow.

Contrary to the above, as of May 6, 2011, the licensee had not verified the adequacy of

the design capability of the containment spray system to remain full of water through

design review, calculation, or testing. Specifically, the licensee had not analyzed

whether vortexing in the containment spray additive tank would affect system flow. The

analysis demonstrated that no air should be entrained as a result of vortexing. The

licensee documented this issue in Condition Report 38715. Because this finding was of

very low safety significance and has been entered into the corrective action program, it

is being treated as a noncited violation consistent with Section 2.3.2 of the NRC

Enforcement Policy: NCV 05000482/2011003-10, Failure to Analyze for Vortexing in

Containment Spray Additive Tank.

.2 (Closed) NRC TI 2515/183, Followup to the Fukushima Daiichi Nuclear Station Fuel

Damage Event

a. Inspection Scope

The inspectors assessed the activities and actions taken by the licensee to assess its

readiness to respond to an event similar to the Fukushima Daiichi nuclear plant fuel

damage event. This included (1) an assessment of the licensees capability to mitigate

- 60 - Enclosure

conditions that may result from beyond design basis events, with a particular emphasis

on strategies related to the spent fuel pool, as required by NRC Security Order

Section B.5.b issued February 25, 2002, as committed to in severe accident

management guidelines, and as required by 10 CFR 50.54(hh); (2) an assessment of

the licensees capability to mitigate station blackout conditions, as required by

10 CFR 50.63 and station design bases; (3) an assessment of the licensees capability

to mitigate internal and external flooding events, as required by station design bases;

and (4) an assessment of the thoroughness of the walkdowns and inspections of

important equipment needed to mitigate fire and flood events, which were performed by

the licensee to identify any potential loss of function of this equipment during seismic

events possible for the site.

b. Findings and Observations

NRC Inspection Report 05000482/2011008 (ML11133A354) documented detailed results

of this inspection activity. Following issuance of the report, the inspectors conducted

additional follow-up on the following seven selected issues.

1. Extensive damage mitigation guideline procedures specify that if the control room

staff and field operators are compromised, then the shift security commander

becomes the incident coordinator until an operator can be found. The inspectors

identified that shift security commanders are not trained on reactor technology

and mitigating systems, therefore it is not reasonable to assume they would have

a sufficient knowledge base or decision making ability to direct technical

response to an extensive damage situation. The licensee entered the issue into

their corrective action program and is in the process of conducting additional

procedural and technical training for security commanders.

The inspectors reviewed licensee extensive damage mitigation guidelines in

greater detail and compared them to the requirements of 10 CFR 50.54(hh)(2) as

well as to the expectations outlined in the NRC Staff Guidance for Use in

Achieving Satisfactory Compliance with February 25, 2002, Order Section B.5.b

dated February 25, 2005, and determined that Wolf Creeks procedures meet

agency expectations in that they direct security commanders to seek out persons

with the best technical expertise available. This issue of concern is closed with

no finding.

2. The licensee identified that extensive damage mitigation guidelines procedures

to refill the refueling water storage tank are not viable because the connection

point is not readily accessible. The licensee entered this issue into their

corrective action program and is evaluating potential design changes to resolve

this concern.

The inspectors reviewed the applicable extensive damage mitigation attachments

which direct refilling of the refueling water storage tank in greater detail and

compared them to the requirements of 10 CFR 50.54(hh)(2) as well as to the

expectations outlined in the NRC Staff Guidance for Use in Achieving

Satisfactory Compliance with February 25, 2002, Order Section B.5.b, dated

- 61 - Enclosure

February 25, 2005, and determined that these procedures do not meet regulatory

requirements for compliance with Order 10 CFR 50.54(hh)(2) because the

expectation element could not be effectively implemented using existing or

readily available resources and because personnel safety concerns associated

with the expectation element had not been addressed. There is no guidance as

to how the connection is to be accessed, nor is the required equipment needed

access and work safely at heights pre-staged in advance. This issue of concern

is documented as a licensee identified violation in Section 4OA7.1 of this report.

3. The licensee identified that extensive damage mitigation guideline procedures

require additional precautionary guidance to prevent excessive reactor coolant

system depressurization which could compromise natural circulation core

cooling. The licensee entered this issue into their corrective action program and

is evaluating procedural enhancements to remedy this concern.

The inspectors reviewed the applicable licensee extensive damage mitigation

attachments which direct actions which can cool and depressurize the reactor

coolant system and determined that this issue of concern was an enhancement

only and not a violation of regulatory requirements. Since operators reviewing

these procedures identified the same concerns and because the licensee has

entered this issue in their corrective action program this issue of concern is

closed with no finding.

4. The licensee identified that alternate power sources specified by extensive

damage mitigation guidelines procedures are not properly staged in advance.

Additional technical guidance on the configuration and use of these sources

needs to be added to the extensive damage mitigation guidelines procedures.

The licensee entered this issue into their corrective action program and is

evaluating alternative equipment and procedural enhancements to resolve this

concern.

The inspectors reviewed the applicable licensee extensive damage mitigation

attachments which direct the use of alternate dc sources in greater detail and

compared them to the requirements of 10 CFR 50.54(hh)(2) as well as to the

expectations outlined in the NRC Staff Guidance for Use in Achieving

Satisfactory Compliance with February 25, 2002, Order Section B.5.b dated

February 25, 2005, and determined that these procedures do not meet regulatory

requirements for compliance with 10 CFR 50.54(hh)(2) because the expectation

element could not be effectively implemented using existing or readily available

resources. Specifically, the components are not pre-staged in advance. This

issue of concern is documented as a licensee identified violation in

Section 4OA7.1 of this report.

5. During walkdowns with the inspector, nuclear station operators failed to promptly

locate certain station blackout emergency operating procedure components in

the plant. The inspectors determined that this was due to inadequate training,

lack of specific procedural guidance, and over-reliance on a computer database

of equipment locations. The computer database would be unavailable during an

- 62 - Enclosure

actual station blackout. The licensee agreed with this characterization and

entered this issue into their corrective action program.

6. The inspectors determined that this issue of concern was a performance

deficiency and a violation of Technical Specification 5.4.1.a which requires, in

part, that specified station procedures be established, implemented, and

maintained. The inspectors determined that all of the components operators

failed to identify for local actions were backed up by components which would fail

safe in a loss of ac power event and therefore did not have the potential to further

complicate that event. The inspectors evaluated the issue using Inspection

Manual Chapter 0612, Appendix B, Issue Screening, and determined the failure

to comply with Technical Specification 5.4.1.a constituted a violation of minor

significance that is not subject to enforcement action in accordance with the

NRCs Enforcement Policy. The inspectors also found that Wolf Creek had

completed appropriate corrective actions in this area. This issue of concern is

closed as an NRC identified minor violation.

7. The licensee identified that some fire protection equipment is not stored in

seismic or tornado qualified locations. The licensee identified that the water

supply pumps and piping used for fire protection and extensive damage

mitigation guideline actions is not seismic or tornado qualified. The licensee also

identified that equipment used to access underground diesel storage tanks is not

seismic or tornado qualified; also the tanker truck used to refill the diesel-driven

fire pump and fire truck is not parked in a seismic or tornado qualified building.

The licensee entered these issues into their corrective action program.

8. The inspectors reviewed the requirements of 10 CFR 50.54(hh)(2) as well as to

the expectations outlined in the NRC Staff Guidance for Use in Achieving

Satisfactory Compliance with February 25, 2002, Order Section B.5.b, dated

February 25, 2005, and determined that those regulatory requirements apply only

to fire and explosion events, not to earthquakes and tornadoes. Because Wolf

Creek identified this issue and entered into their corrective action program and

because this issue of concern has no associated violation of regulatory

requirements, it does not meet the criteria of a finding under the Inspection

Manual Chapter 0612. This issue of concern is closed with no finding.

9. The condensate storage tank used in station blackout response and extensive

damage mitigation guideline procedures is not seismic or tornado qualified. The

licensee entered the issue into their corrective action program. The inspectors

found that the safety-related source, from the essential service water system,

would not be impacted. The inspectors reviewed applicable sections of Wolf

Creeks USAR and determined that this issue is within the boundaries of Wolf

Creeks NRC-approved design bases. This issue of concern is closed with no

finding.

- 63 - Enclosure

.3 (Closed) NRC TI 2515/184, Availability and Readiness Inspection of Severe Accident

Management Guidelines (SAMGs)

The inspectors reviewed the licensees severe accident management guidelines

(SAMGs), implemented as a voluntary industry initiative in the 1990s, to determine

(1) whether the SAMGs were available and updated, (2) whether the licensee had

procedures and processes in place to control and update its SAMGs, (3) the nature and

extent of the licensees training of personnel on the use of SAMGs, and (4) licensee

personnels familiarity with SAMG implementation.

The results of this review were provided to the NRC task force chartered by the

Executive Director for Operations to conduct a near-term evaluation of the need for

agency actions following the Fukushima Daiichi fuel damage event in Japan. Plant-

specific results for Wolf Creek were provided as Enclosure 14 to a memorandum to the

Chief, Reactor Inspection Branch, Division of Inspection and Regional Support, dated

May 27, 2011 (ML111470264).

.4 (Closed) TI 2515/172, Reactor Coolant System Dissimilar Metal Butt Welds

a. Inspection Scope

Portions of TI 2515/172 were previously performed at Wolf Creek Nuclear Generating

Station, during Refueling Outages 15, 16, and 17. The results of those inspections are

documented in NRC Inspection Reports 05000482/2006005, 05000482/2008003,

05000482/2009005 and 05000482/2011003, respectively. Specific documents reviewed

during this inspection are listed in the attachment. This unit has the following dissimilar

metal butt welds:

COMPONENT ID DESCRIPTION MRP-139 BASELINE EXAM

CATEGORY

RV-301-121-A Loop 1 Outlet D April 2005 RF14

Nozzle to Safe-

End Weld

RV-301-121-B Loop 2 Outlet D April 2005 RF14

Nozzle to Safe-

End Weld

RV-301-121-C Loop 3 Outlet D April 2005 RF14

Nozzle to Safe-

End Weld

RV-301-121-D Loop 4 Outlet D April 2005 RF14

Nozzle to Safe-

End Weld

- 64 - Enclosure

COMPONENT ID DESCRIPTION MRP-139 BASELINE EXAM

CATEGORY

RV-302-121-A Loop 1 Inlet E April 2005 RF14

Nozzle to Safe-

End Weld

RV-302-121-B Loop 2 Inlet E April 2005 RF14

Nozzle to Safe-

End Weld

RV-302-121-C Loop 3 Inlet E April 2005 RF14

Nozzle to Safe-

End Weld

RV-302-121-D Loop 4 Inlet E April 2005 RF14

Nozzle to Safe-

End Weld

TBB03-1-W Pressurizer F October 2006 RF15

/MW7090-WOL-DM Surge Nozzle to

Safe-End Weld

TBB03-2-W Pressurizer B October 2006 RF15

/MW7089-WOL-DM Spray Nozzle to

Safe-End Weld

TBB03-3-A-W Pressurizer B October 2006 RF15

/MW7086-WOL-DM Safety Nozzle A

to Safe-End

Weld

TBB03-3-B-W Pressurizer B October 2006 RF15

/MW7087-WOL-DM Safety Nozzle B

to Safe-End

Weld

TBB03-3-C-W Pressurizer F October 2006 RF15

/MW7088-WOL-DM Safety Nozzle C

to Safe-End

Weld

TBB03-4-W Pressurizer F October 2006 RF15

/MW7085-WOL-DM Relief Nozzle to

- 65 - Enclosure

COMPONENT ID DESCRIPTION MRP-139 BASELINE EXAM

CATEGORY

Safe-End Weld

1. Licensees Implementation of the Materials Reliability Program (MRP-139) Baseline

Inspections (03.01)

The inspectors reviewed records of structural weld overlays and nondestructive

examination activities associated with the licensees pressurizer and hot leg

structural weld overlay mitigation effort. The baseline inspections of the pressurizer

dissimilar metal butt welds were completed as noted in the table above. The

pressurizer dissimilar metal butt welds had full structural weld overlay applied in

Refueling Outage 15. The first Component ID in the preceding table was the

designation prior to the overlay; the latter Component ID is the current weld

designation (after overlay).

The licensee requested the deviations from the MRP-139 baseline inspection

requirements. These locations are now examined in accordance with the approved

alternative of relief request I3R-05. The licensee did not take any other deviations

from the baseline inspection requirements of MRP-139, and all other applicable

dissimilar metal butt welds were scheduled in accordance with MRP-139 guidelines.

2. Volumetric Examinations (03.02)

The results of these inspections are documented in NRC Inspection

Reports 05000482/2006005, 05000482/2008003, and 05000482/2009005.

3. Weld Overlays (03.03)

Only the pressurizer nozzles have been mitigated. The mitigation type was full

structural weld overlay applied in Refueling Outage 15. A pre-service exam in

accordance with relief request I3R-05 was performed. An inservice exam on the

MRP-139, category F welds was performed in Refueling Outage 16 in accordance

with I3R-05. This examination also falls within the guidelines of MRP-139 for

category F welds.

4. Mechanical Stress Improvement (03.04)

The licensee did not employ a mechanical stress improvement process.

5. Inservice Inspection Program (03.05)

The licensee has prepared an MRP-139 inservice inspection program. All the welds

in the MRP-139 inservice inspection program are appropriately categorized in

accordance with MRP-139. The inservice inspection frequencies are consistent with

the inservice inspection frequencies called for by MRP-139.

- 66 - Enclosure

b. Findings

No findings were identified.

4OA6 Meetings

Exit Meeting Summary

On April 1, 2011, the inspectors presented the inservice inspection results to Mr. S. Hedges, Site

Vice President, and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors telephonically re-exited with Mr. Hedges, Site Vice President, and

other members of the licensees staff on June 16, 2011. The inspectors acknowledged review

of proprietary material during the inspection which was returned to the licensee.

On April 5, 2011, the Deputy Director of the Division of Reactor Projects conducted a regulatory

performance meeting in conjunction with the public annual assessment meeting with

Mr. M. Sunseri, President and Chief Executive Officer, and other members of the licensee staff

to review the corrective actions related to the previously White performance indicators for

unplanned scrams per 7000 critical hours, unplanned scrams with complications, and safety

system functional failures.

On May 6, 2011, the inspectors presented the inspection results to Mr. M. Sunseri, President

and Chief Executive Officer, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspectors confirmed that none of the potential report

input discussed was considered proprietary.

On June 8, 2011, the inspector communicated the results of the in-office inspection of changes

to the licensees emergency plan to Mr. T. East, Superintendent, Emergency Planning, and to

Mr. W. Muilenburg, Licensing Engineer, of the licensees staff. The licensee acknowledged the

issues presented. The inspector asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

On July 13, 2011, the inspectors presented the inspection results to Mr. S. Hedges, Site Vice

President, and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspector asked the licensee whether any materials examined during the

inspection should be considered proprietary. Although proprietary information was used during

the inspection, it was returned to the licensee or destroyed.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC

Enforcement Policy for being dispositioned as noncited violations.

.1 Title 10 CFR 50.54(hh)(2)(ii) states: Each licensee shall develop and implement

guidance and strategies intended to maintain or restore core cooling,

containment, and spent fuel pool cooling capabilities under the circumstances

associated with loss of large areas of the plant due to explosions or fire, to

- 67 - Enclosure

include strategies in the following area of operations to mitigate fuel damage.

On April 13, 2011, while performing procedure reviews as part of industry-wide

self-assessments in response to the core damage events at Fukushima Daiichi,

Wolf Creek engineers identified two instances of mitigating strategy procedures

which did not contain sufficient information to accomplish those strategies

successfully. The first example was the ability to refill the refueling water storage

tank, and the second example involved flashing the diesel generator field using

alternate dc sources. These issues were documented in the licensees corrective

action program as Condition Report 37374. The inspectors evaluated these

findings under Inspection Manual Chapter 0609, Appendix L, and determined

these findings to be of very low safety significance because the findings did not

involve unrecoverable unavailability of multiple mitigating strategies such that

spent fuel pool cooling, injection to the reactor vessel, or injection to steam

generators cannot occur, or unrecoverable unavailability of on-site, self-powered,

portable pumping capability, or substantial inability to perform command and

control enhancements.

.2 Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part,

that a test program be established to assure that all testing required to

demonstrate that structures, systems and components will perform satisfactorily

in service is identified and performed in accordance with written test procedures

which incorporate the requirements and acceptance limits contained in the

applicable design documents. On May 13, 2011, Wolf Creek identified a

noncited violation of 10 CFR Part 50, Appendix B, Criterion XI, test control for

stroking residual heat removal containment sump valve 8811B prior to its as-

found diagnostic test. Wolf Creek stroked the valve for a clearance order and as

such, preconditioned the valve prior to its test. Plant computer data from this

stroke, data from the diagnostic stroke, and valve disassembly showed no

deficiencies. Using Inspection Manual Chapter 0609.04, the inspectors

determined the finding to be of very low safety significance because it was

confirmed not to result in the loss of operability or functionality. This issue is

captured in Condition Report 37244.

- 68 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

G. Beckett, Superintendent, Support Engineering

P. Bedgood, Manager, Radiation Protection

R. Evenson, Requalification Program Supervisor

J. Harris, System Engineer

S. Hedges, Site Vice President

S. Henry, Operations Manager

R. Hobby, Licensing Engineer

D. Hooper, Supervisor, Regulatory Affairs

T. Just, Senior Technician, Chemistry

J. Keim, Support Engineering Supervisor

S. Koenig, Manager, Corrective Actions

M. McMullen, Technician, Engineering

C. Medency, Supervisor, Radiation Protection

W. Muilenburg, Licensing Engineer

R. Murray, Simulator Supervisor

B. Norton, Manager, Integrated Plant Scheduling

J. Pankaskie, Engineering Supervisor

G. Pendergrass, Director of Engineering

L. Rockers, Licensing Engineer

G. Sen, Regulatory Affairs Manager

R. Smith, Plant Manager

M. Sunseri, President and Chief Executive Officer

J. Truelove, Supervisor, Chemistry

J. Weeks, System Engineer

M. Westman, Training Manager

NRC Personnel

D. Loveless, Senior Reactor Analyst

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000482/2011003-07 VIO Failure to Correct Procedure for Opening Main Steam Isolation

Valves (EA-11-149) (Section 4OA3.1)

A-1 Attachment

Opened and Closed

05000485/2011003-01 NCV No Procedure for Debris in Transformed and Tank Yards Prior to

Severe Weather (Section 1R01)05000482/2011003-02 NCV Failure to Properly Establish Clearance Order Boundary Isolation

Resulting in Loss of Component Cooling Water Inventory

(Section 1R04)05000482/2011003-03 NCV Failure to Assure Fillet Weld Met Size Requirements on Train B

Charging Header Vent Line (Section 1R08.1)05000482/2011003-04 NCV Failure to Assure Separation of Stainless Steel and Carbon Steel

Grinding and Cutting Equipment (Section 1R08.1)05000482/2011003-05 NCV Failure to Assure Configuration Control of Safety-Related

Systems (Section 1R08.3)05000482/2011003-06 FIN Inadequate Acceptance Criteria for Postmaintenance Testing of

the Startup Feedwater Pump (Section 1R19)05000482/2011003-08 NCV Failure to Maintain Reactor Coolant System Pressure Below

Relief Valve Setpoint (Section 4OA3.2)05000482/2011003-09 NCV Inadequate Fire Watch Defeats Halon Fire Suppression in Vital

Switchgear Rooms During Fire (Section 4OA3.3)05000482/2011003-10 NCV Failure to Analyze for Vortexing in Containment Spray Additive

Tank (Section 4OA5.1)

05000482-2515/177 TI Managing Gas Accumulation in Emergency Core Cooling, Decay

Heat Removal, and Containment Spray Systems (NRC Generic

Letter 2008-01) (Section 4OA5.1)

Closed

05000482/2006-003-00 LER Indications Discovered on Pressurizer during Preplanned In-

service Inspections (Section 4OA3.4)05000482/2010006-05 VIO Notice Of Violation EA-10-160, Failure to correct NRC identified

NCV. Apparent Cause Evaluation vice Root Cause Evaluation for

Essential Service Water (Section 4OA3.5)

A-2 Attachment

05000482-2515/183 TI Followup to the Fukushima Daiichi Nuclear Station Fuel Damage

Event (Section 4OA5.2)

05000482-2515/184 TI NRC Temporary Instruction 2515/184, Availability and Readiness

Inspection of Severe Accident Management Guidelines (SAMGs)

(Section 4OA5.3)

05000482/2515/172 TI Temporary Instruction 2515/172, Reactor Coolant System

Dissimilar Metal Butt Welds (Section 4OA5.4)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

PROCEDURES

NUMBER TITLE REVISION

OFN AF-025 Unit Limitations 32

Ai 14-008 Severe Weather 9A

AP 21C-001 Wolf Creek Substation 11A

OP1450001 Outage Risk Management 000

APF 22B-001-05 Shutdown Risk Assessment 0

APF 22B-001-10 Shutdown Safety function Status and Assessment Summary 1

CONDITION REPORTS

00040573 00040351

WORK ORDERS

11-344384-000

A-3 Attachment

Section 1R04: Equipment Alignment

PROCEDURES

NUMBER TITLE REVISION /

DATE

CKL EN-120 Containment Spray System Lineup 15A

AP 21E-001 Clearance Orders 27

SYS EN-400 Containment Spray System Fill and Vent 11

STN EN-003A Containment Spray Train A Void Monitoring and Venting 3

STN EN-003B Containment Spray Train B Void Monitoring and Venting 3

CKL HB-122 Liquid Waste Evaporator Normal Lineup 15

D-HB-N-029 Clearance Order Liquid Radwaste System March 30,

2011

Standing Order 1 Valve Setup and Operation 43

M-12HB01 Piping and Instrumentation Diagram Liquid Radwaste 19

System

CONDITION REPORTS

13599 25918 28343 28771 32378

33060 33063 33064 34505

WORK ORDERS

93-100775-001 94-100830-001 03-257175-003

DRAWINGS

NUMBER TITLE REVISION

M-13EN03 Piping Orthographic Containment Spray System Reactor 3

Building A & B Trains

M-13EN05 Piping Orthographic Containment Spray System Reactor 2

Building A & B Trains

A-4 Attachment

M-12EN01 Piping and Instrumentation Diagram Containment Spray 12

System

M-13EN01 Piping Isometric Containment Spray System Auxiliary 7

Building A Train

M-13EN01 Piping Isometric Containment Spray System Auxiliary 7

Building B Train

M-13EN06 Small Piping Isometric Containment Spray System Auxiliary 0

Building

Section 1R05: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

E-1F9905 Fire Hazard Analysis 0

AP 10-106 Fire Preplans 7

FPPM-001 Auxiliary Bldg El. 1974 2

DRAWINGS

NUMBER TITLE REVISION

M-663-00017 Penetration Typical Details, Attachment B W21

AP 10-106 Fire Preplans 7

FPPM-001 Auxiliary Bldg El. 1974 2

A-5 Attachment

CONDITION REPORTS

15073

Section 1R08: Inservice Inspection Activities

PROCEDURES

NUMBER TITLE REVISION

AI 16F-001 Evaluation Of Boric Acid Leakage 5A

AI 16F-002 Boric Acid Leakage Management 7

AI 28A-010 Screening Condition Reports 8A

AP 16F-001 Boric Acid Corrosion Control Program 5A/6A

AP 28-100 Condition Reports 13

AP 29A-003 Steam Generator Management 14

APF 28D-001 Self-Assessment Process 12

I-ENG-023 Steam Generator Data Analysis Guidelines 11

MRS 2.4.2 GEN-35 Eddy Current Inspection of Preservice and Inservice 14

Heat Exchanger Tubing

PDI-ISI-254-SE-NB Remote Inservice Examination of Reactor Vessel 1

Nozzle to Safe End, Nozzle to Pipe, and Safe End

to Pipe Welds Using the Nozzle Scanner

Generic Procedure for the Ultrasonic Testing of E

PDI-UT-2

Austenitic Pipe Welds

Generic Procedure for Ultrasonic Through Wall D

PDI-UT-3

Sizing in Pipe Welds

Generic Procedure for the Ultrasonic Testing of F

PDI-UT-6

Reactor Pressure Vessel Welds

Generic Procedure for the Ultrasonic Examination of F

PDI-UT-8

Weld Overlaid Similar and Dissimilar Metal Welds

QCP-20-501 PT (Penetrant Testing) 8

A-6 Attachment

QCP-20-502 Magnetic Particle Examination AC/DC Yoke and AC 8B

Coil Techniques

QCP-20-503 UT Thickness-Wall Thin 3

QCP-20-504 UT For Flaw Detection 5

QCP-20-508 Radiographic Examination of Welds 4A

QCP-20-510 UT Instrument Linearity 3

QCP-20-511 RT of AWS Groove Welds 1B

QCP-20-514 ET Testing 5B

QCP-20-516 PT/NON-STD Temp 05

QCP-20-517 RT Wall Thinning 2A

QCP-20-520 Pressure Test Examination 8B

QCP-20-521 UT Profile and Plotting 1B

QCP-20-522 UT Ferritic Pipe Welds 1B

QCP-20-523 UT Austenitic Pipe Welds 1B

QCP-20-527 UT- Soldering 1

QCP-20-540 VT-1 Visual Exam 0C

QCP-20-541 VT-3 Visual Exam 2A

QCP-20-543 Fluorescent Dye PT Exam 1

QCP-20-600 Visual Examination Of ASME Welds 9A

SG-CDME-10-8 Wolf Creek Steam Generator Secondary Side 0

Condition Monitoring Assessment and Operational

Assessment For Fuel Cycle and Refueling

Outage 18, February 2011

Wolf Creek, RF18 Condition Monitoring Assessment 2

SG-SGMP-09-23

and Operational Assessment, November 2009

Wolf Creek, RF18 Steam Generator Degradation 1

SG-SGMP-10-30

Assessment, March 2011

A-7 Attachment

Foreign Object Search and Retrieval and 11

STN PE-370

Secondary Side Inspections

STN PE-040D RCS Pressure Boundary Integrity Walkdown 3

STS PE-022 Steam Generator Tube Inspection 18

STS PE-040E RPV HEAD VISUAL INSPECTION 2

Ultrasonic Examination of Vessel Welds and 28

UT-2

Adjacent Base Metal

UT-95 Ultrasonic Examination of Austenitic Piping Welds 3

WCRE-24 WESDYNE Year 2011 Reactor Vessel Nozzle Safe- 0

end Examinations Program Plan

WCAL-002 Pulser/Receiver Linearity Procedure 10

WDI-CAL-102 Calibration Procedure for PCI Eddy Current Card 1

Installation and Removal of the WESDYNE Nozzle 5

WDI-EQPT-1021

Scanner (SQUID)

WDI-EQPT-1022 Reactor Vessel Nozzle Scanner Setup and 4

Checkout

WDI-STD-146 ET Examination of Reactor Vessel Pipe Welds 11

Inside Surface

CONDITION REPORTS

21975 28474 21976 28601 22027 28771

22128 28847 22280 28848 22391 28959

23173 28967 23251 28978 23455 29128

23459 29197 23867 29237 24020 29612

24077 29801 24230 30023 24336 30067

24339 30210 24469 30899 24658 31003

24659 31366 24661 31742 24662 31763

24663 31765 24665 31766 24676 31779

24681 31799 24857 31808 24893 31865

25095 32035 25173 32115 25196 32117

25224 32203 25228 32204 25268 32298

25361 32559 25377 32412 25394 32646

25495 32648 25643 32842 25871 33225

26354 33355 26358 33575 27193 33581

A-8 Attachment

27472 33600 27650 33603 27892 33684

28050 33686 28144 33688 28258 33690

28322 33689 28386 35793 28403

WORK ORDERS

08-310289 10-326485 10-324683 10-326486 10-325740

10-324621 09-320607 10-325747 10-325738 10-326483

10-325742

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

2010 3rd Quarter Outside Containment BACCP

Monitoring Walk-down

Boric Acid Leakage Screening/Evaluation for Normal Train May 5, 2010

B Charging Pump (PBG04)

Boric Acid Leakage Screening/Evaluation for Reactor March 5, 2010

Coolant Pump A (PBB01A)

Boric Acid Leakage Screening/Evaluation for Accumulator October 19,

Tank C Discharge Check Valve (EP8956C) 2009

Boric Acid Leakage Screening/Evaluation for RHR HX October 20,

A/CVCS To SI Pump A Upstream Isolation (EMHV8924) 2009

Boric Acid Leakage Screening/Evaluation for SI Pump B July 8, 2010

Suction Check Valve (EM8926B)

Boric Acid Leakage Screening/Evaluation for SI Pump A September 8,

Suction Check Valve (EM8926A) 2010

Boric Acid Leakage Screening/Evaluation for RCS Loop 3 November 20,

Steam Generator Primary Side Downstream Drain 2009

(BBV0476)

Boric Acid Leakage Screening/Evaluation for RCS Loop 1 March 5, 2010

Steam Generator Primary Side Downstream Drain

(BBV0474)

A-9 Attachment

Change Package # 012869, Installation of Vent Valves in 3

the Chemical and Volume Control System (BG), the

Residual Heat Removal (EJ), and the High-Pressure

Coolant Injection System (EM)

Technical Report No. 11-2039-TR-001, Failure Analysis of March 2011

Socket Weld on a Vent Valve Assembly from the CVCS

S/G Eddy Current Calibrated Equipment List October 16,

2009

Steam Generator data Analysis Desktop Instruction 4

RF 18 Steam Generator data Analysis Desktop Instruction 0

SGAMP Self Assessment, Steam Generator Asset October 17,

Management Program 2008

Wolf Creek RF 17 Fall 2009 Steam Generator Secondary August 17,

Side Visual Inspection Recommendations 2009

Wolf Creek RF17 Condition Monitoring Assessment and November

Operational Assessment 2009

APF 28D-001-02 Self Assessment Report SEL 04-038 , Steam Generator 4

Program

APF 29A-003-001 Secondary Chemistry Wet Layup Initial Monitoring 2

Frequency

ET 09-0016 Revision to Technical Specifications 5.5.9, "Steam June 2, 2009

Generator (SG) Program," and TS 5.6.10, "Steam

Generator Tube Inspection Report, for a Permanent

Alternate Repair Criterion

ET-09-0025 Docket No. 50-482: Revision to Technical Specification September 15,

(TS) 5.5.9, "Steam Generator (SG) Program," and 2009

TS 5.6.10, "Steam Generator Tube Inspection Report"

ET-10-0030 Revision to Technical Specifications 5.5.9, Steam November 30,

Generator (SG) Program, and TS (Technical 2010

Specifications) 5.6.10, Steam Generator Tube Inspection

Report, for a Temporary Alternate Repair Criterion

A-10 Attachment

I3R-01 Wolf Creek Generating Station - Third 10-Year Interval February 21,

Inservice Inspection Program Relief Request I3R-01 (TAC 2007

NO. MD0297)

I3R-05 Wolf Creek Generating Station - Authorization Of Relief July 19, 2007

Request I3R-05, Alternatives To Structural Weld Overlay

Requirements (TAC NO. MD1813)

13R-06 Wolf Creek Generating Station -Relief Request 13R-06, July 23, 2009

Alternative To The Examination Requirements Of ASME

Code,Section XI For Class 1 Piping Welds Examined

From The Inside Of The Reactor Vessel (TAC

NO. MD9658)

Docket 10 CFR 50.55a Request 13R-06, Alternative to the September 16,

No. 50-482 Examination Requirements of ASME Section XI for 2008

Class 1 Piping Welds Examined from the Inside of the

Reactor Vessel

Docket Wolf Creek Nuclear Operating Corporation's Response to April 23 , 2009

No. 50-482 Request for Additional Information Regarding

10 CFR 50.55a Request 13R-06

ET 05-0014 10 CFR 50.55a Request Number 13R-03 for the Third September 28

Ten-Year Interval lnservice lnspection (ISI) Program - 2005

Request for Relief to Allow Use of Alternate Requirements

for Snubber lnspection and Testing

ET 06-0042 Wolf Creek Nuclear Operating Corporation's Response to September 27,

the September 20, 2006 NRC Request for Additional 2006

Information Regarding 10 CFR 50.55a Request 13R-05

ET 06-0044 Wolf Creek Nuclear Operating Corporations Revised October 2,

Commitment Regarding 10 CFR 50.55a Request 13R-05 2006

ET 06-001 0 Inservice Inspection Program Plan for the Third Ten-Year March 2, 2006

Interval and 10 CFR 50.55a Requests 13R-01, 13R-02,

and 13R-04

ET 06-0021 10 CFR 50.55a Request 13R-05, Installation and May 19, 2006

Examination of Full Structural Weld Overlays for

Repairing/Mitigating Pressurizer Nozzle-to-Safe End

Dissimilar Metal Welds and Adjacent Safe End-to-Piping

Stainless Steel Welds

A-11 Attachment

ET 06-0031 Wolf Creek Nuclear Operating Corporation's Response to August 4,2006

Request for Additional Information Regarding I 0 CFR

50.55a Request l3R-05 and Submittal of Revision 1 to 10

CFR 50.55a Request 13R-05

ET 06-0043 Wolf Creek Nuclear Operating Corporation's Response to October 5,200

NRC Request for Additional Information Regarding 10 6

CFR 50.55a Request 13R-01

ET 06-0058 Wolf Creek Nuclear Operating Corporation's Response to December 20,

the Second NRC Request for Additional Information 2006

Regarding 10 CFR 50.55a Request 13R-01

MRS-TRC-2087 Use of Appendix H and I Qualified Techniques at Wolf 0

Creek RF18 April 2011 S/G Inspection

SAP-+PT-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-+PTUB-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-01-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-02-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-03-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-04-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-05-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-06-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-07-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-08-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-09-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

A-12 Attachment

SAP-10-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-11-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-12-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-BOB-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-DELTA-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SAP-GHENT-09 Steam Generator Eddy Current Inspection Multi- 0

Frequency Eddy Current Parameters

SEL 04-038 Steam Generator Program 4

SG-CDME-08-15 Wolf Creek RF16 Condition Monitoring Assessment and 1

Operational Assessment, April 2008

SG-CDME-09-1 Wolf Creek Steam Generator Secondary Side Condition 0

Monitoring and Operational Assessment for Fuel Cycle

and Refueling Outage 17

SG-SGMP-09-9 Steam Generator Degradation Assessment for Wolf 0

Creek, RF17 Refueling Outage, October 2009

SEL 09-151 EPRI-WRTC/Utility Welding Program Best Practices

Visual Examination for Leakage of PWR Reactor Head 2

Penetrations

WCRE-15 Program Plan For Management Of Alloy 600 Components 3

And Alloy 82/182 Welds

Section 1R11: Licensed Operator Requalification Program

NUMBER TITLE REVISION

LR5002026 Inadvertent Safety Injection Lab 3

A-13 Attachment

Section 1R12: Maintenance Effectiveness

MISCELLANEOUS

NUMBER TITLE

GK-01 Final Scope Evaluation, System GK, Control Building HVAC

System

CONDITION REPORTS

00035992 00027105 00026250 00028792 00027228

00026251 00034299 00026250

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

MISCELLANEOUS

NUMBER TITLE REVISION

EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to 3

Criteria and Goals

MPE GK-003 Control Room and Class 1E A/C Units Preventive 3

Maintenance Activity

EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to 3

Criteria and Goals

WORK ORDERS

10-330270-000 10-330269-000 10-330270-000 10-330269-000

Section 1R15: Operability Evaluations

NUMBER TITLE REVISION

ALR 501 Standby Diesel Engine System Control Panel KJ-121 13, 14 and 14A

A-14 Attachment

AP 26C-004 Operability Determination and Functionality Assessment 23

OE KJ-10-001 Emergency Diesel Generators KKJ01A and KKJ01B 0

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to 3

Criteria and Goals

Final Scope Evaluation, System GK, Control Building HVAC

System

MPE GK-003 Control Room and Class 1E A/C Units Preventive 3

Maintenance Activity

EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to 3

Criteria and Goals

GK Final Scope Evaluation - Control Building HVAC System

LER 22011-003-00, Diesel Generator Declared Inoperable May 12, 2011

Due to Inadequate Reinstallation of Pipe connection

Resulting in Excessive Governor Oil Coolant Leak

A-EDG Governor Heat Exchanger Water Leak

9.5-16 USAR 19

2011-1027-0 Training Needs Analysis

Operations Requalification Cycle 11-01 Week 0 to Week 6

Schedule

OP1336001 Plant Changes 0

A-15 Attachment

M-018-00110-W13 Electrical Schematic Engine Guide Panel KJ121

E-13KJ02 Schematic Diagram Diesel Generator KKJ01A Annunciator 7

and Miscellaneous Circuits

M-12EF01 Piping & Instrumentation Diagram Essential Service Water 57

System

M-12EF02 Piping & Instrumentation Diagram Essential Service Water 26

System

M-K2EF03 Piping & Instrumentation Diagram Essential Service Water 10

System

M-13EF07(Q) Piping Isometric Essential Service WTR.Sys.Control Bldg 1

Cooler(A&B) Train Supply & Return

M-13EF08 Piping Isometric Essential Service Wtr,-Diesel Generator 01

Bldg.

CONDITION REPORTS

00034661 00038229

REPORTABILITY EVALUATION REPORT

2011-037

Section 1R18: Plant Modifications

NUMBER TITLE REVISION

10-017-EG Temporary Cooling of CCW Radwaste Loads 0

CONDITION REPORTS

00035262

A-16 Attachment

Section 1R19: Postmaintenance Testing

PROCEDURES

NUMBER TITLE REVISION

SYS EG-205 CCW Flow Adjustment to Reactor Coolant Pumps, Seal 9

Water Heat Exchanger, and Excess Letdown Heat

Exchanger

STS AE-209 Main Feed Reg Valve Bypass Valve Inservice Valve Test 2

STN AE-001 Startup Main Feedwater Pump Operational Test 0A

STN AC-007 Turbine Overspeed Trip Set 26

AP 16E-002 Post Maintenance Testing Development 9C

WORK ORDERS

37698 38443 29128 34806 39145

34434 34500 36164

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

Control Room Turnover Checklist-Day Shift March 16,

2011

APF 30E-004-01 Main Feedwater System 2

BD-EMG FR-h1 Response to Loss of Secondary Heat Sink 10

FWIS and Reactor Trip on Low S/G LevelCR 29128 Root

Cause Evaluation

A-17 Attachment

E-0099 Cable Sheath Grounding and Termination Data 7

KD-7496 One Line Diagram 40

CONDITION REPORTS

0037698 00025817 00038443

WORK ORDERS

11-337610-000 11-337610-001 11-337610-002 11-337610-003 11-337610-004

11-337610-005 11-337610-006 11-337610-007 09-322525-000 10-335457-001

11-337610-004 11-337610-005 11-337610-006 11-337610-007 11-337610-000

11-337610-001 11-337610-002 11-337610-003

Section 1R20: Refueling and Other Outage Activities

PROCEDURES

NUMBER TITLE REVISION

FHP 02-007A Reactor Vessel Closure head Removal 10

SYS BB-215 RCS Drain Down with Fuel in Reactor 28

STS IC-439 Channel Calibration NIS Post Accident Monitoring N60 3A

GEN 00-002 Cold Shutdown to Hot Standby 73

STN EJ-002 Containment Inspection 17

DRAWINGS

NUMBER TITLE REVISION

C-OL2901(Q) Reactor Building Line Plate Floor Details, SHT-1 7

A-18 Attachment

C-OS2919(Q) Reactor Building Incore Instrumentation Tube Supports and 8

Platforms

C-OL2914(Q) Reactor Building Liner Place Floor Details-Sheet-3 4

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

11-2039-L-001 ALTRAN SOLUTIONS April 13, 2011

Refuel 18, No. 15 The Daily Howl April 2, 2011

Refuel 18, No. 17 The Daily Howl April 4, 2011

Information Failure of Motor Operated Value Actuator Motors with December 8,

Notice 2008-20 Magnesium Allow Rotors 2008

MS-02 Piping Class Sheets 53

Evaluation of Interim Operation 0

ALARA Planning Survey

RF18 High Impact Teams/Major Projects

Letter NE 11-0009, dated February 28, 2011, from W. H.

Ketchum To R. A. Smith and R. E. Kopecky

AP 22B-001 Outage Risk Management 13

CONDITION REPORTS

00029149 00029322 00030371 00030371 00032254

00033358 00033698 00033699 00033715 00033716

00034068 00034349 00035261 00035262 00035304

00035314 00035419 00035426 00035516 00035533

A-19 Attachment

00035535 00035537 00035539 00035540 00035540

00035541 00035542 00035544 00035545 00035546

00035547 00035548 00035549 00035550 00035551

00035552 00035553 00035554 00035555 00035556

00035557 00035558 00035559 00035560 00035573

00035614 00035615 00035617 00035619 00035620

00035621 00035622 00035623 00035624 00035625

00035626 00035627 00035628 00035629 00035630

00035632 00035663 00035714 00035963 00035965

00035987 00036031 00036032 00036106 00036186

00036272 00036292 00036300 00036492 00036518

00036798 00036799 00036857 00036876 00036880

00036881 00036957 00036966 00036988 00037110

00037289 00037615 00037909 00038083 00038086

00038113 00038333 00038517 00038680 00039099

00039283 2007-000299 00035429 00039721

REPORTABILITY EVALUATION REQUESTS

2011-047 2011-102 2011-103 2011-113 00037048

2011-059 2011-057 2011-046 2011-056

WORK ORDERS

10-324324-000 10-328967-001 10-324322-000 10-339212-003

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION

STS BG-002A Train A ECCS System Vent for Mode 4 10

STS BG-007A ECCS Valve Check and Train A and Common Void 5

Monitoring and Venting

A-20 Attachment

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION

STS BG-007B ECCS Train B Void Monitoring and Venting 5

SYS EM-410 Fill and Vent of Safety Injection System After Maintenance 17 and 18

SYS EJ-110 RHR System Fill and Vent Including Initial RCS Fill 56, 57, 59

and 60

STS IC-211B Actuation Logic Test Train B Solid State Protection System 35

STS PE-018 Containment Integrated Leakage Rate Test 9

AP 21-004 Operator Response Time Program 2

STN TCA-001 Manual Time Critical Action Timing 3

SYS GP-519 CILRT-EN System 2

AP 29E-001 Program Plant for Containment Leakage Measurement 13

AI 21-016 Operator Time Critical Actions Validation 2

STS KJ-001B Integrated Diesel Generator and Safeguards Actuation 42A

Testing Train B

STS IC-615B Slave Relay Test K615 Train B Safety Injection 27

WORK ORDERS

10-326512-001 09-322158-001

CONDITION REPORTS

00037110 00037244 30302 33443 39083

A-21 Attachment

39081

REPORTABILITY EVALUATION REQUESTS

2011-094

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION

AN-99-025 Steam Generator Tube Rupture Overfill Analysis with 1

Revised Operator Action Times

AIF 21-016-02 Time Verification Form 0A

EJHV8811B Analysis Print

EJHV8811B Refuel XVIII Preparation Package

Section 4OA2: Identification and Resolution of Problems

PROCEDURES

NUMBER TITLE REVISION

KMS-4 Mechanical Standard 2

VENDOR DOCUMENTS

NUMBER TITLE REVISION

TB-68-2 Tensile Strength of Threaded Insert Assembly 2

CONDITION REPORTS

38321

WORK ORDERS

11-339714-000 11-337546-000

A-22 Attachment

Section 4OA3: Event Follow-Up

PROCEDURES

NUMBER TITLE REVISION

BD-EMG ES-03 SI Termination 10A

SYS AE-200 Feedwater Preheating During Plant Startup and Shutdown 29 and 30

AP 15C-002 Procedure Use and Adherence33

EMG E-0 Reactor Trip or Safety Injection 25

EMG ES-03 SI Terminations 18

SYS AB-120 Main Steam and Steam Dump Startup and Operation 27

SYS PN-200 Energizing and Deenergizing Inverters PN09 and PN10 11

ALR KC-888 Fire Protection Panel KC-008 Alarm Response 18A

AP 10-104 Breach Authorization 24A

SYS GK-200 Inoperable Class IE A/C Unit 21A

AP-10-103 Fire Protection Impairment Control 23A

AP 21D-003 Control of Information Tagging 15B

SYS BG-120 Chemical and Volume Control System 42

GEN 00-006 Hot Standby to Cold Shutdown 76

AP 21-001 Conduct of Operation 50

SY1300400 Chemical and Volume Control System - Low Pressure 13

Letdown

SY1300400 Chemical and Volume Control System - Plan/Text 25

A-23 Attachment

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

CR 34964 White Streamline Safety Injection When ABHV20 Was Opened 2

Paper

Change Package PRT Sparing Line Bypass 0

012410

Change Package CRDM Nozzle #6 Scratch Evaluation 0

013674

ES-1.1 Background Information for Westinghouse Owners Group April 30, 2005

Emergency Response Guideline

Control Room Turnover Checklist March 11, 19

and 22, 2011

Corrective Action Review Board Meeting Minutes March 23,

2011

Chapter 7.3-39 Updated Safety Analysis Report 13

Site Clock Reset Communication - Condition Report 34964 March 19,

2011

Page 14 of 17 Breach Authorization Permit Log April 22, 2011

Page 6 of 7 Fire Protection Impairment Control Log April 22, 2011

2011-118, 119, Fire Protection Impairment Control Permit

121, 122

2011-148, 149, Breach Authorization Permit

215, 237, 238

Fire Protection Significance Determination Review

04/05/2011 Halon Discharge in ESF Switchgear Room 1

Fire Incident Investigation Report April 5, 2011

FW1431401 Just-in-Time Training - Alternate Planning and/or Training 0

Record

A-24 Attachment

11-339929-001 AMETEK Solidstate Controls

16577-M-658 Technical specification for Furnishing, Installing, and Testing

Halogenated Agent Extinguishing System for the

Standardized Nuclear Unit Power Plant System (SNUPPS)

Wolf Creek Unit Only

SU4-KC02 Fire Protection System Halon Preoperational Test 0

Control Room Turnover Checklist April14, 15,

21, 2011

Boundary Watch Duties

FW1231401 Fire Watch Duties and Responsibilities 10

LR5005012 JIT Plant Shutdown From 100% RTP 3

I-11154 Operation and Maintenance Instructions Solenoid Power 1

Operated Relief Valve

59 99-0007 LTOP TS Bases - B 3.4.12 1

DRAWINGS

NUMBER TITLE REVISION

M-744-00019 SNUPPS Projects Functional Diagram Reactor Trip Signals W07

M-744-00024 SNUPPS Projects Functional Diagram Steam Generator Trip W06

Signals

M-744-00025 SNUPPS Projects Functional Diagram Safeguards Actuation W07

Signals

CONDITION REPORTS

00033745 00034963 00034964 00034964 00034967

00034968 00034969 00034970 00034975 00034987

00034995 00035000 00035001 00035012 00035017

00035246 00035249 00035251 00035319 00035333

A-25 Attachment

00035515 00035638 00035648 00035650 00035652

00036164 00036719 00037931 00038232 00038516

REPORTABILITY EVALUATION REQUEST

2011-040

Work Orders

08-310440-001 08-310449-000 08-310449-001 08-310440-000 11-339200-001

11-339027-000

Section 4OA5: Other Activities

CALCULATIONS

NUMBER TITLE REVISION

CN-SEE-III- Evaluation of Suction Side Gas Void Volumes for Wolf Creek to 0

11-6 Address GL-2008-01

EN-M-024 Critical Submergence in Containment Spray Additive Tank 0

(TEN01) to Avoid Vortex

XX-M-074 Comparison of GOTHIC Gas Transport Calculations with 0

Westinghouse Test Data for Wolf Creek Emergency Core Cooling

System

XX-M-076 Startup Pressure Pulse Analysis for WCGS ECCS Discharge 0

Piping

XX-M-079 ECCS (Emergency Core Cooling System) Horizontal Line 1

Metrology (laser measurements) Data Evaluation,

CONDITION REPORTS

00006250 00008212 00018673 00029160 00033057

00032378 00033060 00033061 00033062 00033063

A-26 Attachment

00033065 00033070 00033071 00038714 00038715

2008-000091

DRAWINGS

NUMBER TITLE REVISION

M-12BG03 Piping and Instrumentation Diagram Chemical & Volume 47

Control System

M-12BN01 Piping and Instrumentation Diagram Borated Refueling 14

Water Storage System

M-12EJ01 Piping and Instrumentation Diagram Residual Heat Removal 46

System, sheet 1

M-12EM01 Piping and Instrumentation Diagram High Pressure Coolant 37

Injection System

M-12EM02 Piping and Instrumentation Diagram High Pressure Coolant 19

Injection System

M-12EP01 Piping and Instrumentation Diagram Accumulator Safety 08

Injection System

M-12EN01 Piping and Instrumentation Containment Spray System 12

M-13EJ01 Piping Isometric Residual Heat Removal System - Auxiliary 09

Building A Train

M-13EM01 Piping Isometric High Pressure Coolant Injection System - 16

Auxiliary Building

A-27 Attachment

INSPECTION REPORTS (05000482/

2008007 2009006 2009007 2010005 2010006

2010007

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

Brooks Metrology Report

Examples of Accumulator Level Alerts

List of discharge and suction vent valves for the

Generic Letter 2008-01 systems

Technical Specifications Surveillance

Requirement 3.5.2.3 Bases

Updated Final Safety Analysis Report, Section 6.3.2.2

Updated Final Safety Analysis Report Change

Request 2008-004 to section 6.3.2.2

2008-01 Managing Gas Accumulation in Emergency Core January 11,

Cooling, Decay Heat Removal, and Containment Spray 2008

Systems

2008-0624 Technical Specifications Document Revision Request

APC 09-20 Generic Letter (GL) 2008-01, Managing Gas May 18, 2009

Accumulation in Emergency Core Cooling, Decay Heat

Removal, and Containment Spray Systems -

Evaluation of Unexpected Voids or Gas Identified in

A-28 Attachment

Plant ECCS and Other Systems

Form Engineering Screening Form 17

APF 05-002-01

Gas Voiding Improvement Plan - Project Report 1

NEI 09-10 Guidelines for Effective Prevention and Management 1

of System Gas Accumulation

Reviewed the set of laser metrology isometric drawings

Report FAI/08-70 Gas Voids Pressure Pulsations Program 1

Report FAI/11-192 Void Acceptance Criteria for Wolf Creek Discharge March /2011

Piping Based on FAI/08-70 Methodology, Revision 1

SEL 2011-196 STARS Gas Team Self-Assessment January 20,

2011

Specification M-204 Technical Specification for Field Fabrication and 46

Installation of Piping and Pipe Supports to ASME

Section III for the Wolf Creek Generating Station

Standing Order 33 Accumulator Level Alert E-mail 0

WCAP-16631-NP Testing and Evaluation of Gas Transport to the Suction 0

of ECCS Pumps - Volume 1

WCAP-17276-P Investigation of Simplified Equation for Gas Transport January 2011

WCNOC122-PR-01 Study of Vent Requirements for Cooling Water 0

Systems

A-29 Attachment

System Walk Down Reports

PROCEDURES

NUMBER NUMBER REVISION

AI 23P-001 Gas Intrusion Program 0

AP 21E-001 Clearance Orders 27

QCP-20-526 Ultrasonic Measurement for Liquid Level Measurement 1

STN IC-252A Calibration of RHR Pump A Mini Flow Valve Control Switch 7A

STN IC-252B Calibration of RHR Pump B Mini Flow Valve Control Switch 8A

STS BG-002 ECCS Valve Check and System Vent 26

STS BG-002A Train A ECCS System Vent for Mode 4 5 and 10

STS BG-002B Train B ECCS System Vent for Mode 4 4 and 10

SYS BG-120 Chemical and Volume Control System Startup 43

SYS EG-400 Component Cooling Water System Fill and Vent 20A

SYS EM-410 Fill and Vent of Safety Injection System After Maintenance 18A

SYS EJ-110 RHR System Fill and Vent Including Initial RCS Fill 60

SYS SJ-002 Void Sampling Using a Sample/Purge Rig 1

A-30 Attachment

SURVEILLANCE TESTS

TITLE TITLE DATE

STS BG-007A ECCS Valve Check and Train A and Common Void March 3, 2011

Monitoring and Venting

STS BG-007B ECCS Train B Monitoring and Venting March 18, 2011

STS EG-003A CCW Train A Monitoring and Venting March 16. 2011

STS EG-003B CCW Train A Monitoring and Venting March 16, 2011

STS EN-003A Containment Spray Train A and Common Void March 2, 2011

Monitoring and Venting

STS EN-003B Containment Spray Train B Void Monitoring and Venting March 15, 2011

Section 4OA5: Other Activities

NUMBER TITLE REVISION

EPP 06-021 Training Programs 8

SAM SAG-01 Inject into the Steam Generators 1

SAM SAG-02 Depressurize the RCS 1

SAM SAG-03 Inject into RCS 1

SAM SAG-04 Inject into Containment 1

A-31 Attachment

SAM SAG-05 Reduce Fission Product Releases 1

SAM SAG-06 Control Containment Conditions 1

SAM SAG-07 Reducing Containment Hydrogen 1

SAM SAG-08 Flood Containment 1

SAM SAEG-01 TSC Long Term Monitoring 2

SAM SAEG-02 SAMG Termination 1

SAM SACRG-02 SACRG for Transients after TSC is Functional 2

SAM SACRG-01 Severe Accident Control Room Guideline Initial Response 2

WOG Severe Accident Management Guidance 1

CONDITION REPORTS

18664 18398

A-32 Attachment