ML102560258

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IR 05000482-10-006; February 16, 2008, Through July 30, 2010: Wolf Creek Generating Station, Biennial Baseline Inspection of the Identification and Resolution of Problems
ML102560258
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 09/13/2010
From: Vegel T
NRC Region 4
To: Matthew Sunseri
Wolf Creek
References
EA-10-160 IR-10-006
Download: ML102560258 (46)


See also: IR 05000482/2010006

Text

UNIT ED STAT ES

NU C LE AR RE G UL AT O RY C O M M I S S I O N

REGION IV

6 12 EAST LAMAR BL VD , S U I T E 4 0 0

A R L I N G T O N , T E X A S 7 6 0 1 1 -41 25

September 13, 2010

EA-10-160

Matthew W. Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

SUBJECT: WOLF CREEK GENERATING STATION - NRC PROBLEM IDENTIFICATION

AND RESOLUTION INSPECTION REPORT 05000482/2010006 AND NOTICE OF

VIOLATION

Dear Mr. Sunseri:

On July 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Wolf Creek Generating Station. The enclosed report documents the inspection findings

discussed with you and members of your staff during an exit briefing on July 30, 2010.

The inspection examined activities conducted under your license as they relate to identification

and resolution of problems, safety and compliance with the Commissions rules and regulations

and with the conditions of your operating license. The inspectors reviewed selected procedures

and records, observed activities, and interviewed personnel. The inspectors also interviewed a

representative sample of personnel regarding the condition of your safety-conscious work

environment.

The NRC noted that a number of plant deficiencies were not being effectively resolved in your

corrective action program. For example, the results of metallurgical examinations performed to

assess piping corrosion and an analysis of water hammer issues affecting the essential service

water system were performed outside the corrective action process and not used to update a

currently open operability evaluation or a completed root cause evaluation. Another example

involves the failure to effectively track and prioritize for corrective actions degraded or non-

conforming conditions. The NRC noted a number of examples that involved deficiencies not

being corrected during the first available opportunity, without adequate justification for the delay.

In addition, the team identified that a large number of control room instrumentation and control

deficiencies currently exist. The NRC identified that some of these deficiencies have not been

corrected for a number of years, the deficiencies impact on plant operations were not well

understood by all plant operators, the deficiencies were not effectively being tracked in the

control room deficiency log, and control room operators were not consistently reviewing these

deficiencies during shift turnover. The NRC determined that additional actions are warranted to

ensure that these control room deficiencies are promptly addressed before they have the

potential to impact plant operations.

Wolf Creek Nuclear -2-

Operating Corporation

This report documents six noncited violations, one cited violation, and one finding, all of very low

safety significance (Green). Because of the very low safety significance of the violations and

because they were entered into your corrective action program, the NRC is treating these

violations as noncited violations consistent with Section VI.A.1 of the NRC Enforcement Policy.

If you contest these noncited violations, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the

Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd.,

Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, United States

Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector

at the Wolf Creek Generating Station.

An NRC-identified violation is cited in the enclosed Notice of Violation (Enclosure 1). The

violation involved the failure to perform an adequate cause evaluation and to take corrective

actions to preclude repetition for a significant condition adverse to quality. Although determined

to be of very low safety significance (Green), this violation is being cited in the Notice of

Violation because not all of the criteria specified in Section VI.A.1 of the NRC Enforcement

Policy were satisfied (EA-10-160). Specifically, the Wolf Creek Generating Station failed to

restore compliance within a reasonable time after a previously-identified was identified in NRC

Inspection Report 05000482/2009007-03. You are required to respond to this letter and should

follow the instructions specified in the enclosed Notice when preparing your response. The

NRC will use your response, in part, to determine whether further enforcement action is

necessary to ensure compliance with regulatory requirements.

If you disagree with the crosscutting aspect assigned to any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at the

Wolf Creek Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web-site at

www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). To the extent

possible, your response should not include any personal privacy, proprietary, or safeguards

information so that it can be made available to the Public without redaction.

Sincerely,

/RA/

Tony Vegel, Deputy Director

Division of Reactor Projects

Docket No. 50-482

License No. NPF-42

Wolf Creek Nuclear -3-

Operating Corporation

Enclosures:

1. Notice of Violation

2. NRC Inspection Report 05000482/2010006

w/Attachment: Supplemental Information

cc w/Enclosures:

Site Vice President

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Jay Silberg, Esq.

Pillsbury Winthrop Shaw Pittman LLP

2300 N Street, NW

Washington, DC 20037

Supervisor Licensing

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Chief Engineer

Utilities Division

Kansas Corporation Commission

1500 SW Arrowhead Road

Topeka, KS 66604-4027

Office of the Governor

State of Kansas

Topeka, KS 66612-1590

Attorney General

120 S.W. 10th Avenue, 2nd Floor

Topeka, KS 66612-1597

Chairman

Coffey County Courthouse

110 South 6th Street

Burlington, KS 66839

Chief, Radiation and Asbestos

Control Section

Bureau of Air and Radiation

Kansas Department of Health and

Environment

1000 SW Jackson, Suite 310

Topeka, KS 66612-1366

Wolf Creek Nuclear -4-

Operating Corporation

Chief, Technological Hazards

Branch

FEMA, Region VII

9221 Ward Parkway

Suite 300

Kansas City, MO 64114-3372

Wolf Creek Nuclear -5-

Operating Corporation

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Acting Director (Tony.Vegel@nrc.gov)

DRP Acting Deputy Director (Troy.Pruett@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Acting Deputy Director(Jeff.Clark@nrc.gov)

Senior Resident Inspector (Chris.Long@nrc.gov)

Resident Inspector(Charles.Peabody@nrc.gov)

WC Administrative Assistant (Shirley.Allen@nrc.gov)

Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Project Engineer, DRP/B (Greg.Tutak@nrc.gov)

Project Engineer, DRP/B (Nestor.Makris@nrc.gov)

Reactor Inspector, DRP/B (Christine.Denissen@nrc.gov)

R4Enforcement (Ray.Keller@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

PublicAffairsOfficer(Lara.Uselding@nrc.gov)

Project Manager (Balwant.Singal@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator(Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROPreports

OEDO RIV Coordinator (Margie.Kotzalas@nrc.gov)

Team Members on Concurrence

R:\_REACTORS\_WC\2010\2010006-RPT-GMV.docx ADAMS ML

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials gmv

Publicly Avail Yes No Sensitive Yes No Sens. Type Initials gmv

RIV:TL:DRS/TSB SRI:DRP/PBD PE:DRP/PBE PE:DRP/PBB RI:DRP/PBB

MVasquez GWarnick JMelfi GTutak CPeabody

/ RA/ /RA/ per T w/gmv /RA/ by E /RA/ by E /RA/ by E

9/1/2010 9/2/2010 9/2/2010 9/2/2010 9/2/2010

C:DRP/PBB RIV:C:DRS/TSB SES:ACES D/DRP

GMiller MHay RKellar AVegel

/RA/ /RA/ /RA/ by E /RA/

9/8/2010 9/12/10 9/9/2010 9/13/2010

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

NOTICE OF VIOLATION

Wolf Creek Nuclear Operating Company Docket No: 50-482

Wolf Creek Generating Station License No: NPF-42

EA-10-160

During an NRC inspection, conducted from July 12 through 30, 2010, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires that

in the case of significant conditions adverse to quality, measures shall assure

that the cause of the condition is determined and corrective action taken to

preclude repetition.

Contrary to the above, from December 4, 2009, to July 30, 2010, the licensee

failed to assure that the cause of a significant condition adverse to quality was

determined and corrective actions were taken to preclude repetition. Specifically,

after a loss of offsite power event on August 19, 2009, the licensee failed to

perform an adequate evaluation to determine the cause of loss of offsite power

induced water hammers and internal corrosion in the essential service water

system, and did not take corrective actions to preclude repetition of additional

water hammer events and system leaks. The licensee performed an apparent

cause evaluation when a root cause evaluation was required.

This violation is associated with a Green Significance Determination Process

finding.

Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Company is hereby

required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the

Regional Administrator, Region IV, and a copy to the NRC Resident Inspector Wolf Creek

Generating Station, within 30 days of the date of the letter transmitting this Notice of Violation

(Notice). This reply should be clearly marked as a "Reply to Notice of Violation EA-10-160," and

should include: (1) the reason for the violation, or, if contested, the basis for disputing the

violation or severity level, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken to avoid further violations, and (4) the date

when full compliance will be achieved. Your response may reference or include previous

docketed correspondence, if the correspondence adequately addresses the required response.

If an adequate reply is not received within the time specified in this Notice, an order or a

Demand for Information may be issued as to why the license should not be modified,

suspended, or revoked, or why such other action as may be proper should not be taken. Where

good cause is shown, consideration will be given to extending the response time. If you contest

this enforcement action, you should also provide a copy of your response, with the basis for

your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001.

Wolf Creek Nuclear -2-

Operating Corporation

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC website at www.nrc.gov/reading-rm/pdr.html or www.nrc.gov/reading-rm/adams.html, to

the extent possible, it should not include any personal privacy, proprietary, or safeguards

information so that it can be made available to the public without redaction. If personal privacy

or proprietary information is necessary to provide an acceptable response, then please provide

a bracketed copy of your response that identifies the information that should be protected and a

redacted copy of your response that deletes such information. If you request withholding of

such material, you must specifically identify the portions of your response that you seek to have

withheld and provide in detail the basis for your claim of withholding (e.g., explain why the

disclosure of information will create an unwarranted invasion of personal privacy or provide the

information required by 10 CFR 2.390(b) to support a request for withholding confidential

commercial or financial information).

Dated this 13th day of September 2010.

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000482

License: NPF-42

Report: 05000482/2001006

Licensee: Wolf Creek Nuclear Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane SE

Burlington, Kansas

Dates: July 12 through 30, 2010

Team Leader: M. Vasquez, Senior Reactor Inspector, Technical Support Branch, DRS

Inspectors: G. Warnick Senior Resident Inspector

C. Peabody, Resident Inspector

J. Melfi, Project Engineer

G. Tutak, Project Engineer

Approved By: Michael C. Hay, Chief

Technical Support Branch

Division of Reactor Safety

-1- Enclosure

SUMMARY OF FINDINGS

IR05000482/2010006; February 16, 2008, through July 30, 2010: Wolf Creek Generating

Station, Biennial Baseline Inspection of the Identification and Resolution of Problems

The report covers a 2-week period of onsite inspection by a senior reactor inspector, a senior

resident inspector, a resident inspector, and two project engineers. The findings from this

inspection include five Green NRC-identified noncited violations, one Green self-revealing

violation, one Green finding, and one Green cited violation. The significance of most findings

is indicated by their color (greater than Green, or Green, White, Yellow, Red), and was

determined using Inspection Manual Chapter 0609, Significance Determination Process.

The crosscutting aspect was determined using Inspection Manual Chapter 0310,

Components Within the Cross Cutting Areas. The findings for which the significance

determination process does not apply may be Green or be assigned a severity level after

NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG 1649, Reactor Oversight Process,

Revision 4, dated December 2006.

Identification and Resolution of Problems

The team concluded that the corrective action program at Wolf Creek Generating Station was

generally performing in a satisfactory manner to ensure safe plant operations. However, as

previously discussed in the past four NRC assessment letters, Wolf Creeks ability to thoroughly

evaluate and prioritize problems such that the resolutions effectively address the causes and

extent of conditions is of concern. Wolf Creek Generating Stations efforts to reverse the trend

of substantive crosscutting issues in problem identification and resolution areas have not shown

to be effective.

The team identified a number of issues that the licensees staff had previous opportunities to

identify. The team also identified instances in which the licensee takes actions outside of the

corrective action program in order to evaluate or correct issues of concern. The inspectors

noted several examples where degraded or nonconforming conditions were not corrected in a

timely manner and no evaluation had been performed that justified delayed correction of the

issue. In addition, the team identified examples where the licensee has taken ineffective

corrective actions, including one example of a cited violation based on the licensees failure to

take corrective actions to restore compliance within a reasonable time after a violation had been

identified.

The team determined that the licensee adequately evaluated industry operating experience for

relevance to the facility, and entered applicable items in the corrective action program. And,

based on focus group interviews, the team concluded that the licensee had a strong safety

conscious work environment. Workers stated they felt they could raise safety concerns without

fear of retaliation.

-2- Enclosure

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the licensees failure to

promptly correct degraded or nonconforming conditions in that the conditions

were not corrected at the first available opportunity or appropriately justify a

longer completion schedule. Some examples of affected degraded or

nonconforming conditions included degraded atmospheric relief valve

discharge line silencer, essential service water system water hammer events

and internal corrosion, and 23 items on the Operability Evaluation Database

that had not been corrected prior to the start of the last refuel outage. As

corrective actions for this issue, the licensee implemented interim procedural

guidance and initiated Condition Report 27071 to evaluate the adequacy of

tracking methods used for degraded, nonconforming, or unanalyzed

conditions. In addition, the licensee initiated a review of work requests,

condition reports, and other items for degraded, nonconforming, or

unanalyzed conditions and is assessing the justification for delayed

implementation of these corrective actions.

This issue was more than minor because it affected the equipment

performance attribute of the Mitigating Systems Cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Using Inspection

Manual Chapter 0609, the issue is determined to have very low safety

significance because the finding is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; did not

represent an actual loss of safety function of the system or train; did not result

in the loss of one or more trains of nontechnical specification equipment; and

did not screen as potentially risk significant due to a seismic, flooding, or

severe weather initiating event. The inspectors determined that the finding

has a crosscutting aspect in the area of human performance associated with

the component of resources because the licensee failed to provide adequate

procedures to assure timely resolution of degraded or nonconforming

conditions H.2(c) (Section 4OA2.5a).

Green. The inspectors identified a noncited violation of Technical

Specification 5.4.1.a for failure to properly implement Procedure AP 14A-003,

Scaffold Construction and Use, Revision 17, when scaffolding was erected

near operable safety-related equipment. On July 14, 15, and 28, the

inspectors identified a total of four instances where the minimum separation

distance between scaffolding and safety-related components was less than

the minimum allowed by procedure and an approved engineering evaluation

to justify the deviation was not performed. The licensee entered the issue

into its corrective action program as Condition Reports 26752 and 27010,

corrected each scaffolding deficiency, and performed comprehensive

-3- Enclosure

walkdowns of all scaffolding around safety-related structures, systems, and

components.

The deficiency was more than minor because if left uncorrected, it would

have the potential to lead to a more significant safety concern. The finding

was associated with the Mitigating Systems Cornerstone. Using Inspection

Manual Chapter 0609, the issue is determined to have very low safety

significance because the finding is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; did not

represent an actual loss of safety function of the system or train; did not result

in the loss of one or more trains of nontechnical specification equipment; and

did not screen as potentially risk significant due to a seismic, flooding, or

severe weather initiating event. The inspectors determined the finding has a

crosscutting aspect in the area of problem identification and resolution

associated with corrective action program because the licensee did not take

appropriate corrective actions to address previously identified scaffolding

construction issues in a timely manner P.1(d) (Section 4OA2.5b).

Green. The inspectors identified a finding for the failure to follow

Procedure AI 22A-001, Operator Work Arounds/Burdens/Control Room

Deficiencies, Revision 8, to adequately identify, document, and track control

room deficiencies associated with instruments and controls to ensure proper

prioritization and timely corrective actions. Specifically, inspectors observed

that the licensee had approximately 52 WR (work request) buttons on the

control boards indicating that work requests had been initiated to correct

problems on instruments and controls. However, not all deficiencies were

logged, and some of the deficiencies had existed for years without correction

or justification. The licensee initiated Condition Report 27034 to document

and evaluate this concern.

The deficiency was more than minor because if left uncorrected, it would

have the potential to lead to a more significant safety concern, in that, the

deficient condition could cause an operator to take an inappropriate action

based on expected plant response or conversely cause an operator not to

take action when action is required. The finding is associated with the

Mitigating Systems Cornerstone. The senior reactor analyst determined that

this finding was not appropriate to be evaluated using the significance

determination process since this finding was associated with numerous

equipment issues and associated human performance aspects that might

impact equipment operation. Using Inspection Manual Chapter 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria,

the finding is determined to have very low safety significance because there

was no adverse impact to plant equipment. The inspectors determined that

the cause of the finding has a crosscutting aspect in the area of problem

identification and resolution associated with the component of corrective

action program because the licensee did not identify issues completely,

accurately, and in a timely manner commensurate with their safety

significance P.1(a) (Section 4OA2.5c).

-4- Enclosure

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures and Drawings, for the

failure to implement Procedure AP 26C-004, Technical Specification

Operability, Revision 20, to adequately evaluate the operability of a

degraded essential service water system. Specifically, operations and

engineering personnel failed to adequately evaluate the operability of the

essential service water system when relevant new information was identified

that challenged a previously performed operability determination and which

challenged the reasonable expectation for operability. Condition Report

27288 was initiated to evaluate the failure to perform adequate operability

determinations.

The issue was more than minor because if left uncorrected, it would have the

potential to lead to a more significant safety concern. The finding is

associated with the Mitigating Systems Cornerstone. Using Inspection

Manual Chapter 0609, the issue is determined to have very low safety

significance because the finding is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; did not

represent an actual loss of safety function of the system or train; did not result

in the loss of one or more trains of nontechnical specification equipment; and

did not screen as potentially risk significant due to a seismic, flooding, or

severe weather initiating event. The inspectors determined that the cause of

the finding has a crosscutting aspect in the area of human performance

associated with resources because the licensee failed to provide complete,

accurate, and up-to-date procedures for performing operability evaluations

H.2(c) (Section 4OA2.5d).

Green. The inspectors identified a cited violation 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, because the licensee failed to

perform an adequate evaluation to determine the cause of loss of offsite

power induced water hammers and internal corrosion in the essential service

water system and did not take corrective actions to preclude repetition of

additional water hammer events and system leaks. Specifically, the licensee

performed an apparent cause evaluation instead of a root cause evaluation

as required, and the licensees evaluation did not consider metallurgical

evaluations that were performed outside the corrective action program. The

inspectors found that the licensee had not corrected a previous

NCV 05000482/2009007-03, Failure to Correctly Screen ESW Piping Leaks

for Significance, which resulted in the licensee failing to perform a root cause

evaluation. Because the licensee failed to restore compliance within a

reasonable time after NCV 05000482/2009007-03 was identified, this

violation is being cited in a Notice of Violation in accordance with

Section VI.A.1 of the NRCs Enforcement Policy. The licensees corrective

action to this cited violation was to initiate Condition Reports 27212, 26466,

and 27075, to evaluate and correct the identified conditions, to start a root

cause evaluation and, separately, to evaluate the licensees failure to

properly respond to NCV 05000482/2009007-03.

-5- Enclosure

The issue was more than minor because it is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and affects the

associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences, and is therefore a finding. Using Inspection Manual

Chapter 0609, the issue is determined to have very low safety significance

because the finding is not a design or qualification issue confirmed not to

result in a loss of operability or functionality; did not represent an actual loss

of safety function of the system or train; did not result in the loss of one or

more trains of nontechnical specification equipment; and did not screen as

potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The inspectors determined that the cause of the finding has a

crosscutting aspect in the area of problem identification and resolution

associated with the component of corrective action program because the

licensee failed to thoroughly evaluate problems such that the resolutions

address causes and extent of conditions P.1(c) (Section 4OA2.5e).

Green. The team identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the

failure to follow the requirements of Procedure AP 26C-004, Technical

Specification Operability, Revision 20. Specifically, Wolf Creek Generating

Station failed to confirm if a deficiency existed with the ability of the ultimate

heat sink to perform its safety function after delaying the 5-year scheduled

dredging of the channel. The licensee initiated Condition Report 27080 and

performed an operability determination to evaluate the deficiency.

The issue was more than minor because it was associated with the

equipment performance attribute of the Mitigating Systems Cornerstone, and

it affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609, the issue is

determined to have very low safety significance because the finding is not a

design or qualification issue confirmed not to result in a loss of operability or

functionality; did not represent an actual loss of safety function of the system

or train; did not result in the loss of one or more trains of nontechnical

specification equipment; and did not screen as potentially risk significant due

to a seismic, flooding, or severe weather initiating event. This finding has a

crosscutting aspect in the area of problem identification and resolution

associated with the corrective action program component because licensee

personnel failed to identify a potential deficiency in the ultimate heat sink in a

timely manner P.1(a) (Section 4OA2.5f).

Green. The inspectors reviewed a self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for failure to identify a

degraded equipment condition in December 2006. As a result, the

emergency diesel generator system experienced a failure on October 22,

2009, which caused the plant to make a notice of unusual event emergency

declaration. Licensee personnel missed an opportunity to identify the

-6- Enclosure

condition because they did not thoroughly evaluate a surveillance failure and

post-mortem testing data available in December 2006.

The finding is more than minor because it was associated with the equipment

performance attribute of the Mitigating Systems Cornerstone, and it affected

the cornerstone objective to ensure the availability, reliability, and capability

of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609, the issue is

determined to have very low safety significance because the finding is not a

design or qualification issue confirmed not to result in a loss of operability or

functionality; did not represent an actual loss of safety function of the system

or train; did not result in the loss of one or more trains of nontechnical

specification equipment; and did not screen as potentially risk significant due

to a seismic, flooding, or severe weather initiating event. A crosscutting

aspect was identified in the problem identification and resolution in that the

licensee did not thoroughly evaluate problems such that the resolution

addressed causes P.1(c) (Section 4OA2.5g).

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, for the failure to translate criteria

from the atmospheric relief valve accumulator leakage calculation into

proceduralized leakage criteria. Specifically, engineering personnel did not

translate the calculated design basis leakage criteria and the required

minimum pressure to start the test into the procedure. The licensee entered

this in to the corrective action program as Condition Report 26771, and the

licensee was developing plans to revise the leakage criteria in the procedure.

This issue was more than minor because it affected the design control

attribute of the Mitigating Systems Cornerstone and affected the objective to

ensure the reliability and capability of systems that respond to initiating

events to prevent undesirable consequences. Using Inspection Manual

Chapter 0609, the issue is determined to have very low safety significance

because the finding is not a design or qualification issue confirmed not to

result in a loss of operability or functionality; did not represent an actual loss

of safety function of the system or train; did not result in the loss of one or

more trains of nontechnical specification equipment; and did not screen as

potentially risk significant due to a seismic, flooding, or severe weather

initiating event. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program

component because licensee personnel failed to take appropriate corrective

actions to previously identified problems P.1(d) (Section 4OA2.5h).

-7- Enclosure

REPORT DETAILS

4. OTHER ACTIVITIES

4OA2 Problem Identification and Resolution (71152)

The inspectors based the following conclusions on the sample of corrective action

documents that were initiated in the assessment period, which ranged from February 16,

2008, to the end of the onsite portion of this inspection on July 30, 2010.

.1 Assessment of the Corrective Action Program Effectiveness

a. Inspection Scope

The inspectors reviewed approximately 275 condition reports, including associated root

cause, apparent cause, and direct cause evaluations that were completed between

February 16, 2008, and July 30, 2010, to determine if problems were being properly

identified, characterized, and entered into the corrective action program for evaluation and

resolution. The inspectors also reviewed system health reports, operability

determinations, self-assessments, trending reports, metrics, and various other documents

related to the corrective action program. The inspectors reviewed work requests and

condition reports to assess the reporting threshold and prioritization processes. The

inspectors review included verifying that the licensee considered the full extent of cause

and extent of condition for problems, as well as how the licensee assessed generic

implications and previous occurrences. The inspectors assessed the timeliness and

effectiveness of corrective actions, completed or planned, and looked for additional

examples of similar problems.

The inspectors also reviewed a sample of corrective action documents that addressed

past NRC-identified violations to ensure that the corrective actions addressed the issues

as described in the inspection reports. The inspectors reviewed a sample of corrective

actions closed to other corrective action documents to verify that corrective actions were

appropriate and timely.

The inspectors considered risk insights to focus the sample selection and plant tours on

risk significant systems and components. Based on this review, the samples reviewed by

the inspectors focused on, but were not limited to, these systems. The inspectors also

expanded this review to include 5 years of evaluations involving portions of the component

cooling water system and essential service water system interfaces, and the nitrogen

accumulators for the steam generator atmospheric relief valves to determine whether

problems were being effectively addressed. The inspectors conducted a walkdown of

these systems to assess whether problems were identified and entered into the corrective

action program.

-8- Enclosure

b. Assessments

Assessment - Effectiveness of Problem Identification

In general, the inspectors found that the licensee has been identifying problems and

entering them into their corrective action program at appropriately low thresholds.

However, the team identified issues that the licensee should have identified prior to the

NRC. Examples of ineffective identification of issues include the following:

NRC inspectors identified deficiencies in scaffolding that were erected near

operable safety-related equipment (Section 4OA2.5b).

Wolf Creek Generating Station failed to identify completely and accurately

deficiencies with instruments and controls associated with 52 WR (work request)

buttons on the control boards indicating that work requests had been initiated to

correct problems. All deficiencies were not logged, and some buttons were near

more than one control item such that it was not clear which buttons went with which

control (Section 4OA2.5c).

The licensee failed to identify a potential operability concern associated with

delaying the 5-year preventive maintenance (dredging) of the ultimate heat sink

(Section 4OA2.5f).

Wolf Creek Generating Station has not given new system engineers training to

identify issues that could impact their ability to identify deficiencies with safety-

related systems. This includes items such as clearance between scaffolding and

safety-related equipment and requirements for chocking carts near safety-related

equipment that would assist system engineers in identifying deficiencies that could

impact safety-related equipment. In addition, Wolf Creek Generating Station did not

require system engineers to attend classroom training on the system assigned to

them. This observation was more important for system engineers who had been

employed at the plant less than 3 years.

Assessment - Effectiveness of Prioritization and Evaluation of Issues

Overall, the team concluded that Wolf Creek Generating Stations staff is correctly

prioritizing and evaluating issues. The inspectors found that Wolf Creek Generating

Station had improved the cause evaluations by training individuals on various levels of

cause evaluations, by establishing teams of trained individuals to perform root cause

evaluations instead of one individual, providing a management sponsor for root cause

evaluation team, and providing greater senior leadership oversight over the cause

evaluations. However, the inspectors also found numerous instances where Wolf Creek

Generating Station failed to adequately evaluate the potential deficiencies with delays in

correcting degraded or nonconforming conditions. While most initial operability

determinations were appropriate, the inspectors identified several examples where poor

evaluations were performed or the basis for operability used engineering judgment that

was not supported by appropriate documentation. The following are examples of

ineffective or inadequate evaluation of issues:

-9- Enclosure

The team identified numerous examples of degraded or nonconforming conditions

with equipment problems that were not fixed prior to restart from the last outage (on

November 21, 2009) with no evaluation performed to justify the delay for fixing the

problem (Section 4OA2.5a).

Licensee personnel failed to adequately evaluate the operability of the essential

service water system when relevant new information was identified that challenged a

previously performed operability determination (Section 4OA2.5d).

The inspectors identified that the licensee failed to perform an adequate evaluation

to determine the cause of loss of offsite power induced water hammers and internal

corrosion in the essential service water system. Specifically, the licensee performed

an apparent cause evaluation instead of a root cause evaluation, and the licensees

evaluation did not consider metallurgical evaluations that were performed outside the

corrective action program (Section 4OA2.5e).

Wolf Creek Generating Station did not evaluate the cause for an emergency diesel

generator speed switch which could not be properly calibrated in December 2006.

Instead, the licensee replaced the speed switch and power supply without

determining that the cause was actually a degraded capacitor in the power supply.

As a result, the emergency diesel generator failed on October 22, 2009, from a

degraded capacitor in the power supply causing the plant to declare a notice of

unusual event emergency declaration (Section 4OA2.5g).

While performing an immediate operability evaluation of an emergency diesel

generator on May 20, 2010, (discussed above), the inspectors noted that testing and

analytical bases for establishing the acceptance criteria for the power supply noise

filter degradation was performed informally and not under the proper purviews of the

corrective action, quality assurance, or other applicable licensee programs.

Furthermore the test results and analysis conclusions were not properly documented

under such program or in any other engineering process document.

The inspectors observed that the licensee conducted activities outside of the

corrective action program in order to address problems related to the essential water

system water hammer events and internal corrosion. For example, the licensee

performed metallurgical analyses of piping corrosion and an analysis of water

hammer issues, outside of the corrective action program. As a result, the

conclusions of the evaluations were not evaluated through an updated operability

determination nor in an updated cause evaluation (Sections 4OA2.5d and 4OA2.5e).

Assessment - Effectiveness of Corrective Action Program

The inspectors concluded that actions to correct conditions adverse to quality were

generally effective. However, the team identified some notable examples where the

licensee had not implemented effective corrective actions or addressed extent of

condition. Some examples included:

- 10 - Enclosure

After the inspectors identified deficiencies with the minimum separation distance

between scaffolding and safety-related equipment, the licensee performed a

walkdown of all impacted scaffolding. After the licensees review, the inspectors

identified another example of the same deficiency. Two weeks later, the inspectors

identified two more examples of the same deficiency, which was reflective of

ineffective corrective actions.

After a previous NRC inspection identified a noncited violation (NCV) involving the

licensees failure to perform a root cause evaluation to determine the cause of the

loss of offsite power induced water hammers and internal corrosion in the essential

service water system, the licensees corrective action addressed the screening

criteria for the condition and failed to perform an adequate evaluation. The licensee

failed to restore compliance to NCV 05000482/2009007-003, Failure to Correctly

Screen ESW Piping Leaks for Significance, and, as a result, the team is issuing a

cited violation for this failure (4OA2.5e).

The licensee failed to take appropriate corrective actions to previously identified

deficiencies involving the failure to translate into procedures appropriate design basis

criteria for the nitrogen accumulators for the atmospheric relief valves. As a result,

the inspectors identified an NCV involving additional failures (Section 4OA2.5h).

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The inspectors examined the licensee's program for reviewing industry operating

experience, including reviewing the governing procedure and self-assessments. The

team reviewed a sample of condition reports examining operating experience documents

that had been issued during the assessment period to assess whether the licensee had

appropriately evaluated the notification for relevance to the facility. The inspectors also

examined whether the licensee had entered those items into their corrective action

program and assigned actions to address the issues. The inspectors reviewed a sample

of root cause evaluations and significant condition reports to verify if the licensee had

appropriately included industry operating experience.

b. Assessment

Overall, the inspectors determined that the licensee had appropriately evaluated industry

operating experience for relevance to the facility, and had entered applicable items in the

corrective action program. Both internal and external operating experience was being

incorporated into lessons learned for training and pre-job briefs.

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed a sample of licensee self-assessments and audits to assess

whether the licensee was regularly identifying performance trends and effectively

- 11 - Enclosure

addressing them. The inspectors also reviewed audit reports to assess the

effectiveness of assessments in specific areas. The specific self-assessment

documents and audits reviewed are listed in the attachment.

b. Assessment

The inspectors concluded that the licensee had an effective self-assessment process.

Licensee management was involved in developing the topics and objectives of self-

assessments. Attention was given to assigning inspectors members with the proper

skills and experience to do an effective self-assessment and to include people from

outside organizations. Audits were self-critical and identified deficiencies in various

programs such as the corrective action program and several root cause evaluations.

.4 Assessment of Safety-Conscious Work Environment

a. Inspection Scope

The inspection team conducted four focus group sessions consisting of approximately

10 individuals randomly chosen. Focus groups were conducted with individuals from

operations, maintenance, planners, and system engineers. These sessions were

designed to elicit a qualitative assessment of the degree to which the participants

believed Wolf Creek Generating Station management had established and maintained a

safety conscious work environment and were based upon the NRCs definition of a

safety conscious work environment:

An environment in which employees feel free to raise safety concerns,

both to their management and to the NRC, without fear of retaliation

and where such concerns are promptly reviewed, given the proper

priority based on their potential safety significance, and appropriately

resolved with timely feedback to employees.

Focus group participants were also asked questions in order for the team to make a

qualitative assessment of Wolf Creek Generating Stations safety culture as defined by

the crosscutting aspects described in NRCs Manual Chapter 0310. The team also

reviewed the results of the licensees 2008 and 2010 Nuclear Safety Culture

Assessment results. In particular, the inspectors reviewed licensee actions related to

issues to reverse the trend of a substantive crosscutting issue in the area of problem

identification and resolution involving Wolf Creek Generating Station personnels ability

to thoroughly evaluate and prioritize problems such that the resolutions effectively

address the causes and extent of conditions. The NRC has identified four consecutive

assessment cycles with this substantive crosscutting issue.

- 12 - Enclosure

comfortable raising concerns in each of the avenues available to them including raising

concerns with the NRC. Workers who had been at the site many years knew the Wolf

Creek Generating Station Ombudsman because the Ombudsman is a long time

employee. Newer employees were also aware of the Ombudsman.

Wolf Creek Generating Stations 2010 Nuclear Safety Culture Assessments identified

several issues which were entered into the licensees corrective action program. Some

of the findings dealt with the substantive crosscutting issue involving Wolf Creek

Generating Station personnels ability to thoroughly evaluate and prioritize problems

such that the resolutions effectively address the causes and extent of conditions. For

example, Condition Report 24196 reviewed the finding that some station personnel

believe root cause analyses are not effective in identifying the fundamental causes of

events. The licensees evaluation of this finding noted the substantial improvements that

had been made to the stations performance in conducting root cause evaluations which

occurred in 2009. These improvements included training for evaluators, dedicating a

team of trained individuals instead of a single individual to perform these evaluations,

assigning a manager to each root cause evaluation, and additional senior management

oversight over the evaluations. The licensee has seen 100 percent corrective action

review board approval of root causes since the beginning of 2009. The condition report

stated that the results of these improvements were not widely communicated to all

employees. In addition, the condition report noted that communications of the root

cause evaluations (the causes and the corrective actions) were not communicated to

station personnel. As a result, the corrective action was to develop corporate

communication strategies. The condition report was closed on June 15, 2010, after

procedure changes were made to improve station communication of root cause

evaluations and corrective actions. Based on this, the team concluded that Wolf Creek

Generating Station management believed its workers perceptions were in error related

to the effectiveness of the cause evaluations.

The team noted that on January 23, 2010, the licensee initiated Condition Report 23032

which was a root cause evaluation dealing with the significant human and corrective

action performance gaps. The condition report also noted that Wolf Creek Generating

Station has had four consecutive assessment cycles of the substantive crosscutting

issue in the area of problem identification and resolution involving Wolf Creek

Generating Station personnels ability to thoroughly evaluate and prioritize problems

such that the resolutions effectively address the causes and extent of conditions. The

condition report also noted that Wolf Creek Generating Station is on the threshold of

exceeding more than three crosscutting aspects in other human performance and

problem identification and resolution themes. The licensees corrective actions

associated with Condition Report 23032 were intended to reverse the trend of

substantive crosscutting issues.

- 13 - Enclosure

In May 2010, Wolf Creek Generating Station performed a self-assessment which

concluded that several root cause evaluations, including the root cause evaluation

associated with Condition Report 23032, had deficiencies with the causes or the

corrective actions. Therefore, the licensee undertook an effort to re-perform the root

cause evaluations. As of the close of this inspection, the licensee had not completed the

root cause evaluation and, as such, the team could not review the licensees plans to

address the substantive crosscutting issue. The team also noted that the deficiencies

found in these root cause evaluations could reinforce workers perceptions that cause

evaluations were not effective in identifying the fundamental causes of events.

.5 Specific Issues Identified During This Inspection

a. Failure to Resolve Degraded Conditions in a Timely Manner

Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, for the licensees failure to assure that conditions

adverse to quality were corrected in a time frame commensurate with the safety

significance of the condition. Specifically, the licensee failed to resolve degraded or

nonconforming conditions at the first available opportunity or appropriately justify a

longer completion schedule.

Description. During the inspection, numerous adverse conditions were identified

associated with safety-related structures, systems, or components and that were initially

identified prior to restart from Refueling Outage 17 on November 21, 2009. Examples of

these degraded or nonconforming conditions included degraded atmospheric relief valve

discharge line silencer, essential service water system water hammers and internal

corrosion, vibration associated with essential service water system Valves EFV58 and

EFV90, fisher butterfly valves, and essential service water system pump room

penetration seals. The inspectors also observed that the Operability Evaluation

Database listed 23 items that were evaluated as operable by a prompt operability

determination prior to the start of the last refueling outage. Further, the inspectors

identified that the licensee had no formal method to track and correct degraded or

nonconforming conditions that were only reviewed by an immediate operability

determination.

Regulatory Information Summary 2005-20, associated with Inspection Manual,

Part 9900: Technical Guidance, Operability Determinations and Functionality

Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to

Quality or Safety, dated April 16, 2008, describes the appropriate time frame for

correcting degraded or nonconforming conditions as the first available opportunity (i.e.,

prior to restart from the next outage). If corrective actions cannot be implemented at the

first available opportunity, then the licensee should appropriately justify a longer

completion schedule. For the degraded or nonconforming conditions described above,

the inspectors concluded that the licensee had not implemented a timely schedule for

completing corrective actions for structures, systems, and components, to correct the

conditions adverse to quality prior to restart after Refueling Outage 17 on November 21,

2009, or appropriately justify a longer completion schedule.

- 14 - Enclosure

On December 17, 2009, Condition Report 22501 was initiated to document issues

associated with Violation 05000482/2009005-11. One of the issues communicated to

the licensee by the NRC senior resident inspector was the lack of timely corrective

actions for degraded condition associated with the violation. Further, the inspector

explained that the timeframe in which corrective actions should be implemented for

degraded or nonconforming conditions was described in Regulatory Information

Summary 2005-20. The licensees evaluation identified that there was not adequate

procedural guidance to assure that degraded or nonconforming conditions were resolved

at the first available opportunity or appropriately justify a longer completion schedule.

The licensee identified corrective actions for interim guidance, until additional procedure

guidance could be developed. Also, a review was in-progress to review for degraded,

nonconforming, or unanalyzed conditions to ensure that any items that have been

delayed or not completed have proper justification for delayed implementation of

corrective actions based on the risk. The licensee initiated Condition Report 27071 to

further evaluate the adequacy of tracking methods used for degraded, nonconforming, or

unanalyzed conditions.

Analysis. The inspectors determined that the failure to take timely corrective actions for

conditions adverse to quality was a performance deficiency. The deficiency was more

than minor because it affected the equipment performance attribute of the Mitigating

Systems Cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using

Inspection Manual Chapter 0609, the issue is determined to have very low safety

significance because the finding is not a design or qualification issue confirmed not to

result in a loss of operability or functionality; did not represent an actual loss of safety

function of the system or train; did not result in the loss of one or more trains of

nontechnical specification equipment; and did not screen as potentially risk significant

due to a seismic, flooding, or severe weather initiating event. The inspectors determined

that the cause of the finding has a crosscutting aspect in the area of human performance

associated with the component of resources because the licensee failed to provide

adequate procedures to assure timely resolution of degraded or nonconforming

conditions H.2(c).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires, in part, that measures shall be established to assure that conditions adverse to

quality are promptly identified and corrected. Contrary to the above, prior to

November 21, 2009, the licensee failed to assure that conditions adverse to quality were

corrected in a time frame commensurate with the safety significance of the condition.

Specifically, the licensee failed to resolve degraded or nonconforming conditions at the

first available opportunity, which was prior to restart after Refueling Outage 17 on

November 21, 2009, or appropriately justify a longer completion schedule. Because this

finding is of very low safety significance and has been entered into the licensees

corrective action program as Condition Reports 22501 and 27071, this violation is being

treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000482/2010006-01, Failure to Resolve Degraded Conditions in a Timely

Manner.

- 15 - Enclosure

b. Scaffolding Installation Inadequacy

Introduction. The inspectors identified a Green NCV of Technical Specification 5.4.1.a

for failure to properly implement Procedure AP 14A-003, Scaffold Construction and

Use, Revision 17, when scaffolding was erected near operable safety-related

equipment. The inspectors identified four instances where the minimum separation

distance between scaffolding and safety-related components was less than the minimum

allowed by procedure and an approved engineering evaluation to justify the deviation

was not performed.

Description. On July 14, 2010, during a walkdown of the component cooling water

system with the system engineer, the inspectors identified scaffolding erected less than

1 inch from safety-related piping. The inspectors reviewed Procedure AP 14A-003,

which included installation and use guidelines for seismically qualified scaffolding, and

observed that the criteria included a 2 inch minimum clearance requirement between

scaffolding and sensitive safety-related or special scope equipment and/or components.

Further, this minimum clearance could be reduced to 1 inch between scaffolding and

piping with diameter equal or greater than 3 inches. When the criteria for seismically

qualified scaffolding could not be met, an engineering evaluation was required. The

inspectors reviewed Scaffolding Request 10-S0109, documented on

Form APF 14A-003-01, and observed that an engineering evaluation and post-

installation inspections had not been completed. The inspectors concluded that the

scaffolding observed on July 14 did not meet the clearance criteria of

Procedure AP 14A-003 and did not have an engineering evaluation. The system

engineer initiated Condition Report 26752 to document the inspectors observation. The

scaffolding was modified to meet the requirements of Procedure AP 14A-003. The

extent of condition associated with the condition report noted that the condition could

exist on other scaffolding near safety-related equipment. Consequently, on July 14,

2010, the licensee performed a walkdown of all scaffolding erected around safety-related

equipment to verify compliance with the requirements of Procedure AP 14A-003.

On July 15, 2010, during a walk down of the essential service water system with the

system engineer, the inspectors identified another instance where scaffolding was

erected less than 1 inch from safety-related piping with diameter greater than 3 inches.

The condition observed by the inspectors was added to Condition Report 26752. The

inspectors questioned why this additional scaffolding problem was not identified during

the extent of condition review in response to the inspectors July 14 observation.

Maintenance personnel stated that the control side was not inspected as part of the

extent of condition walk down, so this scaffolding was not verified. Based on the

inspectors additional observations, the licensee performed a more extensive walkdown

on July 16 which identified two additional installed scaffolding that may not have the

minimum clearances required by Procedure AP 14A-003. These two additional

scaffolding issues were documented in Condition Report 26752. All scaffolding was

modified to meet the requirements of Procedure AP 14A-003.

- 16 - Enclosure

On July 28, 2010, during a walkdown of the essential service water system pump house

with the system engineer, the inspectors identified two instances where scaffold to

instrument tubing clearance was less than the 2-inch minimum clearance requirement of

Procedure AP 14A-003, and no engineering evaluations had been performed for the

conditions. The system engineer initiated Condition Report 27010 to document the

inspectors observation. The scaffolding was modified to meet the requirements of

Procedure AP 14A-003.

A previous NCV (NCV 05000482/2009005-12) was identified when component cooling

water Train B was in contact with a seismically unqualified scaffold while component

cooling water was required to be operable. One of the causes identified was associated

with failing to properly fill out Form APF 14A-003-01. This indicates the licensee has

been challenged with correcting scaffolding issues.

Analysis. The inspectors determined that the failure to properly install and inspect

scaffolding in safety-related areas was contrary to written procedural requirements and

was a performance deficiency. The deficiency was more than minor because if left

uncorrected, it would have the potential to lead to a more significant safety concern. The

finding was associated with the Mitigating Systems Cornerstone. Using Inspection

Manual Chapter 0609, the issue is determined to have very low safety significance

because the finding is not a design or qualification issue confirmed not to result in a loss

of operability or functionality; did not represent an actual loss of safety function of the

system or train; did not result in the loss of one or more trains of nontechnical

specification equipment; and did not screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. The inspectors determined that the

cause of the finding has a crosscutting aspect in the area of problem identification and

resolution associated with the component of corrective action program because the

licensee did not take appropriate corrective actions to address previously identified

scaffolding construction issues in a timely manner P.1(d).

Enforcement. Technical Specification 5.4.1.a requires that procedures be established,

implemented and maintained as recommended in Regulatory Guide 1.33, Appendix A.

Section 9.a of Appendix A, requires, in part, that maintenance affecting safety-related

equipment be accomplished in accordance with procedures. Procedure AP 14A-003

Scaffold Construction and Use, Revision 17, step F.4.1, required a 2 inch minimum

clearance between scaffolding and sensitive safety-related equipment, such as,

instrument tubing lines. The minimum clearance could be reduced to 1 inch between

scaffolding and safety-related piping with diameter equal or greater than 3 inches.

Procedure AP 14A-003, step F.4.2, required an engineering evaluation of the scaffolding

if these clearances could not be met. Contrary to the above, on July 14, 15, and 28,

2010, the inspectors identified four examples where the separation distance between

scaffolding and safety-related components was less than the minimum allowed by

procedure and an approved engineering evaluation to justify the deviation was not

performed. Specifically, the inspectors identified two scaffold poles that were less than 1

inch from the component cooling water and essential cooling water system piping with

diameter greater than 3 inches. The inspectors also identified two locations where

scaffold poles were less than 2 inches from essential service water system instrument

tubing. The licensee inspected other scaffolding erected near safety-related equipment

- 17 - Enclosure

and identified two additional instances where the separation distance between

scaffolding and safety-related components was less than the minimum allowed by

procedure. Because the finding is of very low safety significance and has been entered

into the corrective action program as Condition Reports CRs 26752 and 27010, this

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000482/2010006-02, Scaffolding Installation Inadequacy.

c. Control Room Deficiency Tracking

Introduction. The inspectors identified a Green Finding for the failure of operations

personnel to follow Procedure AI 22A-001, Operator Work Arounds/Burdens/Control

Room Deficiencies, Revision 8, to adequately identify, document, and track control

room deficiencies associated with instruments and controls to ensure proper

prioritization and timely corrective actions.

Description. On July 16, 2010, the inspectors performed a walkdown of the main control

room area. The inspectors observed small blue, round magnets, labeled WR at

various locations on the main control boards. When asked, the reactor operator

informed the inspectors that the magnets were called Buttons, and they were used to

identify control board components that had work requests written against them, and

were placed near the affected equipment. The inspectors estimated that approximately

52 WR buttons were on the control boards, and observed that it was not clear which WR

button corresponded to which control board component since there was no information

provided on the button. The inspectors were informed that the buttons were

implemented several years ago as a method to reduce control board clutter by replacing

larger tags that hung from the control boards with the small blue magnets.

The inspectors questioned the reactor operators how they were able to determine the

equipment issue associated with a WR button. Operations personnel stated that the

information could be retrieved from various methods, including a review of the control

room tag book. The control room tag book, located in the shift managers office,

contained work request tags that tracked the open work requests written against control

room equipment. The inspectors reviewed the control room tag book and observed that

not every WR button had a corresponding work request tag and several tags did not

have corresponding WR buttons.

The inspectors reviewed Procedure AI 22A-001, Operator Work

Arounds/Burdens/Control Room Deficiencies, Revision 8, and noted that a control room

deficiency was defined as, A deficiency involving components in the control room such

that the indication in the control room does not accurately reflect actual plant condition or

the direct control room control is hindered. Procedure AI 22A-001 also directed that

control room deficiencies be monitored to ensure the following: (1) the item meets the

definition of control room deficiency; (2) the proper priority has been assigned; and (3)

the items are progressing to completion in a timely manner.

The inspectors reviewed the control room deficiency log and determined that only eight

items were categorized as control room deficiencies. The inspectors concluded that

numerous open work requests met the definition of a control room deficiency, as defined

in Procedure AI 22A-001, but were not listed in the control room deficiency log. Further,

- 18 - Enclosure

the inconsistent methods used to track control board component issues, such as, WR

buttons, a control room tag book, an information tag book, and the control room

deficiency log, have resulted in deficient equipment conditions that were not receiving

the appropriate prioritization and were not being corrected in a timely manner. For

example, the inspectors noted that one work request tag has been open since 2005

without correction or appropriate justification.

The absence of information and the inability to determine which WR button was

associated with which control board component issue was a concern to the inspectors.

Specifically, the inconsistent method used to track control board component issues was

a concern since important information may not be readily available to operations

personnel while trying to diagnose proper equipment and plant response during routine

and nonroutine operations. The ability to appropriately diagnose proper response during

nonroutine operations, such as, alarm, abnormal, or emergency response situations was

of particular concern. Operations personnel initiated Condition Report 27034 to

document this concern in the corrective action program.

Analysis. The inspectors determined that the failure of operations personnel to follow

administrative requirements for control room deficiency monitoring to ensure proper

prioritization and timely corrective actions was a performance deficiency. The deficiency

was more than minor because if left uncorrected, it would have the potential to lead to a

more significant safety concern, in that, the deficient condition could cause an operator

to take an inappropriate action based on expected plant response or conversely cause

an operator not to take action when action is required. The finding is associated with the

Mitigating Systems Cornerstone. The senior reactor analyst determined that this finding

was not appropriate to be evaluated using the significance determination process since

this finding was associated with numerous equipment issues and associated human

performance aspects that might impact equipment operation. Using Inspection Manual

Chapter 0609, Appendix M, Significance Determination Process Using Qualitative

Criteria, the finding is determined to have very low safety significance because there

was no adverse impact to plant equipment. The inspectors determined that the cause of

the finding has a crosscutting aspect in the area of problem identification and resolution

associated with the component of corrective action program because the licensee did

not identify issues completely, accurately, and in a timely manner commensurate with

their safety significance P.1(a).

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because the

administrative procedure to track control room discrepancies is not required by technical

specifications. The licensee entered the finding into the corrective action program as

Condition Report 27034 to evaluate the issue and identify corrective actions. Because

this finding does not involve a violation of regulatory requirements and has very low

safety significance, it is identified as FIN 05000482/2010006-03, Control Room

Deficiency Tracking.

- 19 - Enclosure

d. Failure to Update an Operability Evaluation

Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures and Drawings, for the failure of operations and

engineering personnel to follow procedures and adequately evaluate degraded

conditions to support operability decision-making.

Description. The inspectors reviewed Operability Evaluation OE EF 09-007 to determine

the adequacy of the evaluation to address essential service water system degraded

conditions. The inspectors also reviewed the operability evaluation to determine

whether it met the requirements of Procedure AP 26C-004, Technical Specification

Operability, Revision 20, OTSC 09-0103, and Procedure AP 28-001, Operability

Evaluations, Revision 17, OTSC 10-0029.

Operability Evaluation OE EF 09-007, Revision 0, was initiated on September 24, 2009,

to support the operations shift managers determination of operability for the essential

service water system (See NCV 05000482/2009007-02). The operability evaluation

compiled the issues associated with essential service water system water hammer

susceptibility and mitigation for determination of continued operability of the system.

Revision 0 of the operability evaluation specifically addressed the effects of pressure

transients as a result of essential service water pump starts and the combined effects of

corrosion in essential service water piping. The inspectors observed that the operability

evaluation primarily focused on the effects of water hammer on only the four

containment cooling units. The operability impact of the degraded water hammer

susceptibility condition for other safety-related essential service water structures,

systems, and components was partially considered, in that previously performed

engineering reviews, operations procedures, and testing practices were credited as the

basis for system operability. The operability evaluation also considered essential service

water corrosion as evaluated in Apparent Cause Evaluation Condition Report 18785,

which determined that the previous through wall leakage events were a result of

localized pits that continued to propagate, over a period of time, from the inner pipe

diameter until the corrosion was through wall. The apparent cause evaluation concluded

that of the three major types of localized corrosion (crevice corrosion, under-deposit

corrosion, and microbiological influenced corrosion), under-deposit corrosion was the

cause of the pitting found at Wolf Creek Generating Station; and that the nature of the

pitting was understood and documented. Microbiological-induced corrosion was

determined to be minimal due to the chemical control measures in place.

Operability Evaluation OE EF 09-007, Revision 1, was initiated on June 29, 2010, to

address the affects of localized pitting corrosion from inside the piping resulting in

through wall leaks. The revised operability evaluation identified a through wall leak that

developed on June 29, 2010, which was determined to be degraded, but operable,

through application of Code Case N-513-2. The revision also discussed testing

performed as a corrective action from Apparent Cause Evaluation Condition

Report 18785 for the evaluated corrosion mechanism, and referenced Project Report

WCN005-PR-01, Analysis of Water Hammer Issues, Revision 0, that was completed

on March 8, 2010. The operability evaluation stated that no immediate concerns were

identified during review of the project report.

- 20 - Enclosure

The inspectors reviewed Apparent Cause Evaluation Condition Report 21127, which

was initiated on October 24, 2009, to document the identification that essential service

water system piping welds and/or their heat affected zones may be affected by a

corrosion mechanism different than the typical under deposit pitting corrosion generally

seen at Wolf Creek. This condition was identified during destructive examination of a

portion of essential service water piping associated with a through wall leak that

occurred on July 27, 2009. The apparent cause evaluation concluded, in part that:

(1) pipe wall thinning specifically and uniquely at welds had not been a noted issue with

essential service water piping prior to this event; (2) the through wall leak resulted from a

combination of erosion and corrosion; (3) turbulence is adding an erosion mechanism;

(4) the essential service water pipe wall-thinning program does not give direction to look

at wall thinning under welds, or potential wall thinning at weldolets; (5) recent history at

Wolf Creek indicates that large bore piping may be more susceptible to through wall

leaks than small bore piping; and (6) past history indicates piping exhibiting low and no

flow rates may be more susceptible to through wall leaks.

The inspectors reviewed metallurgical investigation reports dated October 27, 2009, and

November 25, 2009, performed outside the corrective action program. The inspectors

observed that both reports concluded that the cause of the corrosion that resulted in the

July 27, 2009, and another 30 inch diameter essential service water pipe leak was most

likely caused by microbiologically induced corrosion. The report further concluded that

tubercles formed on the surface of the piping inner diameter which covered the

underlying bacteria on the metallic surface. This helped to shield it from the

antimicrobial chemicals and biocides that were used to chemically control water and

prevent this corrosion mechanism. Once this under deposit corrosion was protected, the

area experienced extremely localized and likely rapidly progressing corrosion.

The inspectors reviewed internal operating experience that was relevant to the essential

service water system degraded condition and found that it had not been fully considered

in Operability Evaluation OE EF 09-007, Revisions 0 and 1. On August 19, 2009, a leak

of approximately 20 gpm from the essential service water system piping occurred on the

1988 elevation level of the auxiliary building concurrent with a loss of offsite power

event. This leak was identified by the NRC resident inspectors since

Procedure STN PE-040G, Transient Event Walkdown, did not identify the essential

service water system as vulnerable to off-normal dynamic forces

(NCV 05000482/2009007-06). The leak was identified when the resident inspector

noted 1 to 3 inches of water buildup on the floor one level below the elevation where the

leak had occurred 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> earlier. During the refueling outage that concluded on

November 21, 2009, and subsequent to initiation of emergency safety features actuation

systems testing, two components connected to the essential service water system

experienced leaks. One was the result of an extruded gasket on the residual heat

removal Train A pump room cooler. The second leak was due to a split in a dissimilar

metal joint in Containment Cooler SGN01C. The inspectors concluded that these

internal operating experience events illustrate that previous corrective actions credited in

Operability Evaluation OE EF 09-007 have been ineffective, and the locations of water

hammer induced leaks following loss of offsite power events are largely unpredictable.

- 21 - Enclosure

The inspectors reviewed Project Report WCN005-PR-01, Analysis of Water Hammer

Issues, Revision 0, dated March 8, 2010, and observed that much of the information,

including the conclusions and recommendations, were not consistent with previously

performed engineering evaluations and calculations described in Operability

Evaluation OE EF 09-007. Procedure AP 28-001, step 6.2.6.1.c, required the evaluator to

consider consequential failures in the evaluation of the deficiency when discussing the

systems capability of performing specified safety functions. The inspectors concluded that

Operability Evaluation OE EF 09-007, Revisions 0 and 1, failed to consider the

consequential failure of safety-related equipment adjacent to essential service water

structures and components that were susceptible to water hammer induced leakage as a

result of the degraded condition.

On July 29, 2010, the inspectors observations were communicated to licensee.

Operability Evaluation OE EF 09-007, Revision 2, was completed on July 30, however, the

revision only acknowledged that microbiologically induced corrosion was present, but

indicated that past history shows that bacteria were not an aggressive contributor to

corrosion due to chemical controls. On August 10, the inspectors informed the licensee

that Operability Evaluation OE EF 09-07, Revision 2, was still inadequate. As a result, the

licensee completed Revision 3 on August 12, 2010, to document an adequate basis for

operability. Condition Report 27288 was initiated to evaluate the failure to perform

adequate operability determinations.

Procedure AP 26C-004, Technical Specification Operability, Revision 20,

OTSC 09-0103, Section 6.1, required that identified deficiencies that could affect the

operability of a structure, system, or component subject to technical specifications be

evaluated for operability. However, there was no specific procedure guidance to ensure

that new information which challenges/changes the assumptions or basis for previously

performed operability determinations, be presented to operations personnel to evaluate

the condition and assure the continued reasonable expectation for operability.

Analysis. The inspectors determined that the failure to adequately evaluate the degraded

conditions to support the operability determination was a performance deficiency. The

deficiency was more than minor because if left uncorrected, it would have the potential to

lead to a more significant safety concern. The finding is associated with the Mitigating

Systems Cornerstone. Using Inspection Manual Chapter 0609, the issue is determined to

have very low safety significance because the finding is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; did not represent an actual

loss of safety function of the system or train; did not result in the loss of one or more trains

of nontechnical specification equipment; and did not screen as potentially risk significant

due to a seismic, flooding, or severe weather initiating event. The inspectors determined

that the cause of the finding has a crosscutting aspect in the area of human performance

associated with resources because the licensee failed to provide complete, accurate, and

up-to-date procedures for performing operability evaluations H.2(c).

- 22 - Enclosure

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures

and Drawings, requires that activities affecting quality shall be prescribed by

instructions, procedures, or drawings and shall be accomplished in accordance with

those instructions, procedures, and drawings. The determination of operability for

technical specification related systems, structures, and components needed to mitigate

accidents was an activity affecting quality and was implemented by

Procedure AP 26C-004, Technical Specification Operability, Revision 20,

OTSC 09-0103. Procedure AP 28-001, Operability Evaluations, Revision 17,

OTSC 10-0029, provided instructions and guidelines to engineering personnel for

performing operability evaluations in support of the prompt operability determination

required by Procedure AP 26C-004. Contrary to the above, from September 25, 2009,

through August 12, 2010, operations and engineering personnel failed to implement

Procedure AP 26C-004, Section 6.1, to adequately evaluate the operability of a

degraded essential service water system. Specifically, operations and engineering

personnel failed to adequately evaluate the operability of the essential service water

system when relevant new information was identified that challenged a previously

performed operability determination and challenged the reasonable expectation for

operability. Because the finding is of very low safety significance and has been entered

into the licensees corrective action program as Condition Report 27288, this violation is

being treated as an NCV, consistent with Section VI.A of the Enforcement Policy:

NCV 05000482/2010006-04, Failure to Update an Operability Evaluation.

e. Failure to Perform Adequate Evaluation for Significant Conditions

Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the licensees failure to perform an

adequate evaluation to determine the cause and take corrective actions to preclude

repetition of a significant condition adverse to quality associated with loss of offsite

power induced water hammers and internal corrosion in the essential service water

system.

Description. On December 4, 2009, the NRC completed a special inspection to examine

activities associated with the stations performance during a loss of offsite power on

August 19, 2009. During the inspection, NCV 05000482/2009007-03, Failure to

Correctly Screen ESW Piping Leaks for Significance, was identified for the failure to

correctly screen for significance occurrences of water hammer damage and essential

service water piping corrosion that resulted in system damage. Because of the failure to

correctly screen the issue for significance, the licensee did not perform a root cause

analysis to evaluate the additive effect of documented loss of offsite power induced

water hammers and internal corrosion. The licensee entered the finding into the

corrective action program as Condition Report 22239.

The inspectors reviewed the apparent cause evaluation to Condition Report 22239 and

noted that the evaluation was primarily focused on the significance screening issue of

concern. The screening error for Condition Report 18785 was not corrected, and

consequently, no root cause evaluation was performed for the significant condition

adverse to quality.

- 23 - Enclosure

The inspectors reviewed the corrective action documents, project plans, and

metallurgical investigation reports, associated with the water hammer and internal

corrosion issues to determine the evaluation adequacy for the significant essential

service water system problems. The inspectors also reviewed the action and project

plans to determine the adequacy of identified corrective actions to preclude repetition of

the significant condition. The inspectors determined that the licensee failed to fully

identify the cause of the condition and identify adequate corrective actions within the

corrective action program. Section 4OA2.5(d) of this report (the previous section)

documents NCV 05000482/2010006-04 and provides the technical description of the

essential service water system corrosion and water hammer degraded conditions.

Based on a review of the technical information, the inspectors determined that the

licensee has pursued a symptom-based approach, both inside and outside the corrective

action program, to evaluate and correct the different aspects of the issues. However, the

information has not been assembled and considered in a single cause determination

which evaluates the additive effect of documented loss of offsite power induced water

hammers and internal corrosion, from which the licensee can develop well-justified

corrective actions to preclude repeated essential service water system damage.

The licensee initiated Condition Report 27212 to document the failure to perform an

adequate evaluation for the significant essential service water system deficiencies.

Condition Report 26466 was in progress to perform a root cause evaluation for the

identified conditions. Additionally, Condition Report 27075 was initiated to evaluate the

failure to properly respond to NCV 05000482/2009007-03.

Analysis. Inspectors determined that the failure to determine the cause and preclude

repetition of a significant condition adverse to quality was a performance deficiency. The

deficiency was more than minor because it is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences, and is therefore a

finding. Using Inspection Manual Chapter 0609, the issue is determined to have very

low safety significance because the finding is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; did not represent an actual

loss of safety function of the system or train; did not result in the loss of one or more

trains of nontechnical specification equipment; and did not screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. The inspectors

determined that the cause of the finding has a crosscutting aspect in the area of problem

identification and resolution associated with the component of corrective action program

because the licensee failed to thoroughly evaluate problems such that the resolutions

address causes and extent of conditions P.1(c).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires that in the case of significant conditions adverse to quality, measures shall

assure that the cause of the condition is determined and corrective action taken to

preclude repetition. Contrary to the above, from December 4, 2009, through July 29,

2010, the licensee failed to perform an adequate evaluation to determine the cause of

loss of offsite power induced water hammers and internal corrosion in the essential

- 24 - Enclosure

service water system and did not take corrective actions to preclude repetition of

additional water hammer events and system leaks. The finding has been entered into the

licensees corrective action program as Condition Reports 27212, 26466, and 27075, to

evaluate and correct the identified conditions. Due to the licensees failure to restore

compliance from the previous NCV 05000482/2009007-03 within a reasonable time after

the violation was identified, this violation is being cited in a Notice of Violation consistent

with Section VI.A of the NRC Enforcement Policy: VIO 05000482/2010006-05, Failure

to Perform Adequate Evaluation for Significant Conditions.

f. Failure to Determine if a Deficiency Existed in the Ultimate Heat Sink

Introduction. The team identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion

V, Instructions, Procedures, and Drawings, for the failure to follow the requirements of

Procedure AP 26C-004, Technical Specification Operability, Revision 20. Specifically,

the licensee failed to confirm if a deficiency existed with the ability of the ultimate heat

sink to perform its safety function.

Description. On July 26, 2010, the NRC reviewed Condition Report 26744, which was

initiated on July 14, 2010, and discussed the licensees failure to budget the money

necessary to perform the dredging of the ultimate heat sink channel before its due date

of September 2009. The preventive maintenance to dredge the channel is performed on

a 5-year frequency and is required to maintain operability of the ultimate heat sink. The

licensee did not evaluate the potential deficiency related to delaying the preventive

maintenance dredging of the ultimate heat sink because Procedure AP 16B-003,

Planning and Scheduling Preventive Maintenance, Revision 3, allows a 25 percent

grace period. As a result, the preventive maintenance is allowed to be performed within

6.25 years before it is considered late. Although Wolf Creek Generating Station

personnel had initiated subwork Order 09-319153-000 on August 4, 2009, to perform the

dredging, Condition Report 26744 was initiated almost a year later when Wolf Creek

Generating Station personnel were concerned that they might miss performing the

preventive maintenance within the 6.25 year deadline.

Prior to 2003, the licensees USAR required annual sedimentation checks in order to

determine the annual growth of sediment in the ultimate heat sink. In 2003, the licensee

evaluated the sedimentation data in Calculation Z065-C-001, and determined that the

ultimate heat sink would remain operable if the channel was dredged every five years

and the entire reservoir was dredged every 15 years. As a result, the licensee changed

its USAR requirements and suspended annual sedimentation checks.

Calculation Z065-C-001 used 18 years of data and calculated an average annual growth

rate in the channel of approximately 3 inches per year. The acceptance criterion is

24 inches of sedimentation growth, and the licensee concluded that sediment would

reach a maximum of 18.75 inches when the preventive maintenance (dredging) was

performed in 6.25 years. However, the team noted that the sediment level grew

10 inches in 1993, which was an unusually wet year according to lake records kept by

the licensee. The licensee believed this was an anomaly and unlikely to recur.

However, in 2002 sediment level grew 8 inches, again possibly due to another wet year.

In its USAR change, the licensee did not take into account the conditions that could

cause the ultimate heat sink to exceed the 24-inch sediment limit and make it inoperable

in less than 6.25 years (e.g., consecutive years of greater than normal precipitation).

- 25 - Enclosure

The inspectors noted that the last time the licensee actual measured sediment growth

was in about 2004.

Wolf Creek Procedure AP 26C-004, step 4.1.1, defined a deficiency as an all-inclusive

term used in reference to any condition or circumstance that reduces the confidence that

a structure, system, or component will perform satisfactorily in service. Step 6.1.3 of

the procedure required: When a potential deficiency affecting plant hardware is

identified but the impact on the ability of an structure, systems, or component to perform

its specified safety function is not known, then action shall be taken without delay to

confirm if a deficiency exists. On July 30, 2010, the inspectors brought the issue to the

attention of the control room operators and questioned the basis for continued operability

of the system. The shift manager made a log entry which stated that the licensee did not

consider this an actual operability issue, and also entered the issue into the corrective

action program as Condition Report 27080. That condition report failed to properly

identify the issue as a potential nonconforming condition per Section 4.2 of the

Regulatory Issue Summary 2005-20 Operability Guidance and take the appropriate

corrective action of determining the current sedimentation depths. The following week,

when the inspectors observed that appropriate actions still had not been taken to

address a potential safety concern, the inspectors again contacted the control room and

discussed the guidance of Regulatory Issue Summary 2005-20 Operability Guidance

with the shift manager. At that time, the shift manager took actions to make a log entry

noting the nonconformance in control room log and equipment out of service logs. She

also directed Condition Report 27080 be revised to include requirements to perform a

hydrographic survey of the ultimate heat sink intake channel to verify that sedimentation

levels were within design basis and licensing basis required limits. The hydrographic

survey was completed on August 14, 2010, and the results were verified and the

ultimate heat sink returned to service on August 29, 2010.

Analysis. The failure to implement Procedure AP 26C-004 was a performance

deficiency. The inspectors determined that this finding was more than minor because it

was associated with the equipment performance attribute of the Mitigating Systems

Cornerstone and it affected the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage). Using Inspection Manual Chapter 0609, the issue is

determined to have very low safety significance because the finding is not a design or

qualification issue confirmed not to result in a loss of operability or functionality; did not

represent an actual loss of safety function of the system or train; did not result in the loss

of one or more trains of nontechnical specification equipment; and did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

This finding has a crosscutting aspect in the area of problem identification and resolution

associated with the corrective action program component because licensee personnel

failed to identify a potential deficiency in the ultimate heat sink in a timely manner

P.1(a).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities

affecting quality shall be prescribed by documented instructions or drawings of a type

appropriate to the circumstances and shall be accomplished in accordance with these

- 26 - Enclosure

instructions or drawings. Wolf Creek Generating Station Procedure AP 26C-004,

Technical Specification Operability, step 6.1.3 required when a potential deficiency

affecting plant hardware is identified but the impact on the ability of an structure, system,

or component to perform its specified safety function is not known, then action shall be

taken without delay to confirm if a deficiency exists. Contrary to the above, from

September 2009 through July 30, 2010, the licensee failed to take action without delay

to determine if a potential deficiency existed that could have affected the operability of

the ultimate heat sink when the licensee decided to delay dredging beyond the

preventive maintenance frequency of 5 years. Because of the very low safety

significance and Wolf Creek Generating Stations action to place this issue in their

corrective action program as Condition Report 27080, this violation is being treated as

an NCV in accordance with Section VI.A.1 of the Enforcement Policy:

NCV 05000482/2010006-07, Failure to Determine if a Deficiency Existed in the Ultimate

Heat Sink.

g. Notice of Unusual Event Due to Loss of Both Emergency Diesel Generators

Introduction. The inspectors reviewed a self-revealing violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action for failure to promptly identify a degraded

equipment condition which resulted in a functional failure of the emergency diesel

generator system and a notice of unusual event emergency declaration during a

refueling outage.

Description. At 12:06 p.m. on October 22, 2009, during Refueling Outage 17 with the

reactor defueled, and the Emergency Diesel Generator B and Transformer XNB02 out of

service for planned maintenance, control room operators received an alarm indicating an

undervoltage or underfrequency condition on the Emergency Diesel Generator A.

Station operators were dispatched to the Emergency Diesel Generator A to investigate

and found that the engine had not started. At 12:08 p.m. the Emergency Diesel

Generator A was taken out of service for troubleshooting. The licensee determined that

a degraded nonsafety-related capacitor was passing ac noise beyond the filtering

capability of the dc speed switches, from the local annunciator cabinet power supply to

dc speed switches that feed into the emergency diesel generator starting circuit. As a

result the speed switches actuated, giving the control system a false indication that the

engine was running, and the appearance of undervoltage and underfrequency on the

generator. This false indication also disabled the starting capability of the engine

because the circuitry assumed the engine was already running. Therefore, the engine

would not have started as designed on a loss of offsite power.

The emergency preparedness manager reviewing the situation later observed that it met

the criteria for a notice of unusual event, and one was declared at 5:40 p.m. The repairs

to the control system were completed at 7:38 a.m. on October 23, 2009, and the notice

of unusual event was exited at 7:40 a.m.

Wolf Creek Generating Station entered this condition into the corrective action program

as Condition Report 21039 and performed an Apparent Cause Evaluation which

determined that the cause of the event was failure to implement preventive maintenance

to monitor a known potential equipment degradation of the nonsafety-related capacitor.

Electrical noise compromising the dc speed switches was first identified during

- 27 - Enclosure

troubleshooting in 1991. As a corrective action, a temporary modification (which later

became permanent) was implemented to install the nonsafety capacitor to provide the

additional noise filtration required. During routine calibration surveillance in December

2006, the dc speed switch could not be properly calibrated. At that time, the as-found

ripple voltage across the speed switch was observed to be 1.35V however it dropped to

0.2V when the ac power supply was de-energized. Both the speed switch and the

power supply were replaced and the control system began functioning within normal

parameters. The speed switch was subsequently bench tested, found to be working

properly, and returned to the warehouse for future use. However, the licensee had not

identified that the power supply was the cause of the problem; specifically, that over time

the nonsafety-related capacitor was becoming a less effective noise filter. If Wolf Creek

Generating Station personnel had properly assembled all of the information from the

2006 troubleshooting, they would have identified the capacitor degradation as the cause,

and implemented the preventive maintenance activities to monitor capacitor degradation

and replace the capacitors in time to preclude future failures of the emergency diesel

generator local control system. As part of the corrective actions of Condition

Report 21039, the licensee implemented a regular preventive maintenance activity to

monitor capacitor degradation. The licensee entered this violation into the corrective

action program as Condition Report 27077 and was evaluating the issue.

Analysis. The inspectors determined that the licensees missed opportunity to identify a

degraded equipment condition in December 2006 was a performance deficiency and is

reflective of current performance. This issue was more than minor because it was

associated with the equipment performance attribute of the Mitigating Systems

Cornerstone. Using Inspection Manual Chapter 0609, the issue is determined to have

very low safety significance because the finding is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; did not represent an actual

loss of safety function of the system or train; did not result in the loss of one or more

trains of nontechnical specification equipment; and did not screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. A crosscutting

aspect was identified in the problem identification and resolution in that the licensee did

not thoroughly evaluate problems such that the resolution addressed causes. P.1(c)

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires, in part, that measures shall be established to assure that conditions adverse to

quality, such as failures, malfunctions, deficiencies, deviations, defective material and

equipment, and nonconformances are promptly identified and corrected. Contrary to the

above, in December 2006, during troubleshooting of an apparent failure of an

emergency diesel generator speed switch, Wolf Creek failed to identify the true cause of

the engine failure. Specifically, Wolf Creek personnel failed to promptly identify that the

condition adverse to quality was a degraded nonsafety-related capacitor. As a result, on

October 22, 2009, Emergency Diesel Generator A experienced a failure and caused the

plant to declare a notice of unusual event emergency declaration. Because this violation

was determined to be of very low safety significance and was placed in the corrective

action program as Condition Report 27077, this violation is being treated as an NCV in

accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000482/2010006-08,

Notice of Unusual Event Due to Loss of Both Emergency Diesel Generators.

- 28 - Enclosure

h. Failure to Translate Design Information Into a Procedure

Introduction. The team identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, for the failure to translate criteria from the atmospheric

relief valve accumulator leakage calculation into proceduralized leakage criteria.

Specifically, engineering personnel did not translate the calculated design basis leakage

criteria and the required minimum pressure to start the test into the procedure. The

licensee entered this into the corrective action program as Condition Report 26771, and

the licensee was developing plans to revise the leakage criteria in the procedure.

Description. During a review of corrective actions associated with the atmospheric relief

valve accumulator leakage criteria, the team observed that there were previous recent

condition reports noting problems with Calculation KA-03-W, "KA system Back-up

Nitrogen Accumulators, Revision 15. Condition Report 15280 had corrective actions to

reduce the allowed leakage rate in Procedure STS KA-010, N2 Accumulator Inservice

Check Valve Test, Revision 14, from 80 psi/hour to 70 psi/hour. Revision 15 was

revised on June 9, 2010, to include a 17 psi drop in 15 minutes (i.e., equivalent to

68 psi/hour).

The team noted the design basis leakage calculation for the atmospheric relief valve

accumulator assumes a consumption rate for the air-operated valves. The licensee has

four essentially identical accumulator tanks, and each tank provides air to an

atmospheric relief valve, and an auxiliary feedwater flow valve. USAR Table 9.3-1,

provides a required bases of three atmospheric relief valve strokes per hour for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

and three auxiliary feedwater valves strokes per hour for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. The calculation

provided the valve pressure usage rates for the valves, and assumed a leakage rate out

of the system. The inspectors noted that Calculation KA-03-W included acceptance

criteria for a 65 psi/hour drop (equivalent to 16.25 psi/15 minutes), with an assumed

initial starting pressure of 700 psi would provide enough pressurized air to stroke the

valves for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. The accumulator system operates with a nominal 750 psi pressure to

the accumulator tanks and a low pressure alarm of 670 psi. The inspectors concluded

that the criteria contained in Procedure STS KA-010 was inadequate because it did not

contain the calculated design basis leakage criteria and the required minimum pressure

to start the test into the procedure. The licensee initiated Condition Report 26771 to

document the inadequate procedure revision and was developing plans to revise the

leakage criteria in the procedure.

The inspectors reviewed the results of previous surveillance tests and noted that the

leakage rate was substantially less than the assumed leakage rate of the calculation.

Subsequently, the licensee reviewed the calculation and concluded that there was no

impact on operability of the atmospheric relief valves. The inspectors reviewed the

licensees analysis and concurred with the determination.

Analysis. The inspectors determined that the licensees failure to translate design

information into procedures was a performance deficiency. This issue was more than

minor because it affected the design control attribute of the Mitigating Systems

Cornerstone and affected the objective to ensure the reliability and capability of systems

that respond to initiating events to prevent undesirable consequences. Using Inspection

Manual Chapter 0609, the issue is determined to have very low safety significance

- 29 - Enclosure

because the finding is not a design or qualification issue confirmed not to result in a loss

of operability or functionality; did not represent an actual loss of safety function of the

system or train; did not result in the loss of one or more trains of nontechnical

specification equipment; and did not screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the corrective

action program component because licensee personnel failed to take appropriate

corrective actions to previously identified problems P.1(d).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires,

in part, that measures shall be established to assure that the design basis for those

structures, systems, and components to which this appendix applies are correctly

translated into specifications, drawings, procedures, and instructions. Contrary to the

above, prior to July 30, 2010, the licensee failed to translate the design bases

requirements into adequate procedural criteria. Specifically, Procedure STS KA-010 ,

N2 Accumulator Inservice Check Valve Test, Revision 15, did not include the

calculated design basis leakage criteria and the required minimum pressure to start the

test into the procedure from Calculation KA-03-W, KA system Back-up Nitrogen

Accumulators, Revision 15. Because this violation was of very low safety significance

and it was entered into the licensees corrective action program as Condition Report

26771, this violation is being treated as an NCV consistent with Section VI.A.1 of the

Enforcement Policy: NCV 05000482/2010006-09, Failure to Translate Design

Information into a Procedure.

4OA5 Other Activities

.1 (Closed) Licensee Event Report 05000482/2009005-00: Loss of Both Diesel Generators

With All Fuel in the Spent Fuel Pool

On December 21, 2009, Wolf Creek submitted LER 2009005 which described a loss of

onsite emergency power generation capability which occurred on October 22 and 23,

2009, during Refueling Outage 17. The Emergency Diesel Generator B was out of

service for planned maintenance when the Emergency Diesel Generator A failed

unexpectedly at 12:06 p.m. on October 22, 2009. This condition resulted in a notice of

unusual event emergency declaration. The cause of the failure was actuation of the

speed switches due to degradation of the capacitor responsible for filtering out noise on

the dc input feed to the annunciators power supply. The annunciator power supply was

replaced and the Emergency Diesel Generator A returned to service at 7:38 a.m. on

October 23, 2009. Wolf Creek Generating Station determined that the root cause of this

event was failure to implement preventive maintenance activities to monitor degradation

of the capacitors. Wolf Creek Generating Station performed a hazard barrier-target

analysis as part of Apparent Cause Evaluation Condition Report 24356 and determined

that they were previously aware the potential for ac noise to adversely impact the speed

switch. Since the licensee was aware of the potential for degradation and had missed

opportunities to fully evaluate and correct the condition as recently as 2006, and

because the event resulted in a loss of diesel generator system safety function and an

emergency declaration, the inspectors determined that this event constituted a

- 30 - Enclosure

self-revealing violation of NRC requirements. Enforcement aspects are discussed in

Section 4OA2.5h. This LER is closed.

4OA6 Meetings

Exit Meeting Summary

On July 30, 2010, the inspectors presented the inspection results to Mr. M. Sunseri, President

and Chief Executive Officer, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspector asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary information

was identified.

- 31 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

S. Henry, Acting Plant Manager

S. Koenig, Manager, Corrective Action Program

B. Masters, Supervisor, Design Engineering

B. Muilenburg, Licensing Engineer

G. Pendergrass, Director, Plant Engineering

E. Peterson, Ombudsman

E. Ray, Manager, Quality Assurance

L. Rockers, Licensing Engineer

M. Sunseri, President and CEO

J. Suter, Acting Manager, Design Engineering

J. Yunk, Human Resources Manager

NRC Personnel

M. Hay, Chief, Technical Support Branch

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000482/2010006-05 VIO Failure to Perform Adequate Evaluation for Significant

Conditions (Section 4OA2.1.5e)

Opened and Closed

05000482/2010006-01 NCV Failure to Resolve Degraded Conditions in a Timely Manner

(Section 4OA2.1.5a)05000482/2010006-02 NCV Unqualified Scaffolding Erected Near Safety-Related Equipment

(Section 4OA2.1.5b)05000482/2010006-03 FIN Failure to Adequately Monitor Control Room Deficiencies

(Section 4OA2.1.5c)05000482/2010006-04 NCV Failure to Update an Operability Evaluation (Section 4OA2.1.5d)05000482/2010006-07 NCV Failure to Determine if a Deficiency Existed in the Ultimate Heat

Sink (Section 4OA2.1.5f)05000482/2010006-08 NCV Notice of Unusual Event Due to Loss of Both Emergency Diesel

Generators (Section 4OA2.1.5g)05000482/2010006-09 NCV Failure to Translate Design Information into a Procedure

(Section 4OA2.1.5h)

A-1 Attachment

LIST OF DOCUMENTS REVIEWED

CONDITION REPORTS

6347 24190 24192 24194 24187

24188 24189 27034 15402 15968

27010 26782 26752 26752 2008-005459

2008-001660 2008-004983 25709 26671 26670

26673 26672 9688 26658 26659

26306 26784 26466 18785 21127

22710 22798 22239 23446 11951

27071 9414 9728 9729 9753

9756 9812 9989 10234 10318

10327 10369 10534 10556 10643

10674 10710 11022 11297 11309

11760 12257 12321 12398 12857

12862 13021 13771 13166 13470

17144 15447 18025 18467 18497

20187 20190 20374 20380 20378

22628 22546 23446 23459 23586

25457 11487 13374 17752 22310

15521 25901 11951 24194 24196

24351 24096 25134 14112 14113

14177 14779 14827 22874 26930

26744 26744 26930 22874 14827

06107 10369 13021 18467 24194

06165 10534 13166 18497 24196

07247 10556 13374 20187 24268

07495 10643 13470 20190 24288

07930 10674 13711 20374 24336

08067 10710 13720 20378 24337

09414 11022 13771 20380 24339

09519 11297 14038 21039 24351

09728 11309 14112 21077 24356

09729 11487 14113 21775 25134

09753 11760 14177 22310 25457

2008-000865 2008-001599 15280 22127 22980

26990 26771 26773 26767 23032

24196 24351 24194 24189 24192

A-2 Attachment

CONDITION REPORTS

24197 24187 24188 24189 24190

24192 24194 24195 24351 24197

24198 24200

PROCEDURES

REVISION /

NUMBER TITLE DATE

AP 28-001 Operability Evaluations 17

AP 26C-004 Technical Specification Operability 20

AI 22A-001 Operator Work Arounds/Burdens/Control Room Deficiencies 8

AP 22-001 Conduct of Pre-Job and Post-Job Briefs 10

AP 21-001 Conduct of Operations 46

AP 22A-001 Screening, Prioritization and Pre-Approval 11

TMP 09-014 CCW Flow Balance for Trouble Shooting Thermal Barrier 0

Closure

AP 21C-001 WCGS Substation 10

SYSKJ-200 Inoperable Emergency Diesel 20

AP 22C-003 Operational Risk Assessment Program 14A

AP 28A-100 Condition Reports 12

AI 28A-010 Screening Condition Reports 5

AP 23L-001 Lake Water Systems Corrosion and Fouling Mitigation 2

Program

AP 28-011 Resolving Deficiencies Impacting SSCs 1C

AP 16C-006 MPAC Work Request/Work Order Process Controls 16

AP 23-008 Equipment Reliability Program 4

AP 16-001 Control of Maintenance 6

AI 16B-002 Updating the PM Activity Module 7

AP 26C-004 Technical Specification Operability 20

MPE NE-004 Alternator Inspection 8

AP 16B-003 Planning and Scheduling Preventive Maintenance 8

A-3 Attachment

PROCEDURES

REVISION /

NUMBER TITLE DATE

STS MT-023 Ultimate Heat Sink Dam Surveillance Vertical Movement 4

and Sedimentation

AP 10-100 Fire Protection Program 15

AP 21C-001 WCGS Substation 10

TMP 04-016 Dredging the UHS 0

AP 22C-002 Work Controls 18

STS AB-201D Atmospheric Relief Valve Inservice Valve Test 24

STS-AL-201C Turbine Driven Auxiliary Feedwater System Inservice Valve 6A

Test

STS-KA-010 N2 Accumulator Inservice Check Valve Test 15

STS-MS-070 ASME Code Testing of Safety/Relief Valves 18

WORK ORDERS

08-309413-010 10-330408-001 10-330408-008 10-330408-009 10-330408-011

09-321437-000 02236874-001 10-325888-000 10-327384-003 04-262017-000

09-318651-000 04-266919-000 06-289655-000 07-297977-000 08-305497-000

08-307922-001 09-313715-000 09-316986-000 09-317878-000 09-319258-000

09-320005-000 09-320207-000 09-320629-000 09-320688-000 09-321867-000

09-321868-000 09-321869-000 09-320688-000 09-322079-000 09-322094-000

09-322137-001 09-322467-001 09-322607-001 09-322825-000 09-322842-000

09-322843-000 09-322912-001 09-323130-000 09-323159-000 09-319153-000

PROCEDURE CHANGE REQUESTS

53032 53031 52982

OPERATIONAL BURDENS

09-OB111 09-OW101 08-CRD100

A-4 Attachment

CALCULATION REVISION /

NUMBER DATE

TITLE

KA-03-W KA System Back-Up Nitrogen Accumulators Capacity 2

Calculation

DRAWINGS

NUMBER TITLE REVISION /

DATE

M-620-00111- Nuclear Containment Cooling Coil 1W

W04

M-620-00011- Type R Coil 31 Tube Face - Carrier Replacement - 6 Row 12/12/07

W05 - 4 Pass (1 1/2 Circuit)

M-12EG03 Piping and Instrumentation Diagram Component Cooling 09

Water System

M-12EG01 Piping and Instrumentation Diagram Component Cooling 16

Water System

M-12EG02 Piping and Instrumentation Diagram Component Cooling 19

Water System

KD7496 One line diagram 37

10466-A-081- Sonicbar Door Division - Schedule and Elevation

4/14/83

0002-X04

CP 15-1-12C Vent Silencer Model AAF - Pulsco BDM 78-2 C

CP 9-1-182 3/4 40-C Regulator F

M-12AB01 Piping and Instrument Diagram Main Steam System 11

M-12AL01 Piping and Instrument Diagram Auxiliary Feedwater System 10

M-12KA05 Piping and Instrument Diagram Compressed Air System 07

M-12KH01 Piping and Instrument Diagram Service Gas System 13

A-5 Attachment

DRAWINGS

NUMBER TITLE REVISION /

DATE

M-13KA51 Small Piping Isometric N2 Back-up Gas Supply Auxiliary

01

Building

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

System Health Report Essential Service Water 01/01-

03/31/10

System Health Report Component Cooling Water 01/01-

03/31/10

APF 21-001-02 Control Room Turnover Checklist 7/16/2010

08-02-OPS Wolf Creek Quality Assurance Audit Report 3/7/2008

10-S0109 WCGS Scaffolding Request 6

2010-052 Reportability Evaluation Request 8

10-S0069 WCGS Scaffolding Request 5A

10-S0066 WCGS Scaffolding Request 5A

10-S0068 WCGS Scaffolding Request 5A

Operator Work Arounds Logs

Operator Burdens Logs

Control Room Deficiency Logs

Control Room Log 7/14-15/2010

Component Cooling Water System Open Work Orders for EG

System Correctives

2005-2525 Performance Improvement Request 6

System Health Report Essential Service Water

USAR 3.4.1.1 Flood Protection Measures for Seismic

Category I

2005-074 USAR Change Request 12/14/2005

Essential Service Water EF System Correctives

A-6 Attachment

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

10-010-EF Temporary Modification Order 00

97-00230 Altran Corporation Technical Report 96227-TR-01 2

09-005-XX Temporary Modification Order 01

Safety Monitor Profile Core Damage Frequency versus Time

2010 Work Week 213

WM06-0011 Wolf Creek Nuclear Operating Corporation Response to NRC 3/31/2006

Generic Letter 2006-02 Grid Reliability and the Impact on

Plant Risk and the Operability of Offsite Power

Safety Monitor Profile Core Damage Frequency versus Time 2

2010 Work Week 211

9301 Section 11 Assessment of Risk Resulting from Performance of 2/22/2000

Maintenance Activities

2032 Action Plan Detail Report 2/26/2009

OE-EF 09-007 Operability Evaluation Section A - Responsible Engineer 0

OE-EF 09-007 Operability Evaluation Section A - Responsible Engineer 01

OE-EF 09-007 Operability Evaluation Section A - Responsible Engineer 02

WCN005-PR-01 Enercon Project Report Analysis of Water Hammer Issues A

WCN005-PR-01 Enercon Project Report Analysis of Water Hammer Issues 0

57809 Metallurgical Failure Evaluation of a Corroded 30 Elbow 11/25/2009

from the Outlet Side of the Self-Cleaning Strainer of an ESW

Line

57652 Metallurgical Investigation of a Corroded 18 Welded Pipe, 10/27/2009

150-HBC-18 from a ESW Lake Water Line

Essential Service Water Issues Project Plan 0

CCP 9952 MSIV/MFIV Replacement (Mechanical) 14

CCP 10414 ALS MSFIS Controls Replacement 1

C-302 Specification for Suction Dredging the Ultimate Heat Sink 2

TOD No. 0300 Outage of the Benton to Wolf Creek 345 kV Line 7/17/2007

TOD No. 0301 Outage of the Rose Hill to Wolf Creek 345 kV Line 7/17/2007

TOD No. 0302 Outage of the Lacygne to Wolf Creek 345 kV Line 7/17/2007

CKL ZL-004 Turbine Building Reading Sheets 0

A-7 Attachment

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

CCP 9952 MSIV/MFIV Replacement (Mechanical) 14

CCP 10414 ALS MSFIS Controls Replacement 1

C-302 Specification for Suction Dredging the Ultimate Heat Sink 2

OE GK-08-004 Control Room AC Unit SGK04B and SGK05B Heat 0

Exchangers

OK KJ-08-005 Emergency Diesel Generator 0

Safety Culture Survey 2008

Safety Culture Survey 2010

Engineering Vent Silencer ABX0003 Deficiency 7/17/2007

Disposition,

Vendor Manual, Masoneilan 40 Series Reducing and Back Pressure

Regulator Instructions

A-8 Attachment