ML091340061
ML091340061 | |
Person / Time | |
---|---|
Site: | Wolf Creek |
Issue date: | 05/13/2009 |
From: | Vincent Gaddy NRC/RGN-IV/DRP/RPB-B |
To: | Muench R Wolf Creek |
References | |
EA-09-110 IR-09-002 | |
Download: ML091340061 (46) | |
See also: IR 05000482/2009002
Text
UNITED STATES
NUC LE AR RE G UL AT O RY C O M M I S S I O N
R E GI ON I V
612 EAST LAMAR BLVD , SU I TE 400
AR LI N GTON , TEXAS 76011-4125
May 13, 2009
Rick A. Muench, President and
Chief Executive Officer
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
SUBJECT: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION
REPORT AND NOTICE OF VIOLATION 05000482/2009002
Dear Mr. Muench:
On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at your Wolf Creek Generating Station. The enclosed integrated inspection report documents
the inspection findings, which were discussed on April 7, 2009, with Mr. Matt Sunseri,
Vice President of Operations and Plant Manager, and other members of your staff.
The inspections examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, one violation is cited in the enclosed Notice of Violation
(Notice) and the circumstances surrounding this violation are described in detail in the enclosed
report. The violation involved failure to implement corrective actions to address the repetitive
incorrect closure of valves that provide cooling to the reactor coolant pump seals (EA-09-110).
Although determined to be of very low safety significance (Green), this violation is being cited
because one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a cited
violation was satisfied. Specifically, Wolf Creek Nuclear Operating Corporation failed to restore
compliance within a reasonable time after the violation was last identified in NRC Inspection
Report 05000482/2007003-003. Please note that you are required to respond to this letter and
should follow the instructions specified in the enclosed Notice when preparing your response.
The NRC will use your response, in part, to determine whether further enforcement action is
necessary to ensure compliance with regulatory requirements.
This report also documents six NRC identified findings of very low safety significance (Green).
Five of these findings were determined to involve violations of NRC requirements. However,
because of the very low safety significance and because they are entered into your corrective
action program, the NRC is treating these findings as noncited violations, consistent with
Section VI.A.1 of the NRC Enforcement Policy. If you contest the violations or the significance
of the noncited violations, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
Wolf Creek Nuclear Operating Corporation - 2 -
ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional
Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400,
Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Wolf Creek
Generating Station. In addition, if you disagree with the characterization of any finding in this
report, you should provide a response within 30 days of the date of this inspection report, with
the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC
Resident Inspector at the Wolf Creek Generating Station. The information you provide will be
considered in accordance with Inspection Manual Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its
enclosure, will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records component of NRCs document system (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
Public Electronic Reading Room).
Sincerely,
/RA/
Vincent G. Gaddy, Chief
Project Branch B
Division of Reactor Projects
Docket No. 50-482
License No. NPF-42
Enclosures: Notice of Violation and
NRC Inspection Report 05000482/2009002
w/attachment: Supplemental Information
cc w/enclosure:
Vice President Operations/Plant Manager
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
Jay Silberg, Esq.
Pillsbury Winthrop Shaw Pittman LLP
2300 N Street, NW
Washington, DC 20037
Supervisor Licensing
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
Wolf Creek Nuclear Operating Corporation - 3 -
Chief Engineer
Utilities Division
Kansas Corporation Commission
1500 SW Arrowhead Road
Topeka, KS 66604-4027
Office of the Governor
State of Kansas
Topeka, KS 66612-1590
Attorney General
120 S.W. 10th Avenue, 2nd Floor
Topeka, KS 66612-1597
County Clerk
Coffey County Courthouse
110 South 6th Street
Burlington, KS 66839
Chief, Radiation and Asbestos
Control Section
Bureau of Air and Radiation
Kansas Department of Health and
Environment
1000 SW Jackson, Suite 310
Topeka, KS 66612-1366
Chief, Technological Hazards Branch
REMA Region VII
9221 Ward Parkway
Suite 300
Kansas City, MO 64114-3372
Wolf Creek Nuclear Operating Corporation - 4 -
Electronic distribution by RIV:
Regional Administrator (Elmo.Collins@nrc.gov)
Deputy Regional Administrator (Chuck.Casto@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)
DRP Deputy Director (Anton.Vegel@nrc.gov)
DRS Director (Roy.Caniano@nrc.gov)
DRS Deputy Director (Troy.Pruett@nrc.gov)
Senior Resident Inspector (Chris.Long@nrc.gov)
Site Secretary (Shirley.Allen@nrc.gov)
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)
Senior Project Engineer, DRP/B (Rick,Deese@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
Regional State Liaison Officer (Bill.Maier@nrc.gov)
NSIR/DPR/EP (Steve.LaVie@nrc.gov)
Senior Enforcement Specialist (Mark.Haire@nrc.gov)
Only inspection reports to the following:
OEDO RIV Coordinator, (John.Adams@nrc.gov)
ROPreports
R:\_REACTORS\_WC\2009\WC 2009-002 RP CML-vgg ADAMS.doc ADAMS ML091340061
SUNSI Rev Compl. : Yes No ADAMS : Yes No Reviewer Initials VGG
Publicly Avail : Yes No Sensitive Yes : No Sens. Type Initials VGG
SRI:DRP/B SPE:DRP/B C:DRS/EB1 C:DRS/EB2 C:DRS/OB
CMLong RDeese TFarnholtz NOkeefe RELantz
/RA/ /RA/ /RA/ /RA/ /RA/
4/27/09 5/4/09 5/5/09 5/5/09 5/5/09
C:DRS/PSB C:DRS/BC ACES C/DRP/B
MPShannon GWerner MHaire VGGaddy
/RA/ /RA/ /RA/ /RA/
5/7/09 5/7/09 4/28/09 5/13/09
OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax
NOTICE OF VIOLATION
Wolf Creek Nuclear Operating Corporation Docket: 50-482
Wolf Creek Plant Generating Station License: NPF-42
During an NRC inspection conducted December 10, 2008, through March 31, 2009, a violation
of NRC requirements was identified. In accordance with the NRC Enforcement Policy, the
violation is listed below:
Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part,
that measures shall be established to assure that conditions adverse to quality, such as
failures, malfunctions, deficiencies, deviations, defective material and equipment, and
nonconformances are promptly identified and corrected.
Contrary to the above, from 2001 through March 31, 2009, the licensee failed to
establish measures to assure that conditions adverse to quality are promptly identified
and corrected. Specifically, the licensee failed to identify the adverse condition of and to
take corrective action for the repetitive, inappropriate closure of the reactor coolant pump
thermal barrier heat exchanger valves, inappropriate closure of the downstream
component cooling water containment isolation valves, and inappropriate circuit
breakers opening associated with the above thermal barrier valves.
This violation is associated with a Green Significance Determination Process finding.
Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Corporation is
hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the
Regional Administrator, Region IV, and a copy to the NRC Senior Resident Inspector at the
facility that is the subject of this Notice of Violation (Notice), within 30 days of the date of the
letter transmitting this Notice. This reply should be clearly marked as a "Reply to Notice of
Violation EA-09-110," and should include: (1) the reason for the violation, or, if contested, the
basis for disputing the violation or severity level, (2) the corrective steps that have been taken
and the results achieved, (3) the corrective steps that will be taken to avoid further violations,
and (4) the date when full compliance will be achieved. Your response may reference or include
previous docketed correspondence, if the correspondence adequately addresses the required
response. If an adequate reply is not received within the time specified in this Notice, an Order
or a Demand for Information may be issued as to why the license should not be modified,
suspended, or revoked, or why such other action as may be proper should not be taken. Where
good cause is shown, consideration will be given to extending the response time.
If you contest this enforcement action, you should also provide a copy of your response, with the
basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory
Commission, Washington, DC 20555-0001.
Because your response will be made available electronically for public inspection in the NRC
Public Document Room or from the NRCs document system (ADAMS), accessible from the
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not
include any personal privacy, proprietary, or safeguards information so that it can be made
available to the public without redaction. If personal privacy or proprietary information is
necessary to provide an acceptable response, then please provide a bracketed copy of your
-1- Enclosure
response that identifies the information that should be protected and a redacted copy of your
response that deletes such information. If you request withholding of such material, you must
specifically identify the portions of your response that you seek to have withheld and provide in
detail the bases for your claim of withholding (e.g., explain why the disclosure of information will
create an unwarranted invasion of personal privacy or provide the information required by
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
information. If safeguards information is necessary to provide an acceptable response, please
provide the level of protection described in 10 CFR 73.21.
Dated this __13th__ day of May 2009
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket: 50-482
License: NPF-42
Report: 05000482/2009002
Licensee: Wolf Creek Nuclear Operating Corporation
Facility: Wolf Creek Generating Station
Location: 1550 Oxen Lane SE
Burlington, Kansas
Dates: January 1 through March 31, 2009
Inspectors: C. Long, Senior Resident Inspector
B. Tindell, Resident Inspector, Comanche Peak
P. Elkmann, Senior Emergency Preparedness Specialist
P. Jayroe, Project Engineer
M. Hayes, Reactor Inspector, Project Engineer
Approved By: V. G. Gaddy, Chief, Project Branch B
Division of Reactor Projects
-1- Enclosure
SUMMARY OF FINDINGS
IR 05000482/2009002; 1/01 - 3/31/2009; Wolf Creek Generating Plant, Integrated Resident and
Regional Report; Adverse Weather, Fire Protection, Maintenance Effectiveness, Surveillance
Testing, Problem Identification and Resolution, Other Activities.
The report covered a 3-month period of inspection by resident inspectors and an announced
baseline inspection and by regional based inspectors. Five Green noncited violations, one
Green finding, and one Green cited violation were identified. The significance of most findings
is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609,
Significance Determination Process. Findings for which the significance determination
process does not apply may be Green or be assigned a severity level after NRC management
review. The NRC's program for overseeing the safe operation of commercial nuclear power
reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated
December 2006.
A. NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Initiating Events
- Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,
Criterion XVI, Conditions Adverse to Quality, involving Wolf Creeks failure to
correct the cause of the reactor coolant pump thermal barrier component cooling
water heat exchanger outlet valves stroking closed on high flow. Specifically,
between 2001 and 2009, Wolf Creek experienced repeated cases of the reactor
coolant pump thermal barrier component cooling water heat exchanger outlet
valves stroking closed during component cooling water pump swaps and during
isolations of the radioactive waste evaporators. Wolf Creek reinitiated evaluation
of the issue after the inspectors questions but did not review the impact on the
operators ability to open the valves given the valves circuit breakers opening.
Repeated throttle valve adjustments have not been successful in stopping the
valve closures. Wolf Creek has corrective action pending to modify valve
circuitry but it has not been implemented. This issue is being tracked by the
licensee as Condition Report 2009-02074.
The failure to correct a condition adverse to quality of ensuring reactor coolant
pump seal cooling as described in the Updated Safety Analysis Report is a
performance deficiency. The finding is more than minor because it is associated
with the equipment performance attribute for the Initiating Events Cornerstone;
and, it affected the cornerstone objective to limit the likelihood of those events
that upset plant stability and challenge critical safety functions during shutdown
as well as power operations. The finding was determined to be of very low safety
significance because the finding would not result in exceeding the Technical
Specification limit for identified reactor coolant system leakage and would not
have affected other mitigation systems resulting in a total loss of the seal cooling
safety function. This finding is being cited because the licensee failed to
establish measures to assure this condition adverse to quality was promptly
identified and corrected. This finding has a crosscutting aspect in the area of
human performance associated with the decision making component because,
even though numerous instances of valve closures occurred since the first
-1- Enclosure
noncited violation, Wolf Creek downgraded the condition report. Using
nonconservative assumptions, the licensee consistently viewed this issue as not
having a risk impact because seal injection was not simultaneously lost [H.1 ( b)]
(Section 4OA2).
Cornerstone: Mitigating Systems
- Green. The inspectors identified a finding for allowing low room temperature to
cause a boric acid flow path to be inoperable. The inspectors reviewed a
Performance Improvement Request from 2005, which identified that boric acid
could decrease below its limits if the room cooler was started while lake
temperature was low which would render the system inoperable. The inspectors
reviewed operator logs of safety injection Room A temperature data and found an
instance where room temperature had decreased below the solubility limit for
boric acid which had not been noted by operators. The licensee entered this
issue into their corrective action programs as Condition Reports 2009-00516 and
2009-0145.
The failure to implement the heat tracing corrective action within 3 years to
maintain the boric acid injection piping operable during the winter is a
performance deficiency. The inspectors determined that this finding was more
than minor because this issue aligned with Inspection Manual Chapter 0612,
Appendix E, example 2.f because the heat tracing was required by Condition
Reports 2005-3461 and 2007-2472 but was not installed and the room
temperature dropped below the boron solubility limit. The inspectors evaluated
the significance of this finding using Phase 1 of Inspection Manual Chapter 0609,
Appendix G, Attachment 1, Checklist 3, and determined that the finding was of
very low safety significance because Wolf Creek maintained shutdown margin in
compliance with its Technical Specifications. No violation of regulatory
requirements occurred. The inspectors determined that this finding has a cross
cutting aspect in the area of human performance associated with the resources
component because Wolf Creek did not maintain long term plant safety by not
correcting this long term (3 years) equipment issue and its compensatory
measure with the boric acid system H.1.a] (Section 1R01).
- Green. The inspectors identified a noncited violation of License
Condition 2.C(5)(a) for a degraded fire seal that separated redundant safe
shutdown equipment. Specifically, a silicone foam seal and ceramic fiber board
separating redundant motor-driven auxiliary feedwater trains was degraded so
that it no longer provided a 3-hour rated fire barrier. The licensee entered the
finding into their corrective action program as Condition Report 2009-001087.
The finding was more than minor because it was similar to example 2.e. of NRC
Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues, in
that, the performance deficiency impacted the ability of the seal to perform its
function. In addition, the performance deficiency was associated with the
Mitigating Systems cornerstone attribute of Protection Against External Events,
and affected the cornerstone objective to ensure the reliability of systems that
respond to Initiating Events to prevent undesirable consequences. Under NRC
Inspection Manual Chapter 0609, Appendix F, Attachment 2, Degradation
Rating Guidance Specific to Various Fire Protection Program Elements the
-2- Enclosure
finding was associated with a Moderate B degradation due to the seal not being
in a tested or evaluated condition. Using Appendix F, Supplemental Screening
for Fire Confinement Findings, the finding screens as Green due to exposing fire
Area A33 featuring an automatic full area water-based suppression system. The
inspectors determined that this finding has a crosscutting aspect in the area of
problem identification and resolution associated with the corrective action
program component because Wolf Creek failed to identify the degraded seal and
missing ceramic board during previous post waterhammer walkdowns P.1.a]
(Section 1R05).
- Green. On February 6, 2009, the inspectors identified a noncited violation of 10
CFR 50 Appendix B, Criterion XI, Test Control for a procedure that allowed
unacceptable preconditioning of the control rods prior to Technical Specification
Surveillance 3.1.4.2. Wolf Creek did not perform any preconditioning
acceptability review when adopting operating experience and revising Procedure
STS SF-001. The licensee entered this issue into their corrective action
programs as Condition Report 2009-00598.
Unacceptable preconditioning of the control rods is a performance deficiency.
The finding was more than minor because it was associated with the equipment
performance attribute of the mitigating systems cornerstone, and it affected the
cornerstone objective to ensure the availability, reliability, and capability of
systems that respond to initiating events to prevent undesirable consequences.
The inspectors evaluated the significance of this finding under the mitigating
systems cornerstone using Phase 1 of Inspection Manual Chapter 0609.04,
Phase 1 - Initial Screening and Characterization of Findings, and determined
that the finding was of very low safety significance (Green) because, it did not
represent an actual loss of safety function and did not screen as potentially risk
significant due to a seismic, flooding, or severe weather initiating event. This
finding was determined to have a crosscutting aspect in the area of problem
identification and resolution associated with the corrective action program
because the condition report that adopted the operating experience failed to
evaluate NRC guidance regarding preconditioning during surveillance testing
which should have disallowed the procedure change. Therefore, the applicable
procedures were not complete and accurate P.1(c) (Section 1R22).
- Green. A self-revealing noncited violation of Technical Specification 5.4.1(a) was
identified when an on-duty operations shift manager was observed to be
inattentive on multiple occasions in 2004 and 2005. This limited his ability to
monitor the safe operation of the plant, assist the control room supervisor with
the control room command function, and respond in the event of an accident.
The licensee entered this issue into the corrective action program as Condition
Report 2008-000572.
The failure of the shift manager to remain attentive is considered a performance
deficiency. This finding is more than minor because it adversely impacts the
Human Performance attribute of the Mitigating Systems cornerstone, and if left
uncorrected this performance deficiency has the potential to lead to a more
significant safety concern because the shift manager plays an important role in
the oversight of post-accident response by all licensed operators on shift. This
issue was reviewed by NRC management using Inspection Manual Chapter 609,
-3- Enclosure
Appendix M, Significance Determination Process Using Qualitative Criteria. NRC
management reviewed the qualitative factors involved with this finding and
determined that this finding is Green. No crosscutting aspect was identified
because the shift manager has not stood watch for several years, and therefore
this issue was not considered current performance (Section 4OA5).
Cornerstone: Barrier Integrity
- Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a, Procedures, for failure to follow Procedure AP 12-003, Foreign Material
Exclusion. On January 17, 2009, inspectors conducted a walkdown of the spent
fuel pool area and found numerous untracked tools and other equipment inside
the fuel pool area. Inspectors also found duct tape attached to various fueling
and control rod tools such that duct tape was above and below the water.
Condition Report 2009-001388 was initiated identifying a loss of spent fuel pool
foreign material control. Subsequently, Wolf Creek began re-inventorying all
materials in the spent fuel pool area.
The inspectors determined that the failure to implement multiple steps of
Procedure AP 12-003 was a performance deficiency. This finding is more than
minor because it impacted the Barrier Integrity cornerstone attribute of
configuration control and affected the cornerstone objective to maintain
functionality of the spent fuel pool system. Using Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this
finding was determined be of very low safety significance because the finding -
only affected the barrier function of the spent fuel pool. This finding has a
crosscutting aspect in the area of human performance associated with the work
practices component because even though personnel had been made aware of
Wolf Creeks policy on procedure use and adherence through site-wide
communications, personnel still failed to follow numerous parts of the procedure,
such that Wolf Creek was not using the procedure H.4.b] (Section 1R05).
- Green. On February 25, 2009, the inspectors identified a noncited violation of
10 CFR 50.65 a(2), the Maintenance Rule, for failure to demonstrate that the
performance of a containment isolation valve was effectively controlled through
the performance of preventive maintenance such that the valve remained
capable of performing its intended function. An inadequate Maintenance Rule
evaluation was performed after a containment isolation valve (SJHV0005)
exceeded its Maintenance Rule a(2) performance criteria, and as a result goal
setting and monitoring were not performed as required by paragraph a(1) of the
Maintenance Rule. This issue was entered into the licensees corrective action
program as Condition Report 2009-001667.
The failure to follow 10 CFR 50.65 a(2) and properly evaluate the failed valve,
establish performance goals, and monitor its performance is considered a
performance deficiency. Per Inspection Manual Chapter 0612, Appendix E,
Section 7, this finding is more than minor because failure to demonstrate
effective control of performance or condition and not putting the affected
structures, systems, and components in (a)(1) necessarily involves degraded
structures, systems, or components performance or condition. Under NRC
Inspection Manual Chapter 0609.04, the Phase I Significance Screening
-4- Enclosure
Process, it was found that the finding is of very low safety significance because it
does not represent an actual open pathway in the physical integrity of the reactor
containment. This finding was determined to have a crosscutting aspect in the
area of problem identification and resolution associated with the corrective action
program because the licensee failed to properly classify, prioritize, and evaluate
a condition adverse to quality P.1.c] (Section 1R12).
-5- Enclosure
REPORT DETAILS
Summary of Plant Status
The plant started the inspection period at 100 percent rated thermal power and remained there
until March 27, 2009, when two of three 345 kV power lines were lost. Reactor power was
subsequently reduced to 80 percent. Wolf Creek returned to full power on March 30, 2009,
when two of the 345 kV lines were restored and breaker 345-110 could be isolated for repairs.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and
1R01 Adverse Weather Protection (71111.01)
.1 Readiness for Seasonal Extreme Weather Conditions
a. Inspection Scope
The inspectors performed a review of the licensees adverse weather procedures for
seasonal extremes (e.g., extreme high temperatures, extreme low temperatures, or
hurricane season preparations). The inspectors verified that weather-related equipment
deficiencies identified during the previous year were corrected prior to the onset of
seasonal extremes; and evaluated the implementation of the adverse weather
preparation procedures and compensatory measures for the affected conditions before
the onset of, and during, the adverse weather conditions
During the inspection, the inspectors focused on plant-specific design features and the
licensees procedures used to mitigate or respond to adverse weather conditions.
Additionally, the inspectors reviewed the Updated Safety Analysis Report and
performance requirements for systems selected for inspection, and verified that operator
actions were appropriate as specified by plant-specific procedures. Specific documents
reviewed during this inspection are listed in the attachment. The inspectors also
reviewed corrective action program items to verify that the licensee was identifying
adverse weather issues at an appropriate threshold and entering them into their
corrective action program in accordance with station corrective action procedures. The
inspectors reviews focused specifically on the following plant systems:
- February 2, 2009, insufficient essential service water warming line temperature,
and February 3, 2009, boric acid system piping temperature
These activities constitute completion of one readiness for seasonal adverse weather
sample as defined in IP 71111.01-05.
b. Findings
Introduction. On January 27, 2009, the inspectors identified a Green finding for allowing
low room temperature to challenge the boric acid flow path due to an uninstalled
-6- Enclosure
Description. On January 27, 2009, the inspectors walked down the safety injection
pump Room A and noted a temporary modification of heat tracing partially installed on
boric acid piping. The inspectors reviewed the temporary modification documentation
and found that Wolf Creek had written Performance Improvement Request 2005-3461 in
December 2005, which identified that if the safety injection pump and the room coolers
were started while lake temperature was low, the room temperature may decrease below
the boric acid solubility limit and that compensatory actions may be needed. The boric
acid system provided reactivity control for emergency boration and boration to hot and
cold shutdown conditions. On February 3, 2009, the inspectors questioned the ability to
accomplish boration during cold weather with incomplete heat tracing. The inspectors
reviewed several years of operator logs of safety injection Room A room temperature
data and found that on March 26, 2008, room temperature decreased to 59.5°F, which is
below the solubility limit for boric acid. On March 24 and 26, 2008, boric acid
concentration determinations were completed for boric acid Tanks A and B and found
that their concentrations were 7530 parts per million and 7680 parts per million,
respectively. The inspectors also reviewed Procedure SYS BG-206, Boric Acid System
Operation, and found that the solubility limit for a 7680 parts per million boric acid
solution was 63°F. Logs taken on March 27, 2008 recorded temperature at 67°F.
Control room operators did not note any deficiencies in STS CR 002, Shift Log Modes
4, 5, and 6, for March 26 or 27, 2008. The inspectors reviewed logs, condition reports,
and risk assessments but could not locate any deficiencies or corrective actions for the
several hours that the boric acid system was inoperable. However, the inspectors found
that during March 26, 2008, the refueling water storage tank was operable and could
have performed the reactivity control function. Wolf Creek was in Mode 6 for Refueling
Outage 16 at this time.
The inspectors reviewed the corrective action history for heat tracing temporary
Modification 07-012-BG. The inspectors reviewed Condition Report 2005-3461 and
found that it was continued under Condition Report 2007-2472. Condition
Report 2007-2472 created Corrective Action 4222 which was to plan and install this
temporary modification. The temporary modification installation work order began on
October 29, 2008. The inspectors found the modification partially installed on
January 27, 2009, and completed on February 9, 2009. Condition Report 2007-2472
also had corrective action to issue guidance to operators taking temperature readings in
the safety injection pump Room A. This guidance was implemented on December 19,
2008, and it instructed operators that the boric acid piping may become inoperable due
to precipitation, if room temperature drops below 67 degrees Fahrenheit.
Analysis. The failure to implement the heat tracing corrective action within 3 years to
maintain the boric acid injection piping operable during the winter is a performance
deficiency. Traditional enforcement does not apply since there were no actual safety
consequences or potential for impacting the NRCs regulatory function, and the finding
was not the result of any willful violation of NRC requirements or Wolf Creek procedures.
The inspectors determined that this finding was more than minor because this issue
aligned with Inspection Manual Chapter 0612, Appendix E, example 2.f because the
heat tracing was required by Condition Report 2007-2472 but it was not installed and the
room temperature dropped below the boron solubility limit on March 26, 2008. The
inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual
Chapter 0609, Appendix G, Attachment 1, Checklist 3, and determined that the finding
was of very low safety significance because Wolf Creek maintained shutdown margin in
compliance with its Technical Specifications. The inspectors determined that this finding
-7- Enclosure
has a cross cutting aspect in the area of human performance associated with the
resources component because Wolf Creek did not maintain long-term plant safety by not
correcting this long-term (3 years) equipment issue and its compensatory measure with
the boric acid system H.1.a].
Enforcement. No violation of regulatory requirements occurred because Wolf Creek still
had one boron injection subsystem available and complied with its Technical
Specifications on March 26, 2008. This finding was of very low safety significance and
the issue was addressed in Wolf Creeks corrective action program as Condition
Reports 2009-000516 and 2009-001495. FIN 05000482/2009002-01, untimely
corrective actions result in room temperature below boric acid solubility limit.
.2 Readiness for Impending Adverse Weather Conditions
a. Inspection Scope
Since thunderstorms with potential tornados and high winds were forecast in the vicinity
of the facility for March 23, 2009, the inspectors reviewed the licensees overall
preparations and protection for the expected weather conditions. On March 23, 2009,
the inspectors walked down the emergency diesel generators and the transformer yard
because their safety-related functions could be affected or required as a result of high
winds or tornado-generated missiles or the loss of offsite power. The inspectors
evaluated the licensee staffs preparations against the sites procedures and determined
that the staffs actions were adequate. During the inspection, the inspectors focused on
plant-specific design features and the licensees procedures used to respond to
specified adverse weather conditions. The inspectors also toured the plant grounds to
look for any loose debris that could become missiles during a tornado. The inspectors
evaluated operator staffing and accessibility of controls and indications for those
systems required to control the plant. Additionally, the inspectors reviewed the Updated
Safety Analysis Report and performance requirements for systems selected for
inspection, and verified that operator actions were appropriate as specified by plant-
specific procedures. The inspectors also reviewed a sample of corrective action
program items to verify that the licensee identified adverse weather issues at an
appropriate threshold and dispositioned them through the corrective action program in
accordance with station corrective action procedures. Specific documents reviewed
during this inspection are listed in the attachment.
These activities constitute completion of one readiness for impending adverse weather
condition sample as defined in IP 71111.01-05.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignments (71111.04)
.1 Partial Walk downs
a. Inspection Scope
The inspectors performed partial equipment walkdowns of the following risk significant
systems:
-8- Enclosure
- January 7, 2009, Auxiliary Feedwater Train B while Train A auxiliary feedwater
out of service for preventive maintenance
- January 27, 2009, Safety Injection Train A while Train B safety injection out of
service for preventive maintenance
- March 11, 2009, Emergency Diesel Generator B auxiliaries while Emergency
Diesel Generator A out of service for preventive maintenance
The inspectors selected these systems based on their risk significance relative to the
Reactor Safety cornerstones at the time they were inspected. The inspectors attempted
to identify any discrepancies that could affect the function of the system, and, therefore,
potentially increase risk. The inspectors reviewed applicable operating procedures,
system diagrams, Updated Safety Analysis Report, Technical Specification requirements,
administrative Technical Specifications, outstanding work orders, condition reports, and
the impact of ongoing work activities on redundant trains of equipment in order to identify
conditions that could have rendered the systems incapable of performing their intended
functions. The inspectors also walked down accessible portions of the systems to verify
system components and support equipment were aligned correctly and operable. The
inspectors examined the material condition of the components and observed operating
parameters of equipment to verify that there were no obvious deficiencies. The
inspectors also verified that the licensee had properly identified and resolved equipment
alignment problems that could cause Initiating Events or impact the capability of
Mitigating Systems or Barriers and entered them into the corrective action program with
the appropriate significance characterization. Specific documents reviewed during this
inspection are listed in the attachment.
These activities constitute completion of three partial system walk down samples as
defined in IP 71111.04-05.
b. Findings
No findings of significance were identified.
.2 Semi-Annual Complete System Walk down
a. Inspection Scope
On February 25, 2009, the inspectors performed a complete system alignment
inspection of the auxiliary feedwater system to verify the functional capability of the
system. The inspectors selected this system because it was considered both safety
significant and risk significant in the licensees probabilistic risk assessment. The
inspectors walked down the system to review mechanical and electrical equipment
lineups, electrical power availability, system pressure and temperature indications, as
appropriate, component labeling, component lubrication, component and equipment
cooling, hangers and supports, operability of support systems, and to ensure that
ancillary equipment or debris did not interfere with equipment operation. The inspectors
reviewed a sample of past and outstanding work orders to determine whether any
deficiencies significantly affected the system function. In addition, the inspectors
reviewed the corrective action program database to ensure that system equipment
alignment problems were being identified and appropriately resolved. Specific
documents reviewed during this inspection are listed in the attachment.
-9- Enclosure
These activities constitute completion of one complete system walk down sample as
defined by IP 71111.04-05.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1 Quarterly Fire Inspection Tours
a. Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability,
accessibility, and the condition of firefighting equipment in the following risk significant
plant areas:
- January 16, 2009, motor-driven auxiliary Feedwater B and 1989 pipe chase
- March 31, 2009, central alarm station cable penetrations, Area C29
- March 31, 2009, lower cable spreading room, Area C21
- January 16, 2009, spent fuel pool area 2047
The inspectors reviewed areas to assess if licensee personnel had implemented a fire
protection program that adequately controlled combustibles and ignition sources within
the plant; effectively maintained fire detection and suppression capability; maintained
passive fire protection features in good material condition; and had implemented
adequate compensatory measures for out of service, degraded or inoperable fire
protection equipment, systems, or features, in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk
as documented in the plants Individual Plant Examination of External Events with later
additional insights, their potential to affect equipment that could initiate or mitigate a plant
transient, or their impact on the plants ability to respond to a security event. Using the
documents listed in the attachment, the inspectors verified that fire hoses and
extinguishers were in their designated locations and available for immediate use; that
fire detectors and sprinklers were unobstructed; that transient material loading was
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition. The inspectors also verified that minor issues identified
during the inspection were entered into the licensees corrective action program.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of four quarterly fire protection inspection samples
as defined in IP 71111.05-05.
b. Findings
.1 Introduction. The inspectors identified a Green noncited violation of License
Condition 2.C(5)(a) for a degraded fire seal that separated redundant safe shutdown
equipment.
Description. On January 17, 2009, while touring Fire Area A13, the inspectors observed
a degraded silicone fire seal for a mechanical penetration in the motor-driven auxiliary
feedwater Pump B floor. Specifically, a silicone foam and ceramic fiber board seal
-10- Enclosure
separating redundant motor-driven auxiliary feedwater trains was degraded so that it no
longer provided a 3-hour rated fire barrier. The seal separated the pump room from fire
Area A33 below, which contained motor-driven auxiliary feedwater Train A equipment.
The inspectors could feel air moving through the seal, indicating that the seal had
separated from the pipe for the entire depth of the seal. Further walkdowns revealed a
portion of the ceramic fiber damming board was missing from the bottom of the
penetration. When notified by the inspectors, the licensee initiated Work
Order 09-313747-000, Breach Permit No. 2009-018, Condition Report 2009-001087,
and compensatory actions for the degraded seal.
Procedure M-663-00017, Penetration Seal Typical Details, Revision W20, provides
design information for installation and inspection of the seals. Detail drawing and limiting
parameters for a M-1 seal specified a one inch thick damming board and an air tight seal
in the required 3-hour rated configuration. Therefore, the inspectors concluded that the
seal would fail to provide the required 3-hour protection from a fire.
The inspectors determined that the degradation was not typical due to a walkdown of
similar seals and by reviewing the licensees seal inspection documentation. The pipe in
the penetration, part of the essential service water system, experienced a water hammer
event on April 7, 2008, which was considered to be the most likely cause of the damage
to the seal. The licensee performed a walkdown of the system following the event and
failed to identify this damage.
Analysis. The failure of the fire seal to have been in the required configuration, which
resulted in a degradation of the 3-hour fire barrier between redundant motor-driven
auxiliary feedwater trains, was a performance deficiency. The finding was more than
minor because it was similar to Not minor if section of example 2.e. of NRC Inspection
Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that, the performance
deficiency impacted the ability of the seal to perform its function. In addition, the
performance deficiency was associated with the Mitigating Systems cornerstone
attribute of Protection Against External Events, and affected the cornerstone objective to
ensure the reliability of systems that respond to Initiating Events to prevent undesirable
consequences. Using NRC Inspection Manual Chapter 0609, Appendix F,
Attachment 2, Degradation Rating Guidance Specific to Various Fire Protection
Program Elements, under Fire Barrier Degradation, Table A2.2, the finding was
associated with a Moderate B degradation due to the seal not being in a tested or
evaluated condition. Using NRC Inspection Manual Chapter 0609, Appendix F, Fire
Protection Significance Determination Process, in supplemental screening for fire
confinement findings, the finding screens as Green due to exposing Fire Area A33
featuring an automatic full area water-based suppression system. The inspectors
determined that this finding has a crosscutting aspect in the area of problem
identification and resolution associated with the corrective action program component
because Wolf Creek failed to identify the degraded seal and missing ceramic board
during previous post waterhammer walkdowns. P.1.a]
Enforcement. Wolf Creek License Condition 2.C.(5)(a) requires, in part, that the licensee
maintain in effect all provisions of the approved fire protection program. The Wolf Creek
Fire Protection Program, as documented, in part, by the Updated Safety Analysis
Report, Revision 22, Table 9.5A-1, Section D.1.(j), states that where fire barriers are
provided to separate redundant safe shutdown trains, piping penetrations are sealed to
provide a fire resistance rating of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. Contrary to the above, floor penetration
-11- Enclosure
Seal OP135S0214, which separates redundant safe shutdown trains of motor-driven
auxiliary feedwater, was degraded such that it would not provide a fire resistance rating
of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> on January 17, 2009. Since the violation was of very low safety significance
and was documented in the licensees corrective action program as Condition
Report 2009-001087, it is being treated as a noncited violation, consistent with Section
VI.A of the NRC Enforcement Policy: NCV 05000482/2009002-02, degraded fire barrier
for auxiliary feedwater.
.2 Introduction. On January 17, 2009, inspectors identified a Green noncited violation of
Technical Specification 5.4.1.a, Procedures, for failure to follow AP 12-003, Foreign
Material Exclusion. Wolf Creek failed to follow multiple sections of this procedure.
Description. On January 17, 2009, inspectors conducted a walkdown of the spent fuel
pool area and found numerous tools and equipment inside the fuel pool area. Inspectors
found duct tape, air hoses running across the boundaries, plastic sheeting, ropes, tools,
a toolbox, cameras, and extension cords. Inspectors also found duct tape attached to
various fueling and control rod tools such that duct tape was above and below the water.
Inspectors questioned Wolf Creek regarding the spent fuel pool area material tracking
practices. Inspectors reviewed Procedure AP 12-003, Foreign Material Exclusion,
Revision 6. The area surrounding the spent fuel pool is posted as a foreign material
exclusion area, a contaminated area, and a hot particle area. Procedure AP 12-003
requires the highest level of foreign material accountability or Level 1 for the spent fuel
pool. Level 1 requires several actions: all materials in the area to be described; all
materials are logged in and out; logs specify how material was removed; logs identify the
person writing on the log itself; and track the pages of the log itself.
Inspectors reviewed the spent fuel pool area logs and found that the logs were
inadequate because Wolf Creek failed to log material in, log material out, state who
logged material out, state how the material was removed, and track the log sheets
themselves. Numerous pieces of duct tape, including that on fueling and control rod
manipulation tools, were not on the logs. Wolf Creek subsequently initiated Condition
Report 2009-000319 which identified the issue as housekeeping problems associated
with the spent fuel pool area. Wolf Creek began cleaning the area and reconciling the
material inside the area with the material logs during the week of January 26, 2009. On
January 30, 2009, Wolf Creek initiated Condition Report 2009-000485 which stated that
foreign material tracking was an ongoing problem. On March 19, 2009, based on
questions from the inspectors, Condition Report 2009-001388 was initiated identifying a
loss of spent fuel pool foreign material control. Using the requirements in Procedure AP
12-003, the inspectors found that Wolf Creek did not have a foreign material exclusion
area Level 1 plan and had not initiated actions for a loss of foreign material exclusion
area control due to the numerous log deficiencies. Subsequently, Wolf Creek again
began re-inventorying all materials in the spent fuel pool area. Inspectors did not identify
a sufficient amount of material to challenge the evaluated combustible loading
calculation.
Analysis. The inspectors determined that the failure to implement multiple steps of
Procedure AP 12-003 was a performance deficiency. Traditional enforcement does not
apply since there were no actual safety consequences or potential for impacting the
NRC's regulatory function, and the finding was not the result of any willful violation of
NRC requirements or Wolf Creek procedures. This finding is more than minor because it
impacted the barrier integrity cornerstone attribute of configuration control and affected
-12- Enclosure
the cornerstone objective to maintain functionality of the spent fuel pool system. Using
Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,
this finding was determined be of very low safety significance because the finding only
affected the barrier function of the spent fuel pool. The inspectors determined that this
finding has a crosscutting aspect in the area of human performance associated with the
work practices component because even though personnel had been made aware of
Wolf Creeks policy on procedure use and adherence through site-wide communications,
personnel still failed to follow numerous parts of the procedure, such that Wolf Creek
was not using the procedure. H.4.b]
Enforcement. Technical Specification 5.4.1.a requires the implementation of written
procedures described in Regulatory Guide 1.33, Revision 2, Appendix A, including
procedures for performing maintenance that can affect the performance of safety-related
equipment. Procedure AP 12-003, Foreign Material Exclusion, Revision 6, requires
that spent fuel pool work comply with theses requirements. Contrary to the above, prior
to March 19, 2009, the licensee failed to adequately implement Procedure AP 12-003 for
spent fuel pool work activities. Specifically, Procedure AP 12-003, was not implemented
and resulted in failure to account for foreign material in the spent fuel pool and the spent
fuel pool exclusion area. Because this violation was determined to be of very low safety
significance and was placed in the corrective action program as Condition
Reports 2009-000319, 2009-000485, and 2009-001388, this violation is being treated as
a noncited violation in accordance with Section VI.A.1 of the Enforcement Policy:
NCV 05000482/2009002-03, failure to implement foreign material exclusion control
procedure for spent fuel pool.
1R11 Licensed Operator Requalification Program (71111.11)
a. Inspection Scope
On March 27, 2009, the inspectors observed a crew of licensed operators in the plants
simulator during licensed operator requalification examinations to verify that operator
performance was adequate, evaluators were identifying and documenting crew
performance problems, and training was being conducted in accordance with licensee
procedures. The inspectors evaluated the following areas:
- Licensed operator performance
- Crews clarity and formality of communications
- Crews ability to take timely actions in the conservative direction
- Crews prioritization, interpretation, and verification of annunciator alarms
- Crews correct use and implementation of abnormal and emergency procedures
- Control board manipulations
- Oversight and direction from supervisors
- Crews ability to identify and implement appropriate Technical Specification
actions and emergency plan actions and notifications
-13- Enclosure
The inspectors compared the crews performance in these areas to pre-established
operator action expectations and successful critical task completion requirements.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one quarterly licensed-operator requalification
program sample as defined in IP 71111.11.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk
significant systems:
- SJ nuclear sampling system
The inspectors reviewed events such as where ineffective equipment maintenance has
resulted in valid or invalid automatic actuations of engineered safeguards systems and
independently verified the licensee's actions to address system performance or condition
problems in terms of the following:
- Implementing appropriate work practices
- Identifying and addressing common cause failures
- Scoping of systems in accordance with 10 CFR 50.65(b)
- Characterizing system reliability issues for performance
- Charging unavailability for performance
- Trending key parameters for condition monitoring
- Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)
- Verifying appropriate performance criteria for structures, systems, and
components classified as having an adequate demonstration of performance
through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as
requiring the establishment of appropriate and adequate goals and corrective
actions for systems classified as not having adequate performance, as described
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system. In addition, the inspectors verified maintenance
effectiveness issues were entered into the corrective action program with the appropriate
significance characterization. Specific documents reviewed during this inspection are
listed in the attachment.
-14- Enclosure
These activities constitute completion of one quarterly maintenance effectiveness
sample as defined in IP 71111.12-05.
b. Findings
Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65
(Maintenance Rule) for failure to demonstrate that the performance of a containment
isolation valve was effectively controlled through the performance of preventive
maintenance such that the valve remained capable of performing its intended function.
Description. An inadequate Maintenance Rule evaluation was performed after a
containment isolation valve (SJHV0005) exceeded its Maintenance Rule a(2)
performance criteria, and as a result, goal setting and monitoring were not performed as
required by paragraph a(1) of the Maintenance Rule. The reactor coolant system liquid
sampling inner containment isolation valve, SJHV-0005, failed a valve stroke test on
May 18, 2008, and again on August 17, 2008. The Maintenance Rule a(2) criteria for
this containment isolation valve is one functional failure per cycle under Function CI-01,
containment isolation. The licensees Maintenance Rule expert panel evaluated the
second failure on August 18, 2008, and kept the valve in a(2) without any evidence that
preventive maintenance was maintaining the valves ability to function properly. The
inspectors found the August 18, 2009, Maintenance Rule expert panel evaluation to be
inadequate because a run-to-failure analysis was not performed, preventive
maintenance was not being performed, and repair work on the valve was not expedited
despite a known cause. The functional failure evaluations stated that the valves could
not be proven closed. The failed valve is a direct acting Valcor solenoid valve.
Engineering has postulated that these failures are potentially an indication failure caused
by the valves reed switches. A historical review of this type of valve installed in Wolf
Creek systems shows that a solution to the reed switch indication problem has been
available from the vendor for several years.
Analysis. The failure to follow 10 CFR 50.65 a(2) and properly evaluate the failed valve,
establish performance goals, and monitor its performance is considered a performance
deficiency. Traditional enforcement does not apply since there were no actual safety
consequences or potential for impacting the NRCs regulatory function, and the finding
was not the result of any willful violation of NRC requirements or Wolf Creek procedures.
Per Inspection Manual Chapter 0612, Appendix E, Section 7, this finding is more than
minor because failure to demonstrate effective control of performance or condition and
not putting the affected structure, system, and component in (a)(1) necessarily involves
degraded structure, system, and component performance or condition. During the
Phase I Significance Screening Process, it was found that the finding is of very low
safety significance because it does not represent an actual open pathway in the physical
integrity of the reactor containment. This finding was determined to have a crosscutting
aspect in the area of problem identification and resolution associated with the corrective
action program because the licensee failed to properly classify, prioritize, and evaluate a
condition adverse to quality. P.1.c]
Enforcement. Title 10 CFR 50.65 paragraph a(2) states, that, Monitoring as specified in
Paragraph a(1) of this section is not required where it has been demonstrated that the
performance or condition of a structure, system, or component is being effectively
controlled through the performance of appropriate preventive maintenance, such that the
structure, system, or component remains capable of performing its intended function.
-15- Enclosure
Contrary to the above, on August 18, 2008, the licensee failed to properly evaluate a
component that had exceeded its functional failure criteria and had not demonstrated
that its ability to perform its intended function was being controlled through the
performance of preventive maintenance. Because the finding is of very low safety
significance and has been entered into the licensees corrective action program as
Condition Report 2009-001667, this violation is being treated as a noncited violation,
consistent with Section VI.A of the NRC Enforcement Policy:
NCV 05000482/2009002-04, failure to follow 10 CFR 50.65a(2) for containment isolation
valve failures.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a. Inspection Scope
The inspectors reviewed licensee personnel's evaluation and management of plant risk
for the maintenance and emergent work activities affecting risk-significant and safety-
related equipment listed below to verify that the appropriate risk assessments were
performed prior to removing equipment for work:
- January 7 to 9, 2009, control power fuse verification in 4160V switchgear
- January 9, 2009, reactor trip Breaker B charging spring motor did not stop
running
- January 24, 2009, reactor trip breaker auxiliary contact wiring insulation losses of
greater than 10 percent acceptance criteria
- February 5, 2009, risk assessment of battery Charger PK23 during planned
maintenance
- March 17, 2009, risk assessment for missed Technical Specification Surveillance
Requirement 3.6.1.1
The inspectors selected these activities based on potential risk significance relative to
the reactor safety cornerstones. As applicable for each activity, the inspectors verified
that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)
and that the assessments were accurate and complete. When licensee personnel
performed emergent work, the inspectors verified that the licensee personnel promptly
assessed and managed plant risk. The inspectors reviewed the scope of maintenance
work, discussed the results of the assessment with the licensee's probabilistic risk
analyst or shift technical advisor, and verified plant conditions were consistent with the
risk assessment. The inspectors also reviewed the Technical Specification requirements
and inspected portions of redundant safety systems, when applicable, to verify risk
analysis assumptions were valid and applicable requirements were met. Specific
documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of five maintenance risk assessments and
emergent work control inspection samples as defined in IP 71111.13 05.
b. Findings
No findings of significance were identified.
-16- Enclosure
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors reviewed the following issues:
- February 9, 2009, spent fuel pool low level transmitter missing silicone fluid
- January 19, 2009, component cooling water heat exchanger leakage
- February 11, 2009, component cooling water pump coupling bolts loose
- January 4, 2009, Emergency Diesel Generator A overspeed limit switch bracket
missing one screw and remaining screw loose
- Emergency diesel generator cotter pins on threaded fuel rack not installed with
sufficient bend
The inspectors selected these potential operability issues based on the risk significance
of the associated components and systems. The inspectors evaluated the technical
adequacy of the evaluations to ensure that Technical Specification operability was
properly justified and the subject component or system remained available such that no
unrecognized increase in risk occurred. The inspectors compared the operability and
design criteria in the appropriate sections of the Technical Specifications and Updated
Safety Analysis Report to the licensees evaluations, to determine whether the
components or systems were operable. Where compensatory measures were required
to maintain operability, the inspectors determined whether the measures inplace would
function as intended and were properly controlled. The inspectors determined, where
appropriate, compliance with bounding limitations associated with the evaluations.
Additionally, the inspectors also reviewed a sampling of corrective action documents to
verify that the licensee was identifying and correcting any deficiencies associated with
operability evaluations. Specific documents reviewed during this inspection are listed in
the attachment.
These activities constitute completion of five operability evaluations inspection samples
as defined in IP 71111.15-05
b. Findings
An unresolved item was identified when Wolf Creek entered Technical Specification 3.8.1
on January 4, 2009, when an operator identified one missing and one loose screw in the
Emergency Diesel Generator A overspeed limit switch. A reportability determination
dated February 19, 2009, determined that the condition was not reportable, although
Wolf Creek stated that the configuration was not seismically qualified and inoperable.
Wolf Creek concluded per NUREG 1022 that because there was not firm evidence that
screws did not fall out of the limit switch bracket immediately before discovery by an
operator, that the issue was not reportable under 10 CFR 50.73(a)(2)(i)(B). The
inspectors questioned this reportability evaluation and requested support from the Office
of Nuclear Reactor Regulations Division of Operating Reactor Oversight and Licensing.
The inspectors found that the last time that maintenance was performed on this limit
switch was 2002. At the completion of the inspection period, there were still unresolved
questions about the assumptions and results associated with the evaluation of the limit
-17- Enclosure
switch, its impact of failure on Emergency Diesel Generator A, operator response
actions, and this issues reportability. These concerns require additional inspection and,
when completed, the inspection results will require significance determination. This
issue is considered unresolved pending additional NRC review of Wolf Creek operability
determination calculations: URI 05000482/2009002-05, seismic operability of
Emergency Diesel Generator A due to overspeed limit switch degradation.
1R19 Postmaintenance Testing (71111.19)
a. Inspection Scope
The inspectors reviewed the following post-maintenance activities to verify that
procedures and test activities were adequate to ensure system operability and functional
capability:
- January 7, 2009, Auxiliary Feedwater Pump A after circuit breaker preventive
maintenance
- February 12, 2009, Emergency Diesel Generator B jacketwater keepwarm pump
current draw and vibrations after replacement
- March 6, 2009, Emergency Diesel Generator A after 18-month preventive
maintenance
- January 15, 2009, personnel air lock test after foreign material removal
The inspectors selected these activities based upon the structure, system, or
component's ability to affect risk. The inspectors evaluated these activities for the
following (as applicable):
- The effect of testing on the plant had been adequately addressed; testing was
adequate for the maintenance performed
- Acceptance criteria were clear and demonstrated operational readiness; test
instrumentation was appropriate
The inspectors evaluated the activities against the Technical Specifications, the Updated
Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various
NRC generic communications to ensure that the test results adequately ensured that the
equipment met the licensing basis and design requirements. In addition, the inspectors
reviewed corrective action documents associated with postmaintenance tests to
determine whether the licensee was identifying problems and entering them in the
corrective action program and that the problems were being corrected commensurate
with their importance to safety. Specific documents reviewed during this inspection are
listed in the attachment.
These activities constitute completion of four post-maintenance testing inspection
sample(s) as defined in IP 71111.19 05.
b. Findings
No findings of significance were identified.
-18- Enclosure
1R22 Surveillance Testing (71111.22)
a. Inspection Scope
The inspectors reviewed the Updated Safety Analysis Report, procedure requirements,
and Technical Specifications to ensure that the three surveillance activities listed below
demonstrated that the systems, structures, and/or components tested were capable of
performing their intended safety functions. The inspectors either witnessed or reviewed
test data to verify that the significant surveillance test attributes were adequate to
address the following:
- Preconditioning
- Evaluation of testing impact on the plant
- Acceptance criteria
- Test equipment
- Procedures
- Jumper/lifted lead controls
- Test data
- Testing frequency and method demonstrated technical specification operability
- Test equipment removal
- Restoration of plant systems
- Fulfillment of ASME Code requirements
- Updating of performance indicator data
- Engineering evaluations, root causes, and bases for returning tested systems,
structures, and components not meeting the test acceptance criteria were correct
- Reference setting data
- Annunciators and alarms setpoints.
The inspectors also verified that licensee personnel identified and implemented any
needed corrective actions associated with the surveillance testing.
- March 18, 2009, Emergency Diesel Generator B
- February 6, 2009, control and shutdown rod operability exercises
- Emergency Diesel Generator A and B hot restart on July 2, 2008, reviewed on
March 5, 2009
-19- Enclosure
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of three surveillance testing inspection sample(s)
as defined in IP 71111.22-05.
b. Findings
Introduction. On February 6, 2009, the inspectors identified a Green noncited violation
of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, for a procedure that allowed
unacceptable preconditioning of the control rods prior to Technical Specification
Surveillance 3.1.4.2.
Description. On February 6, 2009, the inspectors questioned the practice of stepping
each control rod group two steps in and two steps out, and repeated two more
repetitions. Procedure STS SF-001, Control and Shutdown Rod Operability
Verification, Revision 24 contained this guidance which is followed by the Technical
Specification Surveillance Requirement 3.1.4.2. Technical Specification Surveillance
Requirement 3.1.4.2 requires the control rod groups be inserted 10 steps and the rods
can then be withdrawn to the desired number of steps. The inspectors reviewed
operating experience from Westinghouse regarding control rod exercises to reduce crud
buildup at the gripper latches and reduce the frequency of slipped or dropped control
rods. Although the operating experience identifies that a gripper latch has never been
found to be unable to release a control rod, the inspector judged this practice is
unacceptable. Wolf Creek did not perform any preconditioning acceptability review
when adopting this operating experience and revising Procedure STS SF-001. The
inspectors did not find any data or test history that indicates that the Technical
Specification surveillance test would have failed with out the preconditioning, and
therefore, did not challenge the operability of the control rods. The inspectors reviewed
the regulatory positions and guidance on the subject of preconditioning that are
contained in NRC Information Notice (IN) 97-16, Preconditioning of Plant Structures,
Systems, and Components Before ASME Code Inservice Testing or Technical
Specification Surveillance Testing; NRC Inspection Manual Part 9900: Technical
Guidance, Maintenance - Preconditioning of Structures, Systems, and Components
Before Determining Operability; and NUREG-1482, Guidelines for Inservice Testing at
Nuclear Power Plants. The preventive maintenance routinely performed just before the
testing and preventive maintenance was performed for scheduling convenience. The
inspectors consulted with the regional senior technical advisor and determined that the
activity was a preventative maintenance activity that procedurally and routinely preceded
control rod testing. The inspector also determined that the practice could mask an as
found condition if crud accumulation was much more substantial, although this has not
been observed per the vendor. Wolf Creek did not utilize specialty testing equipment to
show the decay current for the gripper coils are showing a slow release of the control
rod.
Analysis. The inspectors considered the unacceptable preconditioning of the control
rods per NRC guidance to be a performance deficiency. Traditional enforcement does
not apply since there were no actual safety consequences or potential for impacting the
NRCs regulatory function, and the finding was not the result of any willful violation of
NRC requirements or Wolf Creek procedures. The finding was more than minor
because it was associated with the equipment performance attribute of the mitigating
systems cornerstone, and it affected the cornerstone objective to ensure the availability,
-20- Enclosure
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences. The inspectors evaluated the significance of this finding
under the mitigating systems cornerstone using Phase 1 of Inspection Manual
Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, and
determined that the finding was of very low safety significance (Green) because, it did
not represent an actual loss of safety function and did not screen as potentially risk
significant due to a seismic, flooding, or severe weather initiating event. This finding was
determined to have a crosscutting aspect in the area of problem identification and
resolution associated with the corrective action program because the condition report
that adopted the operating experience failed to evaluate NRC guidance regarding
preconditioning during surveillance testing which should have disallowed the procedure
change. Therefore, the applicable procedures were not complete and accurate. P.1(c)
Enforcement. 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part,
that a test program be established to assure that all testing required to demonstrate that
structures, systems and components will perform satisfactorily in service is identified and
performed in accordance with written test procedures which incorporate the
requirements and acceptance limits contained in the applicable design documents.
Contrary to the above, on February 6, 2008, the licensee performed STS SF-001,
Control and Shutdown Rod Operability Verification, Revision 24, which failed to
adequately test all of the control rod groups prior to the Technical Specification
Surveillance Requirement 3.1.4.2. The licensee performed maintenance incorporated in
STS SF-001 on the control rods and as such, unacceptably preconditioned the control
rods. Because the finding is of very low safety significance and has been entered into
the licensees corrective action program as Condition Report 2009-000598, this violation
is being treated as a noncited violation, consistent with Section VI.A of the NRC
Enforcement Policy: NCV 05000482/2009002-06, unacceptable preconditioning of
control rods prior to surveillance testing.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
a. Inspection Scope
The inspector performed an in-office review of licensee changes to Emergency Plan
Implementing Procedure APF 06-002-01, AEmergency Action Levels,@ submitted
December 17, 2008. This revision added an automatic or manually-initiated safety
injection in progress as an entry condition to Emergency Action Level 3, Loss of Reactor
Coolant Boundary, and revised the bases of Emergency Action Level 4, Main Steam
Line Break, to provide additional criteria to determine when a steam generator is
faulted.
The revision was compared to its previous revision, to the criteria of NUREG-0654,
ACriteria for Preparation and Evaluation of Radiological Emergency Response Plans and
Preparedness in Support of Nuclear Power Plants,@ Revision 1, to the criteria of Nuclear
Energy Institute Report 99-01, AMethodology for Development of Emergency Action
Levels,@ Revision 2, and to the standards in 10 CFR 50.47(b) to determine if the revision
adequately implemented the requirements of 10 CFR 50.54(q). This review was not
documented in a Safety Evaluation Report and did not constitute an approval of the
licensees changes; therefore, these revisions are subject to future inspection.
-21- Enclosure
These activities constitute completion of one sample as defined in IP 71114.04-05.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06)
a. Inspection Scope
The inspectors evaluated the conduct of a routine licensee emergency drill on
February 12, 2009, to identify any weaknesses and deficiencies in classification,
notification, and protective action recommendation development activities. The
inspectors observed emergency response operations in the simulator and technical
support center to determine whether the event classification, notifications, and protective
action recommendations were performed in accordance with procedures. The
inspectors also attended the licensee drill critique to compare any inspector-observed
weakness with those identified by the licensee staff in order to evaluate the critique and
to verify whether the licensee staff was properly identifying weaknesses and entering
them into the corrective action program. As part of the inspection, the inspectors
reviewed the drill package and other documents listed in the attachment.
These activities constitute completion of one sample as defined in IP 71114.06-05.
b. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
.1 Data Submission Issue
a. Inspection Scope
The inspectors performed a review of the data submitted by the licensee for the fourth
quarter 2008 performance indicators for any obvious inconsistencies prior to its public
release in accordance with Inspection Manual Chapter 0608, Performance Indicator
Program.
This review was performed as part of the inspectors normal plant status activities and,
as such, did not constitute a separate inspection sample.
b. Findings
No findings of significance were identified.
-22- Enclosure
.2 Unplanned Scrams per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical
Hours performance indicator for the period from the first quarter 2008 through the fourth
quarter 2008. To determine the accuracy of the performance indicator data reported
during those periods, performance indicator definitions and guidance contained in NEI
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5,
was used. The inspectors reviewed the licensees operator narrative logs, issue reports,
event reports, and NRC inspection reports for the period of January 1, 2008, through
December 31, 2008, to validate the accuracy of the submittals. The inspectors also
reviewed the licensees issue report database to determine if any problems had been
identified with the performance indicator data collected or transmitted for this indicator
and none were identified. Specific documents reviewed are described in the attachment
to this report.
These activities constitute completion of 1 unplanned scrams per 7000 critical hours
sample as defined in IP 71151-05.
b. Findings
No findings of significance were identified.
.3 Unplanned Scrams with Complications
a. Inspection Scope
The inspectors sampled licensee submittals for the unplanned scrams with
complications performance indicator for the period from the second quarter 2008 through
the fourth quarter 2008. To determine the accuracy of the performance indicator data
reported during those periods, performance indicator definitions and guidance contained
in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Revision 5, was used. The inspectors reviewed the licensees operator narrative logs,
issue reports, event reports, and NRC Integrated Inspection Reports for the period of
April 1, 2008, through December 31, 2008, to validate the accuracy of the submittals.
The inspectors also reviewed the licensees issue report database to determine if any
problems had been identified with the performance indicator data collected or
transmitted for this indicator and none were identified. Specific documents reviewed are
described in the attachment to this report.
These activities constitute completion of 1 unplanned scrams with complications sample
as defined in IP 71151-05.
b. Findings
No findings of significance were identified.
-23- Enclosure
.4 Unplanned Power Changes per 7000 Critical Hours
a. Inspection Scope
The inspectors sampled licensee submittals for the unplanned power changes per 7000
critical hours performance indicator for the period from the first quarter 2008 through the
fourth quarter 2008. To determine the accuracy of the performance indicator data
reported during those periods, performance indicator definitions and guidance contained
in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Revision 5, was used. The inspectors reviewed the licensees operator narrative logs,
issue reports, Maintenance Rule records, event reports and NRC Integrated Inspection
Reports for the period of January 1, 2008, through December 31, 2008, to validate the
accuracy of the submittals. The inspectors also reviewed the licensees issue report
database to determine if any problems had been identified with the performance
indicator data collected or transmitted for this indicator and none were identified.
Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of 1 unplanned power changes per 7000 critical
hours sample as defined in IP 71151-05.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical
Protection
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of
this report, the inspectors routinely reviewed issues during baseline inspection activities
and plant status reviews to verify that they were being entered into the licensees
corrective action program at an appropriate threshold, that adequate attention was being
given to timely corrective actions, and that adverse trends were identified and
addressed. The inspectors reviewed attributes that included: the complete and
accurate identification of the problem; the timely correction, commensurate with the
safety significance; the evaluation and disposition of performance issues, generic
implications, common causes, contributing factors, root causes, extent of condition
reviews, and previous occurrences reviews; and the classification, prioritization, focus,
and timeliness of corrective actions. Minor issues entered into the licensees corrective
action program because of the inspectors observations are included in the attached list
of documents reviewed.
These routine reviews for the identification and resolution of problems did not constitute
any additional inspection samples. Instead, by procedure, they were considered an
integral part of the inspections performed during the quarter and documented in
Section 1 of this report.
-24- Enclosure
b. Findings
No findings of significance were identified.
.2 Daily Corrective Action Program Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific
Human Performance issues for followup, the inspectors performed a daily screening of
items entered into the licensees corrective action program. The inspectors
accomplished this through review of the stations daily corrective action documents.
The inspectors performed these daily reviews as part of their daily plant status
monitoring activities and, as such, did not constitute any separate inspection samples.
b. Findings
No findings of significance were identified.
.3 Selected Issue Follow-up Inspection
a. Inspection Scope
During a review of items entered in the licensees corrective action program, the
inspectors recognized a corrective action item documenting the reactor coolant pump
thermal barrier heat exchanger outlet valves and downstream containment isolation
valves. On January 31, 2009, downstream containment isolation Valve EG HV-62
closed when the radioactive waste evaporators were isolated. Valve EG HV-62 isolated
all four thermal barrier heat exchangers. On November 10, 19, 22, and 24, 2008, Wolf
Creek thermal barrier valves closed themselves without operator action during pump
swaps and isolations of radioactive waste evaporators.
These activities constitute completion of one in-depth problem identification and
resolution sample as defined in IP 71152-05.
c. Findings
Introduction. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,
Criterion XVI, Conditions Adverse to Quality, for failure to correct a condition adverse to
quality with the component cooling water thermal barrier heat exchanger outlet valves to
ensure reactor coolant pump seal cooling. This issue was previously identified in NRC
Inspection Report 2007-03 as NCV 05000482/2007003-03.
Description. When the NRC issued NCV 05000482/2007003-03 on August 16, 2007, for
failing to identify the cause of component cooling valve closure, corrective actions were
tracked under Condition Reports 2007-002064 and 2007-002601. On December 10,
2007, Condition Report 2007-002064 was downgraded from a broke/fix type analysis to
an address management evaluation and the scope was changed to review component
cooling water operating experience and not to correct the issue. No subsequent action
was taken until October 27, 2008, when Wolf Creek realized that this condition report
was in response to NCV 05000482/2007003-03. The condition report was subsequently
-25- Enclosure
upgraded to an apparent cause evaluation on October 28, 2008, which was completed
on February 19, 2009. Wolf Creek found that the apparent cause was a lack of a time
delay in the valves motor circuit. This time delay would allow a high-flow condition to
decay prior to valve closure on high flow. This time delay would also prevent the motor
from reversing direction as soon as the valve was opened and prevent breaker trips. A
modification has yet to be implemented. No additional procedural guidance or
compensatory guidance was provided to operators to alert them to the incorrect closure
of these valves.
In the past, Wolf Creek performed activities such as adding steps to procedures to
instruct operators to expect and accept the mal-operation of these valves, throttling flow
to other portions of the component cooling water system, and adjusting the flow switches
to these valves; however, none stopped the valves from closing. Several corrective
action documents, work orders and work requests have been initiated since 2001
documenting valve closure and corrective actions. A previous operability evaluation
stated that this issue is of low-safety significance because reactor coolant pump seal
injection is also available. The Wolf Creek plant safety analysis identifies providing
reactor coolant pump seal cooling in a timely manner as the most safety-significant
operator action. In some occurrences, inspectors found that during component cooling
water pump swap, the flow element on the down stream containment isolation valve was
also actuated and caused the associated valve to stroke closed. The inspectors found
that Wolf Creek has yet to correct this deficiency.
The inspectors found that these component cooling water valves are safety related as
specified in Updated Safety Analysis Report, Section 9.2.2.2.1. Section 5.1.1.2.2
describes thermal barrier heat exchangers and seal injection as diverse methods to
assure reactor coolant pump seal cooling. Lastly, the inspectors found in
Section 9.2.2.2.3 of the Updated Safety Analysis Report, the component cooling water
system is described as being able to provide cooling to the thermal barriers, to achieve
emergency cold safe shutdown with a single active component failure. The inadvertent,
automatic closure of these valves is contrary to these Updated Safety Analysis Report
sections.
Additionally, the inspectors and the licensee concluded it reasonable that the reactor
coolant pump component cooling water heat exchanger outlet valves will stroke closed
on a loss of offsite power and/or a safety injection signal due to the higher than normal
flow created by component cooling water pumps stop and start. Therefore, the
component cooling water thermal barriers may not be able to fulfill their function to
remain open for cooling of the reactor coolant pump seals during design basis accidents
and events because they will stroke closed on high flow when component cooling water
pumps stop and start and when the radioactive waste evaporator valves close. Reactor
coolant pump seal cooling is necessary to preclude a seal loss of coolant accident.
During NRC questioning of the apparent cause, Wolf Creek wrote Condition
Report 2009-001496 to consider adding emergency procedure steps to alert operators
that the thermal barrier valves need to be open. Although numerous flow balances have
been performed, Wolf Creek has no data on the actual flow balance in the system during
normal operations, during pump swaps, and during isolation of radioactive waste
evaporators. Wolf Creek stated that further flow balances would be performed when
control room annunciators are received in the control room for the component cooling
water valves that cool the reactor coolant pump heat loads.
-26- Enclosure
Analysis. The inspectors determined that the failure to correct the condition adverse to
quality of ensuring reactor coolant pump seal cooling as described in the Updated Safety
Analysis Report is a performance deficiency. Traditional enforcement does not apply
since there were no actual safety consequences or potential for impacting the NRC's
regulatory function, and the finding was not the result of any willful violation of NRC
requirements or Wolf Creek procedures. The inspectors determined that this finding was
more than minor because it is associated with the equipment performance attribute for
the Initiating Events cornerstone; and, it affected the cornerstone objective to limit the
likelihood of those events that upset plant stability and challenge critical safety functions
during shutdown as well as power operations. Specifically, this issue relates to the
reliability example of the equipment performance attribute because the valves have
demonstrated a history of inappropriately stroking closed and being difficult to re-open
when both trains of component cooling water pumps are started, which is similar to
design basis events and accidents. The inspectors evaluated the significance of this
finding using Phase 1 of Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial
Screening and Characterization of Findings, and determined that the finding was of very
low safety significance because assuming worst case degradation, the finding would not
result in exceeding the Technical Specification limit for identified reactor coolant system
leakage and would not have likely affected other Mitigation Systems resulting in a total
loss of their safety function because seal injection was available. This finding has a
crosscutting aspect in the area of human performance associated with the decision
making component because, even though numerous instances of valve closures
occurred since the first noncited violation, Wolf Creek downgraded the condition report.
Using nonconservative assumptions, the licensee consistently viewed this issue as not
having a risk impact because seal injection was not simultaneously lost. [H.1( b)]
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Conditions Adverse to
Quality, requires that conditions adverse to quality, such as failures, malfunctions,
deficiencies, deviations, defective material and equipment, and nonconformances are
promptly identified and corrected. Contrary to the above, from 2001 to 2009, Wolf Creek
did not correct the reactor coolant pump thermal barrier heat exchanger outlet valves
stroking closed on high flow which would be experienced during design basis accidents
and events. This issue and the corrective actions are being tracked by the licensee in
Condition Report 2007-002074. Because the violation was of very low safety
significance and the issue was captured in the licensee's corrective action program, but
the licensee failed to restore compliance, this violation is being treated as a cited
violation consistent with Section VI.A.1.a of the NRC Enforcement Policy:
NOV 05000482/2009002-07, failure to correct component cooling water valve closures.
4OA3 Event Follow-up (71153)
.1 Plant down power due to loss of Benton and Rosehill 345 kV power lines.
a. Inspection Scope
On March 27, 2009, Wolf Creek experienced 180 MWe to 250 MWe load swings and
subsequently lost the 345 kV Benton power line. Emergency diesel generator B was out
of service for planned maintenance. Wolf Creek reduced turbine load to 90 percent
while diverting 10 percent to the steam dump valves. Reactor power was maintained at
-27- Enclosure
100 percent. The grid was determined to be stable early on March 28 and emergency
diesel generator B successfully passed it post maintenance test.
At 9:09 a.m., on March 28, the 345 kV Rosehill line breakers opened. One of these
breakers serves a dual purpose as the main generator output breaker. The other main
generator output breaker remained closed and within its operating limitations. At 10:03
a.m., operators reduced reactor power to match main generator output at approximately
80 percent, and the steam dumps were closed. At 11:11 a.m, the Rosehill line was
restored and sparks were observed from one LaCygne breaker in the switchyard. At
5:18 p.m., the shift manager discussed the grid state estimator calculation with the grid
operator. A standing order allowed splitting of the Wolf Creek 345 kV ring bus. The shift
manager decided that there was confidence in the remaining 345 kV LaCygne line to
provide sufficient voltage following a reactor trip and emergency equipment start in
response to a postulated loss of coolant accident. On March 29 at 6:17 a.m., the
Rosehill line breakers re-opened. One of the Rosehill breakers was determined to have
a bad fault-time-delay timer. Maintenance subsequently planned replacement of the
timer. At 5:05 p.m., one of two of the 345 kV Benton line breakers was closed. At 6:45
p.m, the second Benton line breaker was closed. At 7:20 p.m., the Rosehill breaker with
the bad fault-time-delay timer was successfully replaced. At 7:31 p.m. on March 29, the
Rosehill line was restored. At 7:39 p.m. on March 29, the LaCygne line breaker was
opened so that the breaker disconnects could be opened pending repair. At 8:50 p.m.,
reactor power increase was commenced. Early on March 30, the reactor was returned
to full power. Inspectors interviewed control room personnel, engineering personnel,
reviewed off-normal procedures, equipment limitations, Technical Specifications, and
control room logs.
These activities constitute completion of 1 event followup sample as defined in IP 71153-
05.
b. Findings
No findings of significance were identified.
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors performed observations of security force
personnel and activities to ensure that the activities were consistent with Wolf Creeks
security procedures and regulatory requirements relating to nuclear plant security.
These observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities
did not constitute any additional inspection samples. Rather, they were considered an
integral part of the inspectors normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
-28- Enclosure
.2 Inattentive Shift Manager
a. Inspection Scope
The NRC followed up to determine if a licensed senior operator had been inattentive in
the control room while assigned as shift manager.
b. Findings
Introduction. A Green self-revealing noncited violation of Technical
Specification 5.4.1(a) was identified when an on-duty operations shift manager was
observed to be inattentive on multiple occasions in 2004 and 2005.
Description. Numerous crewmembers indicated that they had observed a shift manager
inattentive to his duties on multiple occasions during 2004 and 2005. The
inattentiveness was of concern because the shift manager was not attentive to plant
conditions at all times. This limited his ability to monitor the safe operation of the plant,
assist the control room supervisor with the control room command function, and respond
in the event of an accident.
Analysis. The failure of the shift manager to remain attentive is considered a
performance deficiency. This finding is more than minor because it adversely impacts
the Human Performance attribute of the Mitigating Systems cornerstone, and if left
uncorrected this performance deficiency has the potential to lead to a more significant
safety concern because the shift manager plays an important role in the oversight of post
accident response by all licensed operators on shift. This issue was reviewed by NRC
management using Inspection Manual Chapter 0609, Appendix M, Significance
Determination Process Using Qualitative Criteria. NRC management reviewed the
qualitative factors involved with this finding and determined that this finding is Green.
The inspectors did not identify a cross cutting aspect because the shift manager has not
stood watch for several years, and therefore, the issue was not considered current
performance.
Enforcement. Wolf Creek Technical Specification 5.4.1(a) states that the applicable
procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated
February 1978, shall be established, implemented, and maintained. Wolf Creek
Procedure AP 21-001, Conduct of Operations, is one of those procedures. Section 6.5
of this procedure states that, no person shall assume a shift position unless he/she is
physically and mentally fit to competently discharge his/her responsibilities."
Furthermore, Section 6.8.4 of this procedure states that control room personnel are
responsible for inplant activities and must maintain control and cognizance of any
activities which have potential to impact plant conditions. Contrary to the above, the
shift manager in question assumed a shift position and subsequently was observed to be
inattentive on several occasions between 2004 and 2005, therefore, he was not
physically or mentally fit to assume the position nor could he have been completely
aware of plant activities. Because this finding is of very low safety significance and was
entered into the licensee's corrective action program as Condition Report 2008-000572,
this violation is being treated as a noncited violation, consistent with Section VI.A.1 of
the NRC Enforcement Policy, NCV 05000482/200902-08, inattentive on-duty senior
reactor operator.
-29- Enclosure
4OA6 Meetings, Including Exit
On January 15, 2009, the inspector conducted a telephonic exit meeting to present the
results of the in-office inspection of changes to the licensees emergency action levels to
Mr. T. East, Superintendent, Emergency Preparedness, who acknowledged the findings.
On April 7, 2009, the inspector presented the inspection results at an exit meeting to Mr.
Matt Sunseri, Vice President of Operations and Plant Manager, who acknowledged the
findings.
-30- Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
R. A. Muench, President and Chief Executive Officer
M. Sunseri, Vice President Operations and Plant Manager
S. E. Hedges, Vice President Oversight
K. Scherich, Director Engineering
T. East, Superintendent, Emergency Preparedness
P. Bedgood, Superintendent, Chemistry/Radiation Protection
G. Pendergrass, Manager, System Engineering
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
Seismic operability of Emergency Diesel Generator A due to
overspeed limit switch degradation (Section 1R15)
Failure to correct component cooling water valve closures05000482/2009002-07 VIO
(Section 4OA2)
Opened and Closed
Untimely corrective actions result in room temperature
below boric acid solubility limit (Section 1RO1)05000482/2009002-02 NCV Degraded fire barrier for auxiliary feedwater (Section 1RO5)
Failure to implement foreign material exclusion control
procedure for spent fuel pool (Section 1RO5)
Unacceptable preconditioning of control rods prior to
surveillance testing (Section 1R22)
Failure to follow 10 CFR 50.65a(2) for containment isolation
valve failures (Section 1R12)05000482/2009002-08 NCV Inattentive on-duty senior reactor operator (Section 4OA5)
A-1 Attachment
LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather
DOCUMENTS
NUMBER TITLE REVISION /
DATE
EGP 0077 CCW A & C Discharge Pressure
EFP 0007 ESW A Discharge Pressure
DNA History Plot
STN GP-001 Plant Winterization 39
SYS BG-206 Boric Acid System Operation 33
STS CH-022 Boric Acid Tank A Boron Concentration Determination 4
STS CH-023 Boric Acid Tank B Boron Concentration Determination 4
CKL ZL-1269 Record Safety Injection Pump A Room Temperature 73
Control Room Logs January 31 February 1, 2009
STN PE-036 Safety-Related Room Cooler Heat Transfer Verification and 13
Performance Trending
Updated Safety Analysis Report 9.4-33
Updated Safety Analysis Report 7.4.3.3, Cold Shutdown
Discussion
Freeze Protection/Heat Trace Systems
AFP 2B-001-02 Shutdown Safety Function Checklist 7
07-012-BG Temporary Modification Order R0
AP 22C-003 Operational Risk Assessment Program 22C
A-2 Attachment
Section 1R01: Adverse Weather
DOCUMENTS
NUMBER TITLE REVISION /
DATE
AI 14-006 Severe Weather 8
OFN SG-003 Natural Events 15
Condition Report
2009-000509 2009-000516 2009-000606 2009-001495
Work Order
07-301826-001 07-301826-002
Performance Improvement Request
96-002440 2001-0391 2005-3461
DOCUMENTS
NUMBER TITLE REVISION /
DATE
CKL AL-120 Auxiliary Feedwater Normal Lineup 34
SYS AL-120 Feeding Steam Generators with a Motor Driven or Turbine 33
Driven AFW Pump
SYS KJ-121 Diesel Generator Lineup for Auto Ops 39
ALR 00-128B TD AFW Start 8
CKL EM-120 Safety Injection Normal Lineup 24A
USAR, Table 3.2-4, Design Comparison to Regulatory Guide 1.26, Revision 3, Dated February
1976, Quality Group Classifications and Standards for Water-, Steam-, and Radioactive-Waste
Containing Components of Nuclear Power Plants
USAR, Table 3.2-1, Sheet 15, Classification of Structures, Components, and Systems
Design Specification for Standby Diesel Generators for the SNUPPS, Job No. 10466-M-018Q
A-3 Attachment
Section 1RO5: Fire Protection
DOCUMENTS
NUMBER TITLE REVISION /
DATE
AP 10-106 Fire Preplans 5
AP 10-106 Fire Preplans 6
E-1F9910 Post Fire Safe Shutdown Area Analysis 2
AP 10-106 Fire Protection Water Supply and Hydrant Locations 6
M-1Y004 Conduit Smoke and Gas Seal Typical Locations 00
M-663-00017 Penetration Seal Typical Details W20
Work Orders
06-290793-040 09-313747-000
Section 1R11: Licensed Operator Requalification
DOCUMENTS
NUMBER TITLE REVISION /
DATE
LR5002010 Loss of ESW (Complex Scenario) 006
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
DOCUMENTS
NUMBER TITLE REVISION /
DATE
Change Use As Is Reactor Trip Bypass Breaker Wiring 0
Package
013975
AP 22C-003 Operational Risk Assessment Program 22C
STS MT-044 Containment Tendon Inspection 7A
A-4 Attachment
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
DOCUMENTS
NUMBER TITLE REVISION /
DATE
012975 Use as is Reactor Trip Bypass Breaker Wiring 0
Work Request
09-071671 09-071887 09-313367-005 09-313367-008 09-313367-004
Work Order
09-313364-000 09-313367-004 08-310078-000
Condition Reports
2007-001482 2009-000113 2009-000354 2009-000355 2009-000357
2009-000506 2009-000354 2009-001392 2009-001302
Section 1R15: Operability Evaluations
NUMBER TITLE REVISION /
DATE
CR 200-111740 CCW Pump to Motor Coupling Bolts
STS EG 100B Component Cooling Wate Pumps B/D Inservice Pump Test Revision 20
WP 118089 Task 1 Rev 0
INC S-0503 Torquing & Sequencing Standards and Practices Rev 4
M-082-00069 Falk Corporation Instructions for installation and W01
maintenance sizes 10 thru 70 Gear Coupling Double
Engagement Horizontal Types G10 & 20 Vertical Types
GV10 & 20
M-082-00068 Falk Corporation Limited end Float Coupling Installation W01
Instructions Gear Couplings Double Engagement Horizontal
Types G10 & 20
Falk Lifelign Gear Couplings Manual
STS IC-615B Slave relay Test K615 Train B Safety Injection 20
M-1G023 Equipment Locations Reactor & Auxiliary Bldg Plan 9
EL 20260
A-5 Attachment
Section 1R15: Operability Evaluations
NUMBER TITLE REVISION /
DATE
SYS KJ-123 Post Maintenance Run of Emergency Diesel Generator A 41
STS KJ-015A Manual/Auto Fast Start, Sync & Loading of EDG NE01 25A
Condition Reports
2009-000259 2009-000262 2009-000666 2009-000310 2009-000643
2009-000733 2009-000666 AR 14667
Work Orders:
0-214187-000-001-003 08-313153-000 09-313686-000 05-279610-000
05-279610-003 05-279610-002 09-314853-000
0-214187-003 0-214187-001
Engineering Disposition:
ECLSL0058 J-Box Silicon Fluid
Drawing:
E-13EC01, Fuel Pool Cooling Pumps, Revision 1
Section 1R19: Postmaintenance Testing
DOCUMENTS
NUMBER TITLE REVISION /
DATE
STS PE-013 Personnel Airlock Seal Test 15
STS IC-615A Slave Relay Test K615 Train A Safety Injection 20
STS KJ-015A Manual/Auto Fast Start, Sync & Loading of EDG NE01 25A
Condition Report
2009-000187
Section 1R22: Surveillance Testing
PROCEDURES
NUMBER TITLE REVISION /
DATE
OE KJ-09-003 Emergency Diesel Generator B Crankcase Vapor Extractor 1 and 3
A-6 Attachment
Section 1R22: Surveillance Testing
PROCEDURES
NUMBER TITLE REVISION /
DATE
Material Safety Data Bulletin-Mobilgard 570
AP 15C-004 Preparation, Review and Approval of Procedures, 33
Instructions and Forms
AP 29B-001 IST Basis Document 3
AP 29B-002 ASME Code Testinig of Pumps and Valves 6
AP 29B-003 Surveillance Testing 9
STS SF-001 Control and Shutdown Rod Operability Verification 24
OSP-SF-00002 Control Bank 18
AP 29B-003 Surveillance Testing 10
Work Order
07-297977-000,
Condition Reports
2009-000598 2009-001357 2009-001391 2009-001401 2007-002911
Work Request
09-072564 09-072565 09-072566 09-072567 09-072568
Other Documents:
NRC Information Notice 97-16, Preconditioning of Plant Structures, Systems, and Components
before ASME Code Inservice Testing or Technical Specification Surveillance Testing
NRC Inforomation Notice 85-14, Failure of a Heavy Control Rod (B4C) Drive Assumbly to Insert
on a Trip Signal.
Generic Letter 89-04, Guidance on Developing Acceptable Inservice Testing Programs
Action Plan:
1344, DRDM Transitory Misstepping Due to Crud
2708, Add Single Stepping of Rods to Rod Operability Surveillance.
A-7 Attachment
2709, CRDM Conditioning to Preclude Crud Buildup
Westinghouse Electric Company Technical Bulleting, CRDM Transitory Misstepping Due to
Crud, No. TB-06-17
Section 1EP6: Drill Evaluation
DOCUMENTS
NUMBER TITLE REVISION /
DATE
SA-01 Station Blackout Followed by Loss of Coolant Accident 00
Section 4OA1: Performance Indicator Verification
DOCUMENTS
NUMBER TITLE REVISION /
DATE
AP 26A-007 NRC Performance Indicators 5
Section 4OA2: Identification and Resolution of Problems
PROCEDURES
NUMBER TITLE REVISION /
DATE
SYS EG-205 CCW to RCP Flow Adjustment 5
012956 RCP Thermal Barrier Flow Loop Time Delay 0
M-12EG03 P&ID Component Cooling Water System 08
Condition Reports
2007-0178 2007-1125 2007-0597 2007-2064 2007-0643
2007-2601 2007-0717 2008-5241 2008-5688 2008-5691
Work Orders
02-246887-00 02-246887-01 01-224201-42 01-227685-00 08-31647-00
Work Requests
01-025637 02-29406 02-036118
A-8 Attachment
Performance Improvements Requests
2001-0866 2002-0734 2002-3039 2004-0298
Section 4OA3: Event Follow-Up
PROCEDURES
NUMBER TITLE REVISION /
DATE
OFN AF-025 Unit Limitations 25
A-9 Attachment