ML111300561

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IR 05000263-11-002, on 01/01/2011 - 03/31/2011; Monticello Nuclear Generating Plant, Refueling Outage Activities; Follow Up of Events; and Notices of Enforcement Discretion
ML111300561
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 05/10/2011
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: O'Connor T
Northern States Power Co
References
EA-11-050 IR-11-002
Download: ML111300561 (58)


See also: IR 05000263/2011002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

May 10, 2011

EA-11-050

Mr. Timothy J. OConnor

Site Vice President

Monticello Nuclear Generating Plant

Northern States Power Company, Minnesota

2807 West County Road 75

Monticello, MN 55362-9637

SUBJECT: MONTICELLO NUCLEAR GENERATING PLANT NRC INTEGRATED AND

POWER UPRATE REVIEW INSPECTION REPORT 05000263/2011002 AND

EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. OConnor:

On March 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed integrated and

power uprate inspections at your Monticello Nuclear Generating Plant. The enclosed report

documents the inspection findings, which were discussed on April 5, 2011, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, licensee-identified issues were discovered that

involved violations of NRC requirements. These 10 CFR 50, Appendix R-related issues,

discussed in Sections 1RO5.2 and 4OA3.4, were screened and determined to warrant

enforcement discretion per Enforcement Guidance Memorandum (EGM) 09-002,

Enforcement Discretion for Fire Induced Circuit Failures. One additional licensee-identified

violation is documented in Section 4OA7 of this report.

Based on the results of this inspection, one NRC-identified and one self-revealed finding of

very low safety significance were identified. The findings each involved a violation of NRC

requirements. However, because of their very low safety significance, and because the issues

were entered into your corrective action program, the NRC is treating the issues as non-cited

violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy.

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with

a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

T. O'Connor -2-

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Monticello Nuclear Generating Plant. In addition, if you disagree with the

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region III, and the NRC Resident Inspector at the Monticello Nuclear

Generating Plant.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket No. 50-263

License No. DPR-22

Enclosure: Inspection Report 05000263/2011002

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-263

License No: DPR-22

Report No: 05000263/2011002

Licensee: Northern States Power Company, Minnesota

Facility: Monticello Nuclear Generating Plant

Location: Monticello, MN

Dates: January 1 through March 31, 2011

Inspectors: S. Thomas, Senior Resident Inspector

P. Voss, Resident Inspector

P. Cardona-Morales, Resident Inspector, Acting

M. Phalen, Senior Health Physicist

C. Tilton, Senior Reactor Inspector

A. Dahbur, Senior Reactor Inspector

D. Jones, Reactor Inspector

N. Shah, Project Engineer

Approved by: K. Riemer, Chief

Branch 2

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 1

REPORT DETAILS ....................................................................................................................... 3

Summary of Plant Status ........................................................................................................... 3

1. REACTOR SAFETY ....................................................................................................... 3

1R01 Adverse Weather Protection (71111.01) ............................................................. 3

1R04 Equipment Alignment (71111.04)........................................................................ 4

1R05 Fire Protection (71111.05) .................................................................................. 5

1R06 Flooding (71111.06) ............................................................................................ 8

1R07 Annual Heat Sink Performance (71111.07A) ...................................................... 8

1R08 Inservice Inspection Activities (71111.08G) ........................................................ 9

1R11 Licensed Operator Requalification Program (71111.11) ................................... 10

1R12 Maintenance Effectiveness (71111.12) ............................................................. 11

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 12

1R15 Operability Evaluations (71111.15) ................................................................... 12

1R18 Plant Modifications (71111.18).......................................................................... 13

1R19 Post-Maintenance Testing (71111.19) .............................................................. 14

1R20 Outage Activities (71111.20) ............................................................................. 14

1R22 Surveillance Testing (71111.22) ....................................................................... 19

1EP6 Drill Evaluation (71114.06) ................................................................................ 20

2. RADIATION SAFETY ................................................................................................... 21

2RS5 Radiation Monitoring Instrumentation (71124.05) ............................................. 21

4. OTHER ACTIVITIES ..................................................................................................... 26

4OA1 Performance Indicator Verification (71151)....................................................... 26

4OA2 Identification and Resolution of Problems (71152) ........................................... 28

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) .............. 30

4OA5 Other Activities .................................................................................................. 35

4OA6 Management Meetings...................................................................................... 38

4OA7 Licensee-Identified Violations ........................................................................... 38

SUPPLEMENTAL INFORMATION ............................................................................................... 1

Key Points of Contact ................................................................................................................ 1

List of Items Opened, Closed and Discussed............................................................................ 2

List of Documents Reviewed ..................................................................................................... 3

List of Acronyms Used ............................................................................................................ 12

Enclosure

SUMMARY OF FINDINGS

IR 05000263/2011002; 01/01/2011 - 03/31/2011; Monticello Nuclear Generating Plant,

Refueling Outage Activities; Follow-Up of Events; and Notices of Enforcement Discretion.

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings, one NRC-identified and

one self-revealed, are documented in this report. These findings were considered non-cited

violations (NCV) of NRC regulations. The significance of most findings is indicated by their

color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

  • Green. A finding of very low safety significance and associated NCV of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed

when the licensee failed to adequately implement the requirements of their fleet tagging

procedure, a procedure affecting quality, during maintenance on the safety-related

CST-88 B low pressure coolant injection (LPCI) fill line check valve. This failure

resulted in an unintentional breach of the condensate service water (CSW) system and

subjected workers to a potentially contaminated, pressurized water source. Additionally,

at the time of the breach, the CSW system was one of the water sources being credited

in support of the shutdown safety function of inventory control. The licensee entered this

issue into the corrective ation program (CAPs 1275935 and 1275963) and took

immediate corrective actions to restore the check valve to its installed configuration to

terminate the water leakage. At the time of this report, the licensee had assembled a

team to perform a root cause evaluation.

The inspectors determined that the licensees failure to adequately implement their

tagging process to protect workers and equipment from the effects of breaching the

pressurized CSW header during maintenance on a safety-related check valve was a

performance deficiency because it was the result of the failure to meet a requirement,

the cause was reasonably within the licensees ability to foresee and correct, and

should have been prevented. The inspectors screened the performance deficiency per

IMC 0612, Power Reactor Inspection Reports, Appendix B, and determined that the

issue was more than minor because the performance deficiency could have reasonably

been viewed as a precursor to a more significant event. In this instance, the

performance deficiency resulted in an unintentional breach of the operating CSW

system and subjected workers to a potentially contaminated, pressurized water source.

Additionally, at the time of the breach, the CSW system was one of the water sources

being credited in support of the shutdown safety function of inventory control. As a

result, this finding was evaluated under the Initiating Events Cornerstone.

The inspectors applied NRC IMC 0609, Significance Determination Process,

Appendix G, "Shutdown Operations Significance Determination," Attachment 1, to this

finding. The finding was determined to have very low safety significance because it did

not adversely affect core heat removal, inventory control, power availability, containment

1 Enclosure

control, or reactivity guidelines. This finding has a cross-cutting aspect in the area of

Human Performance, work control, because the licensee failed to appropriately plan

work activities by incorporating job site conditions impacting plant systems and

components (H.3(a)). (Section 1R20)

Cornerstone: Barrier Integrity

  • Green. A finding of very low safety significance and associated NCV of Technical

Specification 5.4, Procedures, was identified by the inspectors when the licensee

failed to implement the requirements of their foreign material exclusion (FME) and

control procedure during new fuel receipt activities. Specifically, the inspectors

observed two operators exiting and re-entering a Level 1 FME area, without the

knowledge of the FME monitor, at a point that was not being controlled by the FME

monitor. When informed of the issue, the licensee took corrective actions to address

the issue.

The inspectors determined that the licensees failure to adequately implement the

requirements of their FME control procedure during new fuel receipt activities to prevent

the unmonitored access of two operators into a Level 1 FME area was a performance

deficiency because it was the result of the failure to meet a requirement or a standard,

the cause was reasonably within the licensees ability to foresee and correct, and should

have been prevented. The inspectors screened the performance deficiency per

IMC 0612, Power Reactor Inspection Reports, Appendix B, and determined that the

issue was more than minor because it impacted the human performance attribute of the

Barrier Integrity Cornerstones objective to provide reasonable assurance that physical

design barriers (fuel cladding, reactor coolant system, and containment) protect the

public from radionuclide releases caused by accidents or events. The inspectors applied

IMC 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,

to this finding. The inspectors utilized Column 3 of the Table 4a worksheet to screen the

finding. Since the finding only had the potential to impact the fuel barrier, it screened to

be of very low safety significance. This finding has a cross-cutting aspect in the area of

Human Performance, Work Practices because the licensee did not define and effectively

communicate expectations regarding procedural compliance and perosnnel following

procedures (H.4(b)). (Section 4OA3)

B. Licensee-Identified Violations

Violations of very low safety significance that were identified by the licensee have been

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees corrective action program. These violations and corrective

action tracking numbers are listed in Section 4OA7 of this report.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

During the first nine weeks of the inspection period, the plant operated at approximately

100 percent power except for minor power adjustments to facilitate rod pattern adjustments and

routine planned surveillance testing activities. On March 4, 2011, the licensee began a planned

downpower, and on March 5, 2011, at 00:18, the main generator breakers were opened and the

licensee began their refueling outage. The licensee remained shutdown for the remainder of

the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness for Impending Adverse Weather Condition - Extreme Cold Conditions

a. Inspection Scope

Since extreme cold conditions were forecast in the vicinity of the facility for

January 21, 2011, the inspectors reviewed the licensees overall preparations/protection

for the expected weather conditions. On January 20, 2011, the inspectors walked down

the emergency diesel generator (EDG) building and heating boiler system because their

safety-related functions could be affected or required as a result of the extreme cold

conditions forecast for the facility. The inspectors observed insulation, heat trace

circuits, space heater operation, and weatherized enclosures to ensure operability of

affected systems. The inspectors reviewed licensee procedures and discussed potential

compensatory measures with control room personnel. The inspectors focused on plant

managements actions for implementing the stations procedures for ensuring adequate

personnel for safe plant operation and emergency response would be available.

Specific documents reviewed during this inspection are listed in the Attachment to this

report.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

.2 External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The evaluation included a review to check

for deviations from the descriptions provided in the Updated Safety Analysis Report

(USAR) for features intended to mitigate the potential for flooding from external factors.

As part of this evaluation, the inspectors checked for obstructions that could prevent

draining and determined that barriers required to mitigate the flood were in place and

3 Enclosure

operable. Additionally, the inspectors performed a walkdown of the protected area to

identify any modification to the site which would inhibit site drainage during a probable

maximum precipitation event or allow water ingress past a barrier. The inspectors also

reviewed the abnormal operating procedure (AOP) for mitigating the design basis flood

to ensure it could be implemented as written.

This inspection constituted one external flooding sample as defined in IP 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • 12 EDG fuel oil and air start systems while in 11 EDG maintenance window;

maintenance; and

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures;

system diagrams; USAR; Technical Specification (TS) requirements; outstanding work

orders (WOs); condition reports; and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program (CAP) with the appropriate significance characterization.

Documents reviewed are listed in the Attachment to this report.

These activities constituted three partial system walkdown samples as defined in

IP 71111.04-05.

b. Findings

No findings were identified.

4 Enclosure

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Fire Zone 9 (control room);
  • Fire Zones 7-A, B, and C (Division I 125V and 250V battery rooms and

Division II 125V battery room);

  • Fire Zone 23-A (intake structure pump room);
  • Fire Zone 6 (refuel floor); and
  • Fire Zones 19-A, B, and C (makeup demin area, essential motor control center

area, and feedwater pipe chase).

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings were identified.

.2 Circuit Analyses (71111.05T)

Background

Title 10 CFR Part 50, Appendix R, Section III.G.2, identified three acceptable methods to

meet the requirement for maintaining one of the redundant trains in the same fire area,

outside of primary containment, free of fire damage. The three methods included a

combination of physical barriers, spatial separation, and fire detection and automatic

suppression systems.

5 Enclosure

In October 2009, the NRC issued guidance in Regulatory Guide (RG) 1.189,

Fire Protection for Nuclear Power Plant, Revision 2, to identify acceptable methods

for resolving issues related to circuits required for post-fire safe shutdown and circuits

important to post-fire safe shutdown. Equipment required for post-fire safe shutdown

(credited train) must use one of the three methods identified in Section III.G.2 to protect

the circuits located within the same fire area from damage, including single and multiple

spurious operations (MSOs). For important to post-fire safe shutdown circuits,

the licensee may use operator manual actions if the licensee demonstrates they can be

shown to be feasible and reliable or resolve issues using other analysis methods

including fire modeling.

In May 2009, the NRC issued Enforcement Guidance Memorandum (EGM) 09-002,

Enforcement Discretion for Fire Induced Circuit Faults, which described the conditions

limiting enforcement discretion during the resolution of the fire protection concerns

involving MSOs. The EGM limited the enforcement discretion to three years from the

date of issuance of RG 1.189, Revision 2: (1) six months following the issuance of

RG 1.189, Revision 2, for licensees to identify noncompliances related to multiple fire

induced circuit faults, place the noncompliances into their CAP and implement

compensatory measures for the noncompliances, and (2) three years following the

issuance of RG 1.189, Revision 2, for licensees to complete the corrective actions

associated with noncompliant multiple fire induced circuit faults. The enforcement

discretion would not be granted to identified noncompliances that are found to be willful

or findings that the Reactor Oversight Process (ROP) SDP would evaluate as red or

categorize at Severity Level I.

By a letter dated November 30, 2005, Nuclear Management Company (NMC) notified

the NRC of Monticello Nuclear Generating Plants (MNGP) intention to adopt NFP 805

in accordance with 10 CFR 50.48(c), National Fire Protection Association

(NFPA) Standard 805. Xcel Energy, the current Monticello licensee holding company,

later notified the NRC by a letter dated July 16, 2010, of the notice of withdrawal of their

letter of intent to transition to 10 CFR 50.48(c) for Monticello.

a. Inspection Scope

The inspectors conducted a one-week long inspection, during the week of

February 7, 2011, as part of the triennial fire protection inspection. As a result of

the licensees decision to withdraw their intention to comply with 10 CFR 50.48(c),

this inspection was completed prior to the actual date of the triennial fire protection

inspection, scheduled to be completed this year. During the inspection, the inspectors

reviewed a representative sampling of single and multiple spurious issues throughout

the plant to verify:

  • The licensee successfully addressed single and multiple spurious issues in a

way that met regulations;

  • The licensee properly classified equipment required for safe shutdown and

equipment important for safe shutdown;

  • The adequacy of the licensees evaluation of multiple spurious actuations,

in accordance with RG 1.189 and Nuclear Energy Institute (NEI) 00-01,

Revision 2; and

  • The adequacy of the licensees compensatory actions taken for identified

noncompliances.

6 Enclosure

During this inspection, the inspectors reviewed the licensees post-fire safe shutdown

analysis to verify that the licensee had identified both required and important circuits that

could impact safe shutdown. The inspectors reviewed the expert panel results for the

potential fire induced operations of components supporting safe shutdown at MNGP.

The expert panel performed this review in accordance with RG 1.189 and Guidance of

NEI 00-01, Revision 2. The purpose of the expert panel was to review the applicable

industry-developed Generic Owners Group List of MSOs for applicability to MNGP.

The expert panel was also tasked with considering plant-specific MSOs similar to those

in the Generic List, but not specifically listed. The expert panel identified several MSOs,

as applicable to MNGP, and provided recommendations to resolve these issues.

The following is a list of some MSO scenarios reviewed by the inspectors that the expert

panel recommended modifications to because of apparent violations of 10 CFR Part 50,

Appendix R,Section III.G:

(RCIC) test return to condensate storage tank (CST) valves with suction on the

suppression pool which may route the RCIC inventory to the CST;

valve. Multiple fire induced spurious operation of MO-2033 and other valve(s) on

the opposite train;

  • MSO 2.r - Spurious operation that creates Core Spray (CS) pump flow diversion

for injection to the reactor pressure vessel (RPV). Multiple fire induced faults on

MO-1750 circuit that may result in bypassing the torque limit switch; and

  • MSO 4.k - Dedicated CS system, spurious closure of normally open

RPV injection valve. Multiple fire induced faults on MO-1752 or MO1754 circuits

that may result in bypassing the torque limit switch for each valve.

The licensee entered all identified MSO scenarios into their CAP and initiated alternate

compensatory measures, in the form of documented operator rounds, as justified per the

Fire Protection Engineering Evaluation (FPEE 2010-001, Alternate Compensatory

Measures for MSOs Identified Non-Conformances). In addition, the licensee will perform

additional circuit analysis and evaluations for the non-conformances to determine the

appropriate resolutions prior to the end of the enforcement discretion per EGM 09-002.

The licensee evaluated the aforementioned identified MSOs and determined that these

types of issues would not significantly affect the plant margin of safety since they have

low risk of occurrence and low safety consequences.

The inspectors verified that selected safe shutdown cables had either been adequately

protected from the potentially adverse effects of fire damage or mitigated with approved

manual operator actions, or analyzed to show that fire-induced faults (e.g., hot shorts,

open circuits, and shorts to ground) would not prevent safe shutdown. In order to

accomplish this, the inspectors reviewed electrical schematics associated with each of

the selected safe shutdown components. In addition, the inspectors evaluated the

adequacy of the electrical circuits protective coordination for the safe shutdown

systems electrical power and instrumentation busses.

Based upon the inspectors review, it was determined that the aforementioned identified

noncompliances associated with MSOs were violations of 10 CFR Part 50, Appendix R,

Section III.G. Because the violations were associated with multiple fire induced circuit

faults and identified during the discretion period as described in EGM 09-002,

the NRC is exercising enforcement discretion in accordance with EGM 09-002.

7 Enclosure

b. Findings

No findings were identified.

1R06 Flooding (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the USAR, engineering calculations, and AOPs to identify licensee

commitments. The specific documents reviewed are listed in the Attachment to this

report. In addition, the inspectors reviewed licensee drawings to identify areas and

equipment that may be affected by internal flooding caused by the failure or

misalignment of nearby sources of water, such as the fire suppression or the circulating

water systems. The inspectors also reviewed the licensees corrective action documents

with respect to past flood-related items identified in the CAP to verify the adequacy of

the corrective actions. The inspectors performed a walkdown of the following plant

areas to assess the adequacy of watertight doors and verify drains and sumps were

clear of debris and were operable, and that the licensee complied with its commitments:

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b. Findings

No findings were identified.

1R07 Annual Heat Sink Performance (71111.07A)

.1 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the licensees testing of the 12 Residual Heat Removal (RHR)

systems heat exchanger efficiency test to verify that potential deficiencies did not mask

the licensees ability to detect degraded performance, to identify any common cause

issues that had the potential to increase risk, and to ensure that the licensee was

adequately addressing problems that could result in initiating events that would cause

an increase in risk. The inspectors reviewed the licensees observations as compared

against acceptance criteria, the correlation of scheduled testing and the frequency of

testing, and the impact of instrument inaccuracies on test results. Inspectors also

verified that test acceptance criteria considered differences between test conditions,

design conditions, and testing conditions. Documents reviewed for this inspection are

listed in the Attachment to this report.

This annual heat sink performance inspection constituted one sample as defined in

IP 71111.07-05.

8 Enclosure

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08G)

From March 14 through March 24, 2011, the inspectors conducted a review of the

implementation of the licensees inservice inspection (ISI) program for monitoring

degradation of the reactor coolant system, risk-significant piping and components, and

containment systems.

The inservice inspections described in Sections 1R08.1 and 1R08.5 below constituted

one inspection sample as defined in IP 71111.08 05.

.1 Piping Systems Inservice Inspection

a. Inspection Scope

The inspectors observed and/or reviewed the following non-destructive examinations

mandated by the American Society of Mechanical Engineers (ASME)Section XI Code to

evaluate compliance with the ASME Code Section XI and Section V requirements and if

any indications and defects were detected, to determine if these were dispositioned in

accordance with the ASME Code or an NRC-approved alternative requirement.

25, Report No. 2011UT033;

  • UT of the reactor head meriodonal weld 49/50, Report No. 2011UT035;
  • radiographic examination (RT) of the RCIC steam supply line PS-17-3,

Field Welds 1 and 2;

  • in-vessel visual inspection of jet pump riser support pad welds 7/8; and

(RHRSW) piping, weld 10, Report No. BOP- MT-11-057.

The inspectors reviewed the following examination completed during the previous

outage with relevant/recordable conditions/indications accepted for continued service to

determine if acceptance was in accordance with the ASME Code Section IX.

  • UT of nozzle to vessel weld; weld N-3C; Report No. 2009UT024.

The inspectors reviewed the following pressure boundary weld completed for a

risk-significant system since the beginning of the last refueling outage (RFO) to

determine if the licensee applied the pre-service non-destructive examinations and

acceptance criteria required by the ASME Code Section XI. Additionally, the inspectors

reviewed the welding procedure specification and supporting weld procedure

qualification records to determine if the weld procedure was qualified in accordance with

the requirements of Construction Code and the ASME Code Section IX.

b. Findings

No findings were identified.

9 Enclosure

.2 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI-related problems entered into the licensees

CAP and conducted interviews with licensee staff to determine if:

  • the licensee had established an appropriate threshold for identifying ISI-related

problems;

  • the licensee had performed a root cause (if applicable) and taken appropriate

corrective actions; and

  • the licensee had evaluated operating experience (OE) and industry generic

issues related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

On January 21, 2011, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

10 Enclosure

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

  • 12 EDG fuel oil level switch replacement;
  • CS system; and
  • non-essential diesel generator (DG-13).

The inspectors reviewed events, such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems, and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2), or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted three quarterly maintenance effectiveness samples as

defined in IP 71111.12-05.

b. Findings

No findings were identified.

11 Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • repair of leak on RWCU piping near regenerative heat exchangers;
  • evaluation of potential water intrusion into pre-amp enclosures for the

Division I source range monitors (SRMs) and intermediate-range monitors

(IRMs);

  • plant in yellow risk and shutdown limiting condition for operation (LCO) longer

than scheduled while replacing 12 EDG level switches;

  • RFO risk assessment and risk management following shutdown;
  • risk management of suspended fuel assembly during refuel bridge issues; and
  • 1N6 lockout during 1AR power transfer from 10 bank transformer.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work; discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor; and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Documents reviewed are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted

six samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • battery room ventilation issues involving V-EF-40B;
  • operations with the potential to drain the vessel classifications.

12 Enclosure

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and USAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with

the evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

These operability inspections constituted three samples as defined in IP 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

.1 Permanent Plant Modifications

a. Inspection Scope

The following engineering design package was reviewed and selected aspects were

discussed with engineering personnel:

and seat rings hard face material from Stellite 6 to Stellite 21).

This document and related documentation were reviewed for adequacy of the

associated 10 CFR 50.59 safety evaluation screening; consideration of design

parameters; implementation of the modification; post-modification testing; and relevant

procedures, design, and licensing documents were properly updated. The inspectors

observed ongoing and completed work activities to verify that installation was consistent

with the design control documents. During the current RFO, EC 14638 was used to

modify the disc and seating surface for three of the four outboard MSIVs.

The modification will change the MSIV disc and seat hard-faced material from Stellite 6

to Stellite 21.

This inspection constituted one permanent plant modification sample as defined in

IP 71111.18-05.

b. Findings

No findings were identified.

13 Enclosure

1R19 Post-Maintenance Testing (71111.19)

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance (PM) activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • reactor building railroad doors 45 and 46;
  • 14 RHR pump; and
  • 1B low vacuum scram pressure switch (PS-5-11C).

These activities were selected based upon the SSCs ability to impact risk.

The inspectors evaluated these activities for the following (as applicable): the effect of

testing on the plant had been adequately addressed; testing was adequate for the

maintenance performed; acceptance criteria were clear and demonstrated operational

readiness; test instrumentation was appropriate; tests were performed as written in

accordance with properly reviewed and approved procedures; equipment was returned

to its operational status following testing (temporary modifications or jumpers required

for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities

against TS, the USAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with PM tests to determine whether

the licensee was identifying problems and entering them in the CAP and that the

problems were being corrected commensurate with their importance to safety.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted four PM testing samples as defined in IP 71111.19-05.

b. Findings

No findings were identified.

1R20 Outage Activities (71111.20)

.1 Refueling Outage Activities

a. Inspection Scope

The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the

Refueling Outage (RFO), which began on March 5, 2011, and continued through the end

of the inspection period, to confirm that the licensee had appropriately considered risk,

industry experience, and previous site-specific problems in developing and implementing

a plan that assured maintenance of defense-in-depth. During the RFO, the inspectors

observed portions of the shutdown and cooldown processes and monitored licensee

14 Enclosure

controls over the outage activities listed below. Documents reviewed during the

inspection are listed in the Attachment to this report.

  • Licensee configuration management, including maintenance of defense-in-depth

commensurate with the OSP for key safety functions and compliance with the

applicable TS when taking equipment out-of-service;

  • Implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing;

  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error;

  • Controls over the status and configuration of electrical systems to ensure

that TS and OSP requirements were met, and controls over switchyard activities;

  • Controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system;

alternative means for inventory addition, and controls to prevent inventory loss;

  • Controls over activities that could affect reactivity;
  • Maintenance of SCT as required by TS;
  • Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage;

  • Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

left, which could block emergency core cooling system suction strainers, and

reactor physics testing;

  • Licensee identification and resolution of problems related to RFO activities.

This inspection constituted one RFO sample as defined in IP 71111.20-05.

b. Findings

Introduction

A finding of very low safety significance and non-cited violation (NCV) of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed

when the licensee failed to adequately implement the requirements of their fleet tagging

procedure, a procedure affecting quality, during maintenance on the safety-related

CST-88 B low pressure coolant injection (LPCI) fill line check valve. This failure

resulted in an unintentional breach of the condensate service water (CSW) system and

subjected workers to a potentially contaminated, pressurized water source. Additionally,

at the time of the breach, the CSW system was one of the water sources being credited

in support of the shutdown safety function of inventory control.

Description

On March 18, 2011, workers commenced the disassembly and inspection of CST-88,

the B LPCI Fill Line check valve. The workers had been briefed to expect that upon

disassembly of the valve they would experience a small amount of water drainage and

hence had installed a large-sized drainage device to accommodate the leakage.

15 Enclosure

However, when they began to disassemble the valve, upon loosening the bonnet bolts,

the workers were met with pressurized water. The workers determined that this amount

of water leakage was unexpectedly large and quickly retightened the bolts to restore the

valve back to its assembled condition, terminating the leakage.

The licensees investigation into this incident revealed that the check valve the workers

were disassembling had not been properly isolated. The clearance order referenced for

this maintenance activity had only isolated the valve (CST-91) immediately downstream

of the CST-88 check valve (among other valves associated with separate work

activities). The valve (CST-184) located immediately upstream of CST-88 was not

closed, leaving the check valve un-isolated from the pressurized CSW system.

This inadequate isolation left workers unprotected from the pressurized CSW header,

and led to a temporary breach of the CSW system, a system which was being credited

in support of the shutdown safety function of inventory control.

A review of the WO and clearance development activities for this task revealed that on

January 10, 2010, Clearance Order (CO) 37264 was created to support draining and

isolating portions of the RHR B system. While the CO was still in the planning stages,

other WOs were added to it including the WO for the CST-88 check valve maintenance

(WO 394266). In total, 20 additional WOs were added to CO 37264 prior to its approval

and two additional activities were added following its approval. While CO 37264 was

originally generated to support work on the RHR B system, the licensees tagging

procedure allows them to place multiple WOs under one clearance. However, the

procedure also requires that the CO be appropriately developed and reviewed to ensure

that safe boundaries are established for all maintenance activities associated with the

clearance.

During the planning and approval processes for CO 37264 when WO 394266 was added

to its scope, the following errors occurred:

  • during the planning stages, the CO preparer failed to use available references or

perform a walkdown to develop a CO that included appropriate boundaries for all

work associated with the CO 37264;

  • when the CO containing this work was routed for approval, the craft approver

(Supervisor/Lead Clearance Order Holder in the approval chain) failed to verify

that a safe boundary was prepared for all the work contained in CO 37264 by

using available references or walkdowns; and

  • during the approval process, the approving Senior Reactor Operator (SRO)

(Operations Approver) failed to adequately verify that a safe work boundary was

established for work associated with CO 37264.

After CO 37264 was approved, the following additional errors occurred during execution

of the clearance and WO 394266:

  • prior to allowing maintenance to commence work on the procedure,

the Operations Shift Supervision authorized the maintenance group to begin

work on WO 394266, but failed to appropriately authorize the commencement of

work on the procedure being performed under the WO, and failed to complete

the prerequisites specified in the procedure;

16 Enclosure

  • prior to initiating the work activity, the work supervisor (Supervisor/Lead

Clearance Order Holder for the work group) failed to ensure that the tagging

boundary was appropriate for the work being performed; assessment of the

boundary included a craft walkdown, which compared the CO only to the tags

hung on the isolated valves, rather than comparing the CO to plant diagrams or

using insights from the physical valve location in the system to verify appropriate

boundaries; and

  • prior to commencing the work, the supervisor failed to adequately brief the

workers on the tagging boundaries for the work.

Fleet Tagging Procedure, FP-OP-TAG-01, Revision 10, Sections 5.3 and 5.4,

specify the requirements for development and approval of CO checklists for WOs.

These sections state, in part:

  • the Clearance Order/Clearance Order Checklist Preparer SHALL prepare a

Clearance Order and Clearance Order Checklist using available references

and/or walkdowns. Controlled documents SHALL be used, when available

(Sec. 5.3);

  • the Clearance Order/Clearance Order Checklist Preparer SHALL complete the

information field for clearance order steps - to establish a safe work boundary,

as required (Sec. 5.3);

  • the Operations Approver SHALL verify a safe boundary has been established

(Sec. 5.4); and

  • the Supervisor/Lead Clearance Order Holder review SHALL verify that a safe

work boundary has been prepared, using available references and/or walkdowns

(Sec. 5.4).

Section 5.6 of Procedure FP-OP-TAG-01 specifies requirements of supervisors when

commencing a work activity:

  • the Supervisor/Lead Clearance Order Holder review SHALL ensure the tagging

boundary is adequate for the work to be performed; and

  • the Supervisor/Lead Clearance Order Holder review SHALL brief clearance order

holders (worker) on tagging boundaries, potential hazards/stored energy

sources, and field activities.

Additionally, when the time came to perform the work, the Operations Shift Supervision

signed the work order task Authorization to start work. However, the individual did not

sign the Approval to Commence for the procedure being implemented in the WO.

This procedure, 0255-22-IA-1, CST-88 B LPCI Fill Line Check Valve Test, contained

two prerequisites to be performed prior to beginning work on the procedure steps.

One of those prerequisites required verification that CST-88 is isolated as required.

Neither prerequisite was completed before the procedure steps were begun.

The CO development, approval, and execution activities associated with WO 394266

failed to identify the need to close the inlet isolation valve for the check valve that was

being disassembled and inspected, in order to isolate the check valve from the

CSW header. Therefore, these activities failed to ensure that the tagging boundary was

adequate for the work being performed, as required by the procedure.

17 Enclosure

The licensee entered this issue into their corrective action program (CAPs 1275935 and

1275963). Immediate corrective actions taken by the licensee included restoring the

CST-88 check valve to its installed configuration to terminate the water leakage and

revising the clearance boundary for the work to include the appropriate isolation valve.

The site performed a review of all other WOs associated with CO 37264 to validate that

safe work boundaries existed for all associated work activities and reviewed the other

COs prepared and approved by personnel associated with the event. Additionally, to

highlight the significance of the event, the licensee reset their site event clock,

communicated lessons learned from the event to the site, and assembled a team to

perform a root cause evaluation (RCE).

Analysis

The inspectors determined that the licensees failure to adequately implement their

tagging process to protect workers and equipment from the effects of breaching the

pressurized CSW header during maintenance on a safety-related check valve was a

performance deficiency because it was the result of the failure to meet a requirement,

the cause was reasonably within the licensees ability to foresee and correct, and should

have been prevented. The inspectors determined that the contributing cause that

provided the most insight into the performance deficiency was associated with the

cross-cutting area of Human Performance, having work control components, and

involving aspects associated with appropriately planning work activities by incorporating

job site conditions impacting plant systems and components H.3(a).

The inspectors screened the performance deficiency per IMC 0612, Power Reactor

Inspection Reports, Appendix B, and determined that the issue was more than minor

because the performance deficiency could have reasonably been viewed as a precursor

to a more significant event. In this instance, the performance deficiency resulted in an

unintentional breach of the operating CSW system and subjected workers to a

potentially contaminated, pressurized water source. Additionally, at the time of the

breach, the CSW system was one of the water sources being credited in support of the

shutdown safety function of inventory control. The inspectors applied IMC 0609,

Significance Determination Process, Appendix G, "Shutdown Operations Significance

Determination," Attachment 1, to this finding. The finding was determined to have very

low safety significance because it did not adversely affect core heat removal, inventory

control, power availability, containment control, or reactivity guidelines (Green).

Enforcement

Title 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"

requires, in part, that activities affecting quality shall be prescribed by documented

procedures, of a type appropriate to the circumstances, and shall be accomplished in

accordance with these procedures. Contrary to this requirement, the licensee failed to

adequately implement the requirements of Procedure FP-OP-TAG-01, Fleet Tagging,

a procedure affecting quality, during maintenance on the safety-related CST-88 B LPCI

Fill Line check valve. This failure resulted in a breach of the CSW system, led to

workers being unprotected from a potentially contaminated, pressurized water source,

and introduced the potential to impact a system being credited in support of a shutdown

safety function. Because the violation was of very low safety significance and was

entered into the licensees corrective action program (CAPs 1275935 and 1275963),

this violation is being treated as an NCV, consistent with Section 2.3.2 of the

18 Enclosure

NRC Enforcement Policy. (NCV 05000263/2011002-01; Inadequate System Isolation

during Check Valve Maintenance)

1R22 Surveillance Testing (71111.22)

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • surveillance procedure 0192, diesel fuel quality check (routine);
  • surveillance procedure 0007-A, condenser low vacuum scram instruments test

and calibration (routine);

  • surveillance procedure 0021-01, reactor low level scram and low-low level

isolation transmitter calibration procedure (routine);

recirc pump trip with reactor feed pump and turbine trip testing (routine);

  • procedure 0255-03-IA-2A, CS - shutdown valve operability test (inservice test

(IST)); and

  • local leak rate test (LLRT) procedure137-07A, reactor steam supply valves leak

rate testing (containment isolation valve (CIV) LLRT).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the USAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for IST activities, testing was performed in accordance with the

applicable version of Section XI, ASME code, and reference values were

consistent with the system design basis;

19 Enclosure

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing samples, one IST sample,

and one CIV sample as defined in IP 71111.22, Sections -02 and -05.

b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on

February 9, 2011, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities.

The inspectors observed emergency response operations in the control room simulator

and emergency offsite facility to determine whether the event classification, notifications,

and protective action recommendations were performed in accordance with procedures.

The inspectors also attended the licensee drill critique to compare any inspector

observed weakness with those identified by the licensee staff in order to evaluate the

critique and to verify whether the licensee staff was properly identifying weaknesses

and entering them into the corrective action program. As part of the inspection, the

inspectors reviewed the drill package and other documents listed in the Attachment to

this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b. Findings

No findings were identified.

20 Enclosure

2. RADIATION SAFETY

2RS5 Radiation Monitoring Instrumentation (71124.05)

This inspection constituted one complete sample as defined in IP 71124.05-05.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the plant Final Safety Analysis Report (FSAR) to identify

radiation instruments associated with monitoring area radiological conditions including

airborne radioactivity, process streams, effluents, materials/articles, and workers.

Additionally, the inspectors reviewed the instrumentation and the associated

TS requirements for post-accident monitoring instrumentation including instruments used

for remote emergency assessment.

The inspectors reviewed a listing of in-service survey instrumentation including air

samplers and small article monitors, along with instruments used to detect and analyze

workers external contamination. Additionally, the inspectors reviewed personnel

contamination monitors and portal monitors including whole-body counters to detect

workers internal contamination. The inspectors reviewed this list to assess whether an

adequate number and type of instruments are available to support operations.

The inspectors reviewed licensee and third-party evaluation reports of the radiation

monitoring program since the last inspection. These reports were reviewed for insights

into the licensees program and to aid in selecting areas for review (smart sampling).

The inspectors reviewed procedures that govern instrument source checks and

calibrations, focusing on instruments used for monitoring transient high radiological

conditions, including instruments used for underwater surveys. The inspectors reviewed

the calibration and source check procedures for adequacy and as an aid to smart

sampling.

The inspectors reviewed the area radiation monitor alarm setpoint values and setpoint

bases as provided in the TSs and the FSAR.

The inspectors reviewed effluent monitor alarm setpoint bases and the calculational

methods provided in the offsite dose calculation manual (ODCM).

b. Findings

No findings were identified.

.2 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors walked down effluent radiation monitoring systems, including at least one

liquid and one airborne system. Focus was placed on flow measurement devices and all

accessible point-of-discharge liquid and gaseous effluent monitors of the selected

systems. The inspectors assessed whether the effluent/process monitor configurations

21 Enclosure

align with ODCM descriptions and observed monitors for degradation and out-of-service

tags.

The inspectors selected portable survey instruments in use or available for issuance and

assessed calibration and source check stickers for currency as well as instrument

material condition and operability.

The inspectors observed licensee staff performance as the staff demonstrated source

checks for various types of portable survey instruments. The inspectors assessed

whether high-range instruments are source checked on all appropriate scales.

The inspectors walked down area radiation monitors and continuous air monitors to

determine whether they are appropriately positioned relative to the radiation sources or

areas they were intended to monitor. Selectively, the inspectors compared monitor

response (via local or remote control room indications) with actual area conditions for

consistency.

The inspectors selected personnel contamination monitors, portal monitors, and small

article monitors, and evaluated whether the periodic source checks were performed in

accordance with the manufacturers recommendations and licensee procedures.

b. Findings

No findings were identified.

.3 Calibration and Testing Program (02.03)

Process and Effluent Monitors

a. Inspection Scope

The inspectors selected effluent monitor instruments (such as gaseous and liquid)

and evaluated whether channel calibration and functional tests were performed

consistent with radiological effluent TSs/ODCM. The inspectors assessed whether:

(a) the licensee calibrated its monitors with National Institute of Standards and

Technology traceable sources; (b) the primary calibrations adequately represented the

plant nuclide mix; (c) when secondary calibration sources were used, the sources were

verified by the primary calibration; and (d) the licensees channel calibrations

encompassed the instruments alarm set-points.

The inspectors assessed whether the effluent monitor alarm setpoints are established as

provided in the ODCM and station procedures.

For changes to effluent monitor setpoints, the inspectors evaluated the basis for

changes to ensure that an adequate justification exists.

b. Findings

No findings were identified.

22 Enclosure

Laboratory Instrumentation

a. Inspection Scope

The inspectors assessed laboratory analytical instruments used for radiological analyses

to determine whether daily performance checks and calibration data indicate that the

frequency of the calibrations is adequate and there were no indications of degraded

instrument performance.

The inspectors assessed whether appropriate corrective actions were implemented in

response to indications of degraded instrument performance.

b. Findings

No findings were identified.

Whole Body Counter

a. Inspection Scope

The inspectors reviewed the methods and sources used to perform whole body count

functional checks before daily use of the instrument and assessed whether check

sources were appropriate and align with the plants isotopic mix.

The inspectors reviewed whole body count calibration records since the last inspection

and evaluated whether calibration sources were representative of the plants source

term and that appropriate calibration phantoms were used. The inspectors looked for

anomalous results or other indications of instrument performance problems.

b. Findings

No findings were identified.

Post-Accident Monitoring Instrumentation

a. Inspection Scope

Inspectors selected drywell high-range monitors and reviewed the calibration

documentation since the last inspection.

The inspectors assessed whether an electronic calibration was completed for all range

decades above 10 rem/hour, and whether at least one decade at or below 10 rem/hour

was calibrated using an appropriate radiation source.

The inspectors assessed whether calibration acceptance criteria are reasonable,

accounting for the large measuring range and the intended purpose of the instruments.

The inspectors selected two effluent/process monitors that are relied on by the licensee

in its emergency operating procedures as a basis for triggering emergency action levels

and subsequent emergency classifications, or to make protective action

recommendations during an accident. The inspectors evaluated the calibration and

availability of these instruments.

23 Enclosure

The inspectors reviewed the licensees capability to collect high-range, post-accident

iodine effluent samples.

As available, the inspectors observed electronic and radiation calibration of these

instruments to verify conformity with the licensees calibration and test protocols.

b. Findings

No findings were identified.

Portal Monitors, Personnel Contamination Monitors, and Small Article Monitors

a. Inspection Scope

For each type of these instruments used on site, the inspectors assessed whether the

alarm setpoint values are reasonable under the circumstances to ensure that licensed

material is not released from the site.

The inspectors reviewed the calibration documentation for each instrument selected and

discussed the calibration methods with the licensee to determine consistency with the

manufacturers recommendations.

b. Findings

No findings were identified.

Portable Survey Instruments, Area Radiation Monitors, Electronic Dosimetry, and

Air Samplers/Continuous Air Monitors

a. Inspection Scope

The inspectors reviewed calibration documentation for at least one of each type of

instrument. For portable survey instruments and area radiation monitors, the inspectors

reviewed detector measurement geometry and calibration methods and had the licensee

demonstrate use of its instrument calibrator as applicable. The inspectors conducted

comparison of instrument readings versus an NRC survey instrument if problems were

suspected.

As available, the inspectors selected portable survey instruments that did not meet

acceptance criteria during calibration or source checks to assess whether the licensee

had taken appropriate corrective action for instruments found significantly out of

calibration (greater than 50 percent). The inspectors evaluated whether the licensee

had evaluated the possible consequences of instrument use since the last successful

calibration or source check.

b. Findings

No findings were identified.

24 Enclosure

Instrument Calibrator

a. Inspection Scope

As applicable, the inspectors reviewed the current output values for the licensees

portable survey and area radiation monitor instrument calibrator unit(s). The inspectors

assessed whether the licensee periodically measures calibrator output over the range of

the instruments used through measurements by ion chamber/electrometer.

The inspectors assessed whether the measuring devices had been calibrated by a

facility using National Institute of Standards and Technology traceable sources and

whether corrective factors for these measuring devices were properly applied by the

licensee in its output verification.

b. Findings

No findings were identified.

Calibration and Check Sources

a. Inspection Scope

The inspectors reviewed the licensees 10 CFR Part 61, Licensing Requirements for

Land Disposal of Radioactive Waste, source term to assess whether calibration sources

used were representative of the types and energies of radiation encountered in the plant.

b. Findings

No findings were identified.

.4 Problem Identification and Resolution (02.04)

a. Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring

instrumentation were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensee CAP. The inspectors assessed

the appropriateness of the corrective actions for a selected sample of problems

documented by the licensee that involve radiation monitoring instrumentation.

b. Findings

No findings were identified.

25 Enclosure

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness, Public and Occupational Radiation Safety

4OA1 Performance Indicator Verification (71151)

.1 Unplanned Scrams per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical

Hours Performance Indicator (PI) for the period from the 1st Quarter 2010 to the

4th Quarter 2010. To determine the accuracy of the PI data reported during this period,

PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

event reports, and NRC Integrated Inspection Reports for that period to validate the

accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified.

This inspection constituted one unplanned scrams per 7000 critical hours sample as

defined in IP 71151-05.

b. Findings

No findings were identified.

.2 Unplanned Scrams with Complications

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams with

Complications PI for the period from the 1st Quarter 2010 to 4th Quarter 2010.

To determine the accuracy of the PI data reported during those periods, PI definitions

and guidance contained in the NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, dated October 2009, were used.

The inspectors reviewed applicable licensee operator narrative logs, issue reports, event

reports, and NRC Integrated Inspection Reports for that period to validate the accuracy

of the submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified.

This inspection constituted one unplanned scrams with complications sample as defined

in IP 71151-05.

b. Findings

No findings were identified.

26 Enclosure

.3 Unplanned Transients per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Transients per 7000

Critical Hours PI for the period from the 1st Quarter of 2010 to the 4th Quarter of 2010.

To determine the accuracy of the PI data reported during those periods, PI definitions

and guidance contained in the NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, dated October 2009, were used.

The inspectors reviewed the licensees operator narrative logs, issue reports,

maintenance rule records, event reports, and NRC Integrated Inspection Reports for that

period to validate the accuracy of the submittals. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

the PI data collected or transmitted for this indicator and none were identified.

This inspection constituted one unplanned transients per 7000 critical hours sample as

defined in IP 71151-05.

b. Findings

No findings were identified.

.4 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences PI for the period from the 2nd Quarter 2010 through January 2011.

To determine the accuracy of the PI data reported during those periods, PI definitions

and guidance contained in the NEI Document 99 02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, was used. The inspectors reviewed the

licensees assessment of the PI for occupational radiation safety to determine if indicator

related data was adequately assessed and reported. To assess the adequacy of the

licensees PI data collection and analyses, the inspectors discussed with radiation

protection staff, the scope, and breadth of its data review, and the results of those

reviews. The inspectors independently reviewed electronic dosimetry dose rate and

accumulated dose alarm and dose reports and the dose assignments for any intakes

that occurred during the time period reviewed to determine if there were potentially

unrecognized occurrences. The inspectors also conducted walkdowns of numerous

locked high and very high radiation area entrances to determine the adequacy of the

controls in place for these areas.

This inspection constituted one occupational radiological occurrences sample as defined

in IP 71151-05.

b. Findings

No findings were identified.

27 Enclosure

.5 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent TS (RETS)/

ODCM Radiological Effluent Occurrences PI for the period of June 2010 through

January 2011. The inspectors used PI definitions and guidance contained in the

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6, to determine the accuracy of the PI data reported during those periods.

The inspectors reviewed the licensees issue report database and selected individual

reports generated since this indicator was last reviewed to identify any potential

occurrences such as unmonitored, uncontrolled, or improperly calculated effluent

releases that may have impacted offsite dose. The inspectors reviewed gaseous

effluent summary data and the results of associated offsite dose calculations for selected

dates to determine if indicator results were accurately reported. The inspectors also

reviewed the licensees methods for quantifying gaseous and liquid effluents and

determining effluent dose. Documents reviewed are listed in the Attachment to this

report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample

as defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

28 Enclosure

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings were identified.

.3 Selected Issue Follow-Up Inspection: Several CAPs Regarding Fatigue Rule Work Hour

Violations

a. Inspection Scope

During a review of items entered in the licensees CAP, the inspectors recognized a

corrective action item documenting multiple violations of NRC requirements associated

with the fatigue rule. In addition, the inspectors noted that there were multiple

CAPs documenting human performance errors that may result in violations of

NRC fatigue rule requirements, and a few other CAPs documenting other instances of

individual work hour violations. The inspectors reviewed the licensees actions to

address the violations and examined the sites threshold for determining whether an

adverse trend exists in this area. In addition, the inspectors reviewed all fatigue rule

related CAPs generated over the previous year and the causal analyses that were

performed when trends were identified. This review focused on determining whether the

licensee was adequately evaluating these issues, whether the corrective actions

developed by the licensee were appropriate given the results of causal evaluations, and

whether the actions the site has taken to address these issues had been effective.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

During this inspection, the inspectors identified a concern regarding the licensees

implementation of fatigue rule requirements. Specifically, the inspectors reviewed an

29 Enclosure

apparent cause evaluation (ACE) that the licensee had performed after identifying

several violations of NRC fatigue rule requirements. The inspectors noted that one of

the corrective actions developed and implemented in October 2010, as a result of this

evaluation, involved tripling the period of planned shift turnover time on the front end of

schedules of individuals in one department, to account for the turnover period on the

back end of the shift. As a result of this action, the scheduled turnover period for

personnel in this department was not consistent with NRC guidance on reasonable

amounts of time for these activities. In addition, the inspectors noted that this turnover

time period was applied to the front end of the schedules of all personnel in this

department regardless of the amount of time spent performing actual turnover activities.

This may potentially be in conflict with NRC regulations, specifically with respect to

10 CFR 26.205(b)(1), regarding calculation of work hours, 10 CFR 26.205(d) regarding

work hour controls, and 10 CFR 26.203(b)(2) regarding implementation of fatigue rule

procedures to ensure compliance with 10 CFR 26.205.

The NRC inspectors plan to review actual turnover activities and associated records for

the site as a whole to examine how the corrective action of concern has been put into

practice. Pending NRC review of additional licensee information regarding site-wide

practices for exclusion of shift turnover activities, as well as information on how the

application of a fixed and potentially artificially long turnover period has affected actual

work hours reported for individuals at the site, this issue will be treated as an

Unresolved Item (URI) (URI)5000263/2011002-02; Calculation of Work Hours during

Fatigue Rule Implementation).

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 Observations During Plant Downpower to Approximately 50 Percent Power

a. Inspection Scope

On March 4, 2011, the inspectors observed control room operators during power

reductions from approximately full power to 50 percent power. The inspectors focus

was on overall command and control, procedure usage, and conservative practices

while maneuvering the plant.

b. Findings

No findings were identified.

This event follow-up review of a non-routine evolution constituted one sample as defined

in IP 71153-05.

.2 Observation of New Fuel Receipt Inspections Conducted on the Refueling Floor

a. Inspection Scope

The inspectors performed several observations of licensee activities associated with

receipt of new fuel. These activities included unpackaging, inspecting, channeling, and

placement of new fuel in the spent fuel pool. Documents reviewed in this inspection are

listed in the Attachment to this report.

This event follow-up review constituted one sample as defined in IP 71153-05.

30 Enclosure

b. Findings

Introduction

A finding of very low safety significance and NCV of Technical Specification 5.4,

Procedures, was identified by the inspectors when the licensee failed to implement the

requirements of their foreign material exclusion (FME) and control procedure during new

fuel receipt activities. Specifically, the inspectors observed two operators exiting and

re-entering a Level 1 FME area, without knowledge of the FME monitor, at a point that

was not being controlled by the FME monitor.

Description

Over a time period of approximately one week, the inspectors observed the licensee

perform several activities associated with the receipt of new fuel. These activities

included unpackaging new fuel, inspection of the fuel assemblies, installation of fuel

assembly channels, and placing the new fuel in the spent fuel pool. A majority of

these activities were performed within the boundaries of a Level 1 FME area.

On January 24, 2011, during one of these observations, the inspectors noted that two

operators, who were participating in the fuel receipt inspection activities, entered the

FME area, without the FME monitors knowledge, at a point that was not established as

the FME area access point.

The licensee utilizes Procedure FP-MA-FME-01, Foreign Material Exclusion and

Control, to implement its processes for controlling and accounting for material, tools,

and parts to preclude their uncontrolled introduction into an open system or component

during maintenance, modification, or inspection activities. The inspectors reviewed this

procedure and discovered the following requirements which were applicable to the new

fuel receipt inspection activities.

  • Workers were responsible for adhering to and maintaining FME requirements

(Step 3.2.2);

  • FME monitors were responsible for monitoring work activities for proper

FME work practices and inspecting personnel, tools, and materials entering and

leaving the FME area (Steps 3.4.7 and 3.4.8);

  • Loss of FME control may exist when the FME monitor is required but not

attentive or present (Step 4.11, in part);

  • Level 1 FME area is highest level of FME control imposed on an area or system

and is required where new fuel is inspected (Step 5.1.1, in part); and

  • Formal FME control plan is required for large projects with FME Level 1 activities

and prepared utilizing form QF 1812, Foreign Material Exclusion Control Plan,

(Step 5.2.1).

The inspectors reviewed the QF 1812 associated with new fuel receipt activity.

The inspectors noted that the following requirements were included as part of that plan.

  • The FME monitor will ensure personnel entering the FME Level 1 Zone are

appropriately prepared to enter the area by securing all personal items and by

logging all items carried into the area. The FME monitor is one of the last

barriers to the prevention of foreign material entering the FME Level 1 Zone and

as such, the FME monitor must be vigilant with respect to their assigned duties.

31 Enclosure

The inspectors reviewed the training material (MT-SHE-GEN-001L) used in the

qualification of the FME monitors. This material specifically covers the duties of an

FME monitor to include: controlling the FME area when material or personnel control is

established; stopping any entry that is not within the guidelines of the procedure;

monitoring work activities for proper FME work practices; and inspecting personnel

entering and leaving an FME area.

  • All personnel that are required to enter the FME Level 1 Zone shall have read

and/or been briefed on the FME plan;

  • All personnel entering the FME Level 1 Zone will be required to be FME qualified.

The inspectors reviewed the training material (M-7730F-012) used in FME training.

With respect to FME boundaries, the training material specifically states If you see a

FME boundary, dont cross it without approval by the supervisor /FME Monitor.

Subsequent to observing the operators enter the FME area at an unmonitored point;

the inspectors brought this to the attention of the FME monitor. When questioned by

the inspectors, the FME monitor informed the inspectors that he was not aware that the

operators had entered the FME area. The inspectors also brought this issue to the

attention of the SRO that was overseeing the new fuel receipt activities.

Corrective actions taken to address this issue included stopping the work, re-briefing the

workers on FME controls, and verifying no additional material was introduced to the

FME area by the operators. The licensee entered this issue into their corrective action

program as CAP 0126760.

Analysis

The inspectors determined that the licensees failure to adequately implement the

requirements of their FME and control procedure during new fuel receipt activities to

prevent the unmonitored access of two operators into a Level 1 FME area was a

performance deficiency because it was the result of the failure to meet a requirement or

a standard, the cause was reasonably within the licensees ability to foresee and correct,

and should have been prevented. The inspectors determined that the contributing cause

that provided the most insight into the performance deficiency was associated with the

cross-cutting area of Human Performance, having Work Practices components, and

involving aspects associated with the licensee defining and effectively communicating

expectations regarding procedural compliance and personnel following procedures

H.4(b).

The inspectors screened the performance deficiency per IMC 0612, Power Reactor

Inspection Reports, Appendix B, and determined that the issue was more than minor

because it impacted the human performance attribute of the Barrier Integrity

Cornerstones objective to provide reasonable assurance that physical design barriers

(fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events. The inspectors applied IMC 0609,

Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, to this

finding. The inspectors utilized Column 3 of the Table 4a worksheet to screen the

finding. Since the finding only had the potential to impact the fuel barrier, the finding was

screened to be of very low safety significance (Green).

32 Enclosure

Enforcement

Monticello Nuclear Generating Plant TS, Section 5.4.1.a, requires that written

procedures shall be established, implemented, and maintained covering applicable

procedures recommended in RG 1.33, Revision 2, Appendix A, February 1978.

Contrary to this requirement on January 24, 2011, the licensee failed to successfully

implement Procedure FP-MA-FME-01, Foreign Material Exclusion and Control,

a maintenance procedure, during new fuel receipt and channeling activities. Specifically,

two operators exited and reentered a Level 1 FME area, without the knowledge of the

FME monitor, at a point not controlled by the FME monitor. Because the violation was

of very low safety significance and was entered into the licensees corrective action

program (AR 126760), this violation is being treated as NCV, consistent with

Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000263/2011002-03; Failure to

Control a Level 1 FME Area during New Fuel Receipt Activities)

.3 (Closed) Licensee Event Report (LER) 05000263/2010-006-00: Mode Change Made

with Primary Containment Isolation Valves Inoperable

On November 22, 2010, the plant was in Mode 4 with preparations for startup in

progress. The duty crew transferred the reactor vent path to the path through

main steam line drain valves MO-2373 (main steam line drain - inboard), MO-2374

(main steam line drain - outboard), and MO-2565 (steam line drain orifice bypass).

The valves were opened and their associated breakers were tagged open. At 16:47,

the change from Mode 4 to Mode 2 was completed. At 17:00, a page announcement

was made that reactor startup was commencing. The on-coming operations work

control manager recalled helping tag open MO-2373 and MO-2374, which are primary

containment isolation valves (PCIVs), on the previous night shift. He called the control

room to verify the valves had been restored prior to the mode change. He immediately

notified the duty crew and operations management of the TS violation when he was

informed they had not been restored. Startup activities were halted pending

investigation and resolution of the issue. Primary containment isolation valves

operability was subsequently restored. Startup activities were recommenced later in the

shift after prerequisites had been verified as completed and a stand-down was

conducted.

The licensee entered this issue in to their corrective action program as CAP 1259879

and conducted a Root Cause Evaluation (RCE). The licensee determined that

individuals in key roles and oversight positions did not employ sufficient barriers to

ensure error free results, during preparation for and execution of, a complex evolution

(reactor startup) which relied heavily upon knowledge and experience. In addition to

this, the licensee identified two contributing causes. The licensee identified that some

procedure quality issues existed with procedures and checklists necessary for startup.

Secondly, they identified organizational weakness, in that the operability of TS required

equipment was not assessed, evaluated, or rigorously tracked when not in the mode of

applicability for the LCO.

This licensee-identified finding involved a violation of TS 3.0.4. The enforcement

aspects of this violation are discussed in Section 4OA7 of this report. Documents

reviewed as part of this inspection are listed in the Attachment to this report.

This LER is closed.

33 Enclosure

.4 (Closed) Licensee Event Report (LER) 05000263/2009-001-02:

Containment Overpressure Not Ensured in the Appendix R Analysis

The licensee issued Licensee Event Reports (LER 05000263-2009-001-00 and

LER 05000263-2009-001-01) regarding the licensees failure to consider the spurious

opening and venting of the primary containment, via purge and vent valves, in the event

of a fire in the main control room or cable spreading room. Both LER revisions were

closed in Inspection Report 05000263/2009004 and documented as a violation of

NRC requirements. Because the licensee was transitioning to NFPA 805 and the

violation met the criteria established by the NRC Interim Enforcement Policy Regarding

Enforcement Discretion for Certain Fire Protection Issues (10 CFR Part 50.48(c)) for

licensee in NFPA 805 transition, the NRC exercised enforcement discretion to not cite

the violation in accordance with the NRCs Enforcement Policy. On December 22, 2010,

the licensee provided an update to LER 05000263-2009-001-02 to reflect their

withdrawal of the letter of intent to voluntarily implement 10 CFR 50.48(c) at the MNGP.

On May 14, 2009, the NRC issued EGM 09-002, Enforcement Discretion for

Fire Induced Circuit Faults, dated May 14, 2009, which authorized enforcement

discretion for non-compliance issues associated with fire induced multiple circuit cable

faults, providing that the licensee identified the non-compliances, entered them into their

CAPs, and instituted appropriated compensatory measures until the issues were

corrected, within the six month period following a planned revision to RG 1.189,

Fire Protection for Nuclear Power Plants. Regulatory Guide 1.189, Revision 2,

issued in October 2009, provided a method acceptable to the NRC to evaluate and

resolve multiple fire induced circuit faults. After the six month period designated for the

identification of non-compliances, the EGM further authorized enforcement discretion for

an additional 30 month period, for licensees to resolve the identified multiple fire-induced

circuit fault issues.

The inspectors screened this violation and determined that because the violation was

associated with multiple fire induced circuit faults and was identified during the discretion

period as described in EGM 09-002, the NRC is exercising enforcement discretion for

this violation in accordance with EGM 09-002. This LER is closed.

.5 (Closed) Licensee Event Report (LER) 05000263/2011-002-00: ESF [Engineered

Safety Feature] Actuation Due to a Failed Power Supply

On December 20, 2010, the plant was in Mode 1 operating at 100 percent reactor power

when the 'A' Division of the fuel pool/reactor building exhaust plenum primary power

supply failed. The failure resulted in upscale trips on both the fuel pool and reactor

building ventilation plenum radiation monitors. This condition resulted in closure of the

Group II PCIVs, isolation of SCT, initiation of the standby gas treatment system (SBGT),

and a transfer of the control room ventilation (CRV) and control room emergency

filtration (CREF) systems to the high radiation mode. The licensee entered the

appropriate TSs and verified that radiation levels were normal in the affected areas.

The isolation signals were reset and the SCT and CRV/filtration systems were restored

to a normal lineup. All systems functioned properly and there were no human

performance errors associated with this event.

A subsequent investigation identified that the 24 V DC module of the power supply had

failed due to a failure of the C20 Tantalum capacitor on the output of the module.

The capacitor failure was attributed to a manufacturing defect occurring approximately

34 Enclosure

six days after installation. The power supply was subsequently replaced and the

affected components were returned to service.

A similar power supply was installed in the B Division fuel pool/reactor building exhaust

plenum radiation monitor; however, its capacitors were from a different lot. Additionally,

the B Division power supply had not shown any issues since it was installed on

December 2, 2010, or during extensive bench testing occurring prior to installation.

The licensee entered this issue into its corrective action program as CAP 01263610.

The inspectors evaluation did not identify any concerns with the licensees response to

this issue. Since the cause of the event was due to equipment failure and not a licensee

performance deficiency, there is no violation or finding associated with this event.

This LER is closed.

This event follow up constituted one sample as defined in IP 71153-05.

.6 (Closed) Licensee Event Report (LER) 05000263/2010-004-00:

Secondary Containment Briefly Inoperable Due to Simultaneous Opening of

Airlock Doors

On November 4, 2010, at approximately 11:25 with the plant operating in Mode 1 at

93 percent power, both doors for airlock 124 (main access to reactor building) were

inadvertently opened simultaneously, breaching the Secondary Containment (SCT)

boundary. Upon recognition that both airlock doors were open, plant personnel took

prompt actions to ensure that at least one of the airlock doors was closed and the

control room was informed that SCT had been breached for approximately 5 seconds.

The control room staff determined, for the time that both airlock doors were open,

that SCT was inoperable and that the event was reportable under 10 CFR 50.72

(b)(3)(v)(C and D) - events or conditions that could have prevented a safety function of

structures or systems that are needed to control the release of radioactive material or

mitigate the consequences of an accident.

Evaluation of the issue by the licensee determined that the cause of the airlock

124 breach was an intermittent failure of the magnetic bond sensor on the door due to a

lack of periodic maintenance. Corrective actions taken by the licensee to address the

cause of this event included generating WOs to replace the magnets and switches for

the airlock interlock and to develop a periodic interlock component maintenance items

list for inclusion in their preventive maintenance program.

The inspectors did not identify any significant issues during the review of this LER.

This LER is closed.

4OA5 Other Activities

.1 Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the INPO plant assessment conducted

during the weeks of November 30, 2009 and December 7, 2009. The inspectors

reviewed the report to ensure that issues identified were consistent with the

35 Enclosure

NRC perspectives of licensee performance and to verify if any significant safety issues

were identified that required further NRC follow-up.

b. Findings

No findings were identified.

.2 (Closed) Unresolved Item (URI) 05000263/2010008-01: Potential Concern with the

One-time Inspection Program Related to Butt Welds

During the post-approval license renewal inspection, the inspectors identified an

URI due to concerns of the one-time inspection program. This URI, documented in

Inspection Report 05000263/2010008, was related to changes the licensee made to

their original license renewal application. Specifically, in the March 25, 2006, license

renewal annual update (ML060800360), the licensee provided details of changes made

to the original license renewal application. With respect to Class 1 small bore piping, the

licensee determined that all piping in this inspection group is of actual diameter two

inches and less and that only socket weld connections are used in such applications.

Therefore, the licensee committed to perform inspections of this piping for the One-Time

Inspection (OTI) Program that will consist of visual testing VT-2 examinations during

pressure testing for system leaks upon return to service from outages and destructive

examinations of any socket welds removed from service prior to the period of extended

operation.

However, in a letter (ML101370259), dated May 14, 2010, the licensee notified the

NRC of the existence of a limited number of small-bore stainless-steel butt weld

connections (less than four inches in diameter), which was contrary to what was

identified before. As a result, the licensee changed the OTI requirements and

committed to perform augmented ISI volumetric examinations of ASME Class I

stainless steel small bore piping butt welds with a two-inch nominal pipe size through

less than four-inch nominal pipe size in accordance with the ISI aging management

program. The inspectors questioned whether the identification of stainless-steel butt

welds constituted a newly identified component or whether the commitment change was

appropriate and opened an URI pending further discussions with the Nuclear Reactor

Regulation (NRR) program office.

During this inspection period, NRR reviewed the licensees Fourth Ten-Year

ISI Examination Plan, revised in a letter (ML101670584), dated June 10, 2010.

The 10-year ISI interval covers May 1, 2003, to May 31, 2012. The revised plan

includes a section for Class 1 small-bore piping and states that, As required by license

renewal to manage aging effects, examination of small-bore piping has been added as

an augmented program to the ISI Plan. It further states that, Augmented volumetric

examinations of welds are performed on Class 1 stainless steel small-bore piping butt

welds > NPS 2 to < NPS 4. The examinations are performed in support of license

renewal and SHALL be performed through the renewed license period of extended

operation. The base scope of approximately 10 percent of the population will be

examined during each ISI interval. The NRR staff and inspectors determined the

licensees inspection sampling of 10 percent of the weld population is consistent with the

current staff sampling guidance. In addition, the 10-year ISI plan provided a detailed

weld selection methodology to ensure inspection of the most susceptible and

risk-significant welds.

36 Enclosure

The inspectors, with the assistance from NRR, concluded that Monticellos proposed

supplement adequately addresses one-time inspection of small bore piping full

penetration welds.

No finding of significance was identified. This URI is closed.

.3 Flow-Accelerated-Corrosion Inspection In Support of Extended Power Uprate (71004)

a. Inspection Scope

The inspectors performed a review to determine whether licensee programs and

procedures relative to flow-accelerated-corrosion (FAC) monitoring and maintenance

were adequately addressing plant changes resulting from extended power uprate (EPU)

in accordance with 10 CFR 50.65, the Maintenance Rule and licensee commitments to

implement Generic Letter 89-08, Erosion/Corrosion Induced Pipe Wall Thinning.

The inspectors reviewed the FAC Program to determine whether Monticello has taken

required action to detect adverse effects (wall thinning) on systems and components as

a result of operating changes related to EPU, such as increased flow in primary or

secondary systems, including their interfacing systems.

The inspectors reviewed procedures and administrative controls to determine whether

those procedures and controls ensure the structural integrity of high energy

(single phase and two-phase) carbon steel systems. The inspectors reviewed the

Monticello FAC program to determine whether the degradation of piping and

components is described in the procedures and, the examination activities are managed,

maintained, and documented. In particular, the inspectors reviewed those steps taken to

identify specific locations that were most likely to be adversely affected by a change

(increase) in operating variables (temperature, flow, etc.) as a result of increased power

levels. Also, the inspectors reviewed the licensee FAC activity to determine status and

effective utilization of the industry sponsored predictive program (CHECWORKS) to

verify the selection of the most susceptible locations for inspection and additional

locations based on unique operating conditions and industry experience. Also, the

inspectors reviewed how inspection data is trended to determine FAC wear rates and

identify the future inspection locations.

The inspectors selected portions of the feedwater system, a risk significant system

affected by EPU, for review of the licensees FAC monitoring activities and effectiveness.

The inspectors verified that the as built configuration for portions of the selected system

(piping and components) matches the plant specific FAC program isometrics.

The inspectors verified that design changes are reviewed for impact on the FAC

program and incorporated into the FAC database. The inspectors also reviewed

selected locations in this system that had been identified as susceptible to a projected

increase in FAC wear rates using the higher EPU operational variables with the

CHECWORKS model. The inspectors determined that the increase in wear rates was

recognized and being incorporated into the licensees program database for future

inspection sample selection.

b. Findings

No findings were identified.

37 Enclosure

4OA6 Management Meetings

.1 Exit Meeting Summary

On April 5, 2011, the inspectors presented the inspection results to Mr. T. OConnor, and

other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The results of the one-week Fire Protection Inspection related to single and

multiple spurious circuit analysis with Mr. T. OConnor, and other members of

the licensee staff, on February 10, 2011. These results were also discussed

with Mr. S. Speight from the licensee on March 17, 2011;

  • The results of the Inservice Inspection with Plant Manager, J. Grubb,

on March 24, 2011; and

  • Radiation Monitoring Instrumentation, Occupational and Public Radiation

Safety Performance Indicator Verifications with Mr. T. OConnor,

the Site-Vice President, on February 4, 2011.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was

returned to the licensee.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) or Severity Level IV was

identified by the licensee and is a violation of NRC requirements, which meets the

criteria of the NRC Enforcement Policy for being dispositioned as an NCV.

  • Technical Specification LCO 3.0.4 states, in part, that when an LCO is not met,

entry into a MODE in the applicability shall only be made when the associated

ACTIONS to be entered permit continued operation in the MODE or other

specified condition in the applicability for an unlimited period of time.

Technical Specification LCO 3.6.1.3, Primary Containment Isolation Valves

(PCIVs), states, in part, that each PCIV, except reactor building-to-suppression

chamber vacuum breakers, shall be OPERABLE in MODES 1, 2, and 3, when

associated instrumentation is required to be OPERABLE per LCO 3.3.6.1,

Primary Containment Isolation Instrumentation. Technical Specification

LCO 3.3.6.1 states, in part, that the primary containment isolation instrumentation

for Function 1, Main Steam Line Isolation, shall be OPERABLE for the Reactor

Vessel Water Level - Low Low, Main Steam Line Flow - High, and Main Steam

Line Tunnel Temperature - High functions in MODES 1, 2, and 3. Contrary to

the requirement of TS LCO 3.0.4, on November 22, 2010, the inboard and

outboard main steam line PCIVs were not operable (unable to automatically

close on a primary containment isolation signal due to an electrical isolation)

prior to entering Mode 2, and the associated actions to be entered did not permit

continued operation in Mode 2 for an unlimited period of time. Once identified,

38 Enclosure

the licensee restored electrical power to the PCIVs and entered the issue into the

corrective action program as CAP 01259879.

The inspectors applied IMC 0609, Attachment 4, Phase 1 - Initial Screening

and Characterization of Findings, to this finding. Using the Table 4a worksheet,

the inspectors answered Yes to Question 3 and applied IMC 0609, Appendix H,

Containment Integrity Significance Determination Process. Per IMC 0609,

Appendix H, the finding was considered a Type B finding; that is, a finding that

has potentially important implications for integrity of containment without affecting

the likelihood of core damage. Table 6.2, Phase 2 Risk Significance - Type B

Findings at Full Power, provided the risk significance for this finding.

For BWR Mark I reactor types, the significance of Type B findings for less than

three days duration is Green.

ATTACHMENT: SUPPLEMENTAL INFORMATION

39 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. OConnor, Site Vice President

J. Grubb, Plant Manager

W. Paulhardt, Assistant Plant Manager

N. Haskell, Site Engineering Director

K. Jepson, Business Support Manager

S. Radebaugh, Maintenance Manager

M. Holmes, Radiation Protection/Chemistry Manager

D. Neve, Regulatory Affairs Manager

S. Speight, Regulatory Affairs

S. Hafen, Nuclear Oversight Manager

M. Hutin, Program Engineering Director

M. Hippe, Engineering Fire Protection

S. Kibler, Program Engineering

G. Sherwood, Program Engineering Manger

V. Bhardwaj, Design Engineering Director

M. Kelly, Fleet Program Engineering Supervisor

D. Potter, Fleet Engineering Supervisor

T. Jones, NDE Level III

P. Sauerissig, FAC Engineer

S. Oswald, Regulatory Affairs

Nuclear Regulatory Commission

K. Riemer, Chief, Reactor Projects Branch 2

A. M. Stone, Chief, Engineering Branch 2

B. C. Dickson, Chief, Plant Support Team

1 Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

5000263/2011002-02 URI Calculation of Work Hours during Fatigue Rule

Implementation (Section 4OA2.3)

Opened and Closed

05000263/2011002-01 NCV Inadequate System Isolation during Check Valve

Maintenance (Section 1R20)05000263/2011002-03 NCV Failure to Control a Level 1 FME Area during New Fuel

Receipt Activities (Section 4OA3.2)

Closed

05000263/2010-006-00 LER Mode Change Made with PCIVs Inoperable

(Section 4OA3.3)

05000263/2009-001-02 LER Containment Overpressure Not Ensured in the Appendix R

Analysis (Section 4OA3.4)

05000263/2011-002-00 LER ESF Actuation Due to a Failed Power Supply

(Section 4OA3.5)

05000263/2010-004-00 LER Secondary Containment Briefly Inoperable Due to

Simultaneous Opening of Airlock Doors (Section 4OA3.6)5000263/2010008-01 URI Potential Concern with the One-Time Inspection Program

Related to Butt Welds (Section 4OA5.1)

Discussed

None

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01

1151; Winter Checklist; Revision 65

C.4-B.08.03.A; Loss of Heating Boiler; Revision 6

B.08.07-05; Extreme Cold Weather Procedure; Revision 24

8136; SCT Penetrations; Revision 17

CAP 00743426; Reactor Head Vent Found Frozen in Place

CAP 01166397; B.08.07-05 Extreme Cold Weather Procedure; Revision 20

CAP 01209511; E-100A 11 CT Riser Valves Frozen Shut - Near Miss

Emergency Plan for External Flooding Event Reaching Elevation 918; Revision 2

1478; Annual Flood Surveillance; Revision 3

Section 1R04

2154-28; Diesel Generator Air Start System Prestart Valve Checklist; Revision 9

2124; Plant Prestart Checklist Diesel Generators and Fuel Oil System; Revision 8

2154-14; Fuel Oil System Prestart Checklist; Revision 16

NH-36051; P&ID Diesel Fuel Oil System; Revision 77

B.09.08; EDG System; Revision D

CAP 01266032; FO-16 (Fire Pump Supply) Found Out of Position

2154-07; SBLC System Prestart Valve Checklist; Revision 11

2113; Plant Prestart Checklist SBLC System; Revision 13

NH-36253; P&ID SBLC System; Revision 77

B.03.05; SBLC System; Revision 10

CAP 01254014; Received Spurious Alarm C05-B-15 (Standby Liquid Hi/Lo Temp)

00041885; Clearance Order Checklist; FINI-11-67B, Replacement of Lamp Assembly

2154-11; CS System Prestart Valve Checklist; Revision 18

NH-36248; P&ID CS System; Revision 79

B.03.01; CS Cooling System; Revision 3

Section 1R05

4 AWI-08.01.00; Fire Protection Program Plan; Revision 12

Fire Strategy A.3-09; Control Room (9); Revision 7

CAP 01266328; A.3-09; Revision 7

CAP 01266330; A.3-10; Revision 13

CAP 01266331; Discrepancies Noted in A.3 Procedures

Fire Strategy A.3-07-A; 125V Division I Battery Room; Revision 5

Fire Strategy A.3-07-B; 250V Division I Battery Room; Revision 8

Fire Strategy A.3-07-C; 125V Division II Battery Room; Revision 6

CAP 01270371; Questions Raised on 250 VDC and 125 VDC Battery Condition

Fire Strategy A.3-23-A; Intake Structure Pump Room; Revision 11

Fire Strategy A.3-06; Refuel Floor; Revision 6

Fire Strategy A.3-19A; Make-Up Demin Area; Revision 9

3 Attachment

Fire Strategy A.3-19B; Essential Motor Control Center Area (NO. 142 & 143 931 ELEVATION);

Revision 11

Fire Strategy A.3-19C; F.W. Pipe Chase; Revision 5

AR 01270032; Configuration Error Found; February 9, 2011

AR 01270498; No Switch Development for Switch 14A-S3B; February 11, 2011

FPEE 2010-01; Alternate Compensatory Measures for Multiple Spurious Operations Identified

Nonconformances; Revision 0

NX-7833-21-4; Elementary Diagram - CS System; Revision 76

NE-36404-5A; CS Pump P-208B ACB 152-605 Control; Revision S

NE-36394-18A; Emergency Service Water Pump P-111B and Scheme B4319; Revision F

NX-7833-21-4A; Elementary Diagram - CS System; Revision 77

NX-7905-46-1; Elementary Diagram - RHR System; Revision 77

NF-100335-3; Alternate Shutdown System Schematic; Revision 78

Section 1RO6

PRA-CALC-04-004; Flood Initiating Event Frequencies; Revision 0

PRA-CALC-04-003; Flood Source Identification; Revision 0

CAP 1274344; Water Leaking into Lower 4kv Room from Stator Cooling Valves

PRA-CALC-04-001; Flood Areas; Revision 0

PRA-CALC-04-005; Equipment Vulnerabilities to Flooding; Revision 0

CAP 1274346; Water Leaks by SW-250 on C/O 37330

PRA-CALC-04-006; Flood Scenarios and Effects; Revision 0

CAP 1275079; Evidence of Water Pooling in Lower Cubicles of LC-109

Section 1RO7

1136; RHR Heat Exchanger Efficiency Test; Revision 30

CA-97-113; RHR Heat Exchanger Performance Analysis

CA-97-023; RHR Heat Exchanger K Values with Two RHR and Two RHRSW Pumps in

Suppression Cooling Mode

CAP 01028386; RHR Heat Exchanger Modeled Flow Incorrectly in Several Calcs

CAP 01172846; RHR B Heat Exchanger Issue Resolution

B.03.04; RHR System; Revision 5

CAP 01271131; Question about USAR Interpretation and Accuracy

USAR 7.6.3; Primary Containment Isolation System; Revision 27

B.03.04-4 RHR System, References; Revision 40

B.03.04-6 RHR System; Revision 5

1136; RHR Heat Exchanger Efficiency Test; Revision 30

CAP 01172846; RHR B Heat Exchanger Issue Resolution

CAP 01028386; RHR Heat Exchanger Modeled Flow Incorrect in Several Calcs

12 RHR Heat Exchanger Test Data; February 15, 2011

WO 0000229; Plug No. 12 RHR Heat Exchanger Tubes; January 15, 2000

Section 1R08

PEI-02.02.01; Dry Powder Magnetic Particle Examination; Revision 1

FP-PE-NDE-03; Written Practice for Qualification and Certification of NDE Personnel;

Revision 6

FP-PE-NDE-401; UT of Ferritic Pipe Weld-Supplement 3; Revision 3

FP-PE-NDE-406; UT of Reactor Pressure Vessel Welds; Revision 1

4 Attachment

FP-PE-FAC-02; Layout and Marking of Piping and Components for Flow Accelerated Corrosion

Program; Revision 1

ISI Examination Plan, Fourth Interval; Revision 4

AR 01241927; Station OE Evaluation of NRC IN 2010-2; July 19, 2010

AR 01276343; During a QC MT Exam a Linear Indication was Found; March 19, 2011

AR 01177677; Indications Discovered In Shroud Support Legs; April 10, 2009

AR 01174890; ISI Exam Revealed Non-Rotating Bearing on Snubber; March 25, 2009

AR 01176895; Drywell/Torus Surface Inspection Results; April 5, 2009

MNGP-RFO-25-INF-11-03; Indication Notification; March 16, 2011

FP-PE-B31-PIP1-GTSM-001; Groove Welds and Fillet Welds, P1-P1, GTAW/SMAW,

without PWHT; Revision 3

Welding Procedure Specification; FP-PE-B31-P1P1-GTSM-001; Revision 2

SM-1-1; Welding Procedure Qualification Record; Revision 1

Work Order 00380817; Re-Install RCIC Steam Line and Supports; March 30, 2009

Section 1R11

SEG RQ-SS-103

Section 1R12

90-023; Minimum Allowable Fuel Oil Storage Tank Level; Revision 2

50.59 Screening 10-0319; Replace Fuel Oil Transfer Level Switch LS-7211; Revision 0

Equivalency Evaluation Equivalent/Alternate Change 12303; Replace Fuel Oil Transfer Level

LS-721 Switch; Revision 0

B.09.08; Diesel Generators; Revision 10

B.08.11; Diesel Oil System; Revision 7

1052-04; 12 Diesel Generator Auxiliary Systems Test; Revision 15

CAP 01268419; LS-7211 Replacement Switch Failed during Testing

CAP 01267884; 12 EDG Base Tank Level Switches are not Functioning

CAP 01267658; CSP System Health Color Turned YELLOW

System Health Report; CSP, CS; January 24, 2011

CAP 01261935; A CSP Pump Motor Upper Oil Reservoir Cooling Coil HX Leaking

CAP 01265872; Adequacy of Equipment EOC Questioned

CAP 01242119; P-208A Motor Cooling Coil Found with Damage during Disassembly

CAP 01246421; 12 CSP Upper Motor Bearing High Oil Level

Section 1R13

CAP 01265569; WO 420235 Results Require Extent of Condition Evaluation

CAP 01265233; Steam/Water Leak from Piping on RWCU Regenerative Heat Exchangers

CAP 01265544; Potential Adverse Impact from RWCU on SRM/IRM

CAP 01265389; Water Leaking onto SRM and IRM Amplifier Cabinet

CAP 01238597; P225A FO Transfer Pump Leaking Bearing Grease

TS Bases 3.8.1; AC Sources- Operating; Revision 7

B.09.08; Diesel Generators; Revision 10

B.08.11; Diesel Oil System; Revision 7

1052-04; 12 Diesel Generator Auxiliary Systems Test; Revision 15

USAR 08.04; Plant Standby Diesel Generator Systems; Revision 24

NX-9216-5-4A; Physical Schematic and Field Connection- Model 999 No. 12 EDG; Revision 76

NH-36051; P&ID Diesel Fuel Oil System; Revision 77

5 Attachment

CAP 01267884; 12 EDG Base Tank Level Switches are not Functioning

CAP 01268038; Condition of Removed Fuel Oil Level Switches from No. 12 EDG

CAP 01268207; New LS-7211 EDG Level Switch did not Function as Expected

CAP 01268425; Original Level Switch, LS-7211, for No. 12 EDG was Reused

CAP 01268199; Exceeded 50 Percent of LCO Required Action Time for 12 EDG Window

CAP 01268234; 12 EDG LS-7211 Wires were Rolled

WO 00421339; 12 EDG Base Tank Level Switches are not Functioning; January 28, 2011

4 AWI-08.15.03; Risk Management for Outages; Revision 6

SWI-14.01; Risk Management for Outages and On-line Activities; Revision 5

9210; Master RPV Disassembly Procedure; Revision 11

FP-OP-ROM-02; Shutdown Safety Management Program; Revision 0

FP-OP-PEQ-01; Protected Equipment Program; Revision 0

OWI-03.08; Protected Equipment Program; Revision 4

9040; Temporary Vessel Level Instrumentation Installation and Restoration; Revision 10

Operations Manual C.3; Shutdown Procedure; Revision 63

WO 394791; Title 9224 - Dryer Removal High Risk Plan; March 9, 2011

2270; Critical Safety System Checklist - week of March 7, 2011

RF-25 Defense in Depth Variance to the Rev 0 Sched - Critical Safety Functions; March 8, 2011

Outage Risk Plan for RFO 25; week of February 28, 2011

NX7955-119-1; Refueling Platform One-line Diagram; Revision 2

WO 412387; Contingency Troubleshoot/Repair Refuel Bridge; March 17, 2011

CAP 01275823; Refuel Bridge Issues during RFO-25

CAP 01276444; Latest Replacement 8-58 Bridge Hoist Joystick not Adjustable

CAP 01276451; Refuel Bridge Controller Lead Position does not Match Print

CAP 01276919; 1N6 Lockout Occurred on 1AR Power Transfer from 10 Bank

CAP 01227229; 1AR XFMR Lockout Caused by 1N6 Ground Fault

Section 1R15

CAP 01156561; Apparent Degrading Flow Trend - V-EF-40B

WO 371712; V-EF-40B Inspect Ductwork

CAP 1270531; PMT Failure for V-EF-40B, Div II 250VDC Battery Room Vent

CAP 1233587; No Documented Required Flow for RM-9021A/B

B.05.11-05; Process Radiation MonitoringSystem Operation; Revision 29

C.6-242-A-09; Annunciator Response Procedure - V-EF-40B Low Flow; Revision 5

Operations Manual B.08.13-05; Main Control Room Heating, Ventilation, and Emergency

Filtration TrainSystem Operation; Revision 18

Operations Manual B.08.13-01; Main Control Room Heating, Ventilation, and Emergency

Filtration TrainFunction and General Description of System; Revision 10

Operations Manual B.08.07-01; Heating and VentilationFunction and General Description of

System; Revision 6

C.6-242-A-09

USAR Section 7; Plant Instrumentation and Control Systems; Revision 27

USAR Appendix J; Fire Protection Program; Revision 22

ESM-01.02; Design Practices; Revision 12

CAP 01271131; Question about USAR Interpretation and Accuracy; February 17, 2011

MPS-0274; G.E. Design Specification 22A1126; Primary and SCT System

MPS-0277; G.E. Design Specification 22A1132; Containment Isolation Systems

MPS-0346; G.E. Design Specification 22A2501; Engineered Safeguards Sub Systems and

Primary Containment Isolation Systems Separation

NX-7834-67-1; Reactor Protection System; Revision 76

6 Attachment

NX-7823-4-1; Elementary Diagram Primary Containment Isolation System; Revision J

NX-7834-58-1; Interconnect Scheme Reactor Protection System; Revision J

OWI-03.03; Operation with the Potential to Drain the Reactor; Revision 3

WO 314216-14; CRD-104 for HCU 34-39 Body-to-Bonnet Leak

CO 41006; Hang C/L No. 1: CRD-104/34-39 Repair Bonnet Leak

8167-01; Freeze Sealing Using Freeze Master; Revision 9

WO 381642-06; Investigate Repair Leaking CRD-113, Scram Vlv on CRD 22-23

CO 40413; Hang CL No. 1: CRD-113/22-23, Repair/Replace Leaking Valve

WO 368061-08; Investigate and Repair Leak on CRD-104/02-23

CO 41610; Hang C/L No. 1: CRD-104/02-23 Repair Bonnet Leak

NH-36245; P&ID Control Rod Hydraulic System; Revision 77

NH-36244; Control Rod Hydraulic System P&ID; Revision 80

OPDRV Screening Chart

Section 1R18

EC 14638; Change MSIV and Seat Ring Hard-Faced Material from Stellite 6 to Stellite 21

CAP 01278168; Internal Damage to Outboard MSIVs

Section 1R19

CAP 01270939; Reactor Building Doors not Tested per Work Plan after Maintenance

1297-01; SCT Door Interlock Check; Revision 14

WO 419439; Door is Presenting Interferences for Bringing in the New Steam Dryer

4048-PM; SCT Isolation Damper Maintenance; Revision 24

CAP 01270429; V-D-61 Damper Actuator Arm Bent, Prevent Opening

CAP 01270014; Suspected Coil Leak on V-AH-4A

WO 422190; MECH - V-D-61 Damper Motor Linkage Bent

4048-PM; SCT Isolation Damper Maintenance; Revision 24

WO 378941; 186-603 Replace Lockout Relay

WO 388993; RV-1993 14 RHR Pump Suction Relief Valve Replacement

4850-603-PM; 152-603 14 RHR Pump Relay Maintenance, Calibration and Test Tripping;

Revision 6

0007-A; Condenser Low Vacuum Scram Instruments Test and Calibration Procedure

WO 406610; Replace PS-5-11C

Section 1R20

Operations Manual C.3; Shutdown Procedure; Revision 63

C.4-A; Reactor Scram; Revision 34

2300 Reactivity Adjustment; Revision 4

4 AWI-08.15.03; Risk Management for Outages; Revision 6

SWI-14.01; Risk Management for Outages and On-line Activities; Revision 5

9210; Master RPV Disassembly Procedure; Revision 11

FP-OP-ROM-02; Shutdown Safety Management Program; Revision 0

Duty Shift Manager Notes for PORC Meeting 3/1/11

9001; Reactor Well & Dryer-Separator Storage Pool Filling Procedure; Revision 23

8048; Bypass of RWM during Plant Shutdown Using Improved BPWS Control Rod Insertion

Process; Revision 4

EOC25 Shutdown Reactivity Management Plan Overview; March 1, 2011

Reactivity Maneuvering Steps; March 4, 2011

7 Attachment

Operations/Maintenance Site Clock Reset - Red Sheet; March 18, 2011

CAP 1275963; Clearance Order did not Provide Boundary for CST-88 Repair

CAP 1275935; Found Pressurized Water when Dis-Assembling CST-88

Human Performance Event Review Committee for AR 1275935 Notes; March 18, 2011

CAP 1276336; Adverse Trend in Outage Tagging

2270; Critical Safety System Checklist; Revision 3

FP-OP-TAG-01; Fleet Tagging; Revision 10

0255-22-IA-1; CST-88 B LPCI Fill Line Check Valve Test; Revision 9

NH-85509; P&ID Service Condensate SystemRadwaste Building; Revision 77

NH-36039; P&ID Service Condensate System; Revision 75

NH-36247; P&ID RHR System; Revision 79

B.08.09-02; Condensate Storage System; Revision 5

4045-OCD; RHR Loop B Leak Rate Tests; Revision 15

WO 394266; 0255-22-IA-1 CST-88 B Loop LPCI Fill Line CKV Oper

OWI-02.07; Operations Work Control; Revision 34

4263; Maintenance and Construction Pre-Job Briefing Checklist; Revision 23

4 AWI-04.05.07; Procedure Use and Adherence (FP-G-DOC-03); Revision 27

Section 1R22

CAP 01265605; TS Surveillance was Missed for Diesel Fuel Oil

0192; Diesel Fuel Quality Checks; Revision 29

8096; Fuel Oil Transfer from the Diesel Oil Receiving Tank to the Diesel Oil Storage Tank;

Revision 12

OSP-DOL-0543; Fuel Oil Receiving Quality Check; Revision 7

PRA-MEMO-11-002; Risk Assessment of Diesel Fuel Oil Missed Surveillance; January 10, 2011

Lab Number V5002355; T-83A New Diesel Fuel Oil Shipment Analysis; November 1, 2010

Lab Number V5002989; Diesel Oil Storage Tank T-44 Monthly Particulate Sample;

January 12, 2011

0007-A; Condenser Low Vacuum Scram Instruments Test and Calibration Procedure;

Revision 24

B.06.03; Main Condenser; Revision 14

0021-01; Reactor Low Level Scram and Low-Low Level Isolation Transmitter Calibration

Procedure; Revision 14

USAR 7.6; Plant Protection System; Revision 27

B.05.06; Design Basis Document: Plant Protection; Revision C

0278-B; ATWS-Recirc Trip for Reactor Pressure and Level Trip Unit Test and Calibration;

Revision 20

CAP; NRC Questions Whether ATWS Trip Cal Causes Preconditioning

0255-03-IA-2A; CS - Shutdown Valve Operability Test; Revision 21

NH-36248; MNGP P&ID CS System; Revision 79

9001; Reactor Well & Dryer Separator Storage Pool Filling Procedure; Revision 23

Ops Manual B.03.01; CS Cooling System; Revision 3

0137-07A; Reactor Steam Supply Valves Leak Rate Testing; Revision 26

EWI-08.06.01; MNGP Primary Containment Leakage Rate Testing Program; Revision 10

0137; Master Local Leak Rate Test; Revision 34

0137-A; LLRT-LRM-Makeup Flow Method; Revision 1

0137-B; LLRT Pressure Decay Method; Revision 0

0137-07A-02-OCD; Reactor Steam Supply Valve Leak Rate Testing by Pressurizing the Main

Steam Lines; Revision 15

CAP 01275312; Unexpected Configuration Found after Turnover for 0137-07A

8 Attachment

CAP 01275315; Delay in MSIV testing due to Procedure Conflicts

NH-36241; Nuclear Boiler SystemSteam Supply P&ID; Revision 82

CAP 01275532; MO-2075 and MO-2076 Failed App J Admin Limit

B.09.15; Nonessential Diesel Generator

18615.01-E031B; Specification for Standby Diesel Generator; March 18, 1989

Monticello Maintenance Rule Program; System Basis Document; Non-Essential Diesel

Generator; Revision 3

EWI-05.02.01; Monticello Maintenance Rule Program Document; Revision 16

USAR 8.4.2; Non Safeguards Diesel Generator; Revision 27

NDG Non-Essential Diesel Generator System Health Report; February 7, 2011

Unavailability Hours for 13 NDG; January 2011

Operator Rounds; January 23, 2010

Station Logs; January 13, 2011

ACE for CAP 01266100

Maintenance Rule Evaluation for CAP 01266100

Equipment Reliability Clock Evaluation for CAP 01266100

CAP 01266100; 13 Diesel Generator would not Manually Synch to LC-107

CAP 01267418; 13 D. Generator No. 2 Water Jacket Heater not Working; January 22, 2011

CAP 01215001; 13 DG B Side Engine Heater not Working Properly; January 23, 2010

CAP 01270472; No. 13 NDG MR Changed Color to Yellow; February 11, 2011

CAP 01266954; 13 DG Freq Relay Impacts Manual and Auto Breaker Close; January 19, 2011

CAP 01266099; PRA Associated with 13DG not Reflected on Schedule; January 13, 2011

CAP 01262539; 13 D. Generator Jacket Temperature Less than 90 degrees F;

December 2, 2010

Section 1EP6

MNGP Emergency Planning Drill Package; February 9, 2011

Section 2RS5

AR 01238399; Adverse Trend Identified for PRM Equipment; June 26, 2010

Efficiency Calibration Data Files for HPGe Detectors; Selected Dates

Gamma Reports for Liquid and Gaseous Samples; Selected Dates

General Atomic Company; Certificate of Radioactivity Standard; Source Type 0360-0593-01;

July 1981

Nuclear Oversight 1st Quarter 2010 Assessment Report; May 14, 2010

Nuclear Oversight 2nd Quarter 2010 Assessment Report; August 18, 2010

Nuclear Oversight 3rd Quarter 2010 Assessment Report; December 1, 2010

ODCM; Selected Revisions

Process Radiation Monitor Alarm and Trip Points; January 2010

Radioactive Source Transaction Forms; Selected Dates

Snapshot Self-Assessment; 01251738-15; Radiation Protection Instrumentation; January 2011

Title 10 CFR Part 61 Updates Documentation; Selected Dates

USAR; Section 7.5; Plant Radiation Monitoring Systems; Revision 25

0163; Stack Wide Range Gas Monitor Calibration; December 2010

0226; Semiannual Source Inventory and Smear Test; November 2009

0248; Reactor Building Vent Wide Range Gas Monitor Calibration; April 2010

5504; Whole Body Counter Calibration Checklist; Various dates 2009 and 2010

5849; PM-7 Calibration; January 2011

5854; SAM-11/LAM Calibration; Various dates 2010 and 2011

9 Attachment

5871; ARGOS Calibration; Various dates 2010 and 2011

5879; GE ARM Box Calibration Source Verification; March 2010

5598-01; Semiannual Smear Counter Functional Checks; Various dates

5728-02; Semiannual ABACUS Smear Counter Functional Checks; Various dates

Section 4OA1

AR 01211188; Number of HRA and LHRA Entries Challenges Access Control; December 2009

AR 01212497; Dose Alarm Received while Performing Survey in RWCU Room; February 2010

AR 01212747; ED Dose Rate Alarm not Heard during HRA Entry; February 2010

AR 01238088; SJAE Room HELB Barrier Locked with Personnel Working Inside; August 2010

AR 01238171; Unexpected Dose Rates Encountered during RWCU Filter Backwash;

June 21, 2010

AR 01263347; Torus to RCIC Door Lock Not Operating Correctly; December 2010

Electronic Dosimeter Dose and Dose Rate Alarm Log - January 2010 to January 2011;

February 3, 2011

RPGP-01.14; Self-Assessment Program; Revision 14

FP-PA-PI-02; NRC/INPO/WANO PI Reporting; Revision 6

Section 4OA2

CAP 01265921; Hardhats not Worn as Required

CAP 01265922; Door Checks not Being Completed as Required

CAP 01267295; NRC Observations Shared with Plant Manager Staff

CAP 01267450; Surface Oxidation/Corrosion on CRD HCU Riser Valves

CAP 01269945; Toolboxes were not Secured in the TIP Drive Room

CAP 01269953; Oil Leaking from Sight Glasses on RCIC System

CAP 01269976; V-HC-11 Leaking Outside the Catch Funnel onto the Floor

CAP 01272068; Corrosion on Mounting Bolt for Div1 250 Vdc Battery Stand

CAP 01272074; Electrical Department Toolbox not Chalked

CAP 01272253; NRC Question Regarding Fire Watch

CAP 01275597; NRC Question Regarding FME Buffer Zone Requirements

FP-S-WHL-01; 10 CFR 26 Scope of Work Hour Limits; Revision 2

FP-S-FMP-01; 10 CFR 26 Fatigue Management Fleet Procedure; Revision 2

FP-S-CWH-01; 10 CFR 26 Calculating Work Hours; Revision 1

FP-S-FAP-01; 10 CFR 26 Fatigue Assessment Procedure; Revision 1

CAPs generated between March 19, 2010 and March 19, 2011 regarding Work Hour Controls

CAP 1234747; Potential Adverse Trend Work Hour Procedure Adherence

CAP 1219126; Multiple Security Officers Exceeded 10 CFR 26 Rule

CAP 1234413; Work Hours Exceeded on May 23, 2010

CAP 1239945; Adverse Trend in Maint Grp Work Hour Procedure Adherence

CAP 1218230; Supervisor Exceeded MDO requirement of 10 CFR 26

CAP 1253396; Subyard Work Possibly not in Compliance with Work Hour Rules

CAP 1270962; Excess Work Hours for Two Covered Workers

CAP 1276434; Seven DZ Employees Violated 10 CFR 26 Work Hours

CAP 1241474; Violation of Work Hours Rules under 10CFR26

CAP 1254318; WorkForce Security Schedule Change Request

Work Schedules for Select Individuals within the Maintenance, Operations, Fire Brigade, and

Security Departments

10 Attachment

Section 4OA3

FME Control Plan for 1027 Refuel Floor; January 1, 2011 to May 2011

General Employee Training M-7730F-012; On-Line FME; Revision 1

General Employee Training MT-SHE-GEN-001L; FME Monitor Training; Revision 1

9015; Procedure for Inspection of New Fuel; Revision 32

CAP 01267670; FME Control Point Protocol not Followed

FP-MA-FME-01; Foreign Material Exclusion and Control; Revision 2

CAP 1259879; Mode Change with Inoperable PCIVs

RCE CAP 1259879; Mode Change with Inoperable PCIVs

4 AWI-04.05.07; Procedure Use and Adherence; Revision 27

4 AWI-09.02.01; Quality Control Inspections; Revision 15

PRA-MEMO-10-008; Risk Assessment of LER 2010-06; December 2, 2010

FP-G-DOC-03; Procedure Use and Adherence; Revision 9

CAP 1263610; Received Unexpected Alarm ANN-5-A-2, Reactor Bldg Vent & F P

CAP 1263610; ACE; January 19, 2011

PRA-MEMO-11-003; Risk Assessment of LER 2011-02; January 17, 2011

NJ53562; Dual Trip Circuit Drawing; Revision C

Part 21 Evaluation Power Supply Model No. 112C2235G012/ST, S/N 100927-2

Monticello Station Log Entries for December 20, 2020

CAP 1232366-01; ACE; June 9, 2010

CAP 1232366; Failure of ES-17-451B, Causes REAC BLG Vent & FP RAD CH B LO

CAP 1232366-01; ACE; July 23, 2010

CAP 1236790; FP & Plenum PRM Power Supply Refurbishment and Replacement

SC/CNT 00022414; 115349-Refurbish Safety-Related ARM Power Supplies; July 29, 2009

Section 4OA5

FAC Program MNGP 1R24 Outage Summary Report

FAC Program MNGP RFO 23 Outage Summary Report

CD 5.17; Flow Accelerated Corrosion and Service Water Inspection Program Standard;

Revision 5

II.01; Strategic Chemistry Plan; Revision 14

FP-E-MOD-04; Design Inputs; Revision 7

FP-PE-FAC-01, FAC Program; Revision 9

AR 01219342; Update FAC Master Plan; February 22, 2010

2009-04-001; NOS Observation Report - FAC Program; November 2, 2009

PBD/AMP-002, Aging Management Program Basis Document, Flow - Accelerated Corrosion

(FAC) Program; Revision 4

11 Attachment

LIST OF ACRONYMS USED

ACE Apparent Cause Evaluation

ADAMS Agencywide Document Access Management System

AOP Abnormal Operating Procedures

ASME American Society of Mechanical Engineers

ATWS Anticipated Transient without Scram

CAP Corrective Action Program

CFR Code of Federal Regulations

CIV Containment Isolation Valve

CO Clearance Order

CREF Control Room Emergency Filtration

CRV Control Room Ventilation

CS Core Spray

CST Condensate Storage Tank

CSW Condensate Service Water

DRP Division of Reactor Projects

EC Engineering Change

EDG Emergency Diesel Generator

EGM Enforcement Guidance Memorandum

EPU Extended Power Uprate

FAC Flow Accelerated Corrosion

FME Foreign Material Exclusion

FPEE Fire Protection Engineering Evaluation

FSAR Final Safety Analysis Report

IMC Inspection Manual Chapter

INPO Institute of Nuclear Power Operations

IP Inspection Procedure

IRM Intermediate-Range Monitor

ISI Inservice Inspection

IST Inservice Test

kV Kilovolt

LCO Limiting Condition for Operation

LER Licensee Event Report

LLRT Local Leak Rate Test

LPCI Low Pressure Coolant Injection

MNGP Monticello Nuclear Generating Plant

MOV Motor-Operated Valve

MSIV Main Steam Isolation Valve

MSO Multiple Spurious Operations

MSPI Mitigating Systems Performance Index

MT Magnetic Particle Examination

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NFPA National Fire Protection Association

NMC Nuclear Management Company

NOS Nuclear Oversight

NRC U.S. Nuclear Regulatory Commission

NRR Nuclear Reactor Regulation

ODCM Offsite Dose Calculation Manual

OE Operating Experience

12 Attachment

OSP Outage Safety Plan

OTI One-Time Inspection

PARS Publicly Available Records System

PCIV Primary Containment Isolation Valves

PI Performance Indicator

PM Post-Maintenance

RCE Root Cause Evaluation

RCIC Reactor Core Isolation Cooling

RETS Radiological Effluent Technical Specification

RFO Refueling Outage

RG Regulatory Guide

RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water

ROP Reactor Oversight Process

RPV Reactor Pressure Vessel

RT Radiographic Examination

RWCU Reactor Water Cleanup

SBGT Standby Gas Treatment

SBLC Standby Liquid Control

SCT Secondary Containment

SDP Significance Determination Process

SRM Source Range Monitor

SRO Senior Reactor Operator

SSC Structure, System, and Component

TS Technical Specification

URI Unresolved Item

USAR Updated Safety Analysis Report

UT Ultrasonic Examination

Vdc Volts Direct Current

WO Work Order 13 Attachment

T. O'Connor -2-

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Monticello Nuclear Generating Plant. In addition, if you disagree with the

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region III, and the NRC Resident Inspector at the Monticello Nuclear

Generating Plant.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket No. 50-263

License No. DPR-22

Enclosure: Inspection Report 05000263/2011002

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

DISTRIBUTION:

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OFFICE RIII N RIII RIII E RIII

NAME AScarbeary JHeck for SOrth* KRiemer:cs

DATE 05/02/11 05/03/11 05/10/11

OFFICIAL RECORD COPY

  • Sections 1RO5.2, 4OA3.4, and Cover Letter

Letter to T. O'Connor from K. Riemer dated May 10, 2011

SUBJECT: MONTICELLO NUCLEAR GENERATING PLANT NRC INTEGRATED AND

POWER UPRATE REVIEW INSPECTION REPORT 05000263/2011002 AND

EXERCISE OF ENFORCEMENT DISCRETION

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