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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20153B0531998-09-16016 September 1998 Special Rept:On 980817,errors in Implementation of Selected Licensee Commitment Testing Requirements on Fire Protection Sys Instruments,Was Discovered.Caused by Error in Interpretation of SLC Requirement.Will Revise Procedures ML20236M9151998-07-0707 July 1998 Special Rept:On 980611,determined That Required Firewatch Patrol Had Been Missed.Caused by Firewatch Being Performed on Wrong Unit Due to Human Error.Employee Was Verbally Counseled on Firewatches & Documentation Was Corrected ML20236G4451998-07-0101 July 1998 Special Rept:On 980618,declared Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Inoperable.Caused by Failure to Meet TS Definition of Channel Calibr.Will Revise Selected Licensee Commitment ML20248K1431998-06-0202 June 1998 Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Shrinkage of Foam & Improper Installation During Construction of Plant.Posted Fire Watches & Repaired Firestop F-AX-348-W-134 ML20247H5351998-04-12012 April 1998 Special Rept:On 980415,missed Insp of Fire Hose Caskets Was Discovered.Caused by Error in Transferring Info from One Procedure to Another.Planned Rev of Applicable Procedure to Include Gasket Insp at Appropriate Frequency ML20216B0211998-04-0606 April 1998 Special Rept:On 980325,determined That Loose Parts Monitoring Sys Being Inoperable for Greater than Thirty Days.Caused by Incorrect Testing.All Channels of Loose Parts Monitoring Sys Tested Utilizing Revised Test Method ML20217K9271998-03-26026 March 1998 Special Rept:On 971229,procedure Step for Closing Safety Injection Pump Cold Leg Injection Isolation Valve Was Inadvertently Skipped.Caused by Injection of Water Into RCS from Rwst.Simplified Procedures & Discussed Event ML20216D5641998-03-0505 March 1998 Special Rept:On 980204,discovered That Fire Detection Panel Was Apparently Not Communicating W/Several Local Fire Detectors.Caused by Faulty Computer Sys Cards.Replaced Four Computer Cards in Sys ML20202C4701998-02-0505 February 1998 Ro:On 971228:Unit 1 Loose Parts Monitoring Sys Channel 6 Was Declared Inoperable Due to Excessive Static on Channel. Caused by Loose Connection.Work Order Has Been Written to Pursue Repairs ML20138E6851997-04-24024 April 1997 Special Rept:On 970318,Unit 1 Loose Parts Monitoring Sys Channel 13 Was Declared Inoperable Due to Sporadic Electical Static.Channel Was Removed from Svc & Entered Into TS Action Item Logbook as Inoperable ML20149M7251997-01-20020 January 1997 Special Rept:On 961209,Unit 1 Loose Parts Monitoring (Lpm) Sys Channel 20 Declared Inoperable Due to No Signal Being Received from Field.Lpm Channel 20 & 22 Operable & Providing Monitoring Coverage for Primary Side of 1D S/G ML20134K4901996-11-0606 November 1996 Special Rept:On 961009,selective Licensee Commitment for Operability of Fire Protection Sprinkler Sys Not Maintained. Continuous Fire Watch Established within One H Following Identification of Incorrect Remedial Action ML20134H1331996-11-0404 November 1996 Special Rept:On 961004,Unit 1B DG Failed Due to Failure of Motor Operated Pot,Electronic & Mechanical Governor,Governor Droop Relay & Mechanical Binding of Fuel Rack Control Linkage.Dg Procedures Will Be Revised ML20113A1801996-06-17017 June 1996 Special Rept:On 960521,declared Detectors A01 for Zone 69 & A04 for Zone 60 Inoperable Because Detectors Effectively Isolated from Area in Intended Protection.Detectors Relocated,Tested & Declared Operable on 960524 ML20100H9801996-02-20020 February 1996 Special Rept:On 960111,Unit 1 Loose Parts Monitoring Channel 21 Declared Inoperable,Due to Spurious,Unexplainable Electronic Bursts.Work Request Initiated to Pursue Corrective Action ML20100H9751996-02-20020 February 1996 Special Rept:On 960111,Unit 2 Loose Parts Monitoring Sys Channel 7 Declared Inoperable,Due to pre-amp Bias Voltage Indicating Zero Volts Twice During Previous Seven Days.Work Request Written to Pursue Corrective Action ML20097F5011996-02-11011 February 1996 Special Rept:On 960102,Unit 2 Loose Parts Monitoring Sys Channel 17 Was Declared Inoperable.Two Other Channels Operable & Providing Coverage Against Loose Parts ML20096E7731996-01-12012 January 1996 Special Rept:On 951214,unit 2 DG Valid Failure Occurred. Caused by Fuel Line Fitting Backing Off from Cylinder Head Connection,Which Resulted in Fuel Oil Leakage.Dg Successfully Started,Run & Declared Operable on 951215 ML20096A8761995-12-18018 December 1995 Special Rept:On 951120,during Periodic Surveillance Testing, Lpms Channel 5 Declared Inoperable.Caused by Erratic Preamp Bias Voltage Indications.Work Request 95048483 Initiated to Perform Corrective Maint During Unit 1 Cycle 9 ML20094Q5811995-11-13013 November 1995 Special Rept:On 951014,auxiliary Bldg Filtered Exhaust Sys Pump Room Heater Declared Inoperable Due to Blown Fuse & Not Restored to Operable Status within 7 Days Per Ts. Technical Investigation Will Be Performed ML20094B8291995-10-25025 October 1995 Special Rept:On 950919,loose Parts Monitoring Sys Channel 1 Declared Inoperable Due to Erratic Preamp Bias Indication. Work Request Written to Investigate & Repair Channel ML20098A4641995-09-19019 September 1995 Special Rept:On 950817,Unit 2 Lpms Channel 12 Was Declared Inoperable Due to Channel Sensor Failing Acceptance Criteria During Performance of PT/O/A4600/03 ML20092G6041995-09-14014 September 1995 Special Rept:On 950815,CNS Unit 1 DG 1A Invalid Failure Occurred Due to Main Bearing High Temp Trip Signal.Caused by Failed Splice Installed in Circuit for RTD 1LDRD5630.New RTD Installed in Main Bearing 5 ML20086H1401995-07-12012 July 1995 Special Rept:On 950615,Channel 4 Was Declared Inoperable Due to Noise Uncharacteristic of Healthy Channel Detected Via Vibration & Loose Parts Monitoring Sys.Corrective Maint Will Be Performed During 1EOC9 Outage ML20086H1431995-07-11011 July 1995 Special Rept:On 950608,Channel 13 Was Declared Inoperable. Trending of Bias Voltage & Background Rms Evaluated to Conclude Channel Was Experiencing Periodic Failures. Corrective Maint Will Be Performed During 1EOC9 Outage ML20086C6441995-06-29029 June 1995 Special Rept:On 950523,Unit 1 Train a Fuel Handling Ventilation Filter Heaters Declared Inoperable.Evaluation Done to Determine Fault ML20085M4061995-06-20020 June 1995 Special Rept:On 950501,lower Rv Tube 4 Was Declared Inoperable ML20084N7271995-05-25025 May 1995 Special Rept:On 950425,valid Failure of DG 1A Occurred. Caused by Jacket Water Thermostatic Control Valve Sticking in Position Which Reduced Engine Cw Flow Through Heat Exchanger.Thermostatic Cv Internals Removed & Replaced ML20082L2711995-04-17017 April 1995 Special Rept:On 950308,Unit 2 Cathodic Protection Sys Was Declared Inoperable & Remained Inoperable Greater than 10 Days ML20081D4851995-03-13013 March 1995 Special Rept:On 950211,actuation of PORV 1NC32B Occurred. Procedure OP/1(2)/A/6100/02 Revised to Require More Emphasis on Monitoring Pressure Indication During Sensitive Evolutions ML20080Q8701995-03-0202 March 1995 Special Rept:On 950202,Unit 1 DG 1B Invalid Failure Due to Overcurrent Breaker Trip During Governor Troubleshooting ML20149H7821994-12-20020 December 1994 Special Rept:On 941129,discovered That Selective Licensee Commitment (SLC) for Visual Insp of Fire Rated Assemblies Exceeded Due to Misinterpretation of Requirements of SLC 16.9-5.Fire Barriers Visually Inspected ML20078R0021994-12-12012 December 1994 Special Rept:On 941103,Channel 3 (Upper Rv a) Declared Inoperable.Caused by Channel Sensor Failure of Acceptance Criteria During Performance of PT/0/A/4600/03.Repair Planned for End of 2EOC7 Outage Due to Containment Entry Required ML20078K7361994-11-17017 November 1994 Special Rept on 941021,DG 1A Invalid Failure Occurred Due to Main Bearing High Temp Trip.Operability Performance Test Successfully Completed & Engine Declared Operable on 941022 ML20149G8041994-11-0101 November 1994 Special Rept:On 940922,CNS,Unit 2 Cathodic Protection Sys Declared Inoperable & Remained Inoperable for Greater than 10 Days.Wo 94080948-01 Initiated to Replace Prepackaged Anode Well 1.WO Scheduled for 941114 ML20076F3191994-10-0404 October 1994 Special Rept:On 940908,valid Failure of D/G 1A Occurred Due to Air Start Valve Sticking Open.Maint Procedure MP/0/A/7650/99 Revised,New Air Roll Criteria Developed & Sixteen Starting Air Valves Replaced ML20072P4251994-08-23023 August 1994 Ro:On 940719,channel 9 (S/G a Channel 2) Declared Inoperable.Work Request Was Generated to Repair Channel During Future Outage of Sufficient Length Since Containment Entry Required for Work ML20072E5961994-08-15015 August 1994 Special Rept:On 940715,inoperability of Unit 2 Vibration & Loose Parts Monitoring System Channel 4 & 6 Occurred.Caused by Leds Not Lighting During Performance of PT/0/B/4600/03. Work Orders 94051250-01 & 94051251-01 Initiated ML20071N7441994-07-28028 July 1994 Special Rept:On 940711,delta-t Channel on Chart Recorder Found to Be out-of-tolerance Due to Drifting of Analog to Digital (A/D) Converter Card.A/D Card Replaced & delta-t Channel Chart Recorder Declared Operable ML20071N8511994-07-28028 July 1994 Special Rept:On 940711,main Steam Relief Valve Exhaust Monitors Declared Inoperable Due to Engineering Calculation Concerns.Engineering Calculation CNC-1229.00-00-0047 re-performed Using EPA-400 Methodology ML20070K0191994-07-18018 July 1994 Special Rept:On 940630,re Inoperability of Main Steam Line Radiation Monitor 2EMF12.Work Request 94026262 Generated to Reattach 2EMF12 to Main Steamline.Work Request Completed on 940701 ML20069H0861994-05-31031 May 1994 Special Rept:On 940501,Unit 2 DG 2A Invalid Failure Occurred Due to Right Bank Turbocharger Vibration Trip.Based on Cooper-Enterprise Recommendations,Procedure Changes Made to Calibr Procedures for All Four DGs ML20065K5011994-04-13013 April 1994 Special Rept:On 940314,invalid Failure of Diesel Generator 1B Occurred Due to Output Tripping During Calibration of Electronic Governor.Dg 1B Started Successfully on 940315 & Declared Operable ML20064G2911994-03-15015 March 1994 Special Rept:On 940203,SG Channels 9 & 11 Declared Inoperable.Channels Failed to Meet Band Limited Rms Acceptance Criteria During Performance of 18 Month Channel Calibr Test.Work Request Written to Repair Channels ML20064G2771994-03-0707 March 1994 Special Rept:On 940125,Channels 6,7 & 10 Were Declared Inoperable.Channels Failed to Meet Acceptance Criteria During Performance of 18 Month Channel Calibr Test.Work Request Written to Repair Channels 1999-09-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
Text
' Duke Energy Corporation Catawba Nudear Station 4800 Concord Road
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Y York. SC 29745 (803) 831-4251 OFFICE 3
Gary R. Iwerson (go3) g31342Gux Vice hesident December 14, 1998 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
Subject:
Duke Energy Corporation Catawba Nuclear Station Units 1 and 2 Docket Nos. 50-413 and 50-414 Special Report: Fire Protection Program Inoperable Fire Barrier Penetrations Revision 1 l
I Pursuant to Facility Operating License Section 2F, License Conditions 2.c. (8) for Unit 1 and 2.c. (6) for Unit 2, and Selected Licensee Commitment 16.9.5; attached is Revision i 1 of a Special Report concerning inoperable fire barrier I penetrations. Revision 0 of this Special Report, issued j ,
on June 2, 1998; addressed a condition that was discovered l on May 5, 1998. The only commitments contained in this I document are listed in the " Corrective Actions" section of I the attached report. There are no additional commitments I ,
I contained'in revision 1. l l
Questions regarding this Special Report should be addressed to J.W. Glenn at (803) 831-3051. I i
l l
Very trul urs, G. R. Peterson .I I
Attachment . P.C 9812180070 981214 P '
PDR ADOCK 05000413 .
8 PDR , I e
5 U.S. Nuclear Regulatory Commission December 14, 1998 V Page 2 4 Attachment :
Special. Report l
Inoperable Fire Barrier Penetrations e
i Abstract: ,
- On May 5, 1998 both Units were in Mode 1 (Power Operation) at
- approximately 100% power. During a Triennial Fire Protection
- Audit, it was discovered that certain. fire barriers appeared to be degraded. Investigation by Engineering determined that
' one fire barrier in a masonry block wall in the Auxiliary 4 Building was degraded and sixty penetration seals in the fire barrier in the Control Room floor were inoperable. Since these
- fire barriers had been in this condition for an indeterminate !
l time, it was determined that the requirements of Selected Licensee Commitment (SLC) 16.9.5 had not been met in the past history of the plant and the appropriate remedial actions had
. not been taken. The root cause of the problem in the Auxiliary Building was shrinkage of the firestop foam and damage that occurred when a forming board was removed. The root cause for the problem with the Control Room floor
- firestops was improper installation during the construction ,
l- of the plant. Corrective actions were posting the required firewatches and repair of the Auxiliary Building firestop.
I Planned corrective actions include further inspections to j determine the extent of these problems and either removing
- the Control Room floor as a committed fire barrier or '
! repairing the firestops.
l-
! During inspections per Planned Corrective Action #2 of l j Revision 0 of this Special Report, additional problems were l l
noted with void areas in large rectangular block out fire l z penetrations. These problems were caused by poor I installation practices and inadequate installation i procedures during the construction of the plant. I
! Catawba Nuclear Station Units 1 and 2 Facility Operating License NPF-35 and NPF-52 require that Duke Energy Corporation implement and maintain in ef'v:t all provisions of the
~
approved Fire Protection Program as amended. It was i determined that the degradation described in this report constitutes a noncompliance with this license condition.
- j Consequently, this occurrence was reported within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of
- discovery pursuant to the provisions of Facility Operating
! License Section 2F (Reference Event #34208, reported on May l 12, 1996 and updated on May 19, 1998 and November 13, 1998). l j Revision'1.of this Special Report is being provided within l !
- 30
- days of.the November 13, 1998 Update. l
U.S. Nuclear Regulatory Commission December 14, 1998 p Page 3 Introduction i
! Catawba Nuclear Station Units 1 and 2 are four loop
- Westinghouse Units. Selected Licensee Commitment (SLC) 16.9.5, Fire Barrier Penetrations; is a part of the Catawba Fire ,
4 Protection (EIIS:KP) Program and is subject to the provisions I of the Catawba Facility Operating License Condition 2.c.(8)for NPF-35 (Unit 1) and License Condition 2.c. (6) for NPF-52 (Unit I 2). SLC 16.9.5 requires that all fire barriers and all
] sealing devices in fire barrier penetrations shall be operable
}
such that fires would be confined or adequately retarded so i that the following criteria is achieved:
- 1. Fire will not spread from non-safety related areas to safety related areas,
, 2. Fire will not damage redundant analyzed post fire safe ,
j shutdown equipment, a 3. Fire will rot spread from the balance of plant to the
{ control complex (control room, cable rooms and j battery rooms),
! 4. Fire will not spread from non-containment areas to l containment areas.
Firestop number F-AX-348-W-134 is located in a masonry block
] wall that separates the Unit 1 A Train Component Cooling Pumps
- from the Unit 1 B Train Component Cooling Pumps.
Firestops of the K-AX-657-F-XXX series (where XXX represents a sequential number) are located in the floor of the Control Room and separate the Control Room from the Cable Spreading Rooms. There are 79 of these penetrations of which 60 were found to be inoperable.
An audit of the fire protection program is required every three years. The audit is called the " Triennial Fire Protection Audit". This audit was performed at Catawba from 5-4-98 to 5-8-98. The Audit Number was SA-98-100(A11). The problems described in this Special Report were discovered as a result of this audit.
Description of Event 5-5-98 During a triennial fire protection audit 18:15 walkdown insp~ection it was noted that there
l U.S. Nuclear Regulatory Commission 1 December 14, 1998 y Page 4 4 was an excessive gap at the top of wall ,
firestop F-AX-348-W-134. The gap extended l completely through the barrier. Engineering verified that the firestop was inoperable, Operations was notified and a firewatch was posted.
5-5-98 Work request 98021525 (Work order 98044764-18:30 01) was generated for repair of the firestop.
5-6-98 The triennial fire protection audit team i
11:30 noted an excessive gap on the ".nderside of floor firestop numbers K-AX-657-F-104 and K-AX-657-F-109. When viewed from the upper side it appeared that the required eight inch minimum depth of foam had not been achieved.
5-6-98 Work request 98021617 (Work Order 98044845-15:00 01) was initiated to have the depth of foam measured in all circular sleeves in the Control Room Floor.
5-6-98 Hourly firewatenes were established for the 16:00 Control Room - Cable Spreading Rooms Area.
l 5-7-98 Maintenance completed the inspection of firestop foam in the Control Room Cloor penetrations and forwarded the data to Engineering.
5-7-98 Engineering notified Operations of Control 10:30 Room floor firestops with inadequate depth of foam. (A firewatch was already in place).
5-7-98 Maintenance completed repair of wall firestop 13:45 F-AX-348-W-134.
5-18-98 Additional inspections along with an 15:40 Engineering followup evaluation identified 24 additional inadequate floor firestops in six other committed barriers. These penetrations were declared inoperable. Hourly firewatches were established.
U.S. Nuclear Regulatory Commission December 14, 1998 g Page 5 11-12-98 During inspections per planned corrective I action #2 of Revision 0 of this Special l Report, problems were found that appeared I to be generic to all large block out I penetrations through committed fire I boundary walls. l 11-13-98 Engineering declared the 218 fire barriers I of this type inoperable and fire watches I were posted. l Cause Of Event The root cause of the problem for the auxiliary building wall penettation was determined to be shrinkage of the foam such that it pulled away from the top of the penetration blockout.
After the installation of a silicone foam penetration seal, some shrinkage is expected to occur. The installation procedure requires a new foam seal to be inspected 3 to 7 days after installation to ensure the seal is acceptable. The amount of shrinkage noted with this firestop was greater than the normal post installation shrinkage. There was also some apparent damage from the removal of firestop damming boards. I Other firestops were inspected for similar damage and no additional cases were found.
The root cause of the problem with the Control Room floor penetrations was determined to be improper installation of firestop foaming material during the construction of the plant. The Control Room Penetration seals were in embedded sleeves, which project four inches above the floor. Firestop foam was placed in the sleeve up to the top of the four-inch projection. The firestop foam should have been installed within the sleeve in the area of the floor slab instead of the area within the sleeve above top of the floor slab.
While performing intrusive inspections of fire penetrations I (removal of outer fiberboard and visually inspecting the I foam) per planned corrective action 2 of Revision 0 of this l Special Report, several types of deficiencies were I discovered with large rectangular block out fire stop i penetration seals. The type of deficiencies found include I the following: I I
- 1) Inadequate foam fill in the opening l
- 2) Shrinkage of foam away from the top edge of the opening i
- 3) " Cold Joint" gaps between layers of foam fill l
- 4) Voids created by gas bubbles I i
I j
U.S. Nuclear Regulatory Commission December 14, 1998 g Page 6 The first two deficiency types (1 and 2 above) ware created I because the large block out type openings are " foamed" with I a damming board installed on both sides of the opening. This I prevents the installer from being able to see the final I results of the foam injection. The penetration seal design I specifications and installation procedures were intended to I require a 3 to 7 day post installation inspection by I removing the top portion of the damming board on at least I one side of the penetration. Based on the inspections I completed thus far, it appears that the post installation I inspection was not performed consistently. l The second two deficiency types (3 and 4 above) are a result I of the placement of new layers of foam prior to allowing i adequate cure time of the previous layer. This results in l
, the entrapment of hydrogen gas bubbles as the foam layer is l curing. The installation instructions supplied by the I manufacturer of the foam recommends a 15 minute wait time l
, between layers. This wait time apparently was not adhered te I consistently. I 1
An Engineering review of the drawings for large rectangular l block out openings in committed fire barriers identified a I total of 218 locations where large block out penetrations I are installed. Further intrusive inspections on these 216 I block out openings will continue.
The root cause of the problem with the large block out wall I penetrations has been determined to be poor installation I practices and inadequate installation procedures during the I construction of the plant.
Fire watches are in place for all of the affected locations. I Any problems found during inspection of the penetration l seals are being repaired as they are discovered. l There are no EPIX failures associated with this event. This I is not considered to be a recurring problem. However, I similar problems have been noted at all Duke Energy Nuclear l Stations. 1 Corrective Actions Subsequent
- 1. Engineering personnel evaluated the items discovered by the audit team and notified Operations of conclusions.
U.S. Nuclear Regulatory Commission Dacember 14, 1998 ,
/ Page 7
- 2. Operations posted the required fire watches.
- 3. Firestop F-AX-348-W-134 was repaired by Maintenance.
- 4. Additional inspections were initiated to identify other problems.
Planned
- 1. Engineering will evaluate a modification to delete the Control Room Floor as a committed fire barrier. This is based on a study that was performed as a part of the
" Cost Beneficial Licensing Action" initiative. This study identified a new technical criteria for maintaining committed fire barriers. One criterion addressed barriers that separate areas of the control complex from other areas of the station. Since the control room and cuble spreading rooms are both within the control complex, it may be possible to remove the barriers between the two areas as committed fire barriers. If this approach is not feasible, the affected firestops will be repaired.
- 2. Additional inspections of similar configurations will continta and repairs will be made as necessary.
Additional Information The wall firestop in the Component Cooling Pump Area is a part of a boundary that is used to separate redundant Component Cooling Pumps and is intended to prevent a single fire from damaging redundant pumps and motors so as to allow repairs necessary to achieve cold shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> after a fire event.
The firestops as installed in the Control Room floor (and similar) penetrations still afford some level of fire protection. The Control Room and Cable Spreading Rooms have lou combustible loadings, both areas are supplied with fire detection, and the Control Room is continuously occupied.
The current safety significance of the degradation of the I large penetration seals is mitigated by establishing l l compensatory measures consisting of hourly fire watches in I the affected areas and by the fire protection defense in I l
O.S. Nuclear Regulatory Commission December 14, 1998
/ Page 8 depth program. The fire protection program defense in depth I program includes the following: I I
Fire Prevention l I
A program for controlling activities that have I a potential to cause fires (hot work program). I I
Fire Control l I
Control of work activities including control of I combustible materials and housekeeping. I I
Designated storage areas for combustible material. I I
Fire Mitigation Elements l I
Early warning fire detection systems. I Fixed fire suppression systems. I Fire Brigade intervention. l Passive fire protection features including walls and I remaining installed portions of penetration seals. 1 I l In addition, Catawba Nuclear Station has a stand alone Safe 1 Shutdown Facility with an independent diesel generator and I i control room for mitigating 10CFR50 Appendix R Fire Events I and Security Events, i The health and safety of the public were not affected by this event.
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U.S. Nuclear Regulatory Commission December 14, 1998
/ Page 9 xc: L. A. Reyes U. S. Nuclear Regulatory Commission Regional Administrator, Region II Atlanta Federal Center 61 Forsyth S* , SW, Suite 23T85 Atlanta, GA 93 P. S. Tam NRC Senior Project Manager (CNS)
U. S. Nuclear Regulatory Commission Mail Stop O-14H25 Washington, DC 20555-0001 D. J. Roberts Senior Resident Inspector (CNS)
U. S. Nuclear Regulatory Commission Catawba Nuclear Site i
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U.S. Nuclear Regulatory Commission December 14, 1998
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bxc: ELL EC050 KE Nicholson PIP 0-C98-4396 NCPMPA-1 RGC Licensing File NCEMC PMPA SREC CN-801.01 CN04DC Electronic Distribution i
WM Hogan GD Gilbert PR Herran SL Bradshaw GR Peterson RA Jones BJ Horsley GH Savage PR Newton
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