Letter Sequence Other |
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MONTHYEARML20137U0801997-04-14014 April 1997 Requests Addl Info on 960726 Amend Request Entitled, Supporting Monticello Nuclear Generating Plant Power Rerate Program Project stage: Other IR 05000263/19970041997-04-14014 April 1997 Insp Rept 50-263/97-04 on 970310-14.No Violations Noted. Major Areas Inspected:Review of Training Administrative Procedures,Operating Exam Matl,Observation & Operating Exam, & Assessment of Simulator Fidelity Project stage: Request ML20141K9911997-05-19019 May 1997 Informs That Util Will Submit Completed Portions of Response by 970731 & Submit Remaining Portions within Reasonable Time Period Thereafter Re Power Rerate License Amend Request Project stage: Other ML20216H6471997-09-0505 September 1997 Forwards Response to 970414 RAI Re License Amend Request for MNGP Power Rerate Program Project stage: Request ML20203H0001998-02-11011 February 1998 Forwards Request for Addl Info Re 960726 Amend Request to Increase Monticello Nuclear Generating Plant Operating License Max Power Level to 1775 Megawatts Thermal & Revise Supporting Plant TSs Project stage: RAI ML20216E6951998-03-0606 March 1998 Refers to 960726 License Amend Request Submitted by NSP to Increase MNGP Operating License Max Power Limit & Revise Supporting MNGP Ts.Suppl to 980211 RAI Encl Project stage: RAI ML20248L4011998-03-0606 March 1998 Forwards Partial Response to 980211 RAI to Complete Review of License Amend Request.Response to Question 6 Is Under Development Project stage: Other ML20248L9051998-03-19019 March 1998 Informs That NSP Application Re Exhibit E, NEDC-32546P,Rev 1, Power Rerate Safety Analysis Rept for Monticello Nuclear Generating Plant, Will Be Withheld from Public Disclosure,Per 10CFR2.790 Project stage: Other ML20217K1761998-04-17017 April 1998 Provides Supplemental Info on Seismic Qualification of MSIV Leakage Path to Condenser Project stage: Supplement ML20217K1601998-04-22022 April 1998 Provides Supplemental Info on Certain Containment Equipment, Internal Flooding & Turbine Missiles,Per 980417 Telcon Project stage: Supplement ML20217K7711998-04-24024 April 1998 Refers to 960726 License Amend Request Submitted by NSP to Increase MNGP Operating License Max Power Level.Requests That NSP Submit Responses to RAIs & 0306 by 980529 Project stage: RAI ML20247K5661998-05-0505 May 1998 Forwards Proprietary Addl Info Re Containment Response Codes for Rerate Applications for Power Rerate License Amend. GE to Util Re Suppl Info for Licensee Response to Question 13 & GE Affidavit Also Encl.Attachment 1 Withheld Project stage: Other ML20247K3361998-05-12012 May 1998 Responds to 980424 RAI to Complete Review of License Amend Request Re Rerate Program Project stage: Other ML20249C5161998-06-15015 June 1998 Provides Revised Info & Supersedes Re Demonstration of Seismic Qualification of MSIV Leakage Path. Rev to Verification Info & Seismic Calculations Included Project stage: Other ML20236P5331998-07-0101 July 1998 Forwards Summary Description of Power Rerate Ascension Test Program as Supplemental Info to 960726 LAR Re Plant Power Rerate Program.Revised TS Pages,Encl Project stage: Supplement ML20236U7341998-07-20020 July 1998 Provides Supplemental Info Re Seismic Verification of MSIV Leakage Path at Monticello & Power Rerate LAR Project stage: Supplement ML20236U8231998-07-27027 July 1998 Advises That Calculations CA 97-176,rev 2 & CA 98-105,rev 0 Submitted in Attachment 4 to NSP Ltr of 980326 & Marked as Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) & Section 103(b) of AEA of 1954,as Amended Project stage: Other ML20236U7471998-07-27027 July 1998 Discusses NSP Application & GE Affidavit ,executed by G Stramback.Attachment 1 to GE Ltr GLN-98-005,dtd 980428 Will Be Withheld from Public Disclosure Per 10CFR2.790 Project stage: Other ML20236Y3161998-07-30030 July 1998 Forwards Supplementary Info Re Commitments Associated W/ Monticello Power Rerate Program.No New Commitments Proposed. List of Completed Commitments Contained in Attachment 2 Project stage: Supplement IR 05000263/19980091998-07-30030 July 1998 Insp Rept 50-263/98-09 on 980511-0612.No Violations Noted. Major Areas Inspected:Review of 10CFR50.59 Safety Evaluation & Screening Activities Project stage: Request 1998-04-22
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M3801999-10-21021 October 1999 Forwards Insp Rept 50-263/99-06 on 990813-0923.Four Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217G0711999-10-13013 October 1999 Forwards Insp Rept 50-263/99-12 on 990913-17.No Violations Noted ML20216J2491999-09-30030 September 1999 Ack Receipt of 980804,990626 & 0720 Ltrs in Response to GL 98-01,suppl 1, Year 2000 Readiness of Computer Sys at Npps. Staff Review Has Concluded That All Requested Info Has Been Provided ML20217B1421999-09-30030 September 1999 Informs That on 990902,NRC Staff Completed mid-cicle Plant Performance Review of Monticello Nuclear Generating Station. Staff Conducted Reviews for All Operating NPPs to Integrate Performance Information & to Plan for Insp Activities ML20212K9131999-09-30030 September 1999 Refers to 990920 Meeting Conducted at Monticello Nuclear Generating Station to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA ML20216J8091999-09-24024 September 1999 Informs That New Diaphragm Matl Has Corrected Sticking Problem Associated with Increased Control Rod Drive Scram Times.Augmented Testing of Valves at Monticello Has Been Discontinued ML20216G4341999-09-24024 September 1999 Forwards Exam Rept 50-263/99-301 on 990823-26.Violation Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy.Test Was Administered to Two Applicants. Both Applicants Passed All Sections of Exam ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212G9801999-09-23023 September 1999 Refers to Resolution of Unresolved Items Identified Re Security Alarm Station Operations at Both Monitcello & Prairie Island ML20212F0901999-09-21021 September 1999 Confirms Discussion Between M Hammer & Rd Lanksbury to Have Routine Mgt Meeting on 991005 in Lisle,Il.Purpose of Meeting to Discuss Improvement Initiatives in Areas of Operations & Equipment Reliability ML20212A9761999-09-0909 September 1999 Submits 1999 Annual Rept of Any Changes or Errors Identified in ECCS Analytical Models or Applications ML20217A5751999-09-0909 September 1999 Forwards Individual Exam Results for Licensee Applicants Who Took Aug 1999 Initial License Exam.Without Encls ML20211Q6981999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Monticello Operator License Applicants During Wks of 010604 & 11.Validation of Exam Will Occur at Station During Wk of 010514 ML20211L1981999-09-0101 September 1999 Forwards Insp Rept 50-263/99-05 on 990702-0812.No Violations Noted ML20211K7971999-09-0101 September 1999 Informs That Util Reviewed Rvid as Requested in NRC .Recommended Corrections Are Listed ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211F9961999-08-26026 August 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 990101-990630, Revised Effluent & Waste Disposal Semi-Annual Rept for 980701-981231 & Revs to ODCM for Monitcello Nuclear Generating Plant ML20211C9501999-08-23023 August 1999 Forwards Rev 17 to Monticello Nuclear Generating Plant USAR, Updating Info in USAR to Reflect Implementation of Increase in Licensed Core Thermal Power from 1,670 Mwt to 1,775 Mwt.Rept of Changes,Tests & Experiments Not Included ML20210U1831999-08-12012 August 1999 Revises 980202 Commitment Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design- Basis Accident Conditions ML20210T9601999-08-12012 August 1999 Provides Rept on Status of Util RPV Feedwater Nozzle Insps Performed in Response to USI A-10 Re BWR Nozzle Cracking ML20210Q0341999-08-0404 August 1999 Forwards SE Granting Licensee 980724 Relief Request 10 Re Third 10-year Interval ISI Program Plan,Entitled, Limited Exam ML20210H0861999-07-28028 July 1999 Forwards Insp Rept 50-263/99-04 on 990521-0701.No Violations Noted.Licensee Conduct at Monticello Facility Characterized by safety-conscious Operations,Sound Engineering & Maint Practices & Appropriate Radiological Controls ML18107A7051999-07-20020 July 1999 Provides Suppl Info Which Supersedes Info in 990625 Ltr in Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML20212H3191999-07-16016 July 1999 Forwards Aug 1999 Monticello RO Exam Package,Including Revised Outlines.All Changes Are in Blue Font ML20209G5621999-07-14014 July 1999 Forwards Insp Rept 50-263/99-11 on 990621-24.No Violations Noted.Objective of Insp,To Determine Whether Monticello Nuclear Generating Station Emergency Plan Adequate & If Station Personnel Properly Implemented Emergency Plan ML20196J5351999-07-0202 July 1999 Discusses GL 92-01,Rev 1,Supp 1, Rv Integrity, Issued by NRC on 950515 & NSP Responses & 980917 for Monticello Npp.Informs That Staff Revised Info in Rvid & Released Info as Rvid Version 2 ML20196J9681999-07-0101 July 1999 Informs That in Sept 1998,Region III Received Rev 20 to Portions of Util Emergency Plan Under 10CFR50.54(q).Based on Determination That Changes Do Not Decrease Effectiveness of Licensee Emergency Plan,No NRC Approval Required ML20209B6151999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Y2K Readiness Disclosure Attached ML20196H2291999-06-24024 June 1999 Responds to Administrative Ltr 99-02,dtd 990603,requesting Licensee to Provide Estimate of Licensing Action Submittals Anticipated.Four New Submittals Per Year Are Anticipated ML20207D5851999-05-25025 May 1999 Submits Info Re Partial Fulfillment of License Conditions Placed on Amend 101,which Approved Use of Ten Exceptions for 24 Months Subject to Listed App C Conditions.Util Will Submit Second Rept to Obtain Approval for Continued Use ML20206S0911999-05-17017 May 1999 Forwards Response to NRC 990324 RAI Re Proposed Amend to pressure-temp Limits & Surveillance Capsule Withdrawal Schedule, .Supporting Calculations Also Encl ML20206N5601999-05-13013 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Cm Craig Will Be Section Chief for Monticello Npp.Organization Chart Encl ML20206G2181999-05-0505 May 1999 Discusses Completion of Licensing Action for GL 96-01, Testing of Safety-Related Logic Circuits, Dtd 960110,for Plant ML20206G4901999-05-0404 May 1999 Forwards Staff Review of Licensee 960508 Response to NRC Bulletin 96-002, Movement of Heavy Loads Over Sf,Over Fuel in Rc or Over Safety-Related Equipment, .Overall, Responses Acceptable.Tac M95610 Closed ML20206G7741999-05-0303 May 1999 Forwards Insp Rept 50-263/99-02 on 990223-0408.One Violation Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20206D1651999-04-27027 April 1999 Forwards Radiation Environ Monitoring Program for MNGP for Jan-Dec 1998, Per Plant TS 6.7.C.1.Ltr Contains No New NRC Commitments or Modifies Any Prior Commitments ML20205N0821999-04-12012 April 1999 Forwards SE of NSP Response to NRC GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves. Licensee Adequately Addressed Actions Requested in GL ML20205N4811999-04-0909 April 1999 Forwards Licensing Requalification Insp Rept 50-263/99-10 on 990308-12.No Violations Noted.However,Inspectors Through Observation of Simulator Scenario Exams Noted Difficulties in Ability of SM to Simultaneously Implement Duties of SM ML20205N5301999-04-0909 April 1999 Discusses Arrangements Made on 990406 for Administration of Licensing Exams at Monticello Nuclear Generating Station During Wk of 990823.Requests That Exam Outlines Be Submitted by 990128 & Supporting Ref Matls by 990719 ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C4851999-03-26026 March 1999 Informs That on 990203,NRC Staff Completed PPR of Nuclear Plant.Staff Conducts Reviews for All Operating NPPs to Develop an Integrated Understanding of Safety Performance ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20205A5881999-03-24024 March 1999 Forwards Request for Addl Info Re Submittal Requesting Rev of pressure-temperature Limits & Surveillance Capsule Withdrawal Schedule ML20204H4711999-03-18018 March 1999 Forwards SER Concluding That Util Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello & Adequately Addressed Actions Requested in GL 96-05 ML20207H5161999-03-11011 March 1999 Forwards Insp Rept 50-263/99-01 on 990112-0222.No Violations Noted ML20207F4091999-02-28028 February 1999 Forwards Fitness for Duty Program Performance Data for Six Month Period from 980701-981231,IAW 10CFR26.71 ML20207F6741999-02-24024 February 1999 Forwards Summary of Nuclear Property Insurance Maintained at Monticello & Prairie Island Nuclear Generating Plants ML20207F6901999-02-23023 February 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 980701-981231, Off-Site Radiation Dose Assessment for 980101-981231 & Revised Effluent & Waste Disposal Semi- Annual Rept for 980101-980630, for Monticello ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20216J8091999-09-24024 September 1999 Informs That New Diaphragm Matl Has Corrected Sticking Problem Associated with Increased Control Rod Drive Scram Times.Augmented Testing of Valves at Monticello Has Been Discontinued ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212A9761999-09-0909 September 1999 Submits 1999 Annual Rept of Any Changes or Errors Identified in ECCS Analytical Models or Applications ML20211K7971999-09-0101 September 1999 Informs That Util Reviewed Rvid as Requested in NRC .Recommended Corrections Are Listed ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211F9961999-08-26026 August 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 990101-990630, Revised Effluent & Waste Disposal Semi-Annual Rept for 980701-981231 & Revs to ODCM for Monitcello Nuclear Generating Plant ML20211C9501999-08-23023 August 1999 Forwards Rev 17 to Monticello Nuclear Generating Plant USAR, Updating Info in USAR to Reflect Implementation of Increase in Licensed Core Thermal Power from 1,670 Mwt to 1,775 Mwt.Rept of Changes,Tests & Experiments Not Included ML20210U1831999-08-12012 August 1999 Revises 980202 Commitment Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design- Basis Accident Conditions ML20210T9601999-08-12012 August 1999 Provides Rept on Status of Util RPV Feedwater Nozzle Insps Performed in Response to USI A-10 Re BWR Nozzle Cracking ML18107A7051999-07-20020 July 1999 Provides Suppl Info Which Supersedes Info in 990625 Ltr in Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. ML20212H3191999-07-16016 July 1999 Forwards Aug 1999 Monticello RO Exam Package,Including Revised Outlines.All Changes Are in Blue Font ML20209B6151999-06-25025 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Y2K Readiness Disclosure Attached ML20196H2291999-06-24024 June 1999 Responds to Administrative Ltr 99-02,dtd 990603,requesting Licensee to Provide Estimate of Licensing Action Submittals Anticipated.Four New Submittals Per Year Are Anticipated ML20207D5851999-05-25025 May 1999 Submits Info Re Partial Fulfillment of License Conditions Placed on Amend 101,which Approved Use of Ten Exceptions for 24 Months Subject to Listed App C Conditions.Util Will Submit Second Rept to Obtain Approval for Continued Use ML20206S0911999-05-17017 May 1999 Forwards Response to NRC 990324 RAI Re Proposed Amend to pressure-temp Limits & Surveillance Capsule Withdrawal Schedule, .Supporting Calculations Also Encl ML20206D1651999-04-27027 April 1999 Forwards Radiation Environ Monitoring Program for MNGP for Jan-Dec 1998, Per Plant TS 6.7.C.1.Ltr Contains No New NRC Commitments or Modifies Any Prior Commitments ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20207F4091999-02-28028 February 1999 Forwards Fitness for Duty Program Performance Data for Six Month Period from 980701-981231,IAW 10CFR26.71 ML20207F6741999-02-24024 February 1999 Forwards Summary of Nuclear Property Insurance Maintained at Monticello & Prairie Island Nuclear Generating Plants ML20207F6901999-02-23023 February 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept for 980701-981231, Off-Site Radiation Dose Assessment for 980101-981231 & Revised Effluent & Waste Disposal Semi- Annual Rept for 980101-980630, for Monticello ML20203A3081999-01-28028 January 1999 Forwards TS Page 60d,as Supplement 3 to 971125 LAR Re CST Low Level Hpci/Rcic Suction Transfer.Page Includes NRC Approved Amend 103 Changes for Use by NRC in Issuing SER ML20202F7821999-01-27027 January 1999 Forwards 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility, Per 10CFR55.45(b)(5)(ii) & 10CFR55.45(b)(5)(vi).Ltr Contains No New Commitments or Modifies Any Prior Commitments ML20206S0331999-01-20020 January 1999 Submits Annual Rept of Safety & Relief Valves Failure & Challenges ML20206P1221998-12-31031 December 1998 Forwards LAR for License DPR-22,revising TS pressure-temp Curves Contained in Figures 3.6.1,3.6.2,3.6.3 & 3.6.4, Deleting Completed RPV Sample SRs & Requirement to Withdraw Specimen at Next Refueling Outage & Removing Redundant SR ML20198M3271998-12-28028 December 1998 Submits Change to Commitment for Submittal of ITS Application.Util Plans to Provide ITS Conversion Package Submittal to NRC in Dec of 2000 ML20198J7511998-12-22022 December 1998 Informs of Completion of Listed Commitment Made in Re Severe Accident Mgt. Severe Accident Mgt Guidelines Have Been Assessed,Plant Procedures Have Been Modified & Training of Affected Plant Staff Has Been Completed ML20198J4311998-12-21021 December 1998 Forwards Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv. Under Separate Cover,Licensee Is Providing LAR to Revise Curves ML20198J7711998-12-14014 December 1998 Documents 981214 Discussion with NRC Staff Re Deviation from Emergency Procedure Guidelines ML20195C8781998-11-11011 November 1998 Forwards Supplement to 971125 License Amend Request Re Condensate Storage Tank Low Level Suction Transfer Setpoints for HPCI Sys & Reactor Core Isolation Cooling Sys ML20195C9631998-11-11011 November 1998 Forwards 120-day Response to NRC GL 98-04, Potential for Degradation of ECCS & CSS After LOCA Because of Construction & Protective Coating Deficiencies & Foreign Matl in Containment ML20195E2261998-11-10010 November 1998 Submits Suppl 1 to Util Response to NRC Request for Addl Info Re 981118 Request for Deviation from Emergency Procedure Guidelines ML20155H6591998-11-0404 November 1998 Forwards Response to 980910 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20155F9091998-10-27027 October 1998 Forwards Master Table of Contents to Rev 16 of Usar.Info Was Inadvertantly Omitted at Time of 981023 Submittal 05000263/LER-1998-005, Forwards LER 98-005-00,re HPCI Being Removed from Service to Repair Steam Leak in Drain Trap Bypass.Commitments Made by Util Are Listed1998-10-21021 October 1998 Forwards LER 98-005-00,re HPCI Being Removed from Service to Repair Steam Leak in Drain Trap Bypass.Commitments Made by Util Are Listed ML20154L9321998-10-12012 October 1998 Forwards Suppl 2 to LAR & Suppl 980319,which Proposed Changes to Ts,App a of Operating License DPR-22 for Mngp.Number of Addl Typos & One Title Change on Pages Associated with Amend Request Have Been Identified 05000263/LER-1998-004, Forwards LER 98-004-00 Re Manual Scram Inserted Following Pressure Transient Closes Air Ejector Suction Isolation Valves & Trips Offgas Recombiners.Ler Contains Listed Commitment1998-10-0909 October 1998 Forwards LER 98-004-00 Re Manual Scram Inserted Following Pressure Transient Closes Air Ejector Suction Isolation Valves & Trips Offgas Recombiners.Ler Contains Listed Commitment ML20154L8671998-10-0909 October 1998 Forwards Suppl 1 to LAR for License DPR-22, Replacing Exhibits B & C of Original Submittal to Reflect Item 2 & Subsequent Changes.Request for APRM Flow Converter Calibr Interval Extension,Withdrawn ML20154J6201998-10-0505 October 1998 Forwards Rev 49 to Monticello Security Plan.Encl Withheld, Per 10CFR73.21 ML20153F5351998-09-25025 September 1998 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Improved TS ML20153F0051998-09-25025 September 1998 Forwards Suppl 1 to 971031 Application for Amend to License DPR-22,replacing Exhibit C Which Contains TS Pages Incorporating Proposed Changes Described in Original 971031 Request ML20153D8561998-09-17017 September 1998 Forwards Rev 17 to EPIP A.2-414, Large Vol Liquid Sample &/ or Dissolved Gas Sample Obtained at Post Accident Sampling Sys. Superseded Procedures Should Be Destroyed.Ltr Contains No New NRC Commitments,Nor Does It Modify Prior Commitments ML20153D1441998-09-17017 September 1998 Informs NRC That Listed Commitments 1 & 3 Were Completed by End of 1998 Refueling Outage.Commitments Involved Final Disposition of Remaining Outlier Components Re All Known Outstanding Work Associated with GL 87-02,Suppl 1,USI A-46 ML20153E0331998-09-17017 September 1998 Forwards Response to NRC 980629 RAI Re RPV Weld Chemistry Values Previously Submitted as Part of Plant Licensing Basis.Next Monticello RPV Sample Capsule Scheduled to Be Removed During 1999/2000 Refueling Outage ML20153E9011998-09-0909 September 1998 Forwards Rev 1 to MNGP Colr,Cycle 19, Incorporating Changes to power-flow Maps in Figures 6 & 7.Changes Made to Correct Errors in Stability Exclusion Region & Stability Buffer Region Shown on Rev 0 ML20151S7401998-08-28028 August 1998 Responds to NRC Re Violations Noted in Insp Rept 50-263/98-09.Corrective Actions:Procedure 4 AWI-04.04.03 Will Be Revised to Eliminate Term Urgent from Section 4.3.1.D ML20238E8201998-08-26026 August 1998 Forwards Effluent & Waste Disposal Semi-Annual Rept for Jan-June 1998 & Revised Effluent & Waste Disposal Semi- Annual for Jul-Dec 1997. Ltr Contains No New NRC Commitments,Nor Does It Modify Any Prior Commitments ML20237E9741998-08-26026 August 1998 Forwards Rev 4 to EWI-09.04.01, Inservice Testing Program. Rev of Inservice Testing Program Reflects Valves Added as Result of Component Mods Recently Performed ML20237E6821998-08-25025 August 1998 Forwards fitness-for-duty Program Performance Data for Six Months Period Ending 980630 1999-09-09
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I ik,,it.e,T. States Power Company
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- Monticello Nuclear Generating Plant l 2807 West Hwy 75 Monticello, Minnesota 55362-9637 i
I May 12,1998 i
US Nuclear Regulatory Commission
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Attn: Document Control Desk j Washington, DC 20555 MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Response to April 24,1998 Request for Additional Information (RAI) on Monticello Power Rerate License Amendment (TAC No. M96238)
Ref.1 Letter from NRC to R.O. Anderson, NSP, "Monticello Nuclear Generating Plant - Request for Additional Information on License Amendment Request Entitled ' Supporting the Monticello Nuclear Generating Plant (MNGP) Power Rerate Program' (TAC No.
M96238)," April 24,1998 By letter dated April 24,1998 (Ref.1), the NRC staff provided a Request for Additional Information (RAl) to complete its review of NSP's license amendment request for the Monticello Nuclear Generating Plant (MNGP) Power Rerate Program. NSP's response to Ref.1 is provided as Attachment 2 to this letter.
Please contact Joel Beres at (612) 295-106 if additional information is required.
i NN/1& ~**'
Michael F. Hammer -
Plant Manager Monticello Nuclear Generating Plant
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i k 263 PDR b P
i l
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c: Regional Administrator - 111, NRC NRR Project Manager, NRC Sr, Resident inspector, NRC State of Minnesota, Attn: Kris Sanda J. Silberg, Esq.
Attachments Attachment 1 Affidavit to it.e US Nuclear Regulatory Commission Attachment 2 NSP Response to Staff Power Rerate RAI Dated April 24,1998 i _;
UNITED STATES NUCLEAR REGULATORY COMMISSION NORTHERN STATES POWER COMPANY
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l MONTICELLO NUCLEAR GENERATING PLANT DOCKET NO. 50-263 {
Response to April 24,1998 Request for Additional Information (RAI) on Monticello Power Rerate License Amendment (TAC No. M96238)
Northern States Power Company, a Minnesota corporation, by letter dated May 12,1998 i provides its response for the Monticello Nuclear Generating Plant to a US Nuclear Regulatory Commission (NRC) letter dated April 24,1998, with the subject "Monticello Nuclear Generating Plant - Request for Additional Information on License Amendment Request Entitled ' Supporting the Mont! cello Nuclear Generating Plant (MNGP) Power Rerate Program' (TAC No. M96238)." ,
This letter contains no restricted or other defense information.
f NORTHERN STATES POWER COMPANY By h A1/l44LL/ .
Michael'F. Hammer Plant Manager Monticello Nuclear Generaang Plant A
On this IN ay d of I\ Axe \D8 before me a notary public in and for said County, personally appeared Michael F. Hammer, Plant Manager, Monticello Nuclear Generating Plant, and being first duly sworn acknowledged that he is authorized to execute this document on behalf of Northern States Power Company, and that to the best of his knowledge, information, and belief the statements made in it are true.
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. SamuelI. Shire ,
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Notary Public - Minnesota Sherburne County Q)"
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Attachment 2 NSP Responss to Staff Power Rerate RAI Dated April 24,1998 t
I
- 1. NSP concluded that based on its review of scram irip setpoints (and their changes) po.werrerate showed no significant effect on trip (initiating event) frequency. Provide a basis / discussion for this conclusion.
NSP Response l
The GE setpoint methodology used at Monticello include's a spurious trip avoidance calculation. The calculation determines whether the setpoint value is sufficiently removed from a trip given allowances for instrumentation uncertainties such as drift.
This trip avoidance calculation was completed for all scram setpoints affected by power rerate, and the calculations demonstrated that the appropriate acceptance criteria for trip avoidance was met.
NSP also reviewed several events arising from equipment failures and operational maneuvers that involve integrated plant responses in regard to scram trip avoidance.
These events involve equipment setpoints in systems that could eventually result in an inadvertent scram. For example, reactor water high level following a single recirculation pump trip would trip the reactor feed pumps and cause a reactor water low level scram.
For these situations, NSP conducted an evaluation using the core transient models used for cycle analysis. This evaluation demonstrated that the setpoints in question had sufficient trip avoidance margin at rerate conditions.
The PRA team relied on these evaluations in reviewing the impact on the potential for initiating events.
Exhibit D of the rerate license amendment dated December 4,1997 contains a listing of hardware changes and setpoint modifications which support NSP's conclusion that there is no significant potential for increases in the frequency of initiating events modeled in the PRA. For example, the following changes were made to assure reliability of balance of plant systems.
Turbine Trip increase capacity of moisture separator drain valves increase generator isophase bus cooling and stator water cooling capacities Loss of Feedwater - Replace condensate pumps with higher capacity pumps Loss of Condenser Raise condenser low vacuum setpoint These modifications are intended to maintain margin on trip setpoints at rerate power levels and to maintain equipment operation within existing design constraints. As a result, it was concluded that the potential for these transient initiators was no greater due to the rerate.
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it was also concluded that none of the remaining initiating events modeled in the PRA are affected by the rerate. The following are examples.
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LOCAs Frequency dictated by the potential for passive pipe failures, which are independent of power level.
Transient initiators . Transient initiators other than those noted above are I
support systems, which do not directly interface with the primary system and would not be affected by changes in power.
DC power AC power l Service water RBCCW Instrument Air Loss of Offsite Power Dictated by the reliability of the grid and the switchyard which are not degraded by the rerate.
ATWS Rod insertion takes place under the same primary system conditions as existed prior to the rerate.
Combined with the conclusion that there is no change in the transient initiator frequency, the potential for ATWS is also unchanged.
Intemal Flooding Dictated by passive piping system failures and the frequency of maintenance activities which might lead to flooding conditions, neither of which is affected by the rerate.
Intemal Fires Dictated by combustible loading within each fire area and not by the rerate.
- 2. NSP indicated that the likelihood of all eight SRVs [ safety relief valves] failing is not significantly different from the likelihood of at least seven out of eight SRVs failing.
l Provide a besiddiscussion for this conclusion.
NSP Response l ' If only independent valve failures were considered, there would be a difference between the probabilities of seven failures and eight failures. However, the probability of seven and eight valves failing is dominated by common cause. Given that seven valves have
, failed due to common causes, it is highly likely that the eighth is similarly affected and will fail from the same causes. Therefore, the common cause failure probability for eight of l eight failures is virtually the same as for at least seven of eight failures, and the overall probability of eight failures is virtually the same as for at least seven failures.
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- 3. NSP concluded that the failure rates of equipment / component will not change due to power relate. Provide a basis / discussion for this conclusion.
NSP Response NSP conducted and documented comprehensive reviews of all plant systems and associated equipment that had the potential to be affected by power rerate. These reviews were conducted by cognizant system engineers and by subject matter experts.
Each system evaluation received secondary reviews by technical experts and management review teams as described in NSP's response to Question 19 of our letter to the NRC dated March 26,1998.
Changes in equipment service conditions and process changes, if any, were identified.
For the great majority of plant equipment, power rerate does not result in any change to the system processes or service conditions that would involve operation outside of the design constraints that were used to establish the present capabilities of the equipment, such as code allowabies, temperature, pressure, cooling requirements, run times, and electrical loading. In a few cases, these reviews identified modifications which would improve the performance of certain equipment and systems under rerate conditions.
These modifications are included in Exhibit D of our letter to the NRC dated December 4, 1997. Most of these modifications are complete, and all will be completed prior to rerate operation. The F~tA team relied extensively on these deterministic reviews to conclude that plant systems and equipment would continue to be operated within the existing design constraints.
A number of accident sequences would generate conditions which go beyond normal design. Moreover, the failure probability of some components depends on the number of demands the component may receive during the accident. Therefore, in addition to the system reviews described above, the most risk significant components from the PRA were reviewed to determine whether any components were expected to operate in accident sequences that went beyond their design basis or whether the number of demands would change.
To perform the review, all components whose failure could potentially contribute to accident sequences on the order of 1E-6/yr were identified. This threshold for risk significance corresponded to a risk achievement worth (RAW) of 1.07. The following summarizes the results of the review.
Level 1 PRA considerations: In loss of decay heat removal sequences (Accident i Class ll), the containment is allowed to approach its design pressure before containment venting is initiated. The wetwell and drywell vent and purge valves are credited in the PRA as one means of venting. These valve operators are capable of actuating at the containment design pressure. As rerate has no effect on this pressure, the vent valve reliability was rat changed in the rerate accident sequence quantification.
Level 2 PRA considerations: Post Core Damage Environment. A number of i plant components are expected to continue operating after core damage and are credited in the Level 2 PRA even when exposed to the environment associated 3
, with a core melt. This equipment includes the SRVs inside containment and the injection systems located in the reactor building which may be exposed to shine
. from the containment or from coolant recirculated through piping systems or to high temperatures and pressures following failure of the drywell.
A general assumption was made throughout the PRA regarding environmental qualification. Any equipment which was exposed to an environment that exceeded its qualification limits was assumed to be unavailable. For equipment operating within its qualification temperatures, pressures, and radiation levels, random failure probabilities were used. All environmentally qualified equipment will also be qualified for rerate conditions. As a result, no changes were made to the failure probabilities for equipment modeled in the Level 2 PRA.
Changes in the Number of Demands due to Rerate: A higher decay heat levelis expected to slightly increase the number of demands on the SRVs used for pressure relief when the primary coolant system is isolated, thus increasing the potential for a stuck open relief valve during such sequences. It was found that the risk of core damage due to transient initiators followed by a stuck open relief valve is just under 1E-6/yr. The risk of stuck open relief valves is dominated by station blackout sequences because the gradual blowdown of the reactor to the suppression pool will eventually result in a trip of the turbine-driven HPCI and RCIC pumps, leaving only the diesel-driven fire pump as a source of makeup.
Other transient initiators do not contribute significantly to sequences with stuck open relief valves because in those cases the low pressure systems and the CRD pump are available for coolant makeup once the blowdown is complete.
Station blackout sequences were analyzed to determine the effect of rerate with and without a stuck open safety relief valve. The analyses produced the following insights.
The number of demands on the SRVs does increase, but only slightly. Over the first four hours of a station blackout, the rerate case produced 16 demands on the SRV with the lowest setpoint as compared to 15 demands assuming 1670 MWt power. The change is slight because it is offset by the turbine-driven HPCI or RCIC pumps which draw more steam at the higher power level since they must supply more makeup water to the reactor than at the present powerlevel.
if a relief valve does stick open, the time until the turbine-driven pumps trip off due to low pressure is slightly longer for the rerate case. This is because the higher decay heat level produces more steam, which keeps the reactor above the pump's low pressure trip setpoint longer. Analysis of the time available until the water level drops to the top of active fuel at rerate shows an increase of about 5% for rerate over the 1670 MWt case (2.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> versus 2.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />).
The smallincrease in the time available to restore a power source or align a diesel-driven fire pump results in a slight improvement in the CDF. The small increase in the chance of a stuck open relief valve because of the increase in the 4
number of SRV demands from 15 to 16 (7% increase) was evaluated, ar 4 the change in the overall CDF was approximately 1 E-8/yr.
The dete'ministic r reviews confirmed that the plant equipment would continue to be operated as designed following the rerate, and the PRA review found no component expected to operate outside its design following an accident. In addition, a search for a meaningful increase in demands on the most risk-significant components identified only the SRV item discussed above. As a result, there was no need to modify component failure rates used in the PRA for rerate conditions.
- 4. On page 37 of the September 5,1997, submittal, NSP reported that from the baseline Level 2 PRA [probabilistic risk assessment], the potential for a large early release is on the order of 3% of the total CDF [ core damage frequency] and that this frequency remains at about 3% for the rerate CDF. - The large eady release frequency reported in the Monticello IPE[individualplant evaluation] was 4.15E-6/Yr, which represented about 16% ofits estimated CDF (2.6E-5tYr). Provide a basisidiscussion for the difference between LERF [large eady release frequency] estimated for IPE and LERF estimated for baseline and rerate analysis. ,
NSP Response The Monticello IPE submittal does not report a value for LERF. Figure 1.4-5 of the IPE does show the total early releases as being 16% of the total core damage frequency.
Most of these releases, however, are small because they are scrubbed through the suppression pool. The actual large early release frequency for the Monticello IPE would be 2.0E-6/yr, or about 7.4% of the total core damage frequency.
The LERF reported in our response to RAI Question #48 is still less than the IPE value of 2.0E-6/yr. In performing the most recent update for the Monticello PRA, changes to the classification of ATWS sequences were made. In the original IPE, two of the dominant accident sequences were conservatively classified as unscrubbed, when in fact reled:;cc would be scrubbed through the suppression pool. See sequences 9 and 10 of Figure 4.5-6 of the IPE submittal which total 1.5E-6/yr. In these sequences, high and low pressure injection arrest the core melt progression within the vessel once the core has become subcritical. Because the vessel is intact, all releases would be through the SRV tailpipes into the suppression pool before being released through the failed drywell. J
- 5. Page 10-16 of the December 4,1997, submittal stated in part: 'a sensitivity study was performed for tomado missiles which resulted in a negligible increase in risk." Provide a discussion on what this study entails and the basis for concluding that its effect on risk is
-negligible.
NSP Response The Other Extemal Events analysis for the Monticello IPEEE was largely performed by comparing the plant design with the 1975 Standard Review Plan. The exception was tomado missiles. Safety related structures at Monticello provide protection against missiles with the exception of a few doors and ventilation paths into buildings such as the reactor building. The IPEEE evaluated the potential for tornado missiles entering 5
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1 through these penetrations and quantified the expected core damage frequency assuming the failure of all the equipment in the rooms with these penetrations. The core da. mage frequency associated with the tomado missiles wts shown to be below 1E-7/yr which is well below the screening criteria presented in NUREG-1407.
The tornado missile evaluation was repeated for the rerate analysis. As expected, rerate does not affect the tomado frequency or the potential for missiles striking doors or j
ventilation paths into safety-related structures. However, as in the internal events and fire analyses, the timing of the accident sequences is shorter due to the higher decay heat levels. This has a small effect on the time available for the operator actions credited l
in the tomado missile accident sequences such as emergency depressurization and initiation of decay heat removal systems. The change in core damage frequency due to rerate in the tomado missile analysis remained below 1E-7/yr.
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