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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License ML20196J7651999-06-29029 June 1999 Provides Updated Info Re Loss of Feedwater & Loss of Electric Power Accident Analyses to Support TS Change Request 279 Re Core Protection Safety Limit,As Discussed at 990616 Meeting ML20196J7701999-06-29029 June 1999 Forwards LAR 285 for License DPR-50,clarifying Authority to Possess Radioactive Matls Without Unit Distinction,So That After Transfer of TMI-1 License to Amergen,Radioactive Matls May Continue to Be Moved Between TMI-1 & TMI-2 Units ML20209C0391999-06-29029 June 1999 Forwards LAR 77 to License DPR-73,clarifying Authority to Possess Radioactive Matls Without Unit Distinction,So That After Transfer of TMI-2 License to Amergen,Radioactive Matl May Continue to Be Moved Between TMI-1 & TMI-2 Units ML20196G2061999-06-23023 June 1999 Requests That NRC Update Current Service Lists to Reflect Listed Personnel Changes That Occurred at TMI 05000289/LER-1999-006, Forwards LER 99-006-00,providing Complete Description,Extent of Condition & Actions Taken in Association with Determination of Inability of Pressurizer Support Bolts to Meet FSAR Requirements1999-06-23023 June 1999 Forwards LER 99-006-00,providing Complete Description,Extent of Condition & Actions Taken in Association with Determination of Inability of Pressurizer Support Bolts to Meet FSAR Requirements ML20196D2171999-06-17017 June 1999 Forwards Pmpr 99-9, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990508- 0604.New Summary Personnel Table Was Added to Rept Period.Matl Scientist Joined Staff Period ML20196A0431999-06-15015 June 1999 Providess Notification That Design Verification Activities Related to Calculations Supporting Analytical Values Identified in Gpu Nuclear Ltr to NRC Has Been Completed 05000289/LER-1999-004, Forwards LER 99-004-00,re Discovery of Emergency FW Pump Bearing Failure During Performance of Oil Change on 990510. Event Was Determined Reportable IAW 10CFR50.73,since Pump Was Determined to Be Inoperable Longer than TS AOT1999-06-0909 June 1999 Forwards LER 99-004-00,re Discovery of Emergency FW Pump Bearing Failure During Performance of Oil Change on 990510. Event Was Determined Reportable IAW 10CFR50.73,since Pump Was Determined to Be Inoperable Longer than TS AOT ML20212K2541999-06-0808 June 1999 Submits Concerns Re Millstone NPP & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Requests That NRC Provide Adequate Emergency Planning in Case of Radiological Accident ML20212K2671999-06-0808 June 1999 Submits Concerns Re Millstone NPP & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Requests That NRC Provide Adequate Emergency Planning in Case of Radiological Accident ML20195E2751999-06-0404 June 1999 Informs That PCTs & LOCA Lhr Limits Submitted in Util Ltr for LOCA Reanalysis Performed in Support of TMI-1 20% Tube Plugging Amend Request Have Been Revised.Revised PCT & LOCA Lhr Limit Values Are Provided on Encl Table 1 ML20195E3281999-06-0404 June 1999 Forwards Application for Amend to License DPR-50,modifying Conditions Which Allow Reduction in Number of Means for Maintaining Decay Heat Removal Capability During Shutdown Conditions ML20195C5721999-06-0202 June 1999 Forwards Description of Gpu Nuclear Plans for Corrective Actions for 1 H Fire Barriers in Fire Zones AB-FZ-3,AB-FZ-5, AB-FZ-7,FH-FZ-2 & Previous Commitments for Fire Zones CB-FA-1 & FH-FZ-6 ML20207E2561999-05-25025 May 1999 Submits 30-day Written Rept on Significant PCT Change in ECCS Analyses at TMI-1 ML20195B2461999-05-21021 May 1999 Forwards Itemized Response to NRC 990506 RAI for TS Change Request 279 Re Core Protection Safety Limit ML20206R6461999-05-13013 May 1999 Forwards Rev 39 of Modified Amended Physical Security Plan for TMI 05000289/LER-1999-003, Forwards LER 99-003-00, Discovery of Condition Outside UFSAR Design Basis for CR Habitability, Which Was Determined Reportable on 990310.Rept Is Being Submitted Four Weeks Later than Required,Per Discussion with NRC1999-05-0707 May 1999 Forwards LER 99-003-00, Discovery of Condition Outside UFSAR Design Basis for CR Habitability, Which Was Determined Reportable on 990310.Rept Is Being Submitted Four Weeks Later than Required,Per Discussion with NRC ML20206K6301999-05-0707 May 1999 Provides Addl Info Re TMI-1 LOFW Accident re-analysis Assumptions for 20% Average SG Tube Plugging as Discussed on 990421 ML20206H0781999-04-30030 April 1999 Forwards Rev 0 to 1092, TMI Emergency Plan. Summary of Changes Encl ML20206J4811999-04-30030 April 1999 Provides Summary of Activities at TMI-2 During First Quarter of 1999.TMI-2 RB Was Not Inspected During Quarter.Routine Radiological Surveys of Auxiliary & Fuel Handling Bldgs Did Not Identify Any Significant Adverse Trends ML20206E4121999-04-27027 April 1999 Requests That TS Change Request 257 Be Withdrawn ML20206C5211999-04-23023 April 1999 Requests Mod to Encl Indemnity Agreement Number B-64,on Behalf of Gpu & Affiliates,Meed,Jcpl,Penelec & Amergen Energy Co,Llc.Ltr Supersedes & Withdraws 990405 Request Submitted to NRC ML20206C8261999-04-22022 April 1999 Submits Financial Info IAW Requirements of 10CFR50.71(b) & 10CFR140.21 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059H5351990-09-10010 September 1990 Forwards Encls 1-3 of Generic Ltr 90-07 Re Operator Licensing Exam Schedule ML20059G0641990-08-31031 August 1990 Advises That Util Agreed to Revised Frequency of Once Every 12 Months for Corrective Actions Audits Per Tech Spec Change Request 65 Based on 900718 & 19 Discussions ML20059F1691990-08-30030 August 1990 Requests Exemption from Requirements of 10CFR50,App J, Section III.D.1(a) for Facility Re Schedule Requirements for Connecting Type a Testing w/10-yr Inservice Insp Interval, Per 10CFR50.12(a)(2) ML20064A4661990-08-30030 August 1990 Responds to 900803 SALP Rept 50-289/89-99.TMI Does Not Expect to Be Lead Plant for Installation of Advanced Control Sys.Maint Backlog Goals Established.Info on Emergency Preparedness & Engineering/Technical Support Encl ML20059C8791990-08-29029 August 1990 Forwards TMI-1 Semiannual Effluent & Release Rept for Jan - June 1990, Including Executive Summary of Effluent Release Rept,Disposal & Effluent Release Data & Assessment of Radiation Doses.No Changes to ODCM for Reporting Period ML20059D5491990-08-29029 August 1990 Responds to NRC Re Notice of Violation & Proposed Imposition of Civil Penalty Re Personnel Inattentiveness & Failure of Site Managers to Correct Condition.Shift & Immediate Supervisor Discharged ML20059C7851990-08-27027 August 1990 Forwards Rev 5 to Sys Description 3184-007, Solid Waste Staging Facility, Updating Minor Changes to Pages 6,8,9 & 13 ML20059C1091990-08-24024 August 1990 Forwards Rev 6 to Physical Security Contingency Plan.Rev Withheld ML20059B8251990-08-24024 August 1990 Forwards Payment of Civil Penalty in Amount of $50,000,per NRC ML20056B4651990-08-20020 August 1990 Corrects Statement Made in 900716 Response to NRC Bulletin 90-001, Loss of Fill-Oil in Rosemount Transmitters. Identified That Only Half of Operating Crews Provided W/ Briefing on Bulletin ML20058Q1851990-08-17017 August 1990 Requests That Distribution List for TMI-2 Correspondence Be Updated to Be Consistent W/Recently Implemented Organizational Changes.Ee Kintner,Mb Roche & Wj Marshall Should Be Deleted ML20058Q1821990-08-13013 August 1990 Advises That Util Will No Longer Provide Annual Update to Dewatering Sys for Defueling Canisters Sys Description,Per NRC .W/Completion of Defueling & Shipment of All Defueling Canisters Offsite,Sys Has Been Deactivated ML20058Q1721990-08-13013 August 1990 Forwards TMI-2 Effluent & Offsite Dose Rept,First Quarter 1990, Update ML20058M7201990-08-0303 August 1990 Forwards Rev 2 to TER 3232-019, Div Technical Evaluation Rept for Processed Water Disposal Sys. Mods Include Elimination of Pelletizer & Relocation of Druming Station to Discharge of Blender/Dryer ML20055J4581990-07-27027 July 1990 Responds to Violations Noted in Insp Rept 50-289/90-10. Corrective Actions:Missing Support Brace on Cable Tray Support Found & Corrected ML20055J4561990-07-27027 July 1990 Advises That Info Contained in Generic Ltr 90-06,not Applicable to Current Nonoperating & Defueled Condition of Facility.Generic Ltr Will Be Reevaluated,If Decision Made to Restart Facility ML20055H6901990-07-20020 July 1990 Forwards Rev 25 to TMI-2 Organization Plan for NRC Review & Approval.Rev Proposes Consolidation of Plant Operations & Maint Sections Into Plant Operation & Maint Section ML20055G4431990-07-19019 July 1990 Forwards Rev 12 to 990-1745, TMI-1 Fire Hazards Analysis Rept & Update 9 to FSAR for TMI-1 ML20055G8781990-07-19019 July 1990 Discusses Compliance W/Reg Guide 1.97 Re Containment High Range Radiation Monitors,Per 900507-11 Insp.Physical Separation of Power Cables & Required Isolation Will Be Provided to Satisfy Reg Guide Category 1 Requirements ML20055F9601990-07-11011 July 1990 Forwards, 1990 TMI Nuclear Station Annual Emergency Exercise Scenario to Be Conducted on 900912.W/o Encl ML20044A9531990-07-0909 July 1990 Forwards Util Response to Weaknesses Identified in Maint Team Insp Rept 50-289/89-82.Corrective Actions:Engineering Personnel Reminded to Assure Documented Approval Obtained Prior to Proceeding W/Work ML20055E0481990-07-0505 July 1990 Documents Action Taken by Util to Improve Heat Sink Protection Sys & Current Status of Sys.Main Feedwater Logic Circuits Modified Prior to Startup from 8R Outage to Eliminate Potential for Inadvertent Isolation ML20055E0011990-07-0202 July 1990 Forwards Revs 1 & 2 to Topical Rept 067, TMI-1 Cycle 8 Core Operating Limits Rept, Per Tech Spec 6.9.5.4 ML20055C9971990-06-28028 June 1990 Forwards Rev 27 to Physical Security Plan.Rev Withheld ML20055D2071990-06-28028 June 1990 Forwards Certification of TMI-1 Simulation Facility,Per 10CFR55.45.b.5.Resumes of Personnel Involved Encl. Resumes Withheld (Ref 10CFR2.790(a)(6)) ML20055D0861990-06-25025 June 1990 Documents Deviation from Requirements of Reg Guide 1.97,per Insp on 900507-11.Based on Most Limiting Analysis,Existing Range of 0-1,200 Psi Sufficient.Deviation Consistent W/B&W Owners Group Task Force Evaluation of Reg Guide ML20043H4031990-06-18018 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issue Resolved W/Imposition of Requirements or Corrective Actions. ML20043H4851990-06-18018 June 1990 Forwards Application for Amend to License DPR-50,consisting of Tech Spec Change Request 179 ML20043F9921990-06-11011 June 1990 Forwards Listing of Exam Ref Matl Sent on 900601 in Response to 900505 Ltr ML20043F0661990-06-0404 June 1990 Forwards Inservice Insp Data Rept for Period 880816-900304. Owner Rept for Repairs or Replacements Performed on ASME Section XI Class 1 & 2 Components,Also Encl ML20055C9041990-05-23023 May 1990 Advises That App a to Rept Is Set of Recommendations from Safety Advisory Board on Possible Research Opportunities ML20043B2391990-05-18018 May 1990 Revises Commitments in Encl Met Ed 800430 Ltr Re QA of Diesel Generator Fuel Oil.Requirement for QC Review for Acceptability Prior to Filling Diesel Generator Fuel Oil Storage Tanks Deleted from Procedure ML20043A5441990-05-16016 May 1990 Discusses Status of Safety & Performance Improvement Program Portion of B&W Owners Group EOP Review Project ML20043A5311990-05-15015 May 1990 Responds to Violations Noted in Insp Rept 50-289/89-82. Corrective Actions:Periodic Insp Program Established Utilizing Checklist for Stored Equipment & Existing Tool Rooms Will Be Purged of Controlled or Unneeded Matls ML20043A2321990-05-11011 May 1990 Forwards TMI-1 Reactor Bldg 15-Yr Tendon Surveillance (Insp Period 5) Technical Rept 069.Evaluations Conclude That Test & Insp Results Demonstrate TMI-1 Reactor Bldg post- Tensioning Sys in Good Condition ML20042G2741990-05-0404 May 1990 Forwards Semiannual Update of Projects Listed in Categories A,B & C of long-range Planning Program Integrated Schedule ML20012F2621990-04-0202 April 1990 Responds to Violation Noted in Insp Rept 50-289/89-26. Corrective Actions:Util Policy of Shift Supervisor Involvement in Bypassing & Resetting Safety Sys Expanded to Include Shutdown Conditions & Technicians Briefed ML20012F2611990-04-0202 April 1990 Provides Supplemental Response to Station Blackout Rule. Target Reliability of 0.975 Chosen for Emergency Diesel Generators.Diesel Generator Reliability Program May Change Based on Final Resolution of Generic Issue B-56 ML20012F2731990-03-30030 March 1990 Confirms 900328 Conversations & Provides Technical Basis for Planned Actions to Correct Present Power Limitation Due to High Steam Generator Secondary Side Differential Pressure. Main Turbine Will Be Tripped from 80% Power ML20042D8281990-03-23023 March 1990 Fulfills Requirements of Tech Spec Section 4.19.5.a Re once-through Steam Generator Tubes post-inservice Insp Rept for Unscheduled Outage 8U-1 ML20012D7001990-03-22022 March 1990 Forwards Util Response to Generic Ltr 90-01 Re NRC Regulatory Impact Survey.Site Mgt & Staff Hour Categories Added to Response ML20012D7121990-03-21021 March 1990 Forwards Rev 0 to TMI-1 Cycle 8 Core Operating Limits Rept. ML20012C4771990-03-12012 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' Per 10CFR50.54(f). Current Design Adequate W/O Addl Tech Specs ML20012B8241990-03-12012 March 1990 Forwards Application for Tech Spec Change Request 199 to License DPR-50,revising Tech Specs Re Steam Generator Tube Insp Requirements ML20011F5251990-02-23023 February 1990 Documents Interpretation of Tech Spec 5.3.1.1 Re Design Features of Fuel Assemblies in Light of Issuance of Generic Ltr 90-02.Tech Spec Change Request Re Utilization of Dummy Fuel Rods or Open Water Channels Will Be Filed by 900420 ML20055C3931990-02-23023 February 1990 Documents Interpretation of Tech Spec 4.19.5.a Re once- Through Steam Generator Tube post-inservice Insp Rept for Refueling Interval 8R.Total of Eight Tubes Removed from Svc by Plugging ML20011F6651990-02-22022 February 1990 Forwards Updated Status Summary of Consideration of TMI-1 PRA Recommendations as of 891231.Changes to Torque Switch Settings for DH-V-4A & B Will Be Implemented in Refueling Outage 8 Re Closing Against High Differential Pressure ML20006C2901990-01-26026 January 1990 Provides Addl Info Supporting Deferral of Seismic Qualification Util Group Walkdowns to 10R Outage.Performance of Walkdowns Provide Proper Scheduling & Priority for Resolution of USI A-46 for TMI-1 ML20011E1221990-01-26026 January 1990 Forwards Response to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Audit Rept Determined That Operation of Decay Heat Closed Cooling Water Sys Consistent W/Design Basis Documents ML19354E8601990-01-25025 January 1990 Requests Approval for Use of B&W Steam Generator Plugs Mfg W/Alternate Matl (nickel-base Alloy/Alloy 600).Alloy 600 Has Superior Corrosion Resistance to Primary Water Stress Corrosion Cracking 1990-09-10
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GPU Nuclear Corporation Nuclear :::,ome: s 48o Middletown, Pennsylvania 17057 0191 717 944 7621 TELEX 84 2386 1
Writer's Direct Dial Number:
October 13, 1986 5211-86-2169 Dr. Thomas E. Murley Region I, Regional Administrator US Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
Dear Dr. Murley:
Three Mile Island Nuclear Station, Unit 1 (TMI-1)
Operating License No. DPR-50 Docket Nos. 50-289 Response to Notice of Violations on Inspection Report 86-12 Attached is the GPUN response to Appendix A of Inspection Report No.
l 50-289/86-12 " Notice of Violation."
In addition, as you requested, GPUN provides the following summary of actions taken on other modifications.
A broad program has been implemented to ensure PAT I identified problems will be corrected in Cycle 6 (6R) Outage work. This has been accomplished by increased management involvement, training sessions, and audits of specific 6R modifications. This three prong approach was geared to ensure proper implementation of the modification control procedures. Specifically, GPUN targeted four 6R projects to have a comprehensive audit performed. These projects were chosen based on their overall importance and to access a broad range of engineering disciplines. The four mods chosen were HSPS, ESF Ventilation, Appendix R - Remote Shutdown, and Radwaste Pumps.
The detailed audits have been performed and the results are being tabulated.
Concerns or weaknesses found during the audits will be resolved prior to completion of the project. Should the concerns or weaknesses identified indicate generic questions, other projects may be chosen to undergo detailed design verification reviews.
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GPU Nuclear Corporation is a subsidiary of the General Public Utilities Corporation fECI l
5211-86-2169 October 13, 1986 For work performed by Architect-Engineers (AEs), GPUN had each of the three AEs prepare a review of the status of engineering documentation. The AEs per/ormed reviews on key projects for 6R. The results have been tabulated and items identified will be resolved.
Sincerely,
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H. D. k:11 Vice President & Director, TMI-1 HDH/DVH/spb:0685A cc: R. Conte Sworn beforeand mesubscrib{d this d day to of of def f.f u ; , 1986.
aint b blL 'U}G Notary Put)1ic 4
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SEARON P, ERO?!N NOTARY PUEL'C MIDDLETOWN BORD DAUPHIN COUNTY MY COMFIS$10N EXPIRES JUNE 12,1989 Member, rennsylvania Association of Notaries l
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ATTACMENT 1 As a result of an inspection conducted between March 3-27 and July 7-11, 1986 and in accordance with the NRC Enforcement Policy (10 CFR 2, Appendix C), the following violations were identified:
Violation A 10 CFR 50.59(b) states, in part, that, "... Licensee ... records [of changes in the facility or procedures as described in the safety analysis report]
shall include a written safety evaluation which provides the basis for the determination that the change ... does not involve an unreviewed safety question ...."
7 Technical Functions Procedure EP-016, Revision 1-00, dated January 18, 1985, " Nuclear Safety / Environmental Impact Evaluation," Exhibit 3, paragraph 3.3, requires, in part, that the written safety evaluations for facility changes describe how the proposed change will or will not affect the safety functions by addressing concerns such as: (3.3.1) system performance; (3.3.3) natural phenomena with respect to seismic classification; (3.3.9) electrical isolation criteria; and, (3.3.11) single failure criteria.
Contrary to the above, licensee safety evaluations for various safety grade modifications did not fully address various safety performance functions as noted below.
-- As of March 27, 1986, lead shielding was installed on important-to-safety piping without a proper evaluation on system performance during a design basis seismic event.
-- As of March 26, 1986, the two-hour backup instrument air system for the Emergency Feedwater System (EFW) was susceptible to single f ailure.
- 2. Administrative Procedure 1001 A, Revision 10, dated April 17, 1986,
" Procedure Review and Approval," Figure AP 1001 A-5 on procedure change safety evaluations, paragraph 2, requires, in part, that a determination be made that the procedure change does not cause an unreviewed safety question.
Contrary to the above, as of March 27, 1985, safety evaluations related to EFW pump surveillance test (SP 1303-11.42) changes did not adequately determine that an unreviewed safety question existed, in that the surveillance test provided a test lineup that was inconsistent with the applicable section of the updated safety analysis report.
Response to Violation A Action Taken to Resolve Specific Concerns All temporary shielding was removed from TMI Unit 1 important to safety systems prior to startup from the SM Outage. At that time, the shield blocks installed at the letdown prefilters MU-F2A and 2B were considered to be a permanent installation. Since then, this installation has been re-evaluated and is now considered to be a temporary installation. This installation has had an engineering evaluation which included a safety determination. These blocks presently satisfy correct installation requirements. Additionally, after startup one temporary shielding installation was completed. This installation was made only af ter an engineering evaluation which included a Safety Evaluation was performed.
GPUN is revising the procedure for Installation of Lead Shielding. This procedure revision is in the final approval cycle and is scheduled to be completely signed off by the end of October 1986. This procedure revision incorporates the following points:
-- 'An engineering evaluation will be performed prior to each installation of temporary shieldin.g.
To ensure that plant conditions are maintained consistent with possible restrictions imposed by a temporary shielding engineering evaluation, the shif t supervisor shall provide approval for proposed temporary shielding installations.
-- The engineering technical evaluation will consider the
- piping size, code allowables, seismic constraints, and system, operating parameters. The procedure will also specify shielding fastening requirements when applicable.
-- The Safety Evaluation wi.ll follow established GPUN procedure requirements. Additional questions specific to shielding installation following INP0 recommended good practices will be incorporated in the procedure revision.
The Two-Hour Backup Instrument Air system configuration was corrected prior to startup from the SM Outage to allow the system to withstand a single active failure identified during the PAT inspection. A safety evaluation and procedural changes were completed before TMI-l returned to power. This was reported to the NRC by phone and by License Event Report 86-07 (forwarded April 25,1986). With three independent sources for supplying air to the EFW system, the piping arrangement was overly complex. The corrective action was to simplify the design by isolating piping that was not seismically qualified.
A comprehensive Single Failure Analysis on the air supply system to the EFW valves has been completed by the architect-engineer and is currently being reviewed by GPUN. This review will be completed in October,1986. This '
analysis is to ensure that the system will perform its safety design function during design accidents with a single active failure.
EFW pump surveillance test procedure 1303-11.42 has been revised to agree with the FSAR. This revision includes checks for potential back leakage through idle pump check valves. The safety evaluation now properly represents agreement between the surveillance and the FSAR.
Action to Prevent Reoccurrence The revised Lead Shielding Procedure will prevent similar problems in the future. The past problems were due to weak procedure requirements.
Management continued attention to full and precise procedure implementation for Safety Evaluations and the detailed design verification reviews will identify weaknesses such as the single active failure identified by PAT I.
Further programmatic changes in the design area are covered in the response to Violation B.
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Violation B The 10 CFR 50 Appendix B Criterion II and the NRC approved Quality Assurance Plan (QAP), dated November 1985, establish overall quality assurance program requirements for the design and construction of safety-related structures, systems, and components. To implement these requirements, the QAP Appendix C commits to the implementation of Regulatory Guide 1.64, Revision 2, June 1976, and ANSI N45.2.11,1974, on " Quality Assurance Requirements for the Design of Nuclear Power Plants."
- 1. ANSI N45.2.ll, paragraphs 3.1 and 4.2, require, in part, that applicable design inputs and bases be identified in sufficient detail, documented, and their selection reviewed and approved.
Contrary to the above, as of March 27, 1986:
-- The design input review and approval process permitted battery sizing calculations to be performed using a minimum temperature for which no basis was referenced.
(Actual battery temperatures were lower than the minimum
- used in the calculation.) Also other design input data used in the battery sizing calculation, such as pump and valve starting and running current, lacked sufficient references to permit the complete verification of the calculations.
-- The design input review and approval process permitted the use of preliminary, unverified design input as a basis for fuse changes in de power distribution panels.
- 2. ANSI N45.2.11, paragraph 5.1.3, requires, in part, that systematic methods be established for communicating needed design information across external design interfaces.
Contrary to the above, as of March 27, 1986, design input associated with sizing of regulating valves installed in the two-hour backup supply air system was provided by the licensee to an architect-engineer but was subsequently changed without notifying the affected design organization.
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- 3. ANSI N45.2.11, paragraph 6.1, requires, in part, that measures shall be applied to verify the adequacy of design. Technical Functions Division Procedure 5000-ADM-7311.02 (EP-009 ), Revision 1-00, dated July 31, 1985,
" Design Verification," requires, in part, the verification of calculations, the preparation of verification checklists, and the l verification of system designs.
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Contrary to the above, as of March 27, 1986, design verification requirements had not been fully adhered to, as noted below:
-- Three engineering calculations, Calculation No.
1101X-322F-165 - Flow Rates for Two-Hour Backup Air Supply System; Calculation No.1101X-322F-424 EFW System Resistance; and Calculation No.1302X-5320-A50 - Shielding stress, had no calculation verifications performed.
-- Three design verifications, Calculation No.1101X-3228-003
- Air Consumption by EF-Y-30 Valves; Calculation No.
110lX-322F-157 - EFW Pump Turbine Relief Yalve Setpoint; and Calculation No.1101X-3228-004 - Air consumption by MS-V-6, did not have required verification checklists prepared.
-- System Design Descriptions 424A, B, C, D, and E, Division I and II, involving the EFW system, its backup instrument air supply, and supporting instrumentation, had not been design verified.
-- Nine shielding installations were installed prior to the calculations to support the shielding having been verified.
- 4. ANSI N45.2.11, paragraph 6.3, requires, in part, adequate pre-operational testing be specified. Technical Functions Procedure 5000-ADM-7335.01 (SP-001), Revision 0-00, dated November 15,1984, "Startup and Test Program and Test Requirements," paragraph 4.7.1 requires, in part, that functional test procedures verify that modifications perform their intended functions.
Contrary to the above, as of March 27, 1986, post-modification testing of the two-hour backup air supply modification did not confirm that the modification produced expected results per the design basis and did not have acceptance criteria consistent with the system design basis.
Response to Violation B Action Taken to Resolve Specific Concerns The battery sizing calculation has been redone using correct parameters and has undergone a design verification and review. No safety issues were identified.
The preliminary, unverified design input referred to in the violation was a GPUN Technical Data Report (TDR). The fuse change modification had been approved based on this unissued TDR. Since then, this TDR has been properly complete d. In addition, the fuse changes modification was reviewed for any possible impact and none was found.
GPUN is re-evaluating the design input for the sizing of the regulating valves. This evaluation is a portion of an overall evaluation of the Two-Hour Backup Instrument Air system. This overall evaluation will consider the concerns expressed by PAT I, other concerns, and test results. The result of this evaluation will be a document (s) that will be used to maintain the system to the design basis intent. This evaluation is scheduled to be completed by the end of November,1986.
The three calculations noted have had the verifications performed.
The three design verifications noted have had the checklists prepared and completed.
The design verification of System Design Descriptions 424A, B, C, D, and E, Division I & II is being performed as part of a technical audit review by GPUN.
This is presently in progress and is scheduled to be completed by December 31, 1986. A verification plan will be finalized in the documentation package.
For Lead Shielding see Violation A response.
The evaluation of post modification testing of the Two-Hour Backup Air system conducted is part of the previously stated evaluation in the third paragraph of this response. As such, validity of the test results will be considered in this evaluation.
Action Taken to Prevent Reoccurrence Following the PAT I Inspection, GPUN reviewed the existing Design Program.
This review found that many of the problems identified in the PAT I Inspection were due to not following procedures. To correct this problem, two things were done. Procedures were revised to provide clearer direction and correct deficiencies, and a Training / Instruction Program was developed for all i
Technical Functions personnel.
Two of the key procedures, EP-006 (Calculations) and EP-009 (Design Verification) have been revised. Other procedures were revised or in the final approval stages.
The Training / Instruction Program was given to all Technical Functions personnel during the summer. This program reviewed the PAT I major items, procedure changes and reinforced the need to follow all procedures.
GPUN believes the above improvements and training along with continued management involvement will provide positive results. Management controls are being implemented in the modification process to ensure full procedure implementation in this area. Also, as stated in the GPUN response to the l SALP, one or two balanced performance appraisal type audits will be conducted before the end of 1987. This audit (s) will provide the feedback of the effectiveness of our program improvements.
! GPUN has re-emphasized to the Projects group personnel who deal with the architect / engineers that any change to a design document must be formally transmitted to the AE.
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Violation C The 10 CFR 50 Appendix B Criterion XVI and the NRC-approved Quality Assurance Plan (QAP), dated November 1,1985, Sections 8.1.1 and 8.2.1 require, in part, that the licensee assure conditions adverse to quality; such as, deficiencies, deviations, and nonconformances, are promptly corrected.
Contrary to the above, as of March 27, 1986, the licensee did not assure that the below-noted conditions adverse to quality were promptly corrected.
-- At various times between October 3,1985, and March 27, 1986, out-of-specification data for important-to-safety systems existed on auxiliary operator log sheets without being properly identified as such and without being properly explained as required by licensee adninistrative control s.
Design documents, which included control room and engineering drawings for various important-to-safety systems, either (1) were not updated in accordance with licensee administrative control or (2) contained errors.
Response to Violation C and Action to Prevent Reoccurrence Additional emphasis has been placed on Auxiliary Operator (A/0) log sheets.
This emphasis has proven effective in correcting this problem. To ensure our continued success in this area, additional documentation of Operations Engineering review has been added to the daily A/O log sheets. Additionally, review of log sheets has been emphasized in the off-duty management tour program.
The control room drawings have been revised and are up to date. This was confirmed in the PAT II inspection. All of the drawing deficiencies which were identified by PAT I have been corrected. Continuing awareness is being given to this area.
A revision to the GPUN drawings procedure has been issued. This revision establishes priority levels for initiating drawing revisions. The plan is to subdivide the over 60,000 drawings at TMI-l into four separate priority categories with varying drawing revision requirements. For example, a revision priority 1 drawing "must be revised expeditiously (scheduled immediately - target for completion is 30 days) to incorporate any outstanding change document." After review, we have determined that many of the 75 documents discussed in the PAT'I report will be classified a revision priority 3, which will allow six or more change documents to be outstanding because of their infrequent use. Thus, the outstanding posting status for many of these drawings will no longer be procedurally deficient. Those which are deficient are being corrected. The recoding of the TMI-l Plant Configuration Control List, with the drawing revision priorities, has commenced and is scheduled for completion during 1986.
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Violation D i The 10 CFR 50 Appendix B, Criterion V requires that activities affecting quality shall be prescribed by instructions, procedures or drawings and shall be accomplished in accordance with those instructions, procedures, or drawings.
1 i 1. Technical Functions Procedure 5000-ADM-7350.05 (EMP-002), Revision 0-00, dated September 13,1985, " Mini-Mods," in Exhibit 2, paragraphs 2 and 7, require, in part, the documentation of sections of the safety analysis report that need updating for important-to-safety modifications.
] Exhibit 2 also requires the documentation of various design information.
Contrary to the above, as of March 27, 1986, the documents associated with two mini-mods (additional limit switches for the fuel handling crane and removal of instrument air line from EFW pump recirculation valves) were incorrectly marked as no change being required to the FSAR when, in fact, changes to the FSAR were required. For these and other important-to-safety mini mods, not all the design information required to be addressed by EMP-002 was addressed.
- 2. Installation specification for lead shielding around letdown prefilters, 3
MU-F2A and 2B, required that the center of gravity of the top blocks be 4
no more than 12 inches off the floor, the blocks be no closer than 2 feet to important-to-safety (ITS) equipment due to seismic considerations, and that a warning sign be installed identifying the 2 foot requirement.
I Contrary to the above, as of March 27, 1986, the lead shielding
. installation on MU-F2A and 2B had the top block center of gravity 15 l inches off the floor in some locations. ITS valves SF-V-77 and SF-V-71 were located within 6 inches and 19 inches of the blocks, respectively, j and no warning sign was installed.
1 Design Calculation No. 609-0293, Revision 0 " Bottle Rack for RM-13h" (EFW 3.
! Two-Hour Backup Instrument Air (TBIA) Subsystem), required that the air i bottle chain restraints preclude vertical movement with turnbuckles i attached to the chain to assure adequate tension. The chain and
- turnbuckle connection were to be made by open "S" chain links, which were l to be closed after installation.
i Contrary to the above, as of March 27, 1986, the TBIA air bottle i restraints had no turnbuckles, certain restraints were loose, and "S" l links were not closed.
Response to Violation D Action Taken to Resolve Specific Concerns
{ A Task Request was issued to update the FSAR for the two mini mods stated.
I The issued Task Request will result in the FSAR being updated. The Safety Evaluations for these two mini mods are part of the Installation Specifications and are not stand alone documents. Since these mods are complete and a Task Request was issued, the Safety Evaluation itself will not be revised. An audit was performed on the remaining mini mods and no FSAR update problems were found.
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The design information required to be addressed by EMP_002 (Mini Mods)
Exhibit 2 was interpreted by the NRC to be mandatory. Previous guidance had been that the items in Exhibit 2, Procedure Task Requirement outline, were suggested points to address. If the item was not pertinent to the modification, then it need not be addressed. The procedure is being revised to clearly specify that each item need only be addressed if applicable.
The installation of the shielding blocks is covered in Violation A response.
The loose chain restraints for the Bottle Rack have been corrected and the "S" links have been closed. The " missing" turnbuckles are not required as documented in a 1982 Field Change Request.
Action Taken to Prevent Reoccurrence The two examples stated for not correctly completing the Safety Evaluation resulted from a misunderstanding of the FSAR updating requirements. GPUN has clarified the applicable procedure, specifically instructed the individuals involved, and has conducted widespread training on this issue. These actions are considered to be appropriate to address this issue.
The revised lead shielding procedure will eliminate f uture shielding problems.
The issue of the loose chains appears to be an isolated case. Maintenance did check other items in this area and found no similar problems. Therefore no further action is anticipated.
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RECElVED-REG 10tl i 1985 GCI lg pit 2: 57
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