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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML17309A6211997-09-29029 September 1997 Part 21 Rept Re Final Disposition of Masterflow 713 & Embeco 636 Grout Nonconformance Reported by Master Builders,Inc. Licensee Continuing to Monitor shelf-life of Masterflow 713 & Embeco 636 Grouts Produced at Rancho Cucamonga ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML20134H3361996-11-0505 November 1996 Part 21 Rept Re Defective Inner Thrust Bearing 1801461-01 Used in PSA 35 Mechanical Shock Arrestor Used as Restraint on Piping Sys for Nuclear Generating Plant.Lot of Defective Parts Located & Isolated to Three Customers ML20115D2001996-07-0909 July 1996 Part 21 Rept Re Mfg Defect of Enterprise DSR-4 & DSRV-4 Edgs,Originally Mfg by Calcon Corp.Amot Control Corp Purchased Calcon Product Line & Maintains Design & Production.Valves Returned to Cooper Energy Svcs on 960131 ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20127D1491992-09-0404 September 1992 Part 21 Rept Re Defect in Component of DSRV-16-4 Enterprise Standby DG Sys Jacket Water Pump Shaft.Caused by Incorrect Tapers Machined on Shaft Due to Vendor Mismatching.All Affected Shafts Recalled & Quality Insp Plans Changed ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20087D3191992-01-14014 January 1992 Potential Part 21 Rept Re Problems W/Elmwood/Fasco Contactor Carriers Breaking in Contactor Model 30-FO-30. Caused by Distortion/Shrinkage of Molded Phenolic Contactor Carrier.Replacement Contactors Installed ML17223A5941990-03-0909 March 1990 Errata to 900126 Part 21 Rept Re Anchor/Darling Actuators Incorporating Use of Teldyne-Republic four-way Valves.Lists Plants Inadvertently Left Out in Original Rept ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20248E0121989-09-13013 September 1989 Supplemental Part 21 Rept Re Potential Problem W/Six Specific Engine Control Devices in Air Start,Lube Oil, Jacket Water & Crankcase Sys.Initially Reported on 890429. California Controls Co Will Redesign Valve Seating ML20246K7401989-04-26026 April 1989 Part 21 Rept Re Incorrectly Stamped Name Plates on Certain Asco Nuclear Qualified Valves.Vendor Will Contact Each Affected Facility & Furnish Correctly Stamped Plates & in Near Future Discontinue Sale of Rebuild Kits for Valves ML20247P7991989-04-0404 April 1989 Part 21 Rept Re Atmospheric Dump Valves.Cause of Failure Speculative But Result of Piston Ring That Failed to Seal. Resolution to Problem Requires Increasing Pilot Valve Capacity & Reworking of Plug to Enlarge Pilot Flow Area ML20206M4401988-11-21021 November 1988 Deficiency Rept Re Misapplication of Raychem Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880920.Investigation Is in Process.Final Rept Will Be Submitted by 881222 ML20205C9291988-10-18018 October 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow,Per 10CFR21 & 50.55 Requirements.Item Being Tracked by MTS EAI B-5115 & Scheduled for Completion 881030 ML20205D6651988-10-18018 October 1988 Part 21 & Deficiency Rept Re Penetration Seals Found Not to Be Watertight.Initially Reported on 880609.Water Leakage Tests Performed on Unit Upper Cable Spreading Room Seals. All Floor Penetration Seal Assemblies Repaired ML20207P0451988-10-0505 October 1988 Part 21 Rept 146 Re Defect in Left Intercooler Inlet Adapter on Standby Diesel Engine Generator.Recommends Utils Inspect Left Intake Manifold Drain as Part of Operating Plan.Addl Info Expected by 881015 ML20155D6471988-09-28028 September 1988 Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880629.Final Rept Delayed Until 881020 ML20207J7361988-09-20020 September 1988 Interim Deficiency Rept Re Misapplication of Vendor Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880601.Final Rept Expected Prior to 881123 ML20153E2271988-09-0101 September 1988 Part 21 & Deficiency Rept Re ESF Filtration Unit Bolts. Initially Reported on 880628.Contractor Conducted Training Session for Personnel to Stress Importance of Clarifying Incomplete Drawing Info & Requirements of Bolting Procedure ML20151V1901988-08-16016 August 1988 Deficiency Rept Re non-water Tight Penetration Seals.Test Rig Constructed to Simulate Typical Upper Cable Spreading Room Configuration & Sealants Verified to Provide Waterproof Seal.Next Rept Will Be Submitted by 881020 ML20196L4811988-07-0707 July 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880601.Investigation in Progress to Determine Full Scope of Condition.Final Rept Will Be Submitted by 881001 ML20151A7781988-07-0606 July 1988 Deficiency Rept Re nonwater-tight Penetration Seals. Initially Reported on 880609.Investigation Incomplete.Next Rept Expected by 880818 ML20196C2971988-06-28028 June 1988 Deficiency Rept Re ESF Filtration Bolts.Initially Reported on 880601.Investigation of Root Cause of Condition Ongoing. Final Rept Will Be Submitted by 880901 ML20195D8541988-06-16016 June 1988 Part 21 Rept Re Potentially Reportable Condition Associated W/Dresser Model 7440W Check Valves Supplied W/Flow Direction Arrow Stamped Opposite to Valve Flow.Investigation Being Conducted.Evaluation of Bechtel Western Power Co Ltr Encl ML20154J4101988-05-12012 May 1988 Addendum 1 to Supplemental Part 21 Rept 145 Re Potential Problem w/F-573-156 Pressure Sensor/Lube Oil Trip.Initially Reported on 880429.Addl 1-1/8-inch Diameter W/Deep Counterbone in Pressure Head Added to Activate Valve ML20154A6841988-05-10010 May 1988 Deficiency Rept Re Electrical Cable Tray Separation. Initially Reported on 880414.Walkdown of All safety-related Cable Trays Conducted to Ensure Any Unacceptable Separation Distance Identified ML20153B6191988-04-29029 April 1988 Part 21 Rept Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generators Supplied to Utils.Recommends Return of Subj Components in Onsite Warehouse Storage & Suggests Surveillance of Devices Already Installed ML20151K2621988-04-14014 April 1988 Interim Deficiency & Part 21 Rept Re Control Room Essential HVAC Sys.Initially Reported on 870914.Addl Concern Noted Re Incorrect Assumption in Design Calculation.Corrective Action Beyond Calculation Review Involves Logic Mod ML20151K2371988-04-14014 April 1988 Part 21 & Deficiency Rept Re Damage to Emergency Diesel Generator Jacket Water HX During Flushing.Initially Reported on 860917.HX Repaired & Installed in Unit 2.Thermostatic Valves Being Modified ML20148R6441988-01-27027 January 1988 Part 21 & Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies Fabricated by Conax Buffalo Corp.Initially Reported on 871203.LOCA Could Cause One or More of nonsafety-related Circuits to Short Circuit ML20237E9941987-12-22022 December 1987 Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies (Epa).Initially Reported on 871203. Investigations in Progress.Final Rept Will Be Submitted by 880130 ML20236V2981987-11-19019 November 1987 Deficiency Rept Re Electrical Separation Criteria Specified in Const Spec X3AR01.Initially Reported on 870909.Second Test of Electrical Separation Requirements Very Positive. Final Rept Expected to Be Submitted Prior to 880301 ML20236K1431987-11-0202 November 1987 Interim Part 21 & Deficiency Rept Re Inductive Current Interruptive Capacity of Solid State Protection Sys Motor Driven Relay Contacts.Shunt Suppression Device Will Be Added to Solenoid ML20236J5371987-10-29029 October 1987 Part 21 & Deficiency Rept Re Solid State Protection Sys motor-driven Relay Contacts Inductive Current Interruptive Capacity.Initially Reported on 870110.Hardware Mods to Affected Circuits Planned Prior to Fuel Load ML20239A2111987-09-14014 September 1987 Part 21 & Deficiency Rept Re Design of Control Room Essential (CRE) HVAC Sys.Initially Reported on 870713. Backdraft Dampers Added to Unit 1 CRE HVAC Units & Will Be Added to Unit 2 Commensurate W/Const Schedule ML20237H7741987-08-12012 August 1987 Interim Deficiency Rept Re Emergency HVAC Sys in Control Room.Initially Reported on 870713.Engineering Evaluation in Progress to Determine Potential Impacts of Condition on Plant Safety.Final Rept Will Be Submitted by 870915 ML20216E4721987-05-28028 May 1987 Part 21 Rept 140 Re Potential Defect in Air Pressure Regulators Mfg by Bellofram.Dripwell Gasket May Fail Due to Mismachining of Gasket Seating Surface Causing Loss of Control Air & Starting Air Pressure 1999-04-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
[Table view] |
Text
. - - - _ - . - . . - . - . - . . -.
, f Georgia R:wer Cor pany
. - Waync5 born Georg a 30830 !
- 'feWhone 404 %4.'M1, Ente %on 3413 [
404 724 0114. Evernw 340 ,
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P.D. w . Georgia Power !
&a*kf;l ve scaNew:rc wm l e
October 18, 1988
{ [
I i
j U. S. Nuclear Regulatory Commission '
, ATTN: Document Control Desk File: X78G03-M144
- Washington, D. C. 20555 Log
- GN-1500 l I
Reference:
Vogtle Electric Generating Plant - Unit 2; 50-425 !
- Valves Installed Opposite to Direction of Flow I
, GPC Letter GN-1466 dated 6/29/88 In the referenced letter, Georgia Power Company notified the NRC of a potentially reportable condition involving certain Unit 2 valves <
which were inst 41ed opposite to the direction of flow. Georgia Power [
! Company has comy.w w its reportability evaluation on this subject t
- and has determined that a reportable condition as defined by the l l reporting requirements of 10 CFR Parts 21 and 50.55(e) does exist. }
- Based upon NRC guidance in NUREG-0302, Revision 1, and other NRC ;
! correspondence, Georgia Power Company is reporting this condition !
4 pursuant to the reporting requirements of 10CFR50.55(e). A sumary l j of our evaluation for Unit 2 is attached. !
4 This correspondence contains no proprietary information and may be f;
! placed in the NRC Public Document Room.
I c
) i l
1 740 P. D. Rice
- l b l l PDR/wkl l
xc: USRNC - Region II Suite 2900 l 101 Phrtetta Street, N.W. i Atlanta, GA 30323 l
- H. G. Baker D. R. Altman C. W. Hayes !
1 J. P. Kane J. A. Bailey R. W. McManus 2 R. H. Pinson G. Bocxhold, Jr. Sr. Resident (NRC)
E. D. Groover G. R. Frederick D. H. Smith (OPC)
C. T. Moore J. E. Swartzwelder J. E. Joiner (TSLA)
! R. A. Thomas A. B. Gallant NORMS j C. K. McCoy I
es10270022 891010 b
! POR ADOCK 05000425 <}(6 s PCC yg l
i
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I .
EVALUATION OF A POTENTIALLY REPORTABLE CONDITION VALVES INSTALLED OPPOSITE TO DIRECTION GF FLOW ,
f Initial Report: On June 1,1988, Mr. C. W. Hayes, the Vogtle Quality !
Assurance Manager, notified Mr. Charles Patterson of the USNRC-Region II, of a potentially reportable condition under ;
10CFR50.55(e). The potentially reportable condition concerned certain ,
Unit 2 valves installed opposite to their required orientation relative l to the direction of flow.
[
Initial Condition: Piping and Instrument Diagrams (P&ID's) show ;
the flow direction in each process ifne and check valve. The isometric drawings are the fabrication and installation drawings for the piping !
systems and provide flow arrows for system flow. Construction then ;
installs the valves with respect to the direction of flow as indicated e on the isometric drawings. l During system flushing and start-up testing three sets of three valves I were discovered to have been installed opposite to the direction j of the system fluid flow in Unit 2. During system flushing three t Dresser Industries one-inch check valves were found to b2 installed in the wrong direction. This occurred due to the vendor, Dresser Industries, shop stamping the flow arrows on the valves in the wrong i direction. This led to the installation of the valves in the direction '
opposite to the direction of system flow. Six valves were found I during start-up testing to be installed opposite to the direction of system flow. The flow arrows on the associated isometrics for I three of the valves ware not shown or were shown incorrectly. The i flow direction shown on the P&ID's was correct. The other three '
valves were Valcor solenoid valves installed in the wrong direction !
by construction. The flow direction shown on both the PAID's and :
!sometrics was correct, but a flow arrow was not shown on the valve. l Engineering Evaluation: Dresser Industries was questioned as to the cause and extent of the check valves having the flow arrows stamped !
in the wrong direction. Their response dated June 13, 1988, stated {
that the three valves were part of a four valve production order.
However, only three of the four valves were shipped to Plant Vogtle.
The fourth valve was rejected during hydrotest and was not shipped. :
These valves are Dresser type 7440W. The root cause of this flow !
arrow stamping error was determined to be a vendor mistake. Dresser j also identified other type 7440W valves supplied to Plant Vogtle.
These were evaluated for Unit 2 as part of the broadness review :
discussed later.
The root cause for three of the other valves being installed backwards was detemined to be incorrect or missing flow directions shown on i the isometric drawings. This was attributed to either an incorrect j interpretation of system flow from the P&ID onto the isometric, or i branch and miniflow lines on the isometric which did not have a flow l arrow associated with them, i i
. . l i
The root cause for the three Valcor valves being installed backwards was determined to be less than obvious flow direction indication on the valve and installers apparently unfamiliar with the flow indication given. The Valcor valves were stamped with "IN" on one end of the valve, but not with a flow arrow on the valve body as is normal practice for most other valves. It is postulated that the installers were not familiar with this type marking, did not see the inlet indication on the valves, and installed them in the same manner as globe valves (with flow under the seat). However, the valves should have been installed with flow over the seat.
Broadness Review: Tr.e Unit 2 Dresser type 7440W check valves were evaluated to detennine if the flow arrow had been stamped in the wrong direction. This evaluation involved either flow verifying the check valves or visually veri fying that the internals were installed for flow ir the same direction as the flow arrow. This review concluded that of the 59 Dresser type 7440W valves identified on Unit 2. only the three valves identified originally had the flow arrow stamped in the wrong direction.
A review was also conducted to detennine if any other safety related valves were installed opposite to the direction of system flow due to incorrect or missing flow directions on the isometric drawings.
The review consisted of:
1.0 Elimination of the following valves from further review.
1.1 Gate, ball, plug valves - Installation of these valves in either direction will not impact the flow or performance of the valve.
1.2 Check valves - Installation of check valves in the opposite direction will be detected during the system testing.
1.3 Relief valves -
Due to the configuration of relief valves, installation is not physically possible in the reversed direction.
1.4 Vendor preassemblies which include valves -
The isometric drawings are not used for installation of preassembled skids, panels, or equipment.
1.5 Vent and drain valves - The P&ID's and isometric drawings do not show process line flow direction for vent or drain valves.
The constructor installs these valves with the direction of flow away from the header.
2.0 Test connection valves - These valves were reviewed and accepted on a case-by-case basis.
3.0 Identification on the P&ID's of the remaining safety-related valves not eliminated above.
4.0 Comparison of the system and valve flow direction on the P&ID's and the installation isometric drawings for these safety-related valves.
5.0 Walkdowns to verify the actual installed conditions if the system or valve flow directions shown on the isometric drawings were missing, unclear or did not agree with the P&ID's.
6.0 Evaluation of engineering data to determine acceptability of the installed condition for the valves which were found to be installed backwards. The suppliers of valves found to be installed opposite to the direction of ficw were also contacted for information relating to the capability of these valves to perform their intended function for the life of the plant.
The results of this review concluded that a total of 29 valves were installed opposite to the direction of flow, and one valve was installed correctly, but the flow direction shown on the isometric was incorrect. The engineering evaluation of these valves concluded that 12 valves are technically acceptable as is, but the remaining 17 valves are required to be reworked and installed with the proper direction of flow.
All of the Unit 2 Valcor solenoid valves were inspected to confirm that they were installed consistent with the P&!D's. Of the Valcor solenoid valves identified on Unit 2, no others besides the three discussed above were found to be installed opposite to the direction of flow shown on the Pa!D's.
Analysis of Safety Implication: The three Dresser check valves with the incorrect flow arrow were installed in the nitrogen supply lines to steam generators #1, 2, and 3. During plant operation, the nitrogen supply lines are isolated from the steam generators by two normally closed manual globe valves downstream of the check valves. When the steam generators are not in service, the globe vsives are opened to provide nitrogen blanketing to prevent the ingress of oxygen while the steam gene . ators are in wet layup conditions. This is to protect the internals of the steam generators from corrosive attack. Thus the affected check valves would not have had an impact on plant safety during nomal operation or accident conditions. This situation is not considered reportable under 10CFR50.55(e) or 10CFR21.
Of the 29 valves installed opposite to the direction of flow due to incorrect or missing flow arrows on the isometric drawings, one has a potential for impact on plant safety. Valve 2HY-190A f a the train A Chemical and Volume Control System (CVCS) centrifugal charging pump discharge flow control valve for safety grade cold shutdown.
This solenoid-operated globe valve provides flow control of borated water from the centrifugal charging pump to the reactor coolant system during boration to cold shutdown concentration. It also controls makeup for primary system contraction due to cooling while the safety grade cold shutdown is performed. When installed backwards, valve 2HV-190A may not be capable of regulating the charging flow as required for safety grade cold shutdown. Assuming the loss of train B, this could potentially impact the capability to prevent or mitigate consequences of accidents. ;
l .
The three Valcor solenoid-operated valves identified to have been installed backwards, also have a potential impact on plant safety.
Valves 2HV-10951, 10952, and 10953 are 3/4 inch Valcor solenoid-operated globe type isolation valves for the samole lines from the safety injection system accumulators. These valves are opened from the main control room so that samples may be taken from the accumulators for checking the boric acid concentration. They are located inside containment and also serve as containment isolation valves. Each sample line goes through containment to level B of the Auxiliary Building where a locked closed valve serves as the l
other isolation valve. These globe valves fail closed on loss of power. The valve closure is achieved by a spring with the fluid t pressure assisting for a tight seal. The reversed installation may I result in valve seat leakage. This potential valve seat leakage l combined with a single failure of the other isolation valve would
( result in a small but unisolable leak into the Auxiliary Building.
l Georgia Power Company is conservatively considering the four globe valves a substantial safety hazard as defined by 10CFR21 and a significant deficiency as defined by 10CFR50.55(e) since the ability of the containment to perform its function could potentially be compromised and the capability to prevent or mitigate the consequences of accidents could potentially be impacted.
I Evaluation of a Quality Assurance Program Breakdown: The three Dresser l check valves which had an incorrect flow arrow stamped on the valve l body were found to have been from the same production order. All i other Dresser valves of the same type on Unit 2 were reviewed. No l additional valves were identified with incorrect stamping. The
! incorrect stamping was isolated to one production order and is not l considered a significant breakdown in the Dresser Industries QA program f or Vogtle.
i l The root cause for the 29 valves being installed incorrectly has l been attributed to incorrect or missing flow directions shown on l the isometric drawings. Eleven valves were installed wrong due to
! incorrect flow directions on the isometric drawings. Seventeen valves l were installed opposite to the system flow direction in situations where no flow direction was shown on either the isometric or the continuation isometric d rawing. Field engineering, craft and QC made mistakes interpreting inadequate information on some drawings as to flow direction for the valves. Considering the total valve t population of approximately 3500, we conclude that there was not I a significant breakdown of the Project Quality Assurance Program.
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Three Valcor solenoid valves were found to be installed backwards due to craf t error in determining the flow direction for thi.tse valves.
Yalcor valves are marked to indicate the inlet side of the valve instead of flow direction arrows stamped on the valve body. Three Yalcor valves were installed backwards, all other Valcor valves were found acceptable. This is not considered to be a significant breakdown of the Project Qaality Assurance Program.
Conclusion:
It has been concluded that installation of the four globe valves discussed above opposite to the direction of flow could potentially have adversely affected the safety of operations.
Therefore, this condition is considered to be reportable under the requirements 10CFR50.55(e) and 10CFR21. Based on guidance in NUREG-0302, Revision 1, concerning duplicate reporting of an event, Georgia Power Company is reporting this condition per the criteria of 10CFR50.55(e).
Corrective Action: The three Dresser Industries one-inch check valves have been reworked so that the flow arrow and valve internals are consistent with the system flow.
The seventeen valves which were installed backwards due to the isometric drawings and were not acceptable, have also been reworked so they are installed with the system flow. The isometric drawings associated with these valves were revised to clearly reflect the correct flow direction.
The three Valcor solenoid valves which were installed backwards have also been reworked so that they are now installed correctly.
Those invol"ed with the incorrect installations will be advised of these conditions and instructed on how to prevent recurrence. This item is being tracked by MTS No. EA! B-5115 and is scheduled to be completed 10/30/88