ML20236P699
| ML20236P699 | |
| Person / Time | |
|---|---|
| Site: | Vogtle |
| Issue date: | 06/30/1998 |
| From: | Hargis T, Woodard J SOUTHERN NUCLEAR OPERATING CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| LCV-1169-F, NUDOCS 9807170107 | |
| Download: ML20236P699 (7) | |
Text
-.
- s ;-
.g J.D.Woodard Southern Nuclear u
Executive Vice President Operating Company. Inc.
40 inverness Center Parkway Post Office Box 1295 Birrningham. Alabama 35201 Tel 205.992.5086 SOUTHERN L COMPANY Enery to Serve hur%rld" July 13, 1998 LCV-1169-F Docket Nos.
50-424 50-425 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
VOGTLE ELECTRIC GENERATING PLANT MONT11LY OPERATING REPORT - JUNE 1998 Enclosed are the June 1998, monthly operating reports for Vogtle Electric Generating Plant (VEGP) Units 1 and 2. These reports are submitted in accordance with the Technical Specification 5.6.4.
Sincerely, s
. D.
oodard JDW/JLL Enclosures El-VEGP Unit i Monthly Operating Report - June 1998 E2-VEGP Unit 2 Monthly Operating Report - June 1998
. cc:
Southern Nuclear Onerating Comnany Mr. J. B. Beasley, Jr.
Mr. M. Sheibani SNC Document Management U. S. Nuclear Regulatory Commission ch Mr. L. A. Reyes, Regional Administrator j
Mr. D. Jaffe, Senior Project Manager, NRR Mr. J. Zeiler, Senior Resident Inspector, Vogtle l
9807170107 980630 PDR ADOCK 05000424>
I.
R PDR,
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ENCLOSURE 1 VOGTLE ELECTRIC GENERATING PLANT - UNIT 1 MONTiiLY OPERATING REPORT FOR JUNE 1998 TABLE OF CONTENTS OPERATING DATA REPORT and CIIALLENGES to PORV and SAFETY VALVES Page El-1 UNIT SliUTDOWNS and NARRATIVE REPORT Page El-2 l'
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OPERATING DATA REPORT Docket No.:
50-424 i
Unit Narne:
VEGP UNIT 1 Date:
July 1,1998 Completed By:
T.S. Hargis Telephone:
.(7_06] 826-3469 Operating Etatus
- 1. Reporting Period:
Jun-98
- 2. Design Electrical Rating (Net MWe):
1169]
- 3. Maximum Dependable Capacity (Net MWe):
1162 This Month Year _To Date Cumulative
- 4. Number Of Hours Reactor Was Critical:
720.0 4343.0 85,315.0
- 5. Hours Generator On Line:
720.0 4321.5 83,996.3_
- 6. Unit Reserve Shutdown Hours:
0.0 0.0 0.0 7, Net Electrical Energy Generated (MWHe):
832,522 5,056,976 92,519,288 CHALLENGES TO PRESSURIZER PORV AND PRESSURIZER SAFETY VALVES Date Tag No.
Event Description N/A N/A N/A E1-1
ilNIT SHUTDOWNS DockGt No..
50-424
~-
Unit NCme:
5/EGP UNIT 1
~
Date:
July 1,1998 Completed By:
_T.S. Hargis__
Telephone:
(706[826-3469 Reporting Period:
Jun-98 Type
' Method of F: Forced Duration Shutting Cause/ Corrective Actions No.
Date
- s. wm (Hours)
Reason (1).Down (2)
Comments i
N/A N/A N/A N/A N/A N/A N/A j
(1) REASON:
(2) METHOD:
A - Equipment Failure (Explain) E - Operator Training /Ucense Examination
- 1. Manual
- 4. Continuation B - Maintenance or Test F - Administrative
- 2. Manual Tnp/ Scram 5 Other C Refueling G - Operatonal Error (Explain)
- 3. Automate Tnp/ Scram D - Regulatory Restncton H - Other (Explain)
CAUSE/ CORRECTIVE ACTION / COMMENTS:
CAUSE:
CORRECTIVEACTION:
l NARRATIVE REPORT 1
June 01,1998 00:00 Unit 1 at 100% power with no operating problems.
June 30,1998 23:59 Unit 1 at 100% power with no operating problems.
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s ENCLOSURE 2 VOGTLE ELECTRIC GENERATING PLANT - UNIT 2 MONTliLY OPERATING REPORT FOR JUNE 1998 TABLE OF CONTENTS OPERATING DATA REPORT and CilALLENGES to PORV and SAFETY VALVES Page E2-1 UNIT SHUTDOWNS and NARRATIVE REPORT Page E2-2 l
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L____________________________-._______.___________________
j c.
' OPERATING DATA REPORT I
Docket No.:
_50-425___ _
Unit Name:
VEGP UNIT 2 t
Date:
Ju:/1,1998 Comp!eted By:
T.S. Hargis Telephone:
(706) 826-3469 Operating Status
- 1. Reporting Period:
Jun-98
- 2. Design Electrical Rating (Net MWe):
1169_
- 3. Maximum Dependable Capacity (Net MWe):
1167 This Month Year _To Date Cumulative
- 4. Number Of Hours Reactor Was Critical:
597.1 3054.8 71,878.6
- 5. Hours Generator On Line:
580.7 30081 71,167.7
- 6. Unit Reserve Shutdown Hours:
0.0 0.0 0.0
- 7. Net Electrical Energy Generated (MWHe):
647,083 3,351,747 78,938,473 CHALLENGES TO PRESSURIZER PORV AND PRESSURIZER SAFETY VALVES Date Tag No.
Event Description June 09,1998-2PV0455A PORV cycled 6 times during transient to maintain RCS pressure.
See Event 98-5 June,1998 NRC Monthly Operating Report.
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tJNIT SHUTDOWNS Dock".t No.:
50-425 Unit NIme:
VEGP UNIT 2
~
~
Date:
~Juld1998 Completed By:
T.S. Hargis, _
Telephone:
Q06)_826-3469 Rerorting Period:
Jun-98 l Type
- Method of lCause/ Corrective Actions F
- Forced Duration
' Shutting No.
Date s: scheduw (Hours)_ Reason (1)
Down (2)
Comments 4
98-5 06/09/98 F
139.3 A
3 SEE BELOW (1) REASON:
(2) METHOD:
A Equipment Failure (Explain) E - Operator Training /Ucense Examinahon
- 1. Manual
- 4. Conhnuation B Maintenance or Test F - Administrate've
- 2. Manualinp/ Scram
- 5. Other C - Refuehng G - Opershonal Error (Explain)
- 3. AutomaticTnp/ scram D - Regulatory Restnction H - Other (Explain) j CAUSE/ CORRECTIVE ACTION / COMMENTS:
EVENT _98:5 CAUSE:
An equipment fault caused the loss of all Non-1E 13.8 switchgear due to incorrect tap settings for the instantaneous overcurrent relay for breaker 2 NAB 03. This caused a Turbine Trip / Reactor trip when the main generator output breakers opened.
I CORRECTIVEACTJON: Reworked the incorrect tap betting on the overcurrent relay. Performed a broadness review of protective relays, bus transfer scheme and other relay settings. Repaired the turbine bearing (discovery item after trip).
CRITICALPATH WAS:
Disassembly and reassembly of turbine bearing U.
NARRATIVE REPORT June 01,1998 00:00 Unit 2 at 100% power with no operating problems.
June 09,1998 08:58 Unit 2 Reactor Trip / Turbine Trip June 09,1998 09:00 Unit 2 Safety injected due to pressurizer low pressure. Entered Mode 3.
June 10,1998 09:36 Unit 2 Entered Mode 4.
June 11,1998 00:38 Unit 2 Entered Mode 3.
June 14,199810:46 Unit 2 Entered Mode 2.
June 14,199811:51 Unit 2 Reactor Critical.
June 14,1998 23:58 Unit 2 Entered Mode 1.
June 15,1998 04:15 Unit 2 Generator tied to grid.
June 16,199818:48 Unit 2 Retumed to 100% Power.
June 30,1998 23:59 Unit 2 at 100% power with no operating problems.
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