Part 21 & Deficiency Rept Re ESF Filtration Unit Bolts. Initially Reported on 880628.Contractor Conducted Training Session for Personnel to Stress Importance of Clarifying Incomplete Drawing Info & Requirements of Bolting ProcedureML20153E227 |
Person / Time |
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Site: |
Vogtle ![Southern Nuclear icon.png](/w/images/1/14/Southern_Nuclear_icon.png) |
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Issue date: |
09/01/1988 |
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From: |
Rice P GEORGIA POWER CO. |
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To: |
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
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References |
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REF-PT21-88, REF-PT21-88-100-000 GN-1481, PT21-88-100, PT21-88-100-000, NUDOCS 8809060253 |
Download: ML20153E227 (5) |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML17309A6211997-09-29029 September 1997 Part 21 Rept Re Final Disposition of Masterflow 713 & Embeco 636 Grout Nonconformance Reported by Master Builders,Inc. Licensee Continuing to Monitor shelf-life of Masterflow 713 & Embeco 636 Grouts Produced at Rancho Cucamonga ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML20134H3361996-11-0505 November 1996 Part 21 Rept Re Defective Inner Thrust Bearing 1801461-01 Used in PSA 35 Mechanical Shock Arrestor Used as Restraint on Piping Sys for Nuclear Generating Plant.Lot of Defective Parts Located & Isolated to Three Customers ML20115D2001996-07-0909 July 1996 Part 21 Rept Re Mfg Defect of Enterprise DSR-4 & DSRV-4 Edgs,Originally Mfg by Calcon Corp.Amot Control Corp Purchased Calcon Product Line & Maintains Design & Production.Valves Returned to Cooper Energy Svcs on 960131 ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20127D1491992-09-0404 September 1992 Part 21 Rept Re Defect in Component of DSRV-16-4 Enterprise Standby DG Sys Jacket Water Pump Shaft.Caused by Incorrect Tapers Machined on Shaft Due to Vendor Mismatching.All Affected Shafts Recalled & Quality Insp Plans Changed ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20087D3191992-01-14014 January 1992 Potential Part 21 Rept Re Problems W/Elmwood/Fasco Contactor Carriers Breaking in Contactor Model 30-FO-30. Caused by Distortion/Shrinkage of Molded Phenolic Contactor Carrier.Replacement Contactors Installed ML17223A5941990-03-0909 March 1990 Errata to 900126 Part 21 Rept Re Anchor/Darling Actuators Incorporating Use of Teldyne-Republic four-way Valves.Lists Plants Inadvertently Left Out in Original Rept ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20248E0121989-09-13013 September 1989 Supplemental Part 21 Rept Re Potential Problem W/Six Specific Engine Control Devices in Air Start,Lube Oil, Jacket Water & Crankcase Sys.Initially Reported on 890429. California Controls Co Will Redesign Valve Seating ML20246K7401989-04-26026 April 1989 Part 21 Rept Re Incorrectly Stamped Name Plates on Certain Asco Nuclear Qualified Valves.Vendor Will Contact Each Affected Facility & Furnish Correctly Stamped Plates & in Near Future Discontinue Sale of Rebuild Kits for Valves ML20247P7991989-04-0404 April 1989 Part 21 Rept Re Atmospheric Dump Valves.Cause of Failure Speculative But Result of Piston Ring That Failed to Seal. Resolution to Problem Requires Increasing Pilot Valve Capacity & Reworking of Plug to Enlarge Pilot Flow Area ML20206M4401988-11-21021 November 1988 Deficiency Rept Re Misapplication of Raychem Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880920.Investigation Is in Process.Final Rept Will Be Submitted by 881222 ML20205C9291988-10-18018 October 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow,Per 10CFR21 & 50.55 Requirements.Item Being Tracked by MTS EAI B-5115 & Scheduled for Completion 881030 ML20205D6651988-10-18018 October 1988 Part 21 & Deficiency Rept Re Penetration Seals Found Not to Be Watertight.Initially Reported on 880609.Water Leakage Tests Performed on Unit Upper Cable Spreading Room Seals. All Floor Penetration Seal Assemblies Repaired ML20207P0451988-10-0505 October 1988 Part 21 Rept 146 Re Defect in Left Intercooler Inlet Adapter on Standby Diesel Engine Generator.Recommends Utils Inspect Left Intake Manifold Drain as Part of Operating Plan.Addl Info Expected by 881015 ML20155D6471988-09-28028 September 1988 Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880629.Final Rept Delayed Until 881020 ML20207J7361988-09-20020 September 1988 Interim Deficiency Rept Re Misapplication of Vendor Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880601.Final Rept Expected Prior to 881123 ML20153E2271988-09-0101 September 1988 Part 21 & Deficiency Rept Re ESF Filtration Unit Bolts. Initially Reported on 880628.Contractor Conducted Training Session for Personnel to Stress Importance of Clarifying Incomplete Drawing Info & Requirements of Bolting Procedure ML20151V1901988-08-16016 August 1988 Deficiency Rept Re non-water Tight Penetration Seals.Test Rig Constructed to Simulate Typical Upper Cable Spreading Room Configuration & Sealants Verified to Provide Waterproof Seal.Next Rept Will Be Submitted by 881020 ML20196L4811988-07-0707 July 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880601.Investigation in Progress to Determine Full Scope of Condition.Final Rept Will Be Submitted by 881001 ML20151A7781988-07-0606 July 1988 Deficiency Rept Re nonwater-tight Penetration Seals. Initially Reported on 880609.Investigation Incomplete.Next Rept Expected by 880818 ML20196C2971988-06-28028 June 1988 Deficiency Rept Re ESF Filtration Bolts.Initially Reported on 880601.Investigation of Root Cause of Condition Ongoing. Final Rept Will Be Submitted by 880901 ML20195D8541988-06-16016 June 1988 Part 21 Rept Re Potentially Reportable Condition Associated W/Dresser Model 7440W Check Valves Supplied W/Flow Direction Arrow Stamped Opposite to Valve Flow.Investigation Being Conducted.Evaluation of Bechtel Western Power Co Ltr Encl ML20154J4101988-05-12012 May 1988 Addendum 1 to Supplemental Part 21 Rept 145 Re Potential Problem w/F-573-156 Pressure Sensor/Lube Oil Trip.Initially Reported on 880429.Addl 1-1/8-inch Diameter W/Deep Counterbone in Pressure Head Added to Activate Valve ML20154A6841988-05-10010 May 1988 Deficiency Rept Re Electrical Cable Tray Separation. Initially Reported on 880414.Walkdown of All safety-related Cable Trays Conducted to Ensure Any Unacceptable Separation Distance Identified ML20153B6191988-04-29029 April 1988 Part 21 Rept Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generators Supplied to Utils.Recommends Return of Subj Components in Onsite Warehouse Storage & Suggests Surveillance of Devices Already Installed ML20151K2621988-04-14014 April 1988 Interim Deficiency & Part 21 Rept Re Control Room Essential HVAC Sys.Initially Reported on 870914.Addl Concern Noted Re Incorrect Assumption in Design Calculation.Corrective Action Beyond Calculation Review Involves Logic Mod ML20151K2371988-04-14014 April 1988 Part 21 & Deficiency Rept Re Damage to Emergency Diesel Generator Jacket Water HX During Flushing.Initially Reported on 860917.HX Repaired & Installed in Unit 2.Thermostatic Valves Being Modified ML20148R6441988-01-27027 January 1988 Part 21 & Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies Fabricated by Conax Buffalo Corp.Initially Reported on 871203.LOCA Could Cause One or More of nonsafety-related Circuits to Short Circuit ML20237E9941987-12-22022 December 1987 Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies (Epa).Initially Reported on 871203. Investigations in Progress.Final Rept Will Be Submitted by 880130 ML20236V2981987-11-19019 November 1987 Deficiency Rept Re Electrical Separation Criteria Specified in Const Spec X3AR01.Initially Reported on 870909.Second Test of Electrical Separation Requirements Very Positive. Final Rept Expected to Be Submitted Prior to 880301 ML20236K1431987-11-0202 November 1987 Interim Part 21 & Deficiency Rept Re Inductive Current Interruptive Capacity of Solid State Protection Sys Motor Driven Relay Contacts.Shunt Suppression Device Will Be Added to Solenoid ML20236J5371987-10-29029 October 1987 Part 21 & Deficiency Rept Re Solid State Protection Sys motor-driven Relay Contacts Inductive Current Interruptive Capacity.Initially Reported on 870110.Hardware Mods to Affected Circuits Planned Prior to Fuel Load ML20239A2111987-09-14014 September 1987 Part 21 & Deficiency Rept Re Design of Control Room Essential (CRE) HVAC Sys.Initially Reported on 870713. Backdraft Dampers Added to Unit 1 CRE HVAC Units & Will Be Added to Unit 2 Commensurate W/Const Schedule ML20237H7741987-08-12012 August 1987 Interim Deficiency Rept Re Emergency HVAC Sys in Control Room.Initially Reported on 870713.Engineering Evaluation in Progress to Determine Potential Impacts of Condition on Plant Safety.Final Rept Will Be Submitted by 870915 ML20216E4721987-05-28028 May 1987 Part 21 Rept 140 Re Potential Defect in Air Pressure Regulators Mfg by Bellofram.Dripwell Gasket May Fail Due to Mismachining of Gasket Seating Surface Causing Loss of Control Air & Starting Air Pressure 1999-04-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
[Table view] |
Text
e y.
Gecgia Fbwer Cc+ncany Fbst Office Box 282
, Telephone 04 554 9961. Estension 3413 404 724 8114, Extension 3413 ,
b Of,p,c6, Georgia Power Vogtle Project ce m> ten sta: 5,wm September 1, 1988 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk File: X7BG03-M143 Washington, D. C. 20555 Log: GN-1481
Reference:
Vogtle Electric Generating Plant - Unit 2; 50-425 ESF Filtration Unit Bolts GPC Letter GN-1465 dated 6/28/88 In the referenced letter, Georgia Power Company notified the NRC of a poten-tially reportable condition involving the engineered safety feature filtra-tion unit bolts. Georgia Power Company has completed its reportability evaluation and has determined that a reportable condition as defined by the reporting requirements of 10CFR Parts 21 and 50.55(e) does exist.
Based upon NRC guidance in NUREG-0302, Revision 1, and other NRC correspon-dence, Georgia Power Company is reporting this condit!on pursuant to the reporting requirements of 10CFR50.55(e). A summary of our evaluation for Unit 2 is attached.
This correspondence contains no proprietary information and may be placed in the NRC Public Document Room.
O P. D. Rice PDR/sem xc: USNRC - Region II Suite 2900 101 liarietta Street, N. W.
Atlanta, GA 30323 H. G. Baker D. R. Altman C. W. Hayes J. P. Kane J. A. Bailey R. W. McManus R. H. Pinson G. Bockhold, Jr. Sr. Resident (NRC)
E. D. Groover G. R. Frederick D. H. Smith (OPC)
C. T. Moore J. E. Swartzwelder J. E. Joiner (TSLA)
R. A. Thomas A. 8. Gallant NORMS 8G09060253 800901 PDR ADOCK 05000423 S FDC 1,
EVALUATION OF A POTENTIALLY REPORTABLE CONDITION ESF FILTRATION UNIT BOLTS Initial Report: On June 1, 1988, Mr. C. W. Hayes, the Vogtle Quality Assurance Manager, notified Mr. Charles Patterson of the USNRC - Region II, of a potentially reportable condition under 10CFR50.55(e). The potentially reportable condition concerned certain engineered safety features (ESF) air filtration unit foundation bolts.
Background Information: There are four ESF air filtration units in the current Unit 2 design. Two redundant ESF filtration units are provided for the control room and two for the piping penetration area. The electrical penetration area filtration system has been deleted from the Unit 2 ' design and the filtration units are abandoned in place; as such, they are not addressed in this evaluation. Each filtration unit consists of a steel housing containing the following sections in series: (a)moistureseparator, (b) electric heater, (c) upstream HEPA, (d) charcoal adsorber, (e) downstream HEPA, (f) cooling coil (a coolin is part of this assembly only for the control room units.), and (g) fan. g coilThe ESF filtration units are designed to Seismic Category 1 requirements, and are energized upon receipt of an emergency signal to recirculate the air and remove potential airborne radioactivity. All filtration units are activated upon receipt of a safety injection signal; only the control room units are activated upon receipt of a control room isolation signal. The filtration units also provide the required differential pressure to minimize unfiltered leakage into the control room or out of the piping penetration area.
The filtration units are attached to the foundation via a "C" channel on the base of the unit bolted to 4" clip angles anchored to the concrete.
The holes in the clip angles are slotted to accommodate field adjustment.
While investigating an NRC unresolved item on the foundation installation, several other concerns were noted that appeared to violate installation procedures. The high strength bolts utilized for the "C" channel to clip angle connection were not pretensioned. As a result. NRC violation 50-425/88-20-01: "Failure to Install HVAC Systems In Accordance with the FSAR" was issued. Three other discrepancier 50ted in the violation are: l (1) the bolted contact surfaces were not fra M defects, (2) washers were l not installed under the bolt heads over the uotted holes, and (3) one 5/8-inch diameter bolt was used when a 3/4-inch diameter bolt was required.
Communication with the vendor, American Air Filter (AAF), to resolve the initial concern revealed that the installed condition did not meet their criteria for seismic qualification.
These discrepancies are based on comparisons with procedure JP-513 "Installation and Inspection of High Strength Bolts." which is the procedure used by the HVAC contractor, P/XF, for the installation of high strength bolts.
(1)
r
. Engineering Evaluation: This foundation design was supplied by AAF along with the connection hardware to be used. However, the connection hardware was evidently lost while in storage. The parts list on the vendor drawing for the control room filtration unit fan assembly defined each set of the
- bolting hardware for the control room filtration unit fan assembly as -a bolt, nut, and plated washer. A parts list was not provided for the filtration unit, but the detail is similar. The vendor drawings did not specify a material or torque value for the bolting hardware. The drawings do show a slotted hole in the clip angle, but do not show an oversized
, washer or a lock washer for the connection. Since the drawing; do not i specify either a bolt material or a torque requirement, it was assumed ;
i that standard bolting material was to be used, in Unit 2, high strength :
bolts were chosen. The torque value was specified to be snug tight. This is an acceptable substitute for standard bolting per procedure JP-513, ;
] except that per JP-513, a lock washer should have been installed to prevent ,
the nut from loosening, and an oversized washer should also have been 4
installed under the bolt head since there is a slotted hole in the clip i angle. Procedure JP-513 also requires full contact between the bearing serfaces. However, the requirements for extra 'sashers and full bearing surface contact of procedure JP-513 were not followed since this was a vendor designed connection.
While investigating the NRC unresolved item on the lack of full contact
, between the bearing surfaces, AAF stated in their April 1,1988 letter:
"To meet the seismic qualification, the angle clips should be -
i bolted to the base channels with type A-449 high strength bolts, or equivalent, pretensioned to meet the friction connection requirement. Full contact of the two surfaces is not necessary as the friction force is a function of the friction coefficient and the pressure applied (tension of the bolts in this case)
- is independent of the contact area. (Example reference
- 0.W. ;
l Eshbach's Handbook of Engineering Fundamentals)." -
j Thus, full contact of the bearing surfaces is not required for this connection, but high strength bolts pretensioned to meet the friction connection requirement are required. The bol ts were not pretensioned because the AAF drawing did not specify this as a high strength connection and no torque values were given.
Because the vendor drawings did not specify a bolting material or torque requirement, it was mistakenly assumed that standard bolting material was originally supplied. However, high strength bolts were substituted j as allowed by site procedures JP-14.2 and JP-513. No lock washers or oversized washers were installed because the vendor drawings did not show
- the requirements. Plated flat washers were installed on the nut side, t
Therefore, the installed condition was consistent with the parts list and drawing supplied by the vendor, with the exception of the one undersized bolt. On completion of the installation QC also used the vendor drawings as the verification documents for inspection and acceptance. The use i of the one undersized bolt is considered to be of minor significance in
- relation to the total population of over 100 bolts. ;
j (2) i
Since high strength bolts were installed without a lockwasher or without being pretensioned, the nut may eventually loosen and potentially back off. Therefore, the integrity of the as-found connection cannot be assured for the life of the plant. If the connection were to relax or loosen from snug tight, as they were installed, the connection could potentially fail during a seismic event.
The root causes for this condition were determined to be incomplete vendor design information and a judgement mistake by the installation contractor for hardware replacement. The existing procedures require modification to a design to be reviewed and approved by the design agency. Therefore, when the supplied hardware was replaced, and the vendor information was unclear, the vendor should have been contacted for their review and approval per the existing site procedures for field change requests (FCR) and field equipment change orders (FECO).
Broadness Review: Normally, bolted connections installed by P/KF, the installation contractor for HVAC, without specific vendor design are in accordance with procedure JP-14.2 for standard bolts, or JP-513 for high strength bolts. These procedures require either lock washers or torquing which will prevent loosening of the bolted connection. All other equipment within P/KF scope was reviewed. This deficiency occurred in equipment for which P/KF was responsible fcr field engineering, installation and QC inspection; and for which the bolting design and hardware were supplied by the vendor to be installed in the field. Only the ESF filtration units discussed above and the supply fans for the control room ESF filtration system fit into this category. There are two supply fans for the control room EST filtration system. Their foundation detail, also designed by AAF, is similar to the filtration system. Type A-307 standard bolts with lock warhers were found to be installod. A calculation was performed based on the installed condition which indicated that the A-307 bolts would have met the seismic design. Therefore, this is considered to be a unique situation which does not affect any other installation.
Analysis, of Safety implication: Whether the high strength bolts will ,
actually relax cnd loosen during the life of the plant cannot be determined l since the connection was not properly torqued, nor was a locking device i installed. Should this connection become disengaged, the filtration units may move away from the foundation, thereby possibly separating the {
filtration units from the ductwork, and rendering them inoperable. In the case of a potential accident involving a release of radiation, this condition may cause a loss of pressurization of the control room and an increase in radiation exposure to the operators. An analysis to determine the dose to the operators that could result from failure of the control room ESF filtration system, or the increase in radioactive release due to a failure of the piping penetration area filtration unit has not been performed for this condition. A loss of these ESF filtration systems j could potentially result in a substantial safety haza rd as defined by 10CFR21 and a significant deficiency relating to the construction of a system as defined by 10CFR50.55(e).
Therefore, Georgia Power Company I has concluded that this condition is reportable for Vogtle Unit 2 under i 10CFR50.55(e) and 10CFR21.
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Evaluation of a Quality Assurance Program Breakdown: The ESF filtration units were installed and QC inspected per the requirements of an approved mechanical installation package (MIP) and the vendor drawings. The original hardware supplied by the vendor was lost. In replacing the lost hardware, i it was mistakenly assumed that standard hardware was originally si pplied since the vendor drawings and parts list did not give any other requirements. High strength bolts were substituted an6 installed at a snug tight condition. This is a normally acceptable substitution and was not construed as a design modification. Therefore an FCR or FEC0 was not written. In retrospect, the vendor drawings were not as clear '
as they needed to be and the vendor should have been consulted before replacement bolts were specified. We believe this indicates a mistake in judgement by P/KF field engineering and not a significant breakdown of the quality program.
Conclusion:
It has been concluded that the long term seismic qualification of these ESF filtration units was not assured since the untorqued, high 1 strength bolts may loosen over the life of the plant. An analysis to
, determine the consequences of these loose bolts has not been performed.
- but conservitively assuming the ESF filtration units come off their !
foundations and separate from the ductwork results in a situation outside t of the design bases of the plant. This could cause the operators to receive a higher radiation dose during a potential accident, as well as a higher off-site release from the piping penetration area. Therefore, this condition is considered to be reportable under the requirements of 10CFR50.55(e) and 10CFR21. Based on guidance in NUREG-0302, Revision 1, concerning duplicate reporting of an event, Georgia Power Company is "
reporting this condition per the criteria of 10CFR50.55(e). '
Corrective Action: Two deviation reports were generated to replace the existing bolting hardware between the clip angles and the "C" channels I under the filtration unit housings (Deviation Report's PK-4208 and PK-4211).
High strength bolts and oversized washers were installed, torqued to the requirements of AISC slotted hole configuration, including replacement ;
of the undersized bolt. This work has been completed. 1 Another Deviation Report (CD-9372) was written for the control room ESF filtration system supply fans (also supplied by AAF) which have a similar !
- foundation design. Type A-307 standard bol ts and lockwashers were originally installed in accordance with procedure JP-14.2. A calculation was performed based on the installed condition which indicated that the ;
A-307 bolts would have met the seismic design. However, all of the '
accessible bolts (12 out of 20 per fan) were replaced with high strength l
! bolts and oversized washers, torqued to the requirements of AISC. This )
work has also been completed.
To prevent future occurrence of this mistake, the contractor (P/KF) has conducted a training session for personnel associated with equipment installation to stress the importance of clarifying possible incomplete drawing infonnation and the requirerents of the bolting procedures. Also, MFCRB-18601 has been issued to add the material specification, oversized washers and torque requirement to the appropriate AAF drawings.
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