ML20151H037

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Insp Repts 50-338/88-06 & 50-339/88-06 on 880328-0401 & 0411-15.Weaknesses Noted.Major Areas Inspected:Current Level of Performance in Areas of Plant Operations,Including Operations,Maint,Qa & Engineering & Training
ML20151H037
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 06/17/1988
From: Shymlock M, Linda Watson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20151H025 List:
References
50-338-88-06, 50-338-88-6, 50-339-88-06, 50-339-88-6, GL-82-02, GL-82-12, GL-82-2, NUDOCS 8808010116
Download: ML20151H037 (44)


See also: IR 05000338/1988006

Text

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S 880g UNITED STATES

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  • , NUCLE AR REGULATORY COMMISSION

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101 MAR 4ETTA STREET. N.W.

7 g ATLANT A.GEORot A 30323

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Report Nos.: 50-338/88-06 and 50-339/88-06

Licensee: Virginia Electric and Pcwer Company

Richmond, VA 23261

Docket Nos.: 50-338 and 50-339 License Nos.: NPF-4 and NPF-7

Facility Name: North Anna 1 and 2

Inspection Conducted: March 28 - April 1 and April 11-15, 1988

Team Leader: MAdv@ [ddn~ 0!/6'[8A

L. Watso t/ Date' Sig/ied

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Team Members: B. Breslau

R. Brewer

R. Croteau

T. O'Connor

R. Schin

M. Scott

M. Shannen

[ INM

Approved by:h. Shymiock, Cfief

/ DM

Dat'e Signed

Operational programs Section

Division of Reactor Safety

1

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l SUMMARY

Scope: This was a special announced Ooerational Performance Assessme.t (OPA).

The OPA evaluated the licensee's current level of performance in the area of

plant operations. The inspection included an evaluation of the effectiveness

of various plant groups including Operations, Maintenance, Quality Assurarce,

Engineering and Training, in supporting safe plant operations. Plant

management awareness of, involvement in, and support of safe plant operetion

was also evaluated.

The inspection was divided into three major areas including Operations.

Maintenance Support of Operations, and Management Controls. Emphasis was

placed on numerous interviews of personnel at all levels, observation of plant

activities and meetings, extended control room observations, and plant and

system walkdowns. The inspectors also reviewed plant deviation reports and

licensee event reports (LERs) for the current Systematic Assessment of Licensee

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Performance (SALP) evaluation period, and evaluated the effectiveness of the

licensee's root cause identification; short term and programmatic corrective

actions; and, repetitive failure trending and related corrective actions.

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i A review of past NRC inspections and reportable events indicated a troubled

performance history at North Anna, Weaknesses had been identified in the

inservice inspection program, environmental qualification of equipment,  ;

i procedural adherence, post maintenance testing, and procedure adequacy. .

j Several of these issues involved potential escalated enforcement actions, t

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l During this inspection, the NRC discussed the performance history with plant [

} and corporate management. The licensee's responses to these discussions and ,

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the results of the OPA indicate that weak areas had been identified by

I management and that significant actions had been taken to correct problems in ,

these areas, }

Long-term actions included the establishment of a Quality Maintenance Team l

concept; a substantial procedure rewrite effort; establishment of a Human >

Performance Evaluation System to systematically review personnel errors and

take appropriate programmatic corrective actions; Employee Involvement Teams; ,

and, analyses of the structure of site and corporate organizations including  !

i redefining and reassigning responsibilities to enhance operational performance. l

! More recent efforts included additional emphasis on employee awareness of the [

need to follow procedure; an increased emphasis on individual ownership and  !

responsibility for quality work; additional guidance on post maintenance i
testing and plans to provide further post maintenance test guidance upgrades; j

l reduction of equipment deficiencies; and new trending programs to evaluate  :

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similar deficiencies and identify programmatic weaknesses. The licensee has  !

l also added an onsite systems engineering group and plans additions to the

i maintenance planning staff.  !

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In general, the licensee's programs in the areas inspected were found to be l

adequate with a number of particularly strong features. Management appears to  !

be taking the appropriate actions to achieve improved performance. Weaknesses t

j were identifiec', in some programs as indicated below, The licensee committed to (

j evaluate these areas and take appropriate actions to enhance performance in  !

these areas, Strengths and weaknesses are summarized below: i

i Strengths ,

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! In the area of Operations, strengths included:

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Control room operators were professional, att.entive, and knowledgeable, ,

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Maintenance coordination and tagging control were conducted outside the l

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, control room which greatly contributed to reduced noise levels and traffic i

flow in the control room,

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Equipment operator rounds consisted of a quantitative tour and a second I

qualitative tour,

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Operations managers were aware of plant conditions, conducted frequent l'

) control room visits and plant tours and were actively involved in

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day-to-day activities.

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A number of Operations managers held Senior Reactor Operator (SRO)

licenses and had an extensive amount of North Anna control room operating

experience.

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Housekeeping plant wide was very good.

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Unit labels, color coding of unit procedures, and the new equipment

identification program were good.

The following strengths were identified in the area of Maintenance Support of

Operations:

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The scheduling and coordination of work activities between Operations and

l Maintenance appeared to be effective.

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The Quality Maintenance Team (QMT) program appeared to be a good approach

l toward higher quality maintenance. Maintenance personnel felt the QMT

l program had increased work quality (but wore uncomfortable performing

l their own Health Physics duties).

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Direct supervision at the job site and and communications between

technicians and foremen appeared to be good.

Strengths in the area of Management Controls included:

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The Inspector of the Day program provided quality control review of daily

activities.

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Effective and terse management meetings were conducted to evaluate issues.

Also, active management involvement in daily activities was observed.

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Managers had supervisors accompany them on tours and took immediate action

to correct undesirable conditions.

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Upper management conducted off-hour tours.

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An Employee Involvement Team Program appeared to be effectively involving

employees in resolution of plant problems.

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Performance evaluations were conducted on QMT inspectors every six months.

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Human Performance Evaluation System (HPES) reports on personnel error

events and corrective actions appeared to be thorough, timely and

effective.

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Responsible individuals and supervisors were present to present their

items to the Station Nuclear Safety and Operating Committee (SNSOC).

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Weaknesses -

Weaknesses in Operations included:

- Some control room instruments, such as instruments for normal cooldown

using the Residual Heat Removal System, were not in a periodic calibration

program.

- Shift turnovers for Shift Supervisors lacked a formalized checklist,

allowing for the possibility of incomplete transfer of plant status.

- Shift turnovers for Assistant Shift Supervisors were incomplete due to the

failure to review the opposite unit's Assistant Shift Supervisor narrative

log book, or Technical Specification action item log.

Weaknesses in Maintenance Support of Operations included:

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There was a backlog of approximately 7800 completed but not closed work

orders. The backlog was affecting the maintenance history files used by

the planners and the equipment history used for trending of repetitive

failures.

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The staffing for mechanical planners appeared to be inadequate to process

approximately 600 work orders per month and to close out the backlog of

completed work orders.

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Interviews with mechanical foremen and mechanics indicated that work

orders issued by Planning were sometimes incomplete.

Weaknesses in the Management Controls area included:

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The Temporary Changes / Procedure Deviations procedure contained weaknesses

in the generation, review, and control of procedure changes. A large

backlog of needed procedure changes existed due to weak procedure change

processing methods.

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The QNT program had not been assessed by QA since implementation.

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Trending of deficiency reports and work orders were not performed and root

cause analyses of equipment deficiencies were not performed in some cases.

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REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • M. Bowling, Assistant Station Manager
  • D. Cruden, Vice President, Nuclear Operations

"R. Driscoll, QA Manager, North Anna

  • L. Edmonds, Superintendent, Nuclear Training

"R. Enfinger, Assistant Station Manager

  • N. Hardwick, Manager, Nuclear Programs and Licensing
  • D. Heacock, Superintendent, Technical Services
'G. Kane, Station Manager

"M. Kansler, Superintendent, Maintenance

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  • R. Harowick, Corporate Manager, Quality Assurance
  • A. Stafford, Superintendent, Health Physics

"J. Stall, Superintendent, Operations

  • W. Stewart, Senior Vice President, Power

"V. West, Supervisor, Planning

  • T. Williams, Manager, Nuclear Training

.

Other Itcensee employees contacted included technicians, Operation's

! personnel, maintenance and instrumentation and controls personnel, and

office personnel.

NRC Representatives

  • J. Caldwell, Senior Resident Inspector
  • L. Engle, Licensing Project Manager
  • M. Ernst, Deputy Regional Administrator

M. Shymiock, Chief, Operational Programs Section

'J. Taylor, Deputy Executive Director for Operations (EDO)

  • W. Troskoski, Regional Coordinator EDO
  • B. Wilson, Branch Chief, Reactor Projects
  • Attended exit interview ,

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2. Exit Interview (30703)

The inspection scope and findings were sumarized on March 11, 1988, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings. No

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dissenting ccenents were received from the licensee. Proprietary

information was reviewed by the inspectors, however, no proprietary j

information is included in this report.

Note: A list of acronyms used in this report is contained in paragraph 8. I

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Item Number Status Description / Reference Paragraph

338, 339/88-06-01 Open VIOLATION - Failure to follow  !

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procedure for (1) audits of operator

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aids; (2) configuration control of the j

j casing cooling system; and, (3)  !

revision of surveillance instruction

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and abnormal procedure to include  ;

Technical Specification revision on

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Mode applicability for containment

4 pressure - high. (paragraphs 5.a.(7),

5.b, and 5.g respectively.)
338, 339/88-06-02 Open UNRESOLVED ITEM - Determination of

j seismic qualifications for H and J  ;

train emergency switchgear cabinets,  !

! (paragraph 5.b)

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338, 339/88-06-03 IFI - Calibration of control room

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instrumentation. (paragraph S.a.(5)) .

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! 3. Licensee Action on Previous Enforcement Matters (91701) i

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This subject was not addressed in the inspection.

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i 4. Unresolved Items  ;

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Unresolved items are matters about which more information is required to

! determine whether they are acceptable or may involve violations or ,

j deviations. An unresolved item identified during this inspection is

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discussed in paragraph 5.b.  ;

j 5. Operations (71707,71710,42700)  !

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The inspectors performed extended observations of control room operations '

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I (including back shifts), shift turnovers, and reviewed applicable operator ,

j logs. The inspectors monitored Operations personnel performance, i

awareness of plant status, use of procedures, and the maintenance of  !

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required station logs and status boards,  ;

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1 Interviews were conducted with the Assistant Station Manager of Operations  !

! and Maintenance (C&M) Superintendent of Operations, Shift Supervisor >  !

! ($$s), Assistant Shift Supervisors (Assistant SSs), Control Room I

! Operators. Shift Technical Advisors (STAS), and various equipment l

[ operators. Random interviews were conducted with operators in the control

i room and equipment operators during system walkdowns, plant tours, obser-

l vations of surveillance and post maintenance testing, and tagging and '

j removal of equipment from service.

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The inspectors noted that many of the Operations managers hold Senior I

Reactor Operator licenses with an extensive amount of on-shift time, which  !

greatly centributed to the Operations staff's confidence in management.

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a. Control Room and Local Plant Operations

(1) Control Room Demeanor

Control room conduct was a noteworthy strength. Licensed

operators were observed to remain within the work area as

required by administrative procedure, ADM-19.10, Limitations on

Licensed Personnel Movement, dated March 31, 1983, and

Regulatory Guide 1.114, Guidance On Being an Operator At The

Controls Of A Nuclear Power Plant. All licensed operators were

attentive to plant operations and alarm status. The attitude of

personnel was consistently professional. Discuss %ns were

limited to plant related activities.

Noise levels were low. The licensee had established a control

room environment which was conducive to attentive operation of

the nuclear units. The licensee had moved the maintenance /

planning functions out of the control room which resulted in a

quiet control room with a minimum number of distractions. The

control room was clean, uncluttered and well organized.

Access to the control room was controlled by administrative

procedure, ADM-20.11, Control Room Access, dated March 31, 1983.

The inspectors observed that personnel requested permission to

enter the work area, waiting out of the way until granted

permission to enter. The access control program was very '

effective despite the absence of any warning sign or pt scical

barrier.

No violations or deviations were identified.

(2) Procedural Compliance

The control room operators were observed performing a number of

procedures and evolutions. Licensed and non-licensed operators

had been instructed to follow procedures verbatim and if the

procedure could not be performed as instructed, a temporary

procedure deviation was to be processed and approved in order to

accomplish the task. Compitance with this instruction was ,

  • videnced when reviewing the large number of temporary procedure ,

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deviations contained within the files located in the control

room. General weaknesses were noted with the temporary

procedure deviation process as noted in paragraph 5 d of this

report, i

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No violations or deviations were identified.

(3) Procedure Terminology versus Control Board Labeling

Procedure 1-AP-20, Operation From The Auxiliary Shutdown Panel,

dated January 21, 1988, was reviewed for consistent terminology  !

between the procedure and the auxiliary shutdown panel. The i

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panels contained all instrumentation required by Technical

Specification 3.3.3.5 with the appropriate measurement range.

Additionally, all instruments were within the current

calibrattor, period, although several were missing current

calibration stickers. The following comments were discussed

with the licensee. Step 5.9.b of 1-AP-20 directed the operator

to adjust the steam generator power operated relief valve (SG

PORV) setpoints as required to maintain steam header pressure,

however, the instrumentation used was labeled "SG PRESSVRE".

The procedure did not caution the operator to ensure that the

auxiliary feedwater flow controller is set to the 100 percent

open position or that the SG PORV controller is set to the O

percent closed position before placing the local-remote switch

into the "LOCAL" position. The inspector noted that the

addition of operating bands or setpoints to the remote shutdown

panel gages could enhance the implementation of the control room

inaccessibility procedure.

No violations or deviations were identified.

(4) Alarm Response

Response to alarms and annunciators by licensed operators was

very good. The licensed operators were able to explain

conditions associated with all lit annunciators. Upon

annunciation of an infrequently received alarm, the licensed

operators were observed reviewing the annunciator response

procedures, directing the appropriate equipment operator to

verify local alarms, and taking corrective action as necessary.

The licensed operators appeared to be cognizant of the

evolutions occurring in the plant and their potential effect on

instrumentation.

No violations or deviations were identified.

(5) Status of Control Boards and Instrumentation

'/requent tours of the control room, including walkdowns of

control panels, were conductcd by the inspectors. The control

taards have very few work tickets outstanding. Work tickets

ccated in the control room are only written for defective

switches or meters and not associated components. The licensee

was continuing efforts to bring the annunciator panels to a

black board condition.

Commensurate with these attempts, a small number of jumpers had

been installed to remove annunciators from operation which the

engineering staff had determined to be non-essential to the safe

operation of the plant and which required final implementation

of the associated engineering work request for removal. The

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jumpers were controlled by a jumper log, and licensed operators

were aware of the specific annunciators in a jumpered condition.

The inspectors noted that although control room operators check

strip chart recorders, entering date and time daily, the strip

chart time increments were not synchronized with standard time.

Synchronization of all strip chart recorders to standard time

could enhance plant operations and greatly assist the licensed

operators' examination and analysis of plant transients.

Calibration stickers were attached to almost all installed

meters, gauges and controllers. However, some of the indicators

had no calibration stickers and some existing stickers were

either illegible, blank or contained past due dates. The

control room operators, when questioned about these discrepan-

cies indicated that they believed that calibration stickers

were no longer required to be placed on control room indicators;

consequently, the discrepancies were not thought to be

significant. In February 1988, an Assistant Shift Supervisor

had sent a memorandum to tne I&C Supervisor requesting a status

of the sticker program. A response to that memorandum was under

development during this inspection.

The inspectors noticed that several calibration stickers

associated with the Unit 1 Residual Heat Removal (RHR) System, a

system required to be operable under the Technical

Specifications, had expired calibration datos. The licensee was

asked to verify that the indicators were included in a periodic

calibration program. The following indicators were submitted

. for licensee review.

Indicator Title

FT-132A and -1328 Component Cooling Water Flow

Through the RHR Heat Exchangers

TE-149A and -149B Component Cooling Water

Outlet Temparature from the RHR

Heat Exchangers

TE-150A and -150B Component Cooling Water

Outlet Temperature f rom the RHR

Pump Seal Coolers

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FS-131A and -131B Component Cooling Water Flow

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Switch from the Outlet of the

RHR Pump Seal Coolers

PT-1402 and -1403 Pressure Transmitters for

Automatic Closure of Valves 1700

and 1702 RHR Loop Suction

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Isolation

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i TE-1604 RHR System Heat Exchanger l

Inlet Temperature [

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TE-1606 RHR System Heat Exchanger l

Outlet Temperatu e  !

PIC-1606 RHR Pump Discharge Pressure

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FT-1605 RHR System Flow Returning to i

Reactor l

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Ammeter RHR Pump Motor Current  !

It was determined that only indicator PT-1402, PT-1403 and .

FT-1605 were included in a periodic calibration program. The l

remaining instruments were calibrated only if required following i

a maintenance repair or replacement effort. Consequently, the

instrumentation channels had not been recently calibrated and  !

available records indicated typical calibration dates of 1976 l

through 1982. l

A brief review of other control room indicators revealed that

the instrumentation channels for numerous plant systems covered

by Technical Specifications were not included in periodic

calibration programs. A sampling of this list follows:

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Indicator Title

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TI-103A Charging Pump Lube Oil I

Cooler Outlet Temperature

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FI-105 Auxiliary Service Water Pump (

Discharge Flow {

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TI-150A Containment Sump Temperature i

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TI-105 Refueling Water Storage Tank

Recirculation Temperature

PI-156A Reactor Coolant pump A Seal i

Differential Pressure i

PI-121 Charging Pump Discharge

Pressure

TI-144 Non-regenerative Heat l

Exchanger Outlet Temperature  !

TI-139 Excess Letdown Heat

Exchanger Outlet Temperature

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. PI-138 Excess Letdown Heat

Exchanger Outlet Pressure

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The licensee indicated that a commitment was made to  :

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I periodically calibrate only that equipment listed in Regulatory

Guide 1.33, Appendix A, Section 8, in a 1981 response to a

Notice of Violation (338/81-07-14 and 339/81-08-14), (Licensee '

. letter serial number 385 dated July 10, 1981.) Appendix A was l

l reviewed and the above mentioned systems, including the RHR ,

system, were not listed. However, for the RHR system, plant

operating procedures were identified which made use of the RHR

l indicators. For example, operations procedure 1-0P-14.1,

t Residual Heat Removal System, dated November 19, 1987, specified

' in step 4.1.14, that T!-1604 be used to monitor RHR system

! temperature increase when reactor coolant temperature is less

I than or equal to 220'F. Additionally, step 4.1.15 contained a

note specifying that component cooling water flow through the

4 RHR heat exchangers not exceed 8,900 gallons per minute. This

flow rate was monitored on flow transmitters FT-132A and

i FT-1328. Also step 4.1.16 specifies that TI-149A and TI-149B be

monitored to ensure that component cooling water return

j temperature from the RHR heat exchanger remains less than or  ;

equal to 200'F during system heatup. Procedure 1-OP-14.3, j

Swapping on Restarting Residual Heat Removal Pumps, dated

July 31, 1987, required in step 4.1.18 that RHR pump amperes be

i verified to be normal. Additional procedures may exist that

utilize instruments not in a periodic calibration program. For

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example, an annunciator response procedure would be used to

respond to low component cooling water flow through the RHR pump

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seal coolers. Since flow switches FS-131A and FS-1318 are not

. periodically checked for calibration accuracy, the annunciator

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might not alarm when required and operator corrective action ,

might be delayed.

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! These procedural examples were discussed with Operations  !

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Department supervisors. The procedural reliance on uncalibrated l

control room instruments was identified as a weakness. The '

i licensee committed to reevaluate the calibration program and  ;

indicated that important control room indicators beyond those

listed in Regulatory Guide 1.33 would be included in the  ;

periodic calibration program. Decisions on specific indicators j

would be made on a case by case basis, depending on their  ;

importance to safety, usage during plant operations and existing ,

procedural requirements. The reevaluation of the previously 1

1 identified instrumentation for incorporation into the plant ,

i calibration program is identified as Inspector Follow-up Item  ;

) 338, 339/38-06-03. l

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l No violations or deviations were identified. ]l

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(6) Communications

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Equipment operators, control room operators, STAS, and the i

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Assistant SSs appear to effectively connunicate, remaining

constantly aware of the status of the plant at any given time.  !

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Interviews with the plant staff indicate that all individuals

appear to have a good working t tpport within each shif t. The

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plant staff further stated that the Operations management was

readily accessible and receptive to their concerns and ideas.

The 0,serations Superintendent was frequently seen in the control 1

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room, where he was able to observe shift operations and readily

communicate with the plant staff. Additionally, the Operations

! Superintendent attempted to meet weekly with the Operations crew '

l in requalification training.

] The $$s spent a majority of their time in the Technical Support

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Center (TSC) controlling the implementation of maintenance

1 activities. The day shift workload on the SS is very

demanding. One SS stated that during the day shift, time was
typically not available to tour the plant or personally observe '

control room operations. It should be noted that the TSC is

l located adjacent to the control room. The SS, however, is ,

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frequently to contact with control room personnel via telephone.

I In light of the SS's day-shift workload involving long absences  ;

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from the control room, the licensee should evaluate the impact '

i of the SS's ability to direct the licensee response to a  :

transient.  !

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No violations or deviations were identified.

(7) Logs and Records ,

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The inspectors reviewed the jumper log, control room operator -

log, the Assistant 55 log, safeguards operater log, night order  !

l log, abnormal status log, and the SS log. The logs kept by the

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control room operators contained accurate information. It was !

noted during shift turnovers that the off going control room }

operator referred heavily to his personal notebook to inform the

oncoming control room operator of evolutions and changes to  :

plant status that occurred during his shift. The licensee

should review this practice to ensure that the control room

operator narrative log contains sufficient and necessary ,

j historical plant operating information.  ;

During the review of the control room operators' narrative log,

the inspector found uncontrolled sketches which could have been

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misconstrued as operator aids. Administrative procedure

ADM-19.27, Control and Use of Operator Aids, dated October 29,

i 1986, delineates the requirements for sources of information

I which are posted to aid operator recall or note an abnormal  !

! condition. ADM-19.27 also requires that "audits of the Operator

J Aid Log index will be conducted each calendar quarter and I

documented on 1-MISC-31." Miscellaneous Procedure 1-MISC-31, i

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Quarterly Operator Aid Log Review, dated August 21, 1986, states

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that "all Operator Aids in the areas of the station will be

surveyed on a quarterly basis (staggered one-third of the areas ,

, every month)."

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Further examination of the operator aid program required audits

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revealed that the licensee failed to perform the required l

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monthly audits for the first, second, and fourth quarters of '

1987 or the first quarter of 1988 as specified in ADM-19.27.

i This failure to perform the required attits is identified as an

example of violation 338, 339/88-06-01. In response to the

j! inspector's findings, the licensee removed the questionable

i sketches and performed an audit of the entire operator aid

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program. Several additional minor discrepancies were identified

i and corrected by the licensee.

! (8) Technical Specification Compliance

The licensee utilizes an Action Statement Status Log to control

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equipment and track Technical Specification action items.

Information contained in this book distir.guished between those

items which actually placed the plant into action statements and

! those which were "info," serving as a warning to the licensed

operators that additional actions may force the plant into an

action statement. Review of the log book is accomplished during

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shift turnover. These methods appeared to provide positive

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control over plant status.

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I No violations or deviations were identified. l

, (9) Shift Turnover Process

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The inspectors observed several shift turnovers for various l

watch stations inside and outside the control room. These l

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turnovers were accomplished efficiently and in accordance with i

i tJrnover procedures. As part of the turnover routine, each  !

Assistant SS completed procedure MISC-35.2, SRO (Senior Reactor  !

Operator) Shift Turnover Checklist, dated December 22, 1987, for i

the nuclear unit for which he had supervisory responsibility. '

Each Control Room Operator (CRO) completed procedure MISC-35.0,

CR0 Turnover Checklist (Medes 1-4), dated December 22, 1987, for

, his assigned unit. The checklists contained sufficient l

information un plant status, parameters, system alignments and

abnorrealities to ensure that adequate turnovers occurred. The

checklists included references to any edor surveillances or i

saintenance evolutions in progress. I

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Turnover weaknesses were nSted ir et eset Anistant SS l

cotepleted detailed plant status i N e ? nle uW while

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making a more general review ed '

site vnit's status.

While procedure MISC-35.2 adequ .4d t sing *a unit,

i l

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_., . - - . - , - - -

- ,- - - - - - . . . - - . a_*, _ , - nor

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- - - .-. -- _

.. ._ _-. - - _- - - . __-

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it did not include requirements to review the equivalent logs on

the opposite unit including the opposite unit's Assistant SS  !

-

narrative log book, Technical Specification action item log, and ,

I reactor operator narrative log book. Consequently, the l

potential existed for an Assistant SS to obtain a much less  ;

detailed review of the opposite unit. With both Assistant SSs l

in the control room this would not be a concern. However, one  !

] Assistant SS frequently leaves the control room to perform tours  !

] and the $$ is typically outside the control room. Consequently, I

J short time periods exist during which only one Assistant SS is  !

<

in the control room. This individual may not be equally  ;

familiar with the status of both units. This potentially i

'

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disadvantageous situation was discussed with the licensee who l

subsequently committed to broaden the turnover requirements for  !

Assistant $$5 to include both units. l

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Both Assistant SSs reported to a single SS who primarily worked l'

in the TSC. It was noted that the SS did not utilize a turnover I

checklist. Exchanges of information between relieving SSs was

observed and found to be adequate. Typical reviews included the

same information contained on procedure MISC-35.2 such as the

2 Contrel Room Logs, Jumper Logs, and Shif t Orders. Although tne i

l observed turnovers were sati sf actory, the lack of a written l

j turnover checklist for the SS position is a weakness which  !

should be corrected. A comprehensive checklist such as those  !

available for the other operating crew positions, could preclude  !

inadvertent failure to review important plant information prior i

to assuming shift responsibtitties. This concern was discussed  !

'

j with the licensee who subsequently committed to promptly develop

t and implement a SS turnover checklist.  :

1

J On-coming shift personnel who are stationed ovAside t,he controi

j room gathered for a briefing in the TSC shortly after completing i

i shif t turnover. The briefing was performed by the 55. The l

a observed briefings were effective in disseminating shift l

1 objectives promulgated in the Shi9 Orders and the Plan of the r

j Day, i

f Control room operators, however, did not participate in any [

i formalized sMf t briefing. Discussions with several control i

j room operators indicated that an operator specific briefing l

1 would be beneficial to their understanding of information s

! disseminated in the Shif t Orders and the Plan of the Day. The [

Operations Superintendent felt that operator turnover procedures j

i provided an adequate knowledge of proposed shif t activities. j

I

Integrated shift performance appeared to be satisfactory. l

1

No violations or deviations were identifieo. I

!

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-__ _-____ _ _ _ _ _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _____________ __________ ____ _____ _ _ _ ___ ___ -__________-__ _____ __ _ _ ______

>

11

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b. System Walkdowns

Two plant syttems, one for each unit, were walked down to assess the ,

adequacy of alignment procedures, housekeeping and configuration

l control. A Unit 1 system alignment was verified using Operating

Procedure (OP) 1-0P-7.10A, Valve Checkoff - Casing Cooling System, ,

dated January 8, 1987. System configuration and drawing accuracy

were verified through comparison to drawing 11715-FM-01SB, Rev. 5.

The drawing and checkoff procedure were determined to bs accurate.

Procedure 1-0P-7.10A was last completed on February 5,1988. The

i

latest completed procedure was verified to be conpletely filled out,

'

initialed where required, and independently verified.

During the system walkdown, performed on April 12, 1988, two

discrepancies were identified and both were promptly corrected. The f

I tags for two Recirculation Spray (RS) test connection isolation

l valves 1-RS-102 and 1-RS-104 were found to be reversed. The valves l

are similarly configured and located in close proximity to each

other. Both valves were closed as required. The tags were promptly

returned to the correct valves. No other tagging deficiencies were

identified and all other system valves contained legible, easily

identifiable tags.

The second identified discrepancy resulted because Casing t'uoling

Tank recirculation pump 4A suction isolation valve 1-RS-105 was found

closed. The valve is required to be open in accordance with align-

rent procedure 1-0P-7.10A, The discrepancy did not adversely impact

the ability to recirculate the Casing Cooling Tank because the 4B

pump was operating and the 4A pump was secured. The Operations -

Superintendent indicated that the valve had apparently been closed on

April 9 or April 10 during system troubleshooting. The trouble-

shooting effort included swapping the operating recirculating pumps  ;

and chiller units in accordance with procedure 1-0P-7.10, Casing

Cooling Subsystem of the Rectreulation Spray System, dated

October 20, 1987. The procedure did not require the normally open

pump suction or discharge valve to have their positions altered. l

However, the system operator was aware that discharge check valve l

1-RS-106 for pump 4A was stuck open as indicated by work request tag l'

WR 531252 which was issued on October 27, 1987. The operator shut

valve 1-R5-105 when he started the 4B recirculation pump to prevent  ;

the existence of an undesired recirculation path backwards through '

the 4A pump and the stuck open check valve. This action precluded

the potential for tank bypass flow. However, the change in vahe l

position was not authorized by either procedure 1-0P-7.10 or l

1-0P-7.10A. Additionally, the operator did not obtain administrative l

approval for the alteration as required by the provisions of i

ADM-14.0, Tagging of Systems and/or Components, dated February 4, 1

'

1988. This failure to utilize the provisions of ADM-14.0 to alter

the valve line-up required by 1-OP-7.10 and 1-0P-7.10A is identified

as an example of violation 338, 339/88-06-01.

A Unit 2 system alignment was verified using procedure 2-OP-7.4A,

Valve Checkof f-Quench Spray (QS) System, dated March 19, 1587.

L

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Configuration and drawing accuracy were verified through comparison

to drawing 12050-FM-91A, Revision 15. The drawing and checkoff

procedure were determined to be accurate. Procedure 2-Op-7.4A was

last completed on October 29, 1987. The latest completed procedure

was verified to be completely filled out, initialled where required

and independently verified.

During the system walkdown, performed on April 12, 1988, two minor

discrepancies were noted. One drain valve associated with pressure

indicator PI-QS-203 did not have a local identification tag attached.

Additionally, leaking drain valve 2-05-20 did not have a work request

submitted. The drain valve had been wrapped in plastic and taped to

catch a small amount of contaminated leakage. Apparently the persons

identifying the leakage did not initially process a repair request.

The licensee submitted a work request promptly after completion of

the system walkdown. The discrepancies did not affect system

operability.

Equipment operators were assigned to make two rounds of their area of

responsibility during the course of their shif t. The first round

consisted mainly of a quantitative examination of plant parameters

within their area of responsibility. The second tour consisted

mainly of a qualitative examination of plant equipment. In addition

to the system walkdowns, the inspectors accompanied several equipment

operators on their tours of the safeguards equipment areas. In

general, all operators appeared to be familiar with the equipment,

its normal mode of operation and alert to equipment abnormalities.

During the course of tcuring the Units 1 and 2 safeguards areas, the

inspector observed lifting hoists and trolleys located on rails which

were attached to the top of the H and J train emergency switchgear

cabinets. At the time of the inspection, the licensee was not able

to provide analyses showing that the Itfting equipment was

seismically qualified. This is identified as unresolved item 338,

339/88-06-02. The licent.ee promptly removed the equipment and began

to perform formal calculations. The licensee has been asked to

provide the seismic qualification calculations and the plant

modification package, which placed the lifting hoists and trolleys on

the cabinets, to the NRC. The licensee placed the use of the hoists

and trolleys under administrative control requiring the equipment to

be removed upon completion of maintenance activities.

While touring portions of the secondary side, equipment operators

were observed isolating a portion of the condensate clean-up system.

The inspector noted that the operators did not perform the tag out in

the sequence specified on the tagging record. This discrepancy was

brought to the attention of the Operations Superintendent. Although

the activity observed had no ssfety-significance, the inspector was

concerned that tagging may be inappropriately conducted during

safety-related tagging. Discussions with the Operations

Superintendent indicated knowledge of deficiencies in the tagging

,__ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

___________ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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l procedure and procedure implementation. The Operations

l Superintendent provided the inspector with two Quality Control

Activity Reports (QCAR) which were issued for lack of compliance with

ADH-14.0, Tagging of Systems and/or Components. The corrective

action to the QCAR, which had not been completed by the licensee,

included a memorandum, to be issued by the Operations  !

Superintendent, which required each shift supervisor to review with '

operations personnel the subject QCARs and the requirements of

ADM-14.0. The herations Superintendent indicated that the lecture

would stress the need for accurate tagging documentation and the

importance of aroper removal and restoration of equipment,

r

Items of noted strength observed during the plant tours included the l

color coding of unit procedures, the numerous signs reminding plant  !

personnel of which unit they are about to enter, and equipment

labeling. These items help ensure that plant personnel are worxing

on the correct piece of equipment with the correct procedure,

c. Operations-Maintenance Interface

Maintenance work orders were reviewed to evaluate the adequacy of t

protective tagging, configuration control, SRO review and approval of

functional testing, independent verification and documentation. L

Operations used Maintenance Operations Procedures (MOPS) to remove

and restore major components from service for mainte'ance. The MOPS

referred to Operations Procedures which specified which Performance

Test (PT) must be run prior to returning the component to service.

Post maintenance testing (PMT) requirements were specified at various l

points during the WR and WC process, but final determination for ,

ensuring adequate PMT was made by the Shift Supervisor. A test i

coordinator was assigned to ensure that valve lineups, periodic i

testing, predictive analyses, and post maintenance testing were

completed prior to each mode change.

PMT requirements and guidance were undergoing revision due to

problems identified by the NRC and the licensee. Quality Control

l'

Activity Report number AR-N-86-1647 was written in December 1986

against improper post maintenance testing on several components. The ,

QCAR stated that the impreper testing indicated a potential program- 1

matic breakdown. Af ter several iterations of correspondence between

maintenance and quality assurance groups, the issue was escalated to ,

plant management. The new escalation policy had been implemented l

recently. Management involved other plant groups and decided to ,

develop and issue a new procedure to control the implementation of {

post maintenance testing. Procedure ADM-16.19, Work Order / ,

Maintenance Procedure Test Follower was issued February 29, 1938. l

The Test Follower supplements existing site maintenance surveillance

procedures by defining post maintenance testing activities. Although

the Follower appeared to assist the Shift Supervisor in coordinating

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l testing requirements, the effectiveness of the program could not be l

l evaluated due to the short period of time since implementation.

l

l

Open Maintenance Work Order (%'0) 178841 for working on the 1A

l charging pump was reviewed. The operations test block on the %'O had

l

been improperly marked as not required. This item was pointed out to

I the maintenance foreman and Shift Supervisor and corrected to reflect

that a test was required. The Shift Supervisor was aware of the need

for functional testing prior to returning the pump to service. The [

maintenance procedure used to perform the work did not specify which ,

PT was required. The charging pump operating procedure specified the l

required PT. Station records wore reviewed and the inspector

verified that the applicable PT had been run following maintenance on

the Unit I charging pumps during the past year. Reviews of other

completed work orders did not indicate any discrepancies in the i

completion of PMT requirements.

The licensee was in the process of upgrading maintenance procedures

to more clearly specify retest requirements and place the retest

requirements in an attachment to the procedure. Approximately 50

procedures have been changed to date.

In summary, the current method used to perfcrm post maintenance

testing it, cumbersome but adequate to ensure components are tested

prior to declaring them operable. Additional emphasis should be

placed on upgrading the post maintenance testing guidance.

No violations or deviatiers was identified.

d. Temporary Procedure Deviations

(

The administrative program by which temporary procedure deviations  ;

are developed and approved, as specified in proceoure ADM-5.8,

Temporary Changes / Procedure Deviations, dated August 8, 1987, was

reviewed and found to be curbersome. Approximately 50 procedure

deviations were reviewed, the vast majority of which were annotated

indicating they should be incorporated as permanent procedure

improvements. However, the temporary change approvals were generally '

authorized for a single use only. The repetitive use of a procedure

necessitated the repetitive generation and approval of the deviation. .

Consequently, this method af fected the workload of the staff. In  !

dddition, the Station Nuclear Safety and Operating Comittee (SNSOC) I

repeatedly received identical deviations for review.  !

<

All of the deviations examined were enhancements which did not change

the intent of the original procedures or received prior SNSOC review. .

'

Consequently, as authorized by Technical Specification 6.8.3, they

were initially approved by two rembers of the plant staff with final

review to be perforned within 14 days by the SNSOC. Following  ;

initial staff approval and prior to SNSOC review, a copy of the i

deviation is placed with the appropriate procedure in the control

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_ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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15

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room files. Typically, this copy is not replaced with a final

approval copy af ter SNSOC review and Assistant Station Manager ,

approval. This is a potential problem because the $NSOC retains the

authority to make recommendations and comments on the deviation and

to promulgate special limitations on its use, as specified in

Attachment 1 of ADM-5.8. Consequently, the Operations Department

procedure files could contain copies of procedure deviations which do

not reflect the SNSOC approved version of the deviation.

A brief review was made to compare previously approved deviations l

held by the Operations Coordinator - Procedures to those deviations

on file in the control room. It was determined that several

deviations to procedures 1-OP-5.5 and 2-OP-5.5 were held by the

Operations Coordinator - Procedures but were not on file in the ,

control room. These deviations were annotated indicating that they

were appropriate for incorporation in a future permanent procedure

change. Their absence from the control room files could result in

performance of a procedure with previously identified enhancements  !

omitted.

Most of the deviations are marked "permanent change required". These

deviations are forwarded for review by the Operations Coordinator -

Procedures to be incorporated in a future procedura revision in  :

accordance with procedure ADM-5.4, Processing New and Revised

Frocedures and Deletion of Procedures, dated March 9, 1988. However, i

no index of deviations requiring permanent incorporation was ,

maintained. The lack of an index was disadvantageous because

approved deviations could be misplaced prior to incorporation. ,

'

Additionally, verification that all appropriate deviations had been

promptly incorporated into procedure revisions was extremely  ;

difficult. For example, a deviation was approved en August 4,1986, '

and marked "permanent change required" for procedure 2-OP-3.3, Unit  !

Shutdown Frvm Hot Shutdown Condition (Mode 4) to Cold Shutdown i

Condition (Modo 5) at 200 Degrees Fahrenheit. The procedure was l

revised in September 1986 but the deviation was not incorporated into '

the revision. As of March 30, 1988, a copy of the deviation remained

in the control room file. The deviation was either missed during the ,

procedure revision or remained in the control room file long after a [

decision had apparently been made not to incorporate the change into

a permanent procedure revision, t

The lack of a deviation index precluded an accurate quantitative

analysis of t,he backlog of procedures requiring revision. A review l

of the control room procedure file, the !&C Department procedure  ;

file, and the file maintained by the Operativns Coordinator - '

Procedures indicated that a substantial backlog existed. The [

licensee had identified the backlog concern prior to this inspection. i

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The Operations Coordinator - Procedures had been designated as the

Site Coordinator Procedures, a newly created position, for the l

purpose of better managing the procedure change process. The ,

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centralization of the change process should improve efficiency and l

reduce the backlog. l

l

Another potential weakness of ADM-5.8 waa that deviations were not  ;

evaluated for applicability to both units when initially approved.  !

Consequently, t.he control room file for Unit 2, procedare 2-0P-5.5,

Filling and Venting the Reactor Coolant System With One or More Loop

Isolation Valves Closed, contained 3 "permanent change required"

l deviations, none of which were included in the Unit 1 file.

l Similarly, Unit 1 procedure,1-0P-b.5, contained a deviation which

was not in the Unit 2 file.

The review process for the deviations was also identified as

containing weaknesses. Presently, ths staff members have no

checklist to use in determining if a proposed change constitutes a

change to the intent of the original procedure. A generalized

definition of "change of intent" is contained in ADM-5.8. The i

procedure does not require applicable sections of the Technical ,

Specifications and Final Safety Analysis Report be reviewed prior to

'

determining if a proposed deviation effects the intent of a  :

i pre-existing procedure. Additionally, proposed deviations are not  !

evaluated to determine whether they change acceptance criteria.

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I

modify hold points, decrease fire protection effectiveness, modify

independent verification requirements, change setpoints, or decrease

the effectiveness of the emergency plan. The licensee has previously [

recognized weaknesses in ADM-5.8 related to defining intent changes t

and a revision is under development. I

The weaknesses identified in the procedure change program were

discussed with the Operations 3uperintendent. Prior to this

inspection the licensee had developed and was reviewing a proposed

revision to ADM-5.8. The licensee committed to evaluate the r

inspection teams coments relative to procedure deviation control and I

to seek additional information from industry sources. Appropriate  ;

modifications would be included in a revision to ADM-5.8 which was '

scheduled for issuance on May 1, 1988. j

Additionally, a complete audit of the control room procedure files ,

was initiated to ensure that all appropriate previously approved  !

deviations were available to the staff. Any deviation copy which did '

not reflect $N50C review and management approval would be replaced

with a copy reflecting the approval.  !

l

No violations or deviations were identified. l

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e. Surveillance Testing  ;

Selected surveillance tests were reviewed and/or witnessed by the  !

inspector to ascertain that current written approved procedures were I

available and in use, that test prerequisites were met, that system j

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____ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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17

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restoration was completed and that test results were adequate and in

compliance with applicable Technical Specifications.

The following tests were either reviewed or witnessed. Tests

witnessed are identified by an asterist.

l

  • 1-PT-213.3, Valve IS! (Consainment Atmosphere Clean Up System) l
  • 2-PT-64.4A, Casing Cooling System 2-RS-P-3A l
  • 2-PT-64.4A.1, Casing Cooling Pump Bearing Temperature i
  • 1-PT-82.2B, IJ DG Test (Simulated Loss of Off-Site Power) i

1-PT-34.2, Charging Pump Test 1-CH-P-1B, ,

Surveillances observed by the inspectors were performed in accordance (

with procedures and in constant communication with the control room i

staff. Prior to the performance of 1-PT-82.28, an infrequently

performed test, a pre-test briefing was held to review all required l

actions and desired responses.

It was noted that operators were signing prerequisites for verifying  !

systems lined up per OP-1A, Pre-Start-Up Checkof f List, based on >

personal knowledge of system conditions but without actually looking

at the completed copy of OP-1A. The licensee comitted to issue l

guidance to Operations personnel with respect to what actions as e

required to verify this specific prerequisite.  :

!

Examination of the Diesel Generator test file led to discussions with

the Superintendent of Technical Services on the subject of the .

licensee's implementation of Regulatory Guide 1.108. Periodic Testing

of Diesel Generator Units Used as Onsite Electric Power Systems at i

Nuclear Power Plants, as comitted to by the licensee in their  !

Technical Specifications, The licensee was in compliance with the  !

provisions of the Technical Specifications and Regulatory Guide  ;

1.108. The inspector noted that the Itcensee performs post main-

tenance testing separate from the operability testing. Post t

maintenance testing which results in a f ailure is not considered a ,

valid failure if the failure was caused as a result, of the inability  !

to correct the original problem. Failures as a result of unrelated  !

problems, however, are considered valid fattures.  !

!

No violations or deviations were identified. {

!

f. Overtime

The use of overtime by Operations was reviewed to ensure compliance l

with NRC guidelines and Technical Specification limits. NRC

l

guidelines on work hours include Generic Letters 82-12 and 82-02.  !

The generic letters note, "in the event that unforeseen problems l

require substantial amounts of overtire to be used, or daring l

extended periods of shutdown for refueling, major maintenance or l

najor plant modifications, on r, temporary basis," that specific  !

guidelines should be adhered to. These guidelines include extended

_ _ _ - - _ _ - - - _ _ _ _ _

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work hours up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in a seven day period. The generic letters

,

also recognize "that very unusual circumstances may arise requiring

deviativ from the above guidelines, such deviation shall be '

authorizeo by the plant manager or his deputy, or higher levels of

management."

The licensee's administrative procedure, ADM-20.3, Hours of Work,

dated November 5, 1987, was reviewed and found to adequately

implement NRC guidelines in this area. Review of the licensee's

"Deviation from Maximum Work Hours" records for 1987, however,

indicated that the maximum guidelines were exceeded by Operations

personnel approximately sixty times. The majority of the deviations ,

were for exceeding 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in seven days during outages and peak

vacation periods. The frequency of exceeding the maximum work hours

in 1987 indicates that overtime is being authorized quite often. The

licensee stated that operators were not remuved from training or

'

required to work on their days off in order to prevent other

oper.. tors from exct Jing the overtime guidelines. The licensee ,

stated that the overtime deviations were utilized to support

vacations and outages. Records for 1988 up to April 11, 1988,

indicate that the guidelines were exceeded four times.

No violations or deviations were identified,

g. Review of Abnormai Operating Procedures

The inspector reviewed five abnormal operating procedure s. The

following discrepancies were noted.

Abnormal procedure Ap-3, Loss of Vital Instrumentation, dated May 15,

1988, was established by the licensee to implement the action

Jtatements for inoperability of, among other instrumentation,

containment pressure - high. The action statement for containment

l pressure - high in Technical Specification Table 3.3-3 required that l

1 an inoperable channel be placed in the tripped condition within one

4 hour for operation to proceed. The inspector noted that the Mode

applicability of the procedure was only for Modes 1, 2 and 3.  ;

Technical Specification 3.3.2.1 required containment pressure - high r

to be operable in Mooes 1, 2, 3 and 4. The inspector determined that '

Technical Specification 3.3.2.1 had been rev' sed to include Mode 4

for containment pressure - high in Amendment Nos. 84 and 71, issued

on August 25, 1986. Further review showed that in addition to the

AP, the 12-hour surveillance procedure for containment pressure -

high, LOG-4, Control Room Operator Log, had also not been changed to

include the Mode 4 applicability, iechnical Specification Table

4.3-2 required a channtil check every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> for containment

pressure - high. The failure to ravise the Ap and the surveillance

i procedure to include Mode 4 applicability for contain ent pressure -

high is identified as an example of violation 338, 339/88-06-01.

,

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s

Review of AP-4.2, Malfunction of Nuclear Instrumentation

(Intermediate Range), dated May 1,1988, indicated that step 5.3.4 -

was in error in that the step directed the operator to jumper out <

only source range channel N32 if either of the intermediate range

detectors failed. The objective of the section was to ensure that

both source range detectors were disabled in the event a second s

intermediate range detector failed and, therefore, avoid actuating

the source range detectors at high power levels. An additional

discrepancy was observed in that the note af ter Step 5.1.1, stated, '

"Do not pull source range instrument fuses," yet step 5.5.3 provided

directions to return the source range fuses if they were pulled. The

licensee indicated that the procedure would be corrected.

The inspector also noted that various APs have actions tied to

Technical Specifications that specify specific time frames for the

action to be performed. The APs do not, however, provide the time

limitations. An exemple of this is AP-1.2, Continuous Rod Insertion,

dated August 27, 1986, step 5.4, which directs che operator to verify

reactor coolant system temperature greater than 541*F yet does not i

include in the "response not obtained" that the plant is to be placed

'

in Hot Standby if temperature is not restored within 15 minutes. The

inspector recommended that the procedures be reviewed to determine if

this information should be added to aid the operator in meeting the ,

Technical Specification time requirements.

The licensee's attention is also directed to an April 27, 1988,

letter from C. A. Julian, NRC, to W. L. Stewart, Virginia Power,

which indicated that deficiencies existed in AP-33, Reactor Coolant

Pump Seal Failure. AP-33 was written such that the operator could

not comply with Step 5.2 and could transition out of the procedure

prior to tripping the reactor coolant pump with the failed seal. .

Two operating procedures were also noted to be deficient. In !

addition to these items, the examiners subsequently determined that

procedure AP-22.7, Loss of Emergency Condensate Storage Tank, did

not contain provisions to fill and vent the firemain when the  ;

firemain is used to supply auxiliary feedwater. The inspectors :

'

verified during the OPA that the license was also aware of the

deficiency in AP-22.7 and that the procedure was corrected,

i t

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The licensee indicated that the APs were being reviewed and '

reformatted into the standard emergency operating procedure format i

in the procedure upgrade program. These findings indicate that  ;

i

additional attention to detail is warranted during these reviews. l

1

6. Maintenance Support of Operations (62700, 62702, 92700)  !

'

{

j The inspectors reviewed station administrative controls; conducted [

interviews with workers and supervisory personnel; and reviewed work

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,

packages, work requests, deficiency reports, the maintenance planning ,

process, the maintenance backlog and the prtventive maintenance program to

ascertain whether the licensee was implementing an eilective program t

('

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relative to maintenance activities. The review included the maintenance

organization work procedures, maintenance programs and the interface with

Operations. Interviews were conducted with maintenance supervisors, the

planning supervisor, planners, he Operations Maintenance Coordinator

(OMC), and a number of craft 9, foreman and supervisors in the

mechanical, electrical, and ,nstrumentation and controls areas.

Interviews indicated an overall good knowledge and understanding of

maintenance duties and responsibilities.

There have been continuing improvements in the corrective maintenance

program at North Anna such as the procedure rewrite program, Quelity

Maintenance Team (OMT) training and increased management attention in

completing corrective -maintenance. The coordination of work activities

between Maintenance and Operations appeared to be vary good. Pihnning,

work history, repetitive failure analysis and root cause analysis were

,

considered to be areas of weakness and are being adversely affected by the

large number of completed but not closed work orders. The QMT program had

been initiated prior to the end of the last SALP period. The QMT program

appeared to be a good program, however, the instrument and controls and

electrical crafts had not completed training. The history of events

during the SAlp period indicated problems in the maintenance area,

however, it appeared that increased management attention had been placed

on improving ths quality of maintenance.

a. Planning Process

Administrative procedure ADM-16.7, Corrective Work Orders, described

the program for processing maintenance work requests including

identifying, prioritizing, authorizing, scheduling, assigning and

documenting associated activities. Work requests were processed and

approved by the OMC. Work orders were then generated by the various

maintenance planners.

The corrective maintenance process could be initiated by any site

employee. The work request form was a te part form. The upper

section was attached to the defective equipment and the bottom

section was forwarded to the OMC, Plant walkdowns and review of

deficiency reports indicate that the licensee was very efficient in

identifying equipment deficiencies.

The OMC screened all work request (WR) forms for accuracy and

completeness. Additionally, the OMC completed the WR form by

assigning priority, plant modo and some of the post maintenance

testing requirements. The work request was then entered into a

maintenance computer program and the following day the OMC verified

that the WR form was properly entered into the maintenance computer

program and approved the work request.

_ , _ - . __ _.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _

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21

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Next, the planning department reviewed the various WRs listed in the

maintenance computer files. The various disciplines in planning

determined responsibility, assigned lead trade and generated a work

order (WO) for each WR. The individual planners placed the assigned

WO in the lead trade planner's file who assigned the WO a title and

added a brief job description. Approximately 50% of the time, the

planner would go into the plant and review the WO to ensure correct-

ness in job description, component, train, location and type of

deficiency. If practical, the planner would then review and list

appropriate prints and schematics, component work history, suggest

procedures to be used, and verify availability o' parts for repairs.

If a Radiation Work Permit (RWP) was required the planner also

requested Health Physics assistance in advance to prevent delays. l

There were various programs used to coordinate maintenance

activities. The plan of the day (POD) listed those maintenance

1 activities that were to be performed during the course of the day.

The POD was used as a notification to the maintenance organizations

and Operations that various systems or components were to be worked.

There was a daily, 11:00 a.m. planning meeting where operational

needs were discussed. A weekly maintenance schedule was reviewed and

approved by the planning department and this scheduling document was

issued to coordinate work activities with the Operations Department's

periodic test schedule. There were also bi-weekly Electrical,

Mechanical and Instrument planning meetings to coordinate the

upcoming maintenance and preventive maintenance items with

Operations; resolve work orders on hold; and, call attention to

overdue maintenance. The OMC also maintained a list of Operation's

"Ten Most Wanted Maintenance Items" which aided in scheduling needed

maintenance activities. At the scheduled time, the WO was forwarded

to the appropriate maintenance foreman, the maintenance was performed

and the WO was sent bath to the planner. The planner reviewed the

completed WO, placed the appropriate data in the equipment history

file, and transferred the completed WO to the vault for permanent

record retention. '

i

j The scheduling of maintenance items and the maintenance interface j

with Operations was not a problem and appeared to function

The OMC was an SRO licensed individual that directly

'

adequately.

interfaced with the Maintenance Planners and Operations Shift '

Supervisor. This greatly enhanced the licensee's ability to schedule

maintenance items.

It was noted during the inspection that an extremely large number of

completed W0s had not been reviewed by the maintenance planners and

also the WO data had not been entered into the equipment history

files. The backlog had been in the 8000 to 10,000 range for all

disciplines for the last six months. It was noted that approximately

600 WRs were submitted to the mechanical maintenance planners per

j month for review and processing. This workload had been effectively

t

5

.

22 l

overloading the mechanical maintenance planners. Another effect of

the large backlog of completed W0s was the inability to track

repetitive failures since the equipment history files were not ,

up-to-date.

The inspection team observed that due to the large workload of the ,

mechanical planners, that the W0s sent to the field did not always

contain all of the needed data such as complete job steps,

procedures, tools, drawings or technical manuals. Interviews with

maintenance mechanics and mechanical supervisors also indicated that

when a WO was issued from planning, the planning process was often

not completed. Work packages received from the Planning Department

were considered to be good for I&C and electrical, however, the

mechanical work packages were lacking. Various foremen stated that

they had to identify appropriate procedures, technical manuals and

prints. The mechanics further stated that they felt the procedures

were only 70 percent effective.

4 The licensee had implemented a number of items to assist in the

planning effort. Two contract planners had been added to the staff

within the last year. An additional clerk was hired by the

mechanical group to assist in completed package preparation prior to

'

forwarding to planning. Two crafts foremen (one Mechanical and one

i Electrical) had been hired by Planning to assist in the planning

effort. planning had established a two week review cycle for W0s

that have been planned but not performed. Craft, Operations, and '

Planning supervision participated in scheduled debriefs of incomplete

work and these discussions impact planned work.

Overall, the progra:a for planning work activities appeared to be

adequate. The coordination and scheduling activities between

Operations, Maintenance, Health Physics and other support i

organizations appeared to be very good. Weaknesses in the planning i

process included the large backlog of completed but not processed l

W0s, the lack of trending, the staffing of mechanical planners, and

incomplete work packages issued to the field by Planning. Actions i

being taken by the licensee should be effective in resolving these

weaknesses.

1

No violations or deviations were identified.

! b. Work Orders

i

Selected open and closed work orders (WO) were reviewed for adequacy, l

detail, authorization, post maintenance testing, procurement, l

housekeeping, QA/QC review, root cause identification and closecut i

< inspection. Approximately 40 work orders were reviewed.

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Work orders that were generated by the planning department were

forwarded to the maintenance foremen. Maintenance foremen indicated

that they often added additional information to complete the work

orders prior to performance. The completed work orders reviewed were

adequately detailed, identified appropriate procedures in most cases,

identified problems and locations, and the job was properly

prioritized. The only area that appeared to need more detail was in

providing identification of drawings and technical manuals.

Procedures appeared to be adequate to ensure that post maintenance

testing was performed prior to returning the equipment to service,

however, referencing from one procedure to the next was cumbersome.

A section titled, Post Maintenance Check / Testing, was included in

certain work procedures and provided for work area cleanup, tag

removal, Shift Supervisor notification, RWP clearance, and post

maintenance test completion.

The Quality Maintenance Team (QMT) concept, discussed in

paragraph 7.d, appeared to have been fully implemented in the

Mechanical Maintenance Department where the quality control functions

were performed by QMT trained individuals. QC personnel were still

utilized for various hold points in Electrical and I&C Procedures.

QC also performed a random cursory review of completed work order

packages. Independent verification was performed as required by

various qualified individuals. The processes controlling QC hold

points, QC review, and independent verification appeared to be

adequate.

The inspectors noted that documentation of root cause for component

failures was not specific, was not always clear, and in some cases

was missing. A working program for tracking repetitive failures and

subsequent root cause analyses for the failures was a weakness

because of the large backlog of completed W0s that have not been

entered into the history files.

Overall, work order packages appeared to adequately document work

activities. Documentation of post maintenance testing and root cause

analysis were areas where added management attention was warranted.

No violations or deviations were identified,

c. Preventive and Predictive Maintenance l

l

(1) Scheduling

.

Scheduling was done by a maintenance scheduler, who made a I

weekly coordinated schedule each Thursday for all planned  !

maintenance to be done during the next week (Friday to Friday). l

This schedule included performance tests (surveillances), i

preventive maintenance, and corrective maintenance. Mechanical, j

electrical, and instrumentation areas were all included and the j

scheduling was done with the aid of a computer system. Then the

weekly schedule was printed out in two formats, by

foreman / maintenance crew assignments and by equipment / system.

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24

The weekly schedule included an estimated 10% overload for each

foreman and maintenance crew, to allow for possible job

deferrals due to unforeseen holdups with parts, Operations, etc.

Also a list of minor maintenance items (no work request

required) was used for fill-in work.

'

1 The weekly maintenance schedule was reviewed and modified daily ,

at the morning maintenance POD meeting. This meeting was i

attended by supervisors from mechanical, electrical, _and

instrumentation maintenance and also Operations and Health

Physics. Overall, scheduling of maintenance appeared to be very

well organized and conducted and is considered to be one of the

licensee's areas of strength.

(2) Scope

The scope of the preventive maintenance (PM) program for

mechanical and electrical areas appeared to be adequate. In

1987, system walkdowns by contractors were done to identify all

equipment and make PM program additions. As a result, about 30

PMs were added and many BOP components (including approximately

1500 manual valves) were added. Additionally, the PMs are under

continual review for updating, readability, initial conditions,

and post maintenance testing. In 1987, approximately 200 PMs

were revised. t

The scope of instrumentation PMs did not appear to be as

complete. Many supplemental gages for Technical Specification

equipment or balance of plant equipment were not included in the

PM program. For example, the calibration program did not

include some control board gages. This concern is discussed in

paragraph 5.a.(5) in more detail.  ;

(3) PM Adjustments

PMs are routinely reviewed for both scope and frequency. Change

recommendations come f rom Mainter,ance and Operations, OERs,

design changes, and predictive analysis. The predictive

maintenance includes oil analysis, vibration measurements, and

motor operated valve analysis and testing (MOVAT). A checkmate

check valve testing program is planned. Based on predictive

maintenance, about 20 changes in pH frequency were made in 1987

'

and about 10 changes in PM frequency were made based on

Maintenance or Operations recommendations. Repetitive failures

of machinery have not been well trended in *he past and have not

been a substantial factor in adjusting PM frequencies. In one

case, the hydrogen and oxygen analyzers for the Waste Gas Decay

Tank (WGDT) were known to be affected by summer temperatures.

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1

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l During the months of April-September, they would predictably

! drift out of calibration. However, no licensee action had been

l taken to increase the PM ' frequency on these safety-related

I instruments. The licensee committed to an increased PM fre-

! quency on these hydrogen and oxygen analyzers. Alv., the

licensee expressed plans for improved trending of Deficiency

l

Reports and machinery failures.

,

l (4) Overdue PMs

The handling of overdue PMs appeared to be adequate. Any  ;

overdue PMs were so identified, and constituted less than 10% of ,

all PMs scheduled for the month. The overdue PMs were

highlighted in weekly and monthly reports, and appeared to be

L

aggressively pursued.

No violations or deviations were identified in this area,

d. Work Order Status

'

Work orders / requests were prioritized during staff meetings.

Identified non-Technical Specification related work is merged with TS

related work during these meetings. The daily meeting participants

l

were supervisory level with the OMC chairing the proceedings. .The

'

Planning Department provided information on material availability and

existing and projected work schedules. Equipment was returned to '

service based on operational needs.

Work order (WO) backlog for emergent work was not significant.

Overall, the three major departments (Instruments and Controls,

l Electrical, and Mechanical) trending showed a slight decline for W0s.

l The number of safety-related W0s that had not been processed by the

planners was approximately 1700. These numbers did not reflect W0s

that had been completed but not reviewed. This backlog is discussed

in paragraph 6.a.

A problem with voiding W0s was identified by the NRC in earlier l

l inspection findings and by the licensee. The licensee had changed

l the review process and the planners indicated that, at the present

l time, it was very difficult to void any work order if the work was

l not done. It now appears that many of the approximate 1500 W0s

l voided during 1987 were worked under other work orders such as

l previously scheduled preventive maintenance items. An example of

l cancelled W0s are valve repackings. The licensee stated that a large

number of scheduled repackings were voided due to difficulties with a

contractor who was to perform the work.

j No violations or deviations were identified.

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26

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e. Training

Qualifications for performing the various assigned maintenance

activities were obtained by "on-the-job training (0JT)." After

performing a given task, a least one time, with a qualified indivi-

dual, the maintenance technician was signed off by his s;pervisor as

qualified to perform the task alone. Technical training was being i

given on and off site in specialized areas. A QMT class covering

welding was attended by an inspector. The instructor was well-

prepared and knowledgeable; and, training materials and course

content appeared excellent. The only retraining noted was general

employee training.

No violations or deviations were identified,

f. Management and Work Controls

Direct supervision appeared to be goed in that at least once per

shift the foreman would visit each job site to inspect work in

progress. There also appears to be good communications between tho

technicians and foremen. Overtime did not appear to affect work

quality. Minimum overtime is worked during non-outage periods and

overtime during outages is regulated by administrative procedures to

16 hrs / day not to exceed 50 hrs / week.

"

Various maintenance superintendents were interviewed in regard to

individual goals, ongoing improvements, planned improvements, staff

training, and identified weaknesses. The following goals were

identified during the interviews:

-

Limit contractors on site

-

Improve public perception

-

Enhance safety

-

Reduce minor injuries

-

Eliminate repeat findings ,

-

Reduce NRC violations to less than the Region II average

.

-

Reduce man-rem

-

No reactor trips caused by maintenance personnel l

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Reduce non-outage corrective W0s to less than 500  ;

t -

Meet all commitment due dates

Ongoing improvements included:

-

More Quality Maintenance Teams ,

,

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Reduced use of contractors i

-

Improved plant material conditions

-

Improved plant housekeeping l

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27

The licensee noted that the following improvements had been made in

plant material conditions:

-

Steam leaks were being reduced by replacing old packing with a

'

new style of grapite packing (Chesterton) and by use of live

loading packing on selected valves such as the MSIVs.

-

Body to bonnet leaks were being reduced by ensuring use of

proper gaskets, using more graphoil type gaskets, and insuring

proper torquing of bonnets. ,

- Communications ~between North Anna and Surry maintenance

departments were improving because of monthly conferences with

corporate support organizations-

No specific problems were identified in material availability and

control, however, mechanical technicians stated that they

return incorrect matorials to stores about 20 percent of the,hadtime to

and

the I&C technicians stated that they had to return incorrect

materials about 15 percent of the time. Parts return was for various

causes. The inspector examined a sample of documentation of

completed work, but found no case where incorrect parts were

installed in the plant. This issue was brought to the attention of

licensee management. An additional problem in obtaining parts was

that some parts had to be ordered one day in advance from the store

house. This sometimes caused delays in returning equipment to

service and loss of man-hours due to waiting for parts.

Maintenance staffing levels were not perceived to be a problem with

the exception of the Planning Department which appeared understaffed

in the Mechanical Section. The need for additional personnel

adequately trend deficiency reports and W0s and to perform root cause

analyses had been recognized by the licensee. Addition of a full

time maintenance engineer for maintenance trending and root cause

analysis was planned. Eleven systems engineers were to be added to '

,

the technical support staff. The specific duties of the maintenance

engineer or the systems engineers had not been determined at the time i

of this inspection. l

Repetitive problems identified by the technicians were failures of  !

the Boric Acid pump seals, charging pump seals, high pressure drain

pump seals and steam traps. Maintenance management was aware of

these problems and were taking actions to improve reliability of this

equipment, ,

1

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No violations or deviations were identified.

g. Maintenance procedure Review

Maintenance procedures have been undergoing major revisions.

Complete procedure rewrites are being performed by contract

personnel. The maintenance group had established a new policy with

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regard to writing / rewriting procedures. Craft personnel are

involved in the procedure revision process. The licensee stated that

this policy stemed from problems with rewritten procedures generated .

by the procedure group solely. The organization and management of L

the procedure rewrite group has also been changed. The inspectors

examined one of the procedures, MMP-P-RC-1, Reactor Coolant Pump

(RCP) Seal Inspection, which had been rewritten by the procedure

group in the recent past and had been worked in January 1988. The

RCP seal procedure was deviated (required change) nineteen times

during the course of work which was a high number compared to

previous seal work using older procedures. The inspectors reviewed a ,

procedure group rewrite (draft) of the RCP seal procedure prior to '

the craft's review (the new policy had not been implemented). The

inspector noted three major points that had not been incorporated

into the draft from the previous deviations. The licensee committed  !

to include the points.

Just prior to this inspection, the licensee had made the decision to

rewrite the major pump procedures in time to support an October 1988

outage. Forty-four procedures, affecting 250 pumps, were included in

the rewrite. Craft input for the procedure revisions was planned. ,

Maintenance personnel considered many maintenance procedures to be

ineffective due to being generic and requiring "write in" steps to ,

accomplish specific tasks. The "write in" steps of the procedure

could be generated at the job site, by a task qualified individual,

who was qualified based on "on the job training", The procedure did

not receive any further review until after the task was completed.

During the review of completed procedures in the various work

packages it was noted that "write-in" pro:edural steps were used.

Although no "write-in" steps were found that made intent changes to

maintenance procedures, administrative instructions did not appear to

be sufficient to prevent the use of "write-in" steps to change the  ;

intent of the procedure. The licensee committed to enhance the t

! guidance on the use of "write-in" steps.

Another problem identified by maintenance personnel was that

individuals at different levels of the craft were allowed to sign-off

1 steps as "Not Applicable." The licensee should review this practice i

j to assure proper controls are in place, j

No violations or deviations were identified. l

h. Review of Licensee Event Reports (LERs) and Deviation Reports (DRs) <

Licensee's LERs for events that occurred during the SALP period were i

reviewed. From those, a total of six LERs were selected for further )

inspection effort. Two involved maintenance personnel errors and '

four others involved machinery failures. In addition, licensee's DRs I

were reviewed. From the DRs, two cases of repetitive equipment l

i f ailures were selected for inspection. The inspectors reviewed the l

, documents to determine the adequacy of the licensee's investigation,

corrective actions, and reporting.

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29 ,

(1) Unit 2 LER 86-14 involved a temporary jumper, placed 'in

accordance with an I&C maintenance procedure, which fell off

. resulting in a reactor trip. Human Performance Evaluation

"

System (HPES) Report 86-117, issued approximately two months

after the LER, documented a thorough review of the incident.

The HPES report made three recommendations to management. Two

of the recommendations had been implemented and the Licensing

Department Commitment Tracking System (CTS) was tracking the

third action until completed. Overall, the licensee's

' investigation and corrective actions following this LER appeared

to be thorough and timely. The HPES reports receive further

management review and distribution through the corporate

,

Operational Experience Review (OER) system. HPES was considered

by the inspectors to be a licensee strength.

(2) Unit 2 LER 87-018 covered an inadvertent 2J Emergency Diesel

'

Generator start during an electrical maintenance undervoltage

periodic test on the 2H emergency bus. An electrician had

J inadvertently entered a test signal in the wrong test cabinet.

4

A thorough HPES evaluation was conducted, and HPES Report 87-173

,

was written. This report included six recommendations to

j management. Completion of these items was being tracked by the

i

'

commitment tracking system as an HPES commitment, however, in

this case, the CTS incorrectly showed the LER as being completed

and ready for NRC closeout.

The licensee stated that plans existed to change the CTS this

year, to make it a more effective management tool. The current ,

CTS tracked commitments by category: 1.e. , LER, NRC Bulletin,

j INPO SOER, HPES report, etc. A particular issue was often

j implemented by several different commitments, but the CTS had no

cross reference and could not be sorted by issue. As a result,

an issue could be tracked under one or several commitment I

categories. To avoid duplication, this LER was closed out and -

the followup corrective actions tracked under the HPES report '

number. In the LER, the licensee made a commitment to the NRC l

.

to conduct an HPES investigation and to implement corrective  ;

] actions. Since these actions were not completed, the LER >

2 corrective actions were in fact not completed or ready for NRC

J

closeout. The change to the CTS should correct the problem of  :

i ability to show the correct status of each commitment.

l (3) Unit 1 LER 88-022 of January 8, 1988, described a manual trip of

1 the reactor due to the simultaneous loss of all three ,

circulating water pumps. A similar simultaneous loss of all I

three circulating waters pumps had also occurred in August 1987.

i Although the circulating water pumps are not safety related,

their total loss challenges the plant protection systems,

requiring a manual reactor trip.

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Af ter the August 1987 occurrence, an engineering review could

not determine the cause. However, a potential cause was

identified to be the CW system protection circuitry. In the

circuitry, the opening of one of two condenser waterbox vacuum

breaker valves on two of four waterboxes will trip all CW pumps.

No report was written on this investigation. The LER indicated

that, to prevent recurrence, an evaluation would be done to

determine if surveillance on the CW system protection circuitry

could identify actual and potential equipment failures. This

commitment is tracked in the CTS, with a scheduled completion

date of August 1, 1988.

'

The inspectors found that the CW system protective circuitry and

vacuum breakers are not included in any regularly scheduled

surveillance, preventive maintenance, or calibration program.

Additionally, inspectors found that many balance of plant

non-safety systems similarly have no preventive maintenance done

on instrumentation and control circuits. The licensee stated

that they plan to test and evaluate the CW system interlocks

during the. upcoming outage.

(4) Unit 2 LER 86-002 covered a reactor trip while in Mode 3 (hot I

standby) following a normal plant shutdown. When the source

range detectors energized, as designed, both detectors spiked

high causing the reactor trip. The detectors were replaced with  :

new ones and an investigatior into the cause of the detector  !

failures was conducted. The root cause of the failures was not

determined. The LER was then closed out in the CTS.

l

In the investigation report these possibilities were presented

for the failure cause:

'

a) Detectors came into service at overrange.

a) Electrical surge to the detectors.

a) End of expected life of the detectors.  ;

1 With regard to the life of the detectors, a statement in the

I

investigation report was made that "due to the frequency of j

detector repl.4 cement, a valid operation time cannot be

determined." Since the licensee maintained records of detector

installation and plant operating history, this statement did not l

'.

seem to mske sense. As for the possibility that the detectors '

came into service at overrange, the LER stated that the source

range detectors came on as designed and intermediat' range

detectors (which generate the signal to energize the source

range) were correctly compensated to read accurately. In

'

summary, each of the possible causes listed in the report were

inadequately followed up or analyzed in the report. The

inspectors found that the author of the investigation report had

been a chemical technician who had been newly assigned to the

Safety E'gineering Department. The licensee stated that

engineering investigations, as committed to be done in LERs, are

now done by engineers.

I I

31

(5) Unit 2 LER 87-002 described an event where, with the plant at

100 percent power, the 1C charging pump discharge check valve

stuck open following pump shutdown. This resulted in the loss

4

of r.harging and seal injection flow due to the backflow through

the IC pump. The cause of the check valve hanging open was

found to be excessive grit in the hanger bracket bushings which

were subsequently replaced. The discharge and recirculation

check valves on the Unit 218 charging pump and on Unit 1 10

charging pump were tested using the MOVATs checkmate system, and i

did not reveal any indications of valve degradation. Further

corrective action to be taken included developmr.nt of a pH

program for check valves used in critical applications, and

development of an Abnormal Procedure for loss of seal injection

and charging flow.

.

The abnormal procedure commitment was tracked in the CTS under

, the LER. The PM program commitment was tracked in the CTS under  !

I

INPO SOER 86-03. The LER stated that a similar event occurred i

on the same valve on March 24, 1986. On that occasion, a work

request was submitted but the work order was cancelled because

the valve appeared to function properly after being seated.

In interviews with mechanical maintenance supervisors who had

been at the plant for many years, the inspectors were told that e

the grit in the valve was an isolated occurrence. No similar :

grit had been seen elsewhere in the charging system, during i

various inspections. This LER did not seem to adequately

describe followup concerns or inspections for grit elsewhere in ,

the system, nor did it seem to fully discuss followup testing of I

all other check valves in the system. It appeared to the  ;

'

'

inspectors that a more thorough followup engineering investiga-

tion of this event should have been done.

(6) Unit 2 LER 87-012 reported a failure of Type "C" local leak rate

,

testing by three containment isolation valves. These valves

1

provide isolation for the condenser air ejector discharge when .

it is diverted to the containment, l

,

'

This LER was submitted later than the required 30 days from the

time of the event (event date August 31, 1987, LER date l

a October 14, 1987). The stated reason for report lateness was

procedure inadequacy. The acceptance criteria for the procedure

'

did not require a deviation report for "as found" leak rate

greater than the required limit of 0.60 La. Also, the LER did

not contain a licensee contact name and telephone number.

l The engineering investigation report that was done subsequent to

} this LER found that the cause of valve leakage was not debris,

as stated in the LER, but instead was an incorrect testing

method. Pressure had been injected between two valves in

4

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series, which tested one from a direction in which it was not '

i designed to hold the test pressure. A corrected test method was i

used and the valve did not leak. The inspector found this l

s analysis acceptable, except for one point. If the testing  :

procedure was faulty, how did this valve pass previous Type C [

testing? The licensee investigated this, and found that on the

previous test, the same failure had occurred. An engineering ,

analysis had been done, and a temporary change to the test [

procedure had been written. Apparently, since then the  ;

procedure had not been permanently changed and the temporary

l change had been lost. The use of temporary changes to

1 procedures, instead of needed permanent changes, was found to be

an overall area of weakness for the licensee, and is discussed [

in paragraph 5.d. i

1

Rev. I to this LER was issued to cover the results of the i

engineering investigation and the revision of the test  !

, procedure. Based on this onsite inspection, Unit 2 LER 87-012  !'

Rev. 1 is closed.

i

(7) A review of the DR log revealed a series of repetitive failures I

I

of oxygen and hydrogen analyzers for the Waste Gas Decay Tank j

(WGOT). The safety function of these monitors is to alarm if l

oxygen and hydrogen levels increase toward an explosive mixture, j

During the period of April-September 1987, ten DRs were written [

for operational problems with these analyzers. In each case,  !

the instruments were recalibrated and returned to service. The i

instrumentation maintenance supervisors indicated that the

problems with these analysers were temperature sensitivity and i

being prone to drift. The analyzers were located in the base- f

i ment of the fuel butiding, which was not air conditioned. '

During warm weather, it was not unusual for the analyzers to

]

,

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. drift out of tolerance prior to the scheduled PMs (monthly r

functional test and quarterly calibration). The supervisors

stated that these analyzers were also used in other industries,  !

where calibrations were typically done more frequently,  ;

sometimes weekly or even daily. Increasing the calibration

2 frequency of the WGOT oxygen and hydrogen analyzers was con- l

I sidered by these supervisors,. but was not done. The licensee ,

j made a commitment to increase the calibration frequency of these

l analyzers to at least monthly. The calibration frequency should I

be based on performance. l

The oxygen and hydrogen analyzers have a built-in capability to  !

4 automatically perform a daily calibration check. For the oxygen i

l channel, this would consist of sampling a gas containing zero f

I

percent oxygen for 15 seconds, then sampling a gas mixture l

.

containing 5 percent oxygen for 15 seconds. Zero and five j

i percent are the low and high ends of the recorder scale which is  :

} located in the control room. Inspection of the control room  !

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, 33

,

recorder chart revealed that no daily calibration checks were

recorded for the previous two days. Review of previous charts,

in the records library, revealed that only three daily calibra- ,

tion checks (all on the oxygen channel) were recorded from the f

last week in January through the first week in March 1988. The

daily calibration check had not been operating. Reviews of  :

' control room logs and interviews with operators revealed that

the log sheets did not describe how the operator should inspect

and record the daily calibration check. No standards were l

provided and the operators did not understand that there was a l

'

J

daily calibration check feature, wherein the actual readings of

0% and 5% were important. The hydrogen channel check feature

was found to have never been hooked up. The licensee indicated

to the inspectors that the oxygen channel calibration check

feature would be repaired, control room logs would be changed to [

provide adequate instructions to the operator, and operators

would be trained in proper reading and recording of the daily [

calibration check.

1 The vendor had recommended replacement of the existing oxygen

i and hydrogen monitors with newer models, which are less

i temperature sensitive and less prone to drifting. The

instrumentation maintenance supervisors have submitted a

purchase request for new oxygen and hydrogen monitors.

(8) The DR review also revealed a history of repetitive failures of

radiation monitors during 1987. The instrumentation maintenance

supervisors indicated that these were Kaman Science brand

,

monitors. In response to continual problems, one monitor had

been taken out of service for five weeks in late 1987 and during

'

that five weeks Instrument technicians worked with a vendor j

representative to develop a permanent fix. A field change was

developed and implemented, which appears to have substantially (

improved the reliability of that monitor. The maintenance i

supervisors stated that the other radiation monitors were being

l modified to incorporate the new field changes.

In reviewing DRs for repetitive failures, it was determined that

1 the licensee had not done trending of DRs. The licensee l

, committed to begin trending DRs so that repetitive failures

t

would be noted and would receive management attention. It was

also noted that trending of work orders for repetitive machinery

failures was not effective. A major contributing factor was the

-

large backlog of completed work orders not entered into the

.. machinery history.

(9) A deficiency report and a maintenance work order review revealed ,

a history of repetitive failures of containment isolation valves i

, to pass Type C testing. The valves reviewed were IHV-MOV-100A

'

and -1008 and are the containment purge isclation valves. It

was noted in the work order packages that the valve seats were

i

34 ,

.

greased and then retested after initial failure. A detailed

review was performed by the inspector and discussions with

various technicians disclosed that the greasing of the seat was

for aiding in seal adjustment and for seal removal after

extended periods. In this case it appeared that lubrication of ,

the valve seating material was an acceptable practice and f

enhanced valve performance. l

t

Minor deficiencies in the LERs reviewed we:e noted by the

inspector and were pointed out to the licensee. The inspector

also noted that a new LER format developed by the licensee in

late 1987 appeared to have improved the quality of the LERs, in

that the new format leaves less opportunity to omit required I

information.

The inspectors notea that five of the six LERs reviewed included l

commitments for follow-up investigations. Yet every one of  !

these LERs stated that no supplemental LER was expected to be

submitted. Ir. most of the followup investigations, additional l

information such as a cause of the event or corrective action l

) was determined. But supplemental LERs were not submitted. The

d licensee indicated that HDES and engineering investigation '

I reports would be reviewed in the future for the need to submit

supplemental LERs.

In contrast to the high quality found in the HpES reports, the

inspectors noted that some engineering investigation reports

were not written (i.e., August 1987 trip of all CW pumps) or ,

poorly done. Further, it was noted that HPES reports were  !

distributed through the corporate operational experience review '

j

'

(OER) program, where they got additional review and

dissemination. Engineering reports were not distributed through l

corporate OER. The licensee stated that future engineering i

investigation reports would be of better quality and would be

distributed through corporate OER. ,

'

i

] No violations or deviations were identified.  ;

7. Management Controls (30702, 40700)

7

,

)

The organizational structure was reviewed to determine that it was I

l prescribed by corporate policy documents and standards; that its functions

i were adequately defined by administrative procedures; and, that staffing

and staffing plans appeared adequate to fulfill the chartered roles.

The status of implementation of major organizational functions was

'

determined by review of procedures, review of records, interviews and

,

discussions with licensee managers, supervisors and staff personnel inside

i and outside the departments of interest.

)

i

i

.- _ - _ _ _ _ _ - _ _ _ _ . _ _ _ _

35

a. Station Nuclear Safety and Operating Committee

The activities of the onsite safety review committee, the Station

Nuclear Safety and Operating Committee (SNSOC), were reviewed to

determine if the committee was functioning as required by the -

'

Technical Specifications (TS), was providing adequate interface with  !

various plant disciplines, anc was performing adequate safety  !

. evaluations. [

!

In addition to the requirements delineated in the TS, the SNSOC

, activities are controlled by administrative procedure ADM-1.1. To

i review the committee's activities the inspector reviewed the

following SNSOC documentation:

'

1 -

ADM-1.1, Station Nuclear Safety Operating Committee, dated

1

June 16, 1987 i

i

-

Nuclear Operations Department Administrative Standard, .

i Management Overview, N005-ADM-03, Rev. 0

1 -

N005-ADM-06, Organization, Responsibility and Interfaces, Rev. 0

-

ADM-1.0, Station Organization and Responsibility, dated July 9, ,

!

<

1987

-

TS Section 6.5.1 i

j

-

Selected meeting minutes ,

!  !

- In addition, the inspector attended SNSOC meetings, interviewed

' '

members, and alternate members.

The SNSOC holds meetings usually on the order of once a month. More

frequent meetings or special meetings are held as needed. There is

good member participation during the meetings and evidence of strong

1 management control. The committee encourages outside participation,

1 This was evidenced by participation by individuals and their ,

j supervisor who were initiating a permanent procedure change, i

.

deviation or other administrative action. These individuals were  !

l required to present their issues and resolution at the $NSOC  ;

< meetings.  :

i

'

The SNSOC appears to be accomplishing their mission and performing .

adequate reviews and safety evaluations. The use of outside I

'

individuals and their supervisors is considered an effective

enhancement, promoting clear communication among all parties.

1

! No violations or deviations were identified,

i 1

9 b. Plant Status Meetings  ;

j i

'

Various plant status meetings were attended to determine whether l

day-to-day plant activities and planned future activities were being '

j adequately disseminated to the applicable plant staff.

i

1

!  :

'

l

-. ,_ - --. .

. . .

- -. _- -_ -- .

..

36

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.

,o review the plant status meetings, the inspector attended selected

'*

,

daily plant meetings. The licensee's daily plant status meetings l

consisted of the following:

,

-

8:15 a.m. Executive Management Meeting l

!

-

11:00 a.m. planning Meeting ['

-

3:00 p.m. Plan-of-the-Day meeting

,

There appeared to be good interface between plant groups and good  !

!

participation by personnel in plant status meetings. The various

status meetings provided a discussion of plant conditions and ongoing

planned maintenance and/or testing activities. There is good

, management control at the meetings and adequate multi-discipline

attendance including the security personnel.

The inspector noted that the Superintendent of Operations and the  !

l Superintendent of Maintenance conducted daily tours of the facilities

! and that senior management conducted random assessment visits during  :

! off normal working hours. The inspector observed that during these

l tours the managers take on-the-spot, immediate, and effective actions

l to have problems resolved and more importantly bring it to the  !

i

attention of the individual involved. It was also noted that these

l managers frequently had their next lower tier supervisor acconipany '

,

them during these tours, which reinforced what managemenc considered ,

I to be an acceptable plant standard. L

!

l The licensee appeared to conduct effective and terse management  !

l meetings to evaluate issuss coupled with active management involve-

ment in daily activities. ,

No violations or deviations were identified.

l c. Nuclear Safety Engineering

1  ;

l The activities of the Nuclear Safety Engineering (NSE) group were i

reviewed to determine if they were functioning as required by the TS,  !

were providing adequate interface with various disciplines, and were i

maintaining surveillance of plant activities to provide independent '

verification that these activities were performed correctly and that

,

human errors were reduced as much as practical. l

In addition to the requirements in the TS, the NSE activities are l

delineated in ADM-1.2, Nuclear Safety Engineering, dated February 3,

1988. To review the group's activities the inspector interviewed the

,

4

NSE Supervisor, several engineers and reviewed the following I

administrative procedures:

l

l

l

l

l r

. .

>

37

-

ADM-1.2,. Nuclear Safety Engineering, dated February 3, 1988 i'

- ADM-5.3, Review of Procedures, dated March 10, 1988

-

ADM-6.19, Processing of Significant Operating Experience Reports

(50ER), dated September 11, 1986 .

ADM-16.17 Human Performance Evaluation System (HPES), dated

i

-

May 28, 1987 ,

-

ADM-16.14, Commitment Tracking Program, dated August 20, 1986 '

-

ADM-15.0, Nonconformance Reports, dated May 29, 1986

-

ADM-6.14, Control of Engineering Work Requests, dated March 31,

1983 t

ADM-3.9, Evaluation for Potential Unreviwwed Safety Questions,

'

'

-

March 19, 1987 .

'

1

1 The inspector determined from the above reviews and interviews that

NSE had 16 degreed engineers, of which, seven are certified STAS; six

'

,

are qualified to be certified STAS, and two are to be placed in the  ;

'

next certification class. This group appeared to be providing j

adequate on going reviews and assessments of plant operations.

,

Additionally, the NSE provided adequate reviews of INPO Significant  ;

Operating Experience Reports, industry events, NRC I&E Notices and -

j Bulletins, and Licensee Event Reports.

The NSE was also responsible for coordinating the Human Performance

Evaluation System (HPES) program. A HPES pilot program was imple-

J mented onsite in 1985. The program was designed to uncover specific

adverse administrative practices and human engineering hardware

deficiencies which contribute to inappropriate actions. This program  :

I allowed anyone to report a potential problem that may affect safe  !

t

4 operation, reliability, availability or an inappropriate action

'

concerning personnel performance. The program was formalized in 1

i 1986. A review of HPES reports and resultant actions indicated that t

this program appeared to have a positive impact in reducing human ,

errors in plant operations. The HPES program is considered a

strength. l

i ,

,

j No violations or deviations were identified. [

i

1 d. Quality Control 1

!

The inspector conducted interviews with the Manager Quality

i Assurance, supervisors and inspectors. He also reviewed the

1 following documents

a r

-

Nuclear Operation Department Policy Statement (N00PS)-QA-01,  !

i Quality Assurance / Quality Control, Rev. O j

-

NODPS-QA-02, Corrective Action, Rev. 0 '

-

Nuclear Operations Department Standard (NODS)-QA-01, Corrective  !

Action, Rev. 1 l

- N005-QA-02, Audits, Rev. 1 t

j -

N005-QA-03, Inspection / Surveillance, Rev. 0 (

l

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VEP-1-5A Topical Report, Operations Phase QA Program l

.  !

f

i

> I

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38

.

-

Quality Assurance Organization Policy Statement (QAOPS) -2.3, i

Corrective Action, Draft

-

Quality Assurance Organization Standard (QA05)-2.3, Corrective

,

Action, Oraft

1

- Quality Assurance Department Instruction Nuclear (QADIN) A 4.0, ,

. Certification Program for Inspectors Assigned to the Quality

Assurance Department, Rev. 1 , i

QADIN C1.0, Surveillance Program Administration & Operation,

'

-

.

Rev. 0

- QADIN Guideline 2C.1, Inspector of the Day Guideline, Rev. 0

-

Audit Schedule

'

-

Surveillance Schedule

-

Completed Audit Reports

-

Quality Maintenance Team (QMT) - ADM-2.11, dated February 12,

1988 L

The inspector noted from the above interviews and reviews that the [

, licensee had determined that the audit and surveillance groups spent

approximately 60 percent of their time performing collateral tasks, ,

'

detracting from their basic responsibilities. Although it had not

i prevented QA from meeting its audit schedule, the collatsral tasks

! had caused issuance of the audit reports to be delayed. During the i

t

first quarter of the yea *, the QA surveillance group missed several '

scheduled surveillances. Further review indicated that this was due ,

to special surveillances being implemented in response to industry-

wide INPO and NRC issues. A review of the missed scheduled surveil- F

lances indicated that no TS requirements were impacted. The licensee

is restructuring responsibilities within the QA department to allow

4

the audit and surveillance personnel to devote the majority of their

'

i time to their auditing and surveillance responsibilities.

i The licensee utilized an "Inspector of the Day" (IOD) program to

provide daily coverage of plant activities, seven days a week. The

100 was not assigned any other responsibilities on their "duty" day.

'

,

Their responsibilities included walkdown of areas of management

interest, observation of special evolutions, observation of repairs ,

,

or modification activities, and informing the SS and cognizant l

J supervisor when violations or unsafe conditions were noted. This

program was considered a strength.

J

'

Quality Maintenance Team (QMT) concept was implemented in 1986. The

! licensee's goal is to develop 18 teams. These teams will perform l

'

their own QC inspection and radiological control functions. The  ;

intent is to build quality into the maintenance activity. The team

building was approximately 70% complete. The mechanical maintenance l

, i

teams were the first groups to be formed and the QMT program is '

expanding to include the electrical and I&C disciplines. Maintenance

j personnel stated they felt the QMT program had increased work

i quality. However, the three mechanical maintenance QMT members who

were interviewed all stated they felt uncomfortable performing their l

l

1 own health physics duties, particularly on more complex tasks.

5

J

1

- - - - - _ _ .

39

The licensee appears to have devoted many hours toward developing

this program. They have provided designated personnel from

Corporate, Surry, and North Anna to form a Quality Managing Steering

Team and a Quality Managing Working Team. These teams meet

frequently to discuss problem areas and explore possible

enhancements. This program was considered a strength. A note worthy

concept employed is that the certified QMT inspector will be

administered a recertification performance inspection approximately

every six months. The QMT inspector will perform an inspection i

activity while being observed by a QC department inspector, as '

required by QADIN A 4.0 Rev. 1, Section 5.6.

However, the inspector noted one QMT program area considered to be a

weakness. The QMT is required to perform a pre-job briefing and a ,

post-job briefing. The QC department appears to be attending only

the pre-job briefings. No QC observations were made during the post

maintenance briefings to ensure that the team is addressing the

quality aspect or problems encountered.

In additinn, considering the licensee's high expectation of the QMT

program, there hasn't been a QA assessment conducted since the

program was implemented. This is considered a weakness in that the

licensee has not assessed that the actual mechanics of the main-

tenance activities are providing the quality of work that is

perceived by management.

No violations or deviations were identified.

8. List of Acronyms ,

BOP Balance of Plant

CR0 Control Room Operator  :

CTS Commitment Tracking System  ;

CW Circulating Water System l

DR Deviation Report

EDO Executive Director for Operations

HPES Human Performance Evaluation System

HP Health Physics

ISC Instrumentation and Controls

IEB Inspection and Enforcement Bulletin  ;

IEN Inspection and Enforcement Notice l

IFI Inspector Followup Item  !

INPO Institute of Nuclear Power Operations  !

LER Licensee Event Report  :

MOVAT Motor Operated Valve Analysis and Testing i

MSIV Main Steam Isolation Valve ,

MWO Maintenance Work Order j

N00PS Nuclear Operations Department Policy Statement 1

N005 Nuclear Operations Department Standard '

NPRDS Nuclear Plant Reliability Data System i

NRC Nuclear Regulatory Commission l

NSE Nuclear Safety Engineering i

1

l

l

-- - _ _ - _

!

,

40

'

.

i

OER Operational Experience Review

(k)T On The Job Training

i O&M Operation and Maintenance

1 OMC Operations Maintenance Coordinator ,

'

OP Operating Procedure ,

OPA Operational Performance Assessment  !

PM Preventive Maintenance [

! PMT Post Maintenance Test  :

,

POD Plan Of The Day L

a PORV Power Operated Relief Valve  !

PT Performance Test  :

i

QA Quality Assurance .

l' QADIN Quality Assurance Department Instruction Nuclear F

QACPS Quality Assurance Organization Policy Statement

i QA05 Quality Assurance Organization Standard

! QC Quality Control

QCAR Quality Control Activity Report  ;

<

QMT Quality Maintenance Team l

l QS Quench Spray

RCP Reactor Coolant Pump

1 RHR Residual Heat Removal .

i RS Recirculation Spray i

'

RWP Radiation Work Permit .

-

SALP Systematic Assessment of Licensee Performance t

i SG Steam Generator  :

'

j SNSOC Station Nuclear Safety and Operating Committee

Significant Operating Experience Report

'

SOER l

Senior Reactor Operator

'

SRO

SS Shift Supervisor

j STA Shift Technical Advisor  !

'

TS Technical Specification

i

TSC Technical Support Center '

i URI Unresolved Item l

-

WGDT Waste Gas Decay Tank

j WO Work Order

j WR Work Request l

l

I
:

i

)

1

i

!

!

-